Biweekly Notice; Applications and Amendments to Facility Operating Licenses and Combined Licenses Involving No Significant Hazards Considerations, 55401-55421 [2017-25063]
Download as PDF
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
Commission, Washington, DC 20555–
0001.
For additional direction on obtaining
information and submitting comments,
see ‘‘Obtaining Information and
Submitting Comments’’ in the
SUPPLEMENTARY INFORMATION section of
this document.
FOR FURTHER INFORMATION CONTACT:
Shirley Rohrer, Office of Nuclear
Reactor Regulation, U.S. Nuclear
Regulatory Commission, Washington,
DC 20555–0001; telephone: 301–415–
5411, email: Shirley.Rohrer@nrc.gov.
SUPPLEMENTARY INFORMATION:
The meeting is open to the public.
Patrice Little Murray,
Committee Management Officer.
[FR Doc. 2017–25135 Filed 11–20–17; 8:45 am]
BILLING CODE 7515–01–P
NUCLEAR REGULATORY
COMMISSION
[NRC–2017–0220]
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses and Combined Licenses
Involving No Significant Hazards
Considerations
I. Obtaining Information and
Submitting Comments
Nuclear Regulatory
Commission.
ACTION: Biweekly notice.
AGENCY:
Pursuant to Section 189a.(2)
of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear
Regulatory Commission (NRC) is
publishing this regular biweekly notice.
The Act requires the Commission to
publish notice of any amendments
issued, or proposed to be issued, and
grants the Commission the authority to
issue and make immediately effective
any amendment to an operating license
or combined license, as applicable,
upon a determination by the
Commission that such amendment
involves no significant hazards
consideration, notwithstanding the
pendency before the Commission of a
request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued, from October 24,
2017 to November 6, 2017. The last
biweekly notice was published on
November 7, 2017.
DATES: Comments must be filed by
December 21, 2017. A request for a
hearing must be filed by January 22,
2018.
SUMMARY:
You may submit comments
by any of the following methods (unless
this document describes a different
method for submitting comments on a
specific subject):
• Federal Rulemaking Web site: Go to
https://www.regulations.gov and search
for Docket ID NRC–2017–0220. Address
questions about NRC dockets to Carol
Gallagher; telephone: 301–415–3463;
email: Carol.Gallagher@nrc.gov. For
technical questions, contact the
individual listed in the FOR FURTHER
INFORMATION CONTACT section of this
document.
• Mail comments to: May Ma, Office
of Administration, Mail Stop: OWFN–2–
A13, U.S. Nuclear Regulatory
asabaliauskas on DSKBBXCHB2PROD with NOTICES
ADDRESSES:
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
A. Obtaining Information
Please refer to Docket ID NRC–2017–
0220, facility name, unit number(s),
plant docket number, application date,
and subject when contacting the NRC
about the availability of information for
this action. You may obtain publiclyavailable information related to this
action by any of the following methods:
• Federal Rulemaking Web site: Go to
https://www.regulations.gov and search
for Docket ID NRC–2017–0220.
• NRC’s Agencywide Documents
Access and Management System
(ADAMS): You may obtain publiclyavailable documents online in the
ADAMS Public Documents collection at
https://www.nrc.gov/reading-rm/
adams.html. To begin the search, select
‘‘ADAMS Public Documents’’ and then
select ‘‘Begin Web-based ADAMS
Search.’’ For problems with ADAMS,
please contact the NRC’s Public
Document Room (PDR) reference staff at
1–800–397–4209, 301–415–4737, or by
email to pdr.resource@nrc.gov. The
ADAMS accession number for each
document referenced (if it is available in
ADAMS) is provided the first time that
it is mentioned in this document.
• NRC’s PDR: You may examine and
purchase copies of public documents at
the NRC’s PDR, Room O1–F21, One
White Flint North, 11555 Rockville
Pike, Rockville, Maryland 20852.
B. Submitting Comments
Please include Docket ID NRC–2017–
0220, facility name, unit number(s),
plant docket number, application date,
and subject in your comment
submission.
The NRC cautions you not to include
identifying or contact information that
you do not want to be publicly
disclosed in your comment submission.
The NRC will post all comment
submissions at https://
www.regulations.gov as well as enter the
comment submissions into ADAMS.
PO 00000
Frm 00058
Fmt 4703
Sfmt 4703
55401
The NRC does not routinely edit
comment submissions to remove
identifying or contact information.
If you are requesting or aggregating
comments from other persons for
submission to the NRC, then you should
inform those persons not to include
identifying or contact information that
they do not want to be publicly
disclosed in their comment submission.
Your request should state that the NRC
does not routinely edit comment
submissions to remove such information
before making the comment
submissions available to the public or
entering the comment into ADAMS.
II. Notice of Consideration of Issuance
of Amendments to Facility Operating
Licenses and Combined Licenses and
Proposed No Significant Hazards
Consideration Determination
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
§ 50.92 of title 10 of the Code of Federal
Regulations (10 CFR), this means that
operation of the facility in accordance
with the proposed amendment would
not (1) involve a significant increase in
the probability or consequences of an
accident previously evaluated, or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period if circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility. If
the Commission takes action prior to the
expiration of either the comment period
or the notice period, it will publish in
the Federal Register a notice of
E:\FR\FM\21NON1.SGM
21NON1
55402
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
asabaliauskas on DSKBBXCHB2PROD with NOTICES
issuance. If the Commission makes a
final no significant hazards
consideration determination, any
hearing will take place after issuance.
The Commission expects that the need
to take this action will occur very
infrequently.
A. Opportunity To Request a Hearing
and Petition for Leave To Intervene
Within 60 days after the date of
publication of this notice, any persons
(petitioner) whose interest may be
affected by this action may file a request
for a hearing and petition for leave to
intervene (petition) with respect to the
action. Petitions shall be filed in
accordance with the Commission’s
‘‘Agency Rules of Practice and
Procedure’’ in 10 CFR part 2. Interested
persons should consult a current copy
of 10 CFR 2.309. The NRC’s regulations
are accessible electronically from the
NRC Library on the NRC’s Web site at
https://www.nrc.gov/reading-rm/doccollections/cfr/. Alternatively, a copy of
the regulations is available at the NRC’s
Public Document Room, located at One
White Flint North, Room O1–F21, 11555
Rockville Pike (First Floor), Rockville,
Maryland 20852. If a petition is filed,
the Commission or a presiding officer
will rule on the petition and, if
appropriate, a notice of a hearing will be
issued.
As required by 10 CFR 2.309(d) the
petition should specifically explain the
reasons why intervention should be
permitted with particular reference to
the following general requirements for
standing: (1) The name, address, and
telephone number of the petitioner; (2)
the nature of the petitioner’s right under
the Act to be made a party to the
proceeding; (3) the nature and extent of
the petitioner’s property, financial, or
other interest in the proceeding; and (4)
the possible effect of any decision or
order which may be entered in the
proceeding on the petitioner’s interest.
In accordance with 10 CFR 2.309(f),
the petition must also set forth the
specific contentions which the
petitioner seeks to have litigated in the
proceeding. Each contention must
consist of a specific statement of the
issue of law or fact to be raised or
controverted. In addition, the petitioner
must provide a brief explanation of the
bases for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner intends to
rely in proving the contention at the
hearing. The petitioner must also
provide references to the specific
sources and documents on which the
petitioner intends to rely to support its
position on the issue. The petition must
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
include sufficient information to show
that a genuine dispute exists with the
applicant or licensee on a material issue
of law or fact. Contentions must be
limited to matters within the scope of
the proceeding. The contention must be
one which, if proven, would entitle the
petitioner to relief. A petitioner who
fails to satisfy the requirements at 10
CFR 2.309(f) with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene. Parties have the opportunity
to participate fully in the conduct of the
hearing with respect to resolution of
that party’s admitted contentions,
including the opportunity to present
evidence, consistent with the NRC’s
regulations, policies, and procedures.
Petitions must be filed no later than
60 days from the date of publication of
this notice. Petitions and motions for
leave to file new or amended
contentions that are filed after the
deadline will not be entertained absent
a determination by the presiding officer
that the filing demonstrates good cause
by satisfying the three factors in 10 CFR
2.309(c)(1)(i) through (iii). The petition
must be filed in accordance with the
filing instructions in the ‘‘Electronic
Submissions (E-Filing)’’ section of this
document.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to
establish when the hearing is held. If the
final determination is that the
amendment request involves no
significant hazards consideration, the
Commission may issue the amendment
and make it immediately effective,
notwithstanding the request for a
hearing. Any hearing would take place
after issuance of the amendment. If the
final determination is that the
amendment request involves a
significant hazards consideration, then
any hearing held would take place
before the issuance of the amendment
unless the Commission finds an
imminent danger to the health or safety
of the public, in which case it will issue
an appropriate order or rule under 10
CFR part 2.
A State, local governmental body,
Federally-recognized Indian Tribe, or
agency thereof, may submit a petition to
the Commission to participate as a party
under 10 CFR 2.309(h)(1). The petition
should state the nature and extent of the
PO 00000
Frm 00059
Fmt 4703
Sfmt 4703
petitioner’s interest in the proceeding.
The petition should be submitted to the
Commission no later than 60 days from
the date of publication of this notice.
The petition must be filed in accordance
with the filing instructions in the
‘‘Electronic Submissions (E-Filing)’’
section of this document, and should
meet the requirements for petitions set
forth in this section, except that under
10 CFR 2.309(h)(2) a State, local
governmental body, or federally
recognized Indian Tribe, or agency
thereof does not need to address the
standing requirements in 10 CFR
2.309(d) if the facility is located within
its boundaries. Alternatively, a State,
local governmental body, Federallyrecognized Indian Tribe, or agency
thereof may participate as a non-party
under 10 CFR 2.315(c). If a hearing is
granted, any person who is not a party
to the proceeding and is not affiliated
with or represented by a party may, at
the discretion of the presiding officer, be
permitted to make a limited appearance
pursuant to the provisions of 10 CFR
2.315(a). A person making a limited
appearance may make an oral or written
statement of his or her position on the
issues but may not otherwise participate
in the proceeding. A limited appearance
may be made at any session of the
hearing or at any prehearing conference,
subject to the limits and conditions as
may be imposed by the presiding
officer. Details regarding the
opportunity to make a limited
appearance will be provided by the
presiding officer if such sessions are
scheduled.
B. Electronic Submissions (E-Filing)
All documents filed in NRC
adjudicatory proceedings, including a
request for hearing and petition for
leave to intervene (petition), any motion
or other document filed in the
proceeding prior to the submission of a
request for hearing or petition to
intervene, and documents filed by
interested governmental entities that
request to participate under 10 CFR
2.315(c), must be filed in accordance
with the NRC’s E-Filing rule (72 FR
49139; August 28, 2007, as amended at
77 FR 46562, August 3, 2012). The EFiling process requires participants to
submit and serve all adjudicatory
documents over the internet, or in some
cases to mail copies on electronic
storage media. Detailed guidance on
making electronic submissions may be
found in the Guidance for Electronic
Submissions to the NRC and on the NRC
Web site at https://www.nrc.gov/sitehelp/e-submittals.html. Participants
may not submit paper copies of their
filings unless they seek an exemption in
E:\FR\FM\21NON1.SGM
21NON1
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
accordance with the procedures
described below.
To comply with the procedural
requirements of E-Filing, at least 10
days prior to the filing deadline, the
participant should contact the Office of
the Secretary by email at
hearing.docket@nrc.gov, or by telephone
at 301–415–1677, to (1) request a digital
identification (ID) certificate, which
allows the participant (or its counsel or
representative) to digitally sign
submissions and access the E-Filing
system for any proceeding in which it
is participating; and (2) advise the
Secretary that the participant will be
submitting a petition or other
adjudicatory document (even in
instances in which the participant, or its
counsel or representative, already holds
an NRC-issued digital ID certificate).
Based upon this information, the
Secretary will establish an electronic
docket for the hearing in this proceeding
if the Secretary has not already
established an electronic docket.
Information about applying for a
digital ID certificate is available on the
NRC’s public Web site at https://
www.nrc.gov/site-help/e-submittals/
getting-started.html. Once a participant
has obtained a digital ID certificate and
a docket has been created, the
participant can then submit
adjudicatory documents. Submissions
must be in Portable Document Format
(PDF). Additional guidance on PDF
submissions is available on the NRC’s
public Web site at https://www.nrc.gov/
site-help/electronic-sub-ref-mat.html. A
filing is considered complete at the time
the document is submitted through the
NRC’s E-Filing system. To be timely, an
electronic filing must be submitted to
the E-Filing system no later than 11:59
p.m. Eastern Time on the due date.
Upon receipt of a transmission, the EFiling system time-stamps the document
and sends the submitter an email notice
confirming receipt of the document. The
E-Filing system also distributes an email
notice that provides access to the
document to the NRC’s Office of the
General Counsel and any others who
have advised the Office of the Secretary
that they wish to participate in the
proceeding, so that the filer need not
serve the document on those
participants separately. Therefore,
applicants and other participants (or
their counsel or representative) must
apply for and receive a digital ID
certificate before adjudicatory
documents are filed so that they can
obtain access to the documents via the
E-Filing system.
A person filing electronically using
the NRC’s adjudicatory E-Filing system
may seek assistance by contacting the
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
NRC’s Electronic Filing Help Desk
through the ‘‘Contact Us’’ link located
on the NRC’s public Web site at https://
www.nrc.gov/site-help/esubmittals.html, by email to
MSHD.Resource@nrc.gov, or by a tollfree call at 1–866–672–7640. The NRC
Electronic Filing Help Desk is available
between 9 a.m. and 6 p.m., Eastern
Time, Monday through Friday,
excluding government holidays.
Participants who believe that they
have a good cause for not submitting
documents electronically must file an
exemption request, in accordance with
10 CFR 2.302(g), with their initial paper
filing stating why there is good cause for
not filing electronically and requesting
authorization to continue to submit
documents in paper format. Such filings
must be submitted by: (1) First class
mail addressed to the Office of the
Secretary of the Commission, U.S.
Nuclear Regulatory Commission,
Washington, DC 20555–0001, Attention:
Rulemaking and Adjudications Staff; or
(2) courier, express mail, or expedited
delivery service to the Office of the
Secretary, 11555 Rockville Pike,
Rockville, Maryland 20852, Attention:
Rulemaking and Adjudications Staff.
Participants filing adjudicatory
documents in this manner are
responsible for serving the document on
all other participants. Filing is
considered complete by first-class mail
as of the time of deposit in the mail, or
by courier, express mail, or expedited
delivery service upon depositing the
document with the provider of the
service. A presiding officer, having
granted an exemption request from
using E-Filing, may require a participant
or party to use E-Filing if the presiding
officer subsequently determines that the
reason for granting the exemption from
use of E-Filing no longer exists.
Documents submitted in adjudicatory
proceedings will appear in the NRC’s
electronic hearing docket which is
available to the public at https://
adams.nrc.gov/ehd, unless excluded
pursuant to an order of the Commission
or the presiding officer. If you do not
have an NRC-issued digital ID certificate
as described above, click cancel when
the link requests certificates and you
will be automatically directed to the
NRC’s electronic hearing dockets where
you will be able to access any publicly
available documents in a particular
hearing docket. Participants are
requested not to include personal
privacy information, such as social
security numbers, home addresses, or
personal phone numbers in their filings,
unless an NRC regulation or other law
requires submission of such
information. For example, in some
PO 00000
Frm 00060
Fmt 4703
Sfmt 4703
55403
instances, individuals provide home
addresses in order to demonstrate
proximity to a facility or site. With
respect to copyrighted works, except for
limited excerpts that serve the purpose
of the adjudicatory filings and would
constitute a Fair Use application,
participants are requested not to include
copyrighted materials in their
submission.
For further details with respect to
these license amendment applications,
see the application for amendment
which is available for public inspection
in ADAMS and at the NRC’s PDR. For
additional direction on accessing
information related to this document,
see the ‘‘Obtaining Information and
Submitting Comments’’ section of this
document.
Entergy Nuclear Operations, Inc.,
Docket No. 50–255, Palisades Nuclear
Plant (PNP), Van Buren County,
Michigan
Date of amendment request: August
31, 2017. A publicly-available version is
in ADAMS under Accession No.
ML17248A389.
Description of amendment request:
The proposed amendment would revise
the PNP Site Emergency Plan (SEP) for
the permanently shut down and
defueled condition. The proposed PNP
SEP changes would revise the shift
staffing and Emergency Response
Organization (ERO) staffing.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes to the PNP SEP do
not impact the function of plant structures,
systems, or components (SSCs). The
proposed changes do not affect accident
initiators or precursors, nor does it alter
design assumptions. The proposed changes
do not prevent the ability of the on-shift staff
and augmented ERO to perform their
intended functions to mitigate the
consequences of any accident or event that
will be credible in the permanently shut
down and defueled condition. The proposed
changes only remove positions that will no
longer be credited in the PNP SEP.
Therefore, the proposed amendment does
not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
E:\FR\FM\21NON1.SGM
21NON1
55404
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
Response: No.
The proposed changes reduce the number
of on-shift and augmented ERO positions
commensurate with the hazards associated
with a permanently shut down and defueled
facility. The proposed changes do not involve
installation of new equipment or
modification of existing equipment, so that
no new equipment failure modes are
introduced. Also, the proposed changes do
not result in a change to the way that the
equipment or facility is operated so that no
new accident initiators are created.
Therefore, the proposed amendment does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
Margin of safety is associated with
confidence in the ability of the fission
product barriers (i.e., fuel cladding, reactor
coolant system pressure boundary, and
containment structure) to limit the level of
radiation dose to the public. The proposed
changes are associated with the PNP SEP and
do not impact operation of the plant or its
response to transients or accidents. The
change does not affect the Technical
Specifications. The proposed changes do not
involve a change in the method of plant
operation, and no accident analyses will be
affected by the proposed changes. Safety
analysis acceptance criteria are not affected
by the proposed changes. The revised PNP
SEP will continue to provide the necessary
response staff with the proposed changes.
Therefore, the proposed amendment does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: William Dennis,
Assistant General Counsel, Entergy
Nuclear Operations, Inc., 440 Hamilton
Ave., White Plains, NY 10601.
NRC Branch Chief: Douglas A.
Broaddus.
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Exelon Generation Company (EGC),
LLC, Docket Nos. STN 50–456 and STN
50–457, Braidwood Station, Units 1 and
2, Will County, Illinois and Docket Nos.
STN 50–454 and STN 50–455, Byron
Station, Unit Nos. 1 and 2, Ogle County,
Illinois
Date of amendment request:
September 1, 2017. A publicly-available
version is in ADAMS under Accession
No. ML17244A093.
Description of amendment request:
The amendments would modify the
licensing basis by the addition of a
license condition to allow for the
implementation of the provisions of 10
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
CFR, Section 50.69, ‘‘Risk-informed
categorization and treatment of
structures, systems and components for
nuclear power reactors.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change will permit the use
of a risk-informed categorization process to
modify the scope of SSCs [structures,
systems, and components] subject to NRC
[Nuclear Regulatory Commission] special
treatment requirements and to implement
alternative treatments per the regulations.
The process used to evaluate SSCs for
changes to NRC special treatment
requirements and the use of alternative
requirements ensures the ability of the SSCs
to perform their design function. The
potential change to special treatment
requirements does not change the design and
operation of the SSCs. As a result, the
proposed change does not significantly affect
any initiators to accidents previously
evaluated or the ability to mitigate any
accidents previously evaluated. The
consequences of the accidents previously
evaluated are not affected because the
mitigation functions performed by the SSCs
assumed in the safety analysis are not being
modified. The SSCs required to safely shut
down the reactor and maintain it in a safe
shutdown condition following an accident
will continue to perform their design
functions.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any previously evaluated?
Response: No.
The proposed change will permit the use
of a risk-informed categorization process to
modify the scope of SSCs subject to NRC
special treatment requirements and to
implement alternative treatments per the
regulations. The proposed change does not
change the functional requirements,
configuration, or method of operation of any
SSC. Under the proposed change, no
additional plant equipment will be installed.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed change will permit the use
of a risk-informed categorization process to
modify the scope of SSCs subject to NRC
special treatment requirements and to
implement alternative treatments per the
regulations. The proposed change does not
PO 00000
Frm 00061
Fmt 4703
Sfmt 4703
affect any Safety Limits or operating
parameters used to establish the safety
margin. The safety margins included in
analyses of accidents are not affected by the
proposed change.
The regulation requires that there be no
significant effect on plant risk due to any
change to the special treatment requirements
for SSCs and that the SSCs continue to be
capable of performing their design basis
functions, as well as to perform any beyond
design basis functions consistent with the
categorization process and results.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Tamra Domeyer,
Associate General Counsel, Exelon
Nuclear, 4300 Winfield Road,
Warrenville, IL 60555.
NRC Branch Chief: David J. Wrona.
Exelon Generation Company, LLC and
PSEG Nuclear LLC, Docket Nos. 50–277
and 50–278, Peach Bottom Atomic
Power Station, Units 2 and 3, York and
Lancaster Counties, Pennsylvania
Date of amendment request: August
30, 2017, as supplemented by letter
dated October 24, 2017. Publiclyavailable versions are in ADAMS under
Accession Nos. ML17243A014 and
ML17297B521, respectively.
Description of amendment request:
The amendments would modify the
licensing basis by the addition of a
license condition to allow for the
implementation of the provisions of 10
CFR 50.69, ‘‘Risk-informed
categorization and treatment of
structures, systems and components for
nuclear power reactors.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below, with NRC staff edits shown in
square brackets:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change will permit the use
of a risk-informed categorization process to
modify the scope of [structures, systems, and
components] SSCs subject to NRC special
treatment requirements and to implement
alternative treatments per the regulations.
The process used to evaluate SSCs for
changes to NRC special treatment
E:\FR\FM\21NON1.SGM
21NON1
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
requirements and the use of alternative
requirements ensures the ability of the SSCs
to perform their design function. The
potential change to special treatment
requirements does not change the design and
operation of the SSCs. As a result, the
proposed change does not significantly affect
any initiators to accidents previously
evaluated or the ability to mitigate any
accidents previously evaluated. The
consequences of the accidents previously
evaluated are not affected because the
mitigation functions performed by the SSCs
assumed in the safety analysis are not being
modified. The SSCs required to safely shut
down the reactor and maintain it in a safe
shutdown condition following an accident
will continue to perform their design
functions.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change will permit the use
of a risk-informed categorization process to
modify the scope of SSCs subject to NRC
special treatment requirements and to
implement alternative treatments per the
regulations. The proposed change does not
change the functional requirements,
configuration, or method of operation of any
SSC. Under the proposed change, no
additional plant equipment will be installed.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change will permit the use
of a risk-informed categorization process to
modify the scope of SSCs subject to NRC
special treatment requirements and to
implement alternative treatments per the
regulations. The proposed change does not
affect any Safety Limits or operating
parameters used to establish the safety
margin. The safety margins included in
analyses of accidents are not affected by the
proposed change. The regulation requires
that there be no significant effect on plant
risk due to any change to the special
treatment requirements for SSCs and that the
SSCs continue to be capable of performing
their design basis functions, as well as to
perform any beyond design basis functions
consistent with the categorization process
and results.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
Attorney for licensee: Tamra Domeyer,
Associate General Counsel, Exelon
Generation Company, LLC, 4300
Winfield Rd., Warrenville, IL 60555.
NRC Branch Chief: James G. Danna.
Exelon Generation Company, LLC and
PSEG Nuclear LLC, Docket Nos. 50–277
and 50–278, Peach Bottom Atomic
Power Station, Units 2 and 3, York and
Lancaster Counties, Pennsylvania
Date of amendment request:
September 29, 2017. A publiclyavailable version is in ADAMS under
Accession No. ML17275A069.
Description of amendment request:
The amendments would revise
Technical Specification (TS)
requirements related to the direct
current (DC) electrical power system.
The proposed changes are based on
Technical Specifications Task Force
(TSTF) Traveler TSTF–500, Revision 2,
‘‘DC Electrical Rewrite—Update to
TSTF–360.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change restructures the TS
for the direct current (DC) electrical power
system. The proposed changes add actions to
specifically address battery charger
inoperability. The DC electrical power
system, including associated battery chargers,
is not an initiator of any accident sequence
analyzed in the Updated Final Safety
Analysis Report (UFSAR). Operation in
accordance with the proposed TS ensures
that the DC electrical power system is
capable of performing its function as
described in the UFSAR. Therefore, the
mitigative functions supported by the DC
electrical power system will continue to
provide the protection assumed by the
analysis, and the probability of previously
analyzed accidents will not increase by
implementing these changes.
The relocation of preventive maintenance
surveillances, and certain operating limits
and actions, to a newly created licenseecontrolled Battery Monitoring and
Maintenance Program will not challenge the
ability of the DC electrical power system to
perform its design function. Appropriate
monitoring and maintenance, consistent with
industry standards, will continue to be
performed. In addition, the DC electrical
power system is within the scope of 10 CFR
50.65, ‘‘Requirements for monitoring the
effectiveness of maintenance at nuclear
power plants,’’ which will ensure the control
of maintenance activities associated with the
DC electrical power system.
PO 00000
Frm 00062
Fmt 4703
Sfmt 4703
55405
The integrity of fission product barriers,
plant configuration, and operating
procedures as described in the UFSAR will
not be affected by the proposed changes.
Therefore, the consequences of previously
analyzed accidents will not increase by
implementing these changes.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change involves
restructuring the TS for the DC electrical
power system. The DC electrical power
system, including associated battery chargers,
is not an initiator to any accident sequence
analyzed in the UFSAR. Rather, the DC
electrical power system is used to supply
equipment used to mitigate an accident.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The margin of safety is established through
equipment design, operating parameters, and
the setpoints at which automatic actions are
initiated. The proposed changes will not
adversely affect operation of plant
equipment. These changes will not result in
a change to the setpoints at which protective
actions are initiated. Sufficient DC capacity
to support operation of mitigation equipment
is ensured. The changes associated with the
new battery maintenance and monitoring
program will ensure that the station batteries
are maintained in a highly reliable manner.
The equipment fed by the DC electrical
sources will continue to provide adequate
power to safety related loads in accordance
with analysis assumptions.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Tamra Domeyer,
Associate General Counsel, Exelon
Generation Company, LLC, 4300
Winfield Rd., Warrenville, IL 60555.
NRC Branch Chief: James G. Danna.
Exelon Generation Company, LLC,
Docket No. 50–333, James A. FitzPatrick
Nuclear Power Plant, Oswego County,
New York
Date of amendment request: October
2, 2017. A publicly-available version is
in ADAMS under Accession No.
ML17275A520.
E:\FR\FM\21NON1.SGM
21NON1
55406
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Description of amendment request:
The amendment would revise the James
A. FitzPatrick Nuclear Power Plant
Technical Specifications (TSs) to adopt
Technical Specifications Task Force
(TSTF) Traveler TSTF–542, Revision 2,
‘‘Reactor Pressure Vessel Water
Inventory Control’’ (ADAMS Accession
No. ML16074A448). Specifically, the
licensee proposed changes to replace TS
requirements related to operations with
a potential for draining the reactor
vessel (OPDRVs) with new requirements
on reactor pressure vessel (RPV) water
inventory control (WIC) to protect
Safety Limit 2.1.1.3.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes replace existing TS
requirements related to OPDRVs with new
requirements on RPV WIC that will protect
Safety Limit 2.1.1.3. Draining of RPV water
inventory in Mode 4 (i.e., cold shutdown)
and Mode 5 (i.e., refueling) is not an accident
previously evaluated, and therefore replacing
the existing TS controls to prevent or
mitigate such an event with a new set of
controls has no effect on any accident
previously evaluated. RPV water inventory
control in Mode 4 or Mode 5 is not an
initiator of any accident previously
evaluated. The existing OPDRV controls or
the proposed RPV WIC controls are not
mitigating actions assumed in any accident
previously evaluated.
The proposed changes reduce the
probability of an unexpected draining event
(which is not a previously evaluated
accident) by imposing new requirements on
the limiting time in which an unexpected
draining event could result in the reactor
vessel water level dropping to the top of the
active fuel (TAF). These controls require
cognizance of the plant configuration and
control of configurations with unacceptably
short drain times. These requirements reduce
the probability of an unexpected draining
event. The current TS requirements are only
mitigating actions and impose no
requirements that reduce the probability of
an unexpected draining event.
The proposed changes reduce the
consequences of an unexpected draining
event (which is not a previously evaluated
accident) by requiring an Emergency Core
Cooling System (ECCS) subsystem to be
operable at all times in Modes 4 and 5. The
current TS requirements do not require any
water injection systems, ECCS or otherwise,
to be Operable in certain conditions in Mode
5. The change in requirement from two ECCS
subsystems to one ECCS subsystem in Modes
4 and 5 does not significantly affect the
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
consequences of an unexpected draining
event because the proposed Actions ensure
equipment is available within the limiting
drain time that is as capable of mitigating the
event as the current requirements. The
proposed controls provide escalating
compensatory measures to be established as
calculated drain times decrease, such as
verification of a second method of water
injection and additional confirmations that
containment and/or filtration would be
available if needed.
The proposed changes reduce or eliminate
some requirements that were determined to
be unnecessary to manage the consequences
of an unexpected draining event, such as
automatic initiation of an ECCS subsystem
and control room ventilation. These changes
do not affect the consequences of any
accident previously evaluated since a
draining event in Modes 4 and 5 is not a
previously evaluated accident and the
requirements are not needed to adequately
respond to a draining event.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes replace existing TS
requirements related to OPDRVs with new
requirements on RPV WIC that will protect
Safety Limit 2.1.1.3. The proposed changes
will not alter the design function of the
equipment involved. Under the proposed
changes, some systems that are currently
required to be operable during OPDRVs
would be required to be available within the
limiting drain time or to be in service
depending on the limiting drain time. Should
those systems be unable to be placed into
service, the consequences are no different
than if those systems were unable to perform
their function under the current TS
requirements.
The event of concern under the current
requirements and the proposed changes are
an unexpected draining event. The proposed
changes do not create new failure
mechanisms, malfunctions, or accident
initiators that would cause a draining event
or a new or different kind of accident not
previously evaluated or included in the
design and licensing bases.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes replace existing TS
requirements related to OPDRVs with new
requirements on RPV WIC. The current
requirements do not have a stated safety basis
and no margin of safety is established in the
licensing basis. The safety basis for the new
requirements is to protect Safety Limit
2.1.1.3. New requirements are added to
determine the limiting time in which the
RPV water inventory could drain to the top
of the fuel in the reactor vessel should an
PO 00000
Frm 00063
Fmt 4703
Sfmt 4703
unexpected draining event occur. Plant
configurations that could result in lowering
the RPV water level to the TAF within one
hour are now prohibited. New escalating
compensatory measures based on the limiting
drain time replace the current controls. The
proposed TS establish a safety margin by
providing defense-in-depth to ensure that the
Safety Limit is protected and to protect the
public health and safety. While some less
restrictive requirements are proposed for
plant configurations with long calculated
drain times, the overall effect of the change
is to improve plant safety and to add safety
margin.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Donald P.
Ferraro, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Suite 305, Kennett Square,
PA 19348.
NRC Branch Chief: James G. Danna.
Florida Power & Light Company, Docket
Nos. 50–250 and 50–251, Turkey Point
Nuclear Generating Unit Nos. 3, and 4,
Miami-Dade County, Florida
Date of amendment request: August
23, 2017, as supplemented by letter
dated October 19, 2017. Publiclyavailable versions are in ADAMS under
Accession Nos. ML17235B008 and
ML17292A789, respectively.
Description of amendment request:
The amendments would modify the
Technical Specifications (TSs) to
relocate the Explosive Gas Monitoring
Instrumentation, Explosive Gas Mixture,
and Gas Decay Tanks System
requirements to licensee-controlled
documents and establish a Gas Decay
Tank Explosive Gas and Radioactivity
Monitoring Program. The proposed
amendments also relocate the Standby
Feedwater System requirements to
licensee-controlled documents and
modify related Auxiliary Feedwater
(AFW) System requirements.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
E:\FR\FM\21NON1.SGM
21NON1
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
The proposed license amendments modify
the Turkey Point TS by relocating the
Explosive Gas Monitoring Instrumentation,
Explosive Gas Mixture, Gas Decay Tanks and
Standby Feedwater System requirements to
licensee controlled documents, by relatedly
modifying the AFW System requirements
and by establishing a Gas Decay Tank
Explosive Gas and Radioactivity Monitoring
Program. The proposed changes are
administrative in nature and do not alter any
plant equipment or the manner in which
plant equipment is operated and maintained.
All equipment limitations, applicable
methodologies and surveillances are
maintained by the proposed changes. In
addition, the proposed changes to the AFW
System requirements enhance plant safety.
As such, the proposed changes cannot affect
the initiators, the likelihood or the expected
outcomes of any analyzed accidents.
Therefore, facility operation in accordance
with the proposed changes would not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed license amendments modify
the Turkey Point TS by relocating the
Explosive Gas Monitoring Instrumentation,
Explosive Gas Mixture, Gas Decay Tanks and
Standby Feedwater System requirements to
licensee controlled documents, by relatedly
modifying the AFW System requirements
and by establishing a Gas Decay Tank
Explosive Gas and Radioactivity Monitoring
Program. The proposed changes neither
install or remove plant equipment nor alter
any plant equipment design, configuration,
or method of operation. Hence, no new
failure mechanisms are introduced as a result
of the proposed changes.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed license amendments modify
the Turkey Point TS by relocating the
Explosive Gas Monitoring Instrumentation,
Explosive Gas Mixture, Gas Decay Tanks and
Standby Feedwater System requirements to
licensee controlled documents, by relatedly
modifying the AFW System requirements
and by establishing a Gas Decay Tank
Explosive Gas and Radioactivity Monitoring
Program. The proposed changes neither
involve changes to safety analyses
assumptions, safety limits, or limiting safety
system settings nor adversely impact plant
operating margins or the reliability of
equipment credited in safety analyses.
Therefore, operation of the facility in
accordance with the proposed changes will
not involve a significant reduction in the
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: William S.
Blair, Managing Attorney—Nuclear,
Florida Power & Light Company, 700
Universe Blvd., MS LAW/JB, Juno
Beach, FL 33408–0420.
NRC Branch Chief: Undine Shoop.
NextEra Energy Duane Arnold, LLC,
Docket No. 50–331, Duane Arnold
Energy Center (DAEC), Linn County,
Iowa
Date of amendment request:
September 5, 2017. A publicly-available
version is in ADAMS under Accession
No. ML17248A284.
Description of amendment request:
The proposed amendment would revise
DAEC Technical Specifications 3.5.1,
‘‘ECCS [emergency core cooling system]Operating.’’ The proposed change
would decrease the nitrogen supply
requirement for the Automatic
Depressurization System (ADS) in
Surveillance Requirement (SR) 3.5.1.3
from 100 days to 30 days.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change modifies a SR for
verification of the nitrogen supply for the
ADS accumulators. Accidents are initiated by
the malfunction of plant equipment, or the
catastrophic failure of plant structures,
systems or components. The performance of
this surveillance is not a precursor to any
accident previously evaluated and does not
change the manner in which the ADS
operates. Technical evaluation of the change
concluded that a 30-day nitrogen supply is
more than adequate to ensure that the reactor
is depressurized, so the consequences of an
accident remain unchanged.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequence of a previously
evaluated accident.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not involve
physical alterations to the plant. No new or
different type of equipment will be installed,
and there are no physical modifications
required to existing installed equipment
associated with the proposed change. The
proposed change does not create any failure
PO 00000
Frm 00064
Fmt 4703
Sfmt 4703
55407
mechanism, malfunction or accident initiator
not already considered in the design and
licensing basis.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
Although the proposed change will
decrease the required supply of nitrogen for
the ADS accumulators from 100 days to 30
days, the assessment above has shown that
the reactor would be depressurized within 3
days following any postulated accident or
event that would create a hostile
environment in the drywell. Once initial
depressurization is completed, long term core
cooling can be assured without ADS.
Therefore, the proposed change will not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: William Blair,
P.O. Box 14000, Juno Beach, FL 33408–
0420.
NRC Branch Chief: David J. Wrona.
NextEra Energy Duane Arnold, LLC,
Docket No. 50–331, Duane Arnold
Energy Center, Linn County, Iowa
Date of amendment request: August
31, 2017. A publicly-available version is
in ADAMS under Accession No.
ML17243A469.
Description of amendment request:
The proposed amendment would
modify the licensing basis by the
addition of a license condition to allow
for the implementation of the provisions
of 10 CFR, part 50.69, ‘‘Risk-Informed
Categorization and Treatment of
Structures, Systems, and Components
(SSCs) for Nuclear Power Reactors.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change will permit the use
of a risk-informed categorization process to
modify the scope of SSCs subject to NRC
special treatment requirements and to
implement alternative treatments per the
regulations. The process used to evaluate
SSCs for changes to NRC special treatment
E:\FR\FM\21NON1.SGM
21NON1
asabaliauskas on DSKBBXCHB2PROD with NOTICES
55408
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
requirements and the use of alternative
requirements ensures the ability of the SSCs
to perform their design function. The
potential change to special treatment
requirements does not change the design and
operation of the SSCs. As a result, the
proposed change does not significantly affect
any initiators to accidents previously
evaluated or the ability to mitigate any
accidents previously evaluated. The
consequences of the accidents previously
evaluated are not affected because the
mitigation functions performed by the SSCs
assumed in the safety analysis are not being
modified. The SSCs required to safely shut
down the reactor and maintain it in a safe
shutdown condition following an accident
will continue to perform their design
functions.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change will permit the use
of a risk-informed categorization process to
modify the scope of SSCs subject to NRC
special treatment requirements and to
implement alternative treatments per the
regulations. The proposed change does not
change the functional requirements,
configuration, or method of operation of any
SSC. Under the proposed change, no
additional plant equipment will be installed.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change will permit the use
of a risk-informed categorization process to
modify the scope of SSCs subject to NRC
special treatment requirements and to
implement alternative treatments per the
regulations. The proposed change does not
affect any Safety Limits or operating
parameters used to establish the safety
margin. The safety margins included in
analyses of accidents are not affected by the
proposed change. The regulation requires
that there be no significant effect on plant
risk due to any change to the special
treatment requirements for SSCs and that the
SSCs continue to be capable of performing
their design basis functions, as well as to
perform any beyond design basis functions
consistent with the categorization process
and results.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
Attorney for licensee: William Blair,
P.O. Box 14000, Juno Beach, FL 33408–
0420.
NRC Branch Chief: David J. Wrona.
NextEra Energy, Point Beach Nuclear
Plant (PBNP), LLC, Docket Nos. 50–266
and 50–301, Point Beach Nuclear Plant,
Units 1 and 2, Town of Two Creeks,
Manitowoc County, Wisconsin
Date of amendment request: June 23,
2017, as supplemented by letter dated
August 21, 2017. Publicly-available
versions are in ADAMS under
Accession Nos. ML17174A458, and
ML17233A283, respectively.
Description of amendment request:
The amendments would revise the
Emergency Plan for PBNP to adopt the
Nuclear Energy lnstitute’s (NEl’s)
revised Emergency Action Level (EAL)
scheme described in NEI 99–01,
Revision 6, ‘‘Development of Emergency
Action Levels for Non-Passive
Reactors,’’ which has been endorsed by
the NRC.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change does not impact the
physical configuration or function of plant
structures, systems, or components (SSCs) or
the manner in which SSCs are operated,
maintained, modified, tested, or inspected.
No actual facility equipment or accident
analyses are affected by the proposed
changes.
The change revises the NextEra Emergency
Action Levels to be consistent with the NRC
endorsed EAL scheme contained in NEI 99–
01, Revision 6, ‘‘Methodology for
Development of Emergency Action Levels,’’
but does not alter any of the requirements of
the Operating License or the Technical
Specifications.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not involve a
physical alteration of the plant (no new or
different type of equipment will be installed).
The proposed change does not create any
new failure modes for existing equipment or
any new limiting single failures.
Additionally, the proposed change does not
involve a change in the methods governing
normal plant operation, and all safety
functions will continue to perform as
PO 00000
Frm 00065
Fmt 4703
Sfmt 4703
previously assumed in the accident analyses.
Thus, the proposed change does not
adversely affect the design function or
operation of any structures, systems, and
components important to safety. No new
accident scenarios, failure mechanisms, or
limiting single failures are introduced as a
result of the proposed change. The proposed
change does not challenge the performance
or integrity of any safety-related system.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The margin of safety associated with the
acceptance criteria of any accident is
unchanged. The proposed change will have
no affect on the availability, operability, or
performance of safety-related systems and
components. The proposed change will not
adversely affect the operation of plant
equipment or the function of equipment
assumed in the accident analysis. The
proposed amendment does not involve
changes to any safety analyses assumptions,
safety limits, or limiting safety system
settings. The changes do not adversely
impact plant operating margins or the
reliability of equipment credited in the safety
analyses.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: William Blair,
Managing Attorney—Nuclear, Florida
Power & Light Company, P.O. Box
14000, 700 Universe Boulevard, Juno
Beach, FL 33408–0420.
NRC Branch Chief: David J. Wrona.
PSEG Nuclear LLC and Exelon
Generation Company, LLC, Docket Nos.
50–272 and 50–311, Salem Nuclear
Generating Station, Unit Nos. 1 and 2,
Salem County, New Jersey
Date of amendment request:
September 27, 2017. A publiclyavailable version is in ADAMS under
Accession No. ML17270A076.
Description of amendment request:
The amendments would relocate the
reactor coolant system pressure
isolation valve (RCS PIV) table from the
technical specifications (TSs) to the
technical requirements manual (TRM).
The request would also remove
references to the table and move all
notes and leakage acceptance criteria
from the table to the TS surveillance
requirements.
E:\FR\FM\21NON1.SGM
21NON1
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes to the TS will not
alter the way any structure, system, or
component (SSC) functions, and will not
alter the manner in which the plant is
operated. The proposed changes do not alter
the design of any SSC. The relocation of the
RCS PIV valve lists from the TS to the TRM
is an administrative change. Future revisions
to the TRM are subject to 10 CFR 50.59.
Therefore the probability of an accident
previously evaluated is not significantly
increased.
The proposed changes do not alter the RCS
PIV leakage limits contained in the TS nor do
they alter the frequency for testing of the RCS
PIV. Therefore, the consequences of an
accident previously evaluated are not
increased.
Therefore, these proposed changes do not
represent a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes do not involve a
modification to the physical configuration of
the plant or changes in the methods
governing normal plant operation. The
proposed changes will not impose any new
or different requirement or introduce a new
accident initiator, accident precursor, or
malfunction mechanism. The proposed
changes are administrative in nature.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes to the RCS PIV TS
are administrative in nature. The proposed
changes do not alter the RCS PIV leakage
limits contained in the TS nor do they alter
the frequency for testing of the RCS PIV. The
proposed changes will not result in changes
to system design or setpoints that are
intended to ensure timely identification of
plant conditions that could be precursors to
accidents or potential degradation of accident
mitigation systems.
The proposed amendment will not result
in a design basis or safety limit being
exceeded or altered. Therefore, since the
proposed changes do not impact the response
of the plant to a design basis accident, the
proposed changes do not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jeffrie J. Keenan,
PSEG Nuclear LLC—N21, P.O. Box 236,
Hancocks Bridge, NJ 08038.
NRC Branch Chief: James G. Danna.
South Carolina Electric & Gas Company,
South Carolina Public Service
Authority, Docket No. 50–395, Virgil C.
Summer Nuclear Station, Unit No. 1,
Fairfield County, South Carolina
Date of amendment request: October
6, 2017. A publicly-available version is
in ADAMS under Accession No.
ML17279A715.
Description of amendment request:
The proposed amendment would
increase the Integrated Leak Rate Test
(ILRT) Peak Calculated Containment
Internal Pressure, Pa, listed in Technical
Specification (TS) 6.8.4.g, ‘‘Containment
Leakage Rate Testing Program,’’ to
remove the reference to Regulatory
Guide (RG) 1.163, ‘‘Performance-Based
Containment Leak Test Program,’’ dated
September 1995 and ANSI/ANS
(American National Standards Institute/
American Nuclear Society)—56.8–2002,
‘‘Containment System Leakage Testing
Requirements,’’ and to replace the
reference of Nuclear Energy Institute
(NEI) 94–01, Revision 3–A, ‘‘Industry
Guideline for Implementing
Performance-Based option of 10 CFR
part 50, Appendix J,’’ with NEI 94–01,
Revision 2–A.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below, with NRC staff edits in square
brackets:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes involve removal of
RG 1.163 and ANSl/ANS–56.8–2002
references, replacement of NEI 94–01,
Revision 3–A with NEI 94–01, Revision 2–A,
and an increase in the Pa [Peak Calculated
Containment Internal Pressure] value for
containment leakage testing. The activity
does not involve a physical change to the
plant or a change in the manner in which the
plant is operated or controlled. The
containment is designed to provide an
essentially leak tight barrier against the
uncontrolled release of radioactivity to the
environment for postulated accidents. As
such, the reactor containment itself and the
testing requirements invoked to periodically
PO 00000
Frm 00066
Fmt 4703
Sfmt 4703
55409
demonstrate the integrity of the reactor
containment exist to ensure the plant’s
ability to mitigate the consequences of an
accident, and do not involve the prevention
or identification of any precursors of an
accident.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The integrity of the reactor containment is
subject to two types of failure mechanisms
which can be categorized as (1) activity based
and (2) time based. Activity based failure
mechanisms are defined as degradation due
to system and/or component modifications or
maintenance. Local leak rate test
requirements and administrative controls
such as configuration management and
procedural requirements for system
restoration ensure that containment integrity
is not degraded by plant modifications or
maintenance activities. The updated Pa value
reflects the updated mass and energy release
and containment response calculations,
ensuring a sound technical basis for the local
and integrated leakage tests.
To mitigate time-based mechanisms, the
design and construction requirements of the
containment itself combined with the
containment inspections performed in
accordance with ASME [American Society of
Mechanical Engineers], Section XI and the
Maintenance Rule serve to provide a high
degree of assurance that the containment will
not degrade in a manner that is detectable
only by a Type A test. The change to the Pa
value is less than 1 psid [per square inch
differential]. Radiological consequences will
continue to be evaluated at the Technical
Specification allowed leakage, La [allowed
leakage] of 0.20 percent by weight of air,
which will not be increased despite the
increase in Pa. As described in Section 3.5,
past leakage testing yielded values well
under La. Based on the above, neither the
reference changes nor the Pa change involves
a significant increase in the consequences of
an accident previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes involve removal of
RG 1.163 and ANSl/ANS–56.8–2002
references, replacement of NEI 94–01,
Revision 3–A with NEI 94–01, Revision 2–A,
and an increase in the Pa value for
containment leakage testing. The reactor
containment and the testing requirements
invoked to periodically demonstrate the
integrity of the reactor containment exist to
ensure the plant’s ability to mitigate the
consequences of an accident. There are not
any accident initiators or precursors affected
by the revision. The proposed TS change
does not involve a physical change to the
plant or the manner in which the plant is
operated or controlled.
Therefore, the proposed TS change does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
E:\FR\FM\21NON1.SGM
21NON1
55410
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Response: No.
The proposed changes involve removal of
RG 1.163 and ANSl/ANS–56.8–2002
references, replacement of NEI 94–01,
Revision 3–A with NEI 94–01, Revision 2–A,
and an increase in the Pa value for
containment leakage testing. The proposed
TS change does not involve a physical
change to the plant or a change in the manner
in which the plant is operated or controlled.
Using the same analysis methodology as
described in WCAP–10325–P–A
[Westinghouse LOCA [loss-of-accident
coolant] Mass and Energy Release Model for
Containment Design], the updated mass and
energy release and containment response
analyses corrected input errors identified in
the NSALs [Westinghouse Nuclear Safety
Advisory Letters] described previously. As
shown in Figure 1 [October 6, 2017,
submittal], the correction of these errors
resulted in a slightly higher predicted peak
pressure than that of the current licensing
basis but does not pose a significant
challenge to the design limit.
The specific requirements and conditions
of the Primary Containment Leak Rate
Testing Program, as defined in the Technical
Specifications, exist to ensure that the degree
of reactor containment structural integrity
and leak-tightness that is considered in the
plant safety analysis is maintained. The
overall containment leak rate limit specified
by the Technical Specification is maintained.
The containment inspections performed in
accordance with ASME, Section XI and the
Maintenance Rule serve to provide a high
degree of assurance that the containment will
not degrade in a manner that is detectable
only by Type A testing. The combination of
these factors ensures that the margin of safety
that is in plant safety analysis is maintained.
The design, operation, testing methods and
acceptance criteria for Type A, B, and C
containment leakage tests specified in
applicable codes and standards will continue
to be met.
Therefore, the proposed TS change does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Kathryn M.
Sutton, Morgan, Lewis & Bockius LLP,
1111 Pennsylvania Avenue NW.,
Washington, DC 20004.
NRC Branch Chief: Michael T.
Markley.
Southern Nuclear Operating Company,
Docket Nos. 52–025 and 52–026, Vogtle
Electric Generating Plant, Units 3 and 4,
Burke County, Georgia
Date of amendment request: July 28,
2017. A publicly-available version is in
ADAMS under Accession No.
ML17209A759.
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
Description of amendment request:
The amendment request proposes to
revise Technical Specification Section
1.1 (TS), Definition of Actuation Logic
Test, by adding a new TS Section 1.1
Definition of Actuation Logic Output
Test (ALOT), revising existing
Surveillance Requirements 3.3.15.1 and
3.3.16.1 and adding new Surveillance
Requirements 3.3.15.2 and 3.3.16.2 to
implement the new ALOT. This
submittal requests approval of the
license amendment that is necessary to
implement these changes.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(A),
licensee has provided its analysis of the
issue on no significant hazards
consideration determination, which is
presented below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
There are no design changes associated
with the proposed amendment. All design,
material, and construction standards that
were applicable prior to this amendment
request will continue to be applicable.
The [Processor Module Self-Diagnostic
(PMS)] will continue to function in a manner
consistent with the plant design basis. There
will be no changes to the PMS operating
limits. The existing ACTUATION LOGIC
TEST Surveillance Requirements are revised
such that different portions of the PMS logic
circuitry are tested on appropriate
surveillance test frequencies.
The proposed change will not adversely
affect accident initiators or precursors or
adversely alter the design assumptions,
conditions, and configuration of the facility,
or the manner in which the plant is operated
and maintained, with respect to such
initiators or precursors.
The proposed changes will not alter the
ability of structures, systems, and
components (SSCs) to perform their specified
safety functions to mitigate the consequences
of an initiating event within the assumed
acceptance limits.
Accident analysis acceptance criteria will
continue to be met with the proposed
changes. The proposed changes will not
affect the source term, containment isolation,
or radiological release assumptions used in
evaluating the radiological consequences of
any accident previously evaluated. The
proposed changes will not alter any
assumptions or change any mitigation actions
in the radiological consequence evaluations
in the Updated Final Safety Analysis Report
(UFSAR).
The applicable radiological dose
acceptance criteria will continue to be met.
The proposed change revises the frequency
of testing certain portions of the PMS logic
circuitry, but does not physically alter any
safety-related systems.
Therefore, the proposed amendment does
not involve a significant increase in the
PO 00000
Frm 00067
Fmt 4703
Sfmt 4703
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a different kind of accident
from any accident previously evaluated?
Response: No.
With respect to any new or different kind
of accident, there are no proposed design
changes nor are there any changes in the
method by which any safety-related plant
SSC performs its specified safety function.
The proposed change will not affect the
normal method of plant operation or change
any operating parameters. No equipment
performance requirements will be affected.
The proposed change will not alter any
assumptions made in the safety analyses.
The proposed change revises the frequency
of testing certain portions of the PMS logic
circuitry. The proposed change does not
involve a physical modification of the plant.
No new accident scenarios, transient
precursors, failure mechanisms, or limiting
single failures will be introduced as a result
of this amendment. There will be no adverse
effect or challenges imposed on any safetyrelated system as a result of this amendment.
Therefore, the proposed amendment does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The existing ACTUATION LOGIC TEST
Surveillance Requirements are revised such
that different portions of the PMS logic
circuitry are tested on appropriate
surveillance test frequencies. The reliability
of the PMS is such that not testing the
Component Interface Module (CIM) logic and
driver output circuits when the reactor is at
power will have a net positive impact on
Engineered Safety Feature Actuation System
(ESFAS) availability. There will be a
reduction in the potential for challenges to
the safety systems, coupled with less time
that the safety systems are unavailable.
There will be no effect on those plant
systems necessary to effect the
accomplishment of protection functions.
No instrument setpoints or system
response times are affected. None of the
acceptance criteria for any accident analysis
will be changed.
The proposed change will have no impact
on the radiological consequences of a design
basis accident.
Therefore, the proposed amendment does
not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M. Stanford
Blanton, Balch & Bingham LLP, 1710
Sixth Avenue North, Birmingham, AL
35203–2015.
E:\FR\FM\21NON1.SGM
21NON1
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
NRC Branch Chief: Jennifer DixonHerrity.
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Southern Nuclear Operating Company,
Docket Nos. 52–025 and 52–026, Vogtle
Electric Generating Plant, Units 3 and 4,
Burke County, Georgia
Date of amendment request: August
18, 2017. A publicly-available version is
in ADAMS under Accession No.
ML17230A365.
Description of amendment request:
The requested amendment proposes to
depart from approved AP1000 Design
Control Document (DCD) Tier 2
information (text) and involved Tier 2*
information (as incorporated into the
Updated Final Safety Analysis Report
(UFSAR) as plant-specific DCD
information).
This amendment request proposes
increasing the design pressure of the
main steam (MS) isolation valve (MSIV)
compartments from 6.0 to 6.5 psi and
proposes other changes to the licensing
basis regarding descriptions of the MSIV
compartments.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented below
with Nuclear Regulatory Commission
(NRC) staff’s edits in square brackets:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes do not adversely
affect the operation of any structures,
systems, and components inside or outside
the auxiliary building that could initiate or
mitigate abnormal events, e.g., accidents,
anticipated operational occurrences,
earthquakes, floods, tornado missiles, and
turbine missiles, or their safety or design
analyses, evaluated in the UFSAR. The
changes do not adversely affect any design
function of the auxiliary building or the
structures, systems, and components
contained therein. The ability of the affected
auxiliary building main steam isolation valve
compartments and adjacent rooms, including
the main control room, to withstand the
pressurization effects from the postulated
pipe ruptures is not adversely affected by the
increase in design pressure, since the
structures, systems, and components therein
remain qualified for this service.
Therefore, the proposed activity does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes do not affect the
operation of any systems or equipment that
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
might initiate a new or different kind of
accident, or alter any [structure, system, and
component (SSC)] such that a new accident
initiator or initiating sequence of events is
created. The proposed changes do not
adversely affect the physical design and
operation of the [in-containment refueling
water storage tank (IRWST)] injection, drain,
containment recirculation, and fourth-stage
[automatic depressurization system (ADS)]
valves, including as-installed inspections,
and maintenance requirements, as described
in the UFSAR. Therefore, the operation of the
IRWST injection, drain, containment
recirculation, and fourth-stage ADS valves is
not adversely affected. These proposed
changes do not adversely affect any other
SSC design functions or methods of
operation in a manner that results in a new
failure mode, malfunction, or sequence of
events that affect safety-related or nonsafetyrelated equipment. Therefore, this activity
does not allow for a new fission product
release path, result in a new fission product
barrier failure mode, or create a new
sequence of events that result in significant
fuel cladding failures.
Therefore, the proposed amendment does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The margin of safety for the design of the
auxiliary building is maintained through
continued use of approved codes and
standards as stated in the UFSAR, and
adherence to the assumptions used in the
analyses of this structure and the events
associated with this structure. The auxiliary
building continues to be a seismic Category
I building with all current structural safety
margins maintained. The 3-hour fire rating
requirements for the impacted auxiliary
building walls are maintained. The
equipment housed in the main steam
isolation valve compartments continue to be
environmentally qualified for their intended
service in accordance with the approved
codes and standards stated within the
UFSAR. Thus, the requested changes will not
adversely affect any safety-related
equipment, design code, function, design
analysis, safety analysis input or result, or
design/safety margin. No safety analysis or
design basis acceptance limit/criterion is
challenged or exceeded by the requested
change, thus, no margin of safety is reduced.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M. Stanford
Blanton, Balch & Bingham LLP, 1710
Sixth Avenue North, Birmingham, AL
35203–2015.
PO 00000
Frm 00068
Fmt 4703
Sfmt 4703
55411
NRC Branch Chief: Jennifer DixonHerrity.
Southern Nuclear Operating Company,
Docket Nos. 52–025 and 52–026, Vogtle
Electric Generating Plant, Units 3 and 4,
Burke County, Georgia
Date of amendment request: October
6, 2017. A publicly-available version is
in ADAMS under Accession No.
ML17279A084.
Description of amendment request:
The amendment request proposes to
depart from Tier 2 information in the
Updated Final Safety Analysis Report
(UFSAR) (which includes the plantspecific Design Control Document
(DCD) Tier 2 information) and involves
related changes to plant-specific Tier 1
information, with corresponding
changes to the associated combined
license (COL) Appendix C information.
Pursuant to the provisions of 10 CFR
52.63(b)(1), an exemption from elements
of the design as certified in the 10 CFR
part 52, Appendix D, design
certification rule is also requested for
the plant-specific DCD Tier 1 material
departures. Specifically, the requested
amendment proposes to depart from
Tier 2 information in UFSAR
Subsection 8.3.2.4 describing raceway
and cable routing criteria and hazard
protection, and involves related changes
to plant-specific Tier 1 Table 3.3–6,
inspections, tests, analyses, and
acceptance criteria information, with
corresponding changes to the associated
COL Appendix C information.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented below
with NRC staff edits in square brackets:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Changes 1, 3 and 4 are clarifications only
and do not represent a change to the
minimum required separation distance
between raceways. Change 2 reduces the
required separation distances between
raceways from those documented in
[Institute of Electrical and Electronics
Engineers (IEEE)] 384–1981. These reduced
separation distances are based on specific
tests performed on the specified raceway
configurations, and the recommendations
from those tests contained in the associated
report. The NRC staff previously reviewed
the descriptions of the ten tests documented
in this report, including the ones applicable
to the existing UFSAR exceptions, and
concluded that they were acceptable, as
documented in NUREG–1793, ‘‘Final Safety
Evaluation Report Related to Certification of
E:\FR\FM\21NON1.SGM
21NON1
55412
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
asabaliauskas on DSKBBXCHB2PROD with NOTICES
the AP1000 Standard Design,’’ (Initial
Report) Subsection 8.3.2.2.
The reduced separation does not adversely
impact the ability to safely shutdown the
plant, and maintain it shutdown. The
referenced test report has shown a failure of
a faulted cable will not propagate to a nearby
target cable in way that adversely impacts its
function.
Therefore, the proposed amendment does
not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
Changes 1, 3 and 4 are clarifications only
and do not represent a change to the
minimum required separation distance
between circuits. Change 2 reduces the
required separation distances between
circuits from those documented in IEEE 384–
1981. This change does not result in a new
accident initiator or impact a current
accident initiator.
Therefore, the proposed amendment does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
Changes 1, 3 and 4 are clarifications only
and do not represent a change to the
minimum required separation distance
between circuits. Change 2 reduces the
required separation distances between
circuits from those documented in IEEE 384–
1981. These reduced separation distances are
based on specific tests performed on the
specified raceway configurations, and the
recommendations from those tests contained
in the associated report. The NRC staff
previously reviewed the descriptions of the
ten tests documented in this report,
including the ones applicable to the existing
UFSAR exceptions, and concluded that they
were acceptable, as documented in NUREG–
1793, ‘‘Final Safety Evaluation Report
Related to Certification of the AP1000
Standard Design,’’ (Initial Report) Subsection
8.3.2.2.
The reduced separation does not adversely
impact the ability to safely shutdown the
plant, and maintain it shutdown. The
referenced test report has shown a failure of
a faulted cable will not propagate to a nearby
target cable in a way that adversely impacts
its function.
Therefore, the proposed amendment does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M. Stanford
Blanton, Balch & Bingham LLP, 1710
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
Sixth Avenue North, Birmingham, AL
35203–2015.
NRC Branch Chief: Jennifer DixonHerrity.
Southern Nuclear Operating Company,
Inc., Georgia Power Company,
Oglethorpe Power Corporation,
Municipal Electric Authority of Georgia,
City of Dalton, Georgia, Docket Nos. 50–
321 and 50–366, Edwin I. Hatch Nuclear
Plant, Unit Nos. 1 and 2, Appling
County, Georgia
Date of amendment request: July 10,
2017. A publicly-available version is in
ADAMS under Accession No.
ML17191B163.
Description of amendment request:
The amendments would revise the
technical specifications (TSs) by: (1)
Adding a Note to the surveillance
requirements (SRs) of TS 3.7.7, ‘‘Main
Turbine Bypass System,’’ to clarify that
the SRs are not required to be met when
the limiting condition for operation
(LCO) does not require the Main
Turbine Bypass System to be operable,
(2) clarifying that LCO 3.2.3, ‘‘LINEAR
HEAT GENERATION RATE (LHGR),’’
also has limits for an inoperable Main
Turbine Bypass System that are made
applicable as specified in the Core
Operating Limits Report, and (3)
deleting an outdated footnote for LCO
3.2.3.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change (1) adds a Note to the
Surveillance Requirements (SRs) of the Hatch
Nuclear Plant (HNP) Unit 1 and Unit 2
Technical Specifications (TS) 3.7.7 clarifying
that the SRs are not required to be met when
the LCO does not require the Main Turbine
Bypass System to be Operable, (2) clarifies
that LCO 3.2.3, ‘‘LINEAR HEAT
GENERATION RATE’’ also has limits for an
inoperable Main Turbine Bypass System that
are made applicable as specified in the Core
Operating Limits Report, and (3) deletes an
outdated footnote for LCO 3.2.3. The
proposed change does not affect the
requirement to meet the LCO, nor does it
affect the requirements to perform the SRs
when the Main Turbine Bypass System is
being used to meet the LCO. This change
simply clarifies the existing allowance to
apply the Main Turbine Bypass System
inoperable limits to minimum critical power
ratio (MCPR) and linear heat generation rate
(LHGR) in lieu of the requirement for the
Main Turbine Bypass System to be Operable.
PO 00000
Frm 00069
Fmt 4703
Sfmt 4703
The current safety analysis evaluation is
unaffected by this proposed change. The
change regarding the outdated footnote has
no effect on the actual TS requirements.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change (1) adds a Note to the
Surveillance Requirements (SRs) of the Hatch
Nuclear Plant (HNP) Unit 1 and Unit 2
Technical Specifications (TS) 3.7.7 clarifying
that the SRs are not required to be met when
the LCO does not require the Main Turbine
Bypass System to be Operable, (2) clarifies
that LCO 3.2.3, ‘‘LINEAR HEAT
GENERATION RATE’’ also has limits for an
inoperable Main Turbine Bypass System that
are made applicable as specified in the Core
Operating Limits Report, and (3) deletes an
outdated footnote for LCO 3.2.3. This change
simply clarifies the existing allowance to
apply the Main Turbine Bypass System
inoperable limits to minimum critical power
ratio (MCPR) and linear heat generation rate
(LHGR) in lieu of the requirement for the
Main Turbine Bypass System to be Operable.
The change regarding the outdated footnote
has no effect on the actual TS requirements.
The current safety analysis evaluation is
unaffected by these proposed changes.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change (1) adds a Note to the
Surveillance Requirements (SRs) of the Hatch
Nuclear Plant (HNP) Unit 1 and Unit 2
Technical Specifications (TS) 3.7.7 clarifying
that the SRs are not required to be met when
the LCO does not require the Main Turbine
Bypass System to be Operable, (2) clarifies
that LCO 3.2.3, ‘‘LINEAR HEAT
GENERATION RATE’’ also has limits for an
inoperable Main Turbine Bypass System that
are made applicable as specified in the Core
Operating Limits Report, and (3) deletes an
outdated footnote for LCO 3.2.3. This change
simply clarifies the existing allowance to
apply the Main Turbine Bypass System
inoperable limits to minimum critical power
ratio (MCPR) and linear heat generation rate
(LHGR) in lieu of the requirement for the
Main Turbine Bypass System to be Operable.
The applicable safety analyses for TS 3.7.7 is
unaffected by this clarification. The change
regarding the outdated footnote has no effect
on the actual TS requirements.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
E:\FR\FM\21NON1.SGM
21NON1
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jennifer M.
Buettner, Associate General Counsel,
Southern Nuclear Operating Company,
40 Inverness Center Parkway,
Birmingham, AL 35242.
NRC Branch Chief: Michael T.
Markley.
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Southern Nuclear Operating Company,
Docket Nos. 52–025 and 52–026, Vogtle
Electric Generating Plant, Units 3 and 4,
Burke County, Georgia
Date of amendment request:
September 13, 2017. A publiclyavailable version is in ADAMS under
Accession No. ML17256A626.
Description of amendment request:
The requested amendment proposes to
depart from approved AP1000 Design
Control Document (DCD) Tier 2
information as incorporated into the
Updated Final Safety Analysis Report
(UFSAR) as plant-specific DCD
information, and from Technical
Specifications as incorporated in
Appendix A of the Combined License
(COL). Specifically, the proposed
changes revise COL Appendix A
Technical Specification 3.6.8 to identify
the trisodium phosphate (TSP) mass
value required in the pH adjustment
baskets. The TSP mass value adjusts the
pH of the containment water to >7.0
following a postulated accident.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed activity revises the mass of
trisodium phosphate (TSP), which raises the
pH of post-accident containment water to 7.0
or greater following a postulated accident.
The change to the TSP mass value does not
adversely impact the ability to support
radionuclide retention with high
radioactivity in containment and helps
prevent corrosion of containment equipment
during long-term floodup conditions. The
proposed changes do not adversely impact
previously evaluated accidents, because pH
control capability is provided to mitigate
already postulated accidents. As described in
Updated Final Safety Analysis Report
(UFSAR) Subsection 15.6.5.3.1.3, the passive
core cooling system (PXS) is assumed to
provide sufficient TSP to the post-loss-ofcoolant accident (LOCA) cooling solution to
maintain the pH at greater than or equal to
7.0 following a LOCA. The pH adjustment
baskets provide for long-term pH control.
Long-term pH control is not adversely
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
impacted as the pH adjustment baskets
contain the required amount of TSP to
support pH control requirements following a
design basis accident (DBA).
No safety-related structure, system,
component (SSC) or function is adversely
affected by this change. The change does not
involve an interface with any SSC accident
initiator or initiating sequence of events, and
thus, the probabilities of the accidents
evaluated in the UFSAR are not affected. The
proposed changes do not involve a change to
the predicted radiological releases due to
postulated accident conditions, thus, the
consequences of the accidents evaluated in
the UFSAR are not affected.
Therefore, the proposed amendment does
not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed activity revises the mass of
TSP, which raises the pH of containment to
7.0 or greater following a postulated accident.
The proposed activity does not create the
possibility of a new or different kind of
accident as pH adjustment is used to support
proper containment chemistry requirements
following an accident. The proposed activity
does not adversely affect any safety related
equipment, and does not add any new
interfaces to safety-related SSCs that
adversely affect safety functions. No system
or design function or equipment qualification
is adversely affected by these changes as the
changes do not modify any SSCs that prevent
safety functions from being performed. The
capability to maintain a maximum
containment pH below 9.5 is not adversely
impacted by these changes. The changes do
not introduce a new failure mode,
malfunction or sequence of events that could
adversely affect safety or safety related
equipment.
Therefore, the proposed amendment does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed activity revises the mass of
TSP, which raises the pH of containment to
7.0 or greater following a postulated accident.
The proposed activity does not affect any
other safety-related equipment or fission
product barriers. Containment water pH
adjustment is not adversely impacted. The
requested changes will not adversely affect
compliance with any design code, function,
design analysis, safety analysis input or
result, or design/safety margin. No safety
analysis or design basis acceptance limit/
criterion is challenged or exceeded by the
requested changes as previously evaluated
accidents are not impacted.
Therefore, the proposed amendment does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and based on this
review it appears that the three
PO 00000
Frm 00070
Fmt 4703
Sfmt 4703
55413
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazard consideration.
Attorney for licensee: M. Stanford
Blanton, Balch & Bingham LLP, 1710
Sixth Avenue North, Birmingham, AL
35203–2015.
NRC Branch Chief: Jennifer DixonHerrity.
Southern Nuclear Operating Company,
Docket Nos. 52–025 and 52–026, Vogtle
Electric Generating Plant (VEGP), Units
3 and 4, Burke County, Georgia
Date of amendment request:
September 29, 2017. A publiclyavailable version is in ADAMS under
Accession No. ML17272A957.
Description of amendment request:
The requested amendment proposes to
depart from Tier 2* and associated Tier
2 information in the Updated Final
Safety Analysis Report (UFSAR) (which
includes the plant-specific DCD Tier 2
information). The requested amendment
proposes to depart from UFSAR Tier 2*
information regarding resolution of
human engineering deficiencies (HEDs)
contained in Westinghouse Electric
Company’s report APP–OCS–GEH–320,
‘‘AP1000 Human Factors Engineering
Integrated Systems Validation Plan,’’
which is incorporated by reference into
the VEGP Units 3 and 4 UFSAR.
The proposed changes would revise
the licensing basis of the combined
licenses regarding the process for
addressing and re-testing of HEDs
identified during the integrated system
validation (ISV) as described in Tier 2*
document, APPOCS–GEH–320 ‘‘AP1000
Human Factors Engineering Integrated
System Validation Plan.’’ APPOCS–
GEH–320 references APP–OCS–GEH–
420, ‘‘Human Factors Engineering
Discrepancy Resolution Process,’’ which
defines the process for tracking,
resolution, and closure of HEDs. The
proposed changes to APP–OCS–GEH–
320 do not impact APP–OCS–GEH–420.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The Integrated System Validation (ISV)
provides a comprehensive human
performance-based assessment of the design
of the AP1000 Human-System Interface (HSI)
resources, based on their realistic operation
E:\FR\FM\21NON1.SGM
21NON1
asabaliauskas on DSKBBXCHB2PROD with NOTICES
55414
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
within a simulator driven Main Control
Room (MCR). The ISV is part of the overall
AP1000 Human Factors Engineering (HFE)
program. The changes to APP–OCS–GEH–
320, which is incorporated by reference into
the UFSAR, clarify the resources and
methodology used during re-testing
performed to verify the effectiveness of
Human Engineering Deficiency (HED)
resolution. The ISV Plan does not affect the
plant itself. Changing APP–OCS–GEH–320
and the UFSAR does not affect prevention
and mitigation of abnormal events, e.g.,
accidents, anticipated operational
occurrences, earthquakes, floods and turbine
missiles, or their safety or design analyses.
No safety-related structure, system,
component (SSC) or function is adversely
affected. The changes neither involve nor
interface with any SSC accident initiator or
initiating sequence of events, and thus, the
probabilities of the accidents evaluated in the
UFSAR are not affected. Because the changes
do not involve any safety-related SSC or
function used to mitigate an accident, the
consequences of the accidents evaluated in
the UFSAR are not affected.
Therefore, the proposed amendment does
not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The changes to APP–OCS–GEH–320 and
the VEGP 3 and 4 UFSAR affect only the
testing and validation of the MCR design and
HSI using a plant simulator. Therefore, the
changes do not affect the safety-related
equipment itself, nor do they affect
equipment which, if it failed, could initiate
an accident or a failure of a fission product
barrier. No analysis is adversely affected. No
system or design function or equipment
qualification is adversely affected by the
changes. This activity does not allow for a
new fission product release path, result in a
new fission product barrier failure mode, or
create a new sequence of events that would
result in significant fuel cladding failures. In
addition, the changes do not result in a new
failure mode, malfunction or sequence of
events that could affect safety or safety
related equipment.
Therefore, the proposed amendment does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The changes to APP–OCS–GEH–320 and
the UFSAR affect the testing and validation
of the MCR design and HSI using a plant
simulator. Therefore, the changes do not
affect the assessments or the plant itself.
These changes do not affect safety-related
equipment or equipment whose failure could
initiate an accident, nor does it adversely
interface with safety-related equipment or
fission product barriers. No safety analysis or
design basis acceptance limit/criterion is
challenged or exceeded by the requested
change.
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
Therefore, the proposed amendment does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and based on this
review it appears that the three
standards of 10 CFR 50.92 (c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazard consideration.
Attorney for licensee: M. Stanford
Blanton, Balch & Bingham LLP, 1710
Sixth Avenue North, Birmingham, AL
35203–2015.
NRC Branch Chief: Jennifer DixonHerrity.
Susquehanna Nuclear, LLC, Docket Nos.
50–387 and 50–388, Susquehanna
Steam Electric Station, Units 1 and 2,
Luzerne County, Pennsylvania
Date of amendment request:
September 20, 2017. A publiclyavailable version is in ADAMS under
Package Accession No. ML17265A434.
Description of amendment request:
The amendments would revise technical
specification (TS) requirements related
to ‘‘operations with a potential for
draining the reactor vessel’’ (OPDRVs)
with new requirements on reactor
pressure vessel (RPV) water inventory
control (WIC) to protect Safety Limit
2.1.1.3. Safety Limit 2.1.1.3 requires
RPV water level to be greater than the
top of active irradiated fuel. The
proposed changes are based on
Technical Specifications Task Force
(TSTF) Traveler TSTF–542, Revision 2,
‘‘Reactor Pressure Vessel Water
Inventory Control,’’ dated December 20,
2016.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes replace existing TS
requirements related to OPDRVs with new
requirements on RPV WIC that will protect
Safety Limit 2.1.1.3. Draining of RPV water
inventory in Mode 4 (i.e., cold shutdown)
and Mode 5 (i.e., refueling) is not an accident
previously evaluated and, therefore,
replacing the existing TS controls to prevent
or mitigate such an event with a new set of
controls has no effect on any accident
previously evaluated. RPV water inventory
control in Mode 4 or Mode 5 is not an
initiator of any accident previously
evaluated. The existing OPDRV controls or
the proposed RPV WIC controls are not
PO 00000
Frm 00071
Fmt 4703
Sfmt 4703
mitigating actions assumed in any accident
previously evaluated.
The proposed changes reduce the
probability of an unexpected draining event
(which is not a previously evaluated
accident) by imposing new requirements on
the limiting time in which an unexpected
draining event could result in the reactor
vessel water level dropping to the top of the
active fuel (TAF). These controls require
cognizance of the plant configuration and
control of configurations with unacceptably
short drain times. These requirements reduce
the probability of an unexpected draining
event. The current TS requirements are only
mitigating actions and impose no
requirements that reduce the probability of
an unexpected draining event.
The proposed changes reduce the
consequences of an unexpected draining
event (which is not a previously evaluated
accident) by requiring an Emergency Core
Cooling System (ECCS) subsystem to be
operable at all times in Modes 4 and 5. The
current TS requirements do not require any
water injection systems, ECCS or otherwise,
to be Operable in certain conditions in Mode
5. The change in requirement from two ECCS
subsystems to one ECCS subsystem in Modes
4 and 5 does not significantly affect the
consequences of an unexpected draining
event because the proposed Actions ensure
equipment is available within the limiting
drain time that is as capable of mitigating the
event as the current requirements. The
proposed controls provide escalating
compensatory measures to be established as
calculated drain times decrease, such as
verification of a second method of water
injection and additional confirmations that
containment and/or filtration would be
available if needed.
The proposed changes reduce or eliminate
some requirements that were determined to
be unnecessary to manage the consequences
of an unexpected draining event, such as
automatic initiation of an ECCS subsystem
and the Control Room Emergency Outside
Air Supply (CREOAS) system. These changes
do not affect the consequences of any
accident previously evaluated since a
draining event in Modes 4 and 5 is not a
previously evaluated accident and the
requirements are not needed to adequately
respond to a draining event.
The administrative update to delete
expired completion time notes is purely
administrative in nature.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes replace existing TS
requirements related to OPDRVs with new
requirements on RPV WIC that will protect
Safety Limit 2.1.1.3. The proposed changes
will not alter the design function of the
equipment involved. Under the proposed
changes, some systems that are currently
required to be operable during OPDRVs
would be required to be available within the
E:\FR\FM\21NON1.SGM
21NON1
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
asabaliauskas on DSKBBXCHB2PROD with NOTICES
limiting drain time or to be in service
depending on the limiting drain time. Should
those systems be unable to be placed into
service, the consequences are no different
than if those systems were unable to perform
their function under the current TS
requirements. The event of concern under the
current requirements and the proposed
changes are an unexpected draining event.
The proposed changes do not create new
failure mechanisms, malfunctions, or
accident initiators that would cause a
draining event or a new or different kind of
accident not previously evaluated or
included in the design and licensing bases.
The administrative update to delete
expired completion time notes is purely
administrative in nature.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes replace existing TS
requirements related to OPDRVs with new
requirements on RPV WIC. The current
requirements do not have a stated safety basis
and no margin of safety is established in the
licensing basis. The safety basis for the new
requirements is to protect Safety Limit
2.1.1.3. New requirements are added to
determine the limiting time in which the
RPV water inventory could drain to the top
of the fuel in the reactor vessel should an
unexpected draining event occur. Plant
configurations that could result in lowering
the RPV water level to the TAF within one
hour are now prohibited. New escalating
compensatory measures based on the limiting
drain time replace the current controls. The
proposed TS establish a safety margin by
providing defense-in-depth to ensure that the
Safety Limit is protected and to protect the
public health and safety. While some less
restrictive requirements are proposed for
plant configurations with long calculated
drain times, the overall effect of the change
is to improve plant safety and to add safety
margin.
The administrative update to delete
expired completion time notes is purely
administrative in nature.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Damon D. Obie,
Associate General Counsel, Talen
Energy Supply, LLC, 835 Hamilton St.,
Suite 150, Allentown, PA 18101.
NRC Branch Chief: James G. Danna.
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
Tennessee Valley Authority (TVA),
Docket Nos. 50–259, 50–260, and 50–
296, Browns Ferry Nuclear Plant (BFN),
Units 1, 2, and 3, Limestone County,
Alabama
Date of amendment request: August
15, 2017. A publicly-available version is
in ADAMS under Accession No.
ML17228A490.
Description of amendment request:
The amendments would revise the BFN,
Units 1, 2, and 3 Technical
Specification (TS) 5.5.12, ‘‘Primary
Containment Leakage Rate Testing
Program,’’ by adopting Nuclear Energy
Institute (NEI) 94–01, Revision 3–A,
‘‘Industry Guideline for Implementing
Performance-Based Option of 10 CFR
part 50, Appendix J,’’ as the
implementation document for the
performance-based Option B of 10 CFR
part 50, Appendix J. The proposed
changes permanently extend the Type A
containment integrated leak rate testing
(ILRT) interval from 10 years to 15 years
and the Type C local leakage rate testing
(LLRT) intervals from 60 months to 75
months.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequence of an accident previously
evaluated?
Response: No.
The proposed revision to TS 5.5.12
changes the testing period to a permanent 15year interval for Type A testing (10 CFR part
50, Appendix J, Option B, ILRT) and a 75month interval for Type C testing (10 CFR
part 50, Appendix J, Option B, LLRT). The
current Type A test interval of 10 years
would be extended to 15 years from the last
Type A test. The proposed extension to Type
A testing does not involve a significant
increase in the consequences of an accident
because research documented in NUREG–
1493, ‘‘Performance-Based Containment
System Leakage Testing Requirements’’
[‘‘Performance-Based Containment Leak-Test
Program’’], September 1995, has found that,
generically, very few potential containment
leakage paths are not identified by Type B
and C tests. NUREG–1493 concluded that
reducing the Type A testing frequency to one
per 20 years was found to lead to an
imperceptible increase in risk. A high degree
of assurance is provided through testing and
inspection that the containment will not
degrade in a manner detectable only by Type
A testing. The last Type A test (performed
November 19, 2010 for BFN, Unit 1, June 3,
2009 for BFN, Unit 2 and May 12, 2012 for
BFN, Unit 3) shows leakage to be below
acceptance criteria, indicating a very leak
tight containment. Inspections required by
PO 00000
Frm 00072
Fmt 4703
Sfmt 4703
55415
the ASME Code [American Society of
Mechanical Engineers Boiler and Press
Vessel Code] Section Xl (Subsection IWE)
and Maintenance Rule monitoring (10 CFR
50.65, ‘‘Requirements for Monitoring the
Effectiveness of Maintenance at Nuclear
Power Plants’’) are performed in order to
identify indications of containment
degradation that could affect that leak
tightness. Types B and C testing required by
TSs will identify any containment opening
such as valves that would otherwise be
detected by the Type A tests. These factors
show that a Type A test interval extension
will not represent a significant increase in
the consequences of an accident.
The proposed amendment involves
changes to the BFN, Units 1, 2, and 3, 10 CFR
50 Appendix J Testing Program Plan. The
proposed amendment does not involve a
physical change to the plant or a change in
the manner in which the units are operated
or controlled. The primary containment
function is to provide an essentially leak
tight barrier against the uncontrolled release
of radioactivity to the environment for
postulated accidents. As such, the
containment itself and the testing
requirements to periodically demonstrate the
integrity of the containment exist to ensure
the plant’s ability to mitigate the
consequences of an accident, and do not
involve any accident precursors or initiators.
Therefore, the probability of occurrence of an
accident previously evaluated is not
significantly increased by the proposed
amendment.
The proposed amendment adopts the NRCaccepted guidelines of NEI 94–01, Revision
3–A, for development of the BFN, Units 1, 2,
and 3, performance-based leakage testing
program. Implementation of these guidelines
continues to provide adequate assurance that
during design basis accidents, the primary
containment and its components will limit
leakage rates to less than the values assumed
in the plant safety analyses. The potential
consequences of extending the ILRT interval
from 10 years to 15 years have been
evaluated by analyzing the resulting changes
in risk. The increase in risk in terms of
person-rem [roentgen equivalent man] per
year resulting from design basis accidents
was estimated to be very small, and the
increase in the LERF [large early release
frequency] resulting from the proposed
change was determined to be within the
guidelines published in NRC RG [Regulatory
Guide] 1.174. Additionally, the proposed
change maintains defense-in-depth by
preserving a reasonable balance among
prevention of core damage, prevention of
containment failure, and consequence
mitigation. TVA has determined that the
increase in CCFP [conditional containment
failure probability] due to the proposed
change would be very small.
Based on the above discussions, the
proposed changes do not involve an increase
in the probability or consequences of an
accident previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
E:\FR\FM\21NON1.SGM
21NON1
asabaliauskas on DSKBBXCHB2PROD with NOTICES
55416
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
The proposed revision to TS 5.5.12
changes the testing period to a permanent 15year interval for Type A testing (10 CFR part
50, Appendix J, Option B, ILRT) and a 75month interval for Type C testing (10 CFR
part 50, Appendix J, Option B, LLRT). The
current test interval of 10 years, based on
past performance, would be extended to 15
years from the last Type A test (performed
November 19, 2010 for BFN, Unit 1, June 3,
2009 for BFN, Unit 2 and May 12, 2012 for
BFN, Unit 3). The proposed extension to
Type A and Type C test intervals does not
create the possibility of a new or different
type of accident because there are no
physical changes being made to the plant and
there are no changes to the operation of the
plant that could introduce a new failure
mode creating an accident or affecting the
mitigation of an accident.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed revision to TS 5.5.12
changes the testing period to a permanent 15year interval for Type A testing (10 CFR part
50, Appendix J, Option B, ILRT) and a 75month interval for Type C testing (10 CFR
part 50, Appendix J, Option B, LLRT). The
current test interval of 10 years, based on
past performance, would be extended to 15
years from the last Type A test (performed
November 19, 2010 for BFN, Unit 1, June 3,
2009 for BFN, Unit 2 and May 12, 2012 for
BFN, Unit 3). The proposed extension to
Type A testing will not significantly reduce
the margin of safety. NUREG–1493,
‘‘Performance-Based Containment System
Leakage Testing Requirements’’
[‘‘Performance-Based Containment Leak-Test
Program’’], September 1995, generic study of
the effects of extending containment leakage
testing, found that a 20 year extension to
Type A leakage testing resulted in an
imperceptible increase in risk to the public.
NUREG–1493 found that, generically, the
design containment leakage rate contributes
about 0.1% to the individual risk and that the
decrease in Type A testing frequency would
have a minimal effect on this risk since 95%
of the potential leakage paths are detected by
Type C testing. Regular inspections required
by the ASME Code Section Xl (Subsection
IWE) and maintenance rule monitoring (10
CFR 50.65, ‘‘Requirements for Monitoring the
Effectiveness of Maintenance at Nuclear
Power Plants’’) will further reduce the risk of
a containment leakage path going undetected.
The proposed amendment adopts the NRCaccepted guidelines of NEI 94–01, Revision
3–A, for development of the BFN, Units 1, 2,
and 3, performance-based leakage testing
program, and establishes a 15-year interval
for the performance of the primary
containment ILRT and a 75-month interval
for Type C testing. The amendment does not
alter the manner in which safety limits,
limiting safety system setpoints, or limiting
conditions for operation are determined. The
specific requirements and conditions of the
10 CFR part 50, Appendix J Testing Program
Plan, as defined in the TS, ensure that the
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
degree of primary containment structural
integrity and leak-tightness that is considered
in the plant safety analyses is maintained.
The overall containment leakage rate limit
specified by the TS is maintained, and the
Type A, B, and C containment leakage tests
will continue to be performed at the
frequencies established in accordance with
the NRC-accepted guidelines of NEI 94–01,
Revision 3–A.
Containment inspections performed in
accordance with other plant programs serve
to provide a high degree of assurance that the
containment will not degrade in a manner
that is detectable only by an ILRT. This
ensures that evidence of containment
structural degradation is identified in a
timely manner. Furthermore, a risk
assessment using the current BFN, Units 1,
2, and 3, PRA [probabilistic risk assessment]
model concluded that extending the ILRT
test interval from 10 years to 15 years results
in a very small change to the BFN, Units 1,
2, and 3, risk profile.
Accordingly, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Dr., WT 6A,
Knoxville, TN 37902.
NRC Branch Chief: Undine Shoop.
Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant, Units 1 and 2 (SQN),
Hamilton County, Tennessee
Tennessee Valley Authority, Docket
Nos. 50–390 and 50–391, Watts Bar
Nuclear Plant, Units 1 and 2 (WBN),
Rhea County, Tennessee
Date of amendment request: August 7,
2017. A publicly-available version is in
ADAMS under Accession No.
ML17219A505.
Description of amendment request:
The amendment would revise Technical
Specification (TS) 3.2.4, ‘‘Quadrant
Power Tilt Ratio (QPTR),’’ and TS 3.3.1,
‘‘Reactor Trip System (RTS)
Instrumentation,’’ to avoid confusion as
to when an incore power distribution
measurement for QPTR is required. The
amendment would also revise the WBN
TSs for consistency with the existing
SQN TSs and Westinghouse Standard
TSs in NUREG–1431, Revision 4.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
PO 00000
Frm 00073
Fmt 4703
Sfmt 4703
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes do not adversely
affect accident initiators or precursors nor
alter the design assumptions, conditions, or
configuration of the facility or the manner in
which the plant is operated and maintained.
The proposed changes do not alter or prevent
the ability of structures, systems, and
components (SSCs) from performing their
intended function to mitigate the
consequences of an initiating event within
the assumed acceptance limits. The proposed
changes do not affect the source term,
containment isolation, or radiological release
assumptions used in evaluating the
radiological consequences of an accident
previously evaluated. Further, the proposed
changes do not increase the types or amounts
of radioactive effluent that may be released
offsite, nor significantly increase individual
or cumulative occupational/public radiation
exposures. The proposed changes do not
significantly increase the probability of an
accident and are consistent with safety
analysis assumptions and resultant
consequences.
Therefore, the changes do not increase the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes do not result in a
change in the manner in which the reactor
trip system (RTS) and engineered safety
feature actuation system (ESFAS) provide
plant protection. The RTS and ESFAS will
continue to have the same setpoints after the
proposed changes are implemented. There
are no design changes associated with the
change. The changes do not involve a
physical alteration of the plant (i.e., no new
or different type of equipment will be
installed) or a change in the methods
governing normal plant operation. In
addition, the changes do not impose any new
or different requirements. The changes do not
alter assumptions made in the safety
analysis. The proposed changes are
consistent with the safety analysis
assumptions and current plant operating
practice.
Therefore, the changes do not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed changes do not alter the
manner in which safety limits, limiting safety
system settings or limiting conditions for
operation are determined. The safety analysis
acceptance criteria are not impacted by these
changes. Redundant RTS and ESFAS trains
are maintained, and diversity with regard to
the signals that provide reactor trip and
engineered safety features actuation is also
E:\FR\FM\21NON1.SGM
21NON1
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
maintained. All signals credited as providing
primary or secondary protection, and all
operator actions credited in the accident
analyses will remain the same. The proposed
changes will not result in plant operation in
a configuration outside the design basis.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, 6A West
Tower, Knoxville, TN 37902.
NRC Branch Chief: Undine Shoop.
asabaliauskas on DSKBBXCHB2PROD with NOTICES
III. Notice of Issuance of Amendments
to Facility Operating Licenses and
Combined Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR chapter I, which are set forth in
the license amendment.
A notice of consideration of issuance
of amendment to facility operating
license or combined license, as
applicable, proposed no significant
hazards consideration determination,
and opportunity for a hearing in
connection with these actions, was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.22(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
Assessment as indicated. All of these
items can be accessed as described in
the ‘‘Obtaining Information and
Submitting Comments’’ section of this
document.
Duke Energy Carolinas, LLC, Docket
Nos. 50–413 and 50–414, Catawba
Nuclear Station, Units 1 and 2, York
County, South Carolina
Date of amendment requests:
December 15, 2016.
Brief description of amendments: The
amendments modified Technical
Specification (TS) 3.4.10, ‘‘Pressurizer
Safety Valves,’’ TS 3.7.4, ‘‘Steam
Generator Power Operated Relief Valves
(SG PORVs),’’ and TS 3.7.6,
‘‘Condensate Storage System,’’ to revise
the Completion Times for Limiting
Condition for Operation (LCO) of TS
LCO 3.4.10 Required Action B.2, TS
LCO 3.7.4 Required Action C.2, and TS
LCO 3.7.6 Required Action B.2 from 12
to 24 hours. The proposed changes are
consistent with Technical Specifications
Task Force (TSTF) Traveler TSTF–352–
A, Revision 1, ‘‘Provide Consistent
Completion Time to Reach MODE 4.’’
Date of issuance: October 23, 2017.
Effective date: These license
amendments are effective as of its date
of issuance and shall be implemented
within 120 days of issuance.
Amendment Nos.: 294 (Unit 1) and
290 (Unit 2). A publicly-available
version is in ADAMS under Accession
No. ML17254A144; documents related
to these amendments are listed in the
Safety Evaluation enclosed with the
amendments.
Renewed Facility Operating License
Nos. NPF–35 and NPF–52: Amendments
revised the renewed licenses and
technical specifications.
Date of initial notice in Federal
Register: April 25, 2017 (82 FR 19099).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 23,
2017.
No significant hazards consideration
comments received: No.
Duke Energy Carolinas, LLC, Docket
Nos. 50–413 and 50–414, Catawba
Nuclear Station, Units 1 and 2, York
County, South Carolina
Date of amendment requests:
December 15, 2016.
Brief description of amendments: The
amendments modified technical
specification (TS) limiting condition for
operation (LCO) 3.7.5, ‘‘Auxiliary
Feedwater (AFW) System,’’ Condition A
and Required Action A.1. Condition A
was revised to include the situation
when one turbine-driven AFW pump is
inoperable in MODE 3, immediately
PO 00000
Frm 00074
Fmt 4703
Sfmt 4703
55417
following a refueling outage, only
applicable if MODE 2 has not been
entered following the refueling outage.
Required Action A.1 was revised to
include the turbine-driven AFW
addition to Condition A. The
amendments are consistent with
Technical Specifications Task Force
(TSTF) Traveler TSTF–340–A, Revision
3, ‘‘Allow 7 day Completion Time for a
turbine-driven AFW pump inoperable.’’
Date of issuance: October 23, 2017.
Effective date: These license
amendments are effective as of its date
of issuance and shall be implemented
within 120 days of issuance.
Amendment Nos.: 295 (Unit 1) and
291 (Unit 2). A publicly-available
version is in ADAMS under Accession
No. ML17257A297; documents related
to these amendments are listed in the
Safety Evaluation enclosed with the
amendments.
Renewed Facility Operating License
Nos. NPF–35 and NPF–52: Amendments
revised the renewed licenses and TSs.
Date of initial notice in Federal
Register: April 25, 2017 (82 FR 19100).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 23,
2017.
No significant hazards consideration
comments received: No.
Duke Energy Carolinas, LLC, Docket
Nos. 50–413 and 50–414, Catawba
Nuclear Station, Units 1 and 2, York
County, South Carolina
Date of amendment requests:
December 15, 2016.
Brief description of amendments: The
amendments revised Technical
Specification 3.1.2, ‘‘Core Reactivity,’’ to
revise the Completion Times of
Required Actions A.1 and A.2 from 72
hours to 7 days. This proposed change
is consistent with Technical
Specifications Task Force (TSTF)
Traveler TSTF–142–A, Revision 0,
‘‘Increase the Completion Time when
the Core Reactivity Balance is Not
Within Limit.’’
Date of issuance: October 23, 2017.
Effective date: As of the date of
issuance and shall be implemented
within 120 days of issuance.
Amendment Nos.: 296 (Unit 1) and
292 (Unit 2). A publicly-available
version is in ADAMS under Accession
No. ML17261B290; documents related
to these amendments are listed in the
Safety Evaluation enclosed with the
amendments.
Renewed Facility Operating License
Nos. NPF–35 and NPF–52: Amendments
revised the Renewed Licenses and
Technical Specifications.
E:\FR\FM\21NON1.SGM
21NON1
55418
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
Date of initial notice in Federal
Register: April 11, 2017 (82 FR 17457).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 23,
2017.
No significant hazards consideration
comments received: No.
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Duke Energy Carolinas, LLC, Docket
Nos. 50–369 and 50–370, McGuire
Nuclear Station, Units 1 and 2,
Mecklenburg County, North Carolina
Date of amendment requests: January
11, 2017.
Brief description of amendments: The
amendments modified Technical
Specification (TS) 3.8.1, ‘‘AC Sources—
Operating,’’ to allow greater flexibility
in performing Surveillance
Requirements (SRs) by modifying Mode
restriction notes in TS SRs 3.8.1.8,
3.8.1.11, 3.8.1.16, 3.8.1.17, and 3.8.1.19.
This proposed change was consistent
with Technical Specifications Task
Force (TSTF) Traveler TSTF–283–A,
Revision 3, ‘‘Modify Section 3.8 Mode
Restriction Notes.’’
Date of issuance: October 25, 2017.
Effective date: These license
amendments are effective as of its date
of issuance and shall be implemented
within 120 days of issuance.
Amendment Nos.: 300 (Unit 1) and
279 (Unit 2). A publicly-available
version is in ADAMS under Accession
No. ML17269A055; documents related
to these amendments are listed in the
Safety Evaluation enclosed with the
amendments.
Renewed Facility Operating License
Nos. NPF–9 and NPF–17: Amendments
revised the renewed facility operating
licenses and technical specifications.
Date of initial notice in Federal
Register: May 23, 2017 (82 FR 23620).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 25,
2017.
No significant hazards consideration
comments received: Yes. One comment
from a member of the public was
received, however it was not related to
the no significant hazards consideration
determination nor the license
amendment request.
Duke Energy Carolinas, LLC, Docket
Nos. 50–369 and 50–370, McGuire
Nuclear Station, Units 1 and 2,
Mecklenburg County, North Carolina
Date of amendment requests: January
11, 2017.
Brief description of amendments: The
amendments modified Technical
Specification (TS) 3.1.8, ‘‘PHYSICS
TESTS Exceptions,’’ to allow the
numbers of channels required by the
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
Limiting Condition for Operation (LCO)
section of TS 3.3.1, ‘‘Reactor Trip
System (RTS) Instrumentation,’’ to be
reduced from ‘‘4’’ to ‘‘3’’ to allow one
nuclear instrumentation channel to be
used as an input to the reactivity
computer for physics testing without
placing the nuclear instrumentation
channel in a tripped condition. This
proposed change is consistent with
Technical Specifications Task Force
(TSTF) Traveler TSTF–315–A, Revision
0, ‘‘Reduce plant trips due to spurious
signals to the NIS [Nuclear
Instrumentation System] during physics
testing.’’
Date of issuance: October 25, 2017.
Effective date: These license
amendments are effective as of their
date of issuance and shall be
implemented within 120 days of
issuance.
Amendment Nos.: 301 (Unit 1) and
280 (Unit 2). A publicly-available
version is in ADAMS under Accession
No. ML17261B218; documents related
to these amendments are listed in the
Safety Evaluation enclosed with the
amendments.
Renewed Facility Operating License
Nos. NPF–9 and NPF–17: Amendments
revised the renewed facility operating
licenses and technical specifications.
Date of initial notice in Federal
Register: May 23, 2017 (82 FR 23621).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 25,
2017.
No significant hazards consideration
comments received: Yes. One comment
from a member of the public was
received, however it was not related to
the proposed no significant hazards
consideration determination or to the
license amendment request.
Duke Energy Carolinas, LLC, Docket
Nos. 50–369 and 50–370, McGuire
Nuclear Station, Units 1 and 2,
Mecklenburg County, North Carolina
Date of amendment requests: January
11, 2017.
Brief description of amendments: The
amendments modify the limiting
condition for operation (LCO) Required
Action B.2 for Technical Specification
(TS) 3.4.10, ‘‘Pressurizer Safety Valves,’’
LCO Required Action C.2 for TS 3.7.4,
‘‘Steam Generator Power Operated
Relief Valves (SG PORVs),’’ and LCO
Required Action G.1 for TS 3.4.12, ‘‘Low
Temperature Overpressure Protection
(LTOP) System.’’ Specifically, the
Completion Times are revised from 12
hours to 24 hours for TS LCO 3.4.10,
Required Action B.2, and TS LCO 3.7.4,
Required Action C.2; and from 8 hours
to 12 hours for TS LCO 3.4.12, Required
PO 00000
Frm 00075
Fmt 4703
Sfmt 4703
Action G.1. The changes are consistent
with Technical Specifications Task
Force (TSTF) Traveler TSTF–352–A,
Revision 1, ‘‘Provide Consistent
Completion Time to Reach MODE 4.’’
Date of issuance: October 31, 2017.
Effective date: These license
amendments are effective as of their
date of issuance and shall be
implemented within 120 days of
issuance.
Amendment Nos.: 302 (Unit 1) and
281 (Unit 2). A publicly-available
version is in ADAMS under Accession
No. ML17269A198; documents related
to these amendments are listed in the
Safety Evaluation enclosed with the
amendments.
Renewed Facility Operating License
Nos. NPF–9 and NPF–17: Amendments
revised the Renewed Licenses and
Technical Specifications.
Date of initial notice in Federal
Register: May 23, 2017 (82 FR 23622).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 31,
2017.
No significant hazards consideration
comments received: Yes. One comment
from a member of the public was
received, however it was not related to
the proposed no significant hazards
consideration determination or to the
license amendment request.
Duke Energy Carolinas, LLC, Docket
Nos. 50–369 and 50–370, McGuire
Nuclear Station, Units 1 and 2,
Mecklenburg County, North Carolina
Date of amendment requests: January
11, 2017.
Brief description of amendments: The
amendments modify Technical
Specification (TS) 3.7.5, ‘‘Auxiliary
Feedwater (AFW) System,’’ Limiting
Condition for Operation (LCO)
Condition A and Required Action A.1.
The proposed changes modify
Condition A to expand the condition to
include when one turbine driven AFW
pump is inoperable in MODE 3. This
expanded condition is applicable
immediately following a refueling
outage and only if MODE 2 has not been
entered. Required Action A.1 is revised
to state ‘‘affected equipment’’ as
opposed to ‘‘steam supply’’ as a result
of the addition of the turbine driven
AFW pump to Condition A. The
changes are consistent with Technical
Specifications Task Force (TSTF)
Traveler TSTF–340–A, Revision 3,
‘‘Allow 7 day Completion Time for a
turbine-driven AFW pump inoperable.’’
Date of issuance: October 31, 2017.
Effective date: These license
amendments are effective as of their
date of issuance and shall be
E:\FR\FM\21NON1.SGM
21NON1
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
asabaliauskas on DSKBBXCHB2PROD with NOTICES
implemented within 120 days of
issuance.
Amendment Nos.: 304 (Unit 1) and
283 (Unit 2). A publicly-available
version is in ADAMS under Accession
No. ML17277A313; documents related
to these amendments are listed in the
Safety Evaluation enclosed with the
amendments.
Renewed Facility Operating License
Nos. NPF–9 and NPF–17: Amendments
revised the renewed facility operating
licenses and technical specifications.
Date of initial notice in Federal
Register: May 23, 2017 (82 FR 23621).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 31,
2017.
No significant hazards consideration
comments received: Yes. One comment
from a member of the public was
received, however it was not related to
the proposed no significant hazards
consideration determination or to the
license amendment request.
Duke Energy Carolinas, LLC, Docket
Nos. 50–369 and 50–370, McGuire
Nuclear Station, Units 1 and 2,
Mecklenburg County, North Carolina
Date of application for amendments:
January 11, 2017.
Brief description of amendments: The
amendments modify Technical
Specification (TS) Limiting Condition
for Operation (LCO) 3.9.6, ‘‘Residual
Heat Removal (RHR) and Coolant
Circulation—Low Water Level,’’ to add
a note which allows all RHR pumps to
be secured for less than or equal to 15
minutes to support the switching of the
shutdown cooling loops from one train
to another. The changes are consistent
with Technical Specifications Task
Force (TSTF) Travelers TSTF–349–A,
Revision 1, ‘‘Add Note to LCO 3.9.5
Allowing Shutdown Cooling Loops
Removal from Operation,’’ TSTF–361–
A, Revision 2, ‘‘Allow standby
[Shutdown Cooling] SDC/RHR/[Decay
Heat Removal] DHR loop to [be]
inoperable to support testing,’’ and
TSTF–438–A, Revision 0, ‘‘Clarify
Exception Notes to be Consistent with
the Requirement Being Excepted.’’
Date of issuance: October 31, 2017.
Effective date: As of the date of
issuance and shall be implemented
within 120 days of issuance.
Amendment Nos.: Unit 1—303; Unit
2—282. A publicly-available version is
in ADAMS under Accession No.
ML17271A034; documents related to
these amendments are listed in the
Safety Evaluation enclosed with the
amendments.
Renewed Facility Operating License
Nos. NPF–9 and NPF–17: Amendments
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
revised the Renewed Licenses and
Technical Specifications.
Date of initial notice in Federal
Register: May 23, 2017 (82 FR 23623).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 31,
2017.
No significant hazards consideration
comments received: Yes. One comment
from a member of the public was
received, however it was not related to
the proposed no significant hazards
consideration determination or the
license amendment request.
Duke Energy Progress, LLC, Docket No.
50–400, Shearon Harris Nuclear Power
Plant, Unit 1, Wake and Chatham
Counties, North Carolina
Date of amendment request:
December 2, 2016, as supplemented by
letters dated April 25, May 22, and
October 2, 2017.
Brief description of amendment: The
amendment revised the Technical
Specifications (TSs) to (1) relocate
cycle-specific parameters to the Core
Operating Limits Report (COLR)
consistent with Technical Specification
Task Force (TSTF)-339, ‘‘Relocate TS
Parameters to COLR;’’ (2) delete
duplicate reporting requirements in the
Administrative Section of TSs
consistent with TSTF–5, ‘‘Delete Safety
Limit Violation Notification
Requirements,’’ Revision 1; and (3)
delete reference to plant procedure
PLP–6, ‘‘Technical Specification
Equipment List Program and Core
Operating Limits Report,’’ in TSs as it
pertains to the COLR.
Date of issuance: November 6, 2017.
Effective date: As of the date of
issuance and shall be implemented
within 90 days of issuance.
Amendment No.: 161. A publiclyavailable version is in ADAMS under
Accession No. ML17250A202;
documents related to this amendment
are listed in the Safety Evaluation
enclosed with the amendment.
Renewed Facility Operating License
No. NPF–63: Amendment revised the
Facility Operating License and TSs.
Date of initial notice in Federal
Register: February 14, 2017 (82 FR
10595). The supplemental letters dated
April 25, May 22, and October 2, 2017,
provided additional information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the staff’s
original proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
PO 00000
Frm 00076
Fmt 4703
Sfmt 4703
55419
Safety Evaluation dated November 6,
2017.
No significant hazards consideration
comments received: No.
Energy Northwest, Docket No. 50–397,
Columbia Generating Station, Benton
County, Washington
Date of amendment request:
November 8, 2016, as supplemented by
letter dated July 11, 2017.
Brief description of amendment: The
amendment would, on a one-time basis,
extend the completion time from 7 days
to 14 days for the Residual Heat
Removal Train A subsystem to operable
status associated with Technical
Specification (TS) 3.5.1, ‘‘ECCS
[Emergency Core Cooling System]—
Operating’’; TS 3.6.1.5, ‘‘Residual Heat
Removal (RHR) Drywell Spray’’; and TS
3.6.2.3, ‘‘Residual Heat Removal (RHR)
Suppression Pool Cooling.’’ This
amendment will be used to support
preventive maintenance, which replaces
the RHR Train A subsystem’s pump and
motor.
Date of issuance: October 30, 2017.
Effective date: As of its date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment No.: 245. A publiclyavailable version is in ADAMS under
Accession No. ML17290A127;
documents related to this amendment
are listed in the Safety Evaluation
enclosed with the amendment.
Renewed Facility Operating License
No. NPF–21: The amendment revised
the Renewed Facility Operating License
and Technical Specifications.
Date of initial notice in Federal
Register: February 14, 2017 (82 FR
10596). The supplemental letter dated
July 11, 2017, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the NRC staff’s
original proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 30,
2017.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC and
PSEG Nuclear LLC, Docket No. 50–277,
Peach Bottom Atomic Power Station,
Unit 2, York and Lancaster Counties,
Pennsylvania
Date of amendment request: May 19,
2017, as supplemented by letter dated
August 29, 2017.
E:\FR\FM\21NON1.SGM
21NON1
55420
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Brief description of amendment: The
amendment revised the Technical
Specifications to decrease the number of
safety relief valves and safety valves
required to be operable when operating
at a power level less than or equal to
3,358 megawatts thermal. This change is
applicable only to the current Cycle 22
that is scheduled to end in October
2018.
Date of issuance: October 25, 2017.
Effective date: As of the date of
issuance and shall be implemented
within 5 days.
Amendment No.: 315. A publiclyavailable version is in ADAMS under
Accession No. ML17249A151;
documents related to this amendment
are listed in the Safety Evaluation
enclosed with the amendment.
Renewed Facility Operating License
No. DPR–44: The amendment revised
the Renewed Facility Operating License
and Technical Specifications.
Date of initial notice in Federal
Register: July 5, 2017 (82 FR 31094).
The supplemental letter dated August
29, 2017, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the NRC staff’s
original proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 25,
2017.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket Nos. 50–373 and 50–374, LaSalle
County Station (LSCS), Units 1 and 2,
LaSalle County, Illinois
Date of application for amendments:
October 27, 2016, as supplemented by
the letters dated July 28, 2017, August
30, 2017, and October 19, 2017.
Brief description of amendments: The
amendments revised the suppression
pool swell design analysis. The new
analysis utilizes a different computer
code and incorporates different analysis
assumptions than the current analysis.
The changes are necessary because the
current design analysis determining the
suppression pool swell response to a
loss-of-coolant accident was determined
to be non-conservative.
These changes to the suppression
pool swell design analysis do not
require any changes to the LSCS
Technical Specifications. Changes to the
LSCS updated final safety analysis
report related to changes to the
suppression pool swell design analysis
shall be made in accordance with 10
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
CFR 50.71(e) based on the NRC approval
of these changes.
Date of issuance: October 30, 2017.
Effective date: These license
amendments are effective as of the date
of its issuance and shall be
implemented within 60 days from the
date of issuance.
Amendment Nos.: 225 for NPF–11
and 211 for NPF–18. A publiclyavailable version is in ADAMS under
Accession No. ML17257A304;
documents related to this amendment
are listed in the Safety Evaluation
enclosed with the amendment.
Facility Operating License Nos. NPF–
11 and NPF–18: The amendments
approved to revise the LSCS updated
final safety analysis report related to
changes to the suppression pool swell
design analysis and the Licenses.
Date of initial notice in Federal
Register: March 8, 2017 (82 FR 13022).
The supplements dated July 28, 2017,
August 30, 2017, and October 19, 2017,
contained clarifying information and
did not change the NRC staff’s initial
proposed finding of no significant
hazards consideration.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 30,
2017.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket No. 50–410, Nine Mile Point
Nuclear Station (Nine Mile Point), Unit
2, Oswego County, New York
Date of amendment request:
December 13, 2016, as supplemented by
letter dated February 17, 2017.
Brief description of amendment: The
amendment revised the Nine Mile Point,
Unit 2, Technical Specification (TS)
safety limit (SL) to increase the low
pressure isolation setpoint allowable
value, which will result in earlier main
steam line isolation. The revised main
steam line low pressure isolation
capability and the revised SL are
intended to ensure that Nine Mile Point,
Unit 2, remains within the TS SLs in the
event of a pressure regulator failure
maximum demand transient.
Date of issuance: October 31, 2017.
Effective date: As of the date of
issuance and shall be implemented
within 180 days of issuance.
Amendment No.: 164. A publiclyavailable version is in ADAMS under
Accession No. ML17268A263;
documents related to this amendment
are listed in the Safety Evaluation
enclosed with the amendment.
Renewed Facility Operating License
No. NPF–69: Amendment revised the
PO 00000
Frm 00077
Fmt 4703
Sfmt 4703
Renewed Facility Operating License and
Technical Specifications.
Date of initial notice in Federal
Register: March 28, 2017 (82 FR
15381). The supplemental letter dated
February 17, 2017, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the NRC staff’s
original proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 31,
2017.
No significant hazards consideration
comments received: No.
Florida Power & Light Company, et al.,
Docket Nos. 50–335 and 50–389, St.
Lucie Plant, Unit Nos. 1 and 2, St. Lucie
County, Florida
Date of amendment request: January
23, 2017, as supplemented by letter
dated July 3, 2017.
Brief description of amendments: The
amendments revised the Technical
Specifications (TSs) by limiting the
MODE of applicability for the Reactor
Protection System, Startup, and
Operating Rate of Change of Power—
High, functional unit trip. Additionally,
the amendments added new Limiting
Condition for Operation (LCO) 3.0.5 and
relatedly modified LCO 3.0.1 and LCO
3.0.2, to provide for placing inoperable
equipment under administrative control
for the purpose of conducting testing
required to demonstrate OPERABILITY.
Date of issuance: November 2, 2017.
Effective date: As of the date of
issuance and shall be implemented
within 90 days of issuance.
Amendment Nos.: 243 and 194. A
publicly-available version is in ADAMS
under Accession No. ML17257A015;
documents related to this amendment
are listed in the Safety Evaluation
enclosed with the amendment.
Renewed Facility Operating License
Nos. DPR–67 and NPF–16: Amendments
revised the Renewed Facility Operating
Licenses and TSs.
Date of initial notice in Federal
Register: March 28, 2017 (82 FR
15383). The supplemental letter dated
July 3, 2017, provided additional
information that expanded the scope of
the application as originally noticed and
changed the NRC staff’s original
proposed no significant hazards
consideration (NSHC) determination as
published in the Federal Register.
Accordingly, the NRC published a
second proposed no significant hazards
consideration determination in the
Federal Register on September 12, 2017
E:\FR\FM\21NON1.SGM
21NON1
Federal Register / Vol. 82, No. 223 / Tuesday, November 21, 2017 / Notices
(82 FR 42849). This notice superseded
the original notice in its entirety. It also
provided an opportunity to request a
hearing by November 13, 2017, but
indicated that if the Commission makes
a final NSHC determination, any such
hearing would take place after issuance
of the amendments.
The Commission’s related evaluation
of the amendments and final NSHC are
contained in a Safety Evaluation dated
November 2, 2017.
No significant hazards consideration
comments received: No.
asabaliauskas on DSKBBXCHB2PROD with NOTICES
Florida Power & Light Company, Docket
Nos. 50–250 and 50–251, Turkey Point
Nuclear Generating Unit Nos. 3 and 4,
Miami-Dade County, Florida
Date of amendment request:
December 21, 2016.
Brief description of amendments: The
amendments modify the Technical
Specifications by deleting high-range
noble gas effluent monitors’
requirements and relocating the
requirements to the Turkey Point Offsite
Dose Calculation Manual.
Date of issuance: October 26, 2017.
Effective date: As of the date of
issuance and shall be implemented
within 90 days of issuance.
Amendment Nos: 277 and 272. A
publicly-available version is in ADAMS
under Accession No. ML17228A563.
Documents related to these amendments
are listed in the Safety Evaluation
enclosed with the amendments.
Renewed Facility Operating License
Nos. DPR–31 and DPR–41: Amendments
revised the Renewed Facility Operating
Licenses and TSs.
Date of initial notice in Federal
Register: March 14, 2017 (82 FR
13666).
The Commission’s related evaluation
of the amendments is contained in a
safety evaluation dated October 26,
2017.
No significant hazards consideration
comments received: No.
Southern Nuclear Operating Company,
Docket Nos. 50–348 and 50–364, Joseph
M. Farley Nuclear Plant, Units 1 and 2,
Houston County, Alabama
Date of amendment request: August
11, 2017.
Brief description of amendments: The
amendments request an extension to the
time to achieve full compliance with 10
CFR 50.48(c), National Fire Protection
Association (NPFA) 805, from
November 6, 2017, to the conclusion of
the FNP, Unit 1, Spring 2018 Refueling
Outage (1R28). The amendments update
Attachment S, ‘‘Modification and
Implementation Items’’; of the
previously approved NFPA–805
amendment.
VerDate Sep<11>2014
18:56 Nov 20, 2017
Jkt 244001
Date of issuance: November 1, 2017.
Effective date: As of the date of
issuance and shall be implemented
within 30 days of issuance.
Amendment Nos.: 215 (Unit 1) and
212 (Unit 2). A publicly-available
version is in ADAMS under Accession
No. ML17269A166; documents related
to these amendments are listed in the
Safety Evaluation enclosed with the
amendments.
Renewed Facility Operating License
Nos. NPF–2 and NPF–8: The
amendments revised the Renewed
Facility Operating Licenses.
Date of initial notice in Federal
Register: August 29, 2017 (82 FR
41059).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated November 1,
2017.
No significant hazards consideration
comments received: No.
Dated at Rockville, Maryland, this 14th day
of November 2017.
For the Nuclear Regulatory Commission.
Kathryn M. Brock,
Acting Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. 2017–25063 Filed 11–20–17; 8:45 am]
BILLING CODE 7590–01–P
OFFICE OF PERSONNEL
MANAGEMENT
Submission for Review: Reinstatement
of a Previously Approved Information
Collection With Revision, U.S. Office of
Personnel Management (OPM)
Standard Form (SF) 15, Application for
10-Point Veteran Preference, OMB No.
3206–0001
U.S. Office of Personnel
Management.
ACTION: 60-Day notice and request for
comments.
AGENCY:
This notice announces the
Office of Personnel Management’s
(OPM) plan to submit to the Office of
Management and Budget (OMB) a
request for reinstatement of a revised
information collection for the Standard
Form (SF) 15, Application for 10-Point
Veteran Preference. The SF–15 is used
by agencies, OPM examining offices,
and agency appointing officials to
adjudicate individuals’ claims for
veterans’ preference in accordance with
the Veterans’ Preference Act of 1944.
OPM’s revisions are necessary to update
language as a result of the enactment of
the Gold Star Fathers Act of 2015,
derived veterans’ preference for parents,
SUMMARY:
PO 00000
Frm 00078
Fmt 4703
Sfmt 4703
55421
and to make additional corrections to
the form.
DATES: Comments are encouraged and
will be accepted until January 22, 2018.
ADDRESSES: You may send or deliver
comments to Kimberly A. Holden,
Deputy Associate Director for Talent
Acquisition and Workforce Shaping,
Employee Services, U.S. Office of
Personnel Management, Room 6351D,
1900 E Street NW., Washington, DC
20415–9700; email at employ@opm.gov;
or fax at (202) 606–2329; and to OMB
Designee, OPM Desk Officer, Office of
Management and Budget, Office of
Information and Regulatory Affairs,
New Executive Office Building NW.,
Room 10235, Washington, DC 20503.
FOR FURTHER INFORMATION CONTACT:
Roseanna Ciarlante by telephone at
(267) 932–8640; by fax at (202) 606–
4430; by TTY at (202) 418–3134; or by
email at Roseanna.Ciarlante@opm.gov.
SUPPLEMENTARY INFORMATION: The Office
of Management and Budget is
particularly interested in comments
that:
1. Evaluate whether the proposed
collection of information is necessary
for the proper performance of the
functions of the agency, including
whether the information will have
practical utility;
2. Evaluate the accuracy of the
agency’s estimate of the burden of the
proposed collection of information,
including the validity of the
methodology and assumptions used;
3. Enhance the quality, utility, and
clarity of the information to be
collected; and
4. Minimize the burden of the
collection of information on those who
are to respond, including through the
use of appropriate automated,
electronic, mechanical, or other
technological collection techniques or
other forms of information technology,
e.g., permitting electronic submissions
of responses.
The SF 15, Application for 10-Point
Veteran Preference, is used by veterans
as both a request for preference and a
guide to determine the appropriate
documentation to submit to support
their claims of 10-point veterans’
preference when applying for Federal
employment. The SF 15, and the
accompanying documentation, is used
by agencies, OPM examining offices,
and agency appointing officials to
adjudicate individuals’ claims for
veterans’ preference in accordance with
the Veterans’ Preference Act of 1944.
The proposed revisions to the SF 15 are
necessary to update language as a result
of the enactment of the Gold Star
Fathers Act of 2015 (Pub. L. 114–62),
E:\FR\FM\21NON1.SGM
21NON1
Agencies
[Federal Register Volume 82, Number 223 (Tuesday, November 21, 2017)]
[Notices]
[Pages 55401-55421]
From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
[FR Doc No: 2017-25063]
=======================================================================
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
[NRC-2017-0220]
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses and Combined Licenses Involving No Significant
Hazards Considerations
AGENCY: Nuclear Regulatory Commission.
ACTION: Biweekly notice.
-----------------------------------------------------------------------
SUMMARY: Pursuant to Section 189a.(2) of the Atomic Energy Act of 1954,
as amended (the Act), the U.S. Nuclear Regulatory Commission (NRC) is
publishing this regular biweekly notice. The Act requires the
Commission to publish notice of any amendments issued, or proposed to
be issued, and grants the Commission the authority to issue and make
immediately effective any amendment to an operating license or combined
license, as applicable, upon a determination by the Commission that
such amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued, from October 24, 2017 to November 6, 2017. The
last biweekly notice was published on November 7, 2017.
DATES: Comments must be filed by December 21, 2017. A request for a
hearing must be filed by January 22, 2018.
ADDRESSES: You may submit comments by any of the following methods
(unless this document describes a different method for submitting
comments on a specific subject):
Federal Rulemaking Web site: Go to https://www.regulations.gov and search for Docket ID NRC-2017-0220. Address
questions about NRC dockets to Carol Gallagher; telephone: 301-415-
3463; email: Carol.Gallagher@nrc.gov. For technical questions, contact
the individual listed in the FOR FURTHER INFORMATION CONTACT section of
this document.
Mail comments to: May Ma, Office of Administration, Mail
Stop: OWFN-2-A13, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001.
For additional direction on obtaining information and submitting
comments, see ``Obtaining Information and Submitting Comments'' in the
SUPPLEMENTARY INFORMATION section of this document.
FOR FURTHER INFORMATION CONTACT: Shirley Rohrer, Office of Nuclear
Reactor Regulation, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001; telephone: 301-415-5411, email: Shirley.Rohrer@nrc.gov.
SUPPLEMENTARY INFORMATION:
I. Obtaining Information and Submitting Comments
A. Obtaining Information
Please refer to Docket ID NRC-2017-0220, facility name, unit
number(s), plant docket number, application date, and subject when
contacting the NRC about the availability of information for this
action. You may obtain publicly-available information related to this
action by any of the following methods:
Federal Rulemaking Web site: Go to https://www.regulations.gov and search for Docket ID NRC-2017-0220.
NRC's Agencywide Documents Access and Management System
(ADAMS): You may obtain publicly-available documents online in the
ADAMS Public Documents collection at https://www.nrc.gov/reading-rm/adams.html. To begin the search, select ``ADAMS Public Documents'' and
then select ``Begin Web-based ADAMS Search.'' For problems with ADAMS,
please contact the NRC's Public Document Room (PDR) reference staff at
1-800-397-4209, 301-415-4737, or by email to pdr.resource@nrc.gov. The
ADAMS accession number for each document referenced (if it is available
in ADAMS) is provided the first time that it is mentioned in this
document.
NRC's PDR: You may examine and purchase copies of public
documents at the NRC's PDR, Room O1-F21, One White Flint North, 11555
Rockville Pike, Rockville, Maryland 20852.
B. Submitting Comments
Please include Docket ID NRC-2017-0220, facility name, unit
number(s), plant docket number, application date, and subject in your
comment submission.
The NRC cautions you not to include identifying or contact
information that you do not want to be publicly disclosed in your
comment submission. The NRC will post all comment submissions at https://www.regulations.gov as well as enter the comment submissions into
ADAMS. The NRC does not routinely edit comment submissions to remove
identifying or contact information.
If you are requesting or aggregating comments from other persons
for submission to the NRC, then you should inform those persons not to
include identifying or contact information that they do not want to be
publicly disclosed in their comment submission. Your request should
state that the NRC does not routinely edit comment submissions to
remove such information before making the comment submissions available
to the public or entering the comment into ADAMS.
II. Notice of Consideration of Issuance of Amendments to Facility
Operating Licenses and Combined Licenses and Proposed No Significant
Hazards Consideration Determination
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in Sec. 50.92 of title 10 of the Code of
Federal Regulations (10 CFR), this means that operation of the facility
in accordance with the proposed amendment would not (1) involve a
significant increase in the probability or consequences of an accident
previously evaluated, or (2) create the possibility of a new or
different kind of accident from any accident previously evaluated; or
(3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period if circumstances change during the 30-day comment
period such that failure to act in a timely way would result, for
example in derating or shutdown of the facility. If the Commission
takes action prior to the expiration of either the comment period or
the notice period, it will publish in the Federal Register a notice of
[[Page 55402]]
issuance. If the Commission makes a final no significant hazards
consideration determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
A. Opportunity To Request a Hearing and Petition for Leave To Intervene
Within 60 days after the date of publication of this notice, any
persons (petitioner) whose interest may be affected by this action may
file a request for a hearing and petition for leave to intervene
(petition) with respect to the action. Petitions shall be filed in
accordance with the Commission's ``Agency Rules of Practice and
Procedure'' in 10 CFR part 2. Interested persons should consult a
current copy of 10 CFR 2.309. The NRC's regulations are accessible
electronically from the NRC Library on the NRC's Web site at https://www.nrc.gov/reading-rm/doc-collections/cfr/. Alternatively, a copy of
the regulations is available at the NRC's Public Document Room, located
at One White Flint North, Room O1-F21, 11555 Rockville Pike (First
Floor), Rockville, Maryland 20852. If a petition is filed, the
Commission or a presiding officer will rule on the petition and, if
appropriate, a notice of a hearing will be issued.
As required by 10 CFR 2.309(d) the petition should specifically
explain the reasons why intervention should be permitted with
particular reference to the following general requirements for
standing: (1) The name, address, and telephone number of the
petitioner; (2) the nature of the petitioner's right under the Act to
be made a party to the proceeding; (3) the nature and extent of the
petitioner's property, financial, or other interest in the proceeding;
and (4) the possible effect of any decision or order which may be
entered in the proceeding on the petitioner's interest.
In accordance with 10 CFR 2.309(f), the petition must also set
forth the specific contentions which the petitioner seeks to have
litigated in the proceeding. Each contention must consist of a specific
statement of the issue of law or fact to be raised or controverted. In
addition, the petitioner must provide a brief explanation of the bases
for the contention and a concise statement of the alleged facts or
expert opinion which support the contention and on which the petitioner
intends to rely in proving the contention at the hearing. The
petitioner must also provide references to the specific sources and
documents on which the petitioner intends to rely to support its
position on the issue. The petition must include sufficient information
to show that a genuine dispute exists with the applicant or licensee on
a material issue of law or fact. Contentions must be limited to matters
within the scope of the proceeding. The contention must be one which,
if proven, would entitle the petitioner to relief. A petitioner who
fails to satisfy the requirements at 10 CFR 2.309(f) with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene.
Parties have the opportunity to participate fully in the conduct of the
hearing with respect to resolution of that party's admitted
contentions, including the opportunity to present evidence, consistent
with the NRC's regulations, policies, and procedures.
Petitions must be filed no later than 60 days from the date of
publication of this notice. Petitions and motions for leave to file new
or amended contentions that are filed after the deadline will not be
entertained absent a determination by the presiding officer that the
filing demonstrates good cause by satisfying the three factors in 10
CFR 2.309(c)(1)(i) through (iii). The petition must be filed in
accordance with the filing instructions in the ``Electronic Submissions
(E-Filing)'' section of this document.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to establish when the hearing is held. If the final determination is
that the amendment request involves no significant hazards
consideration, the Commission may issue the amendment and make it
immediately effective, notwithstanding the request for a hearing. Any
hearing would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, then any hearing held would take place before
the issuance of the amendment unless the Commission finds an imminent
danger to the health or safety of the public, in which case it will
issue an appropriate order or rule under 10 CFR part 2.
A State, local governmental body, Federally-recognized Indian
Tribe, or agency thereof, may submit a petition to the Commission to
participate as a party under 10 CFR 2.309(h)(1). The petition should
state the nature and extent of the petitioner's interest in the
proceeding. The petition should be submitted to the Commission no later
than 60 days from the date of publication of this notice. The petition
must be filed in accordance with the filing instructions in the
``Electronic Submissions (E-Filing)'' section of this document, and
should meet the requirements for petitions set forth in this section,
except that under 10 CFR 2.309(h)(2) a State, local governmental body,
or federally recognized Indian Tribe, or agency thereof does not need
to address the standing requirements in 10 CFR 2.309(d) if the facility
is located within its boundaries. Alternatively, a State, local
governmental body, Federally-recognized Indian Tribe, or agency thereof
may participate as a non-party under 10 CFR 2.315(c). If a hearing is
granted, any person who is not a party to the proceeding and is not
affiliated with or represented by a party may, at the discretion of the
presiding officer, be permitted to make a limited appearance pursuant
to the provisions of 10 CFR 2.315(a). A person making a limited
appearance may make an oral or written statement of his or her position
on the issues but may not otherwise participate in the proceeding. A
limited appearance may be made at any session of the hearing or at any
prehearing conference, subject to the limits and conditions as may be
imposed by the presiding officer. Details regarding the opportunity to
make a limited appearance will be provided by the presiding officer if
such sessions are scheduled.
B. Electronic Submissions (E-Filing)
All documents filed in NRC adjudicatory proceedings, including a
request for hearing and petition for leave to intervene (petition), any
motion or other document filed in the proceeding prior to the
submission of a request for hearing or petition to intervene, and
documents filed by interested governmental entities that request to
participate under 10 CFR 2.315(c), must be filed in accordance with the
NRC's E-Filing rule (72 FR 49139; August 28, 2007, as amended at 77 FR
46562, August 3, 2012). The E-Filing process requires participants to
submit and serve all adjudicatory documents over the internet, or in
some cases to mail copies on electronic storage media. Detailed
guidance on making electronic submissions may be found in the Guidance
for Electronic Submissions to the NRC and on the NRC Web site at https://www.nrc.gov/site-help/e-submittals.html. Participants may not submit
paper copies of their filings unless they seek an exemption in
[[Page 55403]]
accordance with the procedures described below.
To comply with the procedural requirements of E-Filing, at least 10
days prior to the filing deadline, the participant should contact the
Office of the Secretary by email at hearing.docket@nrc.gov, or by
telephone at 301-415-1677, to (1) request a digital identification (ID)
certificate, which allows the participant (or its counsel or
representative) to digitally sign submissions and access the E-Filing
system for any proceeding in which it is participating; and (2) advise
the Secretary that the participant will be submitting a petition or
other adjudicatory document (even in instances in which the
participant, or its counsel or representative, already holds an NRC-
issued digital ID certificate). Based upon this information, the
Secretary will establish an electronic docket for the hearing in this
proceeding if the Secretary has not already established an electronic
docket.
Information about applying for a digital ID certificate is
available on the NRC's public Web site at https://www.nrc.gov/site-help/e-submittals/getting-started.html. Once a participant has obtained a
digital ID certificate and a docket has been created, the participant
can then submit adjudicatory documents. Submissions must be in Portable
Document Format (PDF). Additional guidance on PDF submissions is
available on the NRC's public Web site at https://www.nrc.gov/site-help/electronic-sub-ref-mat.html. A filing is considered complete at the
time the document is submitted through the NRC's E-Filing system. To be
timely, an electronic filing must be submitted to the E-Filing system
no later than 11:59 p.m. Eastern Time on the due date. Upon receipt of
a transmission, the E-Filing system time-stamps the document and sends
the submitter an email notice confirming receipt of the document. The
E-Filing system also distributes an email notice that provides access
to the document to the NRC's Office of the General Counsel and any
others who have advised the Office of the Secretary that they wish to
participate in the proceeding, so that the filer need not serve the
document on those participants separately. Therefore, applicants and
other participants (or their counsel or representative) must apply for
and receive a digital ID certificate before adjudicatory documents are
filed so that they can obtain access to the documents via the E-Filing
system.
A person filing electronically using the NRC's adjudicatory E-
Filing system may seek assistance by contacting the NRC's Electronic
Filing Help Desk through the ``Contact Us'' link located on the NRC's
public Web site at https://www.nrc.gov/site-help/e-submittals.html, by
email to MSHD.Resource@nrc.gov, or by a toll-free call at 1-866-672-
7640. The NRC Electronic Filing Help Desk is available between 9 a.m.
and 6 p.m., Eastern Time, Monday through Friday, excluding government
holidays.
Participants who believe that they have a good cause for not
submitting documents electronically must file an exemption request, in
accordance with 10 CFR 2.302(g), with their initial paper filing
stating why there is good cause for not filing electronically and
requesting authorization to continue to submit documents in paper
format. Such filings must be submitted by: (1) First class mail
addressed to the Office of the Secretary of the Commission, U.S.
Nuclear Regulatory Commission, Washington, DC 20555-0001, Attention:
Rulemaking and Adjudications Staff; or (2) courier, express mail, or
expedited delivery service to the Office of the Secretary, 11555
Rockville Pike, Rockville, Maryland 20852, Attention: Rulemaking and
Adjudications Staff. Participants filing adjudicatory documents in this
manner are responsible for serving the document on all other
participants. Filing is considered complete by first-class mail as of
the time of deposit in the mail, or by courier, express mail, or
expedited delivery service upon depositing the document with the
provider of the service. A presiding officer, having granted an
exemption request from using E-Filing, may require a participant or
party to use E-Filing if the presiding officer subsequently determines
that the reason for granting the exemption from use of E-Filing no
longer exists.
Documents submitted in adjudicatory proceedings will appear in the
NRC's electronic hearing docket which is available to the public at
https://adams.nrc.gov/ehd, unless excluded pursuant to an order of the
Commission or the presiding officer. If you do not have an NRC-issued
digital ID certificate as described above, click cancel when the link
requests certificates and you will be automatically directed to the
NRC's electronic hearing dockets where you will be able to access any
publicly available documents in a particular hearing docket.
Participants are requested not to include personal privacy information,
such as social security numbers, home addresses, or personal phone
numbers in their filings, unless an NRC regulation or other law
requires submission of such information. For example, in some
instances, individuals provide home addresses in order to demonstrate
proximity to a facility or site. With respect to copyrighted works,
except for limited excerpts that serve the purpose of the adjudicatory
filings and would constitute a Fair Use application, participants are
requested not to include copyrighted materials in their submission.
For further details with respect to these license amendment
applications, see the application for amendment which is available for
public inspection in ADAMS and at the NRC's PDR. For additional
direction on accessing information related to this document, see the
``Obtaining Information and Submitting Comments'' section of this
document.
Entergy Nuclear Operations, Inc., Docket No. 50-255, Palisades Nuclear
Plant (PNP), Van Buren County, Michigan
Date of amendment request: August 31, 2017. A publicly-available
version is in ADAMS under Accession No. ML17248A389.
Description of amendment request: The proposed amendment would
revise the PNP Site Emergency Plan (SEP) for the permanently shut down
and defueled condition. The proposed PNP SEP changes would revise the
shift staffing and Emergency Response Organization (ERO) staffing.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes to the PNP SEP do not impact the function
of plant structures, systems, or components (SSCs). The proposed
changes do not affect accident initiators or precursors, nor does it
alter design assumptions. The proposed changes do not prevent the
ability of the on-shift staff and augmented ERO to perform their
intended functions to mitigate the consequences of any accident or
event that will be credible in the permanently shut down and
defueled condition. The proposed changes only remove positions that
will no longer be credited in the PNP SEP.
Therefore, the proposed amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
[[Page 55404]]
Response: No.
The proposed changes reduce the number of on-shift and augmented
ERO positions commensurate with the hazards associated with a
permanently shut down and defueled facility. The proposed changes do
not involve installation of new equipment or modification of
existing equipment, so that no new equipment failure modes are
introduced. Also, the proposed changes do not result in a change to
the way that the equipment or facility is operated so that no new
accident initiators are created.
Therefore, the proposed amendment does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
Margin of safety is associated with confidence in the ability of
the fission product barriers (i.e., fuel cladding, reactor coolant
system pressure boundary, and containment structure) to limit the
level of radiation dose to the public. The proposed changes are
associated with the PNP SEP and do not impact operation of the plant
or its response to transients or accidents. The change does not
affect the Technical Specifications. The proposed changes do not
involve a change in the method of plant operation, and no accident
analyses will be affected by the proposed changes. Safety analysis
acceptance criteria are not affected by the proposed changes. The
revised PNP SEP will continue to provide the necessary response
staff with the proposed changes.
Therefore, the proposed amendment does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: William Dennis, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 440 Hamilton Ave., White Plains, NY
10601.
NRC Branch Chief: Douglas A. Broaddus.
Exelon Generation Company (EGC), LLC, Docket Nos. STN 50-456 and STN
50-457, Braidwood Station, Units 1 and 2, Will County, Illinois and
Docket Nos. STN 50-454 and STN 50-455, Byron Station, Unit Nos. 1 and
2, Ogle County, Illinois
Date of amendment request: September 1, 2017. A publicly-available
version is in ADAMS under Accession No. ML17244A093.
Description of amendment request: The amendments would modify the
licensing basis by the addition of a license condition to allow for the
implementation of the provisions of 10 CFR, Section 50.69, ``Risk-
informed categorization and treatment of structures, systems and
components for nuclear power reactors.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change will permit the use of a risk-informed
categorization process to modify the scope of SSCs [structures,
systems, and components] subject to NRC [Nuclear Regulatory
Commission] special treatment requirements and to implement
alternative treatments per the regulations. The process used to
evaluate SSCs for changes to NRC special treatment requirements and
the use of alternative requirements ensures the ability of the SSCs
to perform their design function. The potential change to special
treatment requirements does not change the design and operation of
the SSCs. As a result, the proposed change does not significantly
affect any initiators to accidents previously evaluated or the
ability to mitigate any accidents previously evaluated. The
consequences of the accidents previously evaluated are not affected
because the mitigation functions performed by the SSCs assumed in
the safety analysis are not being modified. The SSCs required to
safely shut down the reactor and maintain it in a safe shutdown
condition following an accident will continue to perform their
design functions.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any previously evaluated?
Response: No.
The proposed change will permit the use of a risk-informed
categorization process to modify the scope of SSCs subject to NRC
special treatment requirements and to implement alternative
treatments per the regulations. The proposed change does not change
the functional requirements, configuration, or method of operation
of any SSC. Under the proposed change, no additional plant equipment
will be installed.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed change will permit the use of a risk-informed
categorization process to modify the scope of SSCs subject to NRC
special treatment requirements and to implement alternative
treatments per the regulations. The proposed change does not affect
any Safety Limits or operating parameters used to establish the
safety margin. The safety margins included in analyses of accidents
are not affected by the proposed change.
The regulation requires that there be no significant effect on
plant risk due to any change to the special treatment requirements
for SSCs and that the SSCs continue to be capable of performing
their design basis functions, as well as to perform any beyond
design basis functions consistent with the categorization process
and results.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Tamra Domeyer, Associate General Counsel,
Exelon Nuclear, 4300 Winfield Road, Warrenville, IL 60555.
NRC Branch Chief: David J. Wrona.
Exelon Generation Company, LLC and PSEG Nuclear LLC, Docket Nos. 50-277
and 50-278, Peach Bottom Atomic Power Station, Units 2 and 3, York and
Lancaster Counties, Pennsylvania
Date of amendment request: August 30, 2017, as supplemented by
letter dated October 24, 2017. Publicly-available versions are in ADAMS
under Accession Nos. ML17243A014 and ML17297B521, respectively.
Description of amendment request: The amendments would modify the
licensing basis by the addition of a license condition to allow for the
implementation of the provisions of 10 CFR 50.69, ``Risk-informed
categorization and treatment of structures, systems and components for
nuclear power reactors.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below, with NRC staff edits shown in
square brackets:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change will permit the use of a risk-informed
categorization process to modify the scope of [structures, systems,
and components] SSCs subject to NRC special treatment requirements
and to implement alternative treatments per the regulations. The
process used to evaluate SSCs for changes to NRC special treatment
[[Page 55405]]
requirements and the use of alternative requirements ensures the
ability of the SSCs to perform their design function. The potential
change to special treatment requirements does not change the design
and operation of the SSCs. As a result, the proposed change does not
significantly affect any initiators to accidents previously
evaluated or the ability to mitigate any accidents previously
evaluated. The consequences of the accidents previously evaluated
are not affected because the mitigation functions performed by the
SSCs assumed in the safety analysis are not being modified. The SSCs
required to safely shut down the reactor and maintain it in a safe
shutdown condition following an accident will continue to perform
their design functions.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change will permit the use of a risk-informed
categorization process to modify the scope of SSCs subject to NRC
special treatment requirements and to implement alternative
treatments per the regulations. The proposed change does not change
the functional requirements, configuration, or method of operation
of any SSC. Under the proposed change, no additional plant equipment
will be installed.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change will permit the use of a risk-informed
categorization process to modify the scope of SSCs subject to NRC
special treatment requirements and to implement alternative
treatments per the regulations. The proposed change does not affect
any Safety Limits or operating parameters used to establish the
safety margin. The safety margins included in analyses of accidents
are not affected by the proposed change. The regulation requires
that there be no significant effect on plant risk due to any change
to the special treatment requirements for SSCs and that the SSCs
continue to be capable of performing their design basis functions,
as well as to perform any beyond design basis functions consistent
with the categorization process and results.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Tamra Domeyer, Associate General Counsel,
Exelon Generation Company, LLC, 4300 Winfield Rd., Warrenville, IL
60555.
NRC Branch Chief: James G. Danna.
Exelon Generation Company, LLC and PSEG Nuclear LLC, Docket Nos. 50-277
and 50-278, Peach Bottom Atomic Power Station, Units 2 and 3, York and
Lancaster Counties, Pennsylvania
Date of amendment request: September 29, 2017. A publicly-available
version is in ADAMS under Accession No. ML17275A069.
Description of amendment request: The amendments would revise
Technical Specification (TS) requirements related to the direct current
(DC) electrical power system. The proposed changes are based on
Technical Specifications Task Force (TSTF) Traveler TSTF-500, Revision
2, ``DC Electrical Rewrite--Update to TSTF-360.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change restructures the TS for the direct current
(DC) electrical power system. The proposed changes add actions to
specifically address battery charger inoperability. The DC
electrical power system, including associated battery chargers, is
not an initiator of any accident sequence analyzed in the Updated
Final Safety Analysis Report (UFSAR). Operation in accordance with
the proposed TS ensures that the DC electrical power system is
capable of performing its function as described in the UFSAR.
Therefore, the mitigative functions supported by the DC electrical
power system will continue to provide the protection assumed by the
analysis, and the probability of previously analyzed accidents will
not increase by implementing these changes.
The relocation of preventive maintenance surveillances, and
certain operating limits and actions, to a newly created licensee-
controlled Battery Monitoring and Maintenance Program will not
challenge the ability of the DC electrical power system to perform
its design function. Appropriate monitoring and maintenance,
consistent with industry standards, will continue to be performed.
In addition, the DC electrical power system is within the scope of
10 CFR 50.65, ``Requirements for monitoring the effectiveness of
maintenance at nuclear power plants,'' which will ensure the control
of maintenance activities associated with the DC electrical power
system.
The integrity of fission product barriers, plant configuration,
and operating procedures as described in the UFSAR will not be
affected by the proposed changes. Therefore, the consequences of
previously analyzed accidents will not increase by implementing
these changes.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change involves restructuring the TS for the DC
electrical power system. The DC electrical power system, including
associated battery chargers, is not an initiator to any accident
sequence analyzed in the UFSAR. Rather, the DC electrical power
system is used to supply equipment used to mitigate an accident.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The margin of safety is established through equipment design,
operating parameters, and the setpoints at which automatic actions
are initiated. The proposed changes will not adversely affect
operation of plant equipment. These changes will not result in a
change to the setpoints at which protective actions are initiated.
Sufficient DC capacity to support operation of mitigation equipment
is ensured. The changes associated with the new battery maintenance
and monitoring program will ensure that the station batteries are
maintained in a highly reliable manner. The equipment fed by the DC
electrical sources will continue to provide adequate power to safety
related loads in accordance with analysis assumptions.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Tamra Domeyer, Associate General Counsel,
Exelon Generation Company, LLC, 4300 Winfield Rd., Warrenville, IL
60555.
NRC Branch Chief: James G. Danna.
Exelon Generation Company, LLC, Docket No. 50-333, James A. FitzPatrick
Nuclear Power Plant, Oswego County, New York
Date of amendment request: October 2, 2017. A publicly-available
version is in ADAMS under Accession No. ML17275A520.
[[Page 55406]]
Description of amendment request: The amendment would revise the
James A. FitzPatrick Nuclear Power Plant Technical Specifications (TSs)
to adopt Technical Specifications Task Force (TSTF) Traveler TSTF-542,
Revision 2, ``Reactor Pressure Vessel Water Inventory Control'' (ADAMS
Accession No. ML16074A448). Specifically, the licensee proposed changes
to replace TS requirements related to operations with a potential for
draining the reactor vessel (OPDRVs) with new requirements on reactor
pressure vessel (RPV) water inventory control (WIC) to protect Safety
Limit 2.1.1.3.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes replace existing TS requirements related to
OPDRVs with new requirements on RPV WIC that will protect Safety
Limit 2.1.1.3. Draining of RPV water inventory in Mode 4 (i.e., cold
shutdown) and Mode 5 (i.e., refueling) is not an accident previously
evaluated, and therefore replacing the existing TS controls to
prevent or mitigate such an event with a new set of controls has no
effect on any accident previously evaluated. RPV water inventory
control in Mode 4 or Mode 5 is not an initiator of any accident
previously evaluated. The existing OPDRV controls or the proposed
RPV WIC controls are not mitigating actions assumed in any accident
previously evaluated.
The proposed changes reduce the probability of an unexpected
draining event (which is not a previously evaluated accident) by
imposing new requirements on the limiting time in which an
unexpected draining event could result in the reactor vessel water
level dropping to the top of the active fuel (TAF). These controls
require cognizance of the plant configuration and control of
configurations with unacceptably short drain times. These
requirements reduce the probability of an unexpected draining event.
The current TS requirements are only mitigating actions and impose
no requirements that reduce the probability of an unexpected
draining event.
The proposed changes reduce the consequences of an unexpected
draining event (which is not a previously evaluated accident) by
requiring an Emergency Core Cooling System (ECCS) subsystem to be
operable at all times in Modes 4 and 5. The current TS requirements
do not require any water injection systems, ECCS or otherwise, to be
Operable in certain conditions in Mode 5. The change in requirement
from two ECCS subsystems to one ECCS subsystem in Modes 4 and 5 does
not significantly affect the consequences of an unexpected draining
event because the proposed Actions ensure equipment is available
within the limiting drain time that is as capable of mitigating the
event as the current requirements. The proposed controls provide
escalating compensatory measures to be established as calculated
drain times decrease, such as verification of a second method of
water injection and additional confirmations that containment and/or
filtration would be available if needed.
The proposed changes reduce or eliminate some requirements that
were determined to be unnecessary to manage the consequences of an
unexpected draining event, such as automatic initiation of an ECCS
subsystem and control room ventilation. These changes do not affect
the consequences of any accident previously evaluated since a
draining event in Modes 4 and 5 is not a previously evaluated
accident and the requirements are not needed to adequately respond
to a draining event.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes replace existing TS requirements related to
OPDRVs with new requirements on RPV WIC that will protect Safety
Limit 2.1.1.3. The proposed changes will not alter the design
function of the equipment involved. Under the proposed changes, some
systems that are currently required to be operable during OPDRVs
would be required to be available within the limiting drain time or
to be in service depending on the limiting drain time. Should those
systems be unable to be placed into service, the consequences are no
different than if those systems were unable to perform their
function under the current TS requirements.
The event of concern under the current requirements and the
proposed changes are an unexpected draining event. The proposed
changes do not create new failure mechanisms, malfunctions, or
accident initiators that would cause a draining event or a new or
different kind of accident not previously evaluated or included in
the design and licensing bases.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed changes replace existing TS requirements related to
OPDRVs with new requirements on RPV WIC. The current requirements do
not have a stated safety basis and no margin of safety is
established in the licensing basis. The safety basis for the new
requirements is to protect Safety Limit 2.1.1.3. New requirements
are added to determine the limiting time in which the RPV water
inventory could drain to the top of the fuel in the reactor vessel
should an unexpected draining event occur. Plant configurations that
could result in lowering the RPV water level to the TAF within one
hour are now prohibited. New escalating compensatory measures based
on the limiting drain time replace the current controls. The
proposed TS establish a safety margin by providing defense-in-depth
to ensure that the Safety Limit is protected and to protect the
public health and safety. While some less restrictive requirements
are proposed for plant configurations with long calculated drain
times, the overall effect of the change is to improve plant safety
and to add safety margin.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Donald P. Ferraro, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Suite 305,
Kennett Square, PA 19348.
NRC Branch Chief: James G. Danna.
Florida Power & Light Company, Docket Nos. 50-250 and 50-251, Turkey
Point Nuclear Generating Unit Nos. 3, and 4, Miami-Dade County, Florida
Date of amendment request: August 23, 2017, as supplemented by
letter dated October 19, 2017. Publicly-available versions are in ADAMS
under Accession Nos. ML17235B008 and ML17292A789, respectively.
Description of amendment request: The amendments would modify the
Technical Specifications (TSs) to relocate the Explosive Gas Monitoring
Instrumentation, Explosive Gas Mixture, and Gas Decay Tanks System
requirements to licensee-controlled documents and establish a Gas Decay
Tank Explosive Gas and Radioactivity Monitoring Program. The proposed
amendments also relocate the Standby Feedwater System requirements to
licensee-controlled documents and modify related Auxiliary Feedwater
(AFW) System requirements.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
[[Page 55407]]
The proposed license amendments modify the Turkey Point TS by
relocating the Explosive Gas Monitoring Instrumentation, Explosive
Gas Mixture, Gas Decay Tanks and Standby Feedwater System
requirements to licensee controlled documents, by relatedly
modifying the AFW System requirements and by establishing a Gas
Decay Tank Explosive Gas and Radioactivity Monitoring Program. The
proposed changes are administrative in nature and do not alter any
plant equipment or the manner in which plant equipment is operated
and maintained. All equipment limitations, applicable methodologies
and surveillances are maintained by the proposed changes. In
addition, the proposed changes to the AFW System requirements
enhance plant safety. As such, the proposed changes cannot affect
the initiators, the likelihood or the expected outcomes of any
analyzed accidents.
Therefore, facility operation in accordance with the proposed
changes would not involve a significant increase in the probability
or consequences of an accident previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed license amendments modify the Turkey Point TS by
relocating the Explosive Gas Monitoring Instrumentation, Explosive
Gas Mixture, Gas Decay Tanks and Standby Feedwater System
requirements to licensee controlled documents, by relatedly
modifying the AFW System requirements and by establishing a Gas
Decay Tank Explosive Gas and Radioactivity Monitoring Program. The
proposed changes neither install or remove plant equipment nor alter
any plant equipment design, configuration, or method of operation.
Hence, no new failure mechanisms are introduced as a result of the
proposed changes.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed license amendments modify the Turkey Point TS by
relocating the Explosive Gas Monitoring Instrumentation, Explosive
Gas Mixture, Gas Decay Tanks and Standby Feedwater System
requirements to licensee controlled documents, by relatedly
modifying the AFW System requirements and by establishing a Gas
Decay Tank Explosive Gas and Radioactivity Monitoring Program. The
proposed changes neither involve changes to safety analyses
assumptions, safety limits, or limiting safety system settings nor
adversely impact plant operating margins or the reliability of
equipment credited in safety analyses.
Therefore, operation of the facility in accordance with the
proposed changes will not involve a significant reduction in the
margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: William S. Blair, Managing Attorney--
Nuclear, Florida Power & Light Company, 700 Universe Blvd., MS LAW/JB,
Juno Beach, FL 33408-0420.
NRC Branch Chief: Undine Shoop.
NextEra Energy Duane Arnold, LLC, Docket No. 50-331, Duane Arnold
Energy Center (DAEC), Linn County, Iowa
Date of amendment request: September 5, 2017. A publicly-available
version is in ADAMS under Accession No. ML17248A284.
Description of amendment request: The proposed amendment would
revise DAEC Technical Specifications 3.5.1, ``ECCS [emergency core
cooling system]-Operating.'' The proposed change would decrease the
nitrogen supply requirement for the Automatic Depressurization System
(ADS) in Surveillance Requirement (SR) 3.5.1.3 from 100 days to 30
days.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change modifies a SR for verification of the
nitrogen supply for the ADS accumulators. Accidents are initiated by
the malfunction of plant equipment, or the catastrophic failure of
plant structures, systems or components. The performance of this
surveillance is not a precursor to any accident previously evaluated
and does not change the manner in which the ADS operates. Technical
evaluation of the change concluded that a 30-day nitrogen supply is
more than adequate to ensure that the reactor is depressurized, so
the consequences of an accident remain unchanged.
Therefore, the proposed change does not involve a significant
increase in the probability or consequence of a previously evaluated
accident.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change does not involve physical alterations to the
plant. No new or different type of equipment will be installed, and
there are no physical modifications required to existing installed
equipment associated with the proposed change. The proposed change
does not create any failure mechanism, malfunction or accident
initiator not already considered in the design and licensing basis.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
Although the proposed change will decrease the required supply
of nitrogen for the ADS accumulators from 100 days to 30 days, the
assessment above has shown that the reactor would be depressurized
within 3 days following any postulated accident or event that would
create a hostile environment in the drywell. Once initial
depressurization is completed, long term core cooling can be assured
without ADS.
Therefore, the proposed change will not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: William Blair, P.O. Box 14000, Juno Beach,
FL 33408-0420.
NRC Branch Chief: David J. Wrona.
NextEra Energy Duane Arnold, LLC, Docket No. 50-331, Duane Arnold
Energy Center, Linn County, Iowa
Date of amendment request: August 31, 2017. A publicly-available
version is in ADAMS under Accession No. ML17243A469.
Description of amendment request: The proposed amendment would
modify the licensing basis by the addition of a license condition to
allow for the implementation of the provisions of 10 CFR, part 50.69,
``Risk-Informed Categorization and Treatment of Structures, Systems,
and Components (SSCs) for Nuclear Power Reactors.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change will permit the use of a risk-informed
categorization process to modify the scope of SSCs subject to NRC
special treatment requirements and to implement alternative
treatments per the regulations. The process used to evaluate SSCs
for changes to NRC special treatment
[[Page 55408]]
requirements and the use of alternative requirements ensures the
ability of the SSCs to perform their design function. The potential
change to special treatment requirements does not change the design
and operation of the SSCs. As a result, the proposed change does not
significantly affect any initiators to accidents previously
evaluated or the ability to mitigate any accidents previously
evaluated. The consequences of the accidents previously evaluated
are not affected because the mitigation functions performed by the
SSCs assumed in the safety analysis are not being modified. The SSCs
required to safely shut down the reactor and maintain it in a safe
shutdown condition following an accident will continue to perform
their design functions.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change will permit the use of a risk-informed
categorization process to modify the scope of SSCs subject to NRC
special treatment requirements and to implement alternative
treatments per the regulations. The proposed change does not change
the functional requirements, configuration, or method of operation
of any SSC. Under the proposed change, no additional plant equipment
will be installed.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change will permit the use of a risk-informed
categorization process to modify the scope of SSCs subject to NRC
special treatment requirements and to implement alternative
treatments per the regulations. The proposed change does not affect
any Safety Limits or operating parameters used to establish the
safety margin. The safety margins included in analyses of accidents
are not affected by the proposed change. The regulation requires
that there be no significant effect on plant risk due to any change
to the special treatment requirements for SSCs and that the SSCs
continue to be capable of performing their design basis functions,
as well as to perform any beyond design basis functions consistent
with the categorization process and results.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: William Blair, P.O. Box 14000, Juno Beach,
FL 33408-0420.
NRC Branch Chief: David J. Wrona.
NextEra Energy, Point Beach Nuclear Plant (PBNP), LLC, Docket Nos. 50-
266 and 50-301, Point Beach Nuclear Plant, Units 1 and 2, Town of Two
Creeks, Manitowoc County, Wisconsin
Date of amendment request: June 23, 2017, as supplemented by letter
dated August 21, 2017. Publicly-available versions are in ADAMS under
Accession Nos. ML17174A458, and ML17233A283, respectively.
Description of amendment request: The amendments would revise the
Emergency Plan for PBNP to adopt the Nuclear Energy lnstitute's (NEl's)
revised Emergency Action Level (EAL) scheme described in NEI 99-01,
Revision 6, ``Development of Emergency Action Levels for Non-Passive
Reactors,'' which has been endorsed by the NRC.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change does not impact the physical configuration
or function of plant structures, systems, or components (SSCs) or
the manner in which SSCs are operated, maintained, modified, tested,
or inspected. No actual facility equipment or accident analyses are
affected by the proposed changes.
The change revises the NextEra Emergency Action Levels to be
consistent with the NRC endorsed EAL scheme contained in NEI 99-01,
Revision 6, ``Methodology for Development of Emergency Action
Levels,'' but does not alter any of the requirements of the
Operating License or the Technical Specifications.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed change does not involve a physical alteration of
the plant (no new or different type of equipment will be installed).
The proposed change does not create any new failure modes for
existing equipment or any new limiting single failures.
Additionally, the proposed change does not involve a change in the
methods governing normal plant operation, and all safety functions
will continue to perform as previously assumed in the accident
analyses. Thus, the proposed change does not adversely affect the
design function or operation of any structures, systems, and
components important to safety. No new accident scenarios, failure
mechanisms, or limiting single failures are introduced as a result
of the proposed change. The proposed change does not challenge the
performance or integrity of any safety-related system.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The margin of safety associated with the acceptance criteria of
any accident is unchanged. The proposed change will have no affect
on the availability, operability, or performance of safety-related
systems and components. The proposed change will not adversely
affect the operation of plant equipment or the function of equipment
assumed in the accident analysis. The proposed amendment does not
involve changes to any safety analyses assumptions, safety limits,
or limiting safety system settings. The changes do not adversely
impact plant operating margins or the reliability of equipment
credited in the safety analyses.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: William Blair, Managing Attorney--Nuclear,
Florida Power & Light Company, P.O. Box 14000, 700 Universe Boulevard,
Juno Beach, FL 33408-0420.
NRC Branch Chief: David J. Wrona.
PSEG Nuclear LLC and Exelon Generation Company, LLC, Docket Nos. 50-272
and 50-311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of amendment request: September 27, 2017. A publicly-available
version is in ADAMS under Accession No. ML17270A076.
Description of amendment request: The amendments would relocate the
reactor coolant system pressure isolation valve (RCS PIV) table from
the technical specifications (TSs) to the technical requirements manual
(TRM). The request would also remove references to the table and move
all notes and leakage acceptance criteria from the table to the TS
surveillance requirements.
[[Page 55409]]
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes to the TS will not alter the way any
structure, system, or component (SSC) functions, and will not alter
the manner in which the plant is operated. The proposed changes do
not alter the design of any SSC. The relocation of the RCS PIV valve
lists from the TS to the TRM is an administrative change. Future
revisions to the TRM are subject to 10 CFR 50.59. Therefore the
probability of an accident previously evaluated is not significantly
increased.
The proposed changes do not alter the RCS PIV leakage limits
contained in the TS nor do they alter the frequency for testing of
the RCS PIV. Therefore, the consequences of an accident previously
evaluated are not increased.
Therefore, these proposed changes do not represent a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes do not involve a modification to the
physical configuration of the plant or changes in the methods
governing normal plant operation. The proposed changes will not
impose any new or different requirement or introduce a new accident
initiator, accident precursor, or malfunction mechanism. The
proposed changes are administrative in nature.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any accident previously
evaluated.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
Response: No.
The proposed changes to the RCS PIV TS are administrative in
nature. The proposed changes do not alter the RCS PIV leakage limits
contained in the TS nor do they alter the frequency for testing of
the RCS PIV. The proposed changes will not result in changes to
system design or setpoints that are intended to ensure timely
identification of plant conditions that could be precursors to
accidents or potential degradation of accident mitigation systems.
The proposed amendment will not result in a design basis or
safety limit being exceeded or altered. Therefore, since the
proposed changes do not impact the response of the plant to a design
basis accident, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Jeffrie J. Keenan, PSEG Nuclear LLC--N21,
P.O. Box 236, Hancocks Bridge, NJ 08038.
NRC Branch Chief: James G. Danna.
South Carolina Electric & Gas Company, South Carolina Public Service
Authority, Docket No. 50-395, Virgil C. Summer Nuclear Station, Unit
No. 1, Fairfield County, South Carolina
Date of amendment request: October 6, 2017. A publicly-available
version is in ADAMS under Accession No. ML17279A715.
Description of amendment request: The proposed amendment would
increase the Integrated Leak Rate Test (ILRT) Peak Calculated
Containment Internal Pressure, Pa, listed in Technical
Specification (TS) 6.8.4.g, ``Containment Leakage Rate Testing
Program,'' to remove the reference to Regulatory Guide (RG) 1.163,
``Performance-Based Containment Leak Test Program,'' dated September
1995 and ANSI/ANS (American National Standards Institute/American
Nuclear Society)--56.8-2002, ``Containment System Leakage Testing
Requirements,'' and to replace the reference of Nuclear Energy
Institute (NEI) 94-01, Revision 3-A, ``Industry Guideline for
Implementing Performance-Based option of 10 CFR part 50, Appendix J,''
with NEI 94-01, Revision 2-A.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below, with NRC staff edits in square
brackets:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes involve removal of RG 1.163 and ANSl/ANS-
56.8-2002 references, replacement of NEI 94-01, Revision 3-A with
NEI 94-01, Revision 2-A, and an increase in the Pa [Peak
Calculated Containment Internal Pressure] value for containment
leakage testing. The activity does not involve a physical change to
the plant or a change in the manner in which the plant is operated
or controlled. The containment is designed to provide an essentially
leak tight barrier against the uncontrolled release of radioactivity
to the environment for postulated accidents. As such, the reactor
containment itself and the testing requirements invoked to
periodically demonstrate the integrity of the reactor containment
exist to ensure the plant's ability to mitigate the consequences of
an accident, and do not involve the prevention or identification of
any precursors of an accident.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
The integrity of the reactor containment is subject to two types
of failure mechanisms which can be categorized as (1) activity based
and (2) time based. Activity based failure mechanisms are defined as
degradation due to system and/or component modifications or
maintenance. Local leak rate test requirements and administrative
controls such as configuration management and procedural
requirements for system restoration ensure that containment
integrity is not degraded by plant modifications or maintenance
activities. The updated Pa value reflects the updated
mass and energy release and containment response calculations,
ensuring a sound technical basis for the local and integrated
leakage tests.
To mitigate time-based mechanisms, the design and construction
requirements of the containment itself combined with the containment
inspections performed in accordance with ASME [American Society of
Mechanical Engineers], Section XI and the Maintenance Rule serve to
provide a high degree of assurance that the containment will not
degrade in a manner that is detectable only by a Type A test. The
change to the Pa value is less than 1 psid [per square
inch differential]. Radiological consequences will continue to be
evaluated at the Technical Specification allowed leakage,
La [allowed leakage] of 0.20 percent by weight of air,
which will not be increased despite the increase in Pa.
As described in Section 3.5, past leakage testing yielded values
well under La. Based on the above, neither the reference
changes nor the Pa change involves a significant increase
in the consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes involve removal of RG 1.163 and ANSl/ANS-
56.8-2002 references, replacement of NEI 94-01, Revision 3-A with
NEI 94-01, Revision 2-A, and an increase in the Pa value
for containment leakage testing. The reactor containment and the
testing requirements invoked to periodically demonstrate the
integrity of the reactor containment exist to ensure the plant's
ability to mitigate the consequences of an accident. There are not
any accident initiators or precursors affected by the revision. The
proposed TS change does not involve a physical change to the plant
or the manner in which the plant is operated or controlled.
Therefore, the proposed TS change does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
[[Page 55410]]
Response: No.
The proposed changes involve removal of RG 1.163 and ANSl/ANS-
56.8-2002 references, replacement of NEI 94-01, Revision 3-A with
NEI 94-01, Revision 2-A, and an increase in the Pa value
for containment leakage testing. The proposed TS change does not
involve a physical change to the plant or a change in the manner in
which the plant is operated or controlled. Using the same analysis
methodology as described in WCAP-10325-P-A [Westinghouse LOCA [loss-
of-accident coolant] Mass and Energy Release Model for Containment
Design], the updated mass and energy release and containment
response analyses corrected input errors identified in the NSALs
[Westinghouse Nuclear Safety Advisory Letters] described previously.
As shown in Figure 1 [October 6, 2017, submittal], the correction of
these errors resulted in a slightly higher predicted peak pressure
than that of the current licensing basis but does not pose a
significant challenge to the design limit.
The specific requirements and conditions of the Primary
Containment Leak Rate Testing Program, as defined in the Technical
Specifications, exist to ensure that the degree of reactor
containment structural integrity and leak-tightness that is
considered in the plant safety analysis is maintained. The overall
containment leak rate limit specified by the Technical Specification
is maintained. The containment inspections performed in accordance
with ASME, Section XI and the Maintenance Rule serve to provide a
high degree of assurance that the containment will not degrade in a
manner that is detectable only by Type A testing. The combination of
these factors ensures that the margin of safety that is in plant
safety analysis is maintained. The design, operation, testing
methods and acceptance criteria for Type A, B, and C containment
leakage tests specified in applicable codes and standards will
continue to be met.
Therefore, the proposed TS change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Kathryn M. Sutton, Morgan, Lewis & Bockius
LLP, 1111 Pennsylvania Avenue NW., Washington, DC 20004.
NRC Branch Chief: Michael T. Markley.
Southern Nuclear Operating Company, Docket Nos. 52-025 and 52-026,
Vogtle Electric Generating Plant, Units 3 and 4, Burke County, Georgia
Date of amendment request: July 28, 2017. A publicly-available
version is in ADAMS under Accession No. ML17209A759.
Description of amendment request: The amendment request proposes to
revise Technical Specification Section 1.1 (TS), Definition of
Actuation Logic Test, by adding a new TS Section 1.1 Definition of
Actuation Logic Output Test (ALOT), revising existing Surveillance
Requirements 3.3.15.1 and 3.3.16.1 and adding new Surveillance
Requirements 3.3.15.2 and 3.3.16.2 to implement the new ALOT. This
submittal requests approval of the license amendment that is necessary
to implement these changes.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(A), licensee has provided
its analysis of the issue on no significant hazards consideration
determination, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
There are no design changes associated with the proposed
amendment. All design, material, and construction standards that
were applicable prior to this amendment request will continue to be
applicable.
The [Processor Module Self-Diagnostic (PMS)] will continue to
function in a manner consistent with the plant design basis. There
will be no changes to the PMS operating limits. The existing
ACTUATION LOGIC TEST Surveillance Requirements are revised such that
different portions of the PMS logic circuitry are tested on
appropriate surveillance test frequencies.
The proposed change will not adversely affect accident
initiators or precursors or adversely alter the design assumptions,
conditions, and configuration of the facility, or the manner in
which the plant is operated and maintained, with respect to such
initiators or precursors.
The proposed changes will not alter the ability of structures,
systems, and components (SSCs) to perform their specified safety
functions to mitigate the consequences of an initiating event within
the assumed acceptance limits.
Accident analysis acceptance criteria will continue to be met
with the proposed changes. The proposed changes will not affect the
source term, containment isolation, or radiological release
assumptions used in evaluating the radiological consequences of any
accident previously evaluated. The proposed changes will not alter
any assumptions or change any mitigation actions in the radiological
consequence evaluations in the Updated Final Safety Analysis Report
(UFSAR).
The applicable radiological dose acceptance criteria will
continue to be met.
The proposed change revises the frequency of testing certain
portions of the PMS logic circuitry, but does not physically alter
any safety-related systems.
Therefore, the proposed amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a
different kind of accident from any accident previously evaluated?
Response: No.
With respect to any new or different kind of accident, there are
no proposed design changes nor are there any changes in the method
by which any safety-related plant SSC performs its specified safety
function. The proposed change will not affect the normal method of
plant operation or change any operating parameters. No equipment
performance requirements will be affected. The proposed change will
not alter any assumptions made in the safety analyses.
The proposed change revises the frequency of testing certain
portions of the PMS logic circuitry. The proposed change does not
involve a physical modification of the plant.
No new accident scenarios, transient precursors, failure
mechanisms, or limiting single failures will be introduced as a
result of this amendment. There will be no adverse effect or
challenges imposed on any safety-related system as a result of this
amendment.
Therefore, the proposed amendment does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The existing ACTUATION LOGIC TEST Surveillance Requirements are
revised such that different portions of the PMS logic circuitry are
tested on appropriate surveillance test frequencies. The reliability
of the PMS is such that not testing the Component Interface Module
(CIM) logic and driver output circuits when the reactor is at power
will have a net positive impact on Engineered Safety Feature
Actuation System (ESFAS) availability. There will be a reduction in
the potential for challenges to the safety systems, coupled with
less time that the safety systems are unavailable.
There will be no effect on those plant systems necessary to
effect the accomplishment of protection functions.
No instrument setpoints or system response times are affected.
None of the acceptance criteria for any accident analysis will be
changed.
The proposed change will have no impact on the radiological
consequences of a design basis accident.
Therefore, the proposed amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: M. Stanford Blanton, Balch & Bingham LLP,
1710 Sixth Avenue North, Birmingham, AL 35203-2015.
[[Page 55411]]
NRC Branch Chief: Jennifer Dixon-Herrity.
Southern Nuclear Operating Company, Docket Nos. 52-025 and 52-026,
Vogtle Electric Generating Plant, Units 3 and 4, Burke County, Georgia
Date of amendment request: August 18, 2017. A publicly-available
version is in ADAMS under Accession No. ML17230A365.
Description of amendment request: The requested amendment proposes
to depart from approved AP1000 Design Control Document (DCD) Tier 2
information (text) and involved Tier 2* information (as incorporated
into the Updated Final Safety Analysis Report (UFSAR) as plant-specific
DCD information).
This amendment request proposes increasing the design pressure of
the main steam (MS) isolation valve (MSIV) compartments from 6.0 to 6.5
psi and proposes other changes to the licensing basis regarding
descriptions of the MSIV compartments.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below with Nuclear Regulatory
Commission (NRC) staff's edits in square brackets:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes do not adversely affect the operation of
any structures, systems, and components inside or outside the
auxiliary building that could initiate or mitigate abnormal events,
e.g., accidents, anticipated operational occurrences, earthquakes,
floods, tornado missiles, and turbine missiles, or their safety or
design analyses, evaluated in the UFSAR. The changes do not
adversely affect any design function of the auxiliary building or
the structures, systems, and components contained therein. The
ability of the affected auxiliary building main steam isolation
valve compartments and adjacent rooms, including the main control
room, to withstand the pressurization effects from the postulated
pipe ruptures is not adversely affected by the increase in design
pressure, since the structures, systems, and components therein
remain qualified for this service.
Therefore, the proposed activity does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed changes do not affect the operation of any systems
or equipment that might initiate a new or different kind of
accident, or alter any [structure, system, and component (SSC)] such
that a new accident initiator or initiating sequence of events is
created. The proposed changes do not adversely affect the physical
design and operation of the [in-containment refueling water storage
tank (IRWST)] injection, drain, containment recirculation, and
fourth-stage [automatic depressurization system (ADS)] valves,
including as-installed inspections, and maintenance requirements, as
described in the UFSAR. Therefore, the operation of the IRWST
injection, drain, containment recirculation, and fourth-stage ADS
valves is not adversely affected. These proposed changes do not
adversely affect any other SSC design functions or methods of
operation in a manner that results in a new failure mode,
malfunction, or sequence of events that affect safety-related or
nonsafety-related equipment. Therefore, this activity does not allow
for a new fission product release path, result in a new fission
product barrier failure mode, or create a new sequence of events
that result in significant fuel cladding failures.
Therefore, the proposed amendment does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The margin of safety for the design of the auxiliary building is
maintained through continued use of approved codes and standards as
stated in the UFSAR, and adherence to the assumptions used in the
analyses of this structure and the events associated with this
structure. The auxiliary building continues to be a seismic Category
I building with all current structural safety margins maintained.
The 3-hour fire rating requirements for the impacted auxiliary
building walls are maintained. The equipment housed in the main
steam isolation valve compartments continue to be environmentally
qualified for their intended service in accordance with the approved
codes and standards stated within the UFSAR. Thus, the requested
changes will not adversely affect any safety-related equipment,
design code, function, design analysis, safety analysis input or
result, or design/safety margin. No safety analysis or design basis
acceptance limit/criterion is challenged or exceeded by the
requested change, thus, no margin of safety is reduced. Therefore,
the proposed change does not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: M. Stanford Blanton, Balch & Bingham LLP,
1710 Sixth Avenue North, Birmingham, AL 35203-2015.
NRC Branch Chief: Jennifer Dixon-Herrity.
Southern Nuclear Operating Company, Docket Nos. 52-025 and 52-026,
Vogtle Electric Generating Plant, Units 3 and 4, Burke County, Georgia
Date of amendment request: October 6, 2017. A publicly-available
version is in ADAMS under Accession No. ML17279A084.
Description of amendment request: The amendment request proposes to
depart from Tier 2 information in the Updated Final Safety Analysis
Report (UFSAR) (which includes the plant-specific Design Control
Document (DCD) Tier 2 information) and involves related changes to
plant-specific Tier 1 information, with corresponding changes to the
associated combined license (COL) Appendix C information. Pursuant to
the provisions of 10 CFR 52.63(b)(1), an exemption from elements of the
design as certified in the 10 CFR part 52, Appendix D, design
certification rule is also requested for the plant-specific DCD Tier 1
material departures. Specifically, the requested amendment proposes to
depart from Tier 2 information in UFSAR Subsection 8.3.2.4 describing
raceway and cable routing criteria and hazard protection, and involves
related changes to plant-specific Tier 1 Table 3.3-6, inspections,
tests, analyses, and acceptance criteria information, with
corresponding changes to the associated COL Appendix C information.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below with NRC staff edits in square
brackets:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
Changes 1, 3 and 4 are clarifications only and do not represent
a change to the minimum required separation distance between
raceways. Change 2 reduces the required separation distances between
raceways from those documented in [Institute of Electrical and
Electronics Engineers (IEEE)] 384-1981. These reduced separation
distances are based on specific tests performed on the specified
raceway configurations, and the recommendations from those tests
contained in the associated report. The NRC staff previously
reviewed the descriptions of the ten tests documented in this
report, including the ones applicable to the existing UFSAR
exceptions, and concluded that they were acceptable, as documented
in NUREG-1793, ``Final Safety Evaluation Report Related to
Certification of
[[Page 55412]]
the AP1000 Standard Design,'' (Initial Report) Subsection 8.3.2.2.
The reduced separation does not adversely impact the ability to
safely shutdown the plant, and maintain it shutdown. The referenced
test report has shown a failure of a faulted cable will not
propagate to a nearby target cable in way that adversely impacts its
function.
Therefore, the proposed amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
Changes 1, 3 and 4 are clarifications only and do not represent
a change to the minimum required separation distance between
circuits. Change 2 reduces the required separation distances between
circuits from those documented in IEEE 384-1981. This change does
not result in a new accident initiator or impact a current accident
initiator.
Therefore, the proposed amendment does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
Changes 1, 3 and 4 are clarifications only and do not represent
a change to the minimum required separation distance between
circuits. Change 2 reduces the required separation distances between
circuits from those documented in IEEE 384-1981. These reduced
separation distances are based on specific tests performed on the
specified raceway configurations, and the recommendations from those
tests contained in the associated report. The NRC staff previously
reviewed the descriptions of the ten tests documented in this
report, including the ones applicable to the existing UFSAR
exceptions, and concluded that they were acceptable, as documented
in NUREG-1793, ``Final Safety Evaluation Report Related to
Certification of the AP1000 Standard Design,'' (Initial Report)
Subsection 8.3.2.2.
The reduced separation does not adversely impact the ability to
safely shutdown the plant, and maintain it shutdown. The referenced
test report has shown a failure of a faulted cable will not
propagate to a nearby target cable in a way that adversely impacts
its function.
Therefore, the proposed amendment does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: M. Stanford Blanton, Balch & Bingham LLP,
1710 Sixth Avenue North, Birmingham, AL 35203-2015.
NRC Branch Chief: Jennifer Dixon-Herrity.
Southern Nuclear Operating Company, Inc., Georgia Power Company,
Oglethorpe Power Corporation, Municipal Electric Authority of Georgia,
City of Dalton, Georgia, Docket Nos. 50-321 and 50-366, Edwin I. Hatch
Nuclear Plant, Unit Nos. 1 and 2, Appling County, Georgia
Date of amendment request: July 10, 2017. A publicly-available
version is in ADAMS under Accession No. ML17191B163.
Description of amendment request: The amendments would revise the
technical specifications (TSs) by: (1) Adding a Note to the
surveillance requirements (SRs) of TS 3.7.7, ``Main Turbine Bypass
System,'' to clarify that the SRs are not required to be met when the
limiting condition for operation (LCO) does not require the Main
Turbine Bypass System to be operable, (2) clarifying that LCO 3.2.3,
``LINEAR HEAT GENERATION RATE (LHGR),'' also has limits for an
inoperable Main Turbine Bypass System that are made applicable as
specified in the Core Operating Limits Report, and (3) deleting an
outdated footnote for LCO 3.2.3.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change (1) adds a Note to the Surveillance
Requirements (SRs) of the Hatch Nuclear Plant (HNP) Unit 1 and Unit
2 Technical Specifications (TS) 3.7.7 clarifying that the SRs are
not required to be met when the LCO does not require the Main
Turbine Bypass System to be Operable, (2) clarifies that LCO 3.2.3,
``LINEAR HEAT GENERATION RATE'' also has limits for an inoperable
Main Turbine Bypass System that are made applicable as specified in
the Core Operating Limits Report, and (3) deletes an outdated
footnote for LCO 3.2.3. The proposed change does not affect the
requirement to meet the LCO, nor does it affect the requirements to
perform the SRs when the Main Turbine Bypass System is being used to
meet the LCO. This change simply clarifies the existing allowance to
apply the Main Turbine Bypass System inoperable limits to minimum
critical power ratio (MCPR) and linear heat generation rate (LHGR)
in lieu of the requirement for the Main Turbine Bypass System to be
Operable. The current safety analysis evaluation is unaffected by
this proposed change. The change regarding the outdated footnote has
no effect on the actual TS requirements.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change (1) adds a Note to the Surveillance
Requirements (SRs) of the Hatch Nuclear Plant (HNP) Unit 1 and Unit
2 Technical Specifications (TS) 3.7.7 clarifying that the SRs are
not required to be met when the LCO does not require the Main
Turbine Bypass System to be Operable, (2) clarifies that LCO 3.2.3,
``LINEAR HEAT GENERATION RATE'' also has limits for an inoperable
Main Turbine Bypass System that are made applicable as specified in
the Core Operating Limits Report, and (3) deletes an outdated
footnote for LCO 3.2.3. This change simply clarifies the existing
allowance to apply the Main Turbine Bypass System inoperable limits
to minimum critical power ratio (MCPR) and linear heat generation
rate (LHGR) in lieu of the requirement for the Main Turbine Bypass
System to be Operable. The change regarding the outdated footnote
has no effect on the actual TS requirements. The current safety
analysis evaluation is unaffected by these proposed changes.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change (1) adds a Note to the Surveillance
Requirements (SRs) of the Hatch Nuclear Plant (HNP) Unit 1 and Unit
2 Technical Specifications (TS) 3.7.7 clarifying that the SRs are
not required to be met when the LCO does not require the Main
Turbine Bypass System to be Operable, (2) clarifies that LCO 3.2.3,
``LINEAR HEAT GENERATION RATE'' also has limits for an inoperable
Main Turbine Bypass System that are made applicable as specified in
the Core Operating Limits Report, and (3) deletes an outdated
footnote for LCO 3.2.3. This change simply clarifies the existing
allowance to apply the Main Turbine Bypass System inoperable limits
to minimum critical power ratio (MCPR) and linear heat generation
rate (LHGR) in lieu of the requirement for the Main Turbine Bypass
System to be Operable. The applicable safety analyses for TS 3.7.7
is unaffected by this clarification. The change regarding the
outdated footnote has no effect on the actual TS requirements.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
[[Page 55413]]
amendment request involves no significant hazards consideration.
Attorney for licensee: Jennifer M. Buettner, Associate General
Counsel, Southern Nuclear Operating Company, 40 Inverness Center
Parkway, Birmingham, AL 35242.
NRC Branch Chief: Michael T. Markley.
Southern Nuclear Operating Company, Docket Nos. 52-025 and 52-026,
Vogtle Electric Generating Plant, Units 3 and 4, Burke County, Georgia
Date of amendment request: September 13, 2017. A publicly-available
version is in ADAMS under Accession No. ML17256A626.
Description of amendment request: The requested amendment proposes
to depart from approved AP1000 Design Control Document (DCD) Tier 2
information as incorporated into the Updated Final Safety Analysis
Report (UFSAR) as plant-specific DCD information, and from Technical
Specifications as incorporated in Appendix A of the Combined License
(COL). Specifically, the proposed changes revise COL Appendix A
Technical Specification 3.6.8 to identify the trisodium phosphate (TSP)
mass value required in the pH adjustment baskets. The TSP mass value
adjusts the pH of the containment water to >7.0 following a postulated
accident.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed activity revises the mass of trisodium phosphate
(TSP), which raises the pH of post-accident containment water to 7.0
or greater following a postulated accident. The change to the TSP
mass value does not adversely impact the ability to support
radionuclide retention with high radioactivity in containment and
helps prevent corrosion of containment equipment during long-term
floodup conditions. The proposed changes do not adversely impact
previously evaluated accidents, because pH control capability is
provided to mitigate already postulated accidents. As described in
Updated Final Safety Analysis Report (UFSAR) Subsection
15.6.5.3.1.3, the passive core cooling system (PXS) is assumed to
provide sufficient TSP to the post-loss-of-coolant accident (LOCA)
cooling solution to maintain the pH at greater than or equal to 7.0
following a LOCA. The pH adjustment baskets provide for long-term pH
control. Long-term pH control is not adversely impacted as the pH
adjustment baskets contain the required amount of TSP to support pH
control requirements following a design basis accident (DBA).
No safety-related structure, system, component (SSC) or function
is adversely affected by this change. The change does not involve an
interface with any SSC accident initiator or initiating sequence of
events, and thus, the probabilities of the accidents evaluated in
the UFSAR are not affected. The proposed changes do not involve a
change to the predicted radiological releases due to postulated
accident conditions, thus, the consequences of the accidents
evaluated in the UFSAR are not affected.
Therefore, the proposed amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed activity revises the mass of TSP, which raises the
pH of containment to 7.0 or greater following a postulated accident.
The proposed activity does not create the possibility of a new or
different kind of accident as pH adjustment is used to support
proper containment chemistry requirements following an accident. The
proposed activity does not adversely affect any safety related
equipment, and does not add any new interfaces to safety-related
SSCs that adversely affect safety functions. No system or design
function or equipment qualification is adversely affected by these
changes as the changes do not modify any SSCs that prevent safety
functions from being performed. The capability to maintain a maximum
containment pH below 9.5 is not adversely impacted by these changes.
The changes do not introduce a new failure mode, malfunction or
sequence of events that could adversely affect safety or safety
related equipment.
Therefore, the proposed amendment does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed activity revises the mass of TSP, which raises the
pH of containment to 7.0 or greater following a postulated accident.
The proposed activity does not affect any other safety-related
equipment or fission product barriers. Containment water pH
adjustment is not adversely impacted. The requested changes will not
adversely affect compliance with any design code, function, design
analysis, safety analysis input or result, or design/safety margin.
No safety analysis or design basis acceptance limit/criterion is
challenged or exceeded by the requested changes as previously
evaluated accidents are not impacted.
Therefore, the proposed amendment does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and based on
this review it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazard consideration.
Attorney for licensee: M. Stanford Blanton, Balch & Bingham LLP,
1710 Sixth Avenue North, Birmingham, AL 35203-2015.
NRC Branch Chief: Jennifer Dixon-Herrity.
Southern Nuclear Operating Company, Docket Nos. 52-025 and 52-026,
Vogtle Electric Generating Plant (VEGP), Units 3 and 4, Burke County,
Georgia
Date of amendment request: September 29, 2017. A publicly-available
version is in ADAMS under Accession No. ML17272A957.
Description of amendment request: The requested amendment proposes
to depart from Tier 2* and associated Tier 2 information in the Updated
Final Safety Analysis Report (UFSAR) (which includes the plant-specific
DCD Tier 2 information). The requested amendment proposes to depart
from UFSAR Tier 2* information regarding resolution of human
engineering deficiencies (HEDs) contained in Westinghouse Electric
Company's report APP-OCS-GEH-320, ``AP1000 Human Factors Engineering
Integrated Systems Validation Plan,'' which is incorporated by
reference into the VEGP Units 3 and 4 UFSAR.
The proposed changes would revise the licensing basis of the
combined licenses regarding the process for addressing and re-testing
of HEDs identified during the integrated system validation (ISV) as
described in Tier 2* document, APPOCS-GEH-320 ``AP1000 Human Factors
Engineering Integrated System Validation Plan.'' APPOCS-GEH-320
references APP-OCS-GEH-420, ``Human Factors Engineering Discrepancy
Resolution Process,'' which defines the process for tracking,
resolution, and closure of HEDs. The proposed changes to APP-OCS-GEH-
320 do not impact APP-OCS-GEH-420.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The Integrated System Validation (ISV) provides a comprehensive
human performance-based assessment of the design of the AP1000
Human-System Interface (HSI) resources, based on their realistic
operation
[[Page 55414]]
within a simulator driven Main Control Room (MCR). The ISV is part
of the overall AP1000 Human Factors Engineering (HFE) program. The
changes to APP-OCS-GEH-320, which is incorporated by reference into
the UFSAR, clarify the resources and methodology used during re-
testing performed to verify the effectiveness of Human Engineering
Deficiency (HED) resolution. The ISV Plan does not affect the plant
itself. Changing APP-OCS-GEH-320 and the UFSAR does not affect
prevention and mitigation of abnormal events, e.g., accidents,
anticipated operational occurrences, earthquakes, floods and turbine
missiles, or their safety or design analyses. No safety-related
structure, system, component (SSC) or function is adversely
affected. The changes neither involve nor interface with any SSC
accident initiator or initiating sequence of events, and thus, the
probabilities of the accidents evaluated in the UFSAR are not
affected. Because the changes do not involve any safety-related SSC
or function used to mitigate an accident, the consequences of the
accidents evaluated in the UFSAR are not affected.
Therefore, the proposed amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The changes to APP-OCS-GEH-320 and the VEGP 3 and 4 UFSAR affect
only the testing and validation of the MCR design and HSI using a
plant simulator. Therefore, the changes do not affect the safety-
related equipment itself, nor do they affect equipment which, if it
failed, could initiate an accident or a failure of a fission product
barrier. No analysis is adversely affected. No system or design
function or equipment qualification is adversely affected by the
changes. This activity does not allow for a new fission product
release path, result in a new fission product barrier failure mode,
or create a new sequence of events that would result in significant
fuel cladding failures. In addition, the changes do not result in a
new failure mode, malfunction or sequence of events that could
affect safety or safety related equipment.
Therefore, the proposed amendment does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The changes to APP-OCS-GEH-320 and the UFSAR affect the testing
and validation of the MCR design and HSI using a plant simulator.
Therefore, the changes do not affect the assessments or the plant
itself. These changes do not affect safety-related equipment or
equipment whose failure could initiate an accident, nor does it
adversely interface with safety-related equipment or fission product
barriers. No safety analysis or design basis acceptance limit/
criterion is challenged or exceeded by the requested change.
Therefore, the proposed amendment does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and based on
this review it appears that the three standards of 10 CFR 50.92 (c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazard consideration.
Attorney for licensee: M. Stanford Blanton, Balch & Bingham LLP,
1710 Sixth Avenue North, Birmingham, AL 35203-2015.
NRC Branch Chief: Jennifer Dixon-Herrity.
Susquehanna Nuclear, LLC, Docket Nos. 50-387 and 50-388, Susquehanna
Steam Electric Station, Units 1 and 2, Luzerne County, Pennsylvania
Date of amendment request: September 20, 2017. A publicly-available
version is in ADAMS under Package Accession No. ML17265A434.
Description of amendment request: The amendments would revise
technical specification (TS) requirements related to ``operations with
a potential for draining the reactor vessel'' (OPDRVs) with new
requirements on reactor pressure vessel (RPV) water inventory control
(WIC) to protect Safety Limit 2.1.1.3. Safety Limit 2.1.1.3 requires
RPV water level to be greater than the top of active irradiated fuel.
The proposed changes are based on Technical Specifications Task Force
(TSTF) Traveler TSTF-542, Revision 2, ``Reactor Pressure Vessel Water
Inventory Control,'' dated December 20, 2016.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes replace existing TS requirements related to
OPDRVs with new requirements on RPV WIC that will protect Safety
Limit 2.1.1.3. Draining of RPV water inventory in Mode 4 (i.e., cold
shutdown) and Mode 5 (i.e., refueling) is not an accident previously
evaluated and, therefore, replacing the existing TS controls to
prevent or mitigate such an event with a new set of controls has no
effect on any accident previously evaluated. RPV water inventory
control in Mode 4 or Mode 5 is not an initiator of any accident
previously evaluated. The existing OPDRV controls or the proposed
RPV WIC controls are not mitigating actions assumed in any accident
previously evaluated.
The proposed changes reduce the probability of an unexpected
draining event (which is not a previously evaluated accident) by
imposing new requirements on the limiting time in which an
unexpected draining event could result in the reactor vessel water
level dropping to the top of the active fuel (TAF). These controls
require cognizance of the plant configuration and control of
configurations with unacceptably short drain times. These
requirements reduce the probability of an unexpected draining event.
The current TS requirements are only mitigating actions and impose
no requirements that reduce the probability of an unexpected
draining event.
The proposed changes reduce the consequences of an unexpected
draining event (which is not a previously evaluated accident) by
requiring an Emergency Core Cooling System (ECCS) subsystem to be
operable at all times in Modes 4 and 5. The current TS requirements
do not require any water injection systems, ECCS or otherwise, to be
Operable in certain conditions in Mode 5. The change in requirement
from two ECCS subsystems to one ECCS subsystem in Modes 4 and 5 does
not significantly affect the consequences of an unexpected draining
event because the proposed Actions ensure equipment is available
within the limiting drain time that is as capable of mitigating the
event as the current requirements. The proposed controls provide
escalating compensatory measures to be established as calculated
drain times decrease, such as verification of a second method of
water injection and additional confirmations that containment and/or
filtration would be available if needed.
The proposed changes reduce or eliminate some requirements that
were determined to be unnecessary to manage the consequences of an
unexpected draining event, such as automatic initiation of an ECCS
subsystem and the Control Room Emergency Outside Air Supply (CREOAS)
system. These changes do not affect the consequences of any accident
previously evaluated since a draining event in Modes 4 and 5 is not
a previously evaluated accident and the requirements are not needed
to adequately respond to a draining event.
The administrative update to delete expired completion time
notes is purely administrative in nature.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes replace existing TS requirements related to
OPDRVs with new requirements on RPV WIC that will protect Safety
Limit 2.1.1.3. The proposed changes will not alter the design
function of the equipment involved. Under the proposed changes, some
systems that are currently required to be operable during OPDRVs
would be required to be available within the
[[Page 55415]]
limiting drain time or to be in service depending on the limiting
drain time. Should those systems be unable to be placed into
service, the consequences are no different than if those systems
were unable to perform their function under the current TS
requirements. The event of concern under the current requirements
and the proposed changes are an unexpected draining event. The
proposed changes do not create new failure mechanisms, malfunctions,
or accident initiators that would cause a draining event or a new or
different kind of accident not previously evaluated or included in
the design and licensing bases.
The administrative update to delete expired completion time
notes is purely administrative in nature.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed changes replace existing TS requirements related to
OPDRVs with new requirements on RPV WIC. The current requirements do
not have a stated safety basis and no margin of safety is
established in the licensing basis. The safety basis for the new
requirements is to protect Safety Limit 2.1.1.3. New requirements
are added to determine the limiting time in which the RPV water
inventory could drain to the top of the fuel in the reactor vessel
should an unexpected draining event occur. Plant configurations that
could result in lowering the RPV water level to the TAF within one
hour are now prohibited. New escalating compensatory measures based
on the limiting drain time replace the current controls. The
proposed TS establish a safety margin by providing defense-in-depth
to ensure that the Safety Limit is protected and to protect the
public health and safety. While some less restrictive requirements
are proposed for plant configurations with long calculated drain
times, the overall effect of the change is to improve plant safety
and to add safety margin.
The administrative update to delete expired completion time
notes is purely administrative in nature.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Damon D. Obie, Associate General Counsel,
Talen Energy Supply, LLC, 835 Hamilton St., Suite 150, Allentown, PA
18101.
NRC Branch Chief: James G. Danna.
Tennessee Valley Authority (TVA), Docket Nos. 50-259, 50-260, and 50-
296, Browns Ferry Nuclear Plant (BFN), Units 1, 2, and 3, Limestone
County, Alabama
Date of amendment request: August 15, 2017. A publicly-available
version is in ADAMS under Accession No. ML17228A490.
Description of amendment request: The amendments would revise the
BFN, Units 1, 2, and 3 Technical Specification (TS) 5.5.12, ``Primary
Containment Leakage Rate Testing Program,'' by adopting Nuclear Energy
Institute (NEI) 94-01, Revision 3-A, ``Industry Guideline for
Implementing Performance-Based Option of 10 CFR part 50, Appendix J,''
as the implementation document for the performance-based Option B of 10
CFR part 50, Appendix J. The proposed changes permanently extend the
Type A containment integrated leak rate testing (ILRT) interval from 10
years to 15 years and the Type C local leakage rate testing (LLRT)
intervals from 60 months to 75 months.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequence of an accident previously evaluated?
Response: No.
The proposed revision to TS 5.5.12 changes the testing period to
a permanent 15-year interval for Type A testing (10 CFR part 50,
Appendix J, Option B, ILRT) and a 75-month interval for Type C
testing (10 CFR part 50, Appendix J, Option B, LLRT). The current
Type A test interval of 10 years would be extended to 15 years from
the last Type A test. The proposed extension to Type A testing does
not involve a significant increase in the consequences of an
accident because research documented in NUREG-1493, ``Performance-
Based Containment System Leakage Testing Requirements''
[``Performance-Based Containment Leak-Test Program''], September
1995, has found that, generically, very few potential containment
leakage paths are not identified by Type B and C tests. NUREG-1493
concluded that reducing the Type A testing frequency to one per 20
years was found to lead to an imperceptible increase in risk. A high
degree of assurance is provided through testing and inspection that
the containment will not degrade in a manner detectable only by Type
A testing. The last Type A test (performed November 19, 2010 for
BFN, Unit 1, June 3, 2009 for BFN, Unit 2 and May 12, 2012 for BFN,
Unit 3) shows leakage to be below acceptance criteria, indicating a
very leak tight containment. Inspections required by the ASME Code
[American Society of Mechanical Engineers Boiler and Press Vessel
Code] Section Xl (Subsection IWE) and Maintenance Rule monitoring
(10 CFR 50.65, ``Requirements for Monitoring the Effectiveness of
Maintenance at Nuclear Power Plants'') are performed in order to
identify indications of containment degradation that could affect
that leak tightness. Types B and C testing required by TSs will
identify any containment opening such as valves that would otherwise
be detected by the Type A tests. These factors show that a Type A
test interval extension will not represent a significant increase in
the consequences of an accident.
The proposed amendment involves changes to the BFN, Units 1, 2,
and 3, 10 CFR 50 Appendix J Testing Program Plan. The proposed
amendment does not involve a physical change to the plant or a
change in the manner in which the units are operated or controlled.
The primary containment function is to provide an essentially leak
tight barrier against the uncontrolled release of radioactivity to
the environment for postulated accidents. As such, the containment
itself and the testing requirements to periodically demonstrate the
integrity of the containment exist to ensure the plant's ability to
mitigate the consequences of an accident, and do not involve any
accident precursors or initiators. Therefore, the probability of
occurrence of an accident previously evaluated is not significantly
increased by the proposed amendment.
The proposed amendment adopts the NRC-accepted guidelines of NEI
94-01, Revision 3-A, for development of the BFN, Units 1, 2, and 3,
performance-based leakage testing program. Implementation of these
guidelines continues to provide adequate assurance that during
design basis accidents, the primary containment and its components
will limit leakage rates to less than the values assumed in the
plant safety analyses. The potential consequences of extending the
ILRT interval from 10 years to 15 years have been evaluated by
analyzing the resulting changes in risk. The increase in risk in
terms of person-rem [roentgen equivalent man] per year resulting
from design basis accidents was estimated to be very small, and the
increase in the LERF [large early release frequency] resulting from
the proposed change was determined to be within the guidelines
published in NRC RG [Regulatory Guide] 1.174. Additionally, the
proposed change maintains defense-in-depth by preserving a
reasonable balance among prevention of core damage, prevention of
containment failure, and consequence mitigation. TVA has determined
that the increase in CCFP [conditional containment failure
probability] due to the proposed change would be very small.
Based on the above discussions, the proposed changes do not
involve an increase in the probability or consequences of an
accident previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
[[Page 55416]]
The proposed revision to TS 5.5.12 changes the testing period to
a permanent 15-year interval for Type A testing (10 CFR part 50,
Appendix J, Option B, ILRT) and a 75-month interval for Type C
testing (10 CFR part 50, Appendix J, Option B, LLRT). The current
test interval of 10 years, based on past performance, would be
extended to 15 years from the last Type A test (performed November
19, 2010 for BFN, Unit 1, June 3, 2009 for BFN, Unit 2 and May 12,
2012 for BFN, Unit 3). The proposed extension to Type A and Type C
test intervals does not create the possibility of a new or different
type of accident because there are no physical changes being made to
the plant and there are no changes to the operation of the plant
that could introduce a new failure mode creating an accident or
affecting the mitigation of an accident.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed revision to TS 5.5.12 changes the testing period to
a permanent 15-year interval for Type A testing (10 CFR part 50,
Appendix J, Option B, ILRT) and a 75-month interval for Type C
testing (10 CFR part 50, Appendix J, Option B, LLRT). The current
test interval of 10 years, based on past performance, would be
extended to 15 years from the last Type A test (performed November
19, 2010 for BFN, Unit 1, June 3, 2009 for BFN, Unit 2 and May 12,
2012 for BFN, Unit 3). The proposed extension to Type A testing will
not significantly reduce the margin of safety. NUREG-1493,
``Performance-Based Containment System Leakage Testing
Requirements'' [``Performance-Based Containment Leak-Test
Program''], September 1995, generic study of the effects of
extending containment leakage testing, found that a 20 year
extension to Type A leakage testing resulted in an imperceptible
increase in risk to the public. NUREG-1493 found that, generically,
the design containment leakage rate contributes about 0.1% to the
individual risk and that the decrease in Type A testing frequency
would have a minimal effect on this risk since 95% of the potential
leakage paths are detected by Type C testing. Regular inspections
required by the ASME Code Section Xl (Subsection IWE) and
maintenance rule monitoring (10 CFR 50.65, ``Requirements for
Monitoring the Effectiveness of Maintenance at Nuclear Power
Plants'') will further reduce the risk of a containment leakage path
going undetected.
The proposed amendment adopts the NRC-accepted guidelines of NEI
94-01, Revision 3-A, for development of the BFN, Units 1, 2, and 3,
performance-based leakage testing program, and establishes a 15-year
interval for the performance of the primary containment ILRT and a
75-month interval for Type C testing. The amendment does not alter
the manner in which safety limits, limiting safety system setpoints,
or limiting conditions for operation are determined. The specific
requirements and conditions of the 10 CFR part 50, Appendix J
Testing Program Plan, as defined in the TS, ensure that the degree
of primary containment structural integrity and leak-tightness that
is considered in the plant safety analyses is maintained. The
overall containment leakage rate limit specified by the TS is
maintained, and the Type A, B, and C containment leakage tests will
continue to be performed at the frequencies established in
accordance with the NRC-accepted guidelines of NEI 94-01, Revision
3-A.
Containment inspections performed in accordance with other plant
programs serve to provide a high degree of assurance that the
containment will not degrade in a manner that is detectable only by
an ILRT. This ensures that evidence of containment structural
degradation is identified in a timely manner. Furthermore, a risk
assessment using the current BFN, Units 1, 2, and 3, PRA
[probabilistic risk assessment] model concluded that extending the
ILRT test interval from 10 years to 15 years results in a very small
change to the BFN, Units 1, 2, and 3, risk profile.
Accordingly, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: General Counsel, Tennessee Valley Authority,
400 West Summit Hill Dr., WT 6A, Knoxville, TN 37902.
NRC Branch Chief: Undine Shoop.
Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah
Nuclear Plant, Units 1 and 2 (SQN), Hamilton County, Tennessee
Tennessee Valley Authority, Docket Nos. 50-390 and 50-391, Watts Bar
Nuclear Plant, Units 1 and 2 (WBN), Rhea County, Tennessee
Date of amendment request: August 7, 2017. A publicly-available
version is in ADAMS under Accession No. ML17219A505.
Description of amendment request: The amendment would revise
Technical Specification (TS) 3.2.4, ``Quadrant Power Tilt Ratio
(QPTR),'' and TS 3.3.1, ``Reactor Trip System (RTS) Instrumentation,''
to avoid confusion as to when an incore power distribution measurement
for QPTR is required. The amendment would also revise the WBN TSs for
consistency with the existing SQN TSs and Westinghouse Standard TSs in
NUREG-1431, Revision 4.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes do not adversely affect accident initiators
or precursors nor alter the design assumptions, conditions, or
configuration of the facility or the manner in which the plant is
operated and maintained. The proposed changes do not alter or
prevent the ability of structures, systems, and components (SSCs)
from performing their intended function to mitigate the consequences
of an initiating event within the assumed acceptance limits. The
proposed changes do not affect the source term, containment
isolation, or radiological release assumptions used in evaluating
the radiological consequences of an accident previously evaluated.
Further, the proposed changes do not increase the types or amounts
of radioactive effluent that may be released offsite, nor
significantly increase individual or cumulative occupational/public
radiation exposures. The proposed changes do not significantly
increase the probability of an accident and are consistent with
safety analysis assumptions and resultant consequences.
Therefore, the changes do not increase the probability or
consequences of an accident previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed changes do not result in a change in the manner in
which the reactor trip system (RTS) and engineered safety feature
actuation system (ESFAS) provide plant protection. The RTS and ESFAS
will continue to have the same setpoints after the proposed changes
are implemented. There are no design changes associated with the
change. The changes do not involve a physical alteration of the
plant (i.e., no new or different type of equipment will be
installed) or a change in the methods governing normal plant
operation. In addition, the changes do not impose any new or
different requirements. The changes do not alter assumptions made in
the safety analysis. The proposed changes are consistent with the
safety analysis assumptions and current plant operating practice.
Therefore, the changes do not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed changes do not alter the manner in which safety
limits, limiting safety system settings or limiting conditions for
operation are determined. The safety analysis acceptance criteria
are not impacted by these changes. Redundant RTS and ESFAS trains
are maintained, and diversity with regard to the signals that
provide reactor trip and engineered safety features actuation is
also
[[Page 55417]]
maintained. All signals credited as providing primary or secondary
protection, and all operator actions credited in the accident
analyses will remain the same. The proposed changes will not result
in plant operation in a configuration outside the design basis.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: General Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, 6A West Tower, Knoxville, TN 37902.
NRC Branch Chief: Undine Shoop.
III. Notice of Issuance of Amendments to Facility Operating Licenses
and Combined Licenses
During the period since publication of the last biweekly notice,
the Commission has issued the following amendments. The Commission has
determined for each of these amendments that the application complies
with the standards and requirements of the Atomic Energy Act of 1954,
as amended (the Act), and the Commission's rules and regulations. The
Commission has made appropriate findings as required by the Act and the
Commission's rules and regulations in 10 CFR chapter I, which are set
forth in the license amendment.
A notice of consideration of issuance of amendment to facility
operating license or combined license, as applicable, proposed no
significant hazards consideration determination, and opportunity for a
hearing in connection with these actions, was published in the Federal
Register as indicated.
Unless otherwise indicated, the Commission has determined that
these amendments satisfy the criteria for categorical exclusion in
accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b),
no environmental impact statement or environmental assessment need be
prepared for these amendments. If the Commission has prepared an
environmental assessment under the special circumstances provision in
10 CFR 51.22(b) and has made a determination based on that assessment,
it is so indicated.
For further details with respect to the action see (1) the
applications for amendment, (2) the amendment, and (3) the Commission's
related letter, Safety Evaluation and/or Environmental Assessment as
indicated. All of these items can be accessed as described in the
``Obtaining Information and Submitting Comments'' section of this
document.
Duke Energy Carolinas, LLC, Docket Nos. 50-413 and 50-414, Catawba
Nuclear Station, Units 1 and 2, York County, South Carolina
Date of amendment requests: December 15, 2016.
Brief description of amendments: The amendments modified Technical
Specification (TS) 3.4.10, ``Pressurizer Safety Valves,'' TS 3.7.4,
``Steam Generator Power Operated Relief Valves (SG PORVs),'' and TS
3.7.6, ``Condensate Storage System,'' to revise the Completion Times
for Limiting Condition for Operation (LCO) of TS LCO 3.4.10 Required
Action B.2, TS LCO 3.7.4 Required Action C.2, and TS LCO 3.7.6 Required
Action B.2 from 12 to 24 hours. The proposed changes are consistent
with Technical Specifications Task Force (TSTF) Traveler TSTF-352-A,
Revision 1, ``Provide Consistent Completion Time to Reach MODE 4.''
Date of issuance: October 23, 2017.
Effective date: These license amendments are effective as of its
date of issuance and shall be implemented within 120 days of issuance.
Amendment Nos.: 294 (Unit 1) and 290 (Unit 2). A publicly-available
version is in ADAMS under Accession No. ML17254A144; documents related
to these amendments are listed in the Safety Evaluation enclosed with
the amendments.
Renewed Facility Operating License Nos. NPF-35 and NPF-52:
Amendments revised the renewed licenses and technical specifications.
Date of initial notice in Federal Register: April 25, 2017 (82 FR
19099).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated October 23, 2017.
No significant hazards consideration comments received: No.
Duke Energy Carolinas, LLC, Docket Nos. 50-413 and 50-414, Catawba
Nuclear Station, Units 1 and 2, York County, South Carolina
Date of amendment requests: December 15, 2016.
Brief description of amendments: The amendments modified technical
specification (TS) limiting condition for operation (LCO) 3.7.5,
``Auxiliary Feedwater (AFW) System,'' Condition A and Required Action
A.1. Condition A was revised to include the situation when one turbine-
driven AFW pump is inoperable in MODE 3, immediately following a
refueling outage, only applicable if MODE 2 has not been entered
following the refueling outage. Required Action A.1 was revised to
include the turbine-driven AFW addition to Condition A. The amendments
are consistent with Technical Specifications Task Force (TSTF) Traveler
TSTF-340-A, Revision 3, ``Allow 7 day Completion Time for a turbine-
driven AFW pump inoperable.''
Date of issuance: October 23, 2017.
Effective date: These license amendments are effective as of its
date of issuance and shall be implemented within 120 days of issuance.
Amendment Nos.: 295 (Unit 1) and 291 (Unit 2). A publicly-available
version is in ADAMS under Accession No. ML17257A297; documents related
to these amendments are listed in the Safety Evaluation enclosed with
the amendments.
Renewed Facility Operating License Nos. NPF-35 and NPF-52:
Amendments revised the renewed licenses and TSs.
Date of initial notice in Federal Register: April 25, 2017 (82 FR
19100).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated October 23, 2017.
No significant hazards consideration comments received: No.
Duke Energy Carolinas, LLC, Docket Nos. 50-413 and 50-414, Catawba
Nuclear Station, Units 1 and 2, York County, South Carolina
Date of amendment requests: December 15, 2016.
Brief description of amendments: The amendments revised Technical
Specification 3.1.2, ``Core Reactivity,'' to revise the Completion
Times of Required Actions A.1 and A.2 from 72 hours to 7 days. This
proposed change is consistent with Technical Specifications Task Force
(TSTF) Traveler TSTF-142-A, Revision 0, ``Increase the Completion Time
when the Core Reactivity Balance is Not Within Limit.''
Date of issuance: October 23, 2017.
Effective date: As of the date of issuance and shall be implemented
within 120 days of issuance.
Amendment Nos.: 296 (Unit 1) and 292 (Unit 2). A publicly-available
version is in ADAMS under Accession No. ML17261B290; documents related
to these amendments are listed in the Safety Evaluation enclosed with
the amendments.
Renewed Facility Operating License Nos. NPF-35 and NPF-52:
Amendments revised the Renewed Licenses and Technical Specifications.
[[Page 55418]]
Date of initial notice in Federal Register: April 11, 2017 (82 FR
17457).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated October 23, 2017.
No significant hazards consideration comments received: No.
Duke Energy Carolinas, LLC, Docket Nos. 50-369 and 50-370, McGuire
Nuclear Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of amendment requests: January 11, 2017.
Brief description of amendments: The amendments modified Technical
Specification (TS) 3.8.1, ``AC Sources--Operating,'' to allow greater
flexibility in performing Surveillance Requirements (SRs) by modifying
Mode restriction notes in TS SRs 3.8.1.8, 3.8.1.11, 3.8.1.16, 3.8.1.17,
and 3.8.1.19. This proposed change was consistent with Technical
Specifications Task Force (TSTF) Traveler TSTF-283-A, Revision 3,
``Modify Section 3.8 Mode Restriction Notes.''
Date of issuance: October 25, 2017.
Effective date: These license amendments are effective as of its
date of issuance and shall be implemented within 120 days of issuance.
Amendment Nos.: 300 (Unit 1) and 279 (Unit 2). A publicly-available
version is in ADAMS under Accession No. ML17269A055; documents related
to these amendments are listed in the Safety Evaluation enclosed with
the amendments.
Renewed Facility Operating License Nos. NPF-9 and NPF-17:
Amendments revised the renewed facility operating licenses and
technical specifications.
Date of initial notice in Federal Register: May 23, 2017 (82 FR
23620).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated October 25, 2017.
No significant hazards consideration comments received: Yes. One
comment from a member of the public was received, however it was not
related to the no significant hazards consideration determination nor
the license amendment request.
Duke Energy Carolinas, LLC, Docket Nos. 50-369 and 50-370, McGuire
Nuclear Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of amendment requests: January 11, 2017.
Brief description of amendments: The amendments modified Technical
Specification (TS) 3.1.8, ``PHYSICS TESTS Exceptions,'' to allow the
numbers of channels required by the Limiting Condition for Operation
(LCO) section of TS 3.3.1, ``Reactor Trip System (RTS)
Instrumentation,'' to be reduced from ``4'' to ``3'' to allow one
nuclear instrumentation channel to be used as an input to the
reactivity computer for physics testing without placing the nuclear
instrumentation channel in a tripped condition. This proposed change is
consistent with Technical Specifications Task Force (TSTF) Traveler
TSTF-315-A, Revision 0, ``Reduce plant trips due to spurious signals to
the NIS [Nuclear Instrumentation System] during physics testing.''
Date of issuance: October 25, 2017.
Effective date: These license amendments are effective as of their
date of issuance and shall be implemented within 120 days of issuance.
Amendment Nos.: 301 (Unit 1) and 280 (Unit 2). A publicly-available
version is in ADAMS under Accession No. ML17261B218; documents related
to these amendments are listed in the Safety Evaluation enclosed with
the amendments.
Renewed Facility Operating License Nos. NPF-9 and NPF-17:
Amendments revised the renewed facility operating licenses and
technical specifications.
Date of initial notice in Federal Register: May 23, 2017 (82 FR
23621).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated October 25, 2017.
No significant hazards consideration comments received: Yes. One
comment from a member of the public was received, however it was not
related to the proposed no significant hazards consideration
determination or to the license amendment request.
Duke Energy Carolinas, LLC, Docket Nos. 50-369 and 50-370, McGuire
Nuclear Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of amendment requests: January 11, 2017.
Brief description of amendments: The amendments modify the limiting
condition for operation (LCO) Required Action B.2 for Technical
Specification (TS) 3.4.10, ``Pressurizer Safety Valves,'' LCO Required
Action C.2 for TS 3.7.4, ``Steam Generator Power Operated Relief Valves
(SG PORVs),'' and LCO Required Action G.1 for TS 3.4.12, ``Low
Temperature Overpressure Protection (LTOP) System.'' Specifically, the
Completion Times are revised from 12 hours to 24 hours for TS LCO
3.4.10, Required Action B.2, and TS LCO 3.7.4, Required Action C.2; and
from 8 hours to 12 hours for TS LCO 3.4.12, Required Action G.1. The
changes are consistent with Technical Specifications Task Force (TSTF)
Traveler TSTF-352-A, Revision 1, ``Provide Consistent Completion Time
to Reach MODE 4.''
Date of issuance: October 31, 2017.
Effective date: These license amendments are effective as of their
date of issuance and shall be implemented within 120 days of issuance.
Amendment Nos.: 302 (Unit 1) and 281 (Unit 2). A publicly-available
version is in ADAMS under Accession No. ML17269A198; documents related
to these amendments are listed in the Safety Evaluation enclosed with
the amendments.
Renewed Facility Operating License Nos. NPF-9 and NPF-17:
Amendments revised the Renewed Licenses and Technical Specifications.
Date of initial notice in Federal Register: May 23, 2017 (82 FR
23622).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated October 31, 2017.
No significant hazards consideration comments received: Yes. One
comment from a member of the public was received, however it was not
related to the proposed no significant hazards consideration
determination or to the license amendment request.
Duke Energy Carolinas, LLC, Docket Nos. 50-369 and 50-370, McGuire
Nuclear Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of amendment requests: January 11, 2017.
Brief description of amendments: The amendments modify Technical
Specification (TS) 3.7.5, ``Auxiliary Feedwater (AFW) System,''
Limiting Condition for Operation (LCO) Condition A and Required Action
A.1. The proposed changes modify Condition A to expand the condition to
include when one turbine driven AFW pump is inoperable in MODE 3. This
expanded condition is applicable immediately following a refueling
outage and only if MODE 2 has not been entered. Required Action A.1 is
revised to state ``affected equipment'' as opposed to ``steam supply''
as a result of the addition of the turbine driven AFW pump to Condition
A. The changes are consistent with Technical Specifications Task Force
(TSTF) Traveler TSTF-340-A, Revision 3, ``Allow 7 day Completion Time
for a turbine-driven AFW pump inoperable.''
Date of issuance: October 31, 2017.
Effective date: These license amendments are effective as of their
date of issuance and shall be
[[Page 55419]]
implemented within 120 days of issuance.
Amendment Nos.: 304 (Unit 1) and 283 (Unit 2). A publicly-available
version is in ADAMS under Accession No. ML17277A313; documents related
to these amendments are listed in the Safety Evaluation enclosed with
the amendments.
Renewed Facility Operating License Nos. NPF-9 and NPF-17:
Amendments revised the renewed facility operating licenses and
technical specifications.
Date of initial notice in Federal Register: May 23, 2017 (82 FR
23621).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated October 31, 2017.
No significant hazards consideration comments received: Yes. One
comment from a member of the public was received, however it was not
related to the proposed no significant hazards consideration
determination or to the license amendment request.
Duke Energy Carolinas, LLC, Docket Nos. 50-369 and 50-370, McGuire
Nuclear Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of application for amendments: January 11, 2017.
Brief description of amendments: The amendments modify Technical
Specification (TS) Limiting Condition for Operation (LCO) 3.9.6,
``Residual Heat Removal (RHR) and Coolant Circulation--Low Water
Level,'' to add a note which allows all RHR pumps to be secured for
less than or equal to 15 minutes to support the switching of the
shutdown cooling loops from one train to another. The changes are
consistent with Technical Specifications Task Force (TSTF) Travelers
TSTF-349-A, Revision 1, ``Add Note to LCO 3.9.5 Allowing Shutdown
Cooling Loops Removal from Operation,'' TSTF-361-A, Revision 2, ``Allow
standby [Shutdown Cooling] SDC/RHR/[Decay Heat Removal] DHR loop to
[be] inoperable to support testing,'' and TSTF-438-A, Revision 0,
``Clarify Exception Notes to be Consistent with the Requirement Being
Excepted.''
Date of issuance: October 31, 2017.
Effective date: As of the date of issuance and shall be implemented
within 120 days of issuance.
Amendment Nos.: Unit 1--303; Unit 2--282. A publicly-available
version is in ADAMS under Accession No. ML17271A034; documents related
to these amendments are listed in the Safety Evaluation enclosed with
the amendments.
Renewed Facility Operating License Nos. NPF-9 and NPF-17:
Amendments revised the Renewed Licenses and Technical Specifications.
Date of initial notice in Federal Register: May 23, 2017 (82 FR
23623).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated October 31, 2017.
No significant hazards consideration comments received: Yes. One
comment from a member of the public was received, however it was not
related to the proposed no significant hazards consideration
determination or the license amendment request.
Duke Energy Progress, LLC, Docket No. 50-400, Shearon Harris Nuclear
Power Plant, Unit 1, Wake and Chatham Counties, North Carolina
Date of amendment request: December 2, 2016, as supplemented by
letters dated April 25, May 22, and October 2, 2017.
Brief description of amendment: The amendment revised the Technical
Specifications (TSs) to (1) relocate cycle-specific parameters to the
Core Operating Limits Report (COLR) consistent with Technical
Specification Task Force (TSTF)-339, ``Relocate TS Parameters to
COLR;'' (2) delete duplicate reporting requirements in the
Administrative Section of TSs consistent with TSTF-5, ``Delete Safety
Limit Violation Notification Requirements,'' Revision 1; and (3) delete
reference to plant procedure PLP-6, ``Technical Specification Equipment
List Program and Core Operating Limits Report,'' in TSs as it pertains
to the COLR.
Date of issuance: November 6, 2017.
Effective date: As of the date of issuance and shall be implemented
within 90 days of issuance.
Amendment No.: 161. A publicly-available version is in ADAMS under
Accession No. ML17250A202; documents related to this amendment are
listed in the Safety Evaluation enclosed with the amendment.
Renewed Facility Operating License No. NPF-63: Amendment revised
the Facility Operating License and TSs.
Date of initial notice in Federal Register: February 14, 2017 (82
FR 10595). The supplemental letters dated April 25, May 22, and October
2, 2017, provided additional information that clarified the
application, did not expand the scope of the application as originally
noticed, and did not change the staff's original proposed no
significant hazards consideration determination as published in the
Federal Register.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated November 6, 2017.
No significant hazards consideration comments received: No.
Energy Northwest, Docket No. 50-397, Columbia Generating Station,
Benton County, Washington
Date of amendment request: November 8, 2016, as supplemented by
letter dated July 11, 2017.
Brief description of amendment: The amendment would, on a one-time
basis, extend the completion time from 7 days to 14 days for the
Residual Heat Removal Train A subsystem to operable status associated
with Technical Specification (TS) 3.5.1, ``ECCS [Emergency Core Cooling
System]--Operating''; TS 3.6.1.5, ``Residual Heat Removal (RHR) Drywell
Spray''; and TS 3.6.2.3, ``Residual Heat Removal (RHR) Suppression Pool
Cooling.'' This amendment will be used to support preventive
maintenance, which replaces the RHR Train A subsystem's pump and motor.
Date of issuance: October 30, 2017.
Effective date: As of its date of issuance and shall be implemented
within 60 days from the date of issuance.
Amendment No.: 245. A publicly-available version is in ADAMS under
Accession No. ML17290A127; documents related to this amendment are
listed in the Safety Evaluation enclosed with the amendment.
Renewed Facility Operating License No. NPF-21: The amendment
revised the Renewed Facility Operating License and Technical
Specifications.
Date of initial notice in Federal Register: February 14, 2017 (82
FR 10596). The supplemental letter dated July 11, 2017, provided
additional information that clarified the application, did not expand
the scope of the application as originally noticed, and did not change
the NRC staff's original proposed no significant hazards consideration
determination as published in the Federal Register.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated October 30, 2017.
No significant hazards consideration comments received: No.
Exelon Generation Company, LLC and PSEG Nuclear LLC, Docket No. 50-277,
Peach Bottom Atomic Power Station, Unit 2, York and Lancaster Counties,
Pennsylvania
Date of amendment request: May 19, 2017, as supplemented by letter
dated August 29, 2017.
[[Page 55420]]
Brief description of amendment: The amendment revised the Technical
Specifications to decrease the number of safety relief valves and
safety valves required to be operable when operating at a power level
less than or equal to 3,358 megawatts thermal. This change is
applicable only to the current Cycle 22 that is scheduled to end in
October 2018.
Date of issuance: October 25, 2017.
Effective date: As of the date of issuance and shall be implemented
within 5 days.
Amendment No.: 315. A publicly-available version is in ADAMS under
Accession No. ML17249A151; documents related to this amendment are
listed in the Safety Evaluation enclosed with the amendment.
Renewed Facility Operating License No. DPR-44: The amendment
revised the Renewed Facility Operating License and Technical
Specifications.
Date of initial notice in Federal Register: July 5, 2017 (82 FR
31094). The supplemental letter dated August 29, 2017, provided
additional information that clarified the application, did not expand
the scope of the application as originally noticed, and did not change
the NRC staff's original proposed no significant hazards consideration
determination as published in the Federal Register.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated October 25, 2017.
No significant hazards consideration comments received: No.
Exelon Generation Company, LLC, Docket Nos. 50-373 and 50-374, LaSalle
County Station (LSCS), Units 1 and 2, LaSalle County, Illinois
Date of application for amendments: October 27, 2016, as
supplemented by the letters dated July 28, 2017, August 30, 2017, and
October 19, 2017.
Brief description of amendments: The amendments revised the
suppression pool swell design analysis. The new analysis utilizes a
different computer code and incorporates different analysis assumptions
than the current analysis. The changes are necessary because the
current design analysis determining the suppression pool swell response
to a loss-of-coolant accident was determined to be non-conservative.
These changes to the suppression pool swell design analysis do not
require any changes to the LSCS Technical Specifications. Changes to
the LSCS updated final safety analysis report related to changes to the
suppression pool swell design analysis shall be made in accordance with
10 CFR 50.71(e) based on the NRC approval of these changes.
Date of issuance: October 30, 2017.
Effective date: These license amendments are effective as of the
date of its issuance and shall be implemented within 60 days from the
date of issuance.
Amendment Nos.: 225 for NPF-11 and 211 for NPF-18. A publicly-
available version is in ADAMS under Accession No. ML17257A304;
documents related to this amendment are listed in the Safety Evaluation
enclosed with the amendment.
Facility Operating License Nos. NPF-11 and NPF-18: The amendments
approved to revise the LSCS updated final safety analysis report
related to changes to the suppression pool swell design analysis and
the Licenses.
Date of initial notice in Federal Register: March 8, 2017 (82 FR
13022). The supplements dated July 28, 2017, August 30, 2017, and
October 19, 2017, contained clarifying information and did not change
the NRC staff's initial proposed finding of no significant hazards
consideration.
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated October 30, 2017.
No significant hazards consideration comments received: No.
Exelon Generation Company, LLC, Docket No. 50-410, Nine Mile Point
Nuclear Station (Nine Mile Point), Unit 2, Oswego County, New York
Date of amendment request: December 13, 2016, as supplemented by
letter dated February 17, 2017.
Brief description of amendment: The amendment revised the Nine Mile
Point, Unit 2, Technical Specification (TS) safety limit (SL) to
increase the low pressure isolation setpoint allowable value, which
will result in earlier main steam line isolation. The revised main
steam line low pressure isolation capability and the revised SL are
intended to ensure that Nine Mile Point, Unit 2, remains within the TS
SLs in the event of a pressure regulator failure maximum demand
transient.
Date of issuance: October 31, 2017.
Effective date: As of the date of issuance and shall be implemented
within 180 days of issuance.
Amendment No.: 164. A publicly-available version is in ADAMS under
Accession No. ML17268A263; documents related to this amendment are
listed in the Safety Evaluation enclosed with the amendment.
Renewed Facility Operating License No. NPF-69: Amendment revised
the Renewed Facility Operating License and Technical Specifications.
Date of initial notice in Federal Register: March 28, 2017 (82 FR
15381). The supplemental letter dated February 17, 2017, provided
additional information that clarified the application, did not expand
the scope of the application as originally noticed, and did not change
the NRC staff's original proposed no significant hazards consideration
determination as published in the Federal Register.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated October 31, 2017.
No significant hazards consideration comments received: No.
Florida Power & Light Company, et al., Docket Nos. 50-335 and 50-389,
St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
Date of amendment request: January 23, 2017, as supplemented by
letter dated July 3, 2017.
Brief description of amendments: The amendments revised the
Technical Specifications (TSs) by limiting the MODE of applicability
for the Reactor Protection System, Startup, and Operating Rate of
Change of Power--High, functional unit trip. Additionally, the
amendments added new Limiting Condition for Operation (LCO) 3.0.5 and
relatedly modified LCO 3.0.1 and LCO 3.0.2, to provide for placing
inoperable equipment under administrative control for the purpose of
conducting testing required to demonstrate OPERABILITY.
Date of issuance: November 2, 2017.
Effective date: As of the date of issuance and shall be implemented
within 90 days of issuance.
Amendment Nos.: 243 and 194. A publicly-available version is in
ADAMS under Accession No. ML17257A015; documents related to this
amendment are listed in the Safety Evaluation enclosed with the
amendment.
Renewed Facility Operating License Nos. DPR-67 and NPF-16:
Amendments revised the Renewed Facility Operating Licenses and TSs.
Date of initial notice in Federal Register: March 28, 2017 (82 FR
15383). The supplemental letter dated July 3, 2017, provided additional
information that expanded the scope of the application as originally
noticed and changed the NRC staff's original proposed no significant
hazards consideration (NSHC) determination as published in the Federal
Register. Accordingly, the NRC published a second proposed no
significant hazards consideration determination in the Federal Register
on September 12, 2017
[[Page 55421]]
(82 FR 42849). This notice superseded the original notice in its
entirety. It also provided an opportunity to request a hearing by
November 13, 2017, but indicated that if the Commission makes a final
NSHC determination, any such hearing would take place after issuance of
the amendments.
The Commission's related evaluation of the amendments and final
NSHC are contained in a Safety Evaluation dated November 2, 2017.
No significant hazards consideration comments received: No.
Florida Power & Light Company, Docket Nos. 50-250 and 50-251, Turkey
Point Nuclear Generating Unit Nos. 3 and 4, Miami-Dade County, Florida
Date of amendment request: December 21, 2016.
Brief description of amendments: The amendments modify the
Technical Specifications by deleting high-range noble gas effluent
monitors' requirements and relocating the requirements to the Turkey
Point Offsite Dose Calculation Manual.
Date of issuance: October 26, 2017.
Effective date: As of the date of issuance and shall be implemented
within 90 days of issuance.
Amendment Nos: 277 and 272. A publicly-available version is in
ADAMS under Accession No. ML17228A563. Documents related to these
amendments are listed in the Safety Evaluation enclosed with the
amendments.
Renewed Facility Operating License Nos. DPR-31 and DPR-41:
Amendments revised the Renewed Facility Operating Licenses and TSs.
Date of initial notice in Federal Register: March 14, 2017 (82 FR
13666).
The Commission's related evaluation of the amendments is contained
in a safety evaluation dated October 26, 2017.
No significant hazards consideration comments received: No.
Southern Nuclear Operating Company, Docket Nos. 50-348 and 50-364,
Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County, Alabama
Date of amendment request: August 11, 2017.
Brief description of amendments: The amendments request an
extension to the time to achieve full compliance with 10 CFR 50.48(c),
National Fire Protection Association (NPFA) 805, from November 6, 2017,
to the conclusion of the FNP, Unit 1, Spring 2018 Refueling Outage
(1R28). The amendments update Attachment S, ``Modification and
Implementation Items''; of the previously approved NFPA-805 amendment.
Date of issuance: November 1, 2017.
Effective date: As of the date of issuance and shall be implemented
within 30 days of issuance.
Amendment Nos.: 215 (Unit 1) and 212 (Unit 2). A publicly-available
version is in ADAMS under Accession No. ML17269A166; documents related
to these amendments are listed in the Safety Evaluation enclosed with
the amendments.
Renewed Facility Operating License Nos. NPF-2 and NPF-8: The
amendments revised the Renewed Facility Operating Licenses.
Date of initial notice in Federal Register: August 29, 2017 (82 FR
41059).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated November 1, 2017.
No significant hazards consideration comments received: No.
Dated at Rockville, Maryland, this 14th day of November 2017.
For the Nuclear Regulatory Commission.
Kathryn M. Brock,
Acting Director, Division of Operating Reactor Licensing, Office of
Nuclear Reactor Regulation.
[FR Doc. 2017-25063 Filed 11-20-17; 8:45 am]
BILLING CODE 7590-01-P