Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 53774-53784 [E9-24915]
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Federal Register / Vol. 74, No. 201 / Tuesday, October 20, 2009 / Notices
NUCLEAR REGULATORY
COMMISSION
[NRC–2009–0456]
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC)
is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from September
24, 2009, to October 7, 2009. The last
biweekly notice was published on
October 6, 2009 (74 FR 51327).
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Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
Title 10 of the Code of Federal
Regulations (10 CFR), Section 50.92,
this means that operation of the facility
in accordance with the proposed
amendment would not (1) Involve a
significant increase in the probability or
consequences of an accident previously
evaluated; or (2) create the possibility of
a new or different kind of accident from
any accident previously evaluated; or
(3) involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
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publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rulemaking and
Directives Branch (RDB), TWB–05–
B01M, Division of Administrative
Services, Office of Administration, U.S.
Nuclear Regulatory Commission,
Washington, DC 20555–0001, and
should cite the publication date and
page number of this Federal Register
notice. Written comments may also be
faxed to the RDB at 301–492–3446.
Documents may be examined, and/or
copied for a fee, at the NRC’s Public
Document Room (PDR), located at One
White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland.
Within 60 days after the date of
publication of this notice, any person(s)
whose interest may be affected by this
action may file a request for a hearing
and a petition to intervene with respect
to issuance of the amendment to the
subject facility operating license.
Requests for a hearing and a petition for
leave to intervene shall be filed in
accordance with the Commission’s
‘‘Rules of Practice for Domestic
Licensing Proceedings’’ in 10 CFR part
2. Interested person(s) should consult a
current copy of 10 CFR 2.309, which is
available at the Commission’s PDR,
located at One White Flint North, Public
File Area O1F21, 11555 Rockville Pike
(first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed by the above
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date, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also identify the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
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participate fully in the conduct of the
hearing.
If a hearing is requested, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
All documents filed in NRC
adjudicatory proceedings, including a
request for hearing, a petition for leave
to intervene, any motion or other
document filed in the proceeding prior
to the submission of a request for
hearing or petition to intervene, and
documents filed by interested
governmental entities participating
under 10 CFR 2.315(c), must be filed in
accordance with the NRC E-Filing rule,
which the NRC promulgated in August
28, 2007 (72 FR 49139). The E-Filing
process requires participants to submit
and serve all adjudicatory documents
over the internet, or in some cases to
mail copies on electronic storage media.
Participants may not submit paper
copies of their filings unless they seek
an exemption in accordance with the
procedures described below.
To comply with the procedural
requirements of E-Filing, at least ten
(10) days prior to the filing deadline, the
petitioner/requestor should contact the
Office of the Secretary by e-mail at
hearing.docket@nrc.gov, or by calling
(301) 415–1677, to request (1) a digital
ID certificate, which allows the
participant (or its counsel or
representative) to digitally sign
documents and access the E-Submittal
server for any proceeding in which it is
participating; and/or (2) creation of an
electronic docket for the proceeding
(even in instances in which the
petitioner/requestor (or its counsel or
representative) already holds an NRCissued digital ID certificate). Each
petitioner/requestor will need to
download the Workplace Forms
ViewerTM to access the Electronic
Information Exchange (EIE), a
component of the E-Filing system. The
Workplace Forms ViewerTM is free and
is available at https://www.nrc.gov/sitehelp/e-submittals/install-viewer.html.
Information about applying for a digital
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ID certificate is available on NRC’s
public Web site at https://www.nrc.gov/
site-help/e-submittals/applycertificates.html.
Once a petitioner/requestor has
obtained a digital ID certificate, had a
docket created, and downloaded the EIE
viewer, it can then submit a request for
hearing or petition for leave to
intervene. Submissions should be in
Portable Document Format (PDF) in
accordance with NRC guidance
available on the NRC public Web site at
https://www.nrc.gov/site-help/esubmittals.html. A filing is considered
complete at the time the filer submits its
documents through EIE. To be timely,
an electronic filing must be submitted to
the EIE system no later than 11:59 p.m.
Eastern Time on the due date. Upon
receipt of a transmission, the E-Filing
system time-stamps the document and
sends the submitter an e-mail notice
confirming receipt of the document. The
EIE system also distributes an e-mail
notice that provides access to the
document to the NRC Office of the
General Counsel and any others who
have advised the Office of the Secretary
that they wish to participate in the
proceeding, so that the filer need not
serve the documents on those
participants separately. Therefore,
applicants and other participants (or
their counsel or representative) must
apply for and receive a digital ID
certificate before a hearing request/
petition to intervene is filed so that they
can obtain access to the document via
the E-Filing system.
A person filing electronically using
the agency’s adjudicatory e-filing system
may seek assistance through the
‘‘Contact Us’’ link located on the NRC
Web site at https://www.nrc.gov/sitehelp/e-submittals.html or by calling the
NRC Meta-System Help Desk, which is
available between 8 a.m. and 8 p.m.,
Eastern Time, Monday through Friday,
excluding government holidays. The
Meta-System Help Desk can be
contacted by telephone at 1–866–672–
7640 or by e-mail at
MSHD.Resource@nrc.gov.
Participants who believe that they
have a good cause for not submitting
documents electronically must file an
exemption request, in accordance with
10 CFR 2.302(g), with their initial paper
filing requesting authorization to
continue to submit documents in paper
format. Such filings must be submitted
by: (1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; or (2) courier,
express mail, or expedited delivery
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service to the Office of the Secretary,
Sixteenth Floor, One White Flint North,
11555 Rockville Pike, Rockville,
Maryland, 20852, Attention:
Rulemaking and Adjudications Staff.
Participants filing a document in this
manner are responsible for serving the
document on all other participants.
Filing is considered complete by firstclass mail as of the time of deposit in
the mail, or by courier, express mail, or
expedited delivery service upon
depositing the document with the
provider of the service.
Non-timely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission, the presiding officer, or
the Atomic Safety and Licensing Board
that the request and/or petition should
be granted and/or the contentions
should be admitted, based on a
balancing of the factors specified in 10
CFR 2.309(c)(1)(i)–(viii).
Documents submitted in adjudicatory
proceedings will appear in NRC’s
electronic hearing docket which is
available to the public at https://
ehd.nrc.gov/EHD_Proceeding/home.asp,
unless excluded pursuant to an order of
the Commission, an Atomic Safety and
Licensing Board, or a Presiding Officer.
Participants are requested not to include
personal privacy information, such as
social security numbers, home
addresses, or home phone numbers in
their filings, unless an NRC regulation
or other law requires submission of such
information. With respect to
copyrighted works, except for limited
excerpts that serve the purpose of the
adjudicatory filings and would
constitute a Fair Use application,
participants are requested not to include
copyrighted materials in their
submissions.
For further details with respect to this
license amendment application, see the
application for amendment which is
available for public inspection at the
Commission’s PDR, located at One
White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. Publicly
available records will be accessible from
the ADAMS Public Electronic Reading
Room on the Internet at the NRC Web
site, https://www.nrc.gov/reading-rm/
adams.html. Persons who do not have
access to ADAMS or who encounter
problems in accessing the documents
located in ADAMS, should contact the
NRC PDR Reference staff at 1–800–397–
4209, 301–415–4737, or by e-mail to
pdr.resource@nrc.gov.
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Entergy Gulf States Louisiana, LLC, and
Entergy Operations, Inc., Docket No. 50–
458, River Bend Station (RBS), Unit 1,
West Feliciana Parish, Louisiana
Date of amendment request: August
10, 2009.
Description of amendment request:
The proposed amendment would revise
the RBS Technical Specifications (TSs)
to support operation with 24-month fuel
cycles. Specifically, the change
addresses certain TS Surveillance
Requirement (SR) frequencies that are
specified as ‘‘18 months’’ by revising
them to ‘‘24 months’’ in accordance
with the guidance of U.S. Nuclear
Regulatory Commission (NRC) Generic
Letter 91–04, ‘‘Changes in Technical
Specification Surveillance Intervals to
Accommodate a 24-Month Fuel Cycle,’’
dated April 2, 1991.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed TS changes involve a change
in the surveillance testing intervals and
allowable values to facilitate a change in the
operating cycle length. The proposed TS
changes do not physically impact the plant.
The proposed TS changes do not degrade the
performance of, or increase the challenges to,
any safety systems assumed to function in
the accident analysis. The proposed TS
changes do not impact the usefulness of the
SRs in evaluating the operability of required
systems and components, or the way in
which the surveillances are performed. In
addition, the frequency of surveillance
testing is not considered an initiator of any
analyzed accident, nor does a revision to the
frequency introduce any accident initiators.
The specific value of the allowable value is
not considered an initiator of any analyzed
accident. Therefore, the proposed change
does not involve a significant increase in the
probability of an accident previously
evaluated.
The consequences of a previously
evaluated accident are not significantly
increased. The proposed change does not
affect the performance of any equipment
credited to mitigate the radiological
consequences of an accident. Evaluation of
the proposed TS changes demonstrated that
the availability of credited equipment is not
significantly affected because of other more
frequent testing that is performed, the
availability of redundant systems and
equipment, and the high reliability of the
equipment. Historical review of surveillance
test results and associated maintenance
records did not find evidence of failures that
would invalidate the above conclusions.
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The allowable values have been developed
in accordance with [NRC Regulatory Guide]
1.105, ‘‘Instrument Setpoints,’’ to ensure that
the design and safety analysis limits are
satisfied. The methodology used for the
development of the allowable values ensures
the affected instrumentation remains capable
of mitigating design basis events as described
in the safety analyses and that the results and
radiological consequences described in the
safety analyses remain bounding. Therefore,
the proposed change does not alter the ability
to detect and mitigate events and, as such,
does not involve a significant increase in the
consequences of an accident previously
evaluated.
Standby Liquid Control System
The proposed change in required weight of
Boron-10 in [standby liquid control (SLC)]
does not physically impact the plant, nor
does it degrade the performance of, or
increase the challenges to, any safety systems
assumed to function in the accident analysis.
The consequences of a previously evaluated
accident are not increased. The proposed
change does not affect the performance of
any equipment credited to mitigate the
radiological consequences of an accident.
Evaluation of the proposed TS changes
demonstrated that the availability of credited
equipment is not affected. Therefore, the
proposed change does not alter the ability to
detect and mitigate events and, as such, does
not involve a significant increase in the
consequences of an accident previously
evaluated.
Loss of Power Instrumentation
A change to the Allowable Values (AVs) is
proposed for Table 3.3.8.1–1, Item 1.c and
Item 2.c. The proposed change is the result
of application of the RBS Instrument Setpoint
Methodology using plant-specific drift values
and incorporating margins available based on
a revised off-site reliability study.
Application of this methodology results in
AVs that more accurately reflect total device
accuracy, as well as that of test equipment
and calculated drift between surveillances.
The proposed change will not result in any
hardware changes. The instrumentation is
not assumed to be an initiator of any
analyzed event. Existing operating margin
between plant conditions and actual plant
setpoints is not significantly reduced due to
the proposed changes. The role of the
instrumentation is in mitigating and thereby,
limiting the consequences of accidents.
The AVs were developed to ensure the
design and safety analysis limits are satisfied.
The methodology used for the development
of the AVs ensures that: (1) The affected
instrumentation remains capable of
mitigating design basis events as described in
the safety analysis, and (2) the results and
radiological consequences described in the
safety analysis remain bounding.
Additionally, the proposed change does not
alter the plant’s ability to detect and mitigate
events. Therefore, this change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The change in the degraded voltage
protection voltage AVs allows the protection
scheme to function as originally designed.
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The proposed allowable values ensure that
the Class 1E distribution system remains
connected to the offsite power system when
adequate offsite voltage is available and
motor starting transients are considered.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed TS changes involve a change
in the surveillance testing intervals and
allowable values to facilitate a change in the
operating cycle length. The proposed TS
changes do not introduce any failure
mechanisms of a different type than those
previously evaluated, since there are no
physical changes being made to the facility.
No new or different equipment is being
installed. No installed equipment is being
operated in a different manner. As a result,
no new failure modes are being introduced.
The way surveillance tests are performed
remains unchanged. A historical review of
surveillance test results and associated
maintenance records indicated there was no
evidence of any failures that would
invalidate the above conclusions.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
Standby Liquid Control System
The proposed change to the required
weight of Boron-10 in SLC does not
introduce any failure mechanisms of a
different type than those previously
evaluated, since there are no physical
changes being made to the facility. No new
or different equipment is being installed. No
installed equipment is being operated in a
different manner. As a result, no new failure
modes are being introduced. The way
surveillance tests are performed remains
unchanged. A historical review of
surveillance test results and associated
maintenance records indicated there was no
evidence of any failures that would
invalidate the above conclusions.
Loss of Power Instrumentation
The proposed change in AVs is the result
of application of the Instrument Setpoint
Methodology using plant-specific drift values
and does not create the possibility of a new
or different kind of accident from any
accident previously evaluated. This is based
upon the fact that the method and manner of
plant operation are unchanged.
The use of the proposed AVs does not
impact safe operation of the plant in that the
safety analysis limits are maintained. The
proposed change in AVs involves no system
additions. The AVs are revised to ensure the
affected instrumentation remains capable of
mitigating accidents and transients. Plant
equipment will not be operated in a manner
different from previous operation, except that
setpoints may be changed. No additional
failure mechanisms are introduced as a result
of the changes to the allowable values. Since
operational methods remain unchanged and
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the operating parameters were evaluated to
maintain the plant within existing design
basis criteria, no different type of failure or
accident is created.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed TS changes involve a change
in the surveillance testing intervals and
allowable values to facilitate a change in the
operating cycle length. The impact of these
changes on system availability is not
significant, based on other more frequent
testing that is performed, the existence of
redundant systems and equipment, and
overall system reliability. Evaluations have
shown there is no evidence of time
dependent failures that would impact the
availability of the systems. The proposed
changes do not significantly impact the
condition or performance of structures,
systems, and components relied upon for
accident mitigation. The proposed changes in
TS instrumentation allowable values are the
result of application of the RBS setpoint
methodology using plant specific drift
values. The revised allowable values more
accurately reflect total instrumentation loop
accuracy including drift while continuing to
protect any assumed analytical limit. The
proposed changes do not result in any
hardware changes or in any changes to the
analytical limits assumed in accident
analyses. Existing operating margin between
plant conditions and actual plant setpoints is
not significantly reduced due to these
changes. The proposed changes do not
significantly impact any safety analysis
assumptions or results.
Standby Liquid Control System
The proposed change in required weight of
Boron-10 in SLC is to facilitate a change in
the operating cycle length. The proposed
change does not result in any hardware
changes or in any changes to the analytical
limits assumed in accident analyses. Existing
operating margin between plant conditions
and actual plant setpoints is not reduced due
to this change. The proposed change does not
impact any safety analysis assumptions or
results. Therefore, the proposed change does
not involve a significant reduction in a
margin of safety.
Loss of Power Instrumentation
The proposed protection voltage AVs are
low enough to prevent inadvertent power
supply transfer, but high enough to ensure
that sufficient voltage is available to the
required equipment. The proposed change
does not involve a reduction in a margin of
safety. The proposed change was developed
using a methodology to ensure safety analysis
limits are not exceeded. As such, this
proposed change does not involve a
significant reduction in a margin of safety.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
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review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Terence A.
Burke, Associate General Counsel—
Nuclear Entergy Services, Inc., 1340
Echelon Parkway, Jackson, Mississippi
39213.
NRC Branch Chief: Michael T.
Markley.
Entergy Nuclear Operations, Inc.,
Docket No. 50–255, Palisades Nuclear
Plant, Van Buren County, Michigan
Date of amendment request: August
25, 2009.
Description of amendment request:
The proposed amendment would allow
for a one-time extension to the ten-year
frequency for the next Palisades Nuclear
Plant (PNP) containment Type A
integrated leak rate test (ILRT) that is
required by Technical Specification (TS)
5.5.14. The proposed change would
permit the existing ILRT frequency to be
extended from ten years to
approximately 11.25 years.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed exemption involves a onetime extension to the current interval for
Type A containment testing. The current test
interval of 120 months (10 years) would be
extended on a one-time basis to no longer
than approximately 135 months from the last
Type A test. The proposed extension does
not involve either a physical change to the
plant or a change in the manner in which the
plant is operated or controlled. The
containment is designed to provide an
essentially leak tight barrier against the
uncontrolled release of radioactivity to the
environment for postulated accidents. As
such, the containment and the testing
requirements invoked to periodically
demonstrate the integrity of the containment
exist to ensure the plant’s ability to mitigate
the consequences of an accident, and do not
involve the prevention or identification of
any precursors of an accident. Therefore, this
proposed extension does not involve a
significant increase in the probability of an
accident previously evaluated.
This proposed extension is for the Type A
containment leak rate tests only. The Type B
and C containment leak rate tests would
continue to be performed at the frequency
currently required by the PNP TS. As
documented in NUREG 1493, Type B and C
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tests have identified a very large percentage
of containment leakage paths and that the
percentage of containment leakage paths that
are detected only by Type A testing is very
small. The PNP Type A test history supports
this conclusion.
The integrity of the containment is subject
to two types of failure mechanisms that can
be categorized as (1) activity based and (2)
time based. Activity based failure
mechanisms are defined as degradation due
to system and/or component modifications or
maintenance. Local leak rate test
requirements and administrative controls
such as configuration management and
procedural requirements for system
restoration ensure that containment integrity
is not degraded by plant modifications or
maintenance activities. The design and
construction requirements of the
containment combined with the containment
inspections performed in accordance with
ASME Section XI, the Maintenance Rule, and
TS requirements serve to provide a high
degree of assurance that the containment
would not degrade in a manner that is
detectable only by a Type A test. Based on
the above, the proposed extension does not
involve a significant increase in the
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed revision to the TS involves
a one-time extension to the current interval
for Type A containment testing. The
containment and the testing requirements
invoked to periodically demonstrate the
integrity of the containment exist to ensure
the plant’s ability to mitigate the
consequences of an accident and do not
involve the prevention or identification of
any precursors of an accident. The proposed
TS change does not involve a physical
change to the plant or the manner in which
the plant is operated or controlled. Therefore,
the proposed TS change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change to the TS involves a
one-time extension to the current interval for
Type A containment testing. The proposed
TS change does not involve a physical
change to the plant or a change in the manner
in which the plant is operated or controlled.
The specific requirements and conditions of
the TS Containment Leak Rate Testing
Program exist to ensure that the degree of
containment structural integrity and leaktightness that is considered in the plant
safety analysis is maintained. The overall
containment leak rate limit specified by TS
is maintained. The proposed change involves
only the extension of the interval between
Type A containment leak rate tests. The
proposed surveillance interval extension is
bounded by the 15-month extension
currently authorized within NEI 94–01,
Revision 0. Type B and C containment leak
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rate tests would continue to be performed at
the frequency currently required by TS.
Industry experience supports the conclusion
that Type B and C testing detects a large
percentage of containment leakage paths and
that the percentage of containment leakage
paths that are detected only by Type A
testing is small. The containment inspections
performed in accordance with ASME Section
XI and the Maintenance Rule serve to
provide a high degree of assurance that the
containment would not degrade in a manner
that is detectable only by Type A testing. The
combination of these factors ensures that the
margin of safety in the plant safety analysis
is maintained. The design, operation, testing
methods and acceptance criteria for Type A,
B, and C containment leakage tests specified
in applicable codes and standards would
continue to be met, with the acceptance of
this proposed change, since these are not
affected by changes to the Type A test
interval. Therefore, the proposed TS change
does not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. William
Dennis, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 440
Hamilton Ave., White Plains, NY 10601.
NRC Acting Branch Chief: Peter Tam.
Entergy Nuclear Vermont Yankee, LLC
and Entergy Nuclear Operations, Inc.,
Docket No. 50–271, Vermont Yankee
Nuclear Power Station, Vernon,
Vermont
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Date of amendment request: August
26, 2009.
Description of amendment request:
The proposed amendment would revise
the Technical Specification (TS) Section
6.5 that governs administrative controls
of High Radiation Areas (HRA) to
incorporate the HRA administrative
controls contained within the Standard
Technical Specifications, NUREG–1433,
Revision 3.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
1. The operation of Vermont Yankee
Nuclear Power Station (VY) in accordance
with the proposed amendment will not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The proposed amendment does not impact
the operability of any structure, system or
component that affects the probability of an
accident or that supports mitigation of an
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accident previously evaluated. The proposed
amendment does not affect reactor operations
or accident analysis and has no radiological
consequences. The operability requirements
for accident mitigation systems remain
consistent with the licensing and design
basis. Therefore, the proposed amendment
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. The operation of VY in accordance with
the proposed amendment will not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
The proposed amendment does not change
the design or function of any component or
system. No new modes of failure or initiating
events are being introduced. Therefore,
operation of VY in accordance with the
proposed amendment will not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. The operation of VY in accordance with
the proposed amendment will not involve a
significant reduction in a margin of safety.
The proposed amendment does not change
the design or function of any component or
system. The proposed amendment does not
involve any safety limits, safety settings or
safety margins. The TS administrative access
controls for high radiation areas are being
replaced with those contained in section 5.7
of NUREG–1433 to provide additional
requirements and options for the control of
these areas.
Therefore, operation of VY in accordance
with the proposed amendment will not
involve a significant reduction in the margin
to safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. William C.
Dennis, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 400
Hamilton Avenue, White Plains, NY
10601.
NRC Branch Chief: Nancy Salgado.
Nine Mile Point Nuclear Station, LLC
(NMPNS) Docket No. 50–410, Nine Mile
Point Nuclear Station Unit No. 2 (NMP
2), Oswego County, New York
Date of amendment request: May 27,
2009, as supplemented on August 28,
2009.
Description of amendment request:
The proposed amendment requests an
increase in the maximum steady-state
power level at NMP2 from 3467
megawatts thermal (MWt) to 3988 MWt.
This represents a 15-percent increase
over the current licensed thermal
power.
Basis for proposed no significant
hazards consideration determination:
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As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. [Does the proposed amendment] involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
No, the increase in power level discussed
herein will not significantly increase the
probability or consequences of an accident
previously evaluated.
The proposed change will increase NMP2’s
authorized maximum power level from the
current licensed thermal power (CLTP) level
of 3467 megawatts thermal (MWt) to 3988
MWt. In support of this Constant Pressure
Extended Power Uprate (CPPU), a
comprehensive evaluation was performed for
nuclear steam supply system (NSSS) and
balance of plant (BOP) systems, structures,
components, and analyses that could be
affected by this change. The effect of
increasing the maximum power level from
the CLTP of 3467 MWt to 3988 MWt on the
NMP2 licensing and design bases was
evaluated. The result of this evaluation is
that all plant components, as modified, will
continue to be capable of performing their
design function at an uprated core power of
3988 MWt. In addition, an evaluation of the
accident analyses concludes that applicable
analysis acceptance criteria continue to be
met. Power level is an input assumption to
the equipment design and accident analyses,
but it is not an initiator for any transient or
accident. Therefore, no accident initiators are
affected by this uprate and no challenges to
any plant safety barriers are created by this
change.
Therefore, operation of the facility in
accordance with the proposed change does
not involve a significant increase in the
probability of an accident previously
evaluated.
This change does not affect the release
paths, the frequency of release, or the source
term for release for any accidents previously
evaluated in the Updated Safety Analysis
Report (USAR). Structures, systems, and
components (SSC) required to mitigate
transients remain capable of performing their
design functions, and thus were found
acceptable. The source terms used to assess
radiological consequences have been
reviewed and determined to bound operation
at the uprated condition. The results of EPU
[extended power uprate] accident evaluations
do not exceed the U. S. Nuclear Regulatory
Commission (NRC) approved acceptance
limits.
The spectrum of postulated accidents and
transients has been investigated and are
shown to meet the regulatory criteria to
which NMP2 is currently licensed. In the
area of fuel and core design, the Safety Limit
Minimum Critical Power ratio (SLMCPR) and
other applicable Specified Acceptable Fuel
Design Limits (SAFDLS) are still met.
Continued compliance with the SLMCPR and
other SAFDLs is confirmed on a cycle
specific basis consistent with criteria
accepted by the NRC.
Challenges to the reactor coolant pressure
boundary were evaluated at EPU conditions
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(pressure, temperature, flow, and radiation)
and found to meet the acceptance criteria for
allowable stresses. Adequate overpressure
margin is maintained.
Challenges to the containment have been
evaluated and the containment and its
associated cooling system continue to meet
applicable regulatory requirements. The
increase in the calculated post Loss of
Coolant Accident (LOCA) suppression pool
temperature above the current peak
temperature was evaluated and determined
to be acceptable.
Radiological release events (accidents)
have been evaluated and shown to meet the
requirements of 10 CFR 50.67.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. [Does the proposed amendment] create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
No, the increase in power level discussed
herein will not create the possibility of a new
or different kind of accident from any
accident previously evaluated.
The proposed change will increase NMP2’s
authorized maximum power level from the
CLTP level of 3467 MWt to 3988 MWt.
Equipment that could be affected by EPU has
been evaluated. No new operating mode,
safety-related equipment lineup, accident
scenario, or equipment failure mode was
identified. The full spectrum of accident
considerations has been evaluated and no
new or different kind of accident has been
identified. This Constant Pressure Extended
Power Uprate utilizes a standard evaluation
methodology applied to known technology
employed within the range of current or
modified plant capabilities. As such, the
plant safety-related equipment continues to
operate in accordance with regulatory
criteria. Evaluations were performed using
NRC approved codes, standards and
methods. No new accidents or event
precursors have been identified.
All structures, systems and components
previously required for the mitigation of a
transient remain capable of fulfilling their
intended design functions. The proposed
changes do not adversely affect safety-related
systems or components and do not challenge
the performance or integrity of any safetyrelated system. This change does not
adversely affect any current system interfaces
or create any new interfaces that could result
in an accident or malfunction of a different
kind than was previously evaluated.
Operating at a core power level of 3988 MWt
does not create any new accident initiators or
precursors.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. [Does the proposed amendment] involve
a significant reduction in a margin of safety?
No, the increase in power level discussed
herein will not involve a significant
reduction in a margin of safety.
Comprehensive analyses of the proposed
changes have concluded that relevant design
and safety acceptance criteria will be met
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without a significant reduction in margins of
safety. The analyses supporting EPU have
demonstrated that the NMP2 SSCs are
capable of safely performing at EPU
conditions. The analyses identified and
defined the major input parameters to the
NSSS, analyzed NSSS design transients, and
evaluated the capabilities of the NSSS fluid
systems, NSSS/BOP interfaces, NSSS control
systems, and NSSS and BOP components, as
appropriate. Radiological consequences of
design basis events remain within regulatory
limits and are not increased significantly.
The analyses confirmed that NSSS and BOP
SSCs are capable, some with modifications,
of achieving EPU conditions without
significant reduction in margins of safety.
Analyses have shown that the integrity of
primary fission product barriers will not be
significantly affected as a result of the power
increase. Calculated loads on SSCs important
to safety have been shown to remain within
design allowables under EPU conditions for
all design basis event categories. Plant
response to transients and accidents do not
result in exceeding acceptance criteria. As
appropriate, the evaluations that demonstrate
acceptability of EPU have been performed
using methods that have either been
reviewed and approved by the NRC staff, or
that are in compliance with regulatory review
guidance and standards established for
maintaining adequate margins of safety.
These evaluations demonstrate that there are
no significant reductions in the margins of
safety.
Maximum power level is one of the
inherent inputs that determine the safe
operating range defined by the accident
analyses. The Technical Specifications
ensure that NMP2 is operated within the
bounds of the inputs and assumptions used
in the accident analyses. The acceptance
criteria for the accident analyses are
conservative with respect to the operating
conditions defined by the Technical
Specifications. The engineering reviews
performed for the constant pressure extended
power uprate confirm that the accident
analyses criteria are met at the revised
maximum allowable thermal power level of
3988 MWt, as well as at the rated thermal
power (RTP) levels specified in the Facility
Operating License and Technical
Specifications. Therefore, the adequacy of the
revised Facility Operating Licenses and
Technical Specifications to maintain the
plant in a safe operating range is also
confirmed, and the increase in maximum
allowable power level does not involve a
significant decrease in a margin of safety.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mark J.
Wetterhahn, Esquire, Winston & Strawn,
PO 00000
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53779
1700 K Street, NW., Washington, DC
20006.
NRC Branch Chief: Nancy L. Salgado.
Nine Mile Point Nuclear Station, LLC
(NMPNS) Docket No. 50–410, Nine Mile
Point Nuclear Station Unit No. 2
(NMP2), Oswego County, New York
Date of amendment request: June 29,
2009, as supplemented on August 13,
2009.
Description of amendment request:
The proposed amendment would revise
the NMP2 Technical Specification (TS)
5.5.12 by replacing the reference to
Regulatory Guide (RG) 1.163 with a
reference to Nuclear Energy Institute
(NEI) Topical Report NEI 94–01,
Revision 2–A, as the implementation
document used by NMPNS to develop
the NMP2 performance-based leakage
testing program in accordance with
Option B of Title 10 of the Code of
Federal Regulations (10 CFR) Part 50.
The proposed amendment would allow
the next primary containment integrated
leak rate test (ILRT) to be performed
within 15 years from the last ILRT as
opposed to the current 10-year interval,
and would allow successive ILRTs to be
performed at 15-year intervals.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed amendment involves
changes to the NMP2 10 CFR 50 Appendix
J Testing Program Plan. The proposed
amendment does not involve a physical
change to the plant or a change in the manner
in which the plant is operated or controlled.
The primary containment function is to
provide an essentially leak tight barrier
against the uncontrolled release of
radioactivity to the environment for
postulated accidents. As such, the
containment itself and the testing
requirements to periodically demonstrate the
integrity of the containment exist to ensure
the plant’s ability to mitigate the
consequences of an accident, and do not
involve any accident precursors or initiators.
Therefore, the probability of occurrence of an
accident previously evaluated is not
significantly increased by the proposed
amendment.
The proposed amendment adopts the NRCaccepted guidelines of NEI 94–01, Revision 2,
for development of the NMP2 performancebased leakage testing program.
Implementation of these guidelines continues
to provide adequate assurance that during
design basis accidents, the primary
containment and its components will limit
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leakage rates to less [then] the values
assumed in the plant safety analyses. The
potential consequences of extending the ILRT
interval from 10 years to 15 years have been
evaluated by analyzing the resulting changes
in risk. The increase in risk in terms of
person-rem per year within 50 miles
resulting from design basis accidents was
estimated to be acceptably small, and the
increase in the large early release frequency
resulting from the proposed change was
determined to be within the guidelines
published in NRC RG 1.174. Additionally,
the proposed change maintains defense-indepth by preserving a reasonable balance
among prevention of core damage,
prevention of containment failure, and
consequence mitigation. NMPNS has
determined that the increase in conditional
containment failure probability due to the
proposed change would be very small.
Therefore, it is concluded that the proposed
amendment does not significantly increase
the consequences of an accident previously
evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed amendment adopts the NRCaccepted guidelines of NEI–94–01, Revision
2, for development of the NMP2
performance-based leakage testing program,
and establishes a 15 year interval for the
performance of the primary containment
ILRT. The containment and the testing
requirements to periodically demonstrate the
integrity of the containment exist to ensure
the plant’s ability to mitigate the
consequences of an accident, and do not
involve any accident precursors and
initiators. The proposed change does not
involve a physical change to the plant (i.e.,
no new or different type of equipment will
be installed) or a change to the manner in
which the plant is operated or controlled.
Therefore, the proposed amendment does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed amendment adopts the NRCaccepted guidelines of NEI–94–01, Revision
2, for development of the NMP2
performance-based leakage testing program,
and establishes a 15 year interval for the
performance of the primary containment
ILRT. The amendment does not alter the
manner in which safety limits, limiting safety
system setpoints, or limiting conditions for
operation are determined. The specific
requirements and conditions of the 10 CFR
50 Appendix J Testing Program Plan, as
defined in the TS, ensure that the degree of
primary containment structural integrity and
leak-tightness that is considered in the plant
safety analyses is maintained. The overall
containment leakage rate limit specified by
the TS is maintained, and the Type A, B, and
C containment leakage tests will continue to
be performed at the frequencies established
in accordance with the NRC-accepted
guidelines of NEI 94–01, Revision 2.
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Containment inspections performed in
accordance with other plant programs serve
to provide a high degree of assurance that the
containment will not degrade in a manner
that is detectable only by an ILRT. In
addition, the on-line containment monitoring
capability that is inherent to inerted boiling
water reactor containments allows for the
detection of gross containment leakage that
may develop during power operation. This
combination of factors ensures that evidence
of containment structural degradation is
identified in a timely manner. Furthermore,
a risk assessment using the current NMP2
Probabilistic Risk Assessment model
concluded that extending the ILRT test
interval from 10 years to 15 years results in
a very small change to the NMP2 risk profile.
Therefore, the proposed amendment does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mark J.
Wetterhahn, Esquire, Winston & Strawn,
1700 K Street, NW., Washington, DC
20006.
NRC Branch Chief: Nancy L. Salgado.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–348 and 50–364,
Joseph M. Farley Nuclear Plant, Units 1
and 2, Houston County, Alabama
Date of amendment request:
September 15, 2009.
Description of amendment request:
The proposed amendment revises
Technical Specification (TS) 3.3.2, in
Appendix A to Facility Operating
License Nos. NPF–2 and NPF–8 for the
Joseph M. Farley Nuclear Plant Units 1
and 2, respectively. P–11 is an
engineered safety feature actuation
system (ESFAS) permissive/interlock
which permits normal unit cooldown
and depressurization without actuation
of safety injection (SI) from low
pressurizer pressure. P–12 is an ESFAS
permissive/interlock which permits
normal unit cooldown and
depressurization without actuation of SI
and main steam line isolation on the
condition of low steam line pressure.
Both P–11 and P–12 circuits use input
from three protection channels. The
current wording of Condition K in TS
3.3.2 states, ‘‘Two channels inoperable.’’
As a result, Condition K does not
explicitly address the possible
conditions of one channel or three
channels inoperable, possibly creating a
literal compliance issue. The proposed
Condition K change from ‘‘Two
channels inoperable’’ to ‘‘One or more
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channels inoperable’’ will resolve the
current literal compliance issue. The
change does not alter the current
Condition K required action, it simply
clarifies that the required action must be
performed for one, two, or three P–11 or
P–12 channels inoperable. In addition,
an editorial change is proposed for TS
5.6.8 to correct the citation of a
condition requiring a report for the postaccident monitoring instrumentation.
The current TS 5.6.8 text states, ‘‘When
a report is required by Condition B or
G of LCO [limiting conditions for
operation] 3.3.3. * * *’’ The citation of
Condition B is correct while Condition
G does not currently exist for LCO 3.3.3;
instead TS 5.6.8 should cite Condition
F.
Basis for proposed no significant
hazards consideration determination:
As required by Title 10 of the Code of
Federal Regulations (10 CFR) 50.91(a),
the licensee has provided its analysis of
the issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change to TS 3.3.2 does not
significantly increase the probability or
consequences of an accident previously
evaluated in the FSAR. These interlocks do
not directly initiate an accident. The
consequences of accidents previously
evaluated in the FSAR are not adversely
affected by these changes because the
changes are made to reflect the Improved
Standard Technical Specifications and the
interlocks are verified to be in the required
state for the unit condition.
The proposed change to TS 5.6.8 corrects
an editorial error and therefore does not
significantly increase the probability or
consequences of a previously evaluated
accident.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change to TS 3.3.2 does not
create the possibility of a new or different
kind of accident than any accident already
evaluated in the FSAR. No new accident
scenario, failure mechanisms, or limiting
single failures are introduced as a result of
the proposed change. The proposed TS 3.3.2
change does not challenge the performance
or integrity of any safety-related systems.
Therefore, this change does not create the
possibility of a new or different kind of
accident from any accident previously
analyzed.
The proposed change to TS 5.6.8 corrects
an editorial error and therefore does not
create the possibility of a new or different
kind of accident from any accident
previously analyzed.
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3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed change to TS 3.3.2 does not
involve a significant reduction in a margin of
safety. The proposed change is made to
accurately reflect the format of the Improved
Standard Technical Specifications. The
actuation setpoints specified by the
Technical Specifications and safety analysis
limits assumed in the accident analysis are
unchanged. The margin of safety associated
with these trip setpoints and the safety
analysis acceptance criteria is unchanged.
Therefore, the proposed change to TS 3.3.2
will not significantly reduce the margin of
safety as defined in the Technical
Specifications.
The proposed change to TS 5.6.8 corrects
an editorial error and therefore involves no
significant reduction in a margin of safety.
Based on the above, SNC concludes that
the proposed amendment does not involve a
significant hazards consideration under the
standards set forth in 10 CFR 50.92(c), and,
accordingly, a finding of ‘‘no significant
hazards consideration’’ is justified.
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The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M. Stanford
Blanton, Esq., Balch and Bingham, Post
Office Box 306, 1710 Sixth Avenue
North, Birmingham, Alabama 35201.
NRC Branch Chief: Jon H. Thompson,
Acting.
Tennessee Valley Authority (TVA),
Docket Nos. 50–259, 50–260 and 50–
296, Browns Ferry Nuclear Plant, Units
1, 2 and 3, Limestone County, Alabama
Date of amendment request: July 27,
2009 (TS–465).
Description of amendment request:
The proposed change is to eliminate
Technical Specification (TS)
surveillance requirement (SR) 3.6.1.3.11
and the requirement to perform water
leak rate testing on the listed
containment isolation valves. More
specifically, the proposed change
eliminates water local leak rate testing
of valves in the Containment Leak Rate
Program that are being tested to verify
the combined leakage rate is within the
limit that ensures the suppression pool
level is sufficient to keep lines that
terminate below the water level for at
least 30 days without additional makeup.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration.
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1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
This proposal does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
The proposed change to the scope of water
leak rate testing for the subject valves does
not affect the probability of the design basis
accidents. The valves will continue to be
maintained in an operable state, and in their
current design configuration. There is no
correlation between the scope of the water
leak rate testing and accident probability.
TVA reviewed the postulated
consequences of design basis events on
primary containment isolation under the
proposed change. The primary containment
structure, including access openings,
penetrations and the containment heat
removal system, is designed so that the
containment structure and its internal
compartments can withstand, without
exceeding the design leakage rate (2.0% per
day), the peak accident pressure and
temperature that could occur during any
postulated LOCA [loss-of-coolant accident].
For the purposes of considering the
consequences of LOCAs under the proposed
change, a single active failure of a CIV
[containment isolation valve] or a passive
failure of the closed system were reviewed,
within the limits of the existing licensing
basis. Under the existing licensing basis, a
pipe rupture of seismically qualified ECCS
[emergency core cooling system] piping does
not have to be assumed concurrent with the
LOCA, except if it is a consequence of the
LOCA. Consequential failures can be
eliminated, since a LOCA inside containment
is separated from the ECCS piping by the
containment structure. Consequential failures
of the ECCS piping from LOCA’s outside
containment are outside the Appendix J
design considerations, although they are
adequately addressed through the
redundancy and separation of the ECCS
design. A single active failure of the CIV,
under the LOCA condition, can be
accommodated since the closed and filled
system piping and the suppression pool
water inventory remain as the leakage
barriers. The ECCS passive failure criterion
does require consideration of system leaks,
but not pipe breaks, beyond the initiating
LOCA. Pipe leakage, equivalent to the
leakage from a valve or pump seal failure,
should be considered at 24 hours or greater
post-LOCA. The capability to make-up
inventory to the suppression pool is adequate
to ensure that postulated seat leakage and
pipe leakage does not result in a condition
that jeopardizes pool level. Make-up
capability exists to the suppression pool.
Actions to make-up to the suppression pool
are delineated in Emergency Operating
Instructions.
Therefore, the proposal to eliminate the
subject water leak rate tests does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
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accident from any accident previously
evaluated?
This proposal does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
The acceptability of the proposed change
to the scope of water leak rate testing for the
subject valves is based on maintaining the
existing barriers to primary containment
leakage, and ensuring that the suppression
pool level is assured for 30 days during all
design basis, post-accident modes of
operation. By meeting these dual objectives,
the plant response to the design basis events
will be unchanged, and no new accident
scenarios will be encountered. These two
objectives are related, in that, the
suppression pool inventory creates a passive
barrier to primary containment atmospheric
leakage for valves associated with
penetrations which are located below the
minimum water level of the pool.
The proposed Technical Specification
change does not alter the configuration of the
subject containment isolation valves or their
associated systems. The valves will continue
to be tested and maintained to ensure their
operability. The subject valves are all
isolation valves associated with lines that
penetrate the primary containment. For
closed system valves, the redundant isolation
boundary for each of the affected valves is
the closed system associated with the valve.
The closed system piping is verified via a 10
CFR 50 Appendix J Type A test. The integrity
of the closed systems is also monitored and
controlled via Technical Specification 5.5.2,
‘‘Primary Coolant Sources Outside
Containment.’’
The subject valves may be open, or change
state, post-accident to support the design
function of their associated ECCS systems
(HPCI [high-pressure coolant injection], Core
Spray, RHR [residual heat removal]), RCIC
[reactor core isolation coolant] or RHR
Sampling using the Post Accident Sampling
System. The subject valves function as
system valves during the periods when they
are open or in an intermediate state, not as
containment isolation valves. Reliance is
placed on the suppression pool seal and the
closed system piping to maintain the barrier
between primary and secondary containment
atmospheres.
Therefore, with the valve configuration and
closed systems configuration unaffected by
the proposed change, the existing barriers to
primary containment atmospheric leakage are
maintained, so long as the suppression pool
level is ensured.
The suppression pool is designed and
operated so that it is filled with water in
accordance with Technical Specifications
3.6.2.2, ‘‘Suppression Pool Water Level,’’ and
the associated Bases. As such, the supply of
water in the suppression pool is assured for
30 days during all design basis, post-accident
modes of operation. Water leak rate testing
has historically been performed on valves
associated with lines that connect to the
suppression pool. The acceptance criteria for
combined leakage from these penetrations is
72.79 cfh [cubic feet per hour]. This leakage
rate is at a level which ensures the 30-day
post-accident suppression pool level.
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As mentioned above, the integrity of the
closed system piping is verified via a 10 CFR
50 Appendix J Type A test and is monitored
and controlled via Technical Specification
5.5.2. TS 5.5.2 establishes a program to
monitor and control leakage from systems
located outside containment that could
contain highly radioactive fluids during a
serious transient or accident. This program
applies to the ECCS and RCIC systems
affected by the proposed change and ensures
that leakage into secondary containment via
packing, flanges, seals, etc., is controlled.
Leakage from these systems has been found
to be very low, and well below the 20 gpm
[gallons per minute] limit established for
these systems. The proposed change is not
expected to contribute to higher levels of
system leakage. Normal operational
monitoring of suppression pool level,
operator rounds, housekeeping inspections,
and system pressure testing further ensure
external leakage is identified and minimized
while suppression pool level is being
maintained.
A review of water leak rate test data for the
subject CIVs showed that the valves have had
leakage rates within the acceptance criteria.
Testing of the valves in accordance with
ASME [American Society of Mechanical
Engineers] Code requirements ensure valve
operability.
Therefore, leakage past the CIVs is
expected to be low and in keeping with the
design basis for the suppression pool.
However, the capability does exist to makeup water to the suppression pool if
necessary. Existing Emergency Operating
Instructions require actions if suppression
pool level is less than the required level.
Thus, the level of the suppression pool is
ensured, independent of the current CIV
water leak rate testing requirement.
The proposed change to the scope of water
leak rate testing for the subject valves
maintains the existing barriers to primary
containment leakage, and ensures that the
suppression pool level is assured for 30 days
during all design basis, post-accident modes
of operation. Therefore, the plant response to
the design basis events is unchanged, and the
proposal does not create the possibility of a
new or different kind of accident from any
accident previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
This change does not involve a significant
reduction in a margin of safety.
As discussed in the responses to questions
1 and 2, the proposed change does not alter
the plant response to existing accident
scenarios, and does not introduce new or
different scenarios. So the margin of safety
from a design basis accident standpoint is
maintained.
Historically, the leakage rate through the
subject valves has been determined in
accordance with TS SR 3.6.1.3.11. This
leakage rate has always been within the
acceptance criteria. Quantifying leakage past
the CIVs has been used to ensure that the
suppression pool level is assured for 30 days
post-accident. Under the proposed change,
this leakage rate will not be quantified. In
addition, closed system leakage is monitored
and controlled by an existing Technical
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Specification program. Closed system leakage
has been found to be very low on each of the
units, and is currently well below the 20 gpm
allowable. Therefore, leakage past the CIVs is
expected to be low and in keeping with the
design basis for the suppression pool.
However, the capability does exist, and is
proceduralized, to make-up water to the
suppression pool if necessary. Thus the
current capability to maintain adequate
suppression pool level for 30 days postaccident is assured under the proposed
change.
Therefore the proposed change to the scope
of water leak rate testing for the subject
valves does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Thomas H. Boyce.
Previously Published Notices of
Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The following notices were previously
published as separate individual
notices. The notice content was the
same as above. They were published as
individual notices either because time
did not allow the Commission to wait
for this biweekly notice or because the
action involved exigent circumstances.
They are repeated here because the
biweekly notice lists all amendments
issued or proposed to be issued
involving no significant hazards
consideration.
For details, see the individual notice
in the Federal Register on the day and
page cited. This notice does not extend
the notice period of the original notice.
Florida Power and Light Company,
Docket Nos. 50–250 and 251, Turkey
Point Plant Units 3, and 4, Miami-Dade
County, Florida
Date of application for amendment:
September 1, 2009.
Description of amendment request:
Delay the date specified in License
Amendments 234 and 229 for the
implementation of the Boraflex Remedy
in the spent fuel pools.
Date of publication of individual
notice in the Federal Register:
September 15, 2009 (74 FR 47278).
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Expiration date of individual notice:
October 15, 2009 (Public comments) and
November 16, 2009 (Hearing requests).
Florida Power and Light Company,
Docket Nos. 50–250 and 50–251, Turkey
Point Plant, Units 3 and 4, Miami-Dade
County, Florida
Date of application for amendments:
July 23, 2009.
Description of amendments request:
Revise the scope of the inservice
inspections required in the tubesheet
regions of the steam generators.
Date of publication of individual
notice in the1 Federal Register:
August 28, 2009 (74 FR 44405).
Expiration date of individual notice:
September 28, 2009 (Public comments)
and October 27, 2009 (Hearing requests).
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.22(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) The applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
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North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
System (ADAMS) Public Electronic
Reading Room on the internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr.resource@nrc.gov.
Arizona Public Service Company, et al.,
Docket Nos. STN 50–528, STN 50–529,
and STN 50–530, Palo Verde Nuclear
Generating Station, Unit Nos. 1, 2, and
3, Maricopa County, Arizona
Date of application for amendment:
May 28, 2009, as supplemented by letter
dated August 3, 2009.
Brief description of amendment: The
amendments eliminated working hour
restrictions from Technical
Specification (TS) 5.2.2 for Palo Verde
Nuclear Generating Station, Units 1, 2,
and 3, to support compliance with the
revisions to Title 10 of the Code of
Federal Regulations (10 CFR), Part 26,
‘‘Fitness for Duty Programs,’’ that
became effective on March 31, 2008.
The changes are consistent with the
NRC-approved Technical Specification
Task Force (TSTF) Standard Technical
Specification change traveler, TSTF–
511, Revision 0, ‘‘Eliminate Working
Hour Restrictions from TS 5.2.2 to
Support Compliance with 10 CFR part
26.’’
Date of issuance: September 30, 2009.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment No.: Unit 1–175; Unit 2–
175; Unit 3–175.
Facility Operating License Nos. NPF–
41, NPF–51, and NPF–74: The
amendments revised the Operating
Licenses and Technical Specifications.
Date of initial notice in Federal
Register: July 28, 2009 (74 FR 37247).
The supplemental letter dated August 3,
2009, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the NRC staff’s original proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 30,
2009.
No significant hazards consideration
comments received: No.
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Calvert Cliffs Nuclear Power Plant, Inc.,
Docket Nos. 50–317 and 50–318, Calvert
Cliffs Nuclear Power Plant, Unit Nos. 1
and 2, Calvert County, Maryland
Date of application for amendments:
May 13, 2009.
Brief description of amendments: The
amendments revise Technical
Specification (TS) 5.5.8, ‘‘Inservice
Testing Program,’’ by incorporating TS
Task Force Traveler (TSTF) 479,
‘‘Changes to Reflect Revision of 10 CFR
[Title 10 of the Code of Federal
Regulations] 50.55a,’’ and TSTF–497,
‘‘Limit Inservice Testing Program SR
[Surveillance Requirement] 3.0.2
Application to Frequencies of 2 Years or
Less.’’ Specifically, the amendments (1)
replace references to the American
Society of Mechanical Engineers
(ASME) Boiler and Pressure Vessel
Code, Section XI with the ASME Code
for Operation and Maintenance of
Nuclear Power Plants for inservice
testing activities, and (2) applies the
extension allowance of SR 3.0.2 to other
normal and accelerated inservice testing
frequencies of 2 years or less that were
not included in the frequencies of the
table listed in TS 5.5.8.a.
Date of issuance: September 28, 2009.
Effective date: As of the date of
issuance to be implemented within 60
days.
Amendment Nos.: 294 and 270.
Renewed Facility Operating License
Nos. DPR–53 and DPR–69: Amendments
revised the License and Technical
Specifications.
Date of initial notice in Federal
Register: July 14, 2009 (74 FR 34046).
The Commission’s related evaluation of
these amendments is contained in a
Safety Evaluation dated September 28,
2009.
No significant hazards consideration
comments received: No.
Entergy Gulf States Louisiana, LLC, and
Entergy Operations, Inc., Docket No. 50–
458, River Bend Station, Unit 1, West
Feliciana Parish, Louisiana
Date of amendment request:
November 20, 2008, as supplemented by
letter dated August 12, 2009.
Brief description of amendment: The
amendment revised Technical
Specification 5.6.5, ‘‘Core Operating
Limits Report (COLR),’’ to add a
reference to an analytical method that
will be used to determine the core
operating limits. The change is needed
to support the use of GE14 fuel during
refueling outage 15 scheduled for the
fall of 2009.
Date of issuance: September 29, 2009.
Effective date: As of the date of
issuance and shall be implemented
prior to Cycle 16 operation.
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53783
Amendment No.: 166.
Facility Operating License No. NPF–
47: The amendment revised the Facility
Operating License and Technical
Specifications.
Date of initial notice in Federal
Register: January 23, 2009 (74 FR
4249). The supplemental letter dated
August 12, 2009, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 29,
2009.
No significant hazards consideration
comments received: No.
Entergy Operations, Inc., Docket No. 50–
382, Waterford Steam Electric Station,
Unit 3, St. Charles Parish, Louisiana
Date of amendment request:
September 17, 2008, as supplemented
by letters dated February 26, June 30,
and September 24, 2009.
Brief description of amendment: The
amendment revised the Waterford 3
Technical Specifications (TSs) to take
credit for soluble boron in Region 1
(cask storage pit) and Region 2 (spent
fuel pool and refueling canal) fuel
storage racks for the storage of both
Standard and Next Generation Fuel
assemblies. Two new TSs were added
which included a surveillance that
ensures the required boron
concentration is maintained in the spent
fuel storage racks and to reflect the
results of the new criticality analysis.
Date of issuance: September 30, 2009.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment No.: 223.
Facility Operating License No. NPF–
38: The amendment revised the Facility
Operating License and Technical
Specifications.
Date of initial notice in Federal
Register: April 14, 2009 (74 FR 17228).
The application dated September 17,
2008, contained an evaluation of the TS
change in accordance with 10 CFR
50.91(a)(1) using criteria in 10 CFR
50.92(c), and the licensee determined
that the change involved no significant
hazards consideration (NSHC).
However, based on the discussions
between the staff and the licensee, the
licensee provided a revised NSHC in its
supplemental letter dated February 26,
2009. Based on the February 26, 2009,
revised NSHC, the staff’s proposed
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NSHC determination was published in
the Federal Register on April 14, 2009.
The supplemental letters dated June 30
and September 24, 2009, provided
additional information that clarified the
application, did not expand the scope of
the application as noticed, and did not
change the staff’s proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 30,
2009.
No significant hazards consideration
comments received: No.
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FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–412,
Beaver Valley Power Station, Unit No. 2,
Beaver County, Pennsylvania
Date of application for amendment:
October 10, 2008, as supplemented by
letters dated. June 16 and July 14, 2009.
Brief description of amendment: The
amendment revises Technical
Specification (TS) 5.5.5 to allow an
additional method of repair for steam
generator (SG) tubes by installation of
leak limiting Alloy 800 sleeves
developed by Westinghouse and
clarifies an existing reporting
requirement in TS 5.6.6.2.4 concerning
SG tube inspections.
Date of issuance: September 30, 2009.
Effective date: As of the date of
issuance and shall be implemented
prior to achieving Mode 4 during
startup from the fall 2009 refueling
outage.
Amendment No: 170
Facility Operating License No. NPF–
73. Amendment revised the License and
TSs.
Date of initial notice in Federal
Register: February 17, 2009 (74 FR
7482). The June 16 and July 14, 2009,
supplemental letters provided clarifying
information that was within the scope of
the initial notice and did not change the
initial proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 30,
2009.
No significant hazards consideration
comments received: No.
Northern States Power Company—
Minnesota, LLC, Docket No. 50–263,
Monticello Nuclear Generating Plant,
Wright County, Minnesota
Date of application for amendment:
May 29, 2009.
Brief description of amendment: The
amendment changes the Technical
Specifications, revising the applicability
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14:46 Oct 19, 2009
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for isolation of the Reactor Water
Cleanup System on a Standby Liquid
Control system initiation to align with
the modes stated in Specification 3.1.7.
Date of issuance: September 28, 2009.
Effective date: As of the date of
issuance and shall be implemented
within 90 days of issuance.
Amendment No.: 164.
Facility Operating License No. DPR–
22. Amendment revised the Facility
Operating License and the Technical
Specifications.
Date of initial notice in Federal
Register: July 28, 2009 (74 FR 37248).
The Commission’s related evaluation of
the amendment is contained in a Safety
Evaluation dated September 28, 2009.
No significant hazards consideration
comments received: No.
Southern Nuclear Operating Company,
Inc., Georgia Power Company,
Oglethorpe Power Corporation,
Municipal Electric Authority of Georgia,
City of Dalton, Georgia, Docket Nos. 50–
424 and 50–425, Vogtle Electric
Generating Plant, Units 1 and 2, Burke
County, Georgia
Date of application for amendments:
May 19, 2009, as supplemented August
28, 2009 (three submittals) and
September 11, 2009.
Brief description of amendments: The
amendments revised TS 5.5.9, ‘‘Steam
Generator (SG) Program,’’ to exclude
portions of the tubes within the
tubesheet from periodic SG inspections
(establish alternate repair criteria). The
amendments also revised TS 5.6.10,
‘‘Steam Generator Tube Inspection
Report,’’ to remove reference to previous
interim alternate repair criteria and
provide specific reporting requirements
for Unit 1 during refueling outage (RFO)
15 and the subsequent operating cycle,
and for Unit 2 during RFO 14 and the
subsequent operating cycle.
Date of issuance: September 24, 2009.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 157 and 138.
Renewed Facility Operating License
Nos. NPF–68 and NPF–81: Amendments
revised the licenses and the technical
specifications.
Date of initial notice in Federal
Register: June 18, 2009 (74 FR 28962).
The supplements dated August 28,
2009, and September 11, 2009, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination.
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The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 24,
2009.
No significant hazards consideration
comments received: No.
Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of application for amendment:
May 4, 2009.
Brief description of amendment: The
amendment revised the Callaway Plant
Technical Specification (TS) 5.2.2,
‘‘Unit Staff,’’ to eliminate working hour
restrictions in paragraph d of TS 5.2.2
to support compliance with Title 10 of
the Code of Federal Regulations (10
CFR) Part 26. The change is consistent
with U.S. Nuclear Regulatory
Commission (NRC)-approved Revision 0
to TS Task Force (TSTF) Improved
Technical Specification change traveler,
TSTF–511, ‘‘Eliminate Working Hour
Restrictions from TS 5.2.2 to Support
Compliance with 10 CFR Part 26.’’ The
availability of this TS improvement was
announced in the Federal Register on
December 30, 2008 (73 FR 79923), as
part of the consolidated line item
improvement process.
Date of issuance: September 29, 2009.
Effective date: As of its date of
issuance and shall be implemented by
October 1, 2009.
Amendment No.: 193.
Facility Operating License No. NPF–
30: The amendment revised the
Operating License and Technical
Specifications.
Date of initial notice in Federal
Register: July 28, 2009 (74 FR 37250).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 29,
2009.
Date of initial notice in Federal
Register: July 28, 2009 (74 FR 37250).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 29,
2009.
No significant hazards consideration
comments received: No.
Dated at Rockville, Maryland, this 8th day
of October 2009.
For the Nuclear Regulatory Commission.
Joseph G. Giitter,
Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. E9–24915 Filed 10–19–09; 8:45 am]
BILLING CODE 7590–01–P
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Agencies
[Federal Register Volume 74, Number 201 (Tuesday, October 20, 2009)]
[Notices]
[Pages 53774-53784]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: E9-24915]
[[Page 53774]]
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NUCLEAR REGULATORY COMMISSION
[NRC-2009-0456]
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC) is publishing this regular biweekly notice. The Act
requires the Commission publish notice of any amendments issued, or
proposed to be issued and grants the Commission the authority to issue
and make immediately effective any amendment to an operating license
upon a determination by the Commission that such amendment involves no
significant hazards consideration, notwithstanding the pendency before
the Commission of a request for a hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from September 24, 2009, to October 7, 2009. The
last biweekly notice was published on October 6, 2009 (74 FR 51327).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in Title 10 of the Code of Federal
Regulations (10 CFR), Section 50.92, this means that operation of the
facility in accordance with the proposed amendment would not (1)
Involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rulemaking
and Directives Branch (RDB), TWB-05-B01M, Division of Administrative
Services, Office of Administration, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, and should cite the publication date and
page number of this Federal Register notice. Written comments may also
be faxed to the RDB at 301-492-3446. Documents may be examined, and/or
copied for a fee, at the NRC's Public Document Room (PDR), located at
One White Flint North, Public File Area O1F21, 11555 Rockville Pike
(first floor), Rockville, Maryland.
Within 60 days after the date of publication of this notice, any
person(s) whose interest may be affected by this action may file a
request for a hearing and a petition to intervene with respect to
issuance of the amendment to the subject facility operating license.
Requests for a hearing and a petition for leave to intervene shall be
filed in accordance with the Commission's ``Rules of Practice for
Domestic Licensing Proceedings'' in 10 CFR part 2. Interested person(s)
should consult a current copy of 10 CFR 2.309, which is available at
the Commission's PDR, located at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed by the above date, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also identify the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to
[[Page 53775]]
participate fully in the conduct of the hearing.
If a hearing is requested, the Commission will make a final
determination on the issue of no significant hazards consideration. The
final determination will serve to decide when the hearing is held. If
the final determination is that the amendment request involves no
significant hazards consideration, the Commission may issue the
amendment and make it immediately effective, notwithstanding the
request for a hearing. Any hearing held would take place after issuance
of the amendment. If the final determination is that the amendment
request involves a significant hazards consideration, any hearing held
would take place before the issuance of any amendment.
All documents filed in NRC adjudicatory proceedings, including a
request for hearing, a petition for leave to intervene, any motion or
other document filed in the proceeding prior to the submission of a
request for hearing or petition to intervene, and documents filed by
interested governmental entities participating under 10 CFR 2.315(c),
must be filed in accordance with the NRC E-Filing rule, which the NRC
promulgated in August 28, 2007 (72 FR 49139). The E-Filing process
requires participants to submit and serve all adjudicatory documents
over the internet, or in some cases to mail copies on electronic
storage media. Participants may not submit paper copies of their
filings unless they seek an exemption in accordance with the procedures
described below.
To comply with the procedural requirements of E-Filing, at least
ten (10) days prior to the filing deadline, the petitioner/requestor
should contact the Office of the Secretary by e-mail at
hearing.docket@nrc.gov, or by calling (301) 415-1677, to request (1) a
digital ID certificate, which allows the participant (or its counsel or
representative) to digitally sign documents and access the E-Submittal
server for any proceeding in which it is participating; and/or (2)
creation of an electronic docket for the proceeding (even in instances
in which the petitioner/requestor (or its counsel or representative)
already holds an NRC-issued digital ID certificate). Each petitioner/
requestor will need to download the Workplace Forms ViewerTM
to access the Electronic Information Exchange (EIE), a component of the
E-Filing system. The Workplace Forms ViewerTM is free and is
available at https://www.nrc.gov/site-help/e-submittals/install-viewer.html. Information about applying for a digital ID certificate is
available on NRC's public Web site at https://www.nrc.gov/site-help/e-submittals/apply-certificates.html.
Once a petitioner/requestor has obtained a digital ID certificate,
had a docket created, and downloaded the EIE viewer, it can then submit
a request for hearing or petition for leave to intervene. Submissions
should be in Portable Document Format (PDF) in accordance with NRC
guidance available on the NRC public Web site at https://www.nrc.gov/site-help/e-submittals.html. A filing is considered complete at the
time the filer submits its documents through EIE. To be timely, an
electronic filing must be submitted to the EIE system no later than
11:59 p.m. Eastern Time on the due date. Upon receipt of a
transmission, the E-Filing system time-stamps the document and sends
the submitter an e-mail notice confirming receipt of the document. The
EIE system also distributes an e-mail notice that provides access to
the document to the NRC Office of the General Counsel and any others
who have advised the Office of the Secretary that they wish to
participate in the proceeding, so that the filer need not serve the
documents on those participants separately. Therefore, applicants and
other participants (or their counsel or representative) must apply for
and receive a digital ID certificate before a hearing request/petition
to intervene is filed so that they can obtain access to the document
via the E-Filing system.
A person filing electronically using the agency's adjudicatory e-
filing system may seek assistance through the ``Contact Us'' link
located on the NRC Web site at https://www.nrc.gov/site-help/e-submittals.html or by calling the NRC Meta-System Help Desk, which is
available between 8 a.m. and 8 p.m., Eastern Time, Monday through
Friday, excluding government holidays. The Meta-System Help Desk can be
contacted by telephone at 1-866-672-7640 or by e-mail at
MSHD.Resource@nrc.gov.
Participants who believe that they have a good cause for not
submitting documents electronically must file an exemption request, in
accordance with 10 CFR 2.302(g), with their initial paper filing
requesting authorization to continue to submit documents in paper
format. Such filings must be submitted by: (1) First class mail
addressed to the Office of the Secretary of the Commission, U.S.
Nuclear Regulatory Commission, Washington, DC 20555-0001, Attention:
Rulemaking and Adjudications Staff; or (2) courier, express mail, or
expedited delivery service to the Office of the Secretary, Sixteenth
Floor, One White Flint North, 11555 Rockville Pike, Rockville,
Maryland, 20852, Attention: Rulemaking and Adjudications Staff.
Participants filing a document in this manner are responsible for
serving the document on all other participants. Filing is considered
complete by first-class mail as of the time of deposit in the mail, or
by courier, express mail, or expedited delivery service upon depositing
the document with the provider of the service.
Non-timely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission, the presiding
officer, or the Atomic Safety and Licensing Board that the request and/
or petition should be granted and/or the contentions should be
admitted, based on a balancing of the factors specified in 10 CFR
2.309(c)(1)(i)-(viii).
Documents submitted in adjudicatory proceedings will appear in
NRC's electronic hearing docket which is available to the public at
https://ehd.nrc.gov/EHD_Proceeding/home.asp, unless excluded pursuant
to an order of the Commission, an Atomic Safety and Licensing Board, or
a Presiding Officer. Participants are requested not to include personal
privacy information, such as social security numbers, home addresses,
or home phone numbers in their filings, unless an NRC regulation or
other law requires submission of such information. With respect to
copyrighted works, except for limited excerpts that serve the purpose
of the adjudicatory filings and would constitute a Fair Use
application, participants are requested not to include copyrighted
materials in their submissions.
For further details with respect to this license amendment
application, see the application for amendment which is available for
public inspection at the Commission's PDR, located at One White Flint
North, Public File Area O1F21, 11555 Rockville Pike (first floor),
Rockville, Maryland. Publicly available records will be accessible from
the ADAMS Public Electronic Reading Room on the Internet at the NRC Web
site, https://www.nrc.gov/reading-rm/adams.html. Persons who do not have
access to ADAMS or who encounter problems in accessing the documents
located in ADAMS, should contact the NRC PDR Reference staff at 1-800-
397-4209, 301-415-4737, or by e-mail to pdr.resource@nrc.gov.
[[Page 53776]]
Entergy Gulf States Louisiana, LLC, and Entergy Operations, Inc.,
Docket No. 50-458, River Bend Station (RBS), Unit 1, West Feliciana
Parish, Louisiana
Date of amendment request: August 10, 2009.
Description of amendment request: The proposed amendment would
revise the RBS Technical Specifications (TSs) to support operation with
24-month fuel cycles. Specifically, the change addresses certain TS
Surveillance Requirement (SR) frequencies that are specified as ``18
months'' by revising them to ``24 months'' in accordance with the
guidance of U.S. Nuclear Regulatory Commission (NRC) Generic Letter 91-
04, ``Changes in Technical Specification Surveillance Intervals to
Accommodate a 24-Month Fuel Cycle,'' dated April 2, 1991.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed TS changes involve a change in the surveillance
testing intervals and allowable values to facilitate a change in the
operating cycle length. The proposed TS changes do not physically
impact the plant. The proposed TS changes do not degrade the
performance of, or increase the challenges to, any safety systems
assumed to function in the accident analysis. The proposed TS
changes do not impact the usefulness of the SRs in evaluating the
operability of required systems and components, or the way in which
the surveillances are performed. In addition, the frequency of
surveillance testing is not considered an initiator of any analyzed
accident, nor does a revision to the frequency introduce any
accident initiators. The specific value of the allowable value is
not considered an initiator of any analyzed accident. Therefore, the
proposed change does not involve a significant increase in the
probability of an accident previously evaluated.
The consequences of a previously evaluated accident are not
significantly increased. The proposed change does not affect the
performance of any equipment credited to mitigate the radiological
consequences of an accident. Evaluation of the proposed TS changes
demonstrated that the availability of credited equipment is not
significantly affected because of other more frequent testing that
is performed, the availability of redundant systems and equipment,
and the high reliability of the equipment. Historical review of
surveillance test results and associated maintenance records did not
find evidence of failures that would invalidate the above
conclusions.
The allowable values have been developed in accordance with [NRC
Regulatory Guide] 1.105, ``Instrument Setpoints,'' to ensure that
the design and safety analysis limits are satisfied. The methodology
used for the development of the allowable values ensures the
affected instrumentation remains capable of mitigating design basis
events as described in the safety analyses and that the results and
radiological consequences described in the safety analyses remain
bounding. Therefore, the proposed change does not alter the ability
to detect and mitigate events and, as such, does not involve a
significant increase in the consequences of an accident previously
evaluated.
Standby Liquid Control System
The proposed change in required weight of Boron-10 in [standby
liquid control (SLC)] does not physically impact the plant, nor does
it degrade the performance of, or increase the challenges to, any
safety systems assumed to function in the accident analysis. The
consequences of a previously evaluated accident are not increased.
The proposed change does not affect the performance of any equipment
credited to mitigate the radiological consequences of an accident.
Evaluation of the proposed TS changes demonstrated that the
availability of credited equipment is not affected. Therefore, the
proposed change does not alter the ability to detect and mitigate
events and, as such, does not involve a significant increase in the
consequences of an accident previously evaluated.
Loss of Power Instrumentation
A change to the Allowable Values (AVs) is proposed for Table
3.3.8.1-1, Item 1.c and Item 2.c. The proposed change is the result
of application of the RBS Instrument Setpoint Methodology using
plant-specific drift values and incorporating margins available
based on a revised off-site reliability study. Application of this
methodology results in AVs that more accurately reflect total device
accuracy, as well as that of test equipment and calculated drift
between surveillances. The proposed change will not result in any
hardware changes. The instrumentation is not assumed to be an
initiator of any analyzed event. Existing operating margin between
plant conditions and actual plant setpoints is not significantly
reduced due to the proposed changes. The role of the instrumentation
is in mitigating and thereby, limiting the consequences of
accidents.
The AVs were developed to ensure the design and safety analysis
limits are satisfied. The methodology used for the development of
the AVs ensures that: (1) The affected instrumentation remains
capable of mitigating design basis events as described in the safety
analysis, and (2) the results and radiological consequences
described in the safety analysis remain bounding. Additionally, the
proposed change does not alter the plant's ability to detect and
mitigate events. Therefore, this change does not involve a
significant increase in the probability or consequences of an
accident previously evaluated.
The change in the degraded voltage protection voltage AVs allows
the protection scheme to function as originally designed. The
proposed allowable values ensure that the Class 1E distribution
system remains connected to the offsite power system when adequate
offsite voltage is available and motor starting transients are
considered.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed TS changes involve a change in the surveillance
testing intervals and allowable values to facilitate a change in the
operating cycle length. The proposed TS changes do not introduce any
failure mechanisms of a different type than those previously
evaluated, since there are no physical changes being made to the
facility. No new or different equipment is being installed. No
installed equipment is being operated in a different manner. As a
result, no new failure modes are being introduced. The way
surveillance tests are performed remains unchanged. A historical
review of surveillance test results and associated maintenance
records indicated there was no evidence of any failures that would
invalidate the above conclusions.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
Standby Liquid Control System
The proposed change to the required weight of Boron-10 in SLC
does not introduce any failure mechanisms of a different type than
those previously evaluated, since there are no physical changes
being made to the facility. No new or different equipment is being
installed. No installed equipment is being operated in a different
manner. As a result, no new failure modes are being introduced. The
way surveillance tests are performed remains unchanged. A historical
review of surveillance test results and associated maintenance
records indicated there was no evidence of any failures that would
invalidate the above conclusions.
Loss of Power Instrumentation
The proposed change in AVs is the result of application of the
Instrument Setpoint Methodology using plant-specific drift values
and does not create the possibility of a new or different kind of
accident from any accident previously evaluated. This is based upon
the fact that the method and manner of plant operation are
unchanged.
The use of the proposed AVs does not impact safe operation of
the plant in that the safety analysis limits are maintained. The
proposed change in AVs involves no system additions. The AVs are
revised to ensure the affected instrumentation remains capable of
mitigating accidents and transients. Plant equipment will not be
operated in a manner different from previous operation, except that
setpoints may be changed. No additional failure mechanisms are
introduced as a result of the changes to the allowable values. Since
operational methods remain unchanged and
[[Page 53777]]
the operating parameters were evaluated to maintain the plant within
existing design basis criteria, no different type of failure or
accident is created.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed TS changes involve a change in the surveillance
testing intervals and allowable values to facilitate a change in the
operating cycle length. The impact of these changes on system
availability is not significant, based on other more frequent
testing that is performed, the existence of redundant systems and
equipment, and overall system reliability. Evaluations have shown
there is no evidence of time dependent failures that would impact
the availability of the systems. The proposed changes do not
significantly impact the condition or performance of structures,
systems, and components relied upon for accident mitigation. The
proposed changes in TS instrumentation allowable values are the
result of application of the RBS setpoint methodology using plant
specific drift values. The revised allowable values more accurately
reflect total instrumentation loop accuracy including drift while
continuing to protect any assumed analytical limit. The proposed
changes do not result in any hardware changes or in any changes to
the analytical limits assumed in accident analyses. Existing
operating margin between plant conditions and actual plant setpoints
is not significantly reduced due to these changes. The proposed
changes do not significantly impact any safety analysis assumptions
or results.
Standby Liquid Control System
The proposed change in required weight of Boron-10 in SLC is to
facilitate a change in the operating cycle length. The proposed
change does not result in any hardware changes or in any changes to
the analytical limits assumed in accident analyses. Existing
operating margin between plant conditions and actual plant setpoints
is not reduced due to this change. The proposed change does not
impact any safety analysis assumptions or results. Therefore, the
proposed change does not involve a significant reduction in a margin
of safety.
Loss of Power Instrumentation
The proposed protection voltage AVs are low enough to prevent
inadvertent power supply transfer, but high enough to ensure that
sufficient voltage is available to the required equipment. The
proposed change does not involve a reduction in a margin of safety.
The proposed change was developed using a methodology to ensure
safety analysis limits are not exceeded. As such, this proposed
change does not involve a significant reduction in a margin of
safety.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Terence A. Burke, Associate General
Counsel--Nuclear Entergy Services, Inc., 1340 Echelon Parkway, Jackson,
Mississippi 39213.
NRC Branch Chief: Michael T. Markley.
Entergy Nuclear Operations, Inc., Docket No. 50-255, Palisades Nuclear
Plant, Van Buren County, Michigan
Date of amendment request: August 25, 2009.
Description of amendment request: The proposed amendment would
allow for a one-time extension to the ten-year frequency for the next
Palisades Nuclear Plant (PNP) containment Type A integrated leak rate
test (ILRT) that is required by Technical Specification (TS) 5.5.14.
The proposed change would permit the existing ILRT frequency to be
extended from ten years to approximately 11.25 years.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed exemption involves a one-time extension to the
current interval for Type A containment testing. The current test
interval of 120 months (10 years) would be extended on a one-time
basis to no longer than approximately 135 months from the last Type
A test. The proposed extension does not involve either a physical
change to the plant or a change in the manner in which the plant is
operated or controlled. The containment is designed to provide an
essentially leak tight barrier against the uncontrolled release of
radioactivity to the environment for postulated accidents. As such,
the containment and the testing requirements invoked to periodically
demonstrate the integrity of the containment exist to ensure the
plant's ability to mitigate the consequences of an accident, and do
not involve the prevention or identification of any precursors of an
accident. Therefore, this proposed extension does not involve a
significant increase in the probability of an accident previously
evaluated.
This proposed extension is for the Type A containment leak rate
tests only. The Type B and C containment leak rate tests would
continue to be performed at the frequency currently required by the
PNP TS. As documented in NUREG 1493, Type B and C tests have
identified a very large percentage of containment leakage paths and
that the percentage of containment leakage paths that are detected
only by Type A testing is very small. The PNP Type A test history
supports this conclusion.
The integrity of the containment is subject to two types of
failure mechanisms that can be categorized as (1) activity based and
(2) time based. Activity based failure mechanisms are defined as
degradation due to system and/or component modifications or
maintenance. Local leak rate test requirements and administrative
controls such as configuration management and procedural
requirements for system restoration ensure that containment
integrity is not degraded by plant modifications or maintenance
activities. The design and construction requirements of the
containment combined with the containment inspections performed in
accordance with ASME Section XI, the Maintenance Rule, and TS
requirements serve to provide a high degree of assurance that the
containment would not degrade in a manner that is detectable only by
a Type A test. Based on the above, the proposed extension does not
involve a significant increase in the consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed revision to the TS involves a one-time extension to
the current interval for Type A containment testing. The containment
and the testing requirements invoked to periodically demonstrate the
integrity of the containment exist to ensure the plant's ability to
mitigate the consequences of an accident and do not involve the
prevention or identification of any precursors of an accident. The
proposed TS change does not involve a physical change to the plant
or the manner in which the plant is operated or controlled.
Therefore, the proposed TS change does not create the possibility of
a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change to the TS involves a one-time extension to
the current interval for Type A containment testing. The proposed TS
change does not involve a physical change to the plant or a change
in the manner in which the plant is operated or controlled. The
specific requirements and conditions of the TS Containment Leak Rate
Testing Program exist to ensure that the degree of containment
structural integrity and leak-tightness that is considered in the
plant safety analysis is maintained. The overall containment leak
rate limit specified by TS is maintained. The proposed change
involves only the extension of the interval between Type A
containment leak rate tests. The proposed surveillance interval
extension is bounded by the 15-month extension currently authorized
within NEI 94-01, Revision 0. Type B and C containment leak
[[Page 53778]]
rate tests would continue to be performed at the frequency currently
required by TS. Industry experience supports the conclusion that
Type B and C testing detects a large percentage of containment
leakage paths and that the percentage of containment leakage paths
that are detected only by Type A testing is small. The containment
inspections performed in accordance with ASME Section XI and the
Maintenance Rule serve to provide a high degree of assurance that
the containment would not degrade in a manner that is detectable
only by Type A testing. The combination of these factors ensures
that the margin of safety in the plant safety analysis is
maintained. The design, operation, testing methods and acceptance
criteria for Type A, B, and C containment leakage tests specified in
applicable codes and standards would continue to be met, with the
acceptance of this proposed change, since these are not affected by
changes to the Type A test interval. Therefore, the proposed TS
change does not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. William Dennis, Assistant General
Counsel, Entergy Nuclear Operations, Inc., 440 Hamilton Ave., White
Plains, NY 10601.
NRC Acting Branch Chief: Peter Tam.
Entergy Nuclear Vermont Yankee, LLC and Entergy Nuclear Operations,
Inc., Docket No. 50-271, Vermont Yankee Nuclear Power Station, Vernon,
Vermont
Date of amendment request: August 26, 2009.
Description of amendment request: The proposed amendment would
revise the Technical Specification (TS) Section 6.5 that governs
administrative controls of High Radiation Areas (HRA) to incorporate
the HRA administrative controls contained within the Standard Technical
Specifications, NUREG-1433, Revision 3.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. The operation of Vermont Yankee Nuclear Power Station (VY) in
accordance with the proposed amendment will not involve a
significant increase in the probability or consequences of an
accident previously evaluated.
The proposed amendment does not impact the operability of any
structure, system or component that affects the probability of an
accident or that supports mitigation of an accident previously
evaluated. The proposed amendment does not affect reactor operations
or accident analysis and has no radiological consequences. The
operability requirements for accident mitigation systems remain
consistent with the licensing and design basis. Therefore, the
proposed amendment does not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. The operation of VY in accordance with the proposed amendment
will not create the possibility of a new or different kind of
accident from any accident previously evaluated.
The proposed amendment does not change the design or function of
any component or system. No new modes of failure or initiating
events are being introduced. Therefore, operation of VY in
accordance with the proposed amendment will not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. The operation of VY in accordance with the proposed amendment
will not involve a significant reduction in a margin of safety.
The proposed amendment does not change the design or function of
any component or system. The proposed amendment does not involve any
safety limits, safety settings or safety margins. The TS
administrative access controls for high radiation areas are being
replaced with those contained in section 5.7 of NUREG-1433 to
provide additional requirements and options for the control of these
areas.
Therefore, operation of VY in accordance with the proposed
amendment will not involve a significant reduction in the margin to
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. William C. Dennis, Assistant General
Counsel, Entergy Nuclear Operations, Inc., 400 Hamilton Avenue, White
Plains, NY 10601.
NRC Branch Chief: Nancy Salgado.
Nine Mile Point Nuclear Station, LLC (NMPNS) Docket No. 50-410, Nine
Mile Point Nuclear Station Unit No. 2 (NMP 2), Oswego County, New York
Date of amendment request: May 27, 2009, as supplemented on August
28, 2009.
Description of amendment request: The proposed amendment requests
an increase in the maximum steady-state power level at NMP2 from 3467
megawatts thermal (MWt) to 3988 MWt. This represents a 15-percent
increase over the current licensed thermal power.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. [Does the proposed amendment] involve a significant increase
in the probability or consequences of an accident previously
evaluated?
No, the increase in power level discussed herein will not
significantly increase the probability or consequences of an
accident previously evaluated.
The proposed change will increase NMP2's authorized maximum
power level from the current licensed thermal power (CLTP) level of
3467 megawatts thermal (MWt) to 3988 MWt. In support of this
Constant Pressure Extended Power Uprate (CPPU), a comprehensive
evaluation was performed for nuclear steam supply system (NSSS) and
balance of plant (BOP) systems, structures, components, and analyses
that could be affected by this change. The effect of increasing the
maximum power level from the CLTP of 3467 MWt to 3988 MWt on the
NMP2 licensing and design bases was evaluated. The result of this
evaluation is that all plant components, as modified, will continue
to be capable of performing their design function at an uprated core
power of 3988 MWt. In addition, an evaluation of the accident
analyses concludes that applicable analysis acceptance criteria
continue to be met. Power level is an input assumption to the
equipment design and accident analyses, but it is not an initiator
for any transient or accident. Therefore, no accident initiators are
affected by this uprate and no challenges to any plant safety
barriers are created by this change.
Therefore, operation of the facility in accordance with the
proposed change does not involve a significant increase in the
probability of an accident previously evaluated.
This change does not affect the release paths, the frequency of
release, or the source term for release for any accidents previously
evaluated in the Updated Safety Analysis Report (USAR). Structures,
systems, and components (SSC) required to mitigate transients remain
capable of performing their design functions, and thus were found
acceptable. The source terms used to assess radiological
consequences have been reviewed and determined to bound operation at
the uprated condition. The results of EPU [extended power uprate]
accident evaluations do not exceed the U. S. Nuclear Regulatory
Commission (NRC) approved acceptance limits.
The spectrum of postulated accidents and transients has been
investigated and are shown to meet the regulatory criteria to which
NMP2 is currently licensed. In the area of fuel and core design, the
Safety Limit Minimum Critical Power ratio (SLMCPR) and other
applicable Specified Acceptable Fuel Design Limits (SAFDLS) are
still met. Continued compliance with the SLMCPR and other SAFDLs is
confirmed on a cycle specific basis consistent with criteria
accepted by the NRC.
Challenges to the reactor coolant pressure boundary were
evaluated at EPU conditions
[[Page 53779]]
(pressure, temperature, flow, and radiation) and found to meet the
acceptance criteria for allowable stresses. Adequate overpressure
margin is maintained.
Challenges to the containment have been evaluated and the
containment and its associated cooling system continue to meet
applicable regulatory requirements. The increase in the calculated
post Loss of Coolant Accident (LOCA) suppression pool temperature
above the current peak temperature was evaluated and determined to
be acceptable.
Radiological release events (accidents) have been evaluated and
shown to meet the requirements of 10 CFR 50.67.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. [Does the proposed amendment] create the possibility of a new
or different kind of accident from any accident previously
evaluated?
No, the increase in power level discussed herein will not create
the possibility of a new or different kind of accident from any
accident previously evaluated.
The proposed change will increase NMP2's authorized maximum
power level from the CLTP level of 3467 MWt to 3988 MWt. Equipment
that could be affected by EPU has been evaluated. No new operating
mode, safety-related equipment lineup, accident scenario, or
equipment failure mode was identified. The full spectrum of accident
considerations has been evaluated and no new or different kind of
accident has been identified. This Constant Pressure Extended Power
Uprate utilizes a standard evaluation methodology applied to known
technology employed within the range of current or modified plant
capabilities. As such, the plant safety-related equipment continues
to operate in accordance with regulatory criteria. Evaluations were
performed using NRC approved codes, standards and methods. No new
accidents or event precursors have been identified.
All structures, systems and components previously required for
the mitigation of a transient remain capable of fulfilling their
intended design functions. The proposed changes do not adversely
affect safety-related systems or components and do not challenge the
performance or integrity of any safety-related system. This change
does not adversely affect any current system interfaces or create
any new interfaces that could result in an accident or malfunction
of a different kind than was previously evaluated. Operating at a
core power level of 3988 MWt does not create any new accident
initiators or precursors.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any accident previously
evaluated.
3. [Does the proposed amendment] involve a significant reduction
in a margin of safety?
No, the increase in power level discussed herein will not
involve a significant reduction in a margin of safety.
Comprehensive analyses of the proposed changes have concluded
that relevant design and safety acceptance criteria will be met
without a significant reduction in margins of safety. The analyses
supporting EPU have demonstrated that the NMP2 SSCs are capable of
safely performing at EPU conditions. The analyses identified and
defined the major input parameters to the NSSS, analyzed NSSS design
transients, and evaluated the capabilities of the NSSS fluid
systems, NSSS/BOP interfaces, NSSS control systems, and NSSS and BOP
components, as appropriate. Radiological consequences of design
basis events remain within regulatory limits and are not increased
significantly. The analyses confirmed that NSSS and BOP SSCs are
capable, some with modifications, of achieving EPU conditions
without significant reduction in margins of safety.
Analyses have shown that the integrity of primary fission
product barriers will not be significantly affected as a result of
the power increase. Calculated loads on SSCs important to safety
have been shown to remain within design allowables under EPU
conditions for all design basis event categories. Plant response to
transients and accidents do not result in exceeding acceptance
criteria. As appropriate, the evaluations that demonstrate
acceptability of EPU have been performed using methods that have
either been reviewed and approved by the NRC staff, or that are in
compliance with regulatory review guidance and standards established
for maintaining adequate margins of safety. These evaluations
demonstrate that there are no significant reductions in the margins
of safety.
Maximum power level is one of the inherent inputs that determine
the safe operating range defined by the accident analyses. The
Technical Specifications ensure that NMP2 is operated within the
bounds of the inputs and assumptions used in the accident analyses.
The acceptance criteria for the accident analyses are conservative
with respect to the operating conditions defined by the Technical
Specifications. The engineering reviews performed for the constant
pressure extended power uprate confirm that the accident analyses
criteria are met at the revised maximum allowable thermal power
level of 3988 MWt, as well as at the rated thermal power (RTP)
levels specified in the Facility Operating License and Technical
Specifications. Therefore, the adequacy of the revised Facility
Operating Licenses and Technical Specifications to maintain the
plant in a safe operating range is also confirmed, and the increase
in maximum allowable power level does not involve a significant
decrease in a margin of safety.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston &
Strawn, 1700 K Street, NW., Washington, DC 20006.
NRC Branch Chief: Nancy L. Salgado.
Nine Mile Point Nuclear Station, LLC (NMPNS) Docket No. 50-410, Nine
Mile Point Nuclear Station Unit No. 2 (NMP2), Oswego County, New York
Date of amendment request: June 29, 2009, as supplemented on August
13, 2009.
Description of amendment request: The proposed amendment would
revise the NMP2 Technical Specification (TS) 5.5.12 by replacing the
reference to Regulatory Guide (RG) 1.163 with a reference to Nuclear
Energy Institute (NEI) Topical Report NEI 94-01, Revision 2-A, as the
implementation document used by NMPNS to develop the NMP2 performance-
based leakage testing program in accordance with Option B of Title 10
of the Code of Federal Regulations (10 CFR) Part 50. The proposed
amendment would allow the next primary containment integrated leak rate
test (ILRT) to be performed within 15 years from the last ILRT as
opposed to the current 10-year interval, and would allow successive
ILRTs to be performed at 15-year intervals.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed amendment involves changes to the NMP2 10 CFR 50
Appendix J Testing Program Plan. The proposed amendment does not
involve a physical change to the plant or a change in the manner in
which the plant is operated or controlled. The primary containment
function is to provide an essentially leak tight barrier against the
uncontrolled release of radioactivity to the environment for
postulated accidents. As such, the containment itself and the
testing requirements to periodically demonstrate the integrity of
the containment exist to ensure the plant's ability to mitigate the
consequences of an accident, and do not involve any accident
precursors or initiators. Therefore, the probability of occurrence
of an accident previously evaluated is not significantly increased
by the proposed amendment.
The proposed amendment adopts the NRC-accepted guidelines of NEI
94-01, Revision 2, for development of the NMP2 performance-based
leakage testing program. Implementation of these guidelines
continues to provide adequate assurance that during design basis
accidents, the primary containment and its components will limit
[[Page 53780]]
leakage rates to less [then] the values assumed in the plant safety
analyses. The potential consequences of extending the ILRT interval
from 10 years to 15 years have been evaluated by analyzing the
resulting changes in risk. The increase in risk in terms of person-
rem per year within 50 miles resulting from design basis accidents
was estimated to be acceptably small, and the increase in the large
early release frequency resulting from the proposed change was
determined to be within the guidelines published in NRC RG 1.174.
Additionally, the proposed change maintains defense-in-depth by
preserving a reasonable balance among prevention of core damage,
prevention of containment failure, and consequence mitigation. NMPNS
has determined that the increase in conditional containment failure
probability due to the proposed change would be very small.
Therefore, it is concluded that the proposed amendment does not
significantly increase the consequences of an accident previously
evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed amendment adopts the NRC-accepted guidelines of
NEI-94-01, Revision 2, for development of the NMP2 performance-based
leakage testing program, and establishes a 15 year interval for the
performance of the primary containment ILRT. The containment and the
testing requirements to periodically demonstrate the integrity of
the containment exist to ensure the plant's ability to mitigate the
consequences of an accident, and do not involve any accident
precursors and initiators. The proposed change does not involve a
physical change to the plant (i.e., no new or different type of
equipment will be installed) or a change to the manner in which the
plant is operated or controlled.
Therefore, the proposed amendment does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed amendment adopts the NRC-accepted guidelines of
NEI-94-01, Revision 2, for development of the NMP2 performance-based
leakage testing program, and establishes a 15 year interval for the
performance of the primary containment ILRT. The amendment does not
alter the manner in which safety limits, limiting safety system
setpoints, or limiting conditions for operation are determined. The
specific requirements and conditions of the 10 CFR 50 Appendix J
Testing Program Plan, as defined in the TS, ensure that the degree
of primary containment structural integrity and leak-tightness that
is considered in the plant safety analyses is maintained. The
overall containment leakage rate limit specified by the TS is
maintained, and the Type A, B, and C containment leakage tests will
continue to be performed at the frequencies established in
accordance with the NRC-accepted guidelines of NEI 94-01, Revision
2.
Containment inspections performed in accordance with other plant
programs serve to provide a high degree of assurance that the
containment will not degrade in a manner that is detectable only by
an ILRT. In addition, the on-line containment monitoring capability
that is inherent to inerted boiling water reactor containments
allows for the detection of gross containment leakage that may
develop during power operation. This combination of factors ensures
that evidence of containment structural degradation is identified in
a timely manner. Furthermore, a risk assessment using the current
NMP2 Probabilistic Risk Assessment model concluded that extending
the ILRT test interval from 10 years to 15 years results in a very
small change to the NMP2 risk profile.
Therefore, the proposed amendment does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston &
Strawn, 1700 K Street, NW., Washington, DC 20006.
NRC Branch Chief: Nancy L. Salgado.
Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 50-
364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County,
Alabama
Date of amendment request: September 15, 2009.
Description of amendment request: The proposed amendment revises
Technical Specification (TS) 3.3.2, in Appendix A to Facility Operating
License Nos. NPF-2 and NPF-8 for the Joseph M. Farley Nuclear Plant
Units 1 and 2, respectively. P-11 is an engineered safety feature
actuation system (ESFAS) permissive/interlock which permits normal unit
cooldown and depressurization without actuation of safety injection
(SI) from low pressurizer pressure. P-12 is an ESFAS permissive/
interlock which permits normal unit cooldown and depressurization
without actuation of SI and main steam line isolation on the condition
of low steam line pressure. Both P-11 and P-12 circuits use input from
three protection channels. The current wording of Condition K in TS
3.3.2 states, ``Two channels inoperable.'' As a result, Condition K
does not explicitly address the possible conditions of one channel or
three channels inoperable, possibly creating a literal compliance
issue. The proposed Condition K change from ``Two channels inoperable''
to ``One or more channels inoperable'' will resolve the current literal
compliance issue. The change does not alter the current Condition K
required action, it simply clarifies that the required action must be
performed for one, two, or three P-11 or P-12 channels inoperable. In
addition, an editorial change is proposed for TS 5.6.8 to correct the
citation of a condition requiring a report for the post-accident
monitoring instrumentation. The current TS 5.6.8 text states, ``When a
report is required by Condition B or G of LCO [limiting conditions for
operation] 3.3.3. * * *'' The citation of Condition B is correct while
Condition G does not currently exist for LCO 3.3.3; instead TS 5.6.8
should cite Condition F.
Basis for proposed no significant hazards consideration
determination: As required by Title 10 of the Code of Federal
Regulations (10 CFR) 50.91(a), the licensee has provided its analysis
of the issue of no significant hazards consideration, which is
presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change to TS 3.3.2 does not significantly increase
the probability or consequences of an accident previously evaluated
in the FSAR. These interlocks do not directly initiate an accident.
The consequences of accidents previously evaluated in the FSAR are
not adversely affected by these changes because the changes are made
to reflect the Improved Standard Technical Specifications and the
interlocks are verified to be in the required state for the unit
condition.
The proposed change to TS 5.6.8 corrects an editorial error and
therefore does not significantly increase the probability or
consequences of a previously evaluated accident.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed change to TS 3.3.2 does not create the possibility
of a new or different kind of accident than any accident already
evaluated in the FSAR. No new accident scenario, failure mechanisms,
or limiting single failures are introduced as a result of the
proposed change. The proposed TS 3.3.2 change does not challenge the
performance or integrity of any safety-related systems. Therefore,
this change does not create the possibility of a new or different
kind of accident from any accident previously analyzed.
The proposed change to TS 5.6.8 corrects an editorial error and
therefore does not create the possibility of a new or different kind
of accident from any accident previously analyzed.
[[Page 53781]]
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed change to TS 3.3.2 does not involve a significant
reduction in a margin of safety. The proposed change is made to
accurately reflect the format of the Improved Standard Technical
Specifications. The actuation setpoints specified by the Technical
Specifications and safety analysis limits assumed in the accident
analysis are unchanged. The margin of safety associated with these
trip setpoints and the safety analysis acceptance criteria is
unchanged. Therefore, the proposed change to TS 3.3.2 will not
significantly reduce the margin of safety as defined in the
Technical Specifications.
The proposed change to TS 5.6.8 corrects an editorial error and
therefore involves no significant reduction in a margin of safety.
Based on the above, SNC concludes that the proposed amendment
does not involve a significant hazards consideration under the
standards set forth in 10 CFR 50.92(c), and, accordingly, a finding
of ``no significant hazards consideration'' is justified.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: M. Stanford Blanton, Esq., Balch and
Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham,
Alabama 35201.
NRC Branch Chief: Jon H. Thompson, Acting.
Tennessee Valley Authority (TVA), Docket Nos. 50-259, 50-260 and 50-
296, Browns Ferry Nuclear Plant, Units 1, 2 and 3, Limestone County,
Alabama
Date of amendment request: July 27, 2009 (TS-465).
Description of amendment request: The proposed change is to
eliminate Technical Specification (TS) surveillance requirement (SR)
3.6.1.3.11 and the requirement to perform water leak rate testing on
the listed containment isolation valves. More specifically, the
proposed change eliminates water local leak rate testing of valves in
the Containment Leak Rate Program that are being tested to verify the
combined leakage rate is within the limit that ensures the suppression
pool level is sufficient to keep lines that terminate below the water
level for at least 30 days without additional make-up.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration.
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
This proposal does not involve a significant increase in the
probability or consequences of an accident previously evaluated.
The proposed change to the scope of water leak rate testing for
the subject valves does not affect the probability of the design
basis accidents. The valves will continue to be maintained in an
operable state, and in their current design configuration. There is
no correlation between the scope of the water leak rate testing and
accident probability.
TVA reviewed the postulated consequences of design basis events
on primary containment isolation under the proposed change. The
primary containment structure, including access openings,
penetrations and the containment heat removal system, is designed so
that the containment structure and its internal compartments can
withstand, without exceeding the design leakage rate (2.0% per day),
the peak accident pressure and temperature that could occur during
any postulated LOCA [loss-of-coolant accident].
For the purposes of considering the consequences of LOCAs under
the proposed change, a single active failure of a CIV [containment
isolation valve] or a passive failure of the closed system were
reviewed, within the limits of the existing licensing basis. Under
the existing licensing basis, a pipe rupture of seismically
qualified ECCS [emergency core cooling system] piping does not have
to be assumed concurrent with the LOCA, except if it is a
consequence of the LOCA. Consequential failures can be eliminated,
since a LOCA inside containment is separated from the ECCS piping by
the containment structure. Consequential failures of the ECCS piping
from LOCA's outside containment are outside the Appendix J design
considerations, although they are adequately addressed through the
redundancy and separation of the ECCS design. A single active
failure of the CIV, under the LOCA condition, can be accommodated
since the closed and filled system piping and the suppression pool
water inventory remain as the leakage barriers. The ECCS passive
failure criterion does require consideration of system leaks, but
not pipe breaks, beyond the initiating LOCA. Pipe leakage,
equivalent to the leakage from a valve or pump seal failure, should
be considered at 24 hours or greater post-LOCA. The capability to
make-up inventory to the suppression pool is adequate to ensure that
postulated seat leakage and pipe leakage does not result in a
condition that jeopardizes pool level. Make-up capability exists to
the suppression pool. Actions to make-up to the suppression pool are
delineated in Emergency Operating Instructions.
Therefore, the proposal to eliminate the subject water leak rate
tests does not involve a significant increase in the probability or
consequences of an accident previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
This proposal does not create the possibility of a new or
different kind of accident from any accident previously evaluated.
The acceptability of the proposed change to the scope of water
leak rate testing for the subject valves is based on maintaining the
existing barriers to primary containment leakage, and ensuring that
the suppression pool level is assured for 30 days during all design
basis, post-accident modes of operation. By meeting these dual
objectives, the plant response to the design basis events will be
unchanged, and no new accident scenarios will be encountered. These
two objectives are related, in that, the suppression pool inventory
creates a passive barrier to primary containment atmospheric leakage
for valves associated with penetrations which are located below the
minimum water level of the pool.
The proposed Technical