Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 20375-20389 [E7-7534]
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Federal Register / Vol. 72, No. 78 / Tuesday April 24, 2007 / Notices
301–415–1728). Marriott Bethesda
North Hotel, 5701 Marinelli Road,
Rockville, MD 20852.
For More Information Contact: Vicky
D’Onofrio, (202) 314–6410.
Vicky D’Onofrio,
Federal Register Liaison Office.
[FR Doc. 07–2050 Filed 4–20–07; 2:13 pm]
BILLING CODE 7533–01–M
NUCLEAR REGULATORY
COMMISSION
Notice of Sunshine Act Meetings
AGENCY HOLDING THE MEETINGS: Nuclear
Regulatory Commission.
DATES: Weeks of April 23, 30, May 7, 14,
21, 28, 2007.
PLACE: Commissioners’ Conference
Room, 11555 Rockville Pike, Rockville,
Maryland.
STATUS: Public and Closed.
MATTERS TO BE CONSIDERED:
Week of April 23, 2007
Monday, April 23, 2007
2:30 p.m.
Discussion of Security Issues (ClosedEx. 1).
Week of April 30, 2007—Tentative
There are no meetings scheduled for
the Week of April 30, 2007.
Week of May 7, 2007—Tentative
Monday, May 7, 2007
1:25 p.m.
Affirmation Session (Public Meeting)
(Tentative).
a. Consumers Energy Co. (Big Rock
Point ISFSI); License Transfer
Application (Tentative).
This meeting will be webcast live at
the Web address—https://www.nrc.gov.
1:30 p.m.
Briefing on Office of Federal and State
Materials and Environmental
Management Programs (FSME)
Programs, Performance, and Plans
(Public Meeting) (Contact: George
Deegan, 301–415–7834).
This meeting will be webcast live at
the Web address—https://www.nrc.gov.
Week of May 14, 2007—Tentative
There are no meetings scheduled for
the Week of May 14, 2007.
Week of May 21, 2007—Tentative
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There are no meetings scheduled for
the Week of May 21, 2007.
Week of May 28, 2007—Tentative
Tuesday, May 29, 2007
1:30 p.m.
NRC All Hands Meeting (Public
Meeting) (Contact: Rickie Seltzer,
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Wednesday, May 30, 2007
9:30 a.m.
Briefing on Results of the Agency
Action Review Meeting (AARM)—
Materials (Public Meeting).
This meeting will be webcast live at
the Web address—https://www.nrc.gov.
10:15 a.m.
Discussion of Security Issues
(Closed—Ex.1).
Thursday, May 31, 2007
9 a.m.
Briefing on Results of the Agency
Action Review Meeting (AARM)—
Reactors (Public Meeting).
This meeting will be webcast live at
the Web address—https://www.nrc.gov.
* The schedule for Commission
meetings is subject to change on short
notice. To verify the status of meetings
call (recording)—(301) 415–1292.
Contact person for more information:
Michelle Schroll, (301) 415–1662.
Additional Information
By a vote of 5–0 on April 19, 2007,
the Commission determined pursuant to
U.S.C. 552b(e) and § 9.107(a) of the
Commission’s rules that ‘‘Discussion of
Security Issues (Closed-Ex. 1)’’ be held
April 23, 2007, and on less than one
week’s notice to the public.
The NRC Commission Meeting
Schedule can be found on the Internet
at: https://www.nrc.gov/about-nrc/policymaking/schedule.html.
The NRC provides reasonable
accommodation to individuals with
disabilities where appropriate. If you
need a reasonable accommodation to
participate in these public meetings, or
need this meeting notice or the
transcript or other information from the
public meetings in another format (e.g.
braille, large print), please notify the
NRC’s Disability Program Coordinator,
Deborah Chan, at 301–415–7041, TDD:
301–415–2100, or by e-mail at
DLC@nrc.gov. Determinations on
requests for reasonable accommodation
will be made on a case-by-case basis.
This notice is distributed by mail to
several hundred subscribers; if you no
longer wish to receive it, or would like
to be added to the distribution, please
contact the Office of the Secretary,
Washington, DC 20555 (301–415–1969).
In addition, distribution of this meeting
notice over the Internet system is
available. If you are interested in
receiving this Commission meeting
schedule electronically, please send an
electronic message to dkw@nrc.gov.
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20375
Dated: April 19, 2007.
R. Michelle Schroll,
Office of the Secretary.
[FR Doc. 07–2046 Filed 4–20–07; 11:09 am]
BILLING CODE 7590–01–P
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from March 30,
2007 to April 12, 2007. The last
biweekly notice was published on April
10, 2007 (72 FR 17944).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
Involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
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determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rulemaking,
Directives and Editing Branch, Division
of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
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for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
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which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) e-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
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petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
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AmerGen Energy Company, LLC, Docket
No. 50–289, Three Mile Island Nuclear
Station, Unit 1 (TMI–1), Dauphin
County, Pennsylvania
Date of amendment request: March
22, 2007.
Description of amendment request:
The proposed amendment would revise
the Technical Specifications to
incorporate a revised limit for the
variable low reactor coolant system
pressure-temperature core protection
safety limit. The revised limit is
associated with the introduction of
AREVA NP’s Mark-B-HTP fuel design,
which will require more restrictive
Safety Limits and more restrictive
Limiting Safety System Settings for the
Reactor Protection System. The
proposed limits are developed in
accordance with the method described
in the Nuclear Regulatory Commission
(NRC)-approved Topical Report BAW–
10179P–A, ‘‘Safety Criteria and
Methodology for Acceptable Cycle
Reload Analyses.’’ The revised limits
will maintain the same magnitude of
departure from nucleate boiling (DNB)
protection.
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Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed Technical Specification (TS)
limits and reactor protection system (RPS)
trip setpoints are developed in accordance
with the methods and assumptions described
in NRC-approved AREVA NP Topical
Reports BAW–10179 P–A, ‘‘Safety Criteria
and Methodology for Acceptable Cycle
Reload Analyses’’ and BAW–10187 P–A,
‘‘Statistical Core Design for B&W-Designed
177 FA Plants.’’ The core thermal-hydraulic
code (LYNXT) and CHF correlation (BHTP)
have been approved for use with these
methods and the Mark-B-HTP fuel type. The
proposed change preserves the design DNB
Ratio safety criterion that there shall be at
least a 95% [percent] probability at a 95%
confidence level that the hot fuel rod in the
core does not experience a departure from
nucleate boiling during normal operation or
events of moderate frequency. The
corresponding core-wide protection on a pinby-pin basis is greater than 99.9%. The
margin retained for penalties such as
transition core effects, by imposing a
Thermal Design Limit in all DNB analyses
supporting the proposed change, has been
shown to be sufficient to offset the mixed
core conditions at TMI Unit 1, where the
Mark-B-HTP fuel design will be co-resident
with earlier Mark-B fuel designs. The
setpoint calculation methodology utilized,
and the surveillance requirements
established, are in accordance with approved
industry standards and NRC criteria.
The proposed setpoint change does not
involve a significant increase in the
consequences of an accident previously
evaluated because the proposed change does
not alter any assumptions previously made in
the radiological consequence evaluations, or
affect mitigation of the radiological
consequences of an accident previously
evaluated.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed TS limit and reactor
protection system (RPS) trip setpoint provide
a core protection safety limit and variable
low pressure trip setpoint developed in
accordance with NRC-approved methods and
assumptions. No new accident scenarios,
failure mechanisms or single failures are
introduced as a result of the proposed
change. All systems, structures, and
components previously required for the
mitigation of an event remain capable of
fulfilling their intended design function.
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Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed RPS trip setpoint ensures
core protection safety limits will be
preserved during power operation. The
proposed safety limit and setpoint are
developed in accordance with NRC-approved
methods and assumptions. The margin
retained for penalties such as transition core
effects, by imposing a Thermal Design Limit
in all DNB analyses supporting the proposed
change, has been shown to be sufficient to
offset the mixed core conditions at TMI Unit
1. The setpoint calculation methodology
utilized, and the surveillance requirements
established, are in accordance with approved
industry standards and NRC criteria.
Therefore, the proposed changes do not
involve a significant reduction in any margin
of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. Brad
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Harold K.
Chernoff.
Calvert Cliffs Nuclear Power Plant, Inc.,
Docket No. 50–317, Calvert Cliffs
Nuclear Power Plant, Unit No. 1, Calvert
County, Maryland
Date of amendment request: February
27, 2007.
Description of amendment request:
The proposed license amendment
would revise Technical Specification
4.2.1, Fuel Assemblies, to add a
temporary exemption to allow the
insertion of up to four lead fuel
assemblies, which contain non-Zircaloy
based cladding, into the Unit 1 core for
one cycle of operation. These lead fuel
assemblies are currently installed in the
Unit 2 core under a previous exemption
and are scheduled to be discharged
during the 2007 refueling outage.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below. The licensee has determined that
the proposed change:
1. Would not involve a significant increase
in the probability or consequences of an
accident previously evaluated.
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Calvert Cliffs Technical Specification 4.2.1,
Fuel Assemblies, states that fuel rods are clad
with either Zircaloy or ZIRLOTM. Calvert
Cliffs Nuclear Power Plant, Inc. proposes to
re-insert up to four fuel assemblies into
Calvert Cliffs Unit 1 that have some fuel rods
clad in zirconium alloys that do not meet the
definition of Zircaloy or ZIRLOTM. A
temporary exemption to the regulations has
been requested to allow these fuel assemblies
to be re-inserted into Unit 1. The proposed
change to the Calvert Cliffs Technical
Specifications will allow the use of cladding
materials that are not Zircaloy or ZIRLOTM
for one fuel cycle once the temporary
exemption is approved. The proposed change
to the Technical Specification is effective
only as long as the temporary exemption is
effective. The addition of what will be an
approved temporary exemption for Unit 1 to
Technical Specification 4.2.1 does not
change the probability or consequences of an
accident previously evaluated.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Would not create the possibility of a new
or different [kind] of accident from any
accident previously evaluated.
The proposed change does not add any
new equipment, modify any interfaces with
existing equipment, change the equipment’s
function, or change the method of operating
the equipment. The proposed change does
not affect normal plant operations or
configuration. Since the proposed change
does not change the design, configuration, or
operation, it could not become an accident
initiator.
Therefore, the proposed change does not
create the possibility of a new or different
[kind] of accident from any accident
previously evaluated.
3. Would not involve a significant
reduction in [a] margin of safety.
The proposed change will add an approved
temporary exemption to the Calvert Cliffs
Technical Specifications allowing the
installation of up to four lead fuel assemblies.
The assemblies use advanced cladding
materials that are not specifically permitted
by existing regulations or Calvert Cliffs’
Technical Specifications. A temporary
exemption to allow the installation of these
assemblies has been requested. The addition
of an approved temporary exemption to
Technical Specification 4.2.1 is an
administrative change to allow the
installation of the lead fuel assemblies under
the provisions of the temporary exemption.
The license amendment is effective only as
long as the exemption is effective. This
amendment does not change the margin of
safety since it only adds a reference to an
approved, temporary exemption to the
Technical Specifications.
Therefore, the proposed change does not
involve a significant reduction in [a] margin
of safety.
The Nuclear Regulatory Commission
(NRC) staff has reviewed the licensee’s
analysis and, based on this review, it
appears that the three standards of 10
CFR 50.92(c) are satisfied. Therefore, the
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NRC staff proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Carey Fleming,
Esquire, Senior Counsel—Nuclear
Generation, Constellation Generation
Group, LLC, 750 East Pratt Street, 17th
floor, Baltimore, MD 21202.
NRC Acting Branch Chief: John P.
Boska.
Calvert Cliffs Nuclear Power Plant, Inc.,
Docket Nos. 50–317 and 50–318, Calvert
Cliffs Nuclear Power Plant, Unit Nos. 1
and 2, Calvert County, Maryland
Date of amendment request: February
27, 2007.
Description of amendment request:
The proposed license amendment
would revise Technical Specification
5.6.5, Core Operating Limits Report
(COLR), to add the supporting topical
report (WCAP–15604–NP, Revision 2–
A, ‘‘Limited Scope High Burnup Lead
Test Assemblies,’’ September 2003) to
the list of references. The topical report
provides guidance for operation with a
limited number of lead fuel assemblies
to be irradiated to a higher burnup limit
than currently allowed for Calvert Cliffs
fuel assemblies.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below. The licensee has determined that
the proposed change:
1. Would not involve a significant increase
in the probability or consequences of an
accident previously evaluated.
The proposed change would modify the
Calvert Cliffs Units 1 and 2 Technical
Specification 5.6.5.b, Core Operating Limits
Report by adding an approved topical report
to the existing list of topical reports. The
topical report provides the technical basis
that supports irradiating a limited number of
lead fuel assemblies to a higher burnup limit
than currently approved for Calvert Cliffs.
The proposed change is administrative in
nature and has no impact on any plant
configurations or on system performance that
is relied upon to mitigate the consequences
of an accident.
In the safety evaluation report approving
the requested topical report (WCAP–15604–
NP, Revision 2–A), the Nuclear Regulatory
Commission concluded that it is acceptable
for an individual power licensee to irradiate
a limited number of lead fuel assemblies to
a maximum burnup to 75 GWD/MTU
[gigawatt days per metric ton of uranium]
provided that certain conditions are met.
Calvert Cliffs meets those required
conditions. Because those required
conditions are met and only a limited
number of fuel assemblies are included in
this change, the probability or consequences
of an accident previously evaluated are not
significantly increased.
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Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Would not create the possibility of a new
or different [kind] of accident from any
accident previously evaluated.
The proposed change does not add any
new equipment, modify any interfaces with
existing equipment, change the equipment’s
function, or change the method of operating
the equipment. The proposed change does
not affect normal plant operations or
configuration. Since the proposed change
does not change the plant design, operation,
or configuration, it could not become an
accident initiator.
Therefore, the proposed change does not
create the possibility of a new or different
[kind] of accident from any accident
previously evaluated.
3. Would not involve a significant
reduction in a margin of safety.
The proposed change will add a reference
to an approved topical report to allow a
limited number of lead fuel assemblies to be
irradiated to a higher burnup level than is
currently allowed at Calvert Cliffs. The
higher burnup limit has been evaluated and
approved in the topical report being
referenced. Calvert Cliffs conforms to the
requirements of the topical report. The
addition of an approved reference to the
Technical Specifications is administrative in
nature and has no impact on the margin of
safety for any plant configuration or on
system performance that is relied upon to
mitigate the consequences on an accident.
Therefore, the proposed change does not
involve a significant reduction in [a] margin
of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Carey Fleming,
Esquire, Senior Counsel—Nuclear
Generation, Constellation Generation
Group, LLC, 750 East Pratt Street, 17th
floor, Baltimore, MD 21202.
NRC Acting Branch Chief: John P.
Boska.
Carolina Power & Light Company,
Docket No. 50–261, H. B. Robinson
Steam Electric Plant, Unit No. 2,
Darlington County, South Carolina
Date of amendment request: February
2, 2007.
Description of amendment request:
The proposed amendment deletes
requirements from the Technical
Specifications (TS) to maintain
hydrogen recombiners and hydrogen
monitors. Licensees were generally
required to implement upgrades as
described in NUREG–0737,
‘‘Clarification of Three Mile Island
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(TMI) Action Plan Requirements,’’ and
Regulatory Guide (RG) 1.97,
‘‘Instrumentation for Light-WaterCooled Nuclear Power Plants to Assess
Plant and Environs Conditions During
and Following an Accident.’’
Implementation of these upgrades was
an outcome of the lessons learned from
the accident that occurred at TMI, Unit
2. Requirements related to combustible
gas control were imposed by Order for
many facilities and were added to or
included in the TS for nuclear power
reactors currently licensed to operate.
The revised Title 10 of the Code of
Federal Regulations (10 CFR) 50.44,
‘‘Standards for Combustible Gas Control
System in Light-Water-Cooled Power
Reactors,’’ eliminated the requirements
for hydrogen recombiners and relaxed
safety classifications and licensee
commitments to certain design and
qualification criteria for hydrogen and
oxygen monitors.
The NRC staff published a notice of
opportunity for comment in the Federal
Register on August 2, 2002 (67 FR
50374), on possible amendments to
eliminate requirements regarding
containment hydrogen recombiners and
the removal of requirements from TS for
containment hydrogen and oxygen
monitors, including a model safety
evaluation and model No Significant
Hazards Consideration (NSHC)
Determination, in accordance with the
Consolidated Line Item Improvement
Process. The NRC staff subsequently
issued a notice of availability of the
models for referencing in license
amendment applications in the Federal
Register on September 25, 2003 (68 FR
55416). The licensee affirmed the
applicability of the model NSHC
determination in its application dated
February 2, 2007.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
Criterion 1: The Proposed Change Does Not
Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated.
The revised 10 CFR 50.44 no longer defines
a design-basis loss-of-coolant accident
(LOCA) hydrogen release, and eliminates
requirements for hydrogen control systems to
mitigate such a release. The installation of
hydrogen recombiners and/or vent and purge
systems required by 10 CFR 50.44(b)(3) was
intended to address the limited quantity and
rate of hydrogen generation that was
postulated from a design-basis LOCA. The
Commission has found that this hydrogen
release is not risk-significant because the
design-basis LOCA hydrogen release does not
contribute to the conditional probability of a
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large release up to approximately 24 hours
after the onset of core damage. In addition,
these systems were ineffective at mitigating
hydrogen releases from risk-significant
accident sequences that could threaten
containment integrity.
With the elimination of the design-basis
LOCA hydrogen release, hydrogen monitors
are no longer required to mitigate designbasis accidents and, therefore, the hydrogen
monitors do not meet the definition of a
safety-related component as defined in 10
CFR 50.2. RG 1.97 Category 1, is intended for
key variables that most directly indicate the
accomplishment of a safety function for
design-basis accident events. The hydrogen
monitors no longer meet the definition of
Category 1 in RG 1.97. As part of the
rulemaking to revise 10 CFR 50.44 the
Commission found that Category 3, as
defined in RG 1.97, is an appropriate
categorization for the hydrogen monitors
because the monitors are required to
diagnose the course of beyond design-basis
accidents.
The regulatory requirements for the
hydrogen monitors can be relaxed without
degrading the plant emergency response. The
emergency response, in this sense, refers to
the methodologies used in ascertaining the
condition of the reactor core, mitigating the
consequences of an accident, assessing and
projecting offsite releases of radioactivity,
and establishing protective action
recommendations to be communicated to
offsite authorities. Classification of the
hydrogen monitors as Category 3 and
removal of the hydrogen monitors from TS
will not prevent an accident management
strategy through the use of the severe
accident management guidelines, the
emergency plan, the emergency operating
procedures, and site survey monitoring that
support modification of emergency plan
protective action recommendations.
Therefore, the elimination of the hydrogen
recombiner requirements and relaxation of
the hydrogen monitor requirements,
including removal of these requirements
from TS, does not involve a significant
increase in the probability or the
consequences of any accident previously
evaluated.
Criteria 2: The Proposed Change Does Not
Create the Possibility of a New or Different
Kind of Accident From Any Previously
Evaluated.
The elimination of the hydrogen
recombiner requirements and relaxation of
the hydrogen monitor requirements,
including removal of these requirements
from TS, will not result in any failure mode
not previously analyzed. The hydrogen
recombiner and hydrogen monitor equipment
was intended to mitigate a design-basis
hydrogen release. The hydrogen recombiner
and hydrogen monitor equipment are not
considered accident precursors, nor does
their existence or elimination have any
adverse impact on the pre-accident state of
the reactor core or post accident confinement
of radionuclides within the containment
building.
Therefore, this change does not create the
possibility of a new or different kind of
accident from any previously evaluated.
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Criterion 3: The Proposed Change Does Not
Involve a Significant Reduction in the Margin
of Safety.
The elimination of the hydrogen
recombiner requirements and relaxation of
the hydrogen monitor requirements,
including removal of these requirements
from TS, in light of existing plant equipment,
instrumentation, procedures, and programs
that provide effective mitigation of and
recovery from reactor accidents, results in a
neutral impact to the margin of safety.
The installation of hydrogen recombiners
and/or vent and purge systems required by
10 CFR 50.44(b)(3) was intended to address
the limited quantity and rate of hydrogen
generation that was postulated from a designbasis LOCA. The Commission has found that
this hydrogen release is not risk-significant
because the design-basis LOCA hydrogen
release does not contribute to the conditional
probability of a large release up to
approximately 24 hours after the onset of
core damage.
Category 3 hydrogen monitors are adequate
to provide rapid assessment of current
reactor core conditions and the direction of
degradation while effectively responding to
the event in order to mitigate the
consequences of the accident. The intent of
the requirements established as a result of the
TMI, Unit 2 accident can be adequately met
without reliance on safety-related hydrogen
monitors.
Therefore, this change does not involve a
significant reduction in the margin of safety.
Removal of hydrogen monitoring from TS
will not result in a significant reduction in
their functionality, reliability, and
availability.
The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Branch Chief: Thomas H. Boyce.
Detroit Edison Company, Docket No.
50–341, Fermi 2, Monroe County,
Michigan
Date of amendment request: March
19, 2007.
Description of amendment request:
The proposed amendment would revise
the Technical Specifications (TS) 3.8.1
entitled ‘‘AC Sources-Operating’’ to
change the minimum Emergency Diesel
Generator (EDG) output voltage
acceptance criterion from 3740 to 3873
volts. Specifically, the proposed change
would revise the Surveillance
Requirements (SRs) 3.8.1.2, 3.8.1.7,
3.8.1.10, 3.8.1.11, 3.8.1.14, and 3.8.1.17.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
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1. The proposed change does not involve
a significant increase in the probability or
consequences of any accident previously
evaluated.
The increase in the minimum EDG output
voltage acceptance criterion value in TS 3.8.1
surveillance requirements does not adversely
affect any of the parameters in the accident
analyses. The change increases the minimum
allowed EDG output voltage acceptance
criterion to ensure that sufficient voltage is
available to operate the required Emergency
Safety Feature (ESF) equipment under
accident conditions. The increase in the
minimum allowed EDG output voltage in the
TS surveillance requirements ensures that
adequate voltage is available to support the
assumptions made in the Design Bases
Accident (DBA) analyses. DBA analyses
assume that onsite standby emergency power
will provide an adequate power source to
operate safe shutdown equipment and to
mitigate consequences of design bases
accidents. This conservative change of the
acceptance criterion enhances the testing
requirements of the onsite emergency diesel
generators and ensures the reliability of this
power source. Changing the acceptance
criterion does not affect the probability of
evaluated accidents and it provides better
assurance of EDG reliability in mitigating
consequences of accidents. Therefore, the
proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. The proposed change does not create the
possibility of a new or different kind of
accident from an accident previously
evaluated.
The change in the value of the minimum
EDG output voltage acceptance criterion
supports the assumptions in the accident
analyses that sufficient voltage will be
available to operate ESF equipment on the
Class 1E buses when these buses are powered
from the onsite emergency diesel generators.
The maximum EDG output voltage of 4580
volts is not affected by this change. The
change in the minimum EDG output voltage
from 3740 to 3873 volts ensures the
reliability of the onsite emergency power
source. Therefore, the proposed change will
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. The proposed change does not involve
a significant reduction in a margin of safety.
This proposed license amendment involves
a change in the minimum EDG output voltage
acceptance criterion in TS 3.8.1 surveillance
requirements. The surveillance frequency
and the different test requirements are
unchanged. The change provides a better
assurance that the onsite power source is able
to satisfy the design requirements assumed in
the accident analyses to safely shutdown the
reactor and mitigate the consequences of
design bases accidents. Therefore, the
proposed change will not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
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Jkt 211001
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David G.
Pettinari, Legal Department, 688 WCB,
Detroit Edison Company, 2000 2nd
Avenue, Detroit, Michigan 48226–1279.
NRC Branch Chief: L. Raghavan.
Dominion Nuclear Connecticut, Inc.,
Docket No. 50–336, Millstone Power
Station, Unit No. 2, New London
County, Connecticut
Date of amendment request:
November 8, 2006.
Description of amendment request:
The proposed amendment would
modify the Technical Specification (TS)
Action and Surveillance Requirements
(SRs) for instrumentation identified in
TSs 3.3.1 and 3.3.2. In particular, the
proposed amendment adds actions to
address the inoperability of one or more
automatic bypass removal channels;
revises the terminology used in the
notation of TS Tables 2.2–1 and 3.3–1
relative to the implementation and
automatic removal of certain Reactor
Protection System (RPS) trip bypasses;
revises the frequency for performing
surveillance of the automatic bypass
removal function logic; and incorporates
two administrative changes.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
Criterion 1: Does the proposed amendment
involve a significant increase in the
probability or consequences of an accident
previously evaluated?
Response: No.
The proposed changes to Technical
Specifications 2.2.1, 3.3.1 and 3.3.2 do not
adversely impact structure, system, or
component design or operation in a manner
that would result in a change in the
frequency of occurrence of accident
initiation. The proposed technical
specification changes do not involve accident
initiators, do not change the configuration or
method of operation of any plant equipment
that is used to mitigate the consequences of
an accident, and do not alter any conditions
assumed in the plant accident analyses. The
proposed amendment does not change the
function or the manner of operation of the
RPS or ESFAS [engineered safety features
actuation system] trip bypass features.
Adding actions to be taken for an inoperable
automatic bypass removal function places
additional restriction on plant operation in
this condition and does not alter the setpoint
or the logic of the operating bypasses and
automatic bypass removals. Clarifying the
frequency of the SR associated with testing
the automatic bypass removal function does
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not alter the setpoint or the manner of
operation of the operating bypasses and
automatic bypass removals. More accurately
reflecting the input process variable of the
operating bypasses and automatic bypass
removals of the affected reactor trips does not
alter the setpoint nor the manner of operation
of the operating bypasses and automatic
bypass removals. With respect to the
incorporation of the administrative changes,
the proposed changes are spelling corrections
and do not alter any of the requirements of
the affected TS. Therefore, this change does
not impact the consequences of any accident.
Based on this discussion, the proposed
amendment does not increase the probability
or consequence of an accident previously
evaluated.
Criterion 2: Does the proposed amendment
create the possibility of a new or different
kind of accident from any accident
previously evaluated?
Response: No.
No new or different accidents result from
clarifying actions for an inoperable automatic
bypass removal function, clarifying
surveillance requirements for the automatic
bypass removal function, and more
accurately reflecting the parameter being
measured for automatic bypass removal by
referring to logarithmic power, the input
process variable. The results of previously
performed accident analyses remain valid.
The proposed amendment does not introduce
accident initiators or malfunctions that
would cause a new or different kind of
accident. The proposed amendments are
administrative in nature and will not change
the physical plant or the modes of plant
operation defined in the facility operating
license. The changes do not involve the
addition or modification of equipment nor do
they alter the design or operation of plant
systems. Therefore, the proposed amendment
does not create the possibility of a new or
different kind of accident from any accident
previously evaluated.
Criterion 3: Does the proposed amendment
involve a significant reduction in a margin of
safety?
Response: No.
The proposed change does not alter the
function or manner of operation of the
operating bypasses and automatic bypass
removals of the affected reactor trips. The
proposed changes do not affect any of the
assumptions used in the accident analysis,
nor do they affect any operability
requirements for equipment important to
plant safety. Therefore, the proposed
amendment does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Lillian M.
Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc.,
Rope Ferry Road, Waterford, CT 06385.
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NRC Branch Chief: Harold K.
Chernoff.
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Entergy Nuclear Operations, Inc.,
Docket No. 50–293, Pilgrim Nuclear
Power Station, Plymouth County,
Massachusetts
Date of amendment request: January
4, 2007.
Description of amendment request:
The proposed amendment would revise
the Technical Specification for Limiting
Conditions for Operation (LCOs) and
Surveillance Requirements (SRs) for
control rod operability, scram insertion
times, and control rod accumulators.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes extend the
frequency and revise the methodology for
testing control rod scram times, and identify
a new category of ‘‘slow’’ control rods for
assessing control rod operability. The
frequency of control rod scram testing is not
an initiator of any accident previously
evaluated. The frequency of surveillance
testing does not affect the ability to mitigate
any accident previously evaluated, because
the tested component is still required to be
operable. The proposed test methodology is
consistent with industry approved methods
and ensures control rod operability
requirements for the number and distribution
of operable, slow, and stuck control rods
continue to satisfy scram reactivity rate
assumptions used in plant safety analysis.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes do not involve any
physical alteration of the plant (no new or
different type of equipment is being
installed) and do not involve a change in the
design, normal configuration, or basic
operation of the plant. The proposed changes
do not introduce any new accident initiators.
The proposed changes do not involve
significant changes in the fundamental
methods governing normal plant operation
and do not require unusual or uncommon
operator actions. The proposed changes
provide assurance that the plant will not be
operated in a mode or condition that violates
the assumptions or initial conditions in the
safety analyses and that SSCs [structures,
systems, and components] remain capable of
performing their intended safety functions as
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assumed in the same analyses. Consequently,
the response of the plant and the plant
operator to postulated events will not be
significantly different.
Therefore, the proposed TS change does
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
Margin of safety is related to confidence in
the ability of the fission product barriers to
perform their design functions during and
following an accident situation. The
proposed changes address control rod scram
test performance and acceptance criteria as
well as control rod operability requirements.
The scam test acceptance criteria and control
rod operability restrictions are based on
industry approved methodology and will
continue to ensure control rod scram design
functions and reactivity insertion
assumptions used in safety analyses continue
to be protected. The proposed changes also
extend the frequency of testing control rod
scram times while at-power from 120 days to
200 days. The proposed change ensures
scram testing is performed and that test
results verify acceptable operation of the
control rods.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 50.929(c) are satisfied.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Attorney for licensee: Travis C.
McCullough, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 400
Hamilton Avenue, White Plains, NY
10601.
Branch Chief: John P. Boska (Acting).
Entergy Operations, Inc., Docket No. 50–
368, Arkansas Nuclear One, Unit No. 2
(ANO–2), Pope County, Arkansas
Date of amendment request: March
15, 2007.
Description of amendment request:
The proposed amendment would revise
containment systems surveillance
requirements for Technical
Specification (TS) 3/4.6.2,
‘‘Depressurization, Cooling, and pH
Control Systems.’’ The proposed
amendment would revise the frequency
for ANO–2 TS Surveillance
Requirement 4.6.2.1.d to require
verification that spray nozzels are
unobstructed following maintenance
that could result in a nozzel blockage
(loss of foreign material exclusion
control) rather than performing an air or
smoke flow test through each spray
header every 5 years.
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Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do[es] the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The Containment Spray System (CSS) is
not an initiator of any analyzed event. The
proposed change does not have a detrimental
impact on the integrity of any plant structure,
system, or component that may initiate an
analyzed event. The proposed change will
not alter the operation or otherwise increase
the failure probability of any plant
equipment that can initiate an analyzed
accident. This change does not affect the
plant design. There is no increase in the
likelihood of formation of significant
corrosion products. Due to their location at
the top of the containment, introduction of
foreign material into the spray headers is
unlikely. Foreign materials exclusion
controls during and following maintenance
provides assurance that the nozzles remain
unobstructed. Consequently, there is no
significant increase in the probability of an
accident previously evaluated.
The CSS is designed to address the
consequences of a Loss of Coolant Accident
(LOCA) or a Main Steam Line Break (MSLB).
The Containment Spray System is capable of
performing its function effectively with the
single failure of any active component in the
system, any of its subsystems, or any of its
support systems. Therefore, the
consequences of an accident previously
evaluated are not significantly affected by the
proposed change.
2. Do[es] the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change will not physically
alter the plant (no new or different type of
equipment will be installed) or change the
methods governing normal plant operation.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do[es] the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The system is not susceptible to corrosioninduced obstruction or obstruction from
sources external to the system. Strict controls
are established to ensure the foreign material
is not introduced into the CSS during
maintenance or repairs. Maintenance
activities that could introduce significant
foreign material into the system require
subsequent system cleanliness verification
which would prevent nozzle blockage. The
spray header nozzles are expected to remain
unblocked and available in the event that the
safety function is required. The capacity of
the system would remain unaffected.
Therefore, the proposed change does not
involve a reduction in a margin of safety.
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The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Terence A.
Burke, Associate General Council—
Nuclear Entergy Services, Inc., 1340
Echelon Parkway, Jackson, Mississippi
39213.
NRC Branch Chief: Thomas G. Hiltz.
Entergy Operations, Inc., System Energy
Resources, Inc., South Mississippi
Electric Power Association, and Entergy
Mississippi, Inc., Docket No. 50–416,
Grand Gulf Nuclear Station, Unit 1,
Claiborne County, Mississippi
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Date of amendment request: March 1,
2007.
Description of amendment request:
The proposed change would revise the
Grand Gulf Nuclear Station, Unit 1
(GGNS) Technical Specifications (TS) to
add a note to the Required Actions of TS
3.6.1.3, ‘‘Primary Containment Isolation
Valves (PCIVs),’’ Actions A.1 and B.1.
GGNS TS 3.6.1.3 requires specific
actions to be taken for inoperable PCIVs.
The TS Required Actions include
isolating the affected penetration by use
of a closed and deactivated automatic
valve, closed manual valve, blind
flange, or check valve with flow through
the valve secured. The new note would
allow a relief valve to be used without
being deactivated, to comply with TS
3.6.1.3, Actions A.1 and B.1, provided it
has a relief setpoint of at least 1.5 times
containment design pressure (i.e., at
least 23 pounds per square inch gauge)
and meets one of the following criteria:
1. The relief valve is 1-inch nominal
size or less, or
2. The flow path is into a closed
system whose piping pressure rating
exceeds the containment design
pressure rating.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Primary Containment Isolation Valves
(PCIVs) are accident mitigating features
designed to limit releases from the
containment following an accident. The TS
specify actions to be taken to preserve the
containment isolation function if a PClV is
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inoperable. These actions include isolating
the penetration flow path by specific
methods including, closed and de-activated
automatic valves, closed manual valves,
blind flanges, and check valves with flow
through the valve secured. The current TS
Actions do not specifically recognize a closed
relief valve as an acceptable method of
isolating a penetration flow path. Thus,
special measures may need to be taken to
comply with the TS Required Actions, such
as replacing the relief valve with a blind
flange or de-activating the relief valve by
installing a gag. While such actions may
provide additional assurance of preserving
the containment isolation function, it may
also have adverse safety affects such as
disabling the overpressure protective safety
feature, causing additional safety system
unavailability time, and increasing
occupational dose.
The proposed change would allow certain
relief valves to be used for isolating the
penetration flow path without being deactivated. The proposed TS changes do not
alter the design, operation, or capability of
PCIVs. Relief valves are designed to be
normally closed to preserve the piping
boundary integrity yet automatically open on
an abnormal process pressure to protect the
piping from overpressure conditions. Relief
valves may also serve as passive containment
isolation devices (i.e., they do not require
mechanical movement to perform the
isolation function). The proposed TS changes
preserve both the containment isolation and
piping overpressure protection functions.
The failure of a relief valve to remain
closed during or following an accident is
considered a low probability because relief
valves are passive isolation devices that do
not require mechanical movement to perform
the isolation function and the relief setpoint
provides sufficient margin to preclude the
potential for premature opening due to
containment post-accident pressures.
Additional criteria are established to provide
defense-in-depth protection. Relief valves
that are one-inch or smaller provide an
additional physical barrier in that, even in
the unlikely event that a relief valve were to
fail to remain fully closed during or
following an accident, the size restriction
would limit leakage such that a large early
release would not occur. By definition,
penetrations one-inch and smaller do not
contribute to large early releases. Larger relief
valves may be used as isolation devices
provided that the containment penetration
flow path through the relief valve would be
contained in a closed system. In the unlikely
event that a relief valve were to fail to remain
closed, the leakage would be into a system
which forms a closed loop outside primary
containment and any containment leakage
would return to primary containment
through this closed loop.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
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The proposed change does not introduce
any new modes of plant operation or
adversely affect the design function or
operation of safety features. The proposed TS
change allows use of existing plant
equipment as compensatory measures to
maintain the containment isolation design
intent when the normal isolation features are
inoperable. Since relief valves used for this
purpose will not be disabled by gags or blind
flanges, the system piping overpressure
protection design feature will also be
preserved.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The safety margin associated with this
change is that associated with preserving the
containment integrity. NUREG–0800, the
Standard Review Plan, recognizes that relief
valves with relief setpoints greater than 1.5
times containment design pressure are
acceptable as containment isolation devices.
Closed relief valves with relief setpoints of
this margin provide an isolation alternative
that is less susceptible to a single failure (i.e.,
inadvertent opening) yet still preserves the
overpressure protection that the component
was intended to provide. The failure of a
relief valve to remain closed during or
following an accident is considered a low
probability because relief valves are passive
isolation devices that do not require
mechanical movement to perform the
isolation function and the relief setpoint
provides sufficient margin to preclude the
potential for premature opening due to
containment post-accident pressures.
Defense-in-depth containment leakage
protection is provided by additional TS
criteria that limit the use of relief valves to
those one-inch or less in size or those where
containment leakage would be into a closed
system whose piping pressure rating exceeds
the containment design pressure rating.
Relief valves that are one-inch or smaller
provide an additional physical barrier in that,
even in the unlikely event that a relief valve
were to fail to remain closed during or
following an accident, the size restriction
would limit leakage such that a large early
release would not occur. In the unlikely
event that a relief valve larger than one-inch
were to fail to remain closed, the leakage
would be into a system which forms a closed
loop outside primary containment and any
containment leakage would return to primary
containment through this closed loop.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Terence A.
Burke, Associate General Council—
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Nuclear Entergy Services, Inc., 1340
Echelon Parkway, Jackson, Mississippi
39213.
NRC Branch Chief: David Terao.
jlentini on PROD1PC65 with NOTICES
FirstEnergy Nuclear Operating
Company, et al., Docket Nos. 50–334
and 50–412, Beaver Valley Power
Station, Unit Nos. 1 and 2 (BVPS–1 and
2), Beaver County, Pennsylvania
Date of amendment request: February
9, 2007.
Description of amendment request:
The proposed amendment would revise
the Technical Specification (TS) 3.3.2,
‘‘Engineered Safety Feature Actuation
System Instrumentation,’’ TS 3.5.2,
‘‘Emergency Core Cooling System—
Operating,’’ TS 3.6.5, ‘‘Containment Air
Temperature,’’ and TS 5.5.12,
‘‘Containment Leakage Rate Testing
Program.’’ The revised TSs would be
consistent with a proposed change to
the Recirculation Spray System (RSS)
pump start signal due to a modification
to the containment sump screens.
The proposed amendment would also
replace the use of LOCTIC with the
Modular Accident Analysis ProgramDesign Basis Accident (MAAP–DBA) for
calculating containment pressure,
temperature, and condensation rates for
input to the SWNAUA code. The
calculation methodology change would
ultimately change the aerosol removal
coefficients used in dose consequence
analysis.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No. The proposed changes to the
RSS pump start signal, the upper
containment temperature technical
specification (TS) limit, the peak
containment internal pressure, the
nomenclature for automatic switchover to the
containment sump, and the containment
sump screen visual inspection surveillance
requirement do not involve any system or
component that are accident initiators. The
RSS is used for accident mitigation only. The
Refueling Water Storage Tank (RWST) level
and containment pressure instrumentation
will continue to comply with all applicable
regulatory requirements and design criteria
(e.g., train separation, redundancy, single
failure, etc.) following approval of the
proposed changes. The design functions
performed by the RSS and the containment
are not changed by this license amendment
request.
Delaying the start of the RSS pumps and
the change to the upper containment
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temperature affect the long-term containment
pressure and temperature profiles. The
environmental qualification of safety-related
equipment inside containment will be
confirmed to be acceptable and accident
mitigation systems will continue to operate
within design temperatures and pressures.
Delaying the RSS pump start reduces the
emergency diesel generator loading in the
early stage of a design basis accident and
maintaining the staggered loading of the RSS
pump starts avoids overloading on each
emergency diesel generator at Unit 1.
Staggered loading of the emergency diesel
generator is not required for Unit 2.
The methodology change to calculate
containment pressure, temperature and
condensation rates for input to the SWNAUA
code will not involve a significant increase
in the probability of an accident previously
evaluated because this change in
methodology does not impact accident
initiators.
The loss of coolant accident (LOCA) has
been evaluated using the guidance provided
in Regulatory Guide 1.183, ‘‘Alternative
Radiological Source Terms for Evaluating
Design Basis Accidents at Nuclear Power
Reactors.’’ The radiological consequences of
the remaining design basis accidents are not
significantly impacted by the proposed
changes. As demonstrated by the supporting
analyses, the estimated dose consequences at
the Exclusion Area Boundary (EAB), Low
Population Zone (LPZ), and control room
remain within the acceptance criteria of 10
CFR 50.67 as supplemented by Regulatory
Guide 1.183 and Standard Review Plan
Section 15.0.1. In addition, the supporting
analyses also demonstrates that the dose
consequences in the Emergency Response
Facility remain compliant with paragraph
IV.E.8 of Appendix E, to 10 CFR part 50,
Emergency Planning and Preparedness for
Production and Utilization Facilities,
regulatory guidance provided in Supplement
1 of NUREG–0737. The revised radiological
analyses results in a slight increase in control
room and off-site doses; however, the
radiological analyses and evaluations
developed in support of this application
demonstrate that the proposed changes will
not impact compliance with applicable
regulatory requirements and will not involve
a significant increase in the consequences of
an accident previously evaluated. The slight
increase in control room and off-site doses is
more than offset by the increased assurance
of adequate NPSH [net positive suction head]
to the RSS pumps and Emergency Core
Cooling System operability.
The safety analysis acceptance criteria will
continue to be met following the proposed
changes to the RSS pump start signal, visual
sump inspection, TS containment upper
temperature limit, peak containment internal
pressure, nomenclature for automatic
switchover to the containment sump and the
change to the control room and off-site dose
consequences analyses.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
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20383
accident from any accident previously
evaluated?
Response: No. One of the proposed
changes alters the RSS pump start circuitry
by initiating the pump start from a coincident
Containment Pressure High-High/[RWST]
Level Low signal instead of from a timer. The
RSS pump instrumentation will be included
as part of the Engineered Safety Feature
Actuation System (ESFAS) instrumentation
in the TS and will be subject to the ESFAS
surveillance requirements following approval
of the proposed changes. The design of the
RSS pump start instrumentation complies
with all applicable regulatory requirements
and design criteria. The failure modes have
been analyzed to ensure that the revised RSS
pump start circuitry can withstand a single
active failure without affecting the RSS
design functions. The RSS is an accident
mitigation system only, so no new accident
initiators are created.
It is not expected that the change in
containment temperature will have a
significant impact on equipment
qualification. However, any equipment that
must be replaced or re-qualified will be
addressed prior to operation with the
proposed change to RSS pump start. As a
result any such equipment will not introduce
new failure modes, accident initiators, or
malfunctions that would cause a new or
different kind of accident.
The remaining changes do not change
plant equipment design or function and
therefore will not introduce new failure
modes, accident initiators, or malfunctions
that would cause a new or different kind of
accident.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No. The changes to the RSS
pump start signal and the upper containment
temperature limit affect the containment
response and the LOCA dose analyses.
Analyses demonstrate that containment
design basis limits are satisfied and postLOCA offsite and control room dose criteria
will continue to be met following approval of
the proposed changes.
The change to the containment sump
visual inspection will not involve a
significant reduction in a margin of safety
because the revised surveillance will
continue to provide adequate assurance the
sump screens are not blocked with debris
and that signs of corrosion will be detected.
The change to peak containment internal
pressure will not result [in] a significant
reduction in a margin of safety because the
new pressure is lower for each of the units.
Although the control room and off-site
doses slightly increase (due to a combination
of the change to the start signal and the
proposed methodology change), the increase
will not involve a significant reduction in a
margin of safety because operator and public
exposure limits will continue to meet
applicable regulatory requirements.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
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The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David W.
Jenkins, FirstEnergy Nuclear Operating
Company, FirstEnergy Corporation, 76
South Main Street, Akron, OH 44308.
NRC Acting Branch Chief: John P.
Boska.
Nine Mile Point Nuclear Station
(NMPNS), LLC, Docket No. 50–410, Nine
Mile Point Nuclear Station Unit No. 2
(NMP2), Oswego County, New York
Date of amendment request: March 8,
2007.
Description of amendment request:
The proposed amendment would add
Technical Specification (TS) Limiting
Condition for Operation (LCO) 3.0.8 to
allow a delay time for entering a
supported system TS when the
inoperability is due solely to an
inoperable snubber, if risk is assessed
and managed. The proposed change is
consistent with TS Task Force (TSTF)
change TSTF–372-A, Revision 4,
‘‘Addition of LCO 3.0.8, Inoperability of
Snubbers.’’
The NRC staff issued a notice of
availability of a model no significant
hazards consideration determination for
referencing in license amendment
applications in the Federal Register on
November 24, 2004 (69 FR 68412). The
licensee affirmed the applicability of the
model in its application.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
Criterion 1—The Proposed Change
Does Not Involve a Significant Increase
in the Probability or Consequences of an
Accident Previously Evaluated.
The proposed change allows a delay
time for entering a supported system TS
when the inoperability is due solely to
an inoperable snubber if risk is assessed
and managed. The postulated seismic
event requiring snubbers is a lowprobability occurrence and the overall
TS system safety function would still be
available for the vast majority of
anticipated challenges. Therefore, the
probability of an accident previously
evaluated is not significantly increased,
if at all. The consequences of an
accident while relying on allowance
provided by proposed LCO 3.0.8 are no
different than the consequences of an
accident while relying on the TS
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18:32 Apr 23, 2007
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required actions in effect without the
allowance provided by proposed LCO
3.0.8. Therefore, the consequences of an
accident previously evaluated are not
significantly affected by this change.
The addition of a requirement to assess
and manage the risk introduced by this
change will further minimize possible
concerns. Therefore, this change does
not involve a significant increase in the
probability or consequences of an
accident previously evaluated.
Criterion 2—The Proposed Change
Does Not Create the Possibility of a New
or Different Kind of Accident From Any
Previously Evaluated.
The proposed change does not
involve a physical alteration of the plant
(no new or different type of equipment
will be installed). Allowing delay times
for entering supported system TS when
inoperability is due solely to inoperable
snubbers, if risk is assessed and
managed, will not introduce new failure
modes or effects and will not, in the
absence of other unrelated failures, lead
to an accident whose consequences
exceed the consequences of accidents
previously evaluated. The addition of a
requirement to assess and manage the
risk introduced by this change will
further minimize possible concerns.
Thus, this change does not create the
possibility of a new or different kind of
accident from an accident previously
evaluated.
Criterion 3—The Proposed Change
Does Not Involve a Significant
Reduction in the Margin of Safety.
The proposed change allows a delay
time for entering a supported system TS
when the inoperability is due solely to
an inoperable snubber, if risk is assessed
and managed. The postulated seismic
event requiring snubbers is a lowprobability occurrence and the overall
TS system safety function would still be
available for the vast majority of
anticipated challenges. The risk impact
of the proposed TS changes was
assessed following the three-tiered
approach recommended in Regulatory
Guide 1.177. A bounding risk
assessment was performed to justify the
proposed TS changes. This application
of LCO 3.0.8 is predicated upon the
licensee’s performance of a risk
assessment and the management of
plant risk. The net change to the margin
of safety is insignificant. Therefore, this
change does not involve a significant
reduction in a margin of safety.
The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorney for licensee: Mark J.
Wetterhahn, Esquire, Winston & Strawn,
1700 K Street, NW., Washington, DC
20006.
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NRC Acting Branch Chief: John P.
Boska.
Nuclear Management Company, LLC,
Docket No. 50–263, Monticello Nuclear
Generating Plant, Wright County,
Minnesota
Date of amendment request: February
15, 2007.
Description of amendment request:
The proposed amendment would revise
Technical Specifications (TSs)
Surveillance Requirement (SR) 3.8.4.2 to
correct errors inadvertently introduced
by Amendment No. 146. SR 3.8.4.2
currently requires that each battery
charger be verified to supply greater
than or equal to 150 amps for 250-volt
DC subsystems, and greater than or
equal to 50 amp for 125-volt DC
subsystems. The licensee proposed to
correct the errors by differentiating that
the Division 1 battery chargers are
verified to supply greater than or equal
to 150 amps and the Division 2 battery
chargers are verified to supply greater
than or equal to 110 amps. The licensee
stated that the Division 2 battery charger
output current limiter is field-adjusted
to supply 120 to 125 amps in order to
stay within the electrical circuit breaker
ratings in the associated distribution
cabinet.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration (NSHC). The NRC staff
reviewed the licensee’s analysis, and
has performed its own analysis as
follows:
(1) Does the proposed amendment involve
a significant increase in the probability or
consequence of an accident previously
evaluated?
No. The proposed amendment would only
correct the battery chargers’ DC supply
current limits specified by SR 3.8.4.2. The
current limits of the battery chargers were not
considered to be a precursor to, and does not
affect the probability of, an accident. In
addition, there is no design or operation
change associated with the proposed
amendment. Therefore, the proposed
amendment does not increase the probability
of an accident previously evaluated.
The corrected DC supply current limits of
the battery chargers will ensure that the
batteries will be charged under as-designed
conditions. The corrected limits will not
decrease the functionality of the Division 1
or Division 2 battery chargers, or the
functionality of the batteries the battery
chargers support. Therefore, the plant
systems required to mitigate accidents will
remain capable of performing their design
functions. As a result, the proposed
amendment will not lead to a significant
change in the consequences of any accident.
(2) Does the proposed amendment create
the possibility of a new or different kind of
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accident from any accident previously
evaluated?
No. The proposed amendment does not
involve a physical alteration of any system,
structure, or component (SSC) or a change in
the way any SSC is operated. The proposed
amendment does not involve operation of
any SSCs in a manner or configuration
different from those previously recognized or
evaluated. No new failure mechanisms will
be introduced by the revised acceptance
value. Thus, the proposed amendment does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
(3) Does the proposed amendment involve
a significant reduction in a margin of safety?
No. The proposed amendment would only
change the current supply limits of the
battery chargers. There will be no
modification of any TSs limiting condition
for operation, no change to any limit on
previously analyzed accidents, no change to
how previously analyzed accidents or
transients would be mitigated, no change in
any methodology used to evaluate
consequences of accidents, and no change in
any operating procedure or process.
Therefore, the proposed amendment does not
involve a significant reduction in a margin of
safety.
jlentini on PROD1PC65 with NOTICES
The NRC staff has reviewed the
licensee’s analysis and, based on the
NRC staff’s own analysis above, it
appears that the three standards of 10
CFR 50.92(c) are satisfied. Therefore, the
NRC staff proposes to determine that the
proposed amendment involves no
significant hazards consideration.
Attorney for licensee: Jonathan Rogoff,
Esquire, Vice President, Counsel &
Secretary, Nuclear Management
Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Branch Chief: L. Raghavan.
Southern California Edison Company, et
al., Docket Nos. 50–361 and 50–362,
San Onofre Nuclear Generating Station,
Units 2 and 3, San Diego County,
California
Date of amendment requests: March
30, 2007.
Description of amendment requests:
The proposed change will revise
Technical Specifications (TSs)
Surveillance Requirement (SR) 3.3.7.3.b,
‘‘Loss of Voltage Function’’ to a
narrower voltage band and lower
operating time for channel calibration
testing, by replacing the undervoltage
relays with the reset time significantly
lower.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
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18:32 Apr 23, 2007
Jkt 211001
consequences of an accident previously
evaluated?
Response: No.
The proposed change revises the Technical
Specifications Surveillance Requirement
3.3.7.3.b allowable set point values of the
Loss of Voltage Function for the channel
calibration testing. This proposed change
will allow Southern California Edison (SCE)
to increase margin and conservatism for the
loss of voltage relay settings and overall loop
uncertainties while performing Loss of
Voltage Signal (LOVS) channel calibration
testing.
The loss of voltage function is detected by
the LOVS relays installed on the 4.16 kV
Safety Related busses. Normally, these
devices are not considered to be accident
initiators. The proposed change narrows the
voltage operating band and lowers the
allowable upper limit for this loss of voltage
detection by use of the electronic type Basler
BE1–27 under-voltage relays. However, the
reset time of the relay [will be reduced]
significantly. [Therefore, t]he proposed
change does not impact probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from [an] accident previously
evaluated?
Response: No.
The proposed allowable values for the
LOVS relays voltage settings and the
minimum operating voltage of the of[f]site
power will provide acceptable level of
protection for the plant equipment.
3. Does the proposed change involve [a]
significant reduction in a margin of safety?
Response: No.
The proposed loss of voltage function is
designed to ensure that plant equipment will
not operate beyond its normal operating
range for satisfactory operation of all the
safety related equipment. The proposed loss
of voltage function values will not affect the
existing protection criterion for the plant
equipment and will not reduce margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Douglas K.
Porter, Esquire, Southern California
Edison Company, 2244 Walnut Grove
Avenue, Rosemead, California 91770.
NRC Branch Chief: Thomas G. Hiltz.
Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton
County, Tennessee
Date of amendment request: February
16, 2007.
Description of amendment request:
The proposed amendment would
permanently revise Technical
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20385
Specification 2.2.1, Table 2.2–1,
Functional Unit 17.A, Turbine Trip Low
Trip System Pressure allowable value.
The proposed revision was previously
approved for one operating cycle at each
unit.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change revises the allowable
value for reactor trip as a result of a turbine
trip on low trip system pressure. This change
will not alter any plant components, systems,
or processes and will only provide a more
appropriate value to assess operability of the
associated pressure switches. Since the plant
features and operating practices are not
altered, the possibility of an accident is not
affected. This reactor trip is not directly
credited in SQN’s [Sequoyah Nuclear Plant’s]
accident analysis and is maintained as an
anticipatory trip to enhance the overall
reliability of the reactor trip system. As such,
there is not a specific safety limit associated
with this function and the generation of a
reactor trip based on low trip system pressure
is above the required actuations to ensure
acceptable mitigation of accidents. As the
proposed change will continue to provide an
acceptable anticipatory trip signal, the offsite
dose potential is not affected by this change.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
As described above, this change will not
alter any plant equipment or operating
practices that have the ability to create a new
potential for accident generation. The
proposed change revises the operability
limits for a function that generates a trip
signal when appropriate conditions exist to
require accident mitigation response. This
type of function does not have the ability to
create an accident as its purpose and
function is to mitigate events. Therefore, the
proposed change does not create the
possibility of a new or different kind of
accident from any previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change will revise an
allowable value for a reactor trip initiator that
results from a turbine trip condition. This
change will not alter the setpoint, and the
calibration of the associated pressure
switches will continue to be set at the current
value. The allowable value change is in
response to accuracy aspects of the
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instrumentation and does not alter the ability
of this trip function to operate when and as
needed to mitigate accident conditions.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
jlentini on PROD1PC65 with NOTICES
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Thomas H. Boyce.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.22(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) The applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
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18:32 Apr 23, 2007
Jkt 211001
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
Carolina Power & Light Company,
Docket No. 50–261, H. B. Robinson
Steam Electric Plant, Unit No. 2,
Darlington County, South Carolina
Date of application for amendment:
January 19, 2007, as supplemented by
letters dated March 13 and 22, 2007.
Brief description of amendment: The
amendment modifies Technical
Specifications 5.5.9 and 5.6.8 to add
steam generator alternate repair criteria
and additional steam generator
reporting criteria at H. B. Robinson
Steam Electric Plant, Unit No. 2.
Date of issuance: April 9, 2007.
Effective date: This license
amendment is effective as of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 214.
Renewed Facility Operating License
No. DPR–23. Amendment revises the
Technical Specifications.
Date of initial notice in Federal
Register: January 30, 2007 (72 FR
4300). The March 13 and 22, 2007,
supplemental letters provided clarifying
information that did not change the
initial proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 9, 2007.
No significant hazards consideration
comments received: No.
Dominion Nuclear Connecticut, Inc., et
al., Docket No. 50–423, Millstone Power
Station, Unit No. 3, New London
County, Connecticut
Date of application for amendment:
March 28, 2006, as supplemented by
letters dated October 26, and December
4, 2006, and January 26, 2007.
Brief description of amendment: The
amendment revises Millstone Power
Station, Unit No. 3 Technical
Specifications (TS) to delete redundant
surveillance requirements pertaining to
post-maintenance/post-modification
testing.
Date of Issuance: March 29, 2007.
Effective date: As of the date of
issuance and shall be implemented
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within 90 days from the date of
issuance.
Amendment No.: 237.
Facility Operating License No. NPF–
49: Amendment revised the TS.
Date of initial notice in Federal
Register: May 23, 2006 (71 FR 29673).
The supplemental letters provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 29, 2007.
No significant hazards consideration
comments received: No.
Duke Power Company LLC, Docket Nos.
50–269, 50–270, and 50–287, Oconee
Nuclear Station, Units 1, 2, and 3,
Oconee County, South Carolina
Date of application of amendments:
April 11, 2006, as supplemented
October 24, 2006.
Brief description of amendments: The
amendments revised the Technical
Specifications requirements related to
steam generator tube integrity consistent
with the NRC-approved Revision 4 to
Technical Specification Task Force
(TSTF) Standard Technical
Specification Change Traveler TSTF–
449, ‘‘Steam Generator Tube Integrity.’’
These amendments also remove license
conditions that become outdated with
these TS changes. In addition, the
amendments revised the organizational
description in TS 5.2.1, which is solely
administrative and unrelated to steam
generator tube integrity.
Date of Issuance: April 2, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 355, 357, 356.
Renewed Facility Operating License
Nos. DPR–38, DPR–47, and DPR–55:
Amendments revised the licenses and
the technical specifications.
Date of initial notice in Federal
Register: January 3, 2007 (72 FR 149).
The supplement dated October 24, 2006,
provided additional information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the staff’s
original proposed no significant hazards
consideration determination. The
Commission’s related evaluation of the
amendments is contained in a Safety
Evaluation dated April 2, 2007. No
significant hazards consideration
comments received: No.
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Duke Power Company LLC, Docket Nos.
50–269, 50–270, and 50–287, Oconee
Nuclear Station, Units 1, 2, and 3,
Oconee County, South Carolina
Date of application of amendments:
April 11, 2006, as supplemented by
letter dated March 14, 2007.
Brief description of amendments: The
amendments added Technical
Specification (TS) Limiting Condition
for Operation (LCO) 3.0.8 to allow a
delay time for entering a supported
system TS when the inoperability is due
solely to an inoperable snubber, if risk
is assessed and managed with an
approved Bases Control Program that is
consistent with the TS Bases Control
Program described in Section 5.5 of the
applicable vendor’s Standard Technical
Specifications.
Date of Issuance: April 2, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 356, 358, 357.
Renewed Facility Operating License
Nos. DPR–38, DPR–47, and DPR–55:
Amendments revised the licenses and
the Technical Specifications.
Date of initial notice in Federal
Register: January 3, 2007 (72 FR 151).
The supplement provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the NRC staff’s
original proposed no significant hazards
consideration determination as
published in the Federal Register on
January 3, 2007 (72 FR 151). The
Commission’s related evaluation of the
amendments is contained in a Safety
Evaluation dated April 2, 2007.
No significant hazards consideration
comments received: No.
jlentini on PROD1PC65 with NOTICES
Exelon Generation Company, LLC,
Docket Nos. STN 50–454 and STN 50–
455, Byron Station, Unit Nos. 1 and 2,
Ogle County, Illinois; Docket Nos. STN
50–456 and STN 50–457, Braidwood
Station, Units 1 and 2, Will County,
Illinois
Date of application for amendment:
November 18, 2005, as supplemented by
letters dated August 18 and September
28, 2006, and February 15, February 23,
and March 7, 2007.
Brief description of amendment: The
amendments would revise the existing
steam generator tube surveillance
program using Technical Specification
Task Force Traveler No. 449 (TSTF–
449), Revision 4, ‘‘Steam Generator
Tube Integrity’’ as a basis. The
amendments would also revise TS 5.5.9,
‘‘Steam Generator (SG) Tube
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18:32 Apr 23, 2007
Jkt 211001
Surveillance Program,’’ regarding the
required SG inspection scope for Byron
Station, Unit No. 2, during outage
number 13 and subsequent operating
cycle. A similar approval was granted
for Braidwood Station, Unit 2 by letter
from the NRC dated October 24, 2006.
Date of Issuance: March 30, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment Nos.: 150/150, 144/144.
Facility Operating License Nos. NPF–
37, NPF–66, NPF–72 and NPF–77: The
amendments revised the Technical
Specifications and License.
Date of initial notice in Federal
Register: May 23, 2006 (71 FR 29676).
The August 18 and September 28, 2006
and February 15, February 23, and
March 7, 2007 supplements, contained
clarifying information and did not
change the staff’s initial proposed
finding of no significant hazards
consideration.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 30, 2007.
No significant hazards consideration
comments received: No.
FPL Energy Seabrook, LLC, Docket No.
50–443, Seabrook Station, Unit No. 1,
Rockingham County, New Hampshire
Date of amendment request: March
23, 2006, as supplemented by letters
dated August 16 and November 28,
2006.
Description of amendment request:
The amendment revises the Seabrook
Station, Unit No. 1 Technical
Specifications (TSs) Definitions, TS
3.4.5, ‘‘Steam Generator (SG) Tube
Integrity,’’ and TS 3.4.6.2, ‘‘Reactor
Coolant System Operational Leakage’’
consistent with Technical Specification
Task Force (TSTF) Standard Technical
Specification Traveler TSTF–449,
‘‘Steam Generator Tube Integrity,’’
Revision 4. Additionally the
amendment creates TS 6.7.6.k. ‘‘Steam
Generator (SG) Program’’ and TS 6.8.1.7,
‘‘Steam Generator Tube Inspection
Report,’’ consistent with TSTF–449,
Revision 4.
Date of Issuance: March 28, 2007.
Effective date: As of its date of
issuance, and shall be implemented
within 90 days.
Amendment No.: 115.
Facility Operating License No. NPF–
86: The amendment revised the License
and Technical Specifications.
Date of initial notice in Federal
Register: April 25, 2006 (71 FR 23955).
The licensee’s August 16 and November
28, 2006, supplements provided
clarifying information that did not
change the scope of the proposed
PO 00000
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20387
amendment as described in the original
notice of proposed action published in
the Federal Register, and did not
change the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 28, 2007.
No significant hazards consideration
comments received: No.
Nuclear Management Company, LLC,
Docket No. 50–266, Point Beach Nuclear
Plant, Unit 1, Town of Two Creeks,
Manitowoc County, Wisconsin
Date of application for amendments:
July 11, 2006, as supplemented January
19, March 9 and 26, 2007.
Brief description of amendments: The
amendment revises Technical
Specification (TS) 5.5.8, ‘‘Steam
Generator Program,’’ to change the
inspection and repair criteria for
portions of the tubes within the hot-leg
region of the tubesheet for a single
operating cycle. In addition, an
administrative change corrects a page
number in the TS Table of Contents and
deletes two blank pages in TS Section
5.0.
Date of Issuance: April 4, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 45 days.
Amendment No.: 226.
Renewed Facility Operating License
Nos. DPR–24 and DPR–27: Amendments
revised the Technical Specifications/
License.
Date of initial notice in Federal
Register: August 29, 2006 (71 FR
51230). The supplements dated January
19, March 9 and 26, 2007, contained
clarifying information and did not
change the staff’s initial proposed
finding of no significant hazards
consideration.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 4, 2007.
No significant hazards consideration
comments received: No.
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1, Washington County, Nebraska
Date of amendment request:
December 20, 2006.
Brief description of amendment: The
amendment removed annotations
referencing Technical Data Book (TDB)–
VIII, ‘‘Equipment Operability
Guidance,’’ and annotations referencing
Technical Specification Interpretations
(TSIs) from the NRC Authority File of
the Technical Specifications (TSs).
These documents are used by Omaha
Public Power District (OPPD) personnel
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Federal Register / Vol. 72, No. 78 / Tuesday April 24, 2007 / Notices
jlentini on PROD1PC65 with NOTICES
for additional guidance in applying
certain Limiting Conditions of
Operation requirements to specific
equipment and/or situations. OPPD has
annotated references to these documents
in the TS copies used at the Fort
Calhoun Station, Unit No.1 (FCS);
however, these annotations were
inadvertently included into the NRC
Authority File and are not officially part
of the FCS TS. The amendment also
corrected a discrepancy in TS
2.10.4(1)(c).
Date of Issuance: April 3, 2007.
Effective date: As of its date of
issuance and shall be implemented
within 90 days from the date of
issuance.
Amendment No.: 249.
Renewed Facility Operating License
No. DPR–40: The amendment revised
the Operating License and Technical
Specifications.
Date of initial notice in Federal
Register: January 30, 2007 (72 FR
4308).
The Commission’s related evaluation
of the amendment is contained in a
safety evaluation dated April 3, 2007.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket No. 50–311,
Salem Nuclear Generating Station, Unit
No. 2, Salem County, New Jersey
Date of application for amendment:
April 6, 2006, as supplemented by
letters dated January 19, and February
27, 2007.
Brief description of amendment: The
amendment revises the Technical
Specifications (TSs) related to steam
generator tube integrity consistent with
Revision 4 to Technical Specification
Task Force (TSTF) Standard Technical
Specification Change Traveler 449
(TSTF–449), ‘‘Steam Generator Tube
Integrity.’’
Date of Issuance: March 29, 2007.
Effective date: As of the date of
issuance, to be implemented within 60
days.
Amendment No.: 262.
Facility Operating License No. DPR–
75: The amendment revised the TSs and
the License.
Date of initial notice in Federal
Register: July 18, 2006 (71 FR 40753).
The letters dated January 19, and
February 27, 2007, provided clarifying
information that did not change the
initial proposed no significant hazards
consideration determination or expand
the application beyond the scope of the
original Federal Register notice.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 29, 2007.
No significant hazards consideration
comments received: No.
VerDate Aug<31>2005
18:32 Apr 23, 2007
Jkt 211001
Southern California Edison Company, et
al., Docket Nos. 50–361 and 50–362,
San Onofre Nuclear Generating Station,
Units 2 and 3, San Diego County,
California
Date of application for amendments:
June 2, 2006, as supplemented by letter
dated October 19, 2006.
Brief description of amendments: The
amendments revised Technical
Specification (TS) 3.8.1, ‘‘AC
[alternating current] Sources—
Operating,’’ and TS 3.8.3, ‘‘Diesel Fuel
Oil, Lube Oil, and Starting Air,’’ to
increase the required amount of stored
diesel fuel oil to support a change to
Ultra Low Sulfur Diesel fuel from
California diesel fuel presently in use.
This change in the type of fuel oil is
mandated by California air pollution
control regulations.
Date of Issuance: April 4, 2007.
Effective date: As of its issuance and
shall be implemented within 60 days of
issuance.
Amendment Nos.: Unit 2—211; Unit
3—203.
Facility Operating License Nos. NPF–
10 and NPF–15: The amendments
revised the Facility Operating Licenses
and Technical Specifications.
Date of initial notice in Federal
Register: July 18, 2006 (71 FR 40754).
The supplemental letter dated October
19, 2006, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
no significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 4, 2007.
No significant hazards consideration
comments received: No.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Unit Nos.
1 and 2, Somervell County, Texas
Date of amendment request: February
21, 2006.
Brief description of amendments: The
amendments revised Technical
Specifications 1.1, ‘‘Definitions,’’ and
3.4.16, ‘‘RCS [Reactor Coolant System]
Specific Activity.’’ The revisions
replaced the current Limiting Condition
for Operation (LCO) 3.4.16 limit on RCS
grossspecific activity with limits on RCS
Dose Equivalent I–131 (DEI) and Dose
Equivalent Xe-133 (DEX). The
conditions and required actions for LCO
3.4.16 not being met, and surveillance
requirements for LCO 3.4.16, are
revised. The modes of applicability for
LCO 3.4.16 are extended. TS Figure
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Fmt 4703
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3.4.16–1 on the limit for DEI with
respect to rated thermal power is
deleted.
Date of issuance: March 29, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 120 days from the date of
issuance.
Amendment Nos.: 137/137.
Facility Operating License Nos. NPF–
87 and NPF–89: The amendments
revised the Facility Operating Licenses
and Technical Specifications.
Date of initial notice in Federal
Register: February 27, 2007 (72 FR
8805).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 29, 2007.
No significant hazards consideration
comments received: No.
Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of application for amendment:
August 17, 2006.
Brief description of amendment: The
amendment revised Technical
Specifications (TSs) 2.1.1, ‘‘Reactor Core
SLs [Safety Limits],’’ 3.3.1, ‘‘Reactor
Trip System (RTS) Instrumentation,’’
3.4.1, RCS [Reactor Coolant System]
Pressure, Temperature, and Flow
Departure from Nucleate Boiling (DNB)
Limits,’’ and 5.6.5, ‘‘Core Operating
Limits Report (COLR).’’ The changes (1)
relocated certain operating cyclespecific core operating limits, including
TS Figure 2.1.1–1, ‘‘Reactor Core Safety
Limits,’’ from the TSs to the plant
COLR, (2) added two new safety limits
for departure from nucleate boiling ratio
and peak fuel centerline temperature,
and (3) added topical reports to TS 5.6.5
and had the reports cited by only the
report title and number. TS 5.6.5 was
expanded to include the limits from TSs
2.1.1, 3.3.1, and 3.4.1.
Date of Issuance: April 2, 2007.
Effective date: As of its date of
issuance and shall be implemented
within 90 days from the date of
issuance. The final TS Bases changes
including the licensee’s application
dated August 17, 2006, will be
processed under the licensee’s program
for updates to the TS Bases, in
accordance with TS 5.5.14, at the time
this amendment is implemented. The
final changes to the COLR including
those in the licensee’s application dated
August 17, 2006, will be submitted to
the NRC in accordance with the update
process covered by TS 5.6.5.d.
Amendment No.: 183.
Facility Operating License No. NPF–
30: The amendment revised the
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of permanent modifications to the
equipment and associated power supply
configuration. The revisions include the
addition of requirements and/or action
statements addressing the inoperability
of two or more air handling units
(AHUs) on a unit, as well as AHU
powered from an H emergency bus. The
proposed change, paralleling
requirements in the Improved Technical
Virginia Electric and Power Company, et Specifications, also adds MCR and
ESGR ACS requirements during
al., Docket Nos. 50 280 and 50–281,
refueling operations and irradiated fuel
Surry Power Station, Units 1 and 2,
movement in the fuel building. In
Surry County, Virginia
addition, the proposed change clarified
Date of application for amendments:
the service water requirements for the
May 26, 2006, as supplemented on
ACS chillers that serve the MCR and
January 19, 2007.
ESGRs.
Brief Description of amendments:
Date of Issuance: April 2, 2007.
These amendments revised the
Effective date: As of date of issuance
Technical Specification (TS)
and shall be implemented within 45
requirements related to steam generator
days.
tube integrity and Reactor Coolant
Amendment Nos.: 252, 251.
System leakage definitions and
Renewed Facility Operating License
requirements. The TSs were revised to
Nos. DPR–32 and DPR–37: Amendments
implement TS Task Force (TSTF)
changed the licenses and the technical
Standard TS Change Traveler, TSTF–
specifications.
449, ‘‘Steam Generator Tube Integrity,’’
Date of initial notice in Federal
(TSTF–449, Rev. 4) with minor
Register: September 26, 2006 (71 FR
deviations to be consistent with Surry’s
56193). The supplements dated
custom TSs.
September 21 and November 20, 2006,
Date of Issuance: March 29, 2007.
provided additional information that
Effective date: As of date of issuance
clarified the application, did not expand
and shall be implemented within 180
the scope of the application as originally
days.
noticed, and did not change the staff’s
Amendment Nos.: 251, 250.
original proposed no significant hazards
Renewed Facility Operating License
consideration determination. The
Nos. DPR–32 and DPR–37: Amendments
Commission’s related evaluation of the
changed the licenses and the technical
amendments is contained in a Safety
specifications.
Evaluation dated April 2, 2007.
Date of initial notice in Federal
No significant hazards consideration
Register: August 15, 2006 (71 FR
comments received: No.
46941). The supplement dated January
Dated at Rockville, Maryland, this 16th day
19, 2007, provided additional
of April 2007.
information that clarified the
For the Nuclear Regulatory Commission.
application, did not expand the scope of
Catherine Haney,
the application as originally noticed,
and did not change the staff’s original
Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
proposed no significant hazards
Regulation.
consideration determination. The
[FR Doc. E7–7534 Filed 4–23–07; 8:45 am]
Commission’s related evaluation of the
amendments is contained in a Safety
BILLING CODE 7590–01–P
Evaluation dated March 29, 2007.
No significant hazards consideration
comments received: No.
OFFICE OF THE UNITED STATES
Virginia Electric and Power Company, et TRADE REPRESENTATIVE
al., Docket Nos. 50–280 and 50–281,
Notice of Cancellation of Public
Surry Power Station, Units 1 and 2,
Hearing on Potential Withdrawal of
Surry County, Virginia
Tariff Concessions and Increase in
Date of application for amendments:
Applied Duties in Response to
July 5, 2006, as supplemented on
European Union (EU) Enlargement
September 21 and November 20, 2006.
AGENCY: Office of the United States
Brief Description of amendments:
Trade Representative.
These amendments revised the main
control room (MCR) and emergency
ACTION: Notice of cancellation of April
switchgear room (ESGR) air24, 2007 public hearing concerning a
conditioning system (ACS) Technical
list of goods for which tariff concessions
Specifications to reflect the completion
may be withdrawn and duties may be
jlentini on PROD1PC65 with NOTICES
Operating License and Technical
Specifications.
Date of initial notice in Federal
Register: January 16, 2007 (72 FR
1781).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 2, 2007.
No significant hazards consideration
comments received: No.
VerDate Aug<31>2005
18:32 Apr 23, 2007
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20389
increased in the event the United States
cannot reach agreement with the
European Communities (EC) for
adequate compensation owed under
World Trade Organization (WTO) rules
as a result of EU enlargement.
SUMMARY: On March 22, 2007, USTR
published FR Doc E7–5268 (Vol. 72, No.
55) announcing that the Trade Policy
Staff Committee (TPSC) was seeking
public comment on a list of goods for
which U.S. tariff concessions may be
withdrawn and applied duties may be
raised and announcing that the TPSC
will hold a public hearing on Tuesday,
April 24, 2007, on the list. All
respondents to this notice have chosen
to submit their comments in writing
only and there were no requests to
testify. Therefore, the April 24 public
hearing will be cancelled.
The United States is continuing to
negotiate with the EU regarding the EU’s
provision of adequate and permanent
compensation to the United States for
an event that increased duties on U.S.
imports to EU markets above WTO
bound rates of duty. On January 1, 2007,
as part of its enlargement process, the
EU raised tariffs above bound rates on
some imports into the countries of
Romania and Bulgaria. If this issue is
not resolved, the United States may seek
to exercise its rights under Article
XXVIII of the General Agreement on
Tariffs and Trade 1994 (‘‘GATT 1994’’)
to withdraw substantially equivalent
concessions and raise tariffs on select
goods primarily supplied by the EU.
FOR FURTHER INFORMATION CONTACT:
Questions should be directed to: Laurie
Molnar, Director for European Trade
Issues, (202) 395–3320; Office of the
United States Trade Representative.
Carmen Suro-Bredie,
Chairman, Trade Policy Staff Committee.
[FR Doc. E7–7809 Filed 4–23–07; 8:45 am]
BILLING CODE 3190–W7–P
POSTAL SERVICE
Philadelphia, PA 30th Street Post
Office Property Disposition
Postal Service.
Notice.
AGENCY:
ACTION:
SUMMARY: Notice is hereby given of the
disposition of Postal Service(tm)
property, the 30th Street Main Post
Office located in Philadelphia, PA.
DATES: Comments must be submitted on
or before April 30, 2007.
ADDRESSES: Comments may be mailed to
Dallan Wordekemper, Postal Service,
Federal Preservation Officer, 4301
E:\FR\FM\24APN1.SGM
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Agencies
[Federal Register Volume 72, Number 78 (Tuesday, April 24, 2007)]
[Notices]
[Pages 20375-20389]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: E7-7534]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from March 30, 2007 to April 12, 2007. The last
biweekly notice was published on April 10, 2007 (72 FR 17944).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
Involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
[[Page 20376]]
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rulemaking,
Directives and Editing Branch, Division of Administrative Services,
Office of Administration, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, and should cite the publication date and
page number of this Federal Register notice. Written comments may also
be delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike,
Rockville, Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received may be examined at the Commission's
Public Document Room (PDR), located at One White Flint North, Public
File Area O1F21, 11555 Rockville Pike (first floor), Rockville,
Maryland. The filing of requests for a hearing and petitions for leave
to intervene is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland, 20852, Attention: Rulemaking and
Adjudications Staff; (3) e-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
[[Page 20377]]
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket No. 50-289, Three Mile Island
Nuclear Station, Unit 1 (TMI-1), Dauphin County, Pennsylvania
Date of amendment request: March 22, 2007.
Description of amendment request: The proposed amendment would
revise the Technical Specifications to incorporate a revised limit for
the variable low reactor coolant system pressure-temperature core
protection safety limit. The revised limit is associated with the
introduction of AREVA NP's Mark-B-HTP fuel design, which will require
more restrictive Safety Limits and more restrictive Limiting Safety
System Settings for the Reactor Protection System. The proposed limits
are developed in accordance with the method described in the Nuclear
Regulatory Commission (NRC)-approved Topical Report BAW-10179P-A,
``Safety Criteria and Methodology for Acceptable Cycle Reload
Analyses.'' The revised limits will maintain the same magnitude of
departure from nucleate boiling (DNB) protection.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed Technical Specification (TS) limits and reactor
protection system (RPS) trip setpoints are developed in accordance
with the methods and assumptions described in NRC-approved AREVA NP
Topical Reports BAW-10179 P-A, ``Safety Criteria and Methodology for
Acceptable Cycle Reload Analyses'' and BAW-10187 P-A, ``Statistical
Core Design for B&W-Designed 177 FA Plants.'' The core thermal-
hydraulic code (LYNXT) and CHF correlation (BHTP) have been approved
for use with these methods and the Mark-B-HTP fuel type. The
proposed change preserves the design DNB Ratio safety criterion that
there shall be at least a 95% [percent] probability at a 95%
confidence level that the hot fuel rod in the core does not
experience a departure from nucleate boiling during normal operation
or events of moderate frequency. The corresponding core-wide
protection on a pin-by-pin basis is greater than 99.9%. The margin
retained for penalties such as transition core effects, by imposing
a Thermal Design Limit in all DNB analyses supporting the proposed
change, has been shown to be sufficient to offset the mixed core
conditions at TMI Unit 1, where the Mark-B-HTP fuel design will be
co-resident with earlier Mark-B fuel designs. The setpoint
calculation methodology utilized, and the surveillance requirements
established, are in accordance with approved industry standards and
NRC criteria.
The proposed setpoint change does not involve a significant
increase in the consequences of an accident previously evaluated
because the proposed change does not alter any assumptions
previously made in the radiological consequence evaluations, or
affect mitigation of the radiological consequences of an accident
previously evaluated.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed TS limit and reactor protection system (RPS) trip
setpoint provide a core protection safety limit and variable low
pressure trip setpoint developed in accordance with NRC-approved
methods and assumptions. No new accident scenarios, failure
mechanisms or single failures are introduced as a result of the
proposed change. All systems, structures, and components previously
required for the mitigation of an event remain capable of fulfilling
their intended design function.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed RPS trip setpoint ensures core protection safety
limits will be preserved during power operation. The proposed safety
limit and setpoint are developed in accordance with NRC-approved
methods and assumptions. The margin retained for penalties such as
transition core effects, by imposing a Thermal Design Limit in all
DNB analyses supporting the proposed change, has been shown to be
sufficient to offset the mixed core conditions at TMI Unit 1. The
setpoint calculation methodology utilized, and the surveillance
requirements established, are in accordance with approved industry
standards and NRC criteria.
Therefore, the proposed changes do not involve a significant
reduction in any margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. Brad Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200 Exelon Way, Kennett Square, PA
19348.
NRC Branch Chief: Harold K. Chernoff.
Calvert Cliffs Nuclear Power Plant, Inc., Docket No. 50-317, Calvert
Cliffs Nuclear Power Plant, Unit No. 1, Calvert County, Maryland
Date of amendment request: February 27, 2007.
Description of amendment request: The proposed license amendment
would revise Technical Specification 4.2.1, Fuel Assemblies, to add a
temporary exemption to allow the insertion of up to four lead fuel
assemblies, which contain non-Zircaloy based cladding, into the Unit 1
core for one cycle of operation. These lead fuel assemblies are
currently installed in the Unit 2 core under a previous exemption and
are scheduled to be discharged during the 2007 refueling outage.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below. The licensee has determined
that the proposed change:
1. Would not involve a significant increase in the probability
or consequences of an accident previously evaluated.
[[Page 20378]]
Calvert Cliffs Technical Specification 4.2.1, Fuel Assemblies,
states that fuel rods are clad with either Zircaloy or
ZIRLOTM. Calvert Cliffs Nuclear Power Plant, Inc.
proposes to re-insert up to four fuel assemblies into Calvert Cliffs
Unit 1 that have some fuel rods clad in zirconium alloys that do not
meet the definition of Zircaloy or ZIRLOTM. A temporary
exemption to the regulations has been requested to allow these fuel
assemblies to be re-inserted into Unit 1. The proposed change to the
Calvert Cliffs Technical Specifications will allow the use of
cladding materials that are not Zircaloy or ZIRLOTM for
one fuel cycle once the temporary exemption is approved. The
proposed change to the Technical Specification is effective only as
long as the temporary exemption is effective. The addition of what
will be an approved temporary exemption for Unit 1 to Technical
Specification 4.2.1 does not change the probability or consequences
of an accident previously evaluated.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Would not create the possibility of a new or different [kind]
of accident from any accident previously evaluated.
The proposed change does not add any new equipment, modify any
interfaces with existing equipment, change the equipment's function,
or change the method of operating the equipment. The proposed change
does not affect normal plant operations or configuration. Since the
proposed change does not change the design, configuration, or
operation, it could not become an accident initiator.
Therefore, the proposed change does not create the possibility
of a new or different [kind] of accident from any accident
previously evaluated.
3. Would not involve a significant reduction in [a] margin of
safety.
The proposed change will add an approved temporary exemption to
the Calvert Cliffs Technical Specifications allowing the
installation of up to four lead fuel assemblies. The assemblies use
advanced cladding materials that are not specifically permitted by
existing regulations or Calvert Cliffs' Technical Specifications. A
temporary exemption to allow the installation of these assemblies
has been requested. The addition of an approved temporary exemption
to Technical Specification 4.2.1 is an administrative change to
allow the installation of the lead fuel assemblies under the
provisions of the temporary exemption. The license amendment is
effective only as long as the exemption is effective. This amendment
does not change the margin of safety since it only adds a reference
to an approved, temporary exemption to the Technical Specifications.
Therefore, the proposed change does not involve a significant
reduction in [a] margin of safety.
The Nuclear Regulatory Commission (NRC) staff has reviewed the
licensee's analysis and, based on this review, it appears that the
three standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC
staff proposes to determine that the amendment request involves no
significant hazards consideration.
Attorney for licensee: Carey Fleming, Esquire, Senior Counsel--
Nuclear Generation, Constellation Generation Group, LLC, 750 East Pratt
Street, 17th floor, Baltimore, MD 21202.
NRC Acting Branch Chief: John P. Boska.
Calvert Cliffs Nuclear Power Plant, Inc., Docket Nos. 50-317 and 50-
318, Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert
County, Maryland
Date of amendment request: February 27, 2007.
Description of amendment request: The proposed license amendment
would revise Technical Specification 5.6.5, Core Operating Limits
Report (COLR), to add the supporting topical report (WCAP-15604-NP,
Revision 2-A, ``Limited Scope High Burnup Lead Test Assemblies,''
September 2003) to the list of references. The topical report provides
guidance for operation with a limited number of lead fuel assemblies to
be irradiated to a higher burnup limit than currently allowed for
Calvert Cliffs fuel assemblies.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below. The licensee has determined
that the proposed change:
1. Would not involve a significant increase in the probability
or consequences of an accident previously evaluated.
The proposed change would modify the Calvert Cliffs Units 1 and
2 Technical Specification 5.6.5.b, Core Operating Limits Report by
adding an approved topical report to the existing list of topical
reports. The topical report provides the technical basis that
supports irradiating a limited number of lead fuel assemblies to a
higher burnup limit than currently approved for Calvert Cliffs. The
proposed change is administrative in nature and has no impact on any
plant configurations or on system performance that is relied upon to
mitigate the consequences of an accident.
In the safety evaluation report approving the requested topical
report (WCAP-15604-NP, Revision 2-A), the Nuclear Regulatory
Commission concluded that it is acceptable for an individual power
licensee to irradiate a limited number of lead fuel assemblies to a
maximum burnup to 75 GWD/MTU [gigawatt days per metric ton of
uranium] provided that certain conditions are met. Calvert Cliffs
meets those required conditions. Because those required conditions
are met and only a limited number of fuel assemblies are included in
this change, the probability or consequences of an accident
previously evaluated are not significantly increased.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Would not create the possibility of a new or different [kind]
of accident from any accident previously evaluated.
The proposed change does not add any new equipment, modify any
interfaces with existing equipment, change the equipment's function,
or change the method of operating the equipment. The proposed change
does not affect normal plant operations or configuration. Since the
proposed change does not change the plant design, operation, or
configuration, it could not become an accident initiator.
Therefore, the proposed change does not create the possibility
of a new or different [kind] of accident from any accident
previously evaluated.
3. Would not involve a significant reduction in a margin of
safety.
The proposed change will add a reference to an approved topical
report to allow a limited number of lead fuel assemblies to be
irradiated to a higher burnup level than is currently allowed at
Calvert Cliffs. The higher burnup limit has been evaluated and
approved in the topical report being referenced. Calvert Cliffs
conforms to the requirements of the topical report. The addition of
an approved reference to the Technical Specifications is
administrative in nature and has no impact on the margin of safety
for any plant configuration or on system performance that is relied
upon to mitigate the consequences on an accident.
Therefore, the proposed change does not involve a significant
reduction in [a] margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Carey Fleming, Esquire, Senior Counsel--
Nuclear Generation, Constellation Generation Group, LLC, 750 East Pratt
Street, 17th floor, Baltimore, MD 21202.
NRC Acting Branch Chief: John P. Boska.
Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam
Electric Plant, Unit No. 2, Darlington County, South Carolina
Date of amendment request: February 2, 2007.
Description of amendment request: The proposed amendment deletes
requirements from the Technical Specifications (TS) to maintain
hydrogen recombiners and hydrogen monitors. Licensees were generally
required to implement upgrades as described in NUREG-0737,
``Clarification of Three Mile Island
[[Page 20379]]
(TMI) Action Plan Requirements,'' and Regulatory Guide (RG) 1.97,
``Instrumentation for Light-Water-Cooled Nuclear Power Plants to Assess
Plant and Environs Conditions During and Following an Accident.''
Implementation of these upgrades was an outcome of the lessons learned
from the accident that occurred at TMI, Unit 2. Requirements related to
combustible gas control were imposed by Order for many facilities and
were added to or included in the TS for nuclear power reactors
currently licensed to operate. The revised Title 10 of the Code of
Federal Regulations (10 CFR) 50.44, ``Standards for Combustible Gas
Control System in Light-Water-Cooled Power Reactors,'' eliminated the
requirements for hydrogen recombiners and relaxed safety
classifications and licensee commitments to certain design and
qualification criteria for hydrogen and oxygen monitors.
The NRC staff published a notice of opportunity for comment in the
Federal Register on August 2, 2002 (67 FR 50374), on possible
amendments to eliminate requirements regarding containment hydrogen
recombiners and the removal of requirements from TS for containment
hydrogen and oxygen monitors, including a model safety evaluation and
model No Significant Hazards Consideration (NSHC) Determination, in
accordance with the Consolidated Line Item Improvement Process. The NRC
staff subsequently issued a notice of availability of the models for
referencing in license amendment applications in the Federal Register
on September 25, 2003 (68 FR 55416). The licensee affirmed the
applicability of the model NSHC determination in its application dated
February 2, 2007.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
Criterion 1: The Proposed Change Does Not Involve a Significant
Increase in the Probability or Consequences of an Accident
Previously Evaluated.
The revised 10 CFR 50.44 no longer defines a design-basis loss-
of-coolant accident (LOCA) hydrogen release, and eliminates
requirements for hydrogen control systems to mitigate such a
release. The installation of hydrogen recombiners and/or vent and
purge systems required by 10 CFR 50.44(b)(3) was intended to address
the limited quantity and rate of hydrogen generation that was
postulated from a design-basis LOCA. The Commission has found that
this hydrogen release is not risk-significant because the design-
basis LOCA hydrogen release does not contribute to the conditional
probability of a large release up to approximately 24 hours after
the onset of core damage. In addition, these systems were
ineffective at mitigating hydrogen releases from risk-significant
accident sequences that could threaten containment integrity.
With the elimination of the design-basis LOCA hydrogen release,
hydrogen monitors are no longer required to mitigate design-basis
accidents and, therefore, the hydrogen monitors do not meet the
definition of a safety-related component as defined in 10 CFR 50.2.
RG 1.97 Category 1, is intended for key variables that most directly
indicate the accomplishment of a safety function for design-basis
accident events. The hydrogen monitors no longer meet the definition
of Category 1 in RG 1.97. As part of the rulemaking to revise 10 CFR
50.44 the Commission found that Category 3, as defined in RG 1.97,
is an appropriate categorization for the hydrogen monitors because
the monitors are required to diagnose the course of beyond design-
basis accidents.
The regulatory requirements for the hydrogen monitors can be
relaxed without degrading the plant emergency response. The
emergency response, in this sense, refers to the methodologies used
in ascertaining the condition of the reactor core, mitigating the
consequences of an accident, assessing and projecting offsite
releases of radioactivity, and establishing protective action
recommendations to be communicated to offsite authorities.
Classification of the hydrogen monitors as Category 3 and removal of
the hydrogen monitors from TS will not prevent an accident
management strategy through the use of the severe accident
management guidelines, the emergency plan, the emergency operating
procedures, and site survey monitoring that support modification of
emergency plan protective action recommendations.
Therefore, the elimination of the hydrogen recombiner
requirements and relaxation of the hydrogen monitor requirements,
including removal of these requirements from TS, does not involve a
significant increase in the probability or the consequences of any
accident previously evaluated.
Criteria 2: The Proposed Change Does Not Create the Possibility
of a New or Different Kind of Accident From Any Previously
Evaluated.
The elimination of the hydrogen recombiner requirements and
relaxation of the hydrogen monitor requirements, including removal
of these requirements from TS, will not result in any failure mode
not previously analyzed. The hydrogen recombiner and hydrogen
monitor equipment was intended to mitigate a design-basis hydrogen
release. The hydrogen recombiner and hydrogen monitor equipment are
not considered accident precursors, nor does their existence or
elimination have any adverse impact on the pre-accident state of the
reactor core or post accident confinement of radionuclides within
the containment building.
Therefore, this change does not create the possibility of a new
or different kind of accident from any previously evaluated.
Criterion 3: The Proposed Change Does Not Involve a Significant
Reduction in the Margin of Safety.
The elimination of the hydrogen recombiner requirements and
relaxation of the hydrogen monitor requirements, including removal
of these requirements from TS, in light of existing plant equipment,
instrumentation, procedures, and programs that provide effective
mitigation of and recovery from reactor accidents, results in a
neutral impact to the margin of safety.
The installation of hydrogen recombiners and/or vent and purge
systems required by 10 CFR 50.44(b)(3) was intended to address the
limited quantity and rate of hydrogen generation that was postulated
from a design-basis LOCA. The Commission has found that this
hydrogen release is not risk-significant because the design-basis
LOCA hydrogen release does not contribute to the conditional
probability of a large release up to approximately 24 hours after
the onset of core damage.
Category 3 hydrogen monitors are adequate to provide rapid
assessment of current reactor core conditions and the direction of
degradation while effectively responding to the event in order to
mitigate the consequences of the accident. The intent of the
requirements established as a result of the TMI, Unit 2 accident can
be adequately met without reliance on safety-related hydrogen
monitors.
Therefore, this change does not involve a significant reduction
in the margin of safety. Removal of hydrogen monitoring from TS will
not result in a significant reduction in their functionality,
reliability, and availability.
The NRC staff proposes to determine that the amendment request
involves no significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Branch Chief: Thomas H. Boyce.
Detroit Edison Company, Docket No. 50-341, Fermi 2, Monroe County,
Michigan
Date of amendment request: March 19, 2007.
Description of amendment request: The proposed amendment would
revise the Technical Specifications (TS) 3.8.1 entitled ``AC Sources-
Operating'' to change the minimum Emergency Diesel Generator (EDG)
output voltage acceptance criterion from 3740 to 3873 volts.
Specifically, the proposed change would revise the Surveillance
Requirements (SRs) 3.8.1.2, 3.8.1.7, 3.8.1.10, 3.8.1.11, 3.8.1.14, and
3.8.1.17.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
[[Page 20380]]
1. The proposed change does not involve a significant increase
in the probability or consequences of any accident previously
evaluated.
The increase in the minimum EDG output voltage acceptance
criterion value in TS 3.8.1 surveillance requirements does not
adversely affect any of the parameters in the accident analyses. The
change increases the minimum allowed EDG output voltage acceptance
criterion to ensure that sufficient voltage is available to operate
the required Emergency Safety Feature (ESF) equipment under accident
conditions. The increase in the minimum allowed EDG output voltage
in the TS surveillance requirements ensures that adequate voltage is
available to support the assumptions made in the Design Bases
Accident (DBA) analyses. DBA analyses assume that onsite standby
emergency power will provide an adequate power source to operate
safe shutdown equipment and to mitigate consequences of design bases
accidents. This conservative change of the acceptance criterion
enhances the testing requirements of the onsite emergency diesel
generators and ensures the reliability of this power source.
Changing the acceptance criterion does not affect the probability of
evaluated accidents and it provides better assurance of EDG
reliability in mitigating consequences of accidents. Therefore, the
proposed change does not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. The proposed change does not create the possibility of a new
or different kind of accident from an accident previously evaluated.
The change in the value of the minimum EDG output voltage
acceptance criterion supports the assumptions in the accident
analyses that sufficient voltage will be available to operate ESF
equipment on the Class 1E buses when these buses are powered from
the onsite emergency diesel generators. The maximum EDG output
voltage of 4580 volts is not affected by this change. The change in
the minimum EDG output voltage from 3740 to 3873 volts ensures the
reliability of the onsite emergency power source. Therefore, the
proposed change will not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3. The proposed change does not involve a significant reduction
in a margin of safety.
This proposed license amendment involves a change in the minimum
EDG output voltage acceptance criterion in TS 3.8.1 surveillance
requirements. The surveillance frequency and the different test
requirements are unchanged. The change provides a better assurance
that the onsite power source is able to satisfy the design
requirements assumed in the accident analyses to safely shutdown the
reactor and mitigate the consequences of design bases accidents.
Therefore, the proposed change will not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David G. Pettinari, Legal Department, 688
WCB, Detroit Edison Company, 2000 2nd Avenue, Detroit, Michigan 48226-
1279.
NRC Branch Chief: L. Raghavan.
Dominion Nuclear Connecticut, Inc., Docket No. 50-336, Millstone Power
Station, Unit No. 2, New London County, Connecticut
Date of amendment request: November 8, 2006.
Description of amendment request: The proposed amendment would
modify the Technical Specification (TS) Action and Surveillance
Requirements (SRs) for instrumentation identified in TSs 3.3.1 and
3.3.2. In particular, the proposed amendment adds actions to address
the inoperability of one or more automatic bypass removal channels;
revises the terminology used in the notation of TS Tables 2.2-1 and
3.3-1 relative to the implementation and automatic removal of certain
Reactor Protection System (RPS) trip bypasses; revises the frequency
for performing surveillance of the automatic bypass removal function
logic; and incorporates two administrative changes.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
Criterion 1: Does the proposed amendment involve a significant
increase in the probability or consequences of an accident
previously evaluated?
Response: No.
The proposed changes to Technical Specifications 2.2.1, 3.3.1
and 3.3.2 do not adversely impact structure, system, or component
design or operation in a manner that would result in a change in the
frequency of occurrence of accident initiation. The proposed
technical specification changes do not involve accident initiators,
do not change the configuration or method of operation of any plant
equipment that is used to mitigate the consequences of an accident,
and do not alter any conditions assumed in the plant accident
analyses. The proposed amendment does not change the function or the
manner of operation of the RPS or ESFAS [engineered safety features
actuation system] trip bypass features. Adding actions to be taken
for an inoperable automatic bypass removal function places
additional restriction on plant operation in this condition and does
not alter the setpoint or the logic of the operating bypasses and
automatic bypass removals. Clarifying the frequency of the SR
associated with testing the automatic bypass removal function does
not alter the setpoint or the manner of operation of the operating
bypasses and automatic bypass removals. More accurately reflecting
the input process variable of the operating bypasses and automatic
bypass removals of the affected reactor trips does not alter the
setpoint nor the manner of operation of the operating bypasses and
automatic bypass removals. With respect to the incorporation of the
administrative changes, the proposed changes are spelling
corrections and do not alter any of the requirements of the affected
TS. Therefore, this change does not impact the consequences of any
accident. Based on this discussion, the proposed amendment does not
increase the probability or consequence of an accident previously
evaluated.
Criterion 2: Does the proposed amendment create the possibility
of a new or different kind of accident from any accident previously
evaluated?
Response: No.
No new or different accidents result from clarifying actions for
an inoperable automatic bypass removal function, clarifying
surveillance requirements for the automatic bypass removal function,
and more accurately reflecting the parameter being measured for
automatic bypass removal by referring to logarithmic power, the
input process variable. The results of previously performed accident
analyses remain valid. The proposed amendment does not introduce
accident initiators or malfunctions that would cause a new or
different kind of accident. The proposed amendments are
administrative in nature and will not change the physical plant or
the modes of plant operation defined in the facility operating
license. The changes do not involve the addition or modification of
equipment nor do they alter the design or operation of plant
systems. Therefore, the proposed amendment does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
Criterion 3: Does the proposed amendment involve a significant
reduction in a margin of safety?
Response: No.
The proposed change does not alter the function or manner of
operation of the operating bypasses and automatic bypass removals of
the affected reactor trips. The proposed changes do not affect any
of the assumptions used in the accident analysis, nor do they affect
any operability requirements for equipment important to plant
safety. Therefore, the proposed amendment does not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Lillian M. Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc., Rope Ferry Road, Waterford, CT
06385.
[[Page 20381]]
NRC Branch Chief: Harold K. Chernoff.
Entergy Nuclear Operations, Inc., Docket No. 50-293, Pilgrim Nuclear
Power Station, Plymouth County, Massachusetts
Date of amendment request: January 4, 2007.
Description of amendment request: The proposed amendment would
revise the Technical Specification for Limiting Conditions for
Operation (LCOs) and Surveillance Requirements (SRs) for control rod
operability, scram insertion times, and control rod accumulators. Basis
for proposed no significant hazards consideration determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes extend the frequency and revise the
methodology for testing control rod scram times, and identify a new
category of ``slow'' control rods for assessing control rod
operability. The frequency of control rod scram testing is not an
initiator of any accident previously evaluated. The frequency of
surveillance testing does not affect the ability to mitigate any
accident previously evaluated, because the tested component is still
required to be operable. The proposed test methodology is consistent
with industry approved methods and ensures control rod operability
requirements for the number and distribution of operable, slow, and
stuck control rods continue to satisfy scram reactivity rate
assumptions used in plant safety analysis.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes do not involve any physical alteration of
the plant (no new or different type of equipment is being installed)
and do not involve a change in the design, normal configuration, or
basic operation of the plant. The proposed changes do not introduce
any new accident initiators. The proposed changes do not involve
significant changes in the fundamental methods governing normal
plant operation and do not require unusual or uncommon operator
actions. The proposed changes provide assurance that the plant will
not be operated in a mode or condition that violates the assumptions
or initial conditions in the safety analyses and that SSCs
[structures, systems, and components] remain capable of performing
their intended safety functions as assumed in the same analyses.
Consequently, the response of the plant and the plant operator to
postulated events will not be significantly different.
Therefore, the proposed TS change does create the possibility of
a new or different kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
Margin of safety is related to confidence in the ability of the
fission product barriers to perform their design functions during
and following an accident situation. The proposed changes address
control rod scram test performance and acceptance criteria as well
as control rod operability requirements. The scam test acceptance
criteria and control rod operability restrictions are based on
industry approved methodology and will continue to ensure control
rod scram design functions and reactivity insertion assumptions used
in safety analyses continue to be protected. The proposed changes
also extend the frequency of testing control rod scram times while
at-power from 120 days to 200 days. The proposed change ensures
scram testing is performed and that test results verify acceptable
operation of the control rods.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.929(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Travis C. McCullough, Assistant General
Counsel, Entergy Nuclear Operations, Inc., 400 Hamilton Avenue, White
Plains, NY 10601.
Branch Chief: John P. Boska (Acting).
Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit
No. 2 (ANO-2), Pope County, Arkansas
Date of amendment request: March 15, 2007.
Description of amendment request: The proposed amendment would
revise containment systems surveillance requirements for Technical
Specification (TS) 3/4.6.2, ``Depressurization, Cooling, and pH Control
Systems.'' The proposed amendment would revise the frequency for ANO-2
TS Surveillance Requirement 4.6.2.1.d to require verification that
spray nozzels are unobstructed following maintenance that could result
in a nozzel blockage (loss of foreign material exclusion control)
rather than performing an air or smoke flow test through each spray
header every 5 years.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do[es] the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The Containment Spray System (CSS) is not an initiator of any
analyzed event. The proposed change does not have a detrimental
impact on the integrity of any plant structure, system, or component
that may initiate an analyzed event. The proposed change will not
alter the operation or otherwise increase the failure probability of
any plant equipment that can initiate an analyzed accident. This
change does not affect the plant design. There is no increase in the
likelihood of formation of significant corrosion products. Due to
their location at the top of the containment, introduction of
foreign material into the spray headers is unlikely. Foreign
materials exclusion controls during and following maintenance
provides assurance that the nozzles remain unobstructed.
Consequently, there is no significant increase in the probability of
an accident previously evaluated.
The CSS is designed to address the consequences of a Loss of
Coolant Accident (LOCA) or a Main Steam Line Break (MSLB). The
Containment Spray System is capable of performing its function
effectively with the single failure of any active component in the
system, any of its subsystems, or any of its support systems.
Therefore, the consequences of an accident previously evaluated are
not significantly affected by the proposed change.
2. Do[es] the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change will not physically alter the plant (no new
or different type of equipment will be installed) or change the
methods governing normal plant operation.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Do[es] the proposed change involve a significant reduction in
a margin of safety?
Response: No.
The system is not susceptible to corrosion-induced obstruction
or obstruction from sources external to the system. Strict controls
are established to ensure the foreign material is not introduced
into the CSS during maintenance or repairs. Maintenance activities
that could introduce significant foreign material into the system
require subsequent system cleanliness verification which would
prevent nozzle blockage. The spray header nozzles are expected to
remain unblocked and available in the event that the safety function
is required. The capacity of the system would remain unaffected.
Therefore, the proposed change does not involve a reduction in a
margin of safety.
[[Page 20382]]
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Terence A. Burke, Associate General
Council--Nuclear Entergy Services, Inc., 1340 Echelon Parkway, Jackson,
Mississippi 39213.
NRC Branch Chief: Thomas G. Hiltz.
Entergy Operations, Inc., System Energy Resources, Inc., South
Mississippi Electric Power Association, and Entergy Mississippi, Inc.,
Docket No. 50-416, Grand Gulf Nuclear Station, Unit 1, Claiborne
County, Mississippi
Date of amendment request: March 1, 2007.
Description of amendment request: The proposed change would revise
the Grand Gulf Nuclear Station, Unit 1 (GGNS) Technical Specifications
(TS) to add a note to the Required Actions of TS 3.6.1.3, ``Primary
Containment Isolation Valves (PCIVs),'' Actions A.1 and B.1. GGNS TS
3.6.1.3 requires specific actions to be taken for inoperable PCIVs. The
TS Required Actions include isolating the affected penetration by use
of a closed and deactivated automatic valve, closed manual valve, blind
flange, or check valve with flow through the valve secured. The new
note would allow a relief valve to be used without being deactivated,
to comply with TS 3.6.1.3, Actions A.1 and B.1, provided it has a
relief setpoint of at least 1.5 times containment design pressure
(i.e., at least 23 pounds per square inch gauge) and meets one of the
following criteria:
1. The relief valve is 1-inch nominal size or less, or
2. The flow path is into a closed system whose piping pressure
rating exceeds the containment design pressure rating.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
Primary Containment Isolation Valves (PCIVs) are accident
mitigating features designed to limit releases from the containment
following an accident. The TS specify actions to be taken to
preserve the containment isolation function if a PClV is inoperable.
These actions include isolating the penetration flow path by
specific methods including, closed and de-activated automatic
valves, closed manual valves, blind flanges, and check valves with
flow through the valve secured. The current TS Actions do not
specifically recognize a closed relief valve as an acceptable method
of isolating a penetration flow path. Thus, special measures may
need to be taken to comply with the TS Required Actions, such as
replacing the relief valve with a blind flange or de-activating the
relief valve by installing a gag. While such actions may provide
additional assurance of preserving the containment isolation
function, it may also have adverse safety affects such as disabling
the overpressure protective safety feature, causing additional
safety system unavailability time, and increasing occupational dose.
The proposed change would allow certain relief valves to be used
for isolating the penetration flow path without being de-activated.
The proposed TS changes do not alter the design, operation, or
capability of PCIVs. Relief valves are designed to be normally
closed to preserve the piping boundary integrity yet automatically
open on an abnormal process pressure to protect the piping from
overpressure conditions. Relief valves may also serve as passive
containment isolation devices (i.e., they do not require mechanical
movement to perform the isolation function). The proposed TS changes
preserve both the containment isolation and piping overpressure
protection functions.
The failure of a relief valve to remain closed during or
following an accident is considered a low probability because relief
valves are passive isolation devices that do not require mechanical
movement to perform the isolation function and the relief setpoint
provides sufficient margin to preclude the potential for premature
opening due to containment post-accident pressures. Additional
criteria are established to provide defense-in-depth protection.
Relief valves that are one-inch or smaller provide an additional
physical barrier in that, even in the unlikely event that a relief
valve were to fail to remain fully closed during or following an
accident, the size restriction would limit leakage such that a large
early release would not occur. By definition, penetrations one-inch
and smaller do not contribute to large early releases. Larger relief
valves may be used as isolation devices provided that the
containment penetration flow path through the relief valve would be
contained in a closed system. In the unlikely event that a relief
valve were to fail to remain closed, the leakage would be into a
system which forms a closed loop outside primary containment and any
containment leakage would return to primary containment through this
closed loop.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change does not introduce any new modes of plant
operation or adversely affect the design function or operation of
safety features. The proposed TS change allows use of existing plant
equipment as compensatory measures to maintain the containment
isolation design intent when the normal isolation features are
inoperable. Since relief valves used for this purpose will not be
disabled by gags or blind flanges, the system piping overpressure
protection design feature will also be preserved.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The safety margin associated with this change is that associated
with preserving the containment integrity. NUREG-0800, the Standard
Review Plan, recognizes that relief valves with relief setpoints
greater than 1.5 times containment design pressure are acceptable as
containment isolation devices. Closed relief valves with relief
setpoints of this margin provide an isolation alternative that is
less susceptible to a single failure (i.e., inadvertent opening) yet
still preserves the overpressure protection that the component was
intended to provide. The failure of a relief valve to remain closed
during or following an accident is considered a low probability
because relief valves are passive isolation devices that do not
require mechanical movement to perform the isolation function and
the relief setpoint provides sufficient margin to preclude the
potential for premature opening due to containment post-accident
pressures. Defense-in-depth containment leakage protection is
provided by additional TS criteria that limit the use of relief
valves to those one-inch or less in size or those where containment
leakage would be into a closed system whose piping pressure rating
exceeds the containment design pressure rating. Relief valves that
are one-inch or smaller provide an additional physical barrier in
that, even in the unlikely event that a relief valve were to fail to
remain closed during or following an accident, the size restriction
would limit leakage such that a large early release would not occur.
In the unlikely event that a relief valve larger than one-inch were
to fail to remain closed, the leakage would be into a system which
forms a closed loop outside primary containment and any containment
leakage would return to primary containment through this closed
loop.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Terence A. Burke, Associate General
Council--
[[Page 20383]]
Nuclear Entergy Services, Inc., 1340 Echelon Parkway, Jackson,
Mississippi 39213.
NRC Branch Chief: David Terao.
FirstEnergy Nuclear Operating Company, et al., Docket Nos. 50-334 and
50-412, Beaver Valley Power Station, Unit Nos. 1 and 2 (BVPS-1 and 2),
Beaver County, Pennsylvania
Date of amendment request: February 9, 2007.
Description of amendment request: The proposed amendment would
revise the Technical Specification (TS) 3.3.2, ``Engineered Safety
Feature Actuation System Instrumentation,'' TS 3.5.2, ``Emergency Core
Cooling System--Operating,'' TS 3.6.5, ``Containment Air Temperature,''
and TS 5.5.12, ``Containment Leakage Rate Testing Program.'' The
revised TSs would be consistent with a proposed change to the
Recirculation Spray System (RSS) pump start signal due to a
modification to the containment sump screens.
The proposed amendment would also replace the use of LOCTIC with
the Modular Accident Analysis Program-Design Basis Accident (MAAP-DBA)
for calculating containment pressure, temperature, and condensation
rates for input to the SWNAUA code. The calculation methodology change
would ultimately change the aerosol removal coefficients used in dose
consequence analysis.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No. The proposed changes to the RSS pump start signal,
the upper containment temperature technical specification (TS)
limit, the peak containment internal pressure, the nomenclature for
automatic switchover to the containment sump, and the containment
sump screen visual inspection surveillance requirement do not
involve any system or component that are accident initiators. The
RSS is used for accident mitigation only. The Refueling Water
Storage Tank (RWST) level and containment pressure instrumentation
will continue to comply with all applicable regulatory requirements
and design criteria (e.g., train separation, redundancy, single
failure, etc.) following approval of the proposed changes. The
design functions performed by the RSS and the containment are not
changed by this license amendment request.
Delaying the start of the RSS pumps and the change to the upper
containment temperature affect the long-term containment pressure
and temperature profiles. The environmental qualification of safety-
related equipment inside containment will be confirmed to be
acceptable and accident mitigation systems will continue to operate
within design temperatures and pressures. Delaying the RSS pump
start reduces the emergency diesel generator loading in the early
stage of a design basis accident and maintaining the staggered
loading of the RSS pump starts avoids overloading on each emergency
diesel generator at Unit 1. Staggered loading of the emergency
diesel generator is not required for Unit 2.
The methodology change to calculate containment pressure,
temperature and condensation rates for input to the SWNAUA code will
not involve a significant increase in the probability of an accident
previously evaluated because this change in methodology does not
impact accident initiators.
The loss of coolant accident (LOCA) has been evaluated using the
guidance provided in Regulatory Guide 1.183, ``Alternative
Radiological Source Terms for Evaluating Design Basis Accidents at
Nuclear Power Reactors.'' The radiological consequences of the
remaining design basis accidents are not significantly impacted by
the proposed changes. As demonstrated by the supporting analyses,
the estimated dose consequences at the Exclusion Area Boundary
(EAB), Low Population Zone (LPZ), and control room remain within the
acceptance criteria of 10 CFR 50.67 as supplemented by Regulatory
Guide 1.183 and Standard Review Plan Section 15.0.1. In addition,
the supporting analyses also demonstrates that the dose consequences
in the Emergency Response Facility remain compliant with paragraph
IV.E.8 of Appendix E, to 10 CFR part 50, Emergency Planning and
Preparedness for Production and Utilization Facilities, regulatory
guidance provided in Supplement 1 of NUREG-0737. The revised
radiological analyses results in a slight increase in control room
and off-site doses; however, the radiological analyses and
evaluations developed in support of this application demonstrate
that the proposed changes will not impact compliance with applicable
regulatory requirements and will not involve a significant increase
in the consequences of an accident previously evaluated. The slight
increase in control room and off-site doses is more than o