Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 45454-45466 [E7-15459]
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STATUS:
Federal Register / Vol. 72, No. 156 / Tuesday, August 14, 2007 / Notices
Public and Closed.
MATTERS TO BE CONSIDERED:
Week of August 13, 2007
Tuesday, August 14, 2007.
9:30 a.m. Discussion of
Intragovernmental Affairs (ClosedEx. 1 & 9).
Week of August 20, 2007—Tentative
Tuesday, August 21, 2007.
1:25 p.m.
Affirmation Session (Public Meeting)
(Tentative).
a. Final E-Filing Rule (Tentative).
This meeting will be webcast live at
the Web address— https://www.nrc.gov.
1:30 p.m.
Meeting with OAS and CRCPD
(Public Meeting). (Contact: Shawn
Smith, 301 415–2620).
This meeting will be webcast live at
the Web address— https://www.nrc.gov.
Wednesday, August 22, 2007.
9:30 a.m.
Periodic Briefing on New Reactor
Issues (Morning Session)(Public
Meeting) (Contact: Donna Williams,
301 415–1322).
This meeting will be webcast live at
the Web address— https://www.nrc.gov.
1:30 p.m.
Periodic Briefing on New Reactor
Issues (Afternoon Session)(Public
Meeting) (Contact: Donna Williams,
301 415–1322).
This meeting will be webcast live at
the Web address— https://www.nrc.gov.
Week of August 27, 2007—Tentative
There are no meetings scheduled for
the Week of August 27, 2007.
Week of September 3, 2007—Tentative
There are no meetings scheduled for
the Week of September 3, 2007.
Week of September 10, 2007—Tentative
There are no meetings scheduled for
the Week of September 10, 2007.
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Week of September 17, 2007—Tentative
There are no meetings scheduled for
the Week of September 17, 2007.
*The schedule for Commission
meetings is subject to change on short
notice. To verify the status of meetings
call (recording)—(301) 415–1292.
Contact person for more information:
Michelle Schroll, (301) 415–1662.
The NRC Commission Meeting
Schedule can be found on the Internet
at: https://www.nrc.gov/about-nrc/policymaking/schedule.html.
The NRC provides reasonable
accommodation to individuals with
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disabilities where appropriate. If you
need a reasonable accommodation to
participate in these public meetings, or
need this meeting notice or the
transcript or other information from the
public meetings in another format (e.g.
braille, large print), please notify the
NRC’s Disability Program Coordinator,
Rohn Brown, at 301–492–2279, TDD:
301–415–2100, or by e-mail at
REB3@nrc.gov. Determinations on
requests for reasonable accommodation
will be made on a case-by-case basis.
This notice is distributed by mail to
several hundred subscribers; if you no
longer wish to receive it, or would like
to be added to the distribution, please
contact the Office of the Secretary,
Washington, DC 20555 (301–415–1969).
In addition, distribution of this meeting
notice over the Internet system is
available. If you are interested in
receiving this Commission meeting
schedule electronically, please send an
electronic message to dkw@nrc.gov.
Dated: August 9, 2007.
R. Michelle Schroll,
Office of the Secretary.
[FR Doc. 07–3987 Filed 8–10–07; 11:37 am]
BILLING CODE 7590–01–P
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from July 19,
2007, to August 1, 2007. The last
biweekly notice was published on July
31, 2007 (72 FR 41780).
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Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
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Federal Register / Vol. 72, No. 156 / Tuesday, August 14, 2007 / Notices
Written comments may be submitted
by mail to the Chief, Rulemaking,
Directives and Editing Branch, Division
of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
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with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
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the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
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Calvert Cliffs Nuclear Power Plant, Inc.,
Docket Nos. 50–317 and 50–318, Calvert
Cliffs Nuclear Power Plant, Unit Nos. 1
and 2, Calvert County, Maryland
Date of amendments request: June 29,
2007.
Description of amendments request:
The amendment would modify
Technical Specification (TS)
requirements related to control room
envelope (CRE) habitability in TS 3.7.8,
‘‘Control Room Emergency Ventilation
System (CREVS),’’ and TS 5.5,
‘‘Programs and Manuals.’’ The changes
are consistent with the Nuclear
Regulatory Commission approved
Technical Specification Task Force
(TSTF)–448, Revision 3, ‘‘Control Room
Habitability.’’ The availability of the TS
improvement was published in the
Federal Register on January 17, 2007
(72 FR 2022) as part of the consolidated
item improvement process (CLIIP). In
addition, the amendment would remove
a footnote currently contained in the
Completion Time of TS 3.7.8, Required
Action D. The footnote was added in
Amendment Nos. 250/227 and was only
applicable during the Unit 1 2002
refueling outage.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change does not adversely
affect accident initiators or precursors nor
alter the design assumptions, conditions, or
configuration of the facility. The proposed
change does not alter or prevent the ability
of structures, systems, and components
(SSCs) to perform their intended function to
mitigate the consequences of an initiating
event within the assumed acceptance limits.
The proposed change revises the TS for the
CRE emergency ventilation system, which is
a mitigation system designed to minimize
unfiltered air leakage into the CRE and to
filter the CRE atmosphere to protect the CRE
occupants in the event of accidents
previously analyzed. An important part of
the CRE emergency ventilation system is the
CRE boundary. The CRE emergency
ventilation system is not an initiator or
precursor to any accident previously
evaluated. Therefore, the probability of any
accident previously evaluated is not
increased. Performing tests to verify the
operability of the CRE boundary and
implementing a program to assess and
maintain CRE habitability ensure that the
CRE emergency ventilation system is capable
of adequately mitigating radiological
consequences to CRE occupants during
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accident conditions, and that the CRE
emergency ventilation system will perform as
assumed in the consequence analyses of
design basis accidents. Thus, the
consequences of any accident previously
evaluated are not increased.
The removal of a footnote [to TS 3.7.8] that
is no longer applicable is an editorial change
that does not affect accident initiators or
precursors, nor alter the design assumptions,
conditions or configuration of the facility.
The proposed change also does not affect the
ability of SSCs to perform their intended
function to mitigate the consequences of an
accident. Therefore, the proposed editorial
change does not increase the probability or
consequences of an accident previously
evaluated.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not impact the
accident analysis. The proposed change does
not alter the required mitigation capability of
the CRE emergency ventilation system, or its
functioning during accident conditions as
assumed in the licensing basis analyses of
design basis accident radiological
consequences to CRE occupants. No new or
different accidents result from performing the
new surveillance or following the new
program. The proposed change does not
involve a physical alteration of the plant (i.e.,
no new or different type of equipment will
be installed) or a significant change in the
methods governing normal plant operation.
The proposed change does not alter any
safety analysis assumptions and is consistent
with current plant operating practice.
The proposed change is the editorial
removal of a footnote [to TS 3.7.8] that no
longer applies. The removal of a footnote that
no longer applies does not impact the
accident analyses. Additionally, it does not
add or modify any existing plant equipment
and does not introduce any new operational
methods. Therefore, the proposed editorial
change does not create the possibility of a
new or different kind of accident from any
accident previously evaluated.
Therefore, this change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change does not alter the
manner in which safety limits, limiting safety
system settings or limiting conditions for
operation are determined. The proposed
change does not affect safety analysis
acceptance criteria. The proposed change
will not result in plant operation in a
configuration outside the design basis for an
unacceptable period of time without
compensatory measures. The proposed
change does not adversely affect systems that
respond to safely shut down the plant and to
maintain the plant in a safe shutdown
condition.
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The proposed editorial change [removal of
a footnote to TS 3.7.8] does not affect safety
analyses acceptance criteria or safety system
operation. Removal of a footnote that is no
longer applicable does not result in plant
operation outside the design basis. Therefore,
the proposed editorial change does not
involve a reduction in the margin of safety.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Carey Fleming,
Sr. Counsel—Nuclear Generation,
Constellation Generation Group, LLC,
750 East Pratt Street, 17th floor,
Baltimore, MD 21202.
NRC Branch Chief: Mark G. Kowal.
Exelon Generation Company, LLC,
Docket Nos. 50–352 and 50–353,
Limerick Generating Station, Units 1
and 2, Montgomery County,
Pennsylvania
Date of amendment request: February
20, 2007.
Description of amendment request:
The proposed change would revise
Limerick Generating Station (LGS),
Units 1 and 2, Technical Specifications
(TSs), Section 6.8.4.g, ‘‘Primary
Containment Leakage Rate Testing
Program,’’ to allow a one-time extension
of no more than 5 years for the Type A,
Integrated Leakage Rate Test (ILRT)
interval. This revision is a one-time
exception to the 10-year frequency of
the performance-based leakage rate
testing program for Type A tests as
defined in Nuclear Energy Institute
(NEI) document NEI 94–01, Revision 0,
‘‘Industry Guideline For Implementing
Performance-Based Option of 10 CFR
Part 50, Appendix J,’’ pursuant to Title
10 of the Code of Federal Regulations
(10 CFR) Part 50, Appendix J, Option B.
The requested exception is to allow the
ILRT to be performed within 15 years
from the last ILRT as opposed to the
current 10-year frequency. The most
recent containment Type A ILRTs for
LGS Units 1 and 2 were performed on
May 15, 1998, and May 21, 1999,
respectively.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
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consequences of an accident previously
evaluated?
Response: No.
The proposed change will revise TS 6.8.4.g
(‘‘Primary Containment Leakage Rate Testing
Program’’) of the LGS, Units 1 and 2 TS to
reflect a one-time extension to the Type A
Integrated Leak Rate Test (ILRT) as currently
specified in the Technical Specifications.
This change will extend the requirement to
perform the Type A ILRT from the current
requirement of 10 to 15 years, which is ‘‘no
later than May 15, 2013’’ for LGS, Unit 1 and
is ‘‘no later than May 21, 2014’’ for Unit 2.
The function of the containment is to
isolate and contain fission products released
from the reactor coolant system following a
design basis Loss of Coolant Accident
(LOCA) and to confine the postulated release
of radioactive material to within limits. The
test interval associated with Type A ILRTs is
not a precursor of any accident previously
evaluated. Type A ILRTs provide assurance
that the LGS, Units 1 and 2 containments
will not exceed allowable leakage rate values
specified in the TS and will continue to
perform their design function following an
accident. The risk assessment of the
proposed change has concluded that there is
an insignificant increase in Large Early
Release Frequency, Person-Rem, and
Conditional Containment Failure Frequency.
Additionally, containment inspections have
also been performed which demonstrate the
continued structural integrity of the primary
containment and will be performed in the
future as required by the ASME Code.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change for a one-time
extension of the Type A ILRTs for LGS, Units
1 and 2 will not affect the control parameters
governing unit operation or the response of
plant equipment to transient and accident
conditions. The proposed change does not
introduce any new equipment, modes of
system operation or failure mechanisms.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The integrity of the containment
penetrations and isolation valves is verified
through Type B and Type C local leak rate
tests (LLRTs) and the overall leak tight
integrity of the containment is verified by a
Type A ILRT, as required by 10 CFR 50,
Appendix J, ‘‘Primary Reactor Containment
Leakage Testing for Water-Cooled Power
Reactors.’’ These tests are performed to verify
the essentially leak tight characteristics of the
containment at the design basis accident
pressure. The proposed change for a one-time
extension of the Type A ILRT does not affect
the method for Type A, B or C testing or the
test acceptance criteria.
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EGC has conducted a risk assessment to
determine the impact of a change to the LGS,
Units 1 and 2 Type A ILRT from 10 to 15
years. This risk assessment measured the
impact to the Large Early Release Frequency,
Person-Rem, and Conditional Containment
Failure Frequency. This assessment indicated
that the proposed LGS, Units 1 and 2 Type
A ILRT interval extension has a very small
change in risk to the public and is an
acceptable plant change from a risk
perspective.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. Bradley
Fewell, Associate General Counsel,
Exelon Generation Company, LLC, 4300
Winfield Road, Warrenville, IL 60555.
NRC Branch Chief: Harold K.
Chernoff.
Florida Power and Light Company,
Docket Nos. 50–335 and 50–389, St.
Lucie Plant, Units 1 and 2, St. Lucie
County, Florida
Date of amendment request: June 4,
2007.
Description of amendment request:
The proposed amendment would
remove the Technical Specification (TS)
requirements that reference hydrogen
recombiners and hydrogen monitors.
The proposed amendment suggests
changes support implementation of the
revisions to 10 CFR 50.44, ‘‘Standards
for Combustible Gas Control System in
Light Water Cooled Power Reactors,’’
that became effective on September 16,
2003. The changes would be consistent
with Revision 1 of the NRC-approved
Technical Specification Task Force
(TSTF) Standard Technical
Specification Change Traveler, TSTF–
447, ‘‘Elimination of Hydrogen
Recombiners and Change to Hydrogen
and Oxygen Monitors.’’ The particular
TS improvement in question was
announced in the Federal Register
Notice on September 25, 2003, as part
of the consolidated line item
improvement process.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
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Criterion 1—The Proposed Change Does Not
Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated
The revised 10 CFR 50.44 no longer defines
a design-basis loss-of-coolant accident
(LOCA) hydrogen release, and eliminates
requirements for hydrogen control systems to
mitigate such a release. The installation of
hydrogen recombiners and/or vent and purge
systems required by 10 CFR 50.44(b)(3) was
intended to address the limited quantity and
rate of hydrogen generation that was
postulated from a design-basis LOCA. The
Commission has found that this hydrogen
release is not risk-significant because the
design-basis LOCA hydrogen release does not
contribute to the conditional probability of a
large release up to approximately 24 hours
after the onset of core damage. In addition,
these systems were ineffective at mitigating
hydrogen releases from risk-significant
accident sequences that could threaten
containment integrity.
With the elimination of the design-basis
LOCA hydrogen release, hydrogen [and
oxygen] monitors are no longer required to
mitigate design-basis accidents and,
therefore, the hydrogen monitors do not meet
the definition of a safety-related component
as defined in 10 CFR 50.2. RG [Regulatory
Guide] 1.97 Category 1, is intended for key
variables that most directly indicate the
accomplishment of a safety function for
design-basis accident events. The hydrogen
[and oxygen] monitors no longer meet the
definition of Category 1 in RG 1.97. As part
of the rulemaking to revise 10 CFR 50.44 the
Commission found that Category 3, as
defined in RG 1.97, is an appropriate
categorization for the hydrogen monitors
because the monitors are required to
diagnose the course of beyond design-basis
accidents. [Also, as part of the rulemaking to
revise 10 CFR 50.44, the Commission found
that Category 2, as defined in RG 1.97, is an
appropriate categorization for the oxygen
monitors, because the monitors are required
to verify the status of the inert containment.]
The regulatory requirements for the
hydrogen [and oxygen] monitors can be
relaxed without degrading the plant
emergency response. The emergency
response, in this sense, refers to the
methodologies used in ascertaining the
condition of the reactor core, mitigating the
consequences of an accident, assessing and
projecting offsite releases of radioactivity,
and establishing protective action
recommendations to be communicated to
offsite authorities. Classification of the
hydrogen monitors as Category 3,
[classification of the oxygen monitors as
Category 2] and removal of the hydrogen [and
oxygen] monitors from TS will not prevent
an accident management strategy through the
use of the SAMGs [severe accident
management guidelines], the emergency plan
(EP), the emergency operating procedures
(EOP), and site survey monitoring that
support modification of emergency plan
protective action recommendations (PARs).
Therefore, the elimination of the hydrogen
recombiner requirements and relaxation of
the hydrogen [and oxygen] monitor
requirements, including removal of these
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requirements from TS, does not involve a
significant increase in the probability or the
consequences of any accident previously
evaluated.
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Criterion 2—The Proposed Change Does Not
Create the Possibility of a New or Different
Kind of Accident From Any Previously
Evaluated
The elimination of the hydrogen
recombiner requirements and relaxation of
the hydrogen [and oxygen] monitor
requirements, including removal of these
requirements from TS, will not result in any
failure mode not previously analyzed. The
hydrogen recombiner and hydrogen [and
oxygen] monitor equipment was intended to
mitigate a design-basis hydrogen release. The
hydrogen recombiner and hydrogen [and
oxygen] monitor equipment are not
considered accident precursors, nor does
their existence or elimination have any
adverse impact on the pre-accident state of
the reactor core or post accident confinement
of radionuclides within the containment
building.
Therefore, this change does not create the
possibility of a new or different kind of
accident from any previously evaluated.
Criterion 3—The Proposed Change Does Not
Involve a Significant Reduction in the
Margin of Safety
The elimination of the hydrogen
recombiner requirements and relaxation of
the hydrogen [and oxygen] monitor
requirements, including removal of these
requirements from TS, in light of existing
plant equipment, instrumentation,
procedures, and programs that provide
effective mitigation of and recovery from
reactor accidents, results in a neutral impact
to the margin of safety.
The installation of hydrogen recombiners
and/or vent and purge systems required by
10 CFR 50.44(b)(3) was intended to address
the limited quantity and rate of hydrogen
generation that was postulated from a designbasis LOCA. The Commission has found that
this hydrogen release is not risk-significant
because the design-basis LOCA hydrogen
release does not contribute to the conditional
probability of a large release up to
approximately 24 hours after the onset of
core damage.
Category 3 hydrogen monitors are adequate
to provide rapid assessment of current
reactor core conditions and the direction of
degradation while effectively responding to
the event in order to mitigate the
consequences of the accident. The intent of
the requirements established as a result of the
TMI [Three-Mile Island], Unit 2 accident can
be adequately met without reliance on safetyrelated hydrogen monitors.
[Category 2 oxygen monitors are adequate
to verify the status of an inerted
containment.]
Therefore, this change does not involve a
significant reduction in the margin of safety.
The intent of the requirements established as
a result of the TMI, Unit 2 accident can be
adequately met without reliance on safetyrelated oxygen monitors.] Removal of
hydrogen [and oxygen] monitoring from TS
will not result in a significant reduction in
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their functionality, reliability, and
availability.
Based upon the reasoning presented above
and the previous discussion of the
amendment request, the requested change
does not involve a significant hazards
consideration.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Attorney for licensee: M.S. Ross,
Attorney, Florida Power & Light, P.O.
Box 14000, Juno Beach, Florida 33408–
0420.
NRC Branch Chief: Thomas H. Boyce.
Indiana Michigan Power Company,
Docket Nos. 50–315 and 50–316, Donald
C. Cook Nuclear Plant, Units 1 and 2,
Berrien County, Michigan
Date of amendment request: June 13,
2007.
Description of amendment request:
The proposed amendment would revise
Technical Specifications (TS) 5.5.9,
‘‘Ventilation Filter Testing Program
(VFTP),’’ to impose lower (i.e., more
restrictive) limits on the maximum
pressure drop across the combined high
efficiency particulate air filters and
charcoal adsorbers in three safetyrelated ventilation systems. These
ventilation systems are the Control
Room Emergency Ventilation System,
the Engineered Safety Features
Ventilation System, and the FuelHandling Area Exhaust Ventilation
System.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability of
occurrence or consequences of an accident
previously evaluated?
Response: No.
The proposed change consists of
establishing more restrictive criteria in the
Technical Specification (TS) for the
maximum pressure drop across high
efficiency particulate air filters (HEPA) and
charcoal adsorbers in safety-related
ventilation systems. These TS criteria are
used to determine the acceptability of
periodic test results. These criteria are not
accident initiators. Therefore, there will be
no effect on the probability of an accident.
The safety-related ventilation systems
involved in the proposed change function to
mitigate the consequences of accidents. The
proposed change will provide increased
assurance that the HEPA filters and charcoal
adsorbers in these systems will be capable of
performing their safety function of reducing
the release of radioactive material resulting
from evaluated accidents. Therefore, there
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will be no increase in the consequences of
those accidents.
Therefore, the proposed change will not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change consists of
establishing more restrictive acceptance
criteria for existing TS[-]required tests. The
proposed change does not affect the manner
in which the tests are performed. The
proposed change will not result in any new
or different methods or modes of operation
of existing structures, systems, or
components. The proposed change will not
introduce any new structures, system, or
components.
Therefore, the proposed change will not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The margin of safety associated with the
proposed change is the capability of the
applicable safety-related ventilation systems
to prevent radiation exposures from
exceeding acceptable limits due to the release
of radioactive material caused by an
evaluated accident. The proposed change
will provide increased assurance that the
HEPA filters and charcoal adsorbers in these
systems will be capable of performing this
function.
Therefore, the proposed change will not
involve a significant reduction in the margin
of safety.
The Nuclear Regulatory Commission
(NRC) staff has reviewed the licensee’s
analysis and, based on this review, it
appears that the three standards of 10
CFR 50.92(c) are satisfied. Therefore, the
NRC staff proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Kimberly
Harshaw, Esquire, One Cook Place,
Bridgman, MI 49106.
NRC Acting Branch Chief: Travis
Tate.
Indiana Michigan Power Company,
Docket Nos. 50–315 and 50–316, Donald
C. Cook Nuclear Plant, Units 1 and 2,
Berrien County, Michigan
Date of amendment request: June 27,
2007.
Description of amendment request:
The proposed amendment would revise
Technical Specifications (TS)
Surveillance Requirements 3.8.1.2, 8,
12, 13, 16, and 19, changing the steady
state frequency of all diesel generators
(DGs) from the current allowed
frequency range of 59.4–61.2 Hz, to
59.4–60.5 Hz (i.e., a decrease of the
upper limit, resulting in narrowing of
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the current range). The licensee stated
that the current frequency range is
nonconservative and could result in
undesirable effects such as centrifugal
charging pump motor brake horsepower
exceeding its nameplate maximum
horsepower, and overloading the DGs.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee provided its analysis of the
issue of no significant hazards
consideration. The NRC staff has
performed its own analysis, which is
presented below:
(1) Does the proposed change involve a
significant increase in the probability of
occurrence or consequences of an accident
previously evaluated?
Response: No.
The more restrictive steady state frequency
range ensures that the diesel generators and
equipment being powered by the diesel
generators will function as designed to
mitigate an accident as described in the
Update Final Safety Analysis Report
(UFSAR). The DGs and the equipment they
power are part of the systems required to
mitigate accidents; no accident analyzed in
the UFSAR is initiated by mitigation
equipment. Therefore, the proposed change
to the allowed frequency range of the DGs
will not have any impact on the probability
of an accident previously evaluated.
Furthermore, other than narrowing the
allowed frequency range of the DGs, there is
no other design or operational change.
Therefore, the proposed change does not
increase the probability of malfunction of the
DGs or the equipment they power.
Narrowing of the DG maximum steady
state frequency limit will ensure that the DGs
and equipment powered by the DGs will
perform as originally designed and analyzed
to mitigate the consequences of any accident
described in the UFSAR. Therefore, the
proposed change does not involve a
significant increase in the consequences of an
accident previously evaluated in the UFSAR.
(2) Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
There is no design change associated with
the proposed amendment. Making an existing
DG requirement more restrictive alone will
not alter plant configuration because no new
or different type of equipment will be
installed, and because no methods governing
plant operation will be changed. The
proposed change to allowed frequency range
will not have any effect on the assumptions
of accident scenarios previously made in the
UFSAR. Therefore, the proposed change does
not create the possibility of a new or different
kind of accident from any previously
evaluated.
(3) Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
Despite the proposed change to the DG
maximum steady state frequency limit, the
DGs and equipment powered by the DGs will
continue to perform as originally designed,
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and originally analyzed in the UFSAR. There
is no associated change to the methods and
assumptions used to analyze DG
performance. The proposed change will
maintain the required function of the DGs
and the equipment powered by the DGs to
ensure that operation of structures, systems,
or components is as currently set forth in the
UFSAR. Therefore, the proposed change does
not involve a significant reduction in the
margin of safety.
The Nuclear Regulatory Commission
(NRC) staff has reviewed the licensee’s
analysis and, based on its own analysis,
it appears that the three standards of 10
CFR 50.92(c) are satisfied. Therefore, the
NRC staff proposes to determine that the
proposed amendment involves no
significant hazards consideration.
Attorney for licensee: Kimberly
Harshaw, Esquire, One Cook Place,
Bridgman, MI 49106.
NRC Acting Branch Chief: Travis L.
Tate.
Nuclear Management Company, LLC,
Docket No. 50–263, Monticello Nuclear
Generating Plant, Wright County,
Minnesota
Date of amendment request: July 9,
2007.
Description of amendment request:
The proposed amendment would revise
the Technical Specifications (TS), an
NRC-controlled document, by moving
the Table of Contents (TOC) out of the
TS and making the TOC into a licenseecontrolled document.
Basis for proposed no significant
hazards consideration determination:
As required by Title 10 of the Code of
Federal Regulations (10 CFR) Part
50.91(a), the licensee has provided its
analysis of the issue of no significant
hazards consideration (NSHC) which is
reproduced below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
No.
The proposed change is administrative and
affects control of a document, the TOC,
listing the specifications in the plant TS.
Transferring control from the NRC to NMC
(the licensee) does not affect the operation,
physical configuration, or function of plant
equipment or systems. It does not impact the
initiators or assumptions of analyzed events,
nor does it impact the mitigation of accidents
or transient events. The change has no
impact on, and hence cannot increase, the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
No.
The proposed change is administrative and
does not alter the plant configuration, require
installation of new equipment, alter
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assumptions about previously analyzed
accidents, or impact the operation or
function of plant equipment or systems.
Therefore, this change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
No.
The proposed change is administrative.
The TOC is not required by regulation to be
in the TS. [Its] removal does not impact any
safety assumptions or have the potential to
reduce a margin of safety as described in the
TS Bases. The change involves a transfer of
control of the TOC from the NRC to NMC. No
change in the technical content of the TS [
] is involved. Consequently, transfer from the
NRC to NMC has no impact on the margin
of safety, and hence cannot involve a
significant reduction in the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
analysis, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the proposed
amendment involves no significant
hazards consideration.
Attorney for licensee: Jonathan Rogoff,
Esquire, Vice President, Counsel &
Secretary, Nuclear Management
Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Acting Branch Chief: Travis L.
Tate.
PPL Susquehanna, LLC, Docket No. 50–
388, Susquehanna Steam Electric
Station, Unit 2
(SSES 2), Luzerne County,
Pennsylvania.
Date of amendment request: March 2,
2007.
Description of amendment request:
The proposed amendment would add an
ACTIONS Note 3 to the SSES 2
Technical Specification 3.8.1, ‘‘AC
Sources—Operating,’’ to allow a Unit 1
4160 volt subsystem to be de-energized
and removed from service to perform
bus maintenance.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
This change does not involve any physical
change to structures, systems, or components
(SSCs) and does not alter the method of
operation of any SSCs. The current
assumptions in the safety analysis regarding
accident initiators and mitigation of
accidents are unaffected by these changes. No
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SSC failure modes or mechanisms are being
introduced, and the likelihood of previously
analyzed failures remains unchanged.
Operation in accordance with the proposed
new ACTIONS Note 3 in Unit 2 Technical
Specification 3.8.1 ensures that the AC
[alternating current] distribution system and
supported equipment remain capable of
performing their functions as described in
the Final Safety Analysis Report (FSAR).
There are no changes to any accident
initiators or to the mitigating capability of
safety-related equipment supported by the
Class 1E Electrical AC system. The protection
provided by these safety-related systems will
continue to be provided as assumed by the
safety analysis.
Therefore, this proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not involve a
physical alteration of any plant equipment.
No new equipment is being introduced, and
installed equipment is not being operated in
a new or different manner. There are no
setpoints, at which protective or mitigative
actions are initiated, affected by this change.
This change does not alter the manner in
which equipment operation is initiated, nor
will the function demands on credited
equipment be changed. No alterations in the
procedures that ensure the plant remains
within analyzed limits are being proposed,
and no changes are being made to the
procedures relied upon to respond to an offnormal event as described in the FSAR [final
safety analysis report]. As such, no new
failure modes are being introduced. The
change does not alter assumptions made in
the safety analysis and licensing basis.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The margin of safety is established through
equipment design, operating parameters, and
the setpoints at which automatic actions are
initiated. The proposed change is acceptable
because the new ACTIONS Note 3 has been
established to be consistent with the existing
completion times for declaring required
equipment inoperable that has no offsite
power or DG [diesel generator] power
available. Therefore, the plant response to
analyzed events is not affected by this change
and will continue to provide the margin of
safety assumed by the safety analysis.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
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amendment request involves no
significant hazards consideration.
Attorney for licensee: Bryan A. Snapp,
Esquire, Assoc. General Counsel, PPL
Services Corporation, 2 North Ninth St.,
GENTW3, Allentown, PA 18101–1179.
NRC Branch Chief: Mark G. Kowal.
PSEG Nuclear LLC, Docket No. 50–354,
Hope Creek Generating Station, Salem
County, New Jersey
Date of amendment request: July 26,
2007
Description of amendment request:
The proposed amendment would
remove values for turbine first stage
pressure equivalent to Pbypass from the
Technical Specifications. Pbypass is the
reactor power level below which the
turbine stop valve closure and the
turbine control valve fast closure reactor
protection system trip functions and the
end-of-cycle recirculation pump trip are
bypassed automatically.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed removal of values for turbine
first stage pressure associated with Pbypass
from the Technical Specifications does not
alter the requirements for component
operability or surveillance currently in the
Technical Specifications. The proposed
change will have no impact on any safety
related structures, systems or components.
The probability of occurrence of a
previously evaluated accident is not
increased because this change does not
introduce any new potential accident
initiating conditions. The consequences of
accidents previously evaluated in the UFSAR
[Updated Final Safety Analysis Report] are
not affected because the ability of the
components to perform their required
function is not affected.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change is administrative in
nature, and does not result in physical
alterations or changes in the method by
which any safety related system performs its
intended function. The proposed change
does not affect any safety analysis
assumptions. The proposed change does not
create any new accident initiators or involve
an activity that could be an initiator of an
accident of a different type.
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All components will continue to be tested
to the same requirements as defined in the
Technical Specification Surveillance
Requirements. The proposed revision does
not make changes in any method of testing
or how any safety related system performs its
safety functions.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed change to remove values for
turbine first stage pressure associated with
Pbypass from the Technical Specifications does
not alter the Technical Specification
requirements for reactor protection system
operability. The turbine first stage pressure
setpoint will be controlled in accordance
with plant procedures and will be verified
during post-installation testing.
The proposed change will not affect the
current Technical Specification requirements
or the components to which they apply.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. Jeffrie J.
Keenan, Esquire, PSEG Nuclear—N21,
P.O. Box 236, Hancocks Bridge, NJ
08038.
NRC Branch Chief: Harold K.
Chernoff.
STP Nuclear Operating Company,
Docket Nos. 50–498 and 50–499, South
Texas Project, Units 1 and 2, Matagorda
County, Texas
Date of amendment request: June 26,
2007.
Description of amendment request:
The proposed amendment would
modify the Technical Specifications
(TSs) to establish more effective and
appropriate action, surveillance, and
administrative requirements related to
ensuring the habitability of the control
room envelope (CRE) in accordance
with Nuclear Regulatory Commission
(NRC)-approved TS Task Force (TSTF)
Standard Technical Specification
change traveler TSTF–448, Revision 3,
‘‘Control Room Habitability.’’
Specifically, the proposed amendment
would modify TS 3.7.7, Control Room
Makeup and Cleanup Filtration System
(CRMCFS) and TS Section 6.8,
‘‘Administrative Controls-Procedures,
Programs, and Manuals.’’ The NRC staff
issued a ‘‘Notice of Availability of
Technical Specification Improvement to
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Modify Requirements Regarding Control
Room Envelope Habitability Using the
Consolidated Line Item Improvement
Process’’ associated with TSTF–448,
Revision 3, in the Federal Register on
January 17, 2007 (72 FR 2022). The
notice included a model safety
evaluation, a model no significant
hazards consideration (NSHC)
determination, and a model license
amendment request. In its application
dated June 26, 2007, the licensee
affirmed the applicability of the model
NSHC determination which is presented
below.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of NSHC adopted
by the licensee is presented below:
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Criterion 1—The Proposed Change Does Not
Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated
The proposed change does not adversely
affect accident initiators or precursors nor
alter the design assumptions, conditions, or
configuration of the facility. The proposed
change does not alter or prevent the ability
of structures, systems, and components
(SSCs) to perform their intended function to
mitigate the consequences of an initiating
event within the assumed acceptance limits.
The proposed change revises the TS for the
CRE emergency ventilation system, which is
a mitigation system designed to minimize
unfiltered air leakage into the CRE and to
filter the CRE atmosphere to protect the CRE
occupants in the event of accidents
previously analyzed. An important part of
the CRE emergency ventilation system is the
CRE boundary. The CRE emergency
ventilation system is not an initiator or
precursor to any accident previously
evaluated. Therefore, the probability of any
accident previously evaluated is not
increased. Performing tests to verify the
operability of the CRE boundary and
implementing a program to assess and
maintain CRE habitability ensure that the
CRE emergency ventilation system is capable
of adequately mitigating radiological
consequences to CRE occupants during
accident conditions, and that the CRE
emergency ventilation system will perform as
assumed in the consequence analyses of
design basis accidents. Thus, the
consequences of any accident previously
evaluated are not increased. Therefore, the
proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
Criterion 2—The Proposed Change Does Not
Create the Possibility of a New or Different
Kind of Accident from any Accident
Previously Evaluated
The proposed change does not impact the
accident analysis. The proposed change does
not alter the required mitigation capability of
the CRE emergency ventilation system, or its
functioning during accident conditions as
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assumed in the licensing basis analyses of
design basis accident radiological
consequences to CRE occupants. No new or
different accidents result from performing the
new surveillance or following the new
program. The proposed change does not
involve a physical alteration of the plant (i.e.,
no new or different type of equipment will
be installed) or a significant change in the
methods governing normal plant operation.
The proposed change does not alter any
safety analysis assumptions and is consistent
with current plant operating practice.
Therefore, this change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
Criterion 3—The Proposed Change Does Not
Involve a Significant Reduction in the
Margin of Safety
The proposed change does not alter the
manner in which safety limits, limiting safety
system settings or limiting conditions for
operation are determined. The proposed
change does not affect safety analysis
acceptance criteria. The proposed change
will not result in plant operation in a
configuration outside the design basis for an
unacceptable period of time without
compensatory measures. The proposed
change does not adversely affect systems that
respond to safely shut down the plant and to
maintain the plant in a safe shutdown
condition. Therefore, the proposed change
does not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
analysis adopted by the licensee and,
based on this review, it appears that the
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the request
for amendments involves NSHC.
Attorney for licensee: A. H.
Gutterman, Esq., Morgan, Lewis &
Bockius, 1111 Pennsylvania Avenue,
NW., Washington, DC 20004.
NRC Branch Chief: Thomas G. Hiltz.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Units 1 and
2, Somervell County, Texas.
Date of amendment request: April 10,
2007.
Brief description of amendments: The
proposed amendments would revise
Technical Specifications (TS) 3.1,
‘‘Reactivity Control Systems,’’ TS 3.2,
‘‘Power Distribution Limits,’’ TS 3.3,
‘‘Instrumentation,’’ and TS 5.6.5b, ‘‘Core
Operating Limits Report (COLR).’’ The
requested change proposes to
incorporate standard Westinghousedeveloped and NRC-approved analytical
methods into the lists of methodologies
used to establish the core operating
limits.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
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licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
No physical plant changes or changes in
manner in which the plant will be operated
as a result of the methodology changes. The
proposed changes do not impact the
condition or performance of any plant
structure, system or component. The core
operating limits are established to support
Technical Specifications 3.1, 3.2, 3.3, and
3.4. The core operating limits ensure that fuel
design limits are not exceeded during any
conditions of normal operation or in the
event of any Anticipated Operational
Occurrence (AOO). The methods used to
establish the core operating limits for each
operating cycle are based on methods
previously found acceptable by the NRC and
listed in Technical Specifications section
5.6.5.b. Application of these NRC-approved
methods will continue to ensure that
acceptable operating limits are established to
protect the fuel cladding integrity during
normal operation and AOOs. The requested
Technical Specification changes, including
those changes proposed to conform with the
NRC-approved analysis methodologies, do
not involve any plant modifications or
operational changes that could affect system
reliability, performance, or possibility of
operator error. The requested changes do not
affect any postulated accident precursors,
does not affect any accident mitigation
systems, and does not introduce any new
accident initiation mechanisms.
As a result, the proposed changes to the
CPSES [Comanche Peak Steam Electric
Station] Technical Specifications do not
involve any increase in the probability or the
consequences of any accident or malfunction
of equipment important to safety previously
evaluated since neither accident probabilities
nor consequences are being affected by this
proposed change.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
There are no physical changes being made
to the plant. No new modes of plant
operation are being introduced. The
parameters assumed in the analyses are
within the design limits of the existing plant
equipment. All plant systems will perform as
designed during the response to a potential
accident.
Therefore, the proposed change to the
CPSES Technical Specifications does not
create the possibility of a new or different
kind of accident or malfunction of equipment
important to safety from any accident
previously evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The NRC-approved accident analysis
methodologies include restrictions on the
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choice of inputs, the degree of conservatism
inherent in the calculations, and specified
event acceptance criteria. Analyses
performed in accordance with these
methodologies will not result in adverse
effects on the regulated margin of safety.
Similarly, the use of axial power distribution
controls based on the relaxed axial offset
control strategy is a time-proven and NRCapproved method. The method is consistent
with the accident analyses assumptions as
described in the list of NRC-approved
methodologies proposed to be used to
establish the core operating limits. Finally,
the proposed changes to allow operation with
the BEACON [Best Estimate Analyzer for
Core Operation Nuclear] power distribution
monitoring tool provide additional
information to the reactor operators on the
state of the reactor core. Again, the use of the
BEACON tool and the methodology used to
develop the inputs to the tool are consistent
with and controlled by the NRC-approved
methodologies used to establish the core
operating limits. As such, the margin of
safety assumed in the plant safety analysis is
not adversely affected by the proposed
changes.
Based on the above evaluations, TXU
Power concludes that the proposed
amendment(s) present no significant hazards
consideration under the standards set forth in
10 CFR 50.92(c) and, accordingly, a finding
of no significant hazards consideration is
justified.
mstockstill on PROD1PC66 with NOTICES
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: George L. Edgar,
Esq., Morgan, Lewis and Bockius, 1800
M Street, NW., Washington, DC 20036.
NRC Branch Chief: Thomas G. Hiltz.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Units 1 and
2, Somervell County, Texas
Date of amendment request: May 22,
2007.
Brief description of amendments: The
proposed amendment would revise the
Technical Requirements Surveillance
(TRS) 13.3.33.2, Cycling Frequency for
the Turbine Stop and Control Valves.
The proposed change would increase
the frequency interval for the turbine
stop and control valves testing from 12
to 26 weeks.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
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16:35 Aug 13, 2007
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consequences of an accident previously
evaluated?
Response: No.
The proposed change will increase the
frequency interval for testing the high
pressure (HP) and low pressure (LP) turbine
stop and control valves to 26 weeks. This test
requires the movement of the HP and LP
turbine valves through one complete cycle
once every 26 weeks. The test verifies
freedom of movement of the valve
components and is beneficial in early
detection of problems with valve operation.
[The test ensures that all turbine steam inlet
valves are capable of closing to protect the
turbine from excessive overspeed, which
could generate potentially damaging
missiles.]
Siemens, the turbine manufacturer for
Comanche Peak Steam Electric Station
(CPSES), has evaluated the change in the
probability of generating external/hightrajectory turbine missiles resulting from a
hypothetical LP turbine disk failure which
could adversely affect safety-related SSCs
[structures, systems, and components] due to
the change in the surveillance interval weeks
using a previously approved missile
probability analysis methodology. The results
of the analysis show the new valve test
interval of 26 weeks with a turbine
inspection interval of 100,000 hours is safe
and acceptable as the probability of
occurrence of a turbine missile per turbine
year is less than the Nuclear Regulatory
Commission (NRC) limit of 1E–4 per 8760
hours (turbine year) or 11.42E–4 at 100,000
hours (Reference 7.4 [of the licensee’s May
22, 2007, application]). Therefore, the risk of
the loss of an essential system from a single
event is acceptable. Since the probability of
generating external, high-trajectory turbine
missiles resulting from a hypothetical LP
turbine disc failure which could adversely
affect safety related SSCs due to the
increased valve test interval from 12 to 26
weeks is less than the NRC limit, it is
acceptable to increase the turbine test
interval in TRS 13.3.33.2. The test interval
change would increase overall plant capacity
factor and result in a net improvement in
plant safety by reducing the likelihood of
plant trips and stress and wear on plant
components. In addition, the increased test
intervals would reduce the likely cause of a
plant transient and unnecessary burden on
personnel resources which is consistent with
Generic Letter 93–005 (Reference 7.7 [of the
licensee’s May 22, 2007, application]) and
NUREG–1366 (Reference 7.2 [of the
licensee’s May 22, 2007, application]). Based
upon Siemens’ analysis and the updated stop
and control valves failure probability, it is
concluded that the implementation of this
change in testing frequency will not increase
the probability or consequences of an
accident previously evaluated in the UFSAR.
The proposed change does not adversely
affect accident initiators or precursors nor
alter the design assumptions, conditions, or
configuration of the facility or the manner in
which the plant is operated and maintained.
The proposed change does not alter or
prevent the ability of structures, systems, and
components (SSCs) from performing their
intended function to mitigate the
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consequences of an initiating event within
the assumed acceptance limits. The proposed
change does not affect the source term,
containment isolation, or radiological release
assumptions used in evaluating the
radiological consequences of an accident
previously evaluated. The proposed change
is consistent with safety analysis
assumptions and resultant consequences.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change will reduce the
frequency for testing the high pressure (HP)
and low pressure (LP) turbine stop and
control valves. Turbine overspeed is limited
by rapid closure of the turbine stop and
control valves. Turbine overspeed can result
in the occurrence of turbine missiles from a
burst type failure of the low pressure blades
or disks. The damage from turbine missiles
has been previously evaluated in the UFSAR
[updated final safety analysis report]
(Reference 7.3 [of the licensee’s May 22,
2007, application]). The proposed activity
does not introduce the possibility of a new
accident because no new failure modes are
introduced.
Turbine overspeed with the resulting
turbine missiles is the only accident
potentially affected by failure of the turbine
stop and control valves. The turbine missile
analysis is not altered by reducing the
frequency of high and low pressure stop and
control valve testing. Reducing the frequency
of turbine valve testing from every 12 weeks
to every 26 weeks does not result in a
significant change in the failure rate, nor
does it affect the failure modes for the turbine
valves.
There are no hardware changes nor are
there any changes in the method by which
any safety-related plant system performs its
safety function. This amendment will not
affect the normal method of plant operation
or change any operating parameters. No
performance requirements or response time
limits will be affected. No new accident
scenarios, transient precursors, failure
mechanisms, or limiting single failures are
introduced as a result of this amendment.
There will be no adverse effect or challenges
imposed on any safety-related system as a
result of this amendment.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The proposed change does not involve a
significant reduction in a margin of safety
since the conclusions of the safety analyses
in the CPSES FSAR [final safety analysis
report] (Reference 7.3 [of the licensee’s May
22, 2007, application]) are essentially
unchanged and NRC safety limits are not
exceeded.
Therefore the proposed change does not
involve a reduction in a margin of safety.
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Based on the above evaluations, TXU
Power concludes that the proposed
amendment(s) present no significant hazards
under the standards set forth in 10 CFR
50.92(c) and, accordingly, a finding of ‘‘no
significant hazards consideration’’ is
justified.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: George L. Edgar,
Esq., Morgan, Lewis and Bockius, 1800
M Street, NW., Washington, DC 20036.
NRC Branch Chief: Thomas G. Hiltz.
Virginia Electric and Power Company,
Docket Nos. 50–280 and 50–281, Surry
Power Station, Unit Nos. 1 and 2, Surry
County, Virginia
mstockstill on PROD1PC66 with NOTICES
Date of amendment request: July 13,
2007.
Description of amendment request:
The proposed amendment revises the
Technical Specifications (TSs)
requirements related to main control
room and emergency switchgear room
envelope habitability. These changes are
consistent with the Nuclear Regulatory
Commission (NRC)-approved Revision 3
of Technical Specification Task Force
(TSTF) Standard Technical
Specifications (STS) Change Traveler
TSTF–448, ‘‘Control Room
Habitability.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
1. Involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The proposed changes consist of TS
wording, format and conforming changes to
facilitate incorporation of TSTF–448 [72 FR
2022] into the Surry custom TS and for
consistency with NUREG–1431, Revision 3,
to the extent practical. The proposed changes
are administrative in nature and, as such, do
not impact the condition or performance of
any plant structure, system or component.
The proposed changes do not affect the
initiators of any previously analyzed event or
the assumed mitigation of accident or
transient events. As a result, the proposed
administrative changes to the Surry TS do
not involve any increase in the probability or
the consequences of any accident or
malfunction of equipment important to safety
previously evaluated since neither accident
probabilities or consequences are being
affected by the proposed changes.
2. Create the possibility of a new or
different kind of accident from any accident
previously evaluated.
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The proposed changes are administrative
in nature, and therefore do not involve any
changes in station operation or physical
modifications to the plant. In addition, no
changes are being made in the methods used
to respond to plant transients that have been
previously analyzed. No changes are being
made to plant parameters within which the
plant is normally operated or in the
setpoints, which initiate protective or
mitigative actions, and no new failure modes
are being introduced. Therefore, the
proposed changes to the Surry Technical
Specifications do not create the possibility of
a new or different kind of accident or
malfunction of equipment important to safety
from any previously evaluated.
3. Involve a significant reduction in a
margin of safety.
The proposed changes consist of TS
wording, format and conforming changes to
facilitate incorporation of TSTF–448 into the
Surry custom TS and for consistency with
NUREG–1431, Revision 3. The proposed
changes are administrative in nature, and do
not impact station operation or any plant
structure, system or component that is relied
upon for accident mitigation. Furthermore,
the margin of safety assumed in the plant
safety analysis is not affected in any way by
the proposed changes. Therefore, the
proposed administrative changes to the Surry
Technical Specifications do not involve a
reduction in a margin of safety.
The NRC staff has reviewed the
analysis and, based on this review, it
appears that the three standards of 10
CFR 50.92(c) are satisfied. Therefore, the
NRC staff proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Lillian M.
Cuoco, Esq., Senior Counsel, Dominion
Resources Services, Inc., Millstone
Power Station, Building 475, 5th Floor,
Rope Ferry Road, Rt. 156, Waterford,
Connecticut 06385.
NRC Branch Chief: Evangelos C.
Marinos.
Previously Published Notices of
Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The following notices were previously
published as separate individual
notices. The notice content was the
same as above. They were published as
individual notices either because time
did not allow the Commission to wait
for this biweekly notice or because the
action involved exigent circumstances.
They are repeated here because the
biweekly notice lists all amendments
issued or proposed to be issued
involving no significant hazards
consideration.
For details, see the individual notice
in the Federal Register on the day and
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page cited. This notice does not extend
the notice period of the original notice.
Exelon Generation Company, LLC, and
PSEG Nuclear LLC,
Docket Nos. 50–277 and 50–278,
Peach Bottom Atomic Power Station,
Units 2 and 3, York and Lancaster
Counties, Pennsylvania
Date of amendment request: March 6,
2007.
Brief description of amendment
request: The proposed amendment
would modify the main steam isolation
valve (MSIV) leakage Technical
Specification (TS) Surveillance
Requirement (SR) 3.6.1.3.14 to establish
a total leakage rate limit for the sum of
the four main steam lines.
Date of publication of individual
notice in Federal Register: July 24,
2007.
Expiration date of individual notice:
September 22, 2007.
Tennessee Valley Authority, Docket No.
50–259, Browns Ferry Nuclear Plant,
Unit 1, Limestone County, Alabama
Date of application for amendments:
June 25, as supplemented July 3, 2007.
Description of amendments request:
The proposed amendment would allow
deletion of License Condition 2.(G)2
regarding the performance of power
uprate large transient testing.
Date of publication of individual
notice in the Federal Register: July 13,
2007 (72 FR 38627).
Expiration date of individual notice:
August 14, 2007 (Public comments) and
September 11, 2007 (Hearing requests).
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
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amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the internet at the
NRC web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
mstockstill on PROD1PC66 with NOTICES
AmerGen Energy Company, LLC, Docket
No. 50–219, Oyster Creek Nuclear
Generating Station, Ocean County, New
Jersey
Date of application for amendment:
September 28, 2006.
Brief description of amendment: The
amendment revises the Oyster Creek
Technical Specification (TS) definition
of Channel Calibration, Channel Check,
and Channel Test consistent with
NUREG–1433, Revision 3.0, ‘‘Standard
Technical Specifications General
Electric Plants, BWR/4 Specifications,’’
dated June 2004. These definitions
apply to all instrument functions in the
TSs, including Reactor Protection
System instruments.
Date of Issuance: July 27, 2007.
Effective date: As of the date of
Issuance to be implemented within 60
days.
Amendment No.: 263.
Facility Operating License No. DPR–
16: The amendment revised the TSs.
Date of initial notice in Federal
Register: November 21, 2006 (71 FR
67392). The Commission’s related
evaluation of this amendment is
contained in a Safety Evaluation dated
July 27, 2007.
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16:35 Aug 13, 2007
Jkt 211001
No significant hazards consideration
comments received: No.
Arizona Public Service Company, et al.,
Docket Nos. STN 50–528, STN 50–529,
and STN 50–530, Palo Verde Nuclear
Generating Station, Units Nos. 1, 2, and
3, Maricopa County, Arizona
Date of application for amendments:
July 20, 2006, as supplemented by letter
dated May 3, 2007.
Brief description of amendments: The
amendments revised Technical
Specifications (TS) 3.1.6, ‘‘Shutdown
Control Element Assembly (CEA)
Insertion Limits,’’ to modify the TS
Limiting Condition for Operation (LCO)
3.1.6 and Surveillance Requirements
(SRs) 3.1.6.1 to require shutdown CEAs
to be withdrawn to ≥147.75 inches,
instead of the current limit of ≥144.75
inches.
Date of issuance: July 25, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 90 days from the date of
issuance.
Amendment Nos.: Unit 1–168, Unit
2–168, Unit 3–168.
Facility Operating License Nos. NPF–
41, NPF–51, and NPF–74: The
amendments revised the Operating
License and Technical Specifications.
Date of initial notice in Federal
Register: September 26, 2006 (71 FR
56191). The supplement dated May 3,
2007, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register. The Commission’s
related evaluation of the amendment is
contained in a Safety Evaluation dated
July 25, 2007.
No significant hazards consideration
comments received: No.
Carolina Power & Light Company,
Docket No. 50–261, H. B. Robinson
Steam Electric Plant, Unit No. 2,
Darlington County, South Carolina
Date of application for amendment:
February 2, 2007.
Brief description of amendment: This
amendment deletes the technical
specification (TS) requirements related
to containment hydrogen monitors and
supports implementation of the
revisions of 10 CFR 50.44, Combustible
Gas Control for Nuclear Power Reactors,
that became effective on October 16,
2003. This is a Consolidated Line Item
Improvement Program modification,
which adopts TS Task Force (TSTF)
Standard TS Change Traveler, TSTF–
447, Elimination of Hydrogen
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Recombiners and Change to Hydrogen
and Oxygen Monitors.
Date of issuance: July 16, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 216.
Renewed Facility Operating License
No. DPR–23: Amendment revises the
technical specifications.
Date of initial notice in Federal
Register: April 24, 2007 (72 FR 20378).
The Commission’s related evaluation of
the amendment is contained in a safety
evaluation dated March 21, 2007.
No significant hazards consideration
comments received: No.
Carolina Power & Light Company, et al.,
Docket No. 50–400, Shearon Harris
Nuclear Power Plant, Unit 1, Wake and
Chatham Counties, North Carolina
Date of application for amendment:
December 20, 2006.
Brief description of amendment: This
amendment revises Technical
Specification (TS) 6.12, ‘‘High Radiation
Area.’’ The amendment aligns the
requirements contained in the TS with
the revised Regulatory Guide 8.38,
Revision 1, ‘‘Control of Access to High
and Very High Radiation Areas in
Nuclear Power Plants.’’ Specifically, the
changes include differentiating dose
rates associated with high and very high
radiation areas, adding requirements for
groups entering high radiation areas,
and clarifying the communication
requirements for workers in high
radiation areas.
Date of issuance: July 23, 2007.
Effective date: This amendment is
effective as of the date of issuance and
shall be implemented within 60 days of
issuance.
Amendment No.: 125.
Facility Operating License No. NPF–
63: Amendment revises the TSs.
Date of initial notice in Federal
Register: February 27, 2007 (72 FR
8802). The Commission’s related
evaluation of the amendment is
contained in a safety evaluation dated
July 23, 2007.
No significant hazards consideration
comments received: No.
Duke Power Company LLC, Docket Nos.
50–369 and 50–370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg
County, North Carolina
Date of application for amendments:
July 31, 2006 as supplemented May 24,
2007.
Brief description of amendments: The
amendments revised TS 3.6.3,
‘‘Containment Isolation Valves,’’ by
removing the allowance to open the
upper containment purge isolation
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mstockstill on PROD1PC66 with NOTICES
valves in the applicable modes of
operation when containment integrity is
required by the TSs. In addition, the
amendments deleted TS 3.3.6,
‘‘Containment Purge and Exhaust
Isolation Instrumentation’’. The change
made the TSs requirements consistent
for both the upper and lower
containment purge isolation valves.
Date of issuance: July 26, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 243, 224.
Renewed Facility Operating License
Nos. NPF–9 and NPF–17: Amendments
revised the licenses and the technical
specifications.
Date of initial notice in Federal
Register: December 5, 2006 (71 FR
70558) The supplement dated May 24,
2007, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination. The Commission’s
related evaluation of the amendments is
contained in a Safety Evaluation dated
July 26, 2007.
No significant hazards consideration
comments received: No.
FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–440,
Perry Nuclear Power Plant, Unit No. 1,
Lake County, Ohio
Date of application for amendment:
February 10, 2006, as supplemented by
letter dated March 8, 2007.
Brief description of amendment: The
changes would clarify technical
specifications (TSs) for the Perry
Nuclear Power Plant (PNPP) by revising
the TS action requirements that must be
followed when one or more annulus gas
treatment system initiation channels are
inoperable. The clarifying changes will
make the PNPP TSs consistent with
Nuclear Regulatory Commission (NRC)
staff precedents for containment
filtering safety systems that operate
continuously in the protection mode of
operation.
Date of issuance: July 30, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 120 days.
Amendment No.: 147.
Facility Operating License No. NPF–
58: This amendment revised the
Technical Specifications and License.
Date of initial notice in Federal
Register: May 23, 2006 (71 FR 29678).
The March 8, 2007, supplement
contained clarifying information and
did not change the NRC staff’s initial
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17:55 Aug 13, 2007
Jkt 211001
proposed finding of no significant
hazards consideration. The
Commission’s related evaluation of the
amendment is contained in a Safety
Evaluation dated July 30, 2007.
No significant hazards consideration
comments received: No.
Florida Power and Light Company,
Docket Nos. 50–250 and 50–251, Turkey
Point Plant, Units 3 and 4, Miami-Dade
County, Florida
Date of application for amendments:
January 27, 2006, as supplemented
November 28, 2006, April 30, 2007, and
July 17, 2007.
Brief description of amendments:
These amendments revise Technical
Specifications (TS) Section 3/4 9.1,
‘‘Boron Concentration,’’ Section 3/4
9.14, ‘‘Spent Fuel Storage,’’ and Section
3/4 5.5.1, ‘‘Fuel Storage Criticality’’ to
allow use of Metamic rack inserts, and
administrative controls that require
mixing higher reactivity fuel with
lower-reactivity fuel.
Date of issuance: July 17, 2007.
Effective date: As of the date of
issuance and shall be implemented
prior to the end of Unit 4 Cycle 24.
Amendment Nos: 234 and 229.
Renewed Facility Operating License
Nos. DPR–31 and DPR–41: Amendments
revised the TS.
Date of initial notice in Federal
Register: May 9, 2006 (71 FR 26999).
The supplements dated November 28,
2006, April 30, 2007, and July 17, 2007,
provided additional information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the staff’s
original proposed no significant hazards
consideration determination as
published in the Federal Register on
May 9, 2006.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated July 17, 2007.
No significant hazards consideration
comments received: No.
Nuclear Management Company, Docket
No. 50–263, Monticello Nuclear
Generating Plant (MNGP), Wright
County, Minnesota
Date of application for amendment:
January 29, 2007, as supplemented on
June 5, 2007.
Brief description of amendment: The
amendment revised Table 3.3.5.1–1 of
the Technical Specifications for three
low-pressure coolant injection loop
select logic functions. The surveillance
of these three functions was previously
required to be performed every 92 days.
The amended requirement requires a
channel calibration and logic system
functional test, respectively, every 24
PO 00000
Frm 00054
Fmt 4703
Sfmt 4703
45465
months. In addition, the allowable
values associated with these three
functions are changed to match the
extended surveillance interval.
Date of issuance: July 20, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment No: 151.
Renewed Facility Operating License
No. DPR–22: Amendment revised the
Renewed Facility Operating License and
Technical Specifications.
Date of initial notice in Federal
Register: March 13, 2007 (72 FR
11391).
The supplemental letter dated June 5,
2007, contained clarifying information
and did not change the initial no
significant hazards consideration
determination, and did not expand the
scope of the original Federal Register
notice.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated July 20, 2007.
No significant hazards consideration
comments received: No.
STP Nuclear Operating Company,
Docket Nos. 50–498 and 50–499, South
Texas Project, Units 1 and 2, Matagorda
County, Texas
Date of amendment request: February
28, 2006, as supplemented by letters
dated April 6 and May 31, 2007, and
electronic mail dated July 18, 2007.
Brief description of amendments: The
amendments revised TSs 3/4.8.2.1, ‘‘DC
[Direct Current] Sources—Operating,’’
and 3/4.8.2.2, ‘‘DC Sources—
Shutdown,’’ and add a new TS 3/
4.8.2.3, ‘‘Battery Parameters.’’ The
amendments revised allowed outage
times for battery chargers as well as
battery charger testing criteria, and
relocate a number of battery
surveillance requirements to a licenseecontrolled Battery Monitoring and
Maintenance Program. The changes are
consistent with Standard TS Change
Traveler TSTF–360, Revision 1, ‘‘DC
Electrical Rewrite.’’
Date of issuance: July 20, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 120 days of issuance.
Amendment Nos.: Unit 1–180; Unit
2–167.
Facility Operating License Nos. NPF–
76 and NPF–80: The amendments
revised the Facility Operating Licenses
and Technical Specifications.
Date of initial notice in Federal
Register: September 12, 2006 (71 FR
53721). The supplemental letters dated
April 6 and May 31, 2007, and
electronic mail dated July 18, 2007,
provided additional information that
E:\FR\FM\14AUN1.SGM
14AUN1
45466
Federal Register / Vol. 72, No. 156 / Tuesday, August 14, 2007 / Notices
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the staff’s
original proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated July 20, 2007.
No significant hazards consideration
comments received: No.
Dated at Rockville, Maryland, this 2nd day
of August 2007.
For the Nuclear Regulatory Commission.
Catherine Haney,
Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. E7–15459 Filed 8–13–07; 8:45 am]
BILLING CODE 7590–01–P
NUCLEAR REGULATORY
COMMISSION
Notice of Availability of the Final
License Renewal Interim Staff
Guidance LR–ISG–2006–03: Staff
Guidance for Preparing Severe
Accident Mitigation Alternatives
Analyses
Nuclear Regulatory
Commission (NRC).
ACTION: Notice of Availability.
mstockstill on PROD1PC66 with NOTICES
AGENCY:
SUMMARY: NRC is issuing its Final
License Renewal Interim Staff Guidance
LR–ISG–2006–03 for preparing severe
accident mitigation alternatives (SAMA)
analyses. This LR–ISG recommends that
applicants for license renewal use the
Guidance Document Nuclear Energy
Institute 05–01, Revision A, (ADAMS
Accession No. ML060530203) when
preparing their SAMA analyses. The
NRC staff issues LR–ISGs to facilitate
timely implementation of the license
renewal rule and to review activities
associated with a license renewal
application. The NRC staff will also
incorporate the approved LR–ISG into
the next revision of Supplement 1 to
Regulatory Guide 4.2, ‘‘Preparation of
Supplemental Environmental Reports
for Applications to Renew Nuclear
Power Plant Operating Licenses.’’
ADDRESSES: The NRC maintains an
Agencywide Documents Access and
Management System (ADAMS), which
provides text and image files of NRC’s
public documents. These documents
may be accessed through the NRC’s
Public Electronic Reading Room on the
Internet at https://www.nrc.gov/readingrm/adams.html. Persons who do not
have access to ADAMS or who
encounter problems in accessing the
documents located in ADAMS should
VerDate Aug<31>2005
16:35 Aug 13, 2007
Jkt 211001
contact the NRC Public Document Room
(PDR) reference staff at 1–800–397–
4209, 301–415–4737, or by e-mail at
pdr@nrc.gov.
FOR FURTHER INFORMATION CONTACT: Mr.
Richard L. Emch, Jr., Senior Project
Manager, Office of Nuclear Reactor
Regulation, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001; telephone 301–415–1590 or by email at rle@nrc.gov.
SUPPLEMENTARY INFORMATION:
Attachment 1 to this Federal Register
notice, entitled Staff Position and
Rationale for the Final License Renewal
Interim Staff Guidance LR–ISG–2006–
03: Staff Guidance for Preparing Severe
Accident Mitigation Alternatives
(SAMA) Analyses contains the NRC
staff’s rationale for publishing the Final
LR–ISG–2006–03. Attachment 2 to this
Federal Register notice, entitled
Proposed License Renewal Interim Staff
Guidance LR–ISG–2006–03: Staff
Guidance for Preparing Severe Accident
Mitigation Alternatives (SAMA)
Analyses, contains the guidance for
preparing SAMA analyses related to
license renewal applications. The NRC
staff approves this LR–ISG for NRC and
industry use. The NRC staff will also
incorporate the approved LR–ISG into
the next revision of Supplement 1 to
Regulatory Guide 4.2, ‘‘Preparation of
Supplemental Environmental Reports
for Applications to Renew Nuclear
Power Plant Operating Licenses.’’
Dated at Rockville, Maryland, this 2nd day
of August 2007.
For the Nuclear Regulatory Commission.
Pao-Tsin Kuo,
Director, Division of License Renewal, Office
of Nuclear Reactor Regulation.
Attachment 1—Staff Position and
Rationale for the Final License Renewal
Interim Staff Guidance LR–ISG–2006–
03: Staff Guidance for Preparing Severe
Accident Mitigation Alternatives
Analyses
Staff Position: The NRC staff
recommends that applicants for license
renewal follow the guidance provided
in Nuclear Energy Institute (NEI) 05–01,
‘‘Severe Accident Mitigation
Alternatives (SAMA) Analysis—
Guidance Document,’’ Revision A, when
preparing their SAMA analyses.
Rationale: The NEI developed a
generic Guidance Document NEI 05–01,
Revision A, to help clarify the NRC
staff’s expectations regarding the
information that needs to be included in
SAMA analyses. The NRC staff
reviewed and concluded that NEI 05–
01, Revision A, describes existing NRC
regulations and facilitates complete
preparation of SAMA analysis
PO 00000
Frm 00055
Fmt 4703
Sfmt 4703
submittals. The staff finds that
utilization of the guidance provided in
NEI 05–01, Revision A, will result in
improved quality in SAMA analyses
and a reduction in the number of
requests for additional information.
Attachment 2—Final License Renewal
Interim Staff Guidance LR–ISG–2006–
03: Staff Guidance for Preparing Severe
Accident Mitigation Alternatives
Analyses
Introduction
A severe accident mitigation
alternatives (SAMA) analyses is
required as part of a license renewal
application, if a SAMA analysis has not
already been performed for the plant
and reviewed by the NRC staff. SAMA
analyses have been performed and
submitted to the NRC for all
applications for license renewal
received by the staff thus far. Therefore,
this LR–ISG is being recommended as
guidance consistent with our goal to
more effectively and efficiently resolve
license renewal issues identified by the
staff or the industry.
Background and Discussion
After receiving extensive requests for
additional information regarding the
SAMA analyses, several applicants for
license renewal concluded that they did
not fully understand the kind of
information that the NRC staff was
expecting to see in SAMA analyses.
The Nuclear Energy Institute (NEI)
developed a generic guidance document
to help clarify the NRC staff’s
expectations regarding the information
that should be submitted in SAMA
analyses. On April 8, 2005, NEI
submitted NEI 05–01, ‘‘Severe Accident
Mitigation Alternatives (SAMA)
Analysis—Guidance Document.’’ The
NRC staff reviewed this guidance
document, and by letter, dated July 12,
2005, provided comments on NEI 05–
01. The NRC staff’s comments were
discussed during a public meeting
between NEI and NRC on July 21, 2005.
On February 17, 2006, NEI submitted
its NEI 05–01, Revision A, dated
November 2005. The NRC staff reviewed
and concluded that this version fully
resolved the NRC staff’s comments. In
addition, the NRC staff concluded that
NEI 05–01, Revision A, describes
existing NRC regulations, and facilitates
complete preparation of SAMA analysis
submittals.
Some applicants for license renewal
have submitted SAMA analyses using
the guidance provided in NEI 05–01,
Revision A. The NRC staff found
improved quality in the submitted
SAMA analyses and a reduction in the
E:\FR\FM\14AUN1.SGM
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[Federal Register Volume 72, Number 156 (Tuesday, August 14, 2007)]
[Notices]
[Pages 45454-45466]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: E7-15459]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from July 19, 2007, to August 1, 2007. The last
biweekly notice was published on July 31, 2007 (72 FR 41780).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
[[Page 45455]]
Written comments may be submitted by mail to the Chief, Rulemaking,
Directives and Editing Branch, Division of Administrative Services,
Office of Administration, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, and should cite the publication date and
page number of this Federal Register notice. Written comments may also
be delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike,
Rockville, Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received may be examined at the Commission's
Public Document Room (PDR), located at One White Flint North, Public
File Area O1F21, 11555 Rockville Pike (first floor), Rockville,
Maryland. The filing of requests for a hearing and petitions for leave
to intervene is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
[[Page 45456]]
Calvert Cliffs Nuclear Power Plant, Inc., Docket Nos. 50-317 and 50-
318, Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert
County, Maryland
Date of amendments request: June 29, 2007.
Description of amendments request: The amendment would modify
Technical Specification (TS) requirements related to control room
envelope (CRE) habitability in TS 3.7.8, ``Control Room Emergency
Ventilation System (CREVS),'' and TS 5.5, ``Programs and Manuals.'' The
changes are consistent with the Nuclear Regulatory Commission approved
Technical Specification Task Force (TSTF)-448, Revision 3, ``Control
Room Habitability.'' The availability of the TS improvement was
published in the Federal Register on January 17, 2007 (72 FR 2022) as
part of the consolidated item improvement process (CLIIP). In addition,
the amendment would remove a footnote currently contained in the
Completion Time of TS 3.7.8, Required Action D. The footnote was added
in Amendment Nos. 250/227 and was only applicable during the Unit 1
2002 refueling outage.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change does not adversely affect accident
initiators or precursors nor alter the design assumptions,
conditions, or configuration of the facility. The proposed change
does not alter or prevent the ability of structures, systems, and
components (SSCs) to perform their intended function to mitigate the
consequences of an initiating event within the assumed acceptance
limits. The proposed change revises the TS for the CRE emergency
ventilation system, which is a mitigation system designed to
minimize unfiltered air leakage into the CRE and to filter the CRE
atmosphere to protect the CRE occupants in the event of accidents
previously analyzed. An important part of the CRE emergency
ventilation system is the CRE boundary. The CRE emergency
ventilation system is not an initiator or precursor to any accident
previously evaluated. Therefore, the probability of any accident
previously evaluated is not increased. Performing tests to verify
the operability of the CRE boundary and implementing a program to
assess and maintain CRE habitability ensure that the CRE emergency
ventilation system is capable of adequately mitigating radiological
consequences to CRE occupants during accident conditions, and that
the CRE emergency ventilation system will perform as assumed in the
consequence analyses of design basis accidents. Thus, the
consequences of any accident previously evaluated are not increased.
The removal of a footnote [to TS 3.7.8] that is no longer
applicable is an editorial change that does not affect accident
initiators or precursors, nor alter the design assumptions,
conditions or configuration of the facility. The proposed change
also does not affect the ability of SSCs to perform their intended
function to mitigate the consequences of an accident. Therefore, the
proposed editorial change does not increase the probability or
consequences of an accident previously evaluated.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change does not impact the accident analysis. The
proposed change does not alter the required mitigation capability of
the CRE emergency ventilation system, or its functioning during
accident conditions as assumed in the licensing basis analyses of
design basis accident radiological consequences to CRE occupants. No
new or different accidents result from performing the new
surveillance or following the new program. The proposed change does
not involve a physical alteration of the plant (i.e., no new or
different type of equipment will be installed) or a significant
change in the methods governing normal plant operation. The proposed
change does not alter any safety analysis assumptions and is
consistent with current plant operating practice.
The proposed change is the editorial removal of a footnote [to
TS 3.7.8] that no longer applies. The removal of a footnote that no
longer applies does not impact the accident analyses. Additionally,
it does not add or modify any existing plant equipment and does not
introduce any new operational methods. Therefore, the proposed
editorial change does not create the possibility of a new or
different kind of accident from any accident previously evaluated.
Therefore, this change does not create the possibility of a new
or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change does not alter the manner in which safety
limits, limiting safety system settings or limiting conditions for
operation are determined. The proposed change does not affect safety
analysis acceptance criteria. The proposed change will not result in
plant operation in a configuration outside the design basis for an
unacceptable period of time without compensatory measures. The
proposed change does not adversely affect systems that respond to
safely shut down the plant and to maintain the plant in a safe
shutdown condition.
The proposed editorial change [removal of a footnote to TS
3.7.8] does not affect safety analyses acceptance criteria or safety
system operation. Removal of a footnote that is no longer applicable
does not result in plant operation outside the design basis.
Therefore, the proposed editorial change does not involve a
reduction in the margin of safety.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Carey Fleming, Sr. Counsel--Nuclear
Generation, Constellation Generation Group, LLC, 750 East Pratt Street,
17th floor, Baltimore, MD 21202.
NRC Branch Chief: Mark G. Kowal.
Exelon Generation Company, LLC, Docket Nos. 50-352 and 50-353, Limerick
Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
Date of amendment request: February 20, 2007.
Description of amendment request: The proposed change would revise
Limerick Generating Station (LGS), Units 1 and 2, Technical
Specifications (TSs), Section 6.8.4.g, ``Primary Containment Leakage
Rate Testing Program,'' to allow a one-time extension of no more than 5
years for the Type A, Integrated Leakage Rate Test (ILRT) interval.
This revision is a one-time exception to the 10-year frequency of the
performance-based leakage rate testing program for Type A tests as
defined in Nuclear Energy Institute (NEI) document NEI 94-01, Revision
0, ``Industry Guideline For Implementing Performance-Based Option of 10
CFR Part 50, Appendix J,'' pursuant to Title 10 of the Code of Federal
Regulations (10 CFR) Part 50, Appendix J, Option B. The requested
exception is to allow the ILRT to be performed within 15 years from the
last ILRT as opposed to the current 10-year frequency. The most recent
containment Type A ILRTs for LGS Units 1 and 2 were performed on May
15, 1998, and May 21, 1999, respectively.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or
[[Page 45457]]
consequences of an accident previously evaluated?
Response: No.
The proposed change will revise TS 6.8.4.g (``Primary
Containment Leakage Rate Testing Program'') of the LGS, Units 1 and
2 TS to reflect a one-time extension to the Type A Integrated Leak
Rate Test (ILRT) as currently specified in the Technical
Specifications. This change will extend the requirement to perform
the Type A ILRT from the current requirement of 10 to 15 years,
which is ``no later than May 15, 2013'' for LGS, Unit 1 and is ``no
later than May 21, 2014'' for Unit 2.
The function of the containment is to isolate and contain
fission products released from the reactor coolant system following
a design basis Loss of Coolant Accident (LOCA) and to confine the
postulated release of radioactive material to within limits. The
test interval associated with Type A ILRTs is not a precursor of any
accident previously evaluated. Type A ILRTs provide assurance that
the LGS, Units 1 and 2 containments will not exceed allowable
leakage rate values specified in the TS and will continue to perform
their design function following an accident. The risk assessment of
the proposed change has concluded that there is an insignificant
increase in Large Early Release Frequency, Person-Rem, and
Conditional Containment Failure Frequency. Additionally, containment
inspections have also been performed which demonstrate the continued
structural integrity of the primary containment and will be
performed in the future as required by the ASME Code.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed change for a one-time extension of the Type A ILRTs
for LGS, Units 1 and 2 will not affect the control parameters
governing unit operation or the response of plant equipment to
transient and accident conditions. The proposed change does not
introduce any new equipment, modes of system operation or failure
mechanisms.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The integrity of the containment penetrations and isolation
valves is verified through Type B and Type C local leak rate tests
(LLRTs) and the overall leak tight integrity of the containment is
verified by a Type A ILRT, as required by 10 CFR 50, Appendix J,
``Primary Reactor Containment Leakage Testing for Water-Cooled Power
Reactors.'' These tests are performed to verify the essentially leak
tight characteristics of the containment at the design basis
accident pressure. The proposed change for a one-time extension of
the Type A ILRT does not affect the method for Type A, B or C
testing or the test acceptance criteria.
EGC has conducted a risk assessment to determine the impact of a
change to the LGS, Units 1 and 2 Type A ILRT from 10 to 15 years.
This risk assessment measured the impact to the Large Early Release
Frequency, Person-Rem, and Conditional Containment Failure
Frequency. This assessment indicated that the proposed LGS, Units 1
and 2 Type A ILRT interval extension has a very small change in risk
to the public and is an acceptable plant change from a risk
perspective.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. Bradley Fewell, Associate General
Counsel, Exelon Generation Company, LLC, 4300 Winfield Road,
Warrenville, IL 60555.
NRC Branch Chief: Harold K. Chernoff.
Florida Power and Light Company, Docket Nos. 50-335 and 50-389, St.
Lucie Plant, Units 1 and 2, St. Lucie County, Florida
Date of amendment request: June 4, 2007.
Description of amendment request: The proposed amendment would
remove the Technical Specification (TS) requirements that reference
hydrogen recombiners and hydrogen monitors. The proposed amendment
suggests changes support implementation of the revisions to 10 CFR
50.44, ``Standards for Combustible Gas Control System in Light Water
Cooled Power Reactors,'' that became effective on September 16, 2003.
The changes would be consistent with Revision 1 of the NRC-approved
Technical Specification Task Force (TSTF) Standard Technical
Specification Change Traveler, TSTF-447, ``Elimination of Hydrogen
Recombiners and Change to Hydrogen and Oxygen Monitors.'' The
particular TS improvement in question was announced in the Federal
Register Notice on September 25, 2003, as part of the consolidated line
item improvement process.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
Criterion 1--The Proposed Change Does Not Involve a Significant
Increase in the Probability or Consequences of an Accident Previously
Evaluated
The revised 10 CFR 50.44 no longer defines a design-basis loss-
of-coolant accident (LOCA) hydrogen release, and eliminates
requirements for hydrogen control systems to mitigate such a
release. The installation of hydrogen recombiners and/or vent and
purge systems required by 10 CFR 50.44(b)(3) was intended to address
the limited quantity and rate of hydrogen generation that was
postulated from a design-basis LOCA. The Commission has found that
this hydrogen release is not risk-significant because the design-
basis LOCA hydrogen release does not contribute to the conditional
probability of a large release up to approximately 24 hours after
the onset of core damage. In addition, these systems were
ineffective at mitigating hydrogen releases from risk-significant
accident sequences that could threaten containment integrity.
With the elimination of the design-basis LOCA hydrogen release,
hydrogen [and oxygen] monitors are no longer required to mitigate
design-basis accidents and, therefore, the hydrogen monitors do not
meet the definition of a safety-related component as defined in 10
CFR 50.2. RG [Regulatory Guide] 1.97 Category 1, is intended for key
variables that most directly indicate the accomplishment of a safety
function for design-basis accident events. The hydrogen [and oxygen]
monitors no longer meet the definition of Category 1 in RG 1.97. As
part of the rulemaking to revise 10 CFR 50.44 the Commission found
that Category 3, as defined in RG 1.97, is an appropriate
categorization for the hydrogen monitors because the monitors are
required to diagnose the course of beyond design-basis accidents.
[Also, as part of the rulemaking to revise 10 CFR 50.44, the
Commission found that Category 2, as defined in RG 1.97, is an
appropriate categorization for the oxygen monitors, because the
monitors are required to verify the status of the inert
containment.]
The regulatory requirements for the hydrogen [and oxygen]
monitors can be relaxed without degrading the plant emergency
response. The emergency response, in this sense, refers to the
methodologies used in ascertaining the condition of the reactor
core, mitigating the consequences of an accident, assessing and
projecting offsite releases of radioactivity, and establishing
protective action recommendations to be communicated to offsite
authorities. Classification of the hydrogen monitors as Category 3,
[classification of the oxygen monitors as Category 2] and removal of
the hydrogen [and oxygen] monitors from TS will not prevent an
accident management strategy through the use of the SAMGs [severe
accident management guidelines], the emergency plan (EP), the
emergency operating procedures (EOP), and site survey monitoring
that support modification of emergency plan protective action
recommendations (PARs).
Therefore, the elimination of the hydrogen recombiner
requirements and relaxation of the hydrogen [and oxygen] monitor
requirements, including removal of these
[[Page 45458]]
requirements from TS, does not involve a significant increase in the
probability or the consequences of any accident previously
evaluated.
Criterion 2--The Proposed Change Does Not Create the Possibility of a
New or Different Kind of Accident From Any Previously Evaluated
The elimination of the hydrogen recombiner requirements and
relaxation of the hydrogen [and oxygen] monitor requirements,
including removal of these requirements from TS, will not result in
any failure mode not previously analyzed. The hydrogen recombiner
and hydrogen [and oxygen] monitor equipment was intended to mitigate
a design-basis hydrogen release. The hydrogen recombiner and
hydrogen [and oxygen] monitor equipment are not considered accident
precursors, nor does their existence or elimination have any adverse
impact on the pre-accident state of the reactor core or post
accident confinement of radionuclides within the containment
building.
Therefore, this change does not create the possibility of a new
or different kind of accident from any previously evaluated.
Criterion 3--The Proposed Change Does Not Involve a Significant
Reduction in the Margin of Safety
The elimination of the hydrogen recombiner requirements and
relaxation of the hydrogen [and oxygen] monitor requirements,
including removal of these requirements from TS, in light of
existing plant equipment, instrumentation, procedures, and programs
that provide effective mitigation of and recovery from reactor
accidents, results in a neutral impact to the margin of safety.
The installation of hydrogen recombiners and/or vent and purge
systems required by 10 CFR 50.44(b)(3) was intended to address the
limited quantity and rate of hydrogen generation that was postulated
from a design-basis LOCA. The Commission has found that this
hydrogen release is not risk-significant because the design-basis
LOCA hydrogen release does not contribute to the conditional
probability of a large release up to approximately 24 hours after
the onset of core damage.
Category 3 hydrogen monitors are adequate to provide rapid
assessment of current reactor core conditions and the direction of
degradation while effectively responding to the event in order to
mitigate the consequences of the accident. The intent of the
requirements established as a result of the TMI [Three-Mile Island],
Unit 2 accident can be adequately met without reliance on safety-
related hydrogen monitors.
[Category 2 oxygen monitors are adequate to verify the status of
an inerted containment.]
Therefore, this change does not involve a significant reduction
in the margin of safety. The intent of the requirements established
as a result of the TMI, Unit 2 accident can be adequately met
without reliance on safety-related oxygen monitors.] Removal of
hydrogen [and oxygen] monitoring from TS will not result in a
significant reduction in their functionality, reliability, and
availability.
Based upon the reasoning presented above and the previous
discussion of the amendment request, the requested change does not
involve a significant hazards consideration.
Therefore, the NRC staff proposes to determine that the amendment
request involves no significant hazards consideration.
Attorney for licensee: M.S. Ross, Attorney, Florida Power & Light,
P.O. Box 14000, Juno Beach, Florida 33408-0420.
NRC Branch Chief: Thomas H. Boyce.
Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald
C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
Date of amendment request: June 13, 2007.
Description of amendment request: The proposed amendment would
revise Technical Specifications (TS) 5.5.9, ``Ventilation Filter
Testing Program (VFTP),'' to impose lower (i.e., more restrictive)
limits on the maximum pressure drop across the combined high efficiency
particulate air filters and charcoal adsorbers in three safety-related
ventilation systems. These ventilation systems are the Control Room
Emergency Ventilation System, the Engineered Safety Features
Ventilation System, and the Fuel-Handling Area Exhaust Ventilation
System.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability of occurrence or consequences of an accident
previously evaluated?
Response: No.
The proposed change consists of establishing more restrictive
criteria in the Technical Specification (TS) for the maximum
pressure drop across high efficiency particulate air filters (HEPA)
and charcoal adsorbers in safety-related ventilation systems. These
TS criteria are used to determine the acceptability of periodic test
results. These criteria are not accident initiators. Therefore,
there will be no effect on the probability of an accident. The
safety-related ventilation systems involved in the proposed change
function to mitigate the consequences of accidents. The proposed
change will provide increased assurance that the HEPA filters and
charcoal adsorbers in these systems will be capable of performing
their safety function of reducing the release of radioactive
material resulting from evaluated accidents. Therefore, there will
be no increase in the consequences of those accidents.
Therefore, the proposed change will not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change consists of establishing more restrictive
acceptance criteria for existing TS[-]required tests. The proposed
change does not affect the manner in which the tests are performed.
The proposed change will not result in any new or different methods
or modes of operation of existing structures, systems, or
components. The proposed change will not introduce any new
structures, system, or components.
Therefore, the proposed change will not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The margin of safety associated with the proposed change is the
capability of the applicable safety-related ventilation systems to
prevent radiation exposures from exceeding acceptable limits due to
the release of radioactive material caused by an evaluated accident.
The proposed change will provide increased assurance that the HEPA
filters and charcoal adsorbers in these systems will be capable of
performing this function.
Therefore, the proposed change will not involve a significant
reduction in the margin of safety.
The Nuclear Regulatory Commission (NRC) staff has reviewed the
licensee's analysis and, based on this review, it appears that the
three standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC
staff proposes to determine that the amendment requests involve no
significant hazards consideration.
Attorney for licensee: Kimberly Harshaw, Esquire, One Cook Place,
Bridgman, MI 49106.
NRC Acting Branch Chief: Travis Tate.
Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald
C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
Date of amendment request: June 27, 2007.
Description of amendment request: The proposed amendment would
revise Technical Specifications (TS) Surveillance Requirements 3.8.1.2,
8, 12, 13, 16, and 19, changing the steady state frequency of all
diesel generators (DGs) from the current allowed frequency range of
59.4-61.2 Hz, to 59.4-60.5 Hz (i.e., a decrease of the upper limit,
resulting in narrowing of
[[Page 45459]]
the current range). The licensee stated that the current frequency
range is nonconservative and could result in undesirable effects such
as centrifugal charging pump motor brake horsepower exceeding its
nameplate maximum horsepower, and overloading the DGs.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee provided
its analysis of the issue of no significant hazards consideration. The
NRC staff has performed its own analysis, which is presented below:
(1) Does the proposed change involve a significant increase in
the probability of occurrence or consequences of an accident
previously evaluated?
Response: No.
The more restrictive steady state frequency range ensures that
the diesel generators and equipment being powered by the diesel
generators will function as designed to mitigate an accident as
described in the Update Final Safety Analysis Report (UFSAR). The
DGs and the equipment they power are part of the systems required to
mitigate accidents; no accident analyzed in the UFSAR is initiated
by mitigation equipment. Therefore, the proposed change to the
allowed frequency range of the DGs will not have any impact on the
probability of an accident previously evaluated. Furthermore, other
than narrowing the allowed frequency range of the DGs, there is no
other design or operational change. Therefore, the proposed change
does not increase the probability of malfunction of the DGs or the
equipment they power.
Narrowing of the DG maximum steady state frequency limit will
ensure that the DGs and equipment powered by the DGs will perform as
originally designed and analyzed to mitigate the consequences of any
accident described in the UFSAR. Therefore, the proposed change does
not involve a significant increase in the consequences of an
accident previously evaluated in the UFSAR.
(2) Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
There is no design change associated with the proposed
amendment. Making an existing DG requirement more restrictive alone
will not alter plant configuration because no new or different type
of equipment will be installed, and because no methods governing
plant operation will be changed. The proposed change to allowed
frequency range will not have any effect on the assumptions of
accident scenarios previously made in the UFSAR. Therefore, the
proposed change does not create the possibility of a new or
different kind of accident from any previously evaluated.
(3) Does the proposed change involve a significant reduction in
a margin of safety?
Response: No.
Despite the proposed change to the DG maximum steady state
frequency limit, the DGs and equipment powered by the DGs will
continue to perform as originally designed, and originally analyzed
in the UFSAR. There is no associated change to the methods and
assumptions used to analyze DG performance. The proposed change will
maintain the required function of the DGs and the equipment powered
by the DGs to ensure that operation of structures, systems, or
components is as currently set forth in the UFSAR. Therefore, the
proposed change does not involve a significant reduction in the
margin of safety.
The Nuclear Regulatory Commission (NRC) staff has reviewed the
licensee's analysis and, based on its own analysis, it appears that the
three standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC
staff proposes to determine that the proposed amendment involves no
significant hazards consideration.
Attorney for licensee: Kimberly Harshaw, Esquire, One Cook Place,
Bridgman, MI 49106.
NRC Acting Branch Chief: Travis L. Tate.
Nuclear Management Company, LLC, Docket No. 50-263, Monticello Nuclear
Generating Plant, Wright County, Minnesota
Date of amendment request: July 9, 2007.
Description of amendment request: The proposed amendment would
revise the Technical Specifications (TS), an NRC-controlled document,
by moving the Table of Contents (TOC) out of the TS and making the TOC
into a licensee-controlled document.
Basis for proposed no significant hazards consideration
determination: As required by Title 10 of the Code of Federal
Regulations (10 CFR) Part 50.91(a), the licensee has provided its
analysis of the issue of no significant hazards consideration (NSHC)
which is reproduced below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
No.
The proposed change is administrative and affects control of a
document, the TOC, listing the specifications in the plant TS.
Transferring control from the NRC to NMC (the licensee) does not
affect the operation, physical configuration, or function of plant
equipment or systems. It does not impact the initiators or
assumptions of analyzed events, nor does it impact the mitigation of
accidents or transient events. The change has no impact on, and
hence cannot increase, the probability or consequences of an
accident previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
No.
The proposed change is administrative and does not alter the
plant configuration, require installation of new equipment, alter
assumptions about previously analyzed accidents, or impact the
operation or function of plant equipment or systems. Therefore, this
change does not create the possibility of a new or different kind of
accident from any accident previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
No.
The proposed change is administrative. The TOC is not required
by regulation to be in the TS. [Its] removal does not impact any
safety assumptions or have the potential to reduce a margin of
safety as described in the TS Bases. The change involves a transfer
of control of the TOC from the NRC to NMC. No change in the
technical content of the TS [ ] is involved. Consequently, transfer
from the NRC to NMC has no impact on the margin of safety, and hence
cannot involve a significant reduction in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this analysis, it appears that the three standards of 10 CFR 50.92(c)
are satisfied. Therefore, the NRC staff proposes to determine that the
proposed amendment involves no significant hazards consideration.
Attorney for licensee: Jonathan Rogoff, Esquire, Vice President,
Counsel & Secretary, Nuclear Management Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Acting Branch Chief: Travis L. Tate.
PPL Susquehanna, LLC, Docket No. 50-388, Susquehanna Steam Electric
Station, Unit 2
(SSES 2), Luzerne County, Pennsylvania.
Date of amendment request: March 2, 2007.
Description of amendment request: The proposed amendment would add
an ACTIONS Note 3 to the SSES 2 Technical Specification 3.8.1, ``AC
Sources--Operating,'' to allow a Unit 1 4160 volt subsystem to be de-
energized and removed from service to perform bus maintenance.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
This change does not involve any physical change to structures,
systems, or components (SSCs) and does not alter the method of
operation of any SSCs. The current assumptions in the safety
analysis regarding accident initiators and mitigation of accidents
are unaffected by these changes. No
[[Page 45460]]
SSC failure modes or mechanisms are being introduced, and the
likelihood of previously analyzed failures remains unchanged.
Operation in accordance with the proposed new ACTIONS Note 3 in
Unit 2 Technical Specification 3.8.1 ensures that the AC
[alternating current] distribution system and supported equipment
remain capable of performing their functions as described in the
Final Safety Analysis Report (FSAR). There are no changes to any
accident initiators or to the mitigating capability of safety-
related equipment supported by the Class 1E Electrical AC system.
The protection provided by these safety-related systems will
continue to be provided as assumed by the safety analysis.
Therefore, this proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change does not involve a physical alteration of
any plant equipment. No new equipment is being introduced, and
installed equipment is not being operated in a new or different
manner. There are no setpoints, at which protective or mitigative
actions are initiated, affected by this change. This change does not
alter the manner in which equipment operation is initiated, nor will
the function demands on credited equipment be changed. No
alterations in the procedures that ensure the plant remains within
analyzed limits are being proposed, and no changes are being made to
the procedures relied upon to respond to an off-normal event as
described in the FSAR [final safety analysis report]. As such, no
new failure modes are being introduced. The change does not alter
assumptions made in the safety analysis and licensing basis.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
Response: No.
The margin of safety is established through equipment design,
operating parameters, and the setpoints at which automatic actions
are initiated. The proposed change is acceptable because the new
ACTIONS Note 3 has been established to be consistent with the
existing completion times for declaring required equipment
inoperable that has no offsite power or DG [diesel generator] power
available. Therefore, the plant response to analyzed events is not
affected by this change and will continue to provide the margin of
safety assumed by the safety analysis.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Bryan A. Snapp, Esquire, Assoc. General
Counsel, PPL Services Corporation, 2 North Ninth St., GENTW3,
Allentown, PA 18101-1179.
NRC Branch Chief: Mark G. Kowal.
PSEG Nuclear LLC, Docket No. 50-354, Hope Creek Generating Station,
Salem County, New Jersey
Date of amendment request: July 26, 2007
Description of amendment request: The proposed amendment would
remove values for turbine first stage pressure equivalent to
Pbypass from the Technical Specifications.
Pbypass is the reactor power level below which the turbine
stop valve closure and the turbine control valve fast closure reactor
protection system trip functions and the end-of-cycle recirculation
pump trip are bypassed automatically.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed removal of values for turbine first stage pressure
associated with Pbypass from the Technical Specifications
does not alter the requirements for component operability or
surveillance currently in the Technical Specifications. The proposed
change will have no impact on any safety related structures, systems
or components.
The probability of occurrence of a previously evaluated accident
is not increased because this change does not introduce any new
potential accident initiating conditions. The consequences of
accidents previously evaluated in the UFSAR [Updated Final Safety
Analysis Report] are not affected because the ability of the
components to perform their required function is not affected.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed change is administrative in nature, and does not
result in physical alterations or changes in the method by which any
safety related system performs its intended function. The proposed
change does not affect any safety analysis assumptions. The proposed
change does not create any new accident initiators or involve an
activity that could be an initiator of an accident of a different
type.
All components will continue to be tested to the same
requirements as defined in the Technical Specification Surveillance
Requirements. The proposed revision does not make changes in any
method of testing or how any safety related system performs its
safety functions.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed change to remove values for turbine first stage
pressure associated with Pbypass from the Technical
Specifications does not alter the Technical Specification
requirements for reactor protection system operability. The turbine
first stage pressure setpoint will be controlled in accordance with
plant procedures and will be verified during post-installation
testing.
The proposed change will not affect the current Technical
Specification requirements or the components to which they apply.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. Jeffrie J. Keenan, Esquire, PSEG
Nuclear--N21, P.O. Box 236, Hancocks Bridge, NJ 08038.
NRC Branch Chief: Harold K. Chernoff.
STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South
Texas Project, Units 1 and 2, Matagorda County, Texas
Date of amendment request: June 26, 2007.
Description of amendment request: The proposed amendment would
modify the Technical Specifications (TSs) to establish more effective
and appropriate action, surveillance, and administrative requirements
related to ensuring the habitability of the control room envelope (CRE)
in accordance with Nuclear Regulatory Commission (NRC)-approved TS Task
Force (TSTF) Standard Technical Specification change traveler TSTF-448,
Revision 3, ``Control Room Habitability.'' Specifically, the proposed
amendment would modify TS 3.7.7, Control Room Makeup and Cleanup
Filtration System (CRMCFS) and TS Section 6.8, ``Administrative
Controls-Procedures, Programs, and Manuals.'' The NRC staff issued a
``Notice of Availability of Technical Specification Improvement to
[[Page 45461]]
Modify Requirements Regarding Control Room Envelope Habitability Using
the Consolidated Line Item Improvement Process'' associated with TSTF-
448, Revision 3, in the Federal Register on January 17, 2007 (72 FR
2022). The notice included a model safety evaluation, a model no
significant hazards consideration (NSHC) determination, and a model
license amendment request. In its application dated June 26, 2007, the
licensee affirmed the applicability of the model NSHC determination
which is presented below.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of NSHC adopted by the licensee is presented below:
Criterion 1--The Proposed Change Does Not Involve a Significant
Increase in the Probability or Consequences of an Accident Previously
Evaluated
The proposed change does not adversely affect accident
initiators or precursors nor alter the design assumptions,
conditions, or configuration of the facility. The proposed change
does not alter or prevent the ability of structures, systems, and
components (SSCs) to perform their intended function to mitigate the
consequences of an initiating event within the assumed acceptance
limits. The proposed change revises the TS for the CRE emergency
ventilation system, which is a mitigation system designed to
minimize unfiltered air leakage into the CRE and to filter the CRE
atmosphere to protect the CRE occupants in the event of accidents
previously analyzed. An important part of the CRE emergency
ventilation system is the CRE boundary. The CRE emergency
ventilation system is not an initiator or precursor to any accident
previously evaluated. Therefore, the probability of any accident
previously evaluated is not increased. Performing tests to verify
the operability of the CRE boundary and implementing a program to
assess and maintain CRE habitability ensure that the CRE emergency
ventilation system is capable of adequately mitigating radiological
consequences to CRE occupants during accident conditions, and that
the CRE emergency ventilation system will perform as assumed in the
consequence analyses of design basis accidents. Thus, the
consequences of any accident previously evaluated are not increased.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
Criterion 2--The Proposed Change Does Not Create the Possibility of a
New or Different Kind of Accident from any Accident Previously
Evaluated
The proposed change does not impact the accident analysis. The
proposed change does not alter the required mitigation capability of
the CRE emergency ventilation system, or its functioning during
accident conditions as assumed in the licensing basis analyses of
design basis accident radiological consequences to CRE occupants. No
new or different accidents result from performing the new
surveillance or following the new program. The proposed change does
not involve a physical alteration of the plant (i.e., no new or
different type of equipment will be installed) or a significant
change in the methods governing normal plant operation. The proposed
change does not alter any safety analysis assumptions and is
consistent with current plant operating practice. Therefore, this
change does not create the possibility of a new or different kind of
accident from any accident previously evaluated.
Criterion 3--The Proposed Change Does Not Involve a Significant
Reduction in the Margin of Safety
The proposed change does not alter the manner in which safety
limits, limiting safety system settings or limiting conditions for
operation are determined. The proposed change does not affect safety
analysis acceptance criteria. The proposed change will not result in
plant operation in a configuration outside the design basis for an
unacceptable period of time without compensatory measures. The
proposed change does not adversely affect systems that respond to
safely shut down the plant and to maintain the plant in a safe
shutdown condition. Therefore, the proposed change does not involve
a significant reduction in a margin of safety.
The NRC staff has reviewed the analysis adopted by the licensee
and, based on this review, it appears that the standards of 10 CFR
50.92(c) are satisfied. Therefore, the NRC staff proposes to determine
that the request for amendments involves NSHC.
Attorney for licensee: A. H. Gutterman, Esq., Morgan, Lewis &
Bockius, 1111 Pennsylvania Avenue, NW., Washington, DC 20004.
NRC Branch Chief: Thomas G. Hiltz.
TXU Generation Company LP, Docket Nos. 50-445 and 50-446, Comanche Peak
Steam Electric Station, Units 1 and 2, Somervell County, Texas.
Date of amendment request: April 10, 2007.
Brief description of amendments: The proposed amendments would
revise Technical Specifications (TS) 3.1, ``Reactivity Control
Systems,'' TS 3.2, ``Power Distribution Limits,'' TS 3.3,
``Instrumentation,'' and TS 5.6.5b, ``Core Operating Limits Report
(COLR).'' The requested change proposes to incorporate standard
Westinghouse-developed and NRC-approved analytical methods into the
lists of methodologies used to establish the core operating limits.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
No physical plant changes or changes in manner in which the
plant will be operated as a result of the methodology changes. The
proposed changes do not impact the condition or performance of any
plant structure, system or component. The core operating limits are
established to support Technical Specifications 3.1, 3.2, 3.3, and
3.4. The core operating limits ensure that fuel design limits are
not exceeded during any conditions of normal operation or in the
event of any Anticipated Operational Occurrence (AOO). The methods
used to establish the core operating limits for each operating cycle
are based on methods previously found acceptable by the NRC and
listed in Technical Specifications section 5.6.5.b. Application of
these NRC-approved methods will continue to ensure that acceptable
operating limits are established to protect the fuel cladding
integrity during normal operation and AOOs. The requested Technical
Specification changes, including those changes proposed to conform
with the NRC-approved analysis methodologies, do not involve any
plant modifications or operational changes that could affect system
reliability, performance, or possibility of operator error. The
requested changes do not affect any postulated accident precursors,
does not affect any accident mitigation systems, and does not
introduce any new accident initiation mechanisms.
As a result, the proposed changes to the CPSES [Comanche Peak
Steam Electric Station] Technical Specifications do not involve any
increase in the probability or the consequences of any accident or
malfunction of equipment important to safety previously evaluated
since neither accident probabilities nor consequences are being
affected by this proposed change.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
There are no physical changes being made to the plant. No new
modes of plant operation are being introduced. The parameters
assumed in the analyses are within the design limits of the existing
plant equipment. All plant systems will perform as designed during
the response to a potential accident.
Therefore, the proposed change to the CPSES Technical
Specifications does not create the possibility of a new or different
kind of accident or malfunction of equipment important to safety
from any accident previously evaluated.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
Response: No.
The NRC-approved accident analysis methodologies include
restrictions on the
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choice of inputs, the degree of conservatism inherent in the
calculations, and specified event acceptance criteria. Analyses
performed in accordance with these methodologies will not result in
adverse effects on the regulated margin of safety. Similarly, the
use of axial power distribution controls based on the relaxed axial
offset control strategy is a time-proven and NRC-approved method.
The method is consistent with the accident analyses assumptions as
described in the list of NRC-approved methodologies proposed to be
used to establish the core operating limits. Finally, the proposed
changes to allow operation with the BEACON [Best Estimate Analyzer
for Core Operation Nuclear] power distribution monitoring tool
provide additional information to the reactor operators on the state
of the reactor core. Again, the use of the BEACON tool and the
methodology used to develop the inputs to the tool are consistent
with and controlled by the NRC-approved methodologies used to
establish the core operating limits. As such, the margin of safety
assumed in the plant safety analysis is not adversely affected by
the proposed changes.
Based on the above evaluations, TXU Power concludes that the
proposed amendment(s) present no significant hazards consideration
under the standards set forth in 10 CFR 50.92(c) and, accordingly, a
finding of no significant hazards consideration is justified.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and
Bockius, 1800 M Street, NW., Washington, DC 20036.
NRC Branch Chief: Thomas G. Hiltz.
TXU Generation Company LP, Docket Nos. 50-445 and 50-446, Comanche Peak
Steam Electric Station, Units 1 and 2, Somervell County, Texas
Date of amendment request: May 22, 2007.
Brief description of amendments: The proposed amendment would
revise the Technical Requirements Surveillance (TRS) 13.3.33.2, Cycling
Frequency for the Turbine Stop and Control Valves. The proposed change
would increase the frequency interval for the turbine stop and control
valves testing from 12 to 26 weeks.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
The proposed change will increase the frequency interval for
testing the high pressure (HP) and low pressure (LP) turbine stop
and control valves to 26 weeks. This test requires the movement of
the HP and LP turbine valves through one complete cycle once every
26 weeks. The test verifies freedom of movement of the valve
components and is beneficial in early detection of problems with
valve operation. [The test ensures that all turbine steam inlet
valves are capable of closing to protect the turbine from excessive
overspeed, which could generate potentially damaging missiles.]
Siemens, the turbine manufacturer for Comanche Peak Steam
Electric Station (CPSES), has evaluated the change in the
probability of generating external/high-trajectory turbine missiles
resulting from a hypothetical LP turbine disk failure which could
adversely affect safety-related SSCs [structures, systems, and
components] due to the change in the surveillance interval weeks
using a previously approved missile probability analysis
methodology. The results of the analysis show the new valve test
interval of 26 weeks with a turbine inspection interval of 100,000
hours is safe and acceptable as the probability of occurrence of a
turbine missile per turbine year is less than the Nuclear Regulatory
Commission (NRC) limit of 1E-4 per 8760 hours (turbine year) or
11.42E-4 at 100,000 hours (Reference 7.4 [of the licensee's May 22,
2007, application]). Therefore, the risk of the loss of an essential
system from a single event