STP Nuclear Operating Company; Notice of Withdrawal of Application for Amendments to Facility Operating Licenses, 68598 [E7-23536]
Download as PDF
68598
Federal Register / Vol. 72, No. 233 / Wednesday, December 5, 2007 / Notices
NUCLEAR REGULATORY
COMMISSION
NUCLEAR REGULATORY
COMMISSION
[Docket Nos. 50–387 and 50–388]
[Docket Nos. 50–498 and 50–499]
STP Nuclear Operating Company;
Notice of Withdrawal of Application for
Amendments to Facility Operating
Licenses
mstockstill on PROD1PC66 with NOTICES
The U.S. Nuclear Regulatory
Commission (the Commission) has
granted the request of STP Nuclear
Operating Company (the licensee) to
withdraw its June 7, 2006, application
for proposed amendments to Facility
Operating License Nos. NPF–76 and
NPF–80, respectively, for the South
Texas Project, Units 1 and 2, located in
Matagorda County.
The proposed amendments would
have revised the facility’s Spent Fuel
Pool and In-Containment Storage Area
Criticality Analysis.
The Commission had previously
issued a Notice of Consideration of
Issuance of Amendments published in
the Federal Register on September 12,
2006 (71 FR 53721). However, by letter
dated November 28, 2007, the licensee
withdrew the proposed request for
amendments.
For further details with respect to this
action, see the application for
amendments dated June 7, 2006, and the
licensee’s letter dated November 28,
2007, which withdrew the application
for license amendments. Documents
may be examined, and/or copied for a
fee, at the NRC’s Public Document
Room (PDR), located at One White Flint
North, Public File Area O1 F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible electronically from
the Agencywide Documents Access and
Management Systems (ADAMS) Public
Electronic Reading Room on the internet
at the NRC Web site, https://
www.nrc.gov/reading-rm.html. Persons
who do not have access to ADAMS or
who encounter problems in accessing
the documents located in ADAMS
should contact the NRC PDR Reference
staff by telephone at 1–800–397–4209,
or 301–415–4737 or by e-mail to
pdr@nrc.gov.
Dated at Rockville, Maryland, this 28th day
of November, 2007.
For the Nuclear Regulatory Commission.
Carl F. Lyon,
Project Manager, Plant Licensing Branch IV,
Division of Operating Reactor Licensing,
Office of Nuclear Reactor Regulation.
[FR Doc. E7–23536 Filed 12–4–07; 8:45 am]
BILLING CODE 7590–01–P
VerDate Aug<31>2005
19:05 Dec 04, 2007
Jkt 214001
PPL Susquehanna, LLC; Susquehanna
Steam Electric Station, Units 1 and 2;
Draft Environmental Assessment and
Finding of No Significant Impact
Related to the Proposed License
Amendment To Increase the Maximum
Reactor Power Level
U.S. Nuclear Regulatory
Commission (NRC).
ACTION: Notice of Opportunity for Public
Comment.
AGENCY:
SUMMARY: The NRC has prepared a Draft
Environmental Assessment as its
evaluation of a request by PPL
Susquehanna, LLC for a license
amendment to increase the maximum
thermal power at Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1
and 2), from 3,489 megawatts-thermal
(MWt) to 3,952 MWt at each unit. This
represents a power increase of
approximately 13 percent thermal
power. As stated in the NRC staff’s
position paper dated February 8, 1996,
on the Boiling-Water Reactor Extended
Power Uprate (EPU) Program, the NRC
staff (the staff) will prepare an
environmental impact statement if it
believes a power uprate would have a
significant impact on the human
environment. The staff did not identify
any significant impact from the
information provided in the licensee’s
EPU application for Susquehanna Steam
Electric Station, Units 1 and 2, or the
staff’s independent review; therefore,
the staff is documenting its
environmental review in an
Environmental Assessment. Also, in
accordance with the position paper, the
Draft Environmental Assessment and
Finding of No Significant Impact is
being published in the Federal Register
with a 30-day public comment period.
Environmental Assessment
Plant Site and Environs
SSES is located just west of the
Susquehanna River approximately 5
miles northeast of Berwick, in Luzerne
County, Pennsylvania. In total, SSES
majority owner and licensed operator,
PPL Susquehanna, LLC (PPL, the
licensee), owns 2,355 acres of land on
both sides of the Susquehanna River.
Generally, this land is characterized by
open deciduous woodlands interspersed
with grasslands and orchards.
Approximately 487 acres are used for
generation facilities and associated
maintenance facilities, laydown areas,
parking lots, and roads. Approximately
PO 00000
Frm 00046
Fmt 4703
Sfmt 4703
130 acres are leased to local farmers.
PPL maintains a 401-acre nature
preserve, referred to as the Susquehanna
Riverlands, which is located between
SSES and the river; U.S. Route 11
separates the Susquehanna Riverlands
from the plant site. The land on the west
side of the river is about 1,573 acres and
Gould Island, a 65-acre island just north
of SSES on the Susquehanna River, is
currently jointly owned between PPL
(90%) and Allegheny Electric
Cooperative (10%). Also, PPL currently
owns an additional 717 acres of mostly
undeveloped land, which includes
natural recreational, and wildlife areas
on the east side of the river (Reference
10).
SSES is a two-unit plant with General
Electric boiling-water reactors and
generators. NRC approved the Unit 1
operating license on July 17, 1982, and
commercial operation began June 8,
1983. The Unit 2 operating license was
issued on March 3, 1984, and
commercial operation began February
12, 1985. Units 1 and 2 both currently
operate at 3,489 MWt (Reference 8). The
units share a common control room,
refueling floor, turbine operating deck,
radwaste system, and other auxiliary
systems (Reference 9).
SSES uses a closed-cycle heat
dissipation system (two natural-draft
cooling towers) to transfer waste heat
from the circulating water system to the
atmosphere. The circulating water and
the service water systems draw water
from, and discharge to, the
Susquehanna River. The river intake
structure is located on the western bank
of the river and consists of two water
entrance chambers with 1-inch, oncenter vertical trash bars and 3⁄8-inchmesh traveling screens. A low-pressure
screen-wash system periodically
operates to release aquatic organisms
and debris impinged on the traveling
screens to a pit with debris removal
equipment that collects material into a
dumpster for offsite disposal. Cooling
tower blowdown, spray pond overflow,
and other permitted effluents are
discharged to the Susquehanna River
through a buried pipe leading to a
submerged discharge diffuser structure,
approximately 600 feet downstream of
the river intake structure. The diffuser
pipe is 200-feet long, with the last 120
feet containing 72 four-inch portals that
direct the discharge at a 45-degree angle
upwards and downstream. Warm
circulating water from the cooling
towers can be diverted to the river
intake structure to prevent icing; this
usually occurs from November through
March on an as-needed basis (Reference
10).
E:\FR\FM\05DEN1.SGM
05DEN1
Agencies
[Federal Register Volume 72, Number 233 (Wednesday, December 5, 2007)]
[Notices]
[Page 68598]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: E7-23536]
[[Page 68598]]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
[Docket Nos. 50-498 and 50-499]
STP Nuclear Operating Company; Notice of Withdrawal of
Application for Amendments to Facility Operating Licenses
The U.S. Nuclear Regulatory Commission (the Commission) has granted
the request of STP Nuclear Operating Company (the licensee) to withdraw
its June 7, 2006, application for proposed amendments to Facility
Operating License Nos. NPF-76 and NPF-80, respectively, for the South
Texas Project, Units 1 and 2, located in Matagorda County.
The proposed amendments would have revised the facility's Spent
Fuel Pool and In-Containment Storage Area Criticality Analysis.
The Commission had previously issued a Notice of Consideration of
Issuance of Amendments published in the Federal Register on September
12, 2006 (71 FR 53721). However, by letter dated November 28, 2007, the
licensee withdrew the proposed request for amendments.
For further details with respect to this action, see the
application for amendments dated June 7, 2006, and the licensee's
letter dated November 28, 2007, which withdrew the application for
license amendments. Documents may be examined, and/or copied for a fee,
at the NRC's Public Document Room (PDR), located at One White Flint
North, Public File Area O1 F21, 11555 Rockville Pike (first floor),
Rockville, Maryland. Publicly available records will be accessible
electronically from the Agencywide Documents Access and Management
Systems (ADAMS) Public Electronic Reading Room on the internet at the
NRC Web site, https://www.nrc.gov/reading-rm.html. Persons who do not
have access to ADAMS or who encounter problems in accessing the
documents located in ADAMS should contact the NRC PDR Reference staff
by telephone at 1-800-397-4209, or 301-415-4737 or by e-mail to
pdr@nrc.gov.
Dated at Rockville, Maryland, this 28th day of November, 2007.
For the Nuclear Regulatory Commission.
Carl F. Lyon,
Project Manager, Plant Licensing Branch IV, Division of Operating
Reactor Licensing, Office of Nuclear Reactor Regulation.
[FR Doc. E7-23536 Filed 12-4-07; 8:45 am]
BILLING CODE 7590-01-P