Biweekly Notice; Applications and Amendments to Facility Operating Licenses; Involving No Significant Hazards Considerations, 39081-39089 [E7-13537]

Download as PDF Federal Register / Vol. 72, No. 136 / Tuesday, July 17, 2007 / Notices N431CA, Lexington, Kentucky, August 27, 2006. NEWS MEDIA CONTACT: Telephone: (202) 314–6100. Individuals requesting specific accommodations should contact Chris Bisett (202) 314–6305 by Friday, July 20, 2007. The public may view the meeting via a live or archived webcast by accessing a link under ‘‘News & Events’’ on the NTSB home page at www.ntsb.gov. FOR FURTHER INFORMATION CONTACT: Vicky D’Onofrio, (202) 314–6410. Dated: July 13, 2007. Vicky D’Onofrio, Federal Register Liaison Officer. [FR Doc. 07–3491 Filed 7–13–07; 1:34 pm] BILLING CODE 7533–01–M This meeting will be webcast live at the Web address, www.nrc.gov. Week of August 6, 2007—Tentative There are no meetings scheduled for the Week of August 6, 2007. Week of August 13, 2007—Tentative There are no meetings scheduled for the Week of August 13, 2007. Week of August 20, 2007—Tentative Tuesday, August 21, 2007 1:30 p.m. Meeting with OAS and CRCPD (Public Meeting). (Contact: Shawn Smith, (301) 415–2620). This meeting will be webcast live at the Web address, www.nrc.gov. Wednesday, August 22, 2007 9:30 a.m. Periodic Briefing on New Reactor Issues (Public Meeting). NUCLEAR REGULATORY COMMISSION Sunshine Federal Register Notice Weeks of July 16, 23, 30, August 6, 13, 20, 2007. PLACE: Commissioners’ Conference Room, 11555 Rockville Pike, Rockville, Maryland. STATUS: Public and Closed. MATTERS TO BE CONSIDERED: DATES: Week of July 16, 2007 Wednesday, July 18, 2007 10 a.m. Discussion of Security Issues (closed—ex. 1 & 3). 1 p.m. Briefing on Digital Instrumentation and Control (Public Meeting). (Contact: William Kemper, (301) 415–7585). This meeting will be webcast live at the Web address, www.nrc.gov. Week of July 23, 2007—Tentative Tuesday, July 24, 2007 9:30 a.m. Preparation for the 2008 Convention on Nuclear Safety (closed—ex. 9). 2 p.m. Briefing on Palo Verde Nuclear Generating Station (Public Meeting). (Contact: Michael Markley, (301) 415– 5723). This meeting will be webcast live at the Web address, www.nrc.gov. Wednesday, July 25, 2007 2 p.m. Discussion of Management Issues (closed—ex. 2). sroberts on PROD1PC70 with NOTICES Week of July 30, 2007—Tentative Thursday, August 2, 2007 1:30 p.m. Briefing on Risk-Informed, Performance-Based Regulation (Public Meeting). (Contact: John Monninger, (301) 415–6189). VerDate Aug<31>2005 17:40 Jul 16, 2007 Jkt 211001 This meeting will be webcast live at the Web address, www.nrc.gov. * * * * * * The schedule for Commission meetings is subject to change on short notice. To verify the status of meetings call (recording)—(301) 415–1292. Contact person for more information: Michelle Schroll, (301) 415–1662. * * * * * The NRC Commission Meeting Schedule can be found on the Internet at: www.nrc.gov/about-nrc/policymaking/schedule.html. * * * * * The NRC provides reasonable accommodation to individuals with disabilities where appropriate. If you need a reasonable accommodation to participate in these public meetings, or need this meeting notice or the transcript or other information from the public meetings in another format (e.g. braille, large print), please notify the NRC’s Disability Program Coordinator, Rohn Brown, at 301–492–2279, TDD: 301–415–2100, or by e-mail at REB3@nrc.gov. Determinations on requests for reasonable accommodation will be made on a case-by-case basis. * * * * * This notice is distributed by mail to several hundred subscribers; if you no longer wish to receive it, or would like to be added to the distribution, please contact the Office of the Secretary, Washington, DC 20555 (301–415–1969). In addition, distribution of this meeting notice over the Internet system is available. If you are interested in receiving this Commission meeting schedule electronically, please send an electronic message to dkw@nrc.gov. PO 00000 Frm 00040 Fmt 4703 Sfmt 4703 39081 Dated: July 12, 2007. Rochelle C. Bavol, Office of the Secretary. [FR Doc. 07–3481 Filed 7–13–07; 11:09 am] BILLING CODE 7590–01–P NUCLEAR REGULATORY COMMISSION Biweekly Notice; Applications and Amendments to Facility Operating Licenses; Involving No Significant Hazards Considerations I. Background Pursuant to section 189a. (2) of the Atomic Energy Act of 1954, as amended (the Act), the U.S. Nuclear Regulatory Commission (the Commission or NRC staff) is publishing this regular biweekly notice. The Act requires the Commission publish notice of any amendments issued, or proposed to be issued and grants the Commission the authority to issue and make immediately effective any amendment to an operating license upon a determination by the Commission that such amendment involves no significant hazards consideration, notwithstanding the pendency before the Commission of a request for a hearing from any person. This biweekly notice includes all notices of amendments issued, or proposed to be issued from June 21, 2007 to July 3, 2007. The last biweekly notice was published on July 3, 2007 (72 FR 36520). Notice of Consideration of Issuance of Amendments to Facility Operating Licenses, Proposed No Significant Hazards Consideration Determination, and Opportunity for a Hearing The Commission has made a proposed determination that the following amendment requests involve no significant hazards consideration. Under the Commission’s regulations in 10 CFR 50.92, this means that operation of the facility in accordance with the proposed amendment would not (1) Involve a significant increase in the probability or consequences of an accident previously evaluated; or (2) create the possibility of a new or different kind of accident from any accident previously evaluated; or (3) involve a significant reduction in a margin of safety. The basis for this proposed determination for each amendment request is shown below. The Commission is seeking public comments on this proposed determination. Any comments received within 30 days after the date of publication of this notice will be considered in making any final E:\FR\FM\17JYN1.SGM 17JYN1 sroberts on PROD1PC70 with NOTICES 39082 Federal Register / Vol. 72, No. 136 / Tuesday, July 17, 2007 / Notices determination. Within 60 days after the date of publication of this notice, the licensee may file a request for a hearing with respect to issuance of the amendment to the subject facility operating license and any person whose interest may be affected by this proceeding and who wishes to participate as a party in the proceeding must file a written request for a hearing and a petition for leave to intervene. Normally, the Commission will not issue the amendment until the expiration of 60 days after the date of publication of this notice. The Commission may issue the license amendment before expiration of the 60day period provided that its final determination is that the amendment involves no significant hazards consideration. In addition, the Commission may issue the amendment prior to the expiration of the 30-day comment period should circumstances change during the 30-day comment period such that failure to act in a timely way would result, for example in derating or shutdown of the facility. Should the Commission take action prior to the expiration of either the comment period or the notice period, it will publish in the Federal Register a notice of issuance. Should the Commission make a final No Significant Hazards Consideration Determination, any hearing will take place after issuance. The Commission expects that the need to take this action will occur very infrequently. Written comments may be submitted by mail to the Chief, Rulemaking, Directives and Editing Branch, Division of Administrative Services, Office of Administration, U.S. Nuclear Regulatory Commission, Washington, DC 20555– 0001, and should cite the publication date and page number of this Federal Register notice. Written comments may also be delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of written comments received may be examined at the Commission’s Public Document Room (PDR), located at One White Flint North, Public File Area O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The filing of requests for a hearing and petitions for leave to intervene is discussed below. Within 60 days after the date of publication of this notice, the licensee may file a request for a hearing with respect to issuance of the amendment to the subject facility operating license and any person whose interest may be affected by this proceeding and who wishes to participate as a party in the proceeding must file a written request VerDate Aug<31>2005 17:40 Jul 16, 2007 Jkt 211001 for a hearing and a petition for leave to intervene. Requests for a hearing and a petition for leave to intervene shall be filed in accordance with the Commission’s ‘‘Rules of Practice for Domestic Licensing Proceedings’’ in 10 CFR Part 2. Interested persons should consult a current copy of 10 CFR 2.309, which is available at the Commission’s PDR, located at One White Flint North, Public File Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland. Publicly available records will be accessible from the Agencywide Documents Access and Management System’s (ADAMS) Public Electronic Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/ reading-rm/doc-collections/cfr/. If a request for a hearing or petition for leave to intervene is filed within 60 days, the Commission or a presiding officer designated by the Commission or by the Chief Administrative Judge of the Atomic Safety and Licensing Board Panel, will rule on the request and/or petition; and the Secretary or the Chief Administrative Judge of the Atomic Safety and Licensing Board will issue a notice of a hearing or an appropriate order. As required by 10 CFR 2.309, a petition for leave to intervene shall set forth with particularity the interest of the petitioner in the proceeding, and how that interest may be affected by the results of the proceeding. The petition should specifically explain the reasons why intervention should be permitted with particular reference to the following general requirements: (1) The name, address, and telephone number of the requestor or petitioner; (2) the nature of the requestor’s/petitioner’s right under the Act to be made a party to the proceeding; (3) the nature and extent of the requestor’s/petitioner’s property, financial, or other interest in the proceeding; and (4) the possible effect of any decision or order which may be entered in the proceeding on the requestor’s/petitioner’s interest. The petition must also set forth the specific contentions which the petitioner/ requestor seeks to have litigated at the proceeding. Each contention must consist of a specific statement of the issue of law or fact to be raised or controverted. In addition, the petitioner/requestor shall provide a brief explanation of the bases for the contention and a concise statement of the alleged facts or expert opinion which support the contention and on which the petitioner/requestor intends to rely in proving the contention at the hearing. The petitioner/requestor must also provide references to those specific sources and documents of PO 00000 Frm 00041 Fmt 4703 Sfmt 4703 which the petitioner is aware and on which the petitioner/requestor intends to rely to establish those facts or expert opinion. The petition must include sufficient information to show that a genuine dispute exists with the applicant on a material issue of law or fact. Contentions shall be limited to matters within the scope of the amendment under consideration. The contention must be one which, if proven, would entitle the petitioner/ requestor to relief. A petitioner/ requestor who fails to satisfy these requirements with respect to at least one contention will not be permitted to participate as a party. Those permitted to intervene become parties to the proceeding, subject to any limitations in the order granting leave to intervene, and have the opportunity to participate fully in the conduct of the hearing. If a hearing is requested, and the Commission has not made a final determination on the issue of no significant hazards consideration, the Commission will make a final determination on the issue of no significant hazards consideration. The final determination will serve to decide when the hearing is held. If the final determination is that the amendment request involves no significant hazards consideration, the Commission may issue the amendment and make it immediately effective, notwithstanding the request for a hearing. Any hearing held would take place after issuance of the amendment. If the final determination is that the amendment request involves a significant hazards consideration, any hearing held would take place before the issuance of any amendment. A request for a hearing or a petition for leave to intervene must be filed by: (1) First class mail addressed to the Office of the Secretary of the Commission, U.S. Nuclear Regulatory Commission, Washington, DC 20555– 0001, Attention: Rulemaking and Adjudications Staff; (2) courier, express mail, and expedited delivery services: Office of the Secretary, Sixteenth Floor, One White Flint North, 11555 Rockville Pike, Rockville, Maryland 20852, Attention: Rulemaking and Adjudications Staff; (3) E-mail addressed to the Office of the Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov; or (4) facsimile transmission addressed to the Office of the Secretary, U.S. Nuclear Regulatory Commission, Washington, DC, Attention: Rulemaking and Adjudications Staff at (301) 415–1101, verification number is (301) 415–1966. A copy of the request for hearing and E:\FR\FM\17JYN1.SGM 17JYN1 Federal Register / Vol. 72, No. 136 / Tuesday, July 17, 2007 / Notices petition for leave to intervene should also be sent to the Office of the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555– 0001, and it is requested that copies be transmitted either by means of facsimile transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy of the request for hearing and petition for leave to intervene should also be sent to the attorney for the licensee. Nontimely requests and/or petitions and contentions will not be entertained absent a determination by the Commission or the presiding officer of the Atomic Safety and Licensing Board that the petition, request and/or the contentions should be granted based on a balancing of the factors specified in 10 CFR 2.309(a)(1)(i)–(viii). For further details with respect to this action, see the application for amendment which is available for public inspection at the Commission’s PDR, located at One White Flint North, Public File Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland. Publicly available records will be accessible from the ADAMS Public Electronic Reading Room on the Internet at the NRC Web site, https:// www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS or if there are problems in accessing the documents located in ADAMS, contact the PDR Reference staff at 1 (800) 397– 4209, (301) 415–4737 or by e-mail to pdr@nrc.gov. sroberts on PROD1PC70 with NOTICES Nuclear Management Company, LLC, Docket Nos. 50–282 and 50–306, Prairie Island Nuclear Generating Plant (PINGP), Units 1 and 2, Goodhue County, Minnesota Date of amendment request: May 10, 2007. Description of amendment request: The proposed amendments would modify the Technical Specifications (TS) by removing the specific isolation time for the main steam isolation valves from the associated TS Surveillance Requirements (SRs) and by replacing it with the requirement to verify the valve isolation time is within limits. The changes are consistent with Nuclear Regulatory Commission (NRC) approved Industry/Technical Specification Task Force (TSTF)–491, Removal of the Main Steam and Main Feedwater Valve Isolation Time from Technical Specifications, Revision 2. The proposed amendments deviate from TSTF–491 in that the current PINGP TS and associated SRs for the main feedwater isolation valves do not include valve closure times, and thus these changes in TSTF–491 are not VerDate Aug<31>2005 17:40 Jul 16, 2007 Jkt 211001 applicable to the PINGP TSs and are not adopted. The NRC staff issued a notice of opportunity for comment in the Federal Register on October 5, 2006 (71 FR 58884), on possible amendments concerning the consolidation line item improvement process (CLIIP), including a model safety evaluation and a model no significant hazards consideration determination. The NRC staff subsequently issued a notice of availability of the models for referencing in license amendment applications in the Federal Register on December 29, 2006 (71 FR 78472) as part of the CLIIP. In its application dated May 10, 2007, the licensee affirmed the applicability of the following determination. Basis for proposed no significant hazards consideration determination: As required by 10 CFR 50.91(a), an analysis of the issue of no significant hazards consideration is presented below: Criterion 1—The Proposed Change Does Not Involve a Significant Increase in the Probability or Consequences of an Accident Previously Evaluated The proposed change allows relocating main steam and main feedwater valve isolation times to the Licensee Controlled Document that is referenced in the Bases. The proposed change is described in Technical Specification Task Force (TSTF) Standard TS Change Traveler TSTF–491 related to relocating the main steam and main feedwater valves isolation times to the Licensee Controlled Document that is referenced in the Bases and replacing the isolation time with the phrase, within limits. The proposed change does not involve a physical alteration of the plant (no new or different type of equipment will be installed). The proposed changes relocate the main steam and main feedwater isolation valve times to the Licensee Controlled Document that is referenced in the Bases. The requirements to perform the testing of these isolation valves are retained in the TS. Future changes to the Bases or licensee-controlled document will be evaluated pursuant to the requirements of 10 CFR 50.59, Changes, test and experiments, to ensure that such changes do not result in more than minimal increase in the probability or consequences of an accident previously evaluated. The proposed changes do not adversely affect accident initiators or precursors nor alter the design assumptions, conditions, and configuration of the facility or the manner in which the plant is operated and maintained. The proposed changes do not adversely affect the ability of structures, systems and components (SSCs) to perform their intended safety function to mitigate the consequences of an initiating event within the assumed acceptance limits. The proposed changes do not affect the source term, containment isolation, or radiological consequences of any accident previously evaluated. Further, the proposed changes do not increase the types and the amounts of radioactive effluent that PO 00000 Frm 00042 Fmt 4703 Sfmt 4703 39083 may be released, nor significantly increase individual or cumulative occupation/public radiation exposures. Therefore, the changes do not involve a significant increase in the probability or consequences of any accident previously evaluated. Criterion 2—The Proposed Change Does Not Create the Possibility of a New or Different Kind of Accident From any Previously Evaluated The proposed changes relocate the main steam and main feedwater valve isolation times to the Licensee Controlled Document that is referenced in the Bases. In addition, the valve isolation times are replaced in the TS with the phrase ‘‘within limits.’’ The changes do not involve a physical altering of the plant (i.e., no new or different type of equipment will be installed) or a change in methods governing normal plant operation. The requirements in the TS continue to require testing of the main steam and main feedwater isolation valves to ensure the proper functioning of these isolation valves. Therefore, the changes do not create the possibility of a new or different kind of accident from any previously evaluated. Criterion 3—The Proposed Change Does Not Involve a Significant Reduction in the Margin of Safety The proposed changes relocate the main steam and main feedwater valve isolation times to the Licensee Controlled Document that is referenced in the Bases. In addition, the valve isolation times are replaced in the TS with the phrase ‘‘within limits.’’ Instituting the proposed changes will continue to ensure the testing of main steam and main feedwater isolation valves. Changes to the Bases or license controlled document are performed in accordance with 10 CFR 50.59. This approach provides an effective level of regulatory control and ensures that main steam and feedwater isolation valve testing is conducted such that there is no significant reduction in the margin of safety. The margin of safety provided by the isolation valves is unaffected by the proposed changes since there continue to be TS requirements to ensure the testing of main steam and main feedwater isolation valves. The proposed changes maintain sufficient controls to preserve the current margins of safety. The NRC staff has reviewed the licensees analysis and, based on this review, it appears that the three standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff proposes to determine that the amendment requests involve no significant hazards consideration. Attorney for licensee: Jonathan Rogoff, Esquire, Vice President, Counsel & Secretary, Nuclear Management Company, LLC, 700 First Street, Hudson, WI 54016. NRC Acting Branch Chief: Travis L. Tate. E:\FR\FM\17JYN1.SGM 17JYN1 39084 Federal Register / Vol. 72, No. 136 / Tuesday, July 17, 2007 / Notices Southern Nuclear Operating Company, Inc., Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50–321 and 50–366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, Appling County, Georgia sroberts on PROD1PC70 with NOTICES Date of amendment request: October 30, 2006. Description of amendment request: The proposed amendment would revise Technical Specification (TS) Section 5.3.1, Administrative controls, to (1) Improve administrative flexibility and clarity in the wording of the specification and (2) replace a specific position title with a generic position title for the senior individual in charge of health physics. Basis for proposed no significant hazards consideration determination: As required by 10 CFR 50.91(a), an analysis of the issue of no significant hazards consideration is presented below: 1. Does the proposed change involve a significant increase in the probability or consequences of an accident previously evaluated? The proposed change to Technical Specifications Administrative Controls Section 5.3.1 involves the use of a more generic designation for the unit staff position responsible for Health Physics without reducing the level of authority required for that position. The proposed change also allows the flexibility to use an accredited program for qualifying personnel to fill unit staff positions, which represents an acceptable alternative to the qualification requirements for these positions as currently specified in the Technical Specifications. Since the proposed changes are administrative in nature, they do not involve any physical changes to any structures, systems, or components, nor will their performance requirements be altered. The proposed changes also do not affect the operation, maintenance, or testing of the plant. Therefore, the response of the plant to previously analyzed accidents will not be affected. Consequently, the proposed changes do not involve a significant increase or any increase in the probability or consequences of an accident previously evaluated. 2. Does the proposed change create the possibility of a new or different kind of accident from any previously evaluated? The proposed changes to the Technical Specifications will have no adverse impact on the overall qualification of the unit staff. The use of a more generic designation for the unit staff position responsible for Health Physics and the alternative use of an accredited program that has been endorsed by the NRC will ensure the educational requirements and power plant experience for each unit staff position are properly satisfied and will continue to fulfill applicable regulatory requirements. Also, since no change is being made to the design, VerDate Aug<31>2005 17:40 Jul 16, 2007 Jkt 211001 operation, maintenance, or testing of the plant, no new methods of operation or failure modes are introduced by the proposed changes. Therefore, the possibility of a new or different kind of accident from any previously evaluated is not created. 3. Does the proposed change involve a significant decrease in the margin of safety? The proposed changes to the Technical Specifications will have no adverse impact on the onsite organizational features necessary to assure safe operation of the plant. Lines of authority for plant operation are unaffected by the proposed changes. Also, the adoption of the more generic designation of the individual responsible for Health Physics will reduce the regulatory burden of having to devote limited resources to process a license amendment whenever a title change for this position is implemented. Accordingly, this reduction in regulatory burden and the option to use an accredited program endorsed by NRC to qualify the unit staff will improve plant efficiency without compromising plant safety. Therefore, the proposed changes do not involve a significant decrease in the margin of safety. The NRC staff proposes to determine that the amendment request involves no significant hazards consideration. Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037. NRC Branch Chief: Evangelos C. Marinos. Southern Nuclear Operating Company, Inc., Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50–321 and 50–366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, Appling County, Georgia Date of amendment request: June 5 and June 11, 2007. Description of amendment request: The proposed amendment would revise Technical Specification (TS) 3.1.4, Control Rod Scram Times, using the consolidated line-term improvement process. These changes are based on TS Task Force (TSTF) change traveler TSTF–460, that has been approved generically for the boiling water reactor (BWR) Standard TS, NUREG–1433 (BWR/4). The frequency of Surveillance Requirement 3.1.4.2, control rod scram time testing, is revised from ‘‘120 days cumulative operation in MODE 1’’ to ‘‘200 days cumulative operation in MODE 1.’’ The NRC staff issued a notice of availability of a model safety evaluation and model no significant hazards consideration (NSHC) determination for referencing in license amendment applications in the Federal Register on August 23, 2004 (69 FR 51854). The licensee affirmed the applicability of the PO 00000 Frm 00043 Fmt 4703 Sfmt 4703 model NSHC determination in its application and supplement dated June 5 and June 11, 2007. Basis for proposed no significant hazards consideration determination: As required by 10 CFR 50.91(a), an analysis of the issue of no significant hazards consideration is presented below: 1. Does the change involve a significant increase in the probability or consequences of an accident previously evaluated? Response: No. The proposed change extends the frequency for testing control rod scram time testing from every 120 days of cumulative Mode 1 operation to 200 days of cumulative Mode 1 operation. The frequency of surveillance testing is not an initiator of any accident previously evaluated. The frequency of surveillance testing does not affect the ability to mitigate any accident previously evaluated, as the tested component is still required to be operable. Therefore, the proposed change does not involve a significant increase in the probability or consequences of an accident previously evaluated. 2. Does the change create the possibility of a new or different kind of accident from any accident previously evaluated? Response: No. The proposed change extends the frequency for testing control rod scram time testing from every 120 days of cumulative Mode 1 operation to 200 days of cumulative Mode 1 operation. The proposed change does not result in any new or different modes of plant operation. Therefore, the proposed change does not create the possibility of a new or different kind of accident from any previously evaluated. 3. Does the proposed change involve a significant reduction in a margin of safety? Response: No. The proposed change extends the frequency for testing control rod scram time testing from every 120 days of cumulative Mode 1 operation to 200 days of cumulative Mode 1 operation. The proposed change continues to test the control rod scram time to ensure the assumptions in the safety analysis are protected. Therefore, the proposed change does not involve a significant reduction in a margin of safety. The NRC staff proposes to determine that the amendment request involves no significant hazards consideration. Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037. NRC Branch Chief: Evangelos C. Marinos. Virginia Electric and Power Company, Docket Nos. 50–280 and 50–281, Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia Date of amendment request: June 25, 2007. Description of amendment request: The proposed change increases the E:\FR\FM\17JYN1.SGM 17JYN1 Federal Register / Vol. 72, No. 136 / Tuesday, July 17, 2007 / Notices sroberts on PROD1PC70 with NOTICES maximum Technical Specification (TS) service water (SW) temperature limit from 95 °F to 100 °F, and revises the TS Figure 3.8–1, which provides allowable containment air partial pressure versus SW temperature. Basis for proposed no significant hazards consideration determination: As required by 10 CFR 50.91(a), the licensee has provided its analysis of the issue of no significant hazards consideration, which is presented below: 1. Does the proposed change involve a significant increase in the probability or consequences of an accident previously evaluated? Operating with increased maximum service water temperature limits does not affect the frequency of accident initiating events. Therefore, the probability of an accident previously analyzed is not increased. Plant systems supported by SW have been evaluated for operation with a service water temperature limit of 100 °F, and it determined that there is no operational impact when operating at the higher SW temperature. Although the service water temperature limit is being increased, the containment will continue to meet its design basis acceptance criteria following a large-break loss of coolant accident as identified in the UFSAR [Updated Final Safety Analysis Report]. Therefore, there is no increase in the consequences of any accident previously evaluated resulting from operation of Surry Units 1 and 2 with an increased service water temperature limit. 2. Does the proposed change create the possibility of a new or different kind of accident from any accident previously evaluated? There are no new failure modes or mechanisms associated with operating Surry Units 1 and 2 with an increased service water temperature limit of 100 °F. As noted above, the increased service water temperature limit does not affect plant operation, since plant systems supported by SW have been evaluated for operation with a SW temperature limit of 100 °F and no operational impact was identified. Therefore, there are no new or different kinds of accidents created by operation of Surry Units 1 and 2 with increased service water temperature limits. 3. Does the proposed change involve a significant reduction in the margin of safety? The containment analysis acceptance criteria continue to be met when operating with the proposed increased maximum service water temperature limit. Containment integrity will not be challenged and will continue to meet its design basis acceptance criteria following a large break loss of coolant accident. Therefore, the existing margin of safety is not significantly reduced by operation of Surry Units 1 and 2 with increased service water temperature limits. The NRC staff has reviewed the licensee’s analysis and, based on this review, it appears that the three standards of 10 CFR 50.92(c) are VerDate Aug<31>2005 17:40 Jul 16, 2007 Jkt 211001 satisfied. Therefore, the NRC staff proposes to determine that the amendment request involves no significant hazards consideration. Attorney for licensee: Lillian M. Cuoco, Esq., Senior Counsel, Dominion Resources Services, Inc., Millstone Power Station, Building 475, 5th Floor, Rope Ferry Road, Rt. 156, Waterford, Connecticut 06385. NRC Branch Chief: Evangelos C. Marinos. Notice of Issuance of Amendments to Facility Operating Licenses During the period since publication of the last biweekly notice, the Commission has issued the following amendments. The Commission has determined for each of these amendments that the application complies with the standards and requirements of the Atomic Energy Act of 1954, as amended (the Act), and the Commission’s rules and regulations. The Commission has made appropriate findings as required by the Act and the Commission’s rules and regulations in 10 CFR Chapter I, which are set forth in the license amendment. Notice of Consideration of Issuance of Amendment to Facility Operating License, Proposed No Significant Hazards Consideration Determination, and Opportunity for A Hearing in connection with these actions was published in the Federal Register as indicated. Unless otherwise indicated, the Commission has determined that these amendments satisfy the criteria for categorical exclusion in accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), no environmental impact statement or environmental assessment need be prepared for these amendments. If the Commission has prepared an environmental assessment under the special circumstances provision in 10 CFR 51.22(b) and has made a determination based on that assessment, it is so indicated. For further details with respect to the action see (1) The applications for amendment, (2) the amendment, and (3) the Commission’s related letter, Safety Evaluation and/or Environmental Assessment as indicated. All of these items are available for public inspection at the Commission’s Public Document Room (PDR), located at One White Flint North, Public File Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland. Publicly available records will be accessible from the Agencywide Documents Access and Management Systems (ADAMS) Public Electronic Reading Room on the internet at the NRC Web site, https://www.nrc.gov/ PO 00000 Frm 00044 Fmt 4703 Sfmt 4703 39085 reading-rm/adams.html. If you do not have access to ADAMS or if there are problems in accessing the documents located in ADAMS, contact the PDR Reference staff at 1 (800) 397–4209, (301) 415–4737 or by e-mail to pdr@nrc.gov. AmerGen Energy Company, LLC, Docket No. 50–289, Three Mile Island Nuclear Station, Unit 1 (TMI–1), Dauphin County, Pennsylvania Date of application for amendment: September 15, 2006, as supplemented by letters dated February 26, May 22, and June 5, 2007. Brief description of amendment: The amendment revised Technical Specification Section 6.8.5, ‘‘Reactor Building Leakage Rate Testing Program,’’ to allow a one-time deferral of the next Type A, containment integrated leak rate test from ‘‘no later than September 2008’’ to ‘‘prior to startup from T1R18 refueling outage. The T1R18 refueling outage will begin no later than November 1, 2009.’’ Date of issuance: June 29, 2007. Effective date: As of the date of issuance and shall be implemented within 60 days. Amendment No. 259. Facility Operating License No. DPR– 50. Amendment revised the license and the technical specifications. Date of initial notice in Federal Register: December 19, 2006 (71 FR 75989). The supplements dated February 26, May 22, and June 5, 2007 provided additional information that clarified the application, did not expand the scope of the application as originally noticed and did not change the NRC staff’s original proposed no significant hazards determination. The Commission’s related evaluation of the amendment is contained in a Safety Evaluation dated June 29, 2007. No significant hazards consideration comments received: No. Carolina Power & Light Company, Docket No. 50–261, H. B. Robinson Steam Electric Plant, Unit No. 2, Darlington County, South Carolina Date of application for amendment: July 17, 2006. Brief description of amendment: This amendment revises the containment design pressure requirements in Surveillance Requirements 3.6.8 and 5.5.16 due to a revision in the loss-ofcoolant accident containment pressure analysis. Date of issuance: June 15, 2007. Effective date: As of the date of issuance and shall be implemented within 60 days. E:\FR\FM\17JYN1.SGM 17JYN1 39086 Federal Register / Vol. 72, No. 136 / Tuesday, July 17, 2007 / Notices Amendment No. 215. Renewed Facility Operating License No. DPR–23. Amendment revises the technical specifications. Date of initial notice in Federal Register: August 29, 2006 (71 FR 51225). The Commission’s related evaluation of the amendment is contained in a safety evaluation dated June 15, 2007. No significant hazards consideration comments received: No. Duke Power Company LLC, et al., Docket Nos. 50–413 and 50–414, Catawba Nuclear Station, Units 1 and 2, York County, South Carolina sroberts on PROD1PC70 with NOTICES Date of application for amendments: June 5, 2006 as supplemented April 4, 2007. Brief description of amendments: The amendments revised the Technical Specification (TS) Section 3.8.1, ‘‘AC Sources—Operating,’’ surveillance requirement (SR) 3.8.1.13. The changes revised TS SR 3.8.1.13 and its associated Bases to state that the SR only verifies that non-emergency diesel generator (DG) trips are bypassed. The licensee stated that this change is based upon and consistent with Industry Technical Specification Task Force (TSTF), Standard TS Traveler, TSTF– 400–A, Revision 1, ‘‘Clarify Surveillance Requirement on Bypass of DG Automatic Trips.’’ Date of issuance: June 25, 2007. Effective date: As of the date of issuance and shall be implemented within 30 days from the date of issuance. Amendment Nos.: 236, 232. Facility Operating License Nos. NPF– 68 and NPF–81: Amendments revised the licenses and the technical specifications. Date of initial notice in Federal Register: December 5, 2006 (71 FR 70555). The supplement dated April 4, 2007, provided additional information that clarified the application, did not expand the scope of the application as originally noticed, and did not change the staff’s original proposed no significant hazards consideration determination. The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 25, 2007. No significant hazards consideration comments received: No. Duke Power Company LLC, Docket Nos. 50–369 and 50–370, McGuire Nuclear Station,Units 1 and 2, Mecklenburg County, North Carolina Date of application for amendments: June 5, 2006, as supplemented April 4, 2007. VerDate Aug<31>2005 17:40 Jul 16, 2007 Jkt 211001 Brief description of amendments: The amendments revised TS 3.8.1, ‘‘AC Sources—Operating,’’ surveillance requirement (SR) 3.8.1.13. The changes revise the SR 3.8.1.13 and its associated Bases to state that the SR only verifies that non-emergency diesel generator (DG) trips are bypassed. The licensee stated that this change is based upon and consistent with Industry Technical Specification Task Force (TSTF), Standard TS Traveler, TSTF–400–A, Revision 1, ‘‘Clarify Surveillance Requirement on Bypass of DG Automatic Trips.’’ Date of issuance: June 25, 2007. Effective date: As of the date of issuance and shall be implemented within 30 days from the date of issuance. Amendment Nos.: 242, 223. Renewed Facility Operating License Nos. NPF–9 and NPF–17: Amendments revised the licenses and the technical specifications. Date of initial notice in Federal Register: December 5, 2006 (71 FR 70555). The supplement dated April 4, 2007, provided additional information that clarified the application, did not expand the scope of the application as originally noticed, and did not change the staff’s original proposed no significant hazards consideration determination. The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 25, 2007. No significant hazards consideration comments received: No. Entergy Nuclear Operations, Inc., Docket No. 50–333, James A. FitzPatrick Nuclear Power Plant, Oswego County, New York Date of application for amendment: February 15, 2007. Brief description of amendment: The proposed amendment would revise Technical Specification (TS) Section 3.10.1, ‘‘Inservice Leak and Hydrostatic Testing Operation,’’ to expand its scope to include provisions for temperature excursions greater than 212 °F as a consequence of inservice leak or hydrostatic testing, and to allow performance of control rod scram time testing and other required testing when initiated in conjunction with the performance of an inservice leak or hydrostatic test, while considering operational conditions to be in Mode 4. The changes are consistent with NRC approved Revision 0 to Technical Specification Task Force (TSTF) Improved Standard Technical Specification Change Traveler, TSTF– 484, ‘‘Use of TS 3.10.1 for Scram Time Testing Activities.’’ PO 00000 Frm 00045 Fmt 4703 Sfmt 4703 Date of issuance: June 21, 2007. Effective date: As of the date of issuance, and shall be implemented within 30 days. Amendment No.: 288. Facility Operating License No. DPR– 59: The amendment revised the License and the Technical Specifications. Date of initial notice in Federal Register: April 10, 2007 (72 FR 17947). The Commission’s related evaluation of the amendment is contained in a Safety Evaluation dated June 21, 2007. No significant hazards consideration comments received: No. Entergy Operations, Inc., Docket No. 50–368, Arkansas Nuclear One, Unit No. 2, Pope County, Arkansas Date of application for amendment: March 15, 2007. Brief description of amendment: The amendment revises the Surveillance Requirement (SR) 4.6.2.1.d to require verification that containment spray nozzles are unobstructed following maintenance that could result in nozzle blockage, in lieu of the current SR of performing the test every 5 years. Date of issuance: July 2, 2007. Effective date: As of the date of issuance and shall be implemented within 60 days from the date of issuance. Amendment No.: 272. Renewed Facility Operating License No. NPF–6: Amendment revised the Technical Specifications/license. Date of initial notice in Federal Register: April 24, 2007 (72 FR 20381). The Commission’s related evaluation of the amendment is contained in a Safety Evaluation dated July 2, 2007. No significant hazards consideration comments received: No. Exelon Generation Company, LLC, Docket Nos. 50–237 and 50–249, Dresden Nuclear Power Station, Units 2 and 3, Grundy County, Illinois Date of application for amendment: June 2, 2006, as supplemented by letters dated August 18, 2006, October 5, 2006, and January 11, 2007. Brief description of amendment: The amendments revise technical specification to increase the allowable as-found main steam safety valve code safety function lift setpoint tolerance from ±1 percent to ±3 percent to align Dresden Nuclear Power Station, Units 2 and 3, with the American Society of Mechanical Engineers Code for Operation and Maintenance of Nuclear Power Plants and reduce the number of non-safety significant Licensee Event Reports written due to TS violations caused by setpoint drifting. Date of issuance: June 21, 2007. E:\FR\FM\17JYN1.SGM 17JYN1 Federal Register / Vol. 72, No. 136 / Tuesday, July 17, 2007 / Notices Effective date: As of the date of issuance and shall be implemented within 60 days. Amendment Nos.: 223 and 215. Renewed Facility Operating License Nos. DPR–19 and DPR–25: The amendments revised the Technical Specifications and License. Date of initial notice in Federal Register: August 15, 2006 (71 FR 46929). The August 18, 2006, October 5, 2006, and January 11, 2007, supplements contained clarifying information and did not change the NRC staff’s initial proposed finding of no significant hazards consideration. The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 21, 2007. No significant hazards consideration comments received: No. sroberts on PROD1PC70 with NOTICES Exelon Generation Company, LLC, Docket Nos. 50–373 and 50–374, LaSalle County Station, Units 1 and 2, LaSalle County, Illinois Date of application for amendments: March 16, 2006, as supplemented by letter dated April 6, 2007. Brief description of amendments: The amendments revise allowable values for four reactor core isolation cooling leak detection functions in Technical Specification Table 3.3.6.1–1, ‘‘Primary Containment Isolation Instrumentation.’’ Date of issuance: June 29, 2007. Effective date: As of the date of issuance and shall be implemented within 60 days. Amendment Nos.: 182/169. Facility Operating License Nos. NPF– 11 and NPF–18: The amendments revised the Technical Specifications and License. Date of initial notice in Federal Register: August 15, 2006 (71 FR 46929). The April 6, 2007 supplement, contained clarifying information and did not change the NRC staff’s initial proposed finding of no significant hazards consideration. The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 29, 2007. No significant hazards consideration comments received: No. FirstEnergy Nuclear Operating Company, et al., Docket No. 50–440, Perry Nuclear Power Plant, Unit No. 1, Lake County, Ohio Date of application for amendment: December 29, 2006. Brief description of amendment: The amendment modifies the technical specifications requirements for scram discharge volume vent and drain valves. VerDate Aug<31>2005 17:40 Jul 16, 2007 Jkt 211001 Date of issuance: June 22, 2007. Effective date: As of the date of issuance and shall be implemented within 90 days. Amendment No.: 145. Facility Operating License No. NPF– 58: This amendment revised the Technical Specifications and License. Date of initial notice in Federal Register: March 13, 2007 (72 FR 11388). The Commission’s related evaluation of the amendment is contained in a Safety Evaluation dated June 22, 2007. No significant hazards consideration comments received: No. FPL Energy Duane Arnold, LLC, Docket No. 50–331, Duane Arnold Energy Center, Linn County, Iowa Date of application for amendment: July 17, 2006, as supplemented by letter dated March 20, 2007. Brief description of amendment: The amendment revises the Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.3.1 to eliminate the requirement for the Containment Atmospheric Dilution system, allowing its removal from the Duane Arnold Energy Center. In a letter dated June 1, 2007, the licensee withdrew its request to change LCO 3.6.3.2, ‘‘Primary Containment oxygen Concentration,’’ to lengthen the duration of time for the primary containment to be de-inerted. Date of issuance: June 28, 2007. Effective date: As of the date of issuance and shall be implemented within 30 days. Amendment No.: 265. Facility Operating License No. DPR– 49: The amendment revises the Technical Specification. Date of initial notice in Federal Register: November 21, 2006 (71 FR 67395). The supplemental information provided additional information that clarified the application, did not expand the scope of the application as originally noticed, and did not change the Nuclear Regulatory Commission’s staff’s original proposed no significant hazards consideration determination. The Commission’s related evaluation of the amendment is contained in a Safety Evaluation dated June 28, 2007. No significant hazards consideration comments received: No. Nuclear Management Company, LLC, Docket Nos. 50–282 and 50–306, Prairie Island Nuclear Generating Plant, Units 1 and 2, Goodhue County, Minnesota Date of application for amendments: July 6, 2006, as supplemented by letters dated September 15 and December 26, 2006. PO 00000 Frm 00046 Fmt 4703 Sfmt 4703 39087 Brief description of amendments: The amendments incorporate new LargeBreak Loss-of-Coolant Accident (LBLOCA) analyses using the realistic LBLOCA methodology in the Nuclear Regulatory Commission approved WCAP–16009–P–A, ‘‘Realistic Large Break LOCA Evaluation Methodology using Automated Statistical Treatment of Uncertainty Method (ASTRUM)’’ and revise TS 5.6.5.b to include reference to WCAP–16009–P–A. Date of issuance: June 28, 2007. Effective date: As of the date of issuance and shall be implemented with the next fuel cycle (Unit 1 Cycle 25) commencing following the Winter 2008 refueling for Unit 1, and implemented within 90 days for Unit 2. Amendment Nos.: 179 and 169. Facility Operating License Nos. DPR– 42 and DPR–60: Amendments revised the Technical Specifications. Date of initial notice in Federal Register: September 12, 2006 (71 FR 53718). The supplemental letters contained clarifying information and did not change the initial no significant hazards consideration determination, and did not expand the scope of the original Federal Register notice. The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 28, 2007. No significant hazards consideration comments received: No. Pacific Gas and Electric Company, Docket Nos. 50–275 and 50–323, Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, California Date of application for amendments: December 29, 2006. Brief description of amendments: The amendments revised Technical Specification (TS) Section 5.5.8, ‘‘Inservice Testing Program,’’ in order to update references to the American Society of Mechanical Engineers Boiler and Pressure Vessel Code. Specifically, the change adopted the administrative, editorial, and clarification TS changes contained in TS Task Force (TSTF)–479, Revision 0, ‘‘Changes to Reflect Revision of 10 CFR [Title 10 of the Code of Federal Regulations] 50.55a,’’ and TSTF–497, Revision 0, ‘‘Limit Inservice Testing Program SR [Surveillance Requirement] 3.0.2 Application to Frequencies of 2 years or less.’’ Date of issuance: June 25, 2007. Effective date: As of its date of issuance and shall be implemented within 90 days from the date of issuance. Amendment Nos.: Unit 1–196; Unit 2–197 E:\FR\FM\17JYN1.SGM 17JYN1 39088 Federal Register / Vol. 72, No. 136 / Tuesday, July 17, 2007 / Notices Facility Operating License Nos. DPR– 80 and DPR–82: The amendments revised the Facility Operating Licenses and Technical Specifications. Date of initial notice in Federal Register: February 13, 2007 (72 FR 6784). The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 25, 2007. No significant hazards consideration comments received: No. Facility Operating License Nos. DPR– 80 and DPR–82: The amendments revised the Facility Operating Licenses and Technical Specifications. Date of initial notice in Federal Register: February 13, 2007 (72 FR 6784). The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 25, 2007. No significant hazards consideration comments received: No. Pacific Gas and Electric Company, Docket Nos. 50–275 and 50–323, Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, California sroberts on PROD1PC70 with NOTICES Date of application for amendments: December 29, 2006. Brief description of amendments: The amendments revise TS 5.5.16, ‘‘Containment Leakage Rate Testing Program,’’ to comply with the requirements of 10 CFR 50.55a(g)(4) for components classified as Code Class CC. Date of issuance: June 26, 2007. Effective date: As of its date of issuance and shall be implemented within 90 days from the date of issuance. Amendment Nos.: Unit 1–197; Unit 2–198. Facility Operating License Nos. DPR– 80 and DPR–82: The amendments revised the Facility Operating Licenses and Technical Specifications. Date of initial notice in Federal Register: February 13, 2007 (72 FR 6785). The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 26, 2007. No significant hazards consideration comments received: No. Southern Nuclear Operating Company, Inc., Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50–321 and 50–366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, Appling County, Georgia Date of application for amendments: January 30, 2007, as supplemented April 11, 2007. VerDate Aug<31>2005 17:40 Jul 16, 2007 Jkt 211001 Brief description of amendments: The amendments revised staff position duties and titles in Sections 2 and 5 of the Technical Specifications. Date of issuance: June 7, 2007. Effective date: As of the date of issuance and shall be implemented within 30 days from the date of issuance. Amendment Nos.: 252, 196. Renewed Facility Operating License Nos. DPR–57 and NPF–5: Amendments revised the licenses and the technical specifications. Date of initial notice in Federal Register: February 13, 2007 (72 FR 6790). The supplement dated April 11, 2007, provided additional information that clarified the application, did not expand the scope of the application as originally noticed, and did not change the staff’s original proposed no significant hazards consideration determination. The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 7, 2007. No significant hazards consideration comments received: No. Southern Nuclear Operating Company, Inc., Docket Nos. 50–424 and 50–425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County, Georgia Date of application for amendments: January 30, 2007, as supplemented April 11, 2007. Brief description of amendments: The amendments revised staff position duties and titles in Sections 2 and 5 of the Technical Specifications. Date of issuance: June 12, 2007. Effective date: As of the date of issuance and shall be implemented within 30 days from the date of issuance. Amendment Nos.: 148, 128. Renewed Facility Operating License Nos. NPF–68 and NPF–81: Amendments revised the licenses and the technical specifications. Date of initial notice in Federal Register: February 13, 2007 (72 FR 6791). The supplement dated April 11, 2007, provided additional information that clarified the application, did not expand the scope of the application as originally noticed, and did not change the staff’s original proposed no significant hazards consideration determination. The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 12, 2007. No significant hazards consideration comments received: No. PO 00000 Frm 00047 Fmt 4703 Sfmt 4703 STP Nuclear Operating Company, Docket Nos. 50–498 and 50–499, South Texas Project, Units 1 and 2, Matagorda County, Texas Date of amendment request: March 30, 2006, as supplemented by letters dated October 2, 2006, and February 26, 2007. Brief description of amendments: The amendments revise TS 3.3.3.6, ‘‘Accident Monitoring Instrumentation,’’ with respect to the required action for inoperable wide range reactor coolant temperature, wide range steam generator water level, and auxiliary feedwater flow instruments. Date of issuance: June 13, 2007. Effective date: As of the date of issuance and shall be implemented within 60 days of issuance. Amendment Nos.: Unit 1–177; Unit 2–164. Facility Operating License Nos. NPF– 76 and NPF–80: The amendments revised the Facility Operating Licenses and Technical Specifications. Date of initial notice in Federal Register: June 6, 2006 (71 FR 32608). The supplemental letters dated October 2, 2006, and February 26, 2007, provided additional information that clarified the application, did not expand the scope of the application as originally noticed, and did not change the staff’s original proposed no significant hazards consideration determination as published in the Federal Register. The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 13, 2007. No significant hazards consideration comments received: No. STP Nuclear Operating Company, Docket Nos. 50–498 and 50–499, South Texas Project, Units 1 and 2, Matagorda County, Texas Date of amendment request: April 4, 2006. Brief description of amendments: The amendment request changed the name of one licensee, Texas Genco, LP (Texas Genco), to NRG South Texas LP. The name change results from the purchase of Texas Genco’s parent company by NRG Energy, Inc. as approved by the NRC in January 2006. Date of issuance: June 29, 2007. Effective date: As of the date of issuance and shall be implemented within 30 days of issuance. Amendment Nos.: Unit 1–178; Unit 2–165. Facility Operating License Nos. NPF– 76 and NPF–80: The amendments revised the Facility Operating Licenses. Date of initial notice in Federal Register: May 9, 2007 (72 FR 26428). E:\FR\FM\17JYN1.SGM 17JYN1 Federal Register / Vol. 72, No. 136 / Tuesday, July 17, 2007 / Notices The Commission’s related evaluation of the amendments is contained in a Safety Evaluation dated June 29, 2007. No significant hazards consideration comments received: No. Dated at Rockville, Maryland, this sixth day of July 2007. For the Nuclear Regulatory Commission. Catherine Haney, Director, Division of Operating Reactor Licensing, Office of Nuclear Reactor Regulation. [FR Doc. E7–13537 Filed 7–16–07; 8:45 am] BILLING CODE 7590–01–P NUCLEAR REGULATORY COMMISSION Background Notice of Availability of Model Application Concerning Technical Specification Task Force (TSTF) Traveler To Provide Actions for One Steam Supply to Turbine Driven AFW/ EFW Pump Inoperable Using the Consolidated Line Item Improvement Process Nuclear Regulatory Commission. ACTION: Notice of availability. sroberts on PROD1PC70 with NOTICES AGENCY: SUMMARY: Notice is hereby given that the staff of the Nuclear Regulatory Commission (NRC) has prepared a model license amendment request (LAR), model safety evaluation (SE), and model proposed no significant hazards consideration (NSHC) determination related to changes to Actions in the Standard Technical Specifications (STS) relating to One Steam Supply to Turbine Driven Auxiliary Feedwater/Emergency Feedwater (AFW/EFW) Pump Inoperable. This change establishes a Completion Time in the Standard Technical Specifications for the Condition where one steam supply to the turbine driven AFW/EFW pump is inoperable concurrent with an inoperable motor driven AFW/EFW train. The purpose of these models is to permit the NRC to efficiently process amendments that propose to adopt the associated changes into plant-specific technical specifications (TS). Licensees of nuclear power reactors to which the models apply can request amendments confirming the applicability of the SE and NSHC determination to their reactors. DATES: The NRC staff issued a Federal Register Notice (72 FR 12845, March 19, 2007) which provided a model LAR, model SE, and model NSHC related to one steam supply to turbine driven auxiliary feedwater/emergency feedwater pump inoperable; similarly VerDate Aug<31>2005 17:40 Jul 16, 2007 the NRC staff herein provides the model LAR, a revised model SE, and the model NSHC. The NRC staff can most efficiently consider applications based upon the model LAR, which references the model SE, if the application is submitted within one year of this Federal Register Notice. FOR FURTHER INFORMATION CONTACT: Trent L. Wertz, Technical Specifications Branch, Division of Inspection and Regional Support, Office of Nuclear Reactor Regulation, Mail Stop O–12H2, U.S. Nuclear Regulatory Commission, Washington, DC 20555–0001, telephone 301–415–1568. SUPPLEMENTARY INFORMATION: Jkt 211001 Regulatory Issue Summary 2000–06, ‘‘Consolidated Line Item Improvement Process for Adopting Standard Technical Specification Changes for Power Reactors,’’ was issued on March 20, 2000. The consolidated line item improvement process (CLIIP) is intended to improve the efficiency and transparency of NRC licensing processes. This is accomplished by processing proposed changes to the Standard Technical Specifications (STS) (NUREGs 1430—1434) in a manner that supports subsequent license amendment applications. The CLIIP includes an opportunity for the public to comment on proposed changes to the STS following a preliminary assessment by the NRC staff and finding that the change will likely be offered for adoption by licensees. The CLIIP directs the NRC staff to evaluate any comments received for a proposed change to the STS and to either reconsider the change or proceed with announcing the availability of the change to licensees. Those licensees opting to apply for the subject change to TS are responsible for reviewing the NRC staff’s evaluation, referencing the applicable technical justifications, and providing any necessary plant specific information. Each amendment application submitted in response to the notice of availability would be processed and noticed in accordance with applicable rules and NRC procedures. This notice involves establishing a Completion Time in the Limiting Condition for Operation (LCO) 3.7.5 of the STS for the Condition where one steam supply to the turbine driven AFW/EFW pump is inoperable concurrent with an inoperable motor driven AFW/EFW train. This notice also involves two additional changes to the STS that establish specific Conditions and Action requirements: (1) For when two motor driven AFW/EFW trains are PO 00000 Frm 00048 Fmt 4703 Sfmt 4703 39089 inoperable at the same time and; (2) for when the turbine driven AFW/EFW train is inoperable either (a) due solely to one inoperable steam supply, or (b) due to reasons other than one inoperable steam supply. The changes were proposed by the Technical Specification Task Force (TSTF) in TSTF Traveler TSTF–412, Revision 3, which is accessible electronically from the Agencywide Documents Access and Management System (ADAMS) Public Electronic Reading Room on the Internet at the NRC Web site https://www.nrc.gov/ reading-rm/adams.html (Accession No. ML070100363). Persons who do not have access to ADAMS or who encounter problems in accessing the documents located in ADAMS, should contact the NRC Public Document Room Reference staff by telephone at 1–800– 397–4209, 301–415–4737, or by e-mail to pdr@nrc.gov. Applicability This change is applicable to all pressurized water reactors (PWRs) designed by Babcock and Wilcox (B&W), Westinghouse, and Combustion Engineering (CE). To efficiently process the incoming license amendment applications, the NRC staff requests that each licensee applying for the changes use the CLIIP to submit a License Amendment Request (LAR) that conforms to the enclosed Model Application (Enclosure 1). Any deviations from the Model Application should be explained in the licensee’s submittal. Significant deviations from the approach, or inclusion of additional changes to the license, will result in staff rejection of the submittal. Instead, licensees desiring significant variations and/or additional changes should submit a LAR that does not claim to adopt TSTF–412. Variations from the approach recommended in this notice may require additional review by the NRC staff and may increase the time and resources needed for the review. Public Notices The staff issued a Federal Register Notice (72 FR 12845, March 19, 2007) that requested public comment on the NRC’s pending action to establish a Completion Time in the Limiting Condition for Operation (LCO) 3.7.5 of the STS for the Condition where one steam supply to the turbine driven AFW/EFW pump is inoperable concurrent with an inoperable motor driven AFW/EFW train. This notice also involves two additional changes to the STS that establish specific Conditions and Action requirements: (1) For when two motor driven AFW/EFW trains are inoperable at the same time and; (2) for E:\FR\FM\17JYN1.SGM 17JYN1

Agencies

[Federal Register Volume 72, Number 136 (Tuesday, July 17, 2007)]
[Notices]
[Pages 39081-39089]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: E7-13537]


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NUCLEAR REGULATORY COMMISSION


Biweekly Notice; Applications and Amendments to Facility 
Operating Licenses; Involving No Significant Hazards Considerations

I. Background

    Pursuant to section 189a. (2) of the Atomic Energy Act of 1954, as 
amended (the Act), the U.S. Nuclear Regulatory Commission (the 
Commission or NRC staff) is publishing this regular biweekly notice. 
The Act requires the Commission publish notice of any amendments 
issued, or proposed to be issued and grants the Commission the 
authority to issue and make immediately effective any amendment to an 
operating license upon a determination by the Commission that such 
amendment involves no significant hazards consideration, 
notwithstanding the pendency before the Commission of a request for a 
hearing from any person.
    This biweekly notice includes all notices of amendments issued, or 
proposed to be issued from June 21, 2007 to July 3, 2007. The last 
biweekly notice was published on July 3, 2007 (72 FR 36520).

Notice of Consideration of Issuance of Amendments to Facility Operating 
Licenses, Proposed No Significant Hazards Consideration Determination, 
and Opportunity for a Hearing

    The Commission has made a proposed determination that the following 
amendment requests involve no significant hazards consideration. Under 
the Commission's regulations in 10 CFR 50.92, this means that operation 
of the facility in accordance with the proposed amendment would not (1) 
Involve a significant increase in the probability or consequences of an 
accident previously evaluated; or (2) create the possibility of a new 
or different kind of accident from any accident previously evaluated; 
or (3) involve a significant reduction in a margin of safety. The basis 
for this proposed determination for each amendment request is shown 
below.
    The Commission is seeking public comments on this proposed 
determination. Any comments received within 30 days after the date of 
publication of this notice will be considered in making any final

[[Page 39082]]

determination. Within 60 days after the date of publication of this 
notice, the licensee may file a request for a hearing with respect to 
issuance of the amendment to the subject facility operating license and 
any person whose interest may be affected by this proceeding and who 
wishes to participate as a party in the proceeding must file a written 
request for a hearing and a petition for leave to intervene.
    Normally, the Commission will not issue the amendment until the 
expiration of 60 days after the date of publication of this notice. The 
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment 
involves no significant hazards consideration. In addition, the 
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day 
comment period such that failure to act in a timely way would result, 
for example in derating or shutdown of the facility. Should the 
Commission take action prior to the expiration of either the comment 
period or the notice period, it will publish in the Federal Register a 
notice of issuance. Should the Commission make a final No Significant 
Hazards Consideration Determination, any hearing will take place after 
issuance. The Commission expects that the need to take this action will 
occur very infrequently.
    Written comments may be submitted by mail to the Chief, Rulemaking, 
Directives and Editing Branch, Division of Administrative Services, 
Office of Administration, U.S. Nuclear Regulatory Commission, 
Washington, DC 20555-0001, and should cite the publication date and 
page number of this Federal Register notice. Written comments may also 
be delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
Rockville, Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. 
Copies of written comments received may be examined at the Commission's 
Public Document Room (PDR), located at One White Flint North, Public 
File Area O1F21, 11555 Rockville Pike (first floor), Rockville, 
Maryland. The filing of requests for a hearing and petitions for leave 
to intervene is discussed below.
    Within 60 days after the date of publication of this notice, the 
licensee may file a request for a hearing with respect to issuance of 
the amendment to the subject facility operating license and any person 
whose interest may be affected by this proceeding and who wishes to 
participate as a party in the proceeding must file a written request 
for a hearing and a petition for leave to intervene. Requests for a 
hearing and a petition for leave to intervene shall be filed in 
accordance with the Commission's ``Rules of Practice for Domestic 
Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
consult a current copy of 10 CFR 2.309, which is available at the 
Commission's PDR, located at One White Flint North, Public File Area 
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland. 
Publicly available records will be accessible from the Agencywide 
Documents Access and Management System's (ADAMS) Public Electronic 
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition 
for leave to intervene is filed within 60 days, the Commission or a 
presiding officer designated by the Commission or by the Chief 
Administrative Judge of the Atomic Safety and Licensing Board Panel, 
will rule on the request and/or petition; and the Secretary or the 
Chief Administrative Judge of the Atomic Safety and Licensing Board 
will issue a notice of a hearing or an appropriate order.
    As required by 10 CFR 2.309, a petition for leave to intervene 
shall set forth with particularity the interest of the petitioner in 
the proceeding, and how that interest may be affected by the results of 
the proceeding. The petition should specifically explain the reasons 
why intervention should be permitted with particular reference to the 
following general requirements: (1) The name, address, and telephone 
number of the requestor or petitioner; (2) the nature of the 
requestor's/petitioner's right under the Act to be made a party to the 
proceeding; (3) the nature and extent of the requestor's/petitioner's 
property, financial, or other interest in the proceeding; and (4) the 
possible effect of any decision or order which may be entered in the 
proceeding on the requestor's/petitioner's interest. The petition must 
also set forth the specific contentions which the petitioner/requestor 
seeks to have litigated at the proceeding.
    Each contention must consist of a specific statement of the issue 
of law or fact to be raised or controverted. In addition, the 
petitioner/requestor shall provide a brief explanation of the bases for 
the contention and a concise statement of the alleged facts or expert 
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The 
petitioner/requestor must also provide references to those specific 
sources and documents of which the petitioner is aware and on which the 
petitioner/requestor intends to rely to establish those facts or expert 
opinion. The petition must include sufficient information to show that 
a genuine dispute exists with the applicant on a material issue of law 
or fact. Contentions shall be limited to matters within the scope of 
the amendment under consideration. The contention must be one which, if 
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at 
least one contention will not be permitted to participate as a party.
    Those permitted to intervene become parties to the proceeding, 
subject to any limitations in the order granting leave to intervene, 
and have the opportunity to participate fully in the conduct of the 
hearing.
    If a hearing is requested, and the Commission has not made a final 
determination on the issue of no significant hazards consideration, the 
Commission will make a final determination on the issue of no 
significant hazards consideration. The final determination will serve 
to decide when the hearing is held. If the final determination is that 
the amendment request involves no significant hazards consideration, 
the Commission may issue the amendment and make it immediately 
effective, notwithstanding the request for a hearing. Any hearing held 
would take place after issuance of the amendment. If the final 
determination is that the amendment request involves a significant 
hazards consideration, any hearing held would take place before the 
issuance of any amendment.
    A request for a hearing or a petition for leave to intervene must 
be filed by: (1) First class mail addressed to the Office of the 
Secretary of the Commission, U.S. Nuclear Regulatory Commission, 
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications 
Staff; (2) courier, express mail, and expedited delivery services: 
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555 
Rockville Pike, Rockville, Maryland 20852, Attention: Rulemaking and 
Adjudications Staff; (3) E-mail addressed to the Office of the 
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov; 
or (4) facsimile transmission addressed to the Office of the Secretary, 
U.S. Nuclear Regulatory Commission, Washington, DC, Attention: 
Rulemaking and Adjudications Staff at (301) 415-1101, verification 
number is (301) 415-1966. A copy of the request for hearing and

[[Page 39083]]

petition for leave to intervene should also be sent to the Office of 
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 
20555-0001, and it is requested that copies be transmitted either by 
means of facsimile transmission to (301) 415-3725 or by e-mail to 
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition 
for leave to intervene should also be sent to the attorney for the 
licensee.
    Nontimely requests and/or petitions and contentions will not be 
entertained absent a determination by the Commission or the presiding 
officer of the Atomic Safety and Licensing Board that the petition, 
request and/or the contentions should be granted based on a balancing 
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
    For further details with respect to this action, see the 
application for amendment which is available for public inspection at 
the Commission's PDR, located at One White Flint North, Public File 
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland. 
Publicly available records will be accessible from the ADAMS Public 
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS 
or if there are problems in accessing the documents located in ADAMS, 
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or 
by e-mail to pdr@nrc.gov.

Nuclear Management Company, LLC, Docket Nos. 50-282 and 50-306, Prairie 
Island Nuclear Generating Plant (PINGP), Units 1 and 2, Goodhue County, 
Minnesota

    Date of amendment request: May 10, 2007.
    Description of amendment request: The proposed amendments would 
modify the Technical Specifications (TS) by removing the specific 
isolation time for the main steam isolation valves from the associated 
TS Surveillance Requirements (SRs) and by replacing it with the 
requirement to verify the valve isolation time is within limits. The 
changes are consistent with Nuclear Regulatory Commission (NRC) 
approved Industry/Technical Specification Task Force (TSTF)-491, 
Removal of the Main Steam and Main Feedwater Valve Isolation Time from 
Technical Specifications, Revision 2. The proposed amendments deviate 
from TSTF-491 in that the current PINGP TS and associated SRs for the 
main feedwater isolation valves do not include valve closure times, and 
thus these changes in TSTF-491 are not applicable to the PINGP TSs and 
are not adopted.
    The NRC staff issued a notice of opportunity for comment in the 
Federal Register on October 5, 2006 (71 FR 58884), on possible 
amendments concerning the consolidation line item improvement process 
(CLIIP), including a model safety evaluation and a model no significant 
hazards consideration determination. The NRC staff subsequently issued 
a notice of availability of the models for referencing in license 
amendment applications in the Federal Register on December 29, 2006 (71 
FR 78472) as part of the CLIIP. In its application dated May 10, 2007, 
the licensee affirmed the applicability of the following determination.
    Basis for proposed no significant hazards consideration 
determination: As required by 10 CFR 50.91(a), an analysis of the issue 
of no significant hazards consideration is presented below:

Criterion 1--The Proposed Change Does Not Involve a Significant 
Increase in the Probability or Consequences of an Accident 
Previously Evaluated

    The proposed change allows relocating main steam and main 
feedwater valve isolation times to the Licensee Controlled Document 
that is referenced in the Bases. The proposed change is described in 
Technical Specification Task Force (TSTF) Standard TS Change 
Traveler TSTF-491 related to relocating the main steam and main 
feedwater valves isolation times to the Licensee Controlled Document 
that is referenced in the Bases and replacing the isolation time 
with the phrase, within limits.
    The proposed change does not involve a physical alteration of 
the plant (no new or different type of equipment will be installed). 
The proposed changes relocate the main steam and main feedwater 
isolation valve times to the Licensee Controlled Document that is 
referenced in the Bases. The requirements to perform the testing of 
these isolation valves are retained in the TS. Future changes to the 
Bases or licensee-controlled document will be evaluated pursuant to 
the requirements of 10 CFR 50.59, Changes, test and experiments, to 
ensure that such changes do not result in more than minimal increase 
in the probability or consequences of an accident previously 
evaluated.
    The proposed changes do not adversely affect accident initiators 
or precursors nor alter the design assumptions, conditions, and 
configuration of the facility or the manner in which the plant is 
operated and maintained. The proposed changes do not adversely 
affect the ability of structures, systems and components (SSCs) to 
perform their intended safety function to mitigate the consequences 
of an initiating event within the assumed acceptance limits. The 
proposed changes do not affect the source term, containment 
isolation, or radiological consequences of any accident previously 
evaluated. Further, the proposed changes do not increase the types 
and the amounts of radioactive effluent that may be released, nor 
significantly increase individual or cumulative occupation/public 
radiation exposures.
    Therefore, the changes do not involve a significant increase in 
the probability or consequences of any accident previously 
evaluated.

Criterion 2--The Proposed Change Does Not Create the Possibility of 
a New or Different Kind of Accident From any Previously Evaluated

    The proposed changes relocate the main steam and main feedwater 
valve isolation times to the Licensee Controlled Document that is 
referenced in the Bases. In addition, the valve isolation times are 
replaced in the TS with the phrase ``within limits.'' The changes do 
not involve a physical altering of the plant (i.e., no new or 
different type of equipment will be installed) or a change in 
methods governing normal plant operation. The requirements in the TS 
continue to require testing of the main steam and main feedwater 
isolation valves to ensure the proper functioning of these isolation 
valves.
    Therefore, the changes do not create the possibility of a new or 
different kind of accident from any previously evaluated.

Criterion 3--The Proposed Change Does Not Involve a Significant 
Reduction in the Margin of Safety

    The proposed changes relocate the main steam and main feedwater 
valve isolation times to the Licensee Controlled Document that is 
referenced in the Bases. In addition, the valve isolation times are 
replaced in the TS with the phrase ``within limits.'' Instituting 
the proposed changes will continue to ensure the testing of main 
steam and main feedwater isolation valves. Changes to the Bases or 
license controlled document are performed in accordance with 10 CFR 
50.59. This approach provides an effective level of regulatory 
control and ensures that main steam and feedwater isolation valve 
testing is conducted such that there is no significant reduction in 
the margin of safety.
    The margin of safety provided by the isolation valves is 
unaffected by the proposed changes since there continue to be TS 
requirements to ensure the testing of main steam and main feedwater 
isolation valves. The proposed changes maintain sufficient controls 
to preserve the current margins of safety.

    The NRC staff has reviewed the licensees analysis and, based on 
this review, it appears that the three standards of 10 CFR 50.92(c) are 
satisfied. Therefore, the NRC staff proposes to determine that the 
amendment requests involve no significant hazards consideration.
    Attorney for licensee: Jonathan Rogoff, Esquire, Vice President, 
Counsel & Secretary, Nuclear Management Company, LLC, 700 First Street, 
Hudson, WI 54016.
    NRC Acting Branch Chief: Travis L. Tate.

[[Page 39084]]

Southern Nuclear Operating Company, Inc., Georgia Power Company, 
Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, 
City of Dalton, Georgia, Docket Nos. 50-321 and 50-366, Edwin I. Hatch 
Nuclear Plant, Units 1 and 2, Appling County, Georgia

    Date of amendment request: October 30, 2006.
    Description of amendment request: The proposed amendment would 
revise Technical Specification (TS) Section 5.3.1, Administrative 
controls, to (1) Improve administrative flexibility and clarity in the 
wording of the specification and (2) replace a specific position title 
with a generic position title for the senior individual in charge of 
health physics.
    Basis for proposed no significant hazards consideration 
determination: As required by 10 CFR 50.91(a), an analysis of the issue 
of no significant hazards consideration is presented below:

    1. Does the proposed change involve a significant increase in 
the probability or consequences of an accident previously evaluated?
    The proposed change to Technical Specifications Administrative 
Controls Section 5.3.1 involves the use of a more generic 
designation for the unit staff position responsible for Health 
Physics without reducing the level of authority required for that 
position. The proposed change also allows the flexibility to use an 
accredited program for qualifying personnel to fill unit staff 
positions, which represents an acceptable alternative to the 
qualification requirements for these positions as currently 
specified in the Technical Specifications. Since the proposed 
changes are administrative in nature, they do not involve any 
physical changes to any structures, systems, or components, nor will 
their performance requirements be altered. The proposed changes also 
do not affect the operation, maintenance, or testing of the plant. 
Therefore, the response of the plant to previously analyzed 
accidents will not be affected. Consequently, the proposed changes 
do not involve a significant increase or any increase in the 
probability or consequences of an accident previously evaluated.
    2. Does the proposed change create the possibility of a new or 
different kind of accident from any previously evaluated?
    The proposed changes to the Technical Specifications will have 
no adverse impact on the overall qualification of the unit staff. 
The use of a more generic designation for the unit staff position 
responsible for Health Physics and the alternative use of an 
accredited program that has been endorsed by the NRC will ensure the 
educational requirements and power plant experience for each unit 
staff position are properly satisfied and will continue to fulfill 
applicable regulatory requirements. Also, since no change is being 
made to the design, operation, maintenance, or testing of the plant, 
no new methods of operation or failure modes are introduced by the 
proposed changes. Therefore, the possibility of a new or different 
kind of accident from any previously evaluated is not created.
    3. Does the proposed change involve a significant decrease in 
the margin of safety?
    The proposed changes to the Technical Specifications will have 
no adverse impact on the onsite organizational features necessary to 
assure safe operation of the plant. Lines of authority for plant 
operation are unaffected by the proposed changes. Also, the adoption 
of the more generic designation of the individual responsible for 
Health Physics will reduce the regulatory burden of having to devote 
limited resources to process a license amendment whenever a title 
change for this position is implemented. Accordingly, this reduction 
in regulatory burden and the option to use an accredited program 
endorsed by NRC to qualify the unit staff will improve plant 
efficiency without compromising plant safety. Therefore, the 
proposed changes do not involve a significant decrease in the margin 
of safety.

    The NRC staff proposes to determine that the amendment request 
involves no significant hazards consideration.
    Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 
20037.
    NRC Branch Chief: Evangelos C. Marinos.

Southern Nuclear Operating Company, Inc., Georgia Power Company, 
Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, 
City of Dalton, Georgia, Docket Nos. 50-321 and 50-366, Edwin I. Hatch 
Nuclear Plant, Units 1 and 2, Appling County, Georgia

    Date of amendment request: June 5 and June 11, 2007.
    Description of amendment request: The proposed amendment would 
revise Technical Specification (TS) 3.1.4, Control Rod Scram Times, 
using the consolidated line-term improvement process. These changes are 
based on TS Task Force (TSTF) change traveler TSTF-460, that has been 
approved generically for the boiling water reactor (BWR) Standard TS, 
NUREG-1433 (BWR/4). The frequency of Surveillance Requirement 3.1.4.2, 
control rod scram time testing, is revised from ``120 days cumulative 
operation in MODE 1'' to ``200 days cumulative operation in MODE 1.''
    The NRC staff issued a notice of availability of a model safety 
evaluation and model no significant hazards consideration (NSHC) 
determination for referencing in license amendment applications in the 
Federal Register on August 23, 2004 (69 FR 51854). The licensee 
affirmed the applicability of the model NSHC determination in its 
application and supplement dated June 5 and June 11, 2007.
    Basis for proposed no significant hazards consideration 
determination: As required by 10 CFR 50.91(a), an analysis of the issue 
of no significant hazards consideration is presented below:

    1. Does the change involve a significant increase in the 
probability or consequences of an accident previously evaluated?
    Response: No.
    The proposed change extends the frequency for testing control 
rod scram time testing from every 120 days of cumulative Mode 1 
operation to 200 days of cumulative Mode 1 operation. The frequency 
of surveillance testing is not an initiator of any accident 
previously evaluated. The frequency of surveillance testing does not 
affect the ability to mitigate any accident previously evaluated, as 
the tested component is still required to be operable. Therefore, 
the proposed change does not involve a significant increase in the 
probability or consequences of an accident previously evaluated.
    2. Does the change create the possibility of a new or different 
kind of accident from any accident previously evaluated?
    Response: No.
    The proposed change extends the frequency for testing control 
rod scram time testing from every 120 days of cumulative Mode 1 
operation to 200 days of cumulative Mode 1 operation. The proposed 
change does not result in any new or different modes of plant 
operation. Therefore, the proposed change does not create the 
possibility of a new or different kind of accident from any 
previously evaluated.
    3. Does the proposed change involve a significant reduction in a 
margin of safety?
    Response: No.
    The proposed change extends the frequency for testing control 
rod scram time testing from every 120 days of cumulative Mode 1 
operation to 200 days of cumulative Mode 1 operation. The proposed 
change continues to test the control rod scram time to ensure the 
assumptions in the safety analysis are protected. Therefore, the 
proposed change does not involve a significant reduction in a margin 
of safety.

    The NRC staff proposes to determine that the amendment request 
involves no significant hazards consideration.
    Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 
20037.
    NRC Branch Chief: Evangelos C. Marinos.

Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia

    Date of amendment request: June 25, 2007.
    Description of amendment request: The proposed change increases the

[[Page 39085]]

maximum Technical Specification (TS) service water (SW) temperature 
limit from 95 [deg]F to 100 [deg]F, and revises the TS Figure 3.8-1, 
which provides allowable containment air partial pressure versus SW 
temperature.
    Basis for proposed no significant hazards consideration 
determination: As required by 10 CFR 50.91(a), the licensee has 
provided its analysis of the issue of no significant hazards 
consideration, which is presented below:

    1. Does the proposed change involve a significant increase in 
the probability or consequences of an accident previously evaluated?
    Operating with increased maximum service water temperature 
limits does not affect the frequency of accident initiating events. 
Therefore, the probability of an accident previously analyzed is not 
increased. Plant systems supported by SW have been evaluated for 
operation with a service water temperature limit of 100 [deg]F, and 
it determined that there is no operational impact when operating at 
the higher SW temperature.
    Although the service water temperature limit is being increased, 
the containment will continue to meet its design basis acceptance 
criteria following a large-break loss of coolant accident as 
identified in the UFSAR [Updated Final Safety Analysis Report]. 
Therefore, there is no increase in the consequences of any accident 
previously evaluated resulting from operation of Surry Units 1 and 2 
with an increased service water temperature limit.
    2. Does the proposed change create the possibility of a new or 
different kind of accident from any accident previously evaluated?
    There are no new failure modes or mechanisms associated with 
operating Surry Units 1 and 2 with an increased service water 
temperature limit of 100 [deg]F. As noted above, the increased 
service water temperature limit does not affect plant operation, 
since plant systems supported by SW have been evaluated for 
operation with a SW temperature limit of 100 [deg]F and no 
operational impact was identified. Therefore, there are no new or 
different kinds of accidents created by operation of Surry Units 1 
and 2 with increased service water temperature limits.
    3. Does the proposed change involve a significant reduction in 
the margin of safety?
    The containment analysis acceptance criteria continue to be met 
when operating with the proposed increased maximum service water 
temperature limit. Containment integrity will not be challenged and 
will continue to meet its design basis acceptance criteria following 
a large break loss of coolant accident. Therefore, the existing 
margin of safety is not significantly reduced by operation of Surry 
Units 1 and 2 with increased service water temperature limits.

    The NRC staff has reviewed the licensee's analysis and, based on 
this review, it appears that the three standards of 10 CFR 50.92(c) are 
satisfied. Therefore, the NRC staff proposes to determine that the 
amendment request involves no significant hazards consideration.
    Attorney for licensee: Lillian M. Cuoco, Esq., Senior Counsel, 
Dominion Resources Services, Inc., Millstone Power Station, Building 
475, 5th Floor, Rope Ferry Road, Rt. 156, Waterford, Connecticut 06385.
    NRC Branch Chief: Evangelos C. Marinos.

Notice of Issuance of Amendments to Facility Operating Licenses

    During the period since publication of the last biweekly notice, 
the Commission has issued the following amendments. The Commission has 
determined for each of these amendments that the application complies 
with the standards and requirements of the Atomic Energy Act of 1954, 
as amended (the Act), and the Commission's rules and regulations. The 
Commission has made appropriate findings as required by the Act and the 
Commission's rules and regulations in 10 CFR Chapter I, which are set 
forth in the license amendment.
    Notice of Consideration of Issuance of Amendment to Facility 
Operating License, Proposed No Significant Hazards Consideration 
Determination, and Opportunity for A Hearing in connection with these 
actions was published in the Federal Register as indicated.
    Unless otherwise indicated, the Commission has determined that 
these amendments satisfy the criteria for categorical exclusion in 
accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
no environmental impact statement or environmental assessment need be 
prepared for these amendments. If the Commission has prepared an 
environmental assessment under the special circumstances provision in 
10 CFR 51.22(b) and has made a determination based on that assessment, 
it is so indicated.
    For further details with respect to the action see (1) The 
applications for amendment, (2) the amendment, and (3) the Commission's 
related letter, Safety Evaluation and/or Environmental Assessment as 
indicated. All of these items are available for public inspection at 
the Commission's Public Document Room (PDR), located at One White Flint 
North, Public File Area 01F21, 11555 Rockville Pike (first floor), 
Rockville, Maryland. Publicly available records will be accessible from 
the Agencywide Documents Access and Management Systems (ADAMS) Public 
Electronic Reading Room on the internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS 
or if there are problems in accessing the documents located in ADAMS, 
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or 
by e-mail to pdr@nrc.gov.

AmerGen Energy Company, LLC, Docket No. 50-289, Three Mile Island 
Nuclear Station, Unit 1 (TMI-1), Dauphin County, Pennsylvania

    Date of application for amendment: September 15, 2006, as 
supplemented by letters dated February 26, May 22, and June 5, 2007.
    Brief description of amendment: The amendment revised Technical 
Specification Section 6.8.5, ``Reactor Building Leakage Rate Testing 
Program,'' to allow a one-time deferral of the next Type A, containment 
integrated leak rate test from ``no later than September 2008'' to 
``prior to startup from T1R18 refueling outage. The T1R18 refueling 
outage will begin no later than November 1, 2009.''
    Date of issuance: June 29, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 60 days.
    Amendment No. 259.
    Facility Operating License No. DPR-50. Amendment revised the 
license and the technical specifications.
    Date of initial notice in Federal Register: December 19, 2006 (71 
FR 75989).
    The supplements dated February 26, May 22, and June 5, 2007 
provided additional information that clarified the application, did not 
expand the scope of the application as originally noticed and did not 
change the NRC staff's original proposed no significant hazards 
determination. The Commission's related evaluation of the amendment is 
contained in a Safety Evaluation dated June 29, 2007.
    No significant hazards consideration comments received: No.

Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam 
Electric Plant, Unit No. 2, Darlington County, South Carolina

    Date of application for amendment: July 17, 2006.
    Brief description of amendment: This amendment revises the 
containment design pressure requirements in Surveillance Requirements 
3.6.8 and 5.5.16 due to a revision in the loss-of-coolant accident 
containment pressure analysis.
    Date of issuance: June 15, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 60 days.

[[Page 39086]]

    Amendment No. 215.
    Renewed Facility Operating License No. DPR-23. Amendment revises 
the technical specifications.
    Date of initial notice in Federal Register: August 29, 2006 (71 FR 
51225).
    The Commission's related evaluation of the amendment is contained 
in a safety evaluation dated June 15, 2007.
    No significant hazards consideration comments received: No.

Duke Power Company LLC, et al., Docket Nos. 50-413 and 50-414, Catawba 
Nuclear Station, Units 1 and 2, York County, South Carolina

    Date of application for amendments: June 5, 2006 as supplemented 
April 4, 2007.
    Brief description of amendments: The amendments revised the 
Technical Specification (TS) Section 3.8.1, ``AC Sources--Operating,'' 
surveillance requirement (SR) 3.8.1.13. The changes revised TS SR 
3.8.1.13 and its associated Bases to state that the SR only verifies 
that non-emergency diesel generator (DG) trips are bypassed. The 
licensee stated that this change is based upon and consistent with 
Industry Technical Specification Task Force (TSTF), Standard TS 
Traveler, TSTF-400-A, Revision 1, ``Clarify Surveillance Requirement on 
Bypass of DG Automatic Trips.''
    Date of issuance: June 25, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 30 days from the date of issuance.
    Amendment Nos.: 236, 232.
    Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
revised the licenses and the technical specifications.
    Date of initial notice in Federal Register: December 5, 2006 (71 FR 
70555).
    The supplement dated April 4, 2007, provided additional information 
that clarified the application, did not expand the scope of the 
application as originally noticed, and did not change the staff's 
original proposed no significant hazards consideration determination. 
The Commission's related evaluation of the amendments is contained in a 
Safety Evaluation dated June 25, 2007.
    No significant hazards consideration comments received: No.

Duke Power Company LLC, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
Station,Units 1 and 2, Mecklenburg County, North Carolina

    Date of application for amendments: June 5, 2006, as supplemented 
April 4, 2007.
    Brief description of amendments: The amendments revised TS 3.8.1, 
``AC Sources--Operating,'' surveillance requirement (SR) 3.8.1.13. The 
changes revise the SR 3.8.1.13 and its associated Bases to state that 
the SR only verifies that non-emergency diesel generator (DG) trips are 
bypassed. The licensee stated that this change is based upon and 
consistent with Industry Technical Specification Task Force (TSTF), 
Standard TS Traveler, TSTF-400-A, Revision 1, ``Clarify Surveillance 
Requirement on Bypass of DG Automatic Trips.''
    Date of issuance: June 25, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 30 days from the date of issuance.
    Amendment Nos.: 242, 223.
    Renewed Facility Operating License Nos. NPF-9 and NPF-17: 
Amendments revised the licenses and the technical specifications.
    Date of initial notice in Federal Register: December 5, 2006 (71 FR 
70555).
    The supplement dated April 4, 2007, provided additional information 
that clarified the application, did not expand the scope of the 
application as originally noticed, and did not change the staff's 
original proposed no significant hazards consideration determination. 
The Commission's related evaluation of the amendments is contained in a 
Safety Evaluation dated June 25, 2007.
    No significant hazards consideration comments received: No.

Entergy Nuclear Operations, Inc., Docket No. 50-333, James A. 
FitzPatrick Nuclear Power Plant, Oswego County, New York

    Date of application for amendment: February 15, 2007.
    Brief description of amendment: The proposed amendment would revise 
Technical Specification (TS) Section 3.10.1, ``Inservice Leak and 
Hydrostatic Testing Operation,'' to expand its scope to include 
provisions for temperature excursions greater than 212 [deg]F as a 
consequence of inservice leak or hydrostatic testing, and to allow 
performance of control rod scram time testing and other required 
testing when initiated in conjunction with the performance of an 
inservice leak or hydrostatic test, while considering operational 
conditions to be in Mode 4. The changes are consistent with NRC 
approved Revision 0 to Technical Specification Task Force (TSTF) 
Improved Standard Technical Specification Change Traveler, TSTF-484, 
``Use of TS 3.10.1 for Scram Time Testing Activities.''
    Date of issuance: June 21, 2007.
    Effective date: As of the date of issuance, and shall be 
implemented within 30 days.
    Amendment No.: 288.
    Facility Operating License No. DPR-59: The amendment revised the 
License and the Technical Specifications.
    Date of initial notice in Federal Register: April 10, 2007 (72 FR 
17947).

    The Commission's related evaluation of the amendment is contained 
in a Safety Evaluation dated June 21, 2007.
    No significant hazards consideration comments received: No.

Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
No. 2, Pope County, Arkansas

    Date of application for amendment: March 15, 2007.
    Brief description of amendment: The amendment revises the 
Surveillance Requirement (SR) 4.6.2.1.d to require verification that 
containment spray nozzles are unobstructed following maintenance that 
could result in nozzle blockage, in lieu of the current SR of 
performing the test every 5 years.
    Date of issuance: July 2, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 60 days from the date of issuance.
    Amendment No.: 272.
    Renewed Facility Operating License No. NPF-6: Amendment revised the 
Technical Specifications/license.
    Date of initial notice in Federal Register: April 24, 2007 (72 FR 
20381).
    The Commission's related evaluation of the amendment is contained 
in a Safety Evaluation dated July 2, 2007.
    No significant hazards consideration comments received: No.

Exelon Generation Company, LLC, Docket Nos. 50-237 and 50-249, Dresden 
Nuclear Power Station, Units 2 and 3, Grundy County, Illinois

    Date of application for amendment: June 2, 2006, as supplemented by 
letters dated August 18, 2006, October 5, 2006, and January 11, 2007.
    Brief description of amendment: The amendments revise technical 
specification to increase the allowable as-found main steam safety 
valve code safety function lift setpoint tolerance from 1 
percent to 3 percent to align Dresden Nuclear Power 
Station, Units 2 and 3, with the American Society of Mechanical 
Engineers Code for Operation and Maintenance of Nuclear Power Plants 
and reduce the number of non-safety significant Licensee Event Reports 
written due to TS violations caused by setpoint drifting.
    Date of issuance: June 21, 2007.

[[Page 39087]]

    Effective date: As of the date of issuance and shall be implemented 
within 60 days.
    Amendment Nos.: 223 and 215.
    Renewed Facility Operating License Nos. DPR-19 and DPR-25: The 
amendments revised the Technical Specifications and License.
    Date of initial notice in Federal Register: August 15, 2006 (71 FR 
46929).
    The August 18, 2006, October 5, 2006, and January 11, 2007, 
supplements contained clarifying information and did not change the NRC 
staff's initial proposed finding of no significant hazards 
consideration.
    The Commission's related evaluation of the amendments is contained 
in a Safety Evaluation dated June 21, 2007.
    No significant hazards consideration comments received: No.

Exelon Generation Company, LLC, Docket Nos. 50-373 and 50-374, LaSalle 
County Station, Units 1 and 2, LaSalle County, Illinois

    Date of application for amendments: March 16, 2006, as supplemented 
by letter dated April 6, 2007.
    Brief description of amendments: The amendments revise allowable 
values for four reactor core isolation cooling leak detection functions 
in Technical Specification Table 3.3.6.1-1, ``Primary Containment 
Isolation Instrumentation.''
    Date of issuance: June 29, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 60 days.
    Amendment Nos.: 182/169.
    Facility Operating License Nos. NPF-11 and NPF-18: The amendments 
revised the Technical Specifications and License.
    Date of initial notice in Federal Register: August 15, 2006 (71 FR 
46929).
    The April 6, 2007 supplement, contained clarifying information and 
did not change the NRC staff's initial proposed finding of no 
significant hazards consideration.
    The Commission's related evaluation of the amendments is contained 
in a Safety Evaluation dated June 29, 2007.
    No significant hazards consideration comments received: No.

FirstEnergy Nuclear Operating Company, et al., Docket No. 50-440, Perry 
Nuclear Power Plant, Unit No. 1, Lake County, Ohio

    Date of application for amendment: December 29, 2006.
    Brief description of amendment: The amendment modifies the 
technical specifications requirements for scram discharge volume vent 
and drain valves.
    Date of issuance: June 22, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 90 days.
    Amendment No.: 145.
    Facility Operating License No. NPF-58: This amendment revised the 
Technical Specifications and License.
    Date of initial notice in Federal Register: March 13, 2007 (72 FR 
11388).
    The Commission's related evaluation of the amendment is contained 
in a Safety Evaluation dated June 22, 2007.
    No significant hazards consideration comments received: No.

FPL Energy Duane Arnold, LLC, Docket No. 50-331, Duane Arnold Energy 
Center, Linn County, Iowa

    Date of application for amendment: July 17, 2006, as supplemented 
by letter dated March 20, 2007.
    Brief description of amendment: The amendment revises the Technical 
Specification (TS) Limiting Condition for Operation (LCO) 3.6.3.1 to 
eliminate the requirement for the Containment Atmospheric Dilution 
system, allowing its removal from the Duane Arnold Energy Center. In a 
letter dated June 1, 2007, the licensee withdrew its request to change 
LCO 3.6.3.2, ``Primary Containment oxygen Concentration,'' to lengthen 
the duration of time for the primary containment to be de-inerted.
    Date of issuance: June 28, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 30 days.
    Amendment No.: 265.
    Facility Operating License No. DPR-49: The amendment revises the 
Technical Specification.
    Date of initial notice in Federal Register: November 21, 2006 (71 
FR 67395).
    The supplemental information provided additional information that 
clarified the application, did not expand the scope of the application 
as originally noticed, and did not change the Nuclear Regulatory 
Commission's staff's original proposed no significant hazards 
consideration determination.
    The Commission's related evaluation of the amendment is contained 
in a Safety Evaluation dated June 28, 2007.
    No significant hazards consideration comments received: No.

Nuclear Management Company, LLC, Docket Nos. 50-282 and 50-306, Prairie 
Island Nuclear Generating Plant, Units 1 and 2, Goodhue County, 
Minnesota

    Date of application for amendments: July 6, 2006, as supplemented 
by letters dated September 15 and December 26, 2006.
    Brief description of amendments: The amendments incorporate new 
Large-Break Loss-of-Coolant Accident (LBLOCA) analyses using the 
realistic LBLOCA methodology in the Nuclear Regulatory Commission 
approved WCAP-16009-P-A, ``Realistic Large Break LOCA Evaluation 
Methodology using Automated Statistical Treatment of Uncertainty Method 
(ASTRUM)'' and revise TS 5.6.5.b to include reference to WCAP-16009-P-
A.
    Date of issuance: June 28, 2007.
    Effective date: As of the date of issuance and shall be implemented 
with the next fuel cycle (Unit 1 Cycle 25) commencing following the 
Winter 2008 refueling for Unit 1, and implemented within 90 days for 
Unit 2.
    Amendment Nos.: 179 and 169.
    Facility Operating License Nos. DPR-42 and DPR-60: Amendments 
revised the Technical Specifications.
    Date of initial notice in Federal Register: September 12, 2006 (71 
FR 53718).
    The supplemental letters contained clarifying information and did 
not change the initial no significant hazards consideration 
determination, and did not expand the scope of the original Federal 
Register notice.
    The Commission's related evaluation of the amendments is contained 
in a Safety Evaluation dated June 28, 2007.
    No significant hazards consideration comments received: No.

Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
California

    Date of application for amendments: December 29, 2006.
    Brief description of amendments: The amendments revised Technical 
Specification (TS) Section 5.5.8, ``Inservice Testing Program,'' in 
order to update references to the American Society of Mechanical 
Engineers Boiler and Pressure Vessel Code. Specifically, the change 
adopted the administrative, editorial, and clarification TS changes 
contained in TS Task Force (TSTF)-479, Revision 0, ``Changes to Reflect 
Revision of 10 CFR [Title 10 of the Code of Federal Regulations] 
50.55a,'' and TSTF-497, Revision 0, ``Limit Inservice Testing Program 
SR [Surveillance Requirement] 3.0.2 Application to Frequencies of 2 
years or less.''
    Date of issuance: June 25, 2007.
    Effective date: As of its date of issuance and shall be implemented 
within 90 days from the date of issuance.
    Amendment Nos.: Unit 1-196; Unit 2-197

[[Page 39088]]

    Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
revised the Facility Operating Licenses and Technical Specifications.
    Date of initial notice in Federal Register: February 13, 2007 (72 
FR 6784).
    The Commission's related evaluation of the amendments is contained 
in a Safety Evaluation dated June 25, 2007.
    No significant hazards consideration comments received: No.
    Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
revised the Facility Operating Licenses and Technical Specifications.
    Date of initial notice in Federal Register: February 13, 2007 (72 
FR 6784).
    The Commission's related evaluation of the amendments is contained 
in a Safety Evaluation dated June 25, 2007.
    No significant hazards consideration comments received: No.

Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
California

    Date of application for amendments: December 29, 2006.
    Brief description of amendments: The amendments revise TS 5.5.16, 
``Containment Leakage Rate Testing Program,'' to comply with the 
requirements of 10 CFR 50.55a(g)(4) for components classified as Code 
Class CC.
    Date of issuance: June 26, 2007.
    Effective date: As of its date of issuance and shall be implemented 
within 90 days from the date of issuance.
    Amendment Nos.: Unit 1-197; Unit 2-198.
    Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
revised the Facility Operating Licenses and Technical Specifications.
    Date of initial notice in Federal Register: February 13, 2007 (72 
FR 6785).
    The Commission's related evaluation of the amendments is contained 
in a Safety Evaluation dated June 26, 2007.
    No significant hazards consideration comments received: No.

Southern Nuclear Operating Company, Inc., Georgia Power Company, 
Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, 
City of Dalton, Georgia, Docket Nos. 50-321 and 50-366, Edwin I. Hatch 
Nuclear Plant, Units 1 and 2, Appling County, Georgia

    Date of application for amendments: January 30, 2007, as 
supplemented April 11, 2007.
    Brief description of amendments: The amendments revised staff 
position duties and titles in Sections 2 and 5 of the Technical 
Specifications.
    Date of issuance: June 7, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 30 days from the date of issuance.
    Amendment Nos.: 252, 196.
    Renewed Facility Operating License Nos. DPR-57 and NPF-5: 
Amendments revised the licenses and the technical specifications.
    Date of initial notice in Federal Register: February 13, 2007 (72 
FR 6790).
    The supplement dated April 11, 2007, provided additional 
information that clarified the application, did not expand the scope of 
the application as originally noticed, and did not change the staff's 
original proposed no significant hazards consideration determination. 
The Commission's related evaluation of the amendments is contained in a 
Safety Evaluation dated June 7, 2007.
    No significant hazards consideration comments received: No.

Southern Nuclear Operating Company, Inc., Docket Nos. 50-424 and 50-
425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County, 
Georgia

    Date of application for amendments: January 30, 2007, as 
supplemented April 11, 2007.
    Brief description of amendments: The amendments revised staff 
position duties and titles in Sections 2 and 5 of the Technical 
Specifications.
    Date of issuance: June 12, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 30 days from the date of issuance.
    Amendment Nos.: 148, 128.
    Renewed Facility Operating License Nos. NPF-68 and NPF-81: 
Amendments revised the licenses and the technical specifications.
    Date of initial notice in Federal Register: February 13, 2007 (72 
FR 6791).
    The supplement dated April 11, 2007, provided additional 
information that clarified the application, did not expand the scope of 
the application as originally noticed, and did not change the staff's 
original proposed no significant hazards consideration determination. 
The Commission's related evaluation of the amendments is contained in a 
Safety Evaluation dated June 12, 2007.
    No significant hazards consideration comments received: No.

STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
Texas Project, Units 1 and 2, Matagorda County, Texas

    Date of amendment request: March 30, 2006, as supplemented by 
letters dated October 2, 2006, and February 26, 2007.
    Brief description of amendments: The amendments revise TS 3.3.3.6, 
``Accident Monitoring Instrumentation,'' with respect to the required 
action for inoperable wide range reactor coolant temperature, wide 
range steam generator water level, and auxiliary feedwater flow 
instruments.
    Date of issuance: June 13, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 60 days of issuance.
    Amendment Nos.: Unit 1-177; Unit 2-164.
    Facility Operating License Nos. NPF-76 and NPF-80: The amendments 
revised the Facility Operating Licenses and Technical Specifications.
    Date of initial notice in Federal Register: June 6, 2006 (71 FR 
32608). The supplemental letters dated October 2, 2006, and February 
26, 2007, provided additional information that clarified the 
application, did not expand the scope of the application as originally 
noticed, and did not change the staff's original proposed no 
significant hazards consideration determination as published in the 
Federal Register.
    The Commission's related evaluation of the amendments is contained 
in a Safety Evaluation dated June 13, 2007.
    No significant hazards consideration comments received: No.

STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
Texas Project, Units 1 and 2, Matagorda County, Texas

    Date of amendment request: April 4, 2006.
    Brief description of amendments: The amendment request changed the 
name of one licensee, Texas Genco, LP (Texas Genco), to NRG South Texas 
LP. The name change results from the purchase of Texas Genco's parent 
company by NRG Energy, Inc. as approved by the NRC in January 2006.
    Date of issuance: June 29, 2007.
    Effective date: As of the date of issuance and shall be implemented 
within 30 days of issuance.
    Amendment Nos.: Unit 1-178; Unit 2-165.
    Facility Operating License Nos. NPF-76 and NPF-80: The amendments 
revised the Facility Operating Licenses.
    Date of initial notice in Federal Register: May 9, 2007 (72 FR 
26428).

[[Page 39089]]

    The Commission's related evaluation of the amendments is contained 
in a Safety Evaluation dated June 29, 2007.
    No significant hazards consideration comments received: No.

    Dated at Rockville, Maryland, this sixth day of July 2007.

    For the Nuclear Regulatory Commission.
Catherine Haney,
Director, Division of Operating Reactor Licensing, Office of Nuclear 
Reactor Regulation.
 [FR Doc. E7-13537 Filed 7-16-07; 8:45 am]
BILLING CODE 7590-01-P
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