Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 17944-17959 [E7-6632]
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Federal Register / Vol. 72, No. 68 / Tuesday, April 10, 2007 / Notices
Dated: April 5, 2007.
Rochelle C. Bavol,
Office of the Secretary.
[FR Doc. 07–1795 Filed 4–6–07; 11:49 am]
BILLING CODE 7590–01–P
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
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I. Background
Pursuant to section 189a. (2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued, and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from March 16,
2007 to March 29, 2007. The last
biweekly notice was published on
March 27, 2007 (72 FR 14303).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
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determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example,
in derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rulemaking,
Directives and Editing Branch, Division
of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
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for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
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which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
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petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket
No. 50–461, Clinton Power Station, Unit
No. 1, DeWitt County, Illinois
Date of amendment request:
November 13, 2006.
Description of amendment request:
The proposed amendment changes the
technical specification (TS) testing
frequency for the surveillance
requirement (SR) in TS 3.1.4, ‘‘Control
Rod Scram Times.’’ The proposed
change revises the test frequency of SR
3.1.4.2, control rod scram time testing,
from ‘‘120 days cumulative operation in
MODE 1’’ to ‘‘200 days cumulative
operation in Mode 1.’’
AmerGen has reviewed the proposed
no significant hazards consideration
determination published in the Federal
Register on August 23, 2004 (69 FR
51864), as part of the consolidated line
item improvement process (CLIIP) and
has concluded that the proposed
determination presented in the notice is
applicable to Clinton Power Station,
Unit No. 1.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
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hazards consideration is presented
below.
1. Does the change involve a significant
increase in the probability or consequences
of an accident previously evaluated?
Response: No.
The proposed change extends the
frequency for testing control rod scram time
testing from every 120 days of cumulative
Mode 1 operation to 200 days of cumulative
Mode 1 operation. The frequency of
surveillance testing is not an initiator of any
accident previously evaluated. The frequency
of surveillance testing does not affect the
ability to mitigate any accident previously
evaluated, as the tested component is still
required to be operable. Therefore, the
proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the change create the possibility of
a new or different kind of accident from any
accident previously evaluated?
Response: No.
The proposed change extends the
frequency for testing control rod scram time
testing from every 120 days of cumulative
Mode 1 operation to 200 days of cumulative
Mode 1 operation. The proposed change does
not result in any new or different modes of
plant operation. Therefore, the proposed
change does not create the possibility of a
new or different kind of accident from any
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change extends the
frequency for testing control rod scram time
testing from every 120 days of cumulative
Mode 1 operation to 200 days of cumulative
Mode 1 operation. The proposed change
continues to test the control rod scram time
to ensure the assumptions in the safety
analysis are protected. Therefore, the
proposed change does not involve a
significant reduction in a margin of safety.
Based on the above, the proposed
change presents no significant hazards
consideration under the standards set
forth in 10 CFR 50.92(c), and
accordingly, a finding of ‘‘no significant
hazards consideration’’ is justified.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Attorney for licensee: Mr. Bradley J.
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Russell Gibbs.
Detroit Edison Company, Docket No.
50–341, Fermi 2, Monroe County,
Michigan
Date of amendment request: January
26, 2007.
Description of amendment request:
The proposed amendment would revise
technical specifications (TS)
requirements for unavailable barriers by
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adding limiting condition for operation
(LCO) 3.0.9. This would establish
conditions under which TS systems
would remain operable when required
physical barriers are not capable of
providing their related support function.
Also, the proposed amendment would
make editorial changes to LCO 3.0.8 to
be consistent with the terminology in
LCO 3.0.9.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration by a reference to a generic
analysis published in the Federal
Register on October 3, 2006 (71 FR
58444), which is presented below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of any accident previously
evaluated?
Response: No.
The proposed change allows a delay time
for entering a supported system technical
specification (TS) when the inoperability is
due solely to an unavailable barrier if risk is
assessed and managed. The postulated
initiating events which may require a
functional barrier are limited to those with
low frequencies of occurrence, and the
overall TS system safety function would still
be available for the majority of anticipated
challenges. Therefore, the probability of an
accident previously evaluated is not
significantly increased, if at all. The
consequences of an accident while relying on
the allowance provided by proposed LCO
3.0.9 are no different than the consequences
of an accident while relying on the TS
required actions in effect without the
allowance provided by proposed LCO 3.0.9.
Therefore, the consequences of an accident
previously evaluated are not significantly
affected by this change. The addition of a
requirement to assess and manage the risk
introduced by this change will further
minimize possible concerns.
Therefore, this change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not involve a
physical alteration of the plant (no new or
different type of equipment will be installed).
Allowing delay times for entering supported
system TS when inoperability is due solely
to an unavailable barrier, if risk is assessed
and managed, will not introduce new failure
modes or effects and will not, in the absence
of other unrelated failures, lead to an
accident whose consequences exceed the
consequences of accidents previously
evaluated. The addition of a requirement to
assess and manage the risk introduced by this
change will further minimize possible
concerns. Thus, this change does not create
the possibility of a new or different kind of
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accident from an accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change allows a delay time
for entering a supported system TS when the
inoperability is due solely to an unavailable
barrier, if risk is assessed and managed. The
postulated initiating events which may
require a functional barrier are limited to
those with low frequencies of occurrence,
and the overall TS system safety function
would still be available for the majority of
anticipated challenges. The risk impact of the
proposed TS changes was assessed following
the three-tiered approach recommended in
RG 1.177. A bounding risk assessment was
performed to justify the proposed TS
changes. This application of LCO 3.0.9 is
predicated upon the licensee’s performance
of a risk assessment and the management of
plant risk. The net change to the margin of
safety is insignificant as indicated by the
anticipated low levels of associated risk
(ICCDP and ICLERP) as shown in Table 1 of
Section 3.1.1 in the Safety Evaluation.
Therefore, this change does not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David G.
Pettinari, Legal Department, 688 WCB,
Detroit Edison Company, 2000 2nd
Avenue, Detroit, Michigan 48226–1279.
NRC Branch Chief: L. Raghavan.
Entergy Nuclear Operations, Inc.,
Docket No. 50–286, Indian Point
Nuclear Generating Unit No. 3,
Westchester County, New York
Date of amendment request: January
18, 2007.
Description of amendment request:
The proposed amendment would revise
the expiration limit for the reactor
coolant system Pressure/Temperature
(P/T) limit graphs in Technical
Specifications (TS); revise the adjusted
reference temperature for the reactor
vessel; and revise the Low Temperature
Overpressure Protection (LTOP) arming
temperature value specified in TSs. It
would also make editorial changes in
the use of inequality signs in TSs
associated with the LTOP arming
temperature in order to make them
consistent.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
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1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No
The proposed change does not affect the
accident initiators or mitigation assumptions
associated with any of the accidents
previously evaluated. Operating restrictions
on pressure-temperature conditions for the
reactor pressure vessel provide assurance
that reactor vessel integrity will be
maintained under accident or transient
conditions. The proposed change uses
approved criteria and analysis methods to
update the time period for which the current
operating limits remain valid.
The LTOP system performs an automatic
function by opening relief valves if reactor
coolant system pressure reaches a
temperature-dependent limit. The proposed
change includes establishing a more
restrictive temperature limit for when this
system must be in service, to reflect the
material condition of the reactor vessel at the
new EFPY limit proposed for the pressuretemperature graphs. The mitigation function
and capability of the LTOP system is not
being changed by this request.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No
There are no new accident initiators being
introduced by this proposed change. The
proposed change does not involve
installation of new plant equipment,
modification of existing equipment, or
changes in the way that plant equipment is
operated. Pressure-temperature operating
limits depicted by graphs in the technical
specifications will not be changed and will
continue to be used by plant operators. A
change in the LTOP system arming
temperature will assure that the graphs
remain valid for the proposed new operating
period of 27.2 EFPY [effective full power
years].
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No
Operating limits on pressure and
temperature conditions for the reactor
coolant system (RCS) are important to assure
that the RCS pressure boundary stresses are
within analyzed limits. Margins of safety are
inherent in the analysis methods,
assumptions, and limits specified in
regulations and guidance documents. The
proposed change is based on NRC-accepted
methods, assumptions and limits and
maintains the required margin of safety.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
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review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John Fulton,
Assistant General Counsel, Entergy
Nuclear Operations, Inc., 440 Hamilton
Avenue, White Plains, NY 10601.
NRC Acting Branch Chief: Douglas V.
Pickett.
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Entergy Nuclear Operations, Inc.,
Docket Nos. 50–247 and 50–286, Indian
Point Nuclear Generating Unit Nos. 2
(IP2) and 3 (IP3), Westchester County,
New York
Date of amendment request: March
13, 2007.
Description of amendment request:
The amendment would revise License
Condition 2.K for IP2 and License
Condition 2.H for IP3, which require the
implementation and maintenance of an
approved Fire Protection Program for
each unit.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No
The proposed changes are strictly an
administrative relocation of the specific fire
protection SER [safety evaluation report]
references and do not modify any
requirements of the fire protection programs.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes are strictly an
administrative relocation of the specific fire
protection SER references and do not modify
any requirements of the fire protection
programs.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes are strictly an
administrative relocation of the specific fire
protection SER references and do not modify
any requirements of the fire protection
programs.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
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The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John Fulton,
Assistant General Counsel, Entergy
Nuclear Operations, Inc., 440 Hamilton
Avenue, White Plains, NY 10601.
NRC Acting Branch Chief: Douglas V.
Pickett.
Entergy Nuclear Operations, Inc.,
Docket No. 50–247, Indian Point
Nuclear Generating Unit No. 2,
Westchester County, New York
Date of amendment request: March
22, 2007.
Description of amendment request:
The proposed amendment will revise
the test acceptance criteria specified in
Technical Specification Surveillance
Requirement (SR) 3.8.1.10 for the diesel
generator endurance test.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
No. The proposed change revises the
acceptance criteria to be applied to an
existing surveillance test of the facility
emergency diesel generators (DGs).
Performing a surveillance test is not an
accident initiator and does not increase the
probability of an accident occurring. The
proposed new acceptance criteria will assure
that the DGs are capable of carrying the peak
electrical loading assumed in the various
existing safety analyses which take credit for
the operation of the DGs. Establishing
acceptance criteria that bound existing
analyses validates the related assumption
used in those analyses regarding the
capability of equipment to mitigate accident
conditions. Therefore the proposed change
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the change create the possibility of
a new or different kind of accident from any
accident previously evaluated?
No. The proposed change revises the test
acceptance criteria for a specific performance
test conducted on the existing DGs. The
proposed change does not involve
installation of new equipment or
modification of existing equipment, so no
new equipment failure modes are introduced.
The proposed revision to the DG surveillance
test acceptance criteria also is not a change
to the way that the equipment or facility is
operated and no new accident initiators are
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17947
created. Therefore the proposed change does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
No. The conduct of performance tests on
safety-related plant equipment is a means of
assuring that the equipment is capable of
maintaining the margin of safety established
in the safety analyses for the facility. The
proposed change in the DG technical
specification surveillance test acceptance
criteria is consistent with values assumed in
existing safety analyses and is consistent
with the design rating of the DGs. Therefore
the proposed change does not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John Fulton,
Assistant General Counsel, Entergy
Nuclear Operations, Inc., 440 Hamilton
Avenue, White Plains, NY 10601.
NRC Acting Branch Chief: Douglas V.
Pickett.
Entergy Nuclear Operations, Inc.,
Docket No. 50–333, James A. FitzPatrick
Nuclear Power Plant, Oswego County,
New York
Date of amendment request: February
15, 2007.
Description of amendment request:
The proposed changes would revise
Technical Specification (TS) 3.10.1 to
expand its scope to include provisions
for reactor coolant temperature
excursions greater than 212 °F as a
consequence of inservice leak and
hydrostatic testing, and as a
consequence of scram time testing
initiated in conjunction with an
inservice leak or hydrostatic test, while
considering operational conditions to be
in Mode 4, which is defined to be
reactor coolant temperature less than or
equal to 212 °F.
This change was proposed by the
industry’s TS Task Force (TSTF) and is
designated TSTF–484. The NRC staff
issued a notice of opportunity for
comment in the Federal Register on
August 21, 2006 (71 FR 48561), on
possible amendments concerning
TSTF–484, including a model safety
evaluation and model no significant
hazards (NSHC) determination, using
the consolidated line item improvement
process (CLIIP). The NRC staff
subsequently issued a notice of
availability of the models for referencing
in license amendment applications in
the Federal Register on October 27,
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2006 (71 FR 63050). The licensee
affirmed the applicability of the
following NSHC determination in its
application dated February 15, 2007.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
Criterion 1: The proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
Technical Specifications currently allow
for operation at greater than 212 °F while
imposing MODE 4 requirements in addition
to the secondary containment requirements
required to be met. Extending the activities
that can apply this allowance will not
adversely impact the probability or
consequences of an accident previously
evaluated. Therefore, the proposed change
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
Criterion 2: The proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
Technical Specifications currently allow
for operation at greater than 212 °F while
imposing MODE 4 requirements in addition
to the secondary containment requirements
required to be met. No new operational
conditions beyond those currently allowed
by LCO 3.10.1 are introduced. The changes
do not involve a physical alteration of the
plant (i.e., no new or different type of
equipment will be installed) or a change in
the methods governing normal plant
operation. In addition, the changes do not
impose any new or different requirements or
eliminate any existing requirements. The
changes do not alter assumptions made in the
safety analysis. The proposed changes are
consistent with the safety analysis
assumptions and current plant operating
practice. Therefore, the proposed change
does not create the possibility of a new or
different kind of accident from any accident
previously evaluated.
Criterion 3: The proposed change does not
involve a significant reduction in a margin of
safety.
Technical Specifications currently allow
for operation at greater than 212 °F while
imposing MODE 4 requirements in addition
to the secondary containment requirements
required to be met. Extending the activities
that can apply this allowance will not
adversely impact any margin of safety.
Allowing completion of inspections and
testing and supporting completion of scram
time testing initiated in conjunction with an
inservice leak or hydrostatic test prior to
power operation results in enhanced safe
operations by eliminating unnecessary
maneuvers to control reactor temperature and
pressure. Therefore, the proposed change
does not involve a significant reduction in a
margin of safety.
Based on the above, the NRC staff
concludes that the proposed change
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15:22 Apr 09, 2007
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presents no significant hazards
consideration under the standards set
forth in 10 CFR 50.92(c), and,
accordingly, a finding of no significant
hazards consideration is justified.
Attorney for licensee: Mr. John Fulton,
Assistant General Counsel, Entergy
Nuclear Operations, Inc., 440 Hamilton
Avenue, White Plains, NY 10601.
NRC Acting Branch Chief: Douglas V.
Pickett.
Exelon Generation Company, LLC
(EGC), Docket Nos. 50–373 and 50–374,
LaSalle County Station (LSCS), Units 1
and 2, LaSalle County, Illinois
Date of amendment request:
November 17, 2006.
Description of amendment request:
The proposed amendments would
replace references to Section XI of the
American Society of Mechanical
Engineers (ASME) Boiler and Pressure
Vessel Code (Code) with a reference to
the ASME Code of Operation and
Maintenance of Nuclear Power Plants
(OM Code) in Technical Specification
(TS) 5.5.7, ‘‘Inservice Testing Program
[IST].’’ These proposed changes are
consistent with the implementation of
the LSCS, Units 1 and 2 third 10-year
IST program in accordance with the
requirements of Title 10 of the Code of
Federal Regulations (10 CFR) Section
50.55a, ‘‘Codes and standards,’’
paragraph (f), ‘‘Inservice testing
requirements.’’ The third 10-year
interval for LSCS, Units 1 and 2 is
scheduled to start on October 12, 2007.
In addition to the replacement of the
references, EGC is also adding
provisions in TS 5.5.7, item b, to only
apply Surveillance Requirement (SR)
3.0.2 to those inservice testing
frequencies of two years or less. These
proposed changes are based on TS Task
Force (TSTF) Traveler No. 479–A
(TSTF–479–A), Revision 0, ‘‘Changes to
Reflect Revision of 10 CFR 50.55a,’’ as
modified by TSTF–497, Revision 0,
‘‘Limit Inservice Testing Program SR
3.0.2 Application to Frequencies of 2
Years or Less’’ and approved by the
NRC in December 6, 2005, and October
4, 2006.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the change involve a significant
increase in the probability or consequences
of an accident previously evaluated?
Response: No.
The proposed changes revise TS 5.5.7 for
LSCS Units 1 and 2 to conform to the
requirements of 10 CFR 50.55a, ‘‘Codes and
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Sfmt 4703
standards,’’ paragraph (f) regarding the
inservice testing of pumps and calves for the
Third 10-year Interval. The current TS
reference the [American Society of
Mechanical Engineers] ASME Boiler and
Pressure Vessel Code, Section XI,
requirements for the inservice testing of
ASME Code Class 1, 2, and 3 pumps and
valves. The proposed changes would
reference the ASME OM Code, which is
consistent with 10 CFR 50.55a, paragraph (f),
‘‘Inservice testing requirements,’’ and
approved for use by the NRC. In addition,
provisions modifying TS 5.5.7, item b, clarify
that SR 3.0.2 is only applied to those
inservice testing frequencies of two years or
less. The definitions of the frequencies are
not changed by this license amendment
request.
The proposed changes are administrative
in nature, do not affect any accident
initiators, do not affect the ability of LSCS to
successfully respond to previously evaluated
accidents and do not affect radiological
assumptions used in the evaluations. Thus,
the radiological consequences of any
accident previously evaluated are not
increased.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the change create the possibility of
a new or different kind of accident from any
accident previously evaluated?
Response: No.
The proposed changes revise TS 5.5.7 for
LSCS Units 1 and 2 to conform to the
requirements of 10 CFR 50.55a(f) regarding
the inservice testing of pumps and valves for
the Third 10-year Interval. The current TS
reference the ASME Boiler and Pressure
Vessel Code, Section XI, requirements for the
inservice testing of ASME Code Class 1, 2,
and 3 pumps and valves. The proposed
changes would reference the ASME OM
Code, which is consistent with the 10 CFR
50.55a(f) and approved for use by the NRC.
In addition, provisions modifying TS 5.5.7,
item b, clarify that SR 3.0.2 is only applied
to those inservice testing frequencies of two
years or less. The definitions of the
frequencies are not changed by this license
amendment request.
The proposed changes to TS Section 5.5.7
do not affect the performance of any LSCS
structure, system, or component credited
with mitigating any accident previously
evaluated and do not introduce any new
modes of system operation or failure
mechanisms.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the change involve a significant
reduction in a margin of safety?
Response: No.
The proposed changes revise TS 5.5.7 for
LSCS Units 1 and 2 to conform to the
requirements of 10 CFR 50.55a(f) regarding
the inservice testing of pumps and valves for
the Third 10-Year Interval. The current TS
reference the ASME Boiler and Pressure
Vessel Code, Section XI, requirements for the
inservice testing of ASME Code Class 1, 2,
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and 3 pumps and valves. The proposed
changes would reference the ASME OM
Code, which is consistent with the 10 CFR
50.55a(f) and approved for use by the NRC.
In addition, provisions modifying TS 5.5.7,
item b, clarify that SR 3.0.2 is only applied
to those inservice testing frequencies of two
years or less. The definitions of the
frequencies are not changed by this license
amendment request.
The proposed changes do not modify the
safety limits setpoints at which protective
actions are initiated and do not change the
requirements governing operation or
availability of safety equipment assumed to
operate to preserve the margin of safety.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Bradley J.
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Russell Gibbs.
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Exelon Generation Company, LLC,
Docket Nos. 50–352 and 50–353,
Limerick Generating Station, Units 1
and 2, Montgomery County,
Pennsylvania
Date of amendment request: June 2,
2006.
Description of amendment request:
The proposed amendments incorporates
revised 10 CFR Part 20 requirements for
Limerick Generating Station Units 1 and
2 technical specifications (TSs).
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Updating the Technical Specifications (TS)
to be consistent with 10 CFR Part 20 has no
impact on plant structures, systems, or
components, does not affect any accident
initiators, and does not change any safety
analysis. Therefore, the proposed changes do
not involve an increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
Updating the TS to be consistent with 10
CFR Part 20 will not change any equipment,
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require new equipment to be installed, or
change the way current equipment operates.
No credible new failure mechanisms,
malfunctions, or accident initiators are
created by the proposed changes.
Therefore, the changes do not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
Updating the TS to be consistent with 10
CFR Part 20 does not adversely affect existing
plant safety margins or the reliability of
equipment assumed to operate in the safety
analysis. As such, there are no changes being
made to safety analysis assumptions, safety
limits or limiting safety system settings that
would adversely affect plant safety as a result
of the proposed changes. Therefore, the
proposed changes do not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. Brad
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Harold K.
Chernoff.
FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–346,
Davis-Besse Nuclear Power Station, Unit
No. 1, Ottawa County, Ohio
Date of amendment request: February
12, 2007.
Description of amendment request:
The proposed license amendment
would revise Technical Specification
(TS) Limiting Condition for Operation
3.9.4, ‘‘Containment Penetrations’’, to
allow penetrations included under TS
3.9.4(c) to be opened during core
alterations or movement of irradiated
fuel, under administrative controls. This
change is based on the TS Task Force
Traveler No. 312–A, Revision 1.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change would allow
containment penetrations identified under
Technical Specification 3.9.4(c) to remain
open during fuel movement and core
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17949
alterations. These penetrations are normally
closed during this time period to prevent the
release of radioactive material in the event of
a Fuel Handling Accident inside
containment. These penetrations are not
initiators of any accident. The probability of
a Fuel Handling Accident is unaffected by
the status of these penetrations.
The Fuel Handling Accident analyses
demonstrate that the maximum offsite dose is
well [within] the acceptance limits specified
in SRP [Standard Review Plan] 15.7.4, and
the control room dose is within the
acceptance criteria specified in GDC [General
Design Criterion] 19. Furthermore, the
existing analysis results are independent of
the containment release path, and therefore
are unaffected by the proposed change.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not involve the
addition or modification of any plant
equipment. Also, the proposed change will
not alter the design, configuration, or method
of operation of the plant beyond the standard
functional capabilities of the equipment. The
proposed change involves a Technical
Specification change that will allow
containment penetrations identified under
Technical Specification 3.9.4(c) to remain
open during fuel movement and core
alterations. Open penetrations are not
accident initiators, and will not create the
possibility of a new kind of accident.
Administrative controls will be implemented
to ensure the capability to close the affected
containment penetrations in the event of a
Fuel Handling Accident.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed change has the potential to
slightly increase the post-Fuel Handling
Accident dose at the site boundary and in the
control room. However, the existing analyses
take no credit for containment of the release,
so that the existing analysis results will
remain bounding.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David W.
Jenkins, Attorney, FirstEnergy
Corporation, Mail Stop A–GO–18, 76
South Main Street, Akron, OH 44308.
NRC Branch Chief: Russell Gibbs.
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FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–440,
Perry Nuclear Power Plant, Unit No. 1,
Lake County, Ohio
Date of amendment request: January
19, 2007.
Description of amendment request:
The proposed amendment would
modify Technical Specification (TS)
5.5.9, ‘‘Diesel Fuel Oil Testing
Program,’’ by relocating a reference to a
specific American Society for Testing
and Materials (ASTM) international
standard for fuel oil testing to licenseecontrolled documents, and by adding an
alternate criteria to the ‘‘clear and
bright’’ acceptance test for new fuel oil,
per the consolidated line item
improvement process (CLIIP).
The U.S. Nuclear Regulatory
Commission (NRC) staff issued a notice
of opportunity for comment in the
Federal Register on February 22, 2006
(71 FR 9179), on possible amendments
concerning the CLIIP, including a model
safety evaluation and a model no
significant hazards consideration
determination. The NRC staff
subsequently issued a notice of
availability of the models for referencing
in license amendment applications in
the Federal Register on April 21, 2006
(71 FR 20735), as part of the CLIIP.
In its application dated January 19,
2007, the licensee affirmed the
applicability of the following
determination.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of any accident previously
evaluated?
Response: No.
The proposed changes relocate the specific
ASTM standard references from the
Administrative Controls Section of TS to a
licensee-controlled document. Requirements
to perform testing in accordance with
applicable ASTM standards are retained in
the TS as are requirements to perform
surveillances of both new and stored diesel
fuel oil. Future changes to the licenseecontrolled document will be evaluated
pursuant to the requirements of 10 CFR
50.59, ‘‘Changes, tests and experiments,’’ to
ensure that such changes do not result in
more than a minimal increase in the
probability or consequences of an accident
previously evaluated. In addition, the ‘‘clear
and bright’’ test used to establish the
acceptability of new fuel oil for use prior to
addition to storage tanks has been expanded
to recognize more rigorous testing of water
and sediment content. Relocating the specific
ASTM standard references from the TS to a
licensee-controlled document and allowing a
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water and sediment content test to be
performed to establish the acceptability of
new fuel oil will not affect nor degrade the
ability of the emergency diesel generators
(DGs) to perform their specified safety
function. Fuel oil quality will continue to
meet ASTM requirements.
The proposed changes do not adversely
affect accident initiators or precursors nor
alter the design assumptions, conditions, and
configuration of the facility or the manner in
which the plant is operated and maintained.
The proposed changes do not adversely affect
the ability of structures, systems, and
components (SSCs) to perform their intended
safety function to mitigate the consequences
of an initiating event within the assumed
acceptance limits. The proposed changes do
not affect the source term, containment
isolation, or radiological release assumptions
used in evaluating the radiological
consequences of any accident previously
evaluated. Further, the proposed changes do
not increase the types and amounts of
radioactive effluent that may be released
offsite, nor significantly increase individual
or cumulative occupational/public radiation
exposures.
Therefore, the changes do not involve a
significant increase in the probability or
consequences of any accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes relocate the specific
ASTM standard references from the
Administrative Controls Section of TS to a
licensee-controlled document. In addition,
the ‘‘clear and bright’’ test used to establish
the acceptability of new fuel oil for use prior
to addition to storage tanks has been
expanded to allow a water and sediment
content test to be performed to establish the
acceptability of new fuel oil. The changes do
not involve a physical alteration of the plant
(i.e., no new or different type of equipment
will be installed) or a change in the methods
governing normal plant operation. The
requirements retained in the TS continue to
require testing of the diesel fuel oil to ensure
the proper functioning of the DGs.
Therefore, the changes do not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes relocate the specific
ASTM standard references from the
Administrative Controls Section of TS to a
licensee-controlled document. Instituting the
proposed changes will continue to ensure the
use of applicable ASTM standards to
evaluate the quality of both new and stored
fuel oil designated for use in the emergency
DGs.
Changes to the licensee-controlled
document are performed in accordance with
the provisions of 10 CFR 50.59. This
approach provides an effective level of
regulatory control and ensures that diesel
fuel oil testing is conducted such that there
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is no significant reduction in a margin of
safety.
The ‘‘clear and bright’’ test used to
establish the acceptability of new fuel oil for
use prior to addition to storage tanks has
been expanded to allow a water and
sediment content test to be performed to
establish the acceptability of new fuel oil.
The margin of safety provided by the DGs is
unaffected by the proposed changes since
there continue to be TS requirements to
ensure fuel oil is of the appropriate quality
for emergency DG use. The proposed changes
provide the flexibility needed to improve fuel
oil sampling and analysis methodologies
while maintaining sufficient controls to
preserve the current margins of safety.
The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorney for licensee: David W.
Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street,
Akron, OH 44308.
NRC Branch Chief: Russell A. Gibbs
Florida Power Corporation, et al.,
Docket No. 50–302, Crystal River Unit 3
Nuclear Generating Plant (CR–3), Citrus
County, Florida
Date of amendment request:
December 14, 2006, as supplemented by
letter dated March 14, 2007.
Description of amendment request:
The proposed amendment would
modify the technical specification (TS)
requirements for inoperable snubbers by
adding Limiting Condition for
Operation (LCO) 3.0.8. The changes are
consistent with NRC approved Industry/
Technical Specification Task Force
(TSTF) standard TS change TSTF–372,
Revision 4.
The proposed amendment includes an
administrative change to LCO 3.0.1 that
will clarify that LCO 3.0.7 allows
specified TS requirements to be
suspended during physics tests
performed in accordance with TSs 3.1.8
and 3.1.9. This administrative change
will make the CR–3 TSs more consistent
with the standard TSs and with TSTF–
372, Revision 4.
The NRC staff issued a notice of
availability of a model safety evaluation
and model no significant hazards
consideration (NSHC) determination for
referencing in license amendment
applications in the Federal Register on
May 4, 2005 (70 FR 23252). The licensee
affirmed the applicability of the model
NSHC determination in its application
dated April 26, 2006.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
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1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change allows a delay time
before declaring supported TS systems
inoperable when the associated snubber(s)
cannot perform its required safety function.
Entrance into Actions or delaying entrance
into Actions is not an initiator of any
accident previously evaluated. Consequently,
the probability of an accident previously
evaluated is not significantly increased. The
consequences of an accident while relying on
the delay time allowed before declaring a TS
supported system inoperable and taking its
Conditions and Required Actions are no
different than the consequences of an
accident under the same plant conditions
while relying on the existing TS supported
system Conditions and Required Actions.
Therefore, the consequences of an accident
previously evaluated are not significantly
increased by this change. Therefore, this
change does not involve a significant
increase in the probability or consequences
of an accident previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change allows a delay time
before declaring supported TS systems
inoperable when the associated snubber(s)
cannot perform its required safety function.
The proposed change does not involve a
physical alteration of the plant (no new or
different type of equipment will be installed)
or a change in the methods governing normal
plant operations. Thus, this change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change allows a delay time
before declaring supported TS systems
inoperable when the associated snubber(s)
cannot perform its required safety function.
The proposed change restores an allowance
in the pre-ISTS [improved Standard
Technical Specifications] conversion TS that
was unintentionally eliminated by the
conversion. The pre-ISTS TSs were
considered to provide an adequate margin of
safety for plant operation, as does the postISTS conversion TS. Therefore, this change
does not involve a significant reduction in a
margin of safety.
The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Branch Chief: Thomas H. Boyce.
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PSEG Nuclear LLC, Docket Nos. 50–272
and 50–311, Salem Nuclear Generating
Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of amendment request: March
16, 2007.
Description of amendment request:
The proposed amendment would add
new Technical Specification (TS)
requirements for the response times
associated with a steam generator
feedwater pump (SGFP) trip and
feedwater isolation valve (FIV) closure.
The amendment would also revise the
TS requirements for the containment fan
cooler unit (CFCU) cooling water flow
rate. These changes are associated with
a revised containment response analysis
that credits a SGFP trip and FIV closure
(on a feedwater regulator valve failure)
to reduce the mass/energy release to the
containment during a main steam line
break (MSLB). The containment analysis
also credits a reduced heat removal
capability for the CFCUs, allowing a
reduction in the required service water
(SW) flow to the CFCUs.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated. The proposed change establishes
response time requirements for feedwater
isolation and reduced CFCU flow rates to
support containment analyses to
accommodate reduced CFCU heat removal
capacity. The changes in analysis input
assumptions affect plant response to an
accident and are not accident initiators;
therefore, they have no bearing on the
probability of an accident. The Salem FSAR
[Final Safety Analysis Report] Chapter 15
accidents which are impacted by a change in
the CFCU modeling parameters are LOCA
[loss-of-coolant accident] and MSLB mass
and energy release Containment analyses.
The consequences of these postulated
accidents are shown to be acceptable using
assumptions consistent with the proposed
changes.
For the LOCA transients, the containment
cooling systems are considered for three
aspects: core response, containment response
and dose. The core response is most limiting
when the containment conditions minimize
back pressure since this increases the
blowdown and reduces the effectiveness of
the ECCS [emergency core cooling system].
The LOCA core response (10 CFR 50.46
[Section 50.46 of Title 10 of the Code of
Federal Regulations]—PCT [peak cladding
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temperature]) is conservatively biased to
minimize the containment backpressure such
that any safety injection effectiveness is
minimized (the core becomes the highest
resistance flow path). Thus, any reduction in
the accident capability of the CFCUs has no
bearing on the LOCA core response.
The bounding containment integrity
analyses are the LBLOCA [large-break LOCA]
and the MSLB Inside Containment events.
The containment integrity analysis relies on
two heat removal paths to maintain
containment pressure and temperature
conditions. The CFCU air-to-water heat
exchangers reject containment energy to the
SW System and the Containment Spray
System removes containment energy by using
spray droplet direct contact heat exchange to
transfer the energy from the containment
ambient to the containment sump, where it
is transferred out of containment via the RHR
[residual heat removal] heat exchanger and
CCW [component cooling water]/SW
Systems. Containment integrity analyses for
both LOCA and MSLB, using input
assumptions consistent with the proposed
changes, show that containment integrity is
maintained with reduced CFCU heat removal
capacity.
The potential dose impacts due to reduced
CFCU heat removal capacity are bounded as
the design basis assumptions concerning the
number of operating CFCUs (three of five),
and the thermal-hydraulic transient
operation of the Containment Spray System
are unchanged. The Salem design basis only
credits Containment Spray iodine removal
effectiveness during the LOCA injection and
recirculation phases based on a single failure
of an entire ESF [engineered safety features]
train. This assumption results in 3 of 5
CFCUs being available to ensure adequate
mixing of the containment ambient air as
well as operation of a single Containment
Spray Train, which controls containment
spray droplet size and pH, as described in
UFSAR [updated FSAR] Section 6.2.3. As a
further conservatism, the current LOCA
Alternate Source Term (AST) analysis
(Calculation S–C–ZZ–MDC–1945, an interim
revision of which was sent to the NRC
[Nuclear Regulatory Commission] staff for
review via letter dated September 16, 2004)
only credits two CFCUs for mixing. The
Containment Building and Auxiliary
Building leakage rates are unaffected by the
revised containment analysis as the peak
containment pressure and temperatures are
less than the design basis values described in
the Salem UFSAR. Therefore, there is no
impact on offsite dose rates due to the
reduced CFCU heat removal capacity.
One other high energy line break for
consideration is the rupture of a feedwater
line break. From a containment response
aspect, this event is bounded by the MSLB
event, so it is not explicitly analyzed (or even
discussed in the Salem UFSAR).
A review of the Salem design basis for AST
dose calculations shows that the revised
Containment Integrity Analysis, WCAP–
16503, does not challenge any of the
assumptions that are part of the AST design
basis.
Section 6.2 of the UFSAR indicates that the
Appendix J Type A containment leak rate test
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pressure is based on the containment design
pressure of 47.0 psig, not the calculated
accident pressure. Since the design pressure
value bounds the peak pressure calculated in
WCAP–16503 and is not being changed, the
Appendix J testing requirements are not
impacted.
Thus, in conclusion, the proposed change
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated. The proposed change
modifies response time requirements for
feedwater isolation, and reduces CFCU flow
rates and heat removal requirements
consistent with the new containment
analysis.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated. The proposed changes support
revised containment analysis to
accommodate the reduced CFCU heat
removal capacity.
The response time-related changes impose
new surveillance acceptance criteria to
existing plant equipment that actuates to
isolate feedwater following a safety injection
signal. There is no change in actuation logic
associated with the addition of response time
criteria; therefore no new accident sequences
would result from the imposition of response
time test criteria to existing plant equipment.
The reduction in minimum service water
system flow to the CFCUs is supported by
analyses demonstrating acceptable system
performance and containment integrity
following a demand for system operation.
The post-accident conditions resulting from
the proposed reduction in flow do not
adversely impact the environmental
qualification of equipment, such that no new
consequential failures are introduced to any
design basis accident scenario. CFCU
operation with the proposed reduction in
minimum required accident flow would not
result in the progression of any design basis
event into a previously unanalyzed accident.
Therefore, no new accident scenarios are
created from the CFCU flowrate reduction.
3. Does the proposed change involve a
significant reduction in [a] margin of safety?
Response: No.
The proposed change does not involve a
significant reduction in the margin of safety.
The revised containment analyses
accommodate reduced CFCU heat removal
capacity using input assumptions consistent
with the proposed changes.
The proposed change involves the addition
of feedwater isolation response time
surveillance criteria and reduction in
minimum service water system flows to
CFCUs. These changes affect input to the
analyses of mass/energy releases and
containment response to a design basis main
steam line break or loss of coolant accident.
The analyses, consistent with the proposed
changes, demonstrate that the acceptance
criteria continue to be met, and the postaccident conditions do not adversely affect
containment integrity or otherwise challenge
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any safety limit. The margin of safety with
respect to containment pressure is preserved
by demonstrating that the calculated
pressures do not exceed the design limit of
47 psig.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jeffrie J. Keenan,
Esquire, Nuclear Business Unit—N21,
P.O. Box 236, Hancocks Bridge, NJ
08038.
NRC Branch Chief: Harold K.
Chernoff.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Units 1 and
2, Somervell County, Texas
Date of amendment request:
December 19, 2006.
Brief description of amendments: The
amendments requested would revise
Technical Specifications (TS)
requirement 3.7.5, ‘‘Auxiliary Feedwater
(AFW) System,’’ TS 3.8.1, ‘‘AC
Sources—Operating,’’ TS 3.8.9,
‘‘Distribution Systems—Operating,’’ and
TS Example 1.3–3.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. D[o] the proposed change[s] involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes eliminate certain
Completion Times from the Technical
Specifications. Completion Times are not an
initiator to any accident previously
evaluated. As a result, the probability of an
accident previously evaluated is not affected.
The consequences of an accident during the
revised Completion Time are no different
than the consequences of the same accident
during the existing Completion Times. As a
result, the consequences of an accident
previously evaluated are not affected by this
change. The proposed changes do not alter or
prevent the ability of structures, systems, and
components from performing their intended
function to mitigate the consequences of an
initiating event within the assumed
acceptance limits. The proposed changes do
not affect the source term, containment
isolation, or radiological release assumptions
used in evaluating the radiological
consequences of an accident previously
evaluated. Further, the proposed changes do
not increase the types or amounts of
radioactive effluent that may be released
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offsite, nor significantly increase individual
or cumulative occupational/public radiation
exposures. The proposed changes are
consistent with the safety analysis
assumptions and resultant consequences.
Therefore, the proposed change[s] d[o] not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. D[o] the proposed change[s] create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The changes do not involve a physical
alteration of the plant (i.e., no new or
different type of equipment will be installed)
or a change in the methods governing normal
plant operation. The changes do not alter any
assumptions made in the safety analysis.
Therefore, the proposed change[s] d[o] not
create the possibility of a new or different
accident from any accident previously
evaluated.
3. D[o] the proposed change[s] involve a
significant reduction in a margin of safety?
Response: No.
The proposed change to delete the second
Completion Time does not alter the manner
in which safety limits, limiting safety system
settings or limiting conditions for operation
are determined. The safety analysis
acceptance criteria are not affected by this
change. The proposed changes will not result
in plant operation in a configuration outside
of the design basis.
Therefore, the proposed change[s] d[o] not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: George L. Edgar,
Esq., Morgan, Lewis and Bockius, 1800
M Street, NW., Washington, DC 20036.
NRC Branch Chief: David Terao
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Units 1 and
2, Somervell County, Texas
Date of amendment request: January
18, 2007.
Brief description of amendments: The
amendments requested would revise
Technical Specifications (TS)
requirement 3.8.1, ‘‘AC Sources—
Operating,’’ Extension of Completion
Times for Diesel Generators.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
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1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed Technical Specification (TS)
changes do not significantly increase the
probability of occurrence of a previously
evaluated accident because the Diesel
Generators (DGs) are not initiators of
previously evaluated accidents involving a
loss of offsite power (LOOP). The proposed
changes to the TS Required Actions and
Completion Times (CT) do not affect any of
the assumptions used in the deterministic or
the Probabilistic Safety Assessment (PSA)
analysis. Implementation of the proposed
changes does not result in a risk significant
impact. The onsite AC [alternating current]
power sources will remain highly reliable
and the proposed changes will not result in
a significant increase in the risk of plant
operation. This is demonstrated by showing
that the impact on plant safety as measured
by the increase in core damage frequency
(CDF) is less than 1E–06 per year and the
increase in large early release frequency
(LERF) is less than 1E–07 per year. In
addition, for the CT changes, the incremental
conditional core damage probabilities
(ICCDP) and incremental conditional large
early release probabilities (ICLERP) are less
than 5E–07 and 5E–08, respectively. These
changes meet the acceptance criteria in
Regulatory Guides 1.174 and 1.177.
Therefore, since the onsite AC power sources
will continue to perform their functions with
high reliability as originally assumed and the
increase in risk as measured by DCDF,
DLERF, ICCDP, and ICLERP risk metrics is
within the acceptance criteria of existing
regulatory guidance, there will not be a
significant increase in the consequences of
any accidents.
The proposed changes do not adversely
affect accident initiators or precursors nor
alter the design assumptions, conditions, or
configuration of the facility or the manner in
which the plant is operated and maintained.
The proposed changes do not alter or
prevent the ability of structures, systems, and
components (SSCs) from performing their
intended function to mitigate the
consequences of an initiating event within
the assumed acceptance limits. The proposed
changes do not affect the source term,
containment isolation, or radiological release
assumptions used in evaluating the
radiological consequences of an accident
previously evaluated. The proposed changes
are consistent with safety analysis
assumptions and resultant consequences.
The proposed TS changes will continue to
ensure the DGs perform their function when
called upon. Extending the TS CT to 14 days,
when an AACPS [alternate AC power source]
is available, does not affect the design, the
operational characteristics, the function, or
the reliability of the DGs. Additionally, the
CT extension to 14 days does not affect the
interfaces between the DGs and other plant
systems. Conversely, in the absence of an
AACPS, the DG 72-hour CT will be applied.
The availability of the onsite AC power
system to perform its accident mitigation
function is not affected by the proposed
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activity and thus there is no impact to the
radiological consequences of any accident
analysis.
To fully evaluate the effect of the changes
to the CT, PSA methods were utilized. The
results of this analysis show no significant
increase in the CDF and LERF.
The Configuration Risk Management
Program (CRMP) in TS 5.5.18 is an
administrative program that assesses risk
based on plant status. The risk-informed CT
will be implemented consistent with the
CRMP and approved plant procedures. When
utilizing the 14-day extension, requirements
of the CRMP per TS 5.5.18 call for the
consideration of other measures to mitigate
the consequences of an accident occurring
while a DG is inoperable. Furthermore,
administrative controls will be applied when
exercising the 14-day CT extension and are
adequate to maintain defense-in-depth and
sufficient safety margins.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes do not result in a
change in the manner in which the electrical
distribution subsystems provide plant
protection. The changes to the CT do not
change any existing accident scenarios, nor
create any new or different accident
scenarios.
In addition, the changes do not impose any
new or different accident mitigation
requirements or eliminate any existing
requirements.
The proposed changes are consistent with
the safety analysis assumptions and current
plant operating practice.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes do not alter the
manner in which safety limits, limiting safety
system settings or limiting conditions for
operation are determined. Neither the safety
analyses nor the safety analysis acceptance
criteria are impacted by these changes. The
proposed changes will not result in plant
operation in a configuration outside the
current design basis. The proposed activities
only involve changes to certain TS CTs.
Therefore the proposed change does not
involve a reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: George L. Edgar,
Esq., Morgan, Lewis and Bockius, 1800
M Street, NW., Washington, DC 20036.
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NRC Branch Chief: David Terao.
Previously Published Notices of
Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The following notices were previously
published as separate individual
notices. The notice content was the
same as above. They were published as
individual notices either because time
did not allow the Commission to wait
for this biweekly notice or because the
action involved exigent circumstances.
They are repeated here because the
biweekly notice lists all amendments
issued or proposed to be issued
involving no significant hazards
consideration.
For details, see the individual notice
in the Federal Register on the day and
page cited. This notice does not extend
the notice period of the original notice.
Duke Power Company LLC, Docket Nos.
50–369 and 50–370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg
County, North Carolina
Date of amendment request: March 8,
2007.
Brief description of amendment
request: The proposed amendments
would revise the McGuire Nuclear
Station, Units 1 and 2, Technical
Specification 3.5.2.8, and the associated
Bases and authorizes changes to the
Updated Final Safety Analysis Reports
concerning modifications to the
emergency core cooling system sump.
Date of publication of individual
notice in Federal Register: March 19,
2007.
Expiration date of individual notice:
Comments April 18, 2007; Hearing May
18, 2007.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
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and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.22(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
Carolina Power & Light Company, et al.,
Docket No. 50–400, Shearon Harris
Nuclear Power Plant, Unit 1, Wake and
Chatham Counties, North Carolina
Date of application for amendment:
May 23, 2006, as supplemented by
letters dated October 3, 2006, and
October 24, 2006.
Brief description of amendment: This
amendment revises Technical
Specification by modifying the steam
generator tube surveillance program at
Shearon Harris Nuclear Power Plant,
Unit 1.
Date of issuance: March 16, 2007.
Effective date: This amendment is
effective as of the date of issuance and
shall be implemented within 90 days of
issuance.
Amendment No. 124.
Facility Operating License No. NPF–
63: Amendment revises the Technical
Specifications.
Date of initial notice in Federal
Register: December 19, 2006 (71 FR
75991). The supplemental letters
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provided additional information that
was within the scope of the initial
notice and did not change the initial
proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in the
Safety Evaluation dated: March 16,
2007.
No significant hazards consideration
comments received: No.
Dominion Nuclear Connecticut, Inc.,
Docket No. 50–423, Millstone Power
Station, Unit No. 3 New London County,
Connecticut
Date of application for amendment:
July 19, 2006.
Brief description of amendment: The
proposed amendment changed the
Millstone Power Station, Unit No. 3
(MPS3) reactor core safety limits
Technical Specification (TS) and
relocated the reactor core safety limit
figure to the Core Operating Limits
Report in the MPS3 Technical
Requirements Manual.
Date of issuance: March 14, 2007
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment No.: 236
Facility Operating License No. NPF–
49: The amendment revised the TSs.
Date of initial notice in Federal
Register: August 29, 2006 (71 FR
51227). The Commission’s related
evaluation of the amendment is
contained in a Safety Evaluation dated
March 14, 2007.
No significant hazards consideration
comments received: No.
Duke Power Company LLC, et al.,
Docket Nos. 50–413 and 50–414,
Catawba Nuclear Station, Units 1 and 2,
York County, South Carolina
Date of application for amendments:
April 11, 2006.
Brief description of amendments:
(TSTF–372, Rev. 4) The amendments
added Technical Specification (TS)
Limiting Condition for Operation (LCO)
3.0.8 to allow a delay time for entering
a supported system TS when the
inoperability is due solely to an
inoperable snubber, if risk is assessed
and managed with an approved Bases
Control Program that is consistent with
the TS Bases Control Program described
in Section 5.5 of the applicable vendor’s
Standard Technical Specifications. The
amendment also made an administrative
change, renumbering existing LCO 3.0.8
to LCO 3.0.9.
Date of issuance: March 19, 2007
Effective date: As of the date of
issuance and shall be implemented
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within 120 days from the date of
issuance.
Amendment Nos.: 235, 231
Renewed Facility Operating License
Nos. NPF–35 and NPF–52: Amendments
revised the licenses and the technical
specifications.
Date of initial notice in Federal
Register: December 5, 2006 (71 FR
70555). The Commission’s related
evaluation of the amendments is
contained in a Safety Evaluation dated
March 19, 2007.
No significant hazards consideration
comments received: No
Duke Power Company LLC, Docket Nos.
50–369 and 50–370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg
County, North Carolina
Date of application for amendments:
April 11, 2006.
Brief description of amendments:
(TSTF–372, Rev. 4) The amendments
added Technical Specification (TS)
Limiting Condition for Operation (LCO)
3.0.8 to allow a delay time for entering
a supported system TS when the
inoperability is due solely to an
inoperable snubber, if risk is assessed
and managed with an approved Bases
Control Program that is consistent with
the TS Bases Control Program described
in Section 5.5 of the applicable vendor’s
Standard Technical Specifications. The
amendment also made an administrative
change, renumbering existing LCO 3.0.8
to LCO 3.0.9.
Date of issuance: March 29, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 120 days from the date of
issuance.
Amendment Nos.: 238, 220.
Renewed Facility Operating License
Nos. NPF–9 and NPF–17: Amendments
revised the licenses and the technical
specifications.
Date of initial notice in Federal
Register: December 5, 2006 (71 FR
70556). The Commission’s related
evaluation of the amendments is
contained in a Safety Evaluation dated
March 29, 2007.
No significant hazards consideration
comments received: No.
Energy Northwest, Docket No. 50–397,
Columbia Generating Station, Benton
County, Washington
Date of application for amendment:
May 22, 2006, as supplemented by letter
dated February 5, 2007.
Brief description of amendment: The
amendment revised Technical
Specification Surveillance
Requirements 3.8.1.11, 3.8.1.12,
3.8.1.16, and 3.8.1.19 to eliminate the
specific test-performance mode
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restrictions for the High-Pressure Core
Spray Division 3 diesel generator.
Date of issuance: March 23, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 45 days from the date of
issuance.
Amendment No.: 203.
Facility Operating License No. NPF–
21: The amendment revised the
Technical Specifications and Facility
Operating License.
Date of initial notice in Federal
Register: July 18, 2006 (71 FR 40745).
The supplemental letter dated February
5, 2007, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 23, 2007.
No significant hazards consideration
comments received: No.
Entergy Nuclear Operations, Inc.,
Docket No. 50–293, Pilgrim Nuclear
Power Station, Plymouth County,
Massachusetts.
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Date of application for amendment:
December 27, 2006.
Brief description of amendment: The
amendment revised the Technical
Specification Limiting Condition for
Operation 3.14.A to adopt the Technical
Specification Task Force 484, Revision
0, ‘‘Use of Technical Specification
3.10.1 for Scram Time Testing
Activities.’’
Date of issuance: March 26, 2007.
Effective date: As of the date of
issuance, and shall be implemented
within 60 days.
Amendment No.: 226.
Facility Operating License No. DPR–
35: The amendment revised the Facility
Operating License and Technical
Specifications.
Date of initial notice in Federal
Register: February 20, 2007 (72 FR
7776). The Commission’s related
evaluation of the amendment is
contained in a Safety Evaluation dated
March 26, 2007.
No significant hazards consideration
comments received: No
Entergy Nuclear Operations, Inc.,
Docket No. 50–293, Pilgrim Nuclear
Power Station, Plymouth County,
Massachusetts.
Date of application for amendment:
January 15, 2007.
Brief description of amendment: The
amendment revised the Technical
Specifications (TS) to extend the use of
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the current pressure-temperature limits
as specified in TS Figures 3.6.1, 3.6.2,
and 3.6.3 through the end of operating
cycle 18.
Date of issuance: March 26, 2007.
Effective date: As of the date of
issuance, and shall be implemented
within 60 days.
Amendment No.: 227.
Facility Operating License No. DPR–
35: The amendment revised the Facility
Operating License and Technical
Specifications.
Date of initial notice in Federal
Register: February 12, 2007 (72 FR
6609). The Commission’s related
evaluation of the amendment is
contained in a Safety Evaluation dated
March 26, 2007.
No significant hazards consideration
comments received: No.
Assemblies,’’ to allow the use of
hafnium as an additional type of control
material.
Date of issuance: March 16, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment No: 174.
Facility Operating License No. NPF–
29: The amendment revises the Facility
Operating License and Technical
Specifications.
Date of initial notice in Federal
Register: February 13, 2007 (72 FR
6782). The Commission’s related
evaluation of the amendment is
contained in a Safety Evaluation dated
March 16, 2007.
No significant hazards consideration
comments received: No.
Entergy Nuclear Vermont Yankee, LLC
and Entergy Nuclear Operations, Inc.,
Docket No. 50–271, Vermont Yankee
Nuclear Power Station, Vernon,
Vermont
Entergy Operations, Inc., Docket No. 50–
382, Waterford Steam Electric Station,
Unit 3, St. Charles Parish, Louisiana
Date of application for amendment:
April 22, 2006.
Brief description of amendment: The
amendment revised Technical
Specification (TS) requirements for
inoperable snubbers by relocating the
current TS requirements Limiting
Condition for Operation (LCO) 3.6.I and
Surveillance Requirement (SR) 4.6.I to
the Technical Requirements Manual and
adding LCO 3.0.8 to the TSs. The
associated TS Bases section has also
been relocated.
Date of Issuance: March 26, 2007.
Effective date: As of the date of
issuance, and shall be implemented
within 60 days.
Amendment No.: 230.
Facility Operating License No. DPR–
28: The amendment revised the License
and TSs.
Date of initial notice in Federal
Register: June 6, 2006 (71 FR 32604).
The Commission’s related evaluation of
this amendment is contained in a Safety
Evaluation dated March 26, 2007.
No significant hazards consideration
comments received: No.
Entergy Operations, Inc., System Energy
Resources, Inc., South Mississippi
Electric Power Association, and Entergy
Mississippi, Inc., Docket No. 50–416,
Grand Gulf Nuclear Station, Unit 1,
Claiborne County, Mississippi
Date of application for amendment:
January 18, 2007.
Brief description of amendment: The
amendment revised the description of
the control rod assemblies in Grand Gulf
Nuclear Station, Unit 1, Technical
Specification 4.2.2, ‘‘Control Rod
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Date of amendment request:
September 26, 2006.
Brief description of amendment: The
amendment deleted reference to the
containment fan cooler condensate flow
switch from Technical Specification
3.4.5.1, ‘‘Reactor Coolant System
Leakage—Leakage Detection
Instrumentation,’’ and modified or
deleted associated actions. The Nuclear
Regulatory Commission staff had
determined that the remaining leak
detection methods provided adequate
means for detecting, and to the extent
practical, identifying the location of the
source of potential reactor coolant
leakage.
Date of issuance: March 19, 2007.
Effective date: As of the date of
issuance and shall be implemented 60
days from the date of issuance.
Amendment No.: 212.
Facility Operating License No. NPF–
38: The amendment revised the
Operating License and the Technical
Specifications.
Date of initial notice in Federal
Register: February 13, 2007 (72 FR
6782). The Commission’s related
evaluation of the amendment is
contained in a Safety Evaluation dated
March 19, 2007.
No significant hazards consideration
comments received: No.
Indiana Michigan Power Company,
Docket Nos. 50–315 and 50–316, Donald
C. Cook Nuclear Plant, Units 1 and 2,
Berrien County, Michigan
Date of application for amendments:
May 26, 2006, as supplemented on
December 26, 2006, and March 14, 2007.
Brief description of amendments: The
amendments revised the existing steam
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generator (SG) tube surveillance
program. The changes are modeled after
Technical Specifications Task Force
(TSTF) traveler TSTF–449, Revision 4,
‘‘Steam Generator Tube Integrity,’’ and
the model safety evaluation prepared by
the Nuclear Regulatory Commission
staff and published in the Federal
Register on March 2, 2005 (70 FR
10298). In this regard, the scope of the
amendments includes changes to the
definition of leakage, changes to the
primary-to-secondary leakage
requirements, changes to the SG tube
surveillance program (SG tube
integrity), and changes to the SG
reporting requirements.
Date of issuance: March 14, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment Nos.: 298 and 279.
Facility Operating License Nos. DPR–
58 and DPR–74: Amendments revise the
Technical Specifications.
Date of initial notice in Federal
Register: July 5, 2006 (71 FR 38183).
The supplemental letters provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the NRC staff’s
original proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 14, 2007.
No significant hazards consideration
comments received: No.
cprice-sewell on PROD1PC66 with NOTICES
Nuclear Management Company, LLC,
Docket No. 50–263, Monticello Nuclear
Generating Plant, Wright County,
Minnesota
Date of application for amendment:
March 7, 2006, as supplemented by
letters dated May 30, September 7,
December 15, 2006, and January 2, 2007.
Brief description of amendment: The
amendment revised Section 4.3, ‘‘Fuel
Storage,’’ of the Monticello Nuclear
Generating Plant, technical
specifications to allow for installation of
an additional temporary 8x8 (64-cell)
high-density spent fuel storage rack in
the spent fuel pool to maintain full core
off-load capability.
Date of issuance: March 9, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 150.
Facility Operating License No. DPR–
22. Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: April 3, 2006 (71 FR 16599).
The supplemental letters contained
clarifying information and did not
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change the initial no significant hazards
consideration determination, and did
not expand the scope of the original
Federal Register notice.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 9, 2007.
No significant hazards consideration
comments received: No.
Nuclear Management Company, LLC,
Docket Nos. 50–266 and 50–301, Point
Beach Nuclear Plant, Units 1 and 2,
Town of Two Creeks, Manitowoc
County, Wisconsin
Date of application for amendments:
March 23, 2006, as supplemented on
December 19, 2006.
Brief description of amendments: The
amendments revise Technical
Specification (TS) 3.3.4, ‘‘Loss of Power
(LOP) Diesel Generator (DG) Start and
Load Sequence Instrumentation,’’ and
surveillance requirement 3.3.4.3.b to
modify the TS title and correct
nonconservatisms in the allowable
values for the degraded voltage time
delay.
Date of issuance: March 21, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 45 days.
Amendment Nos.: 225 & 231.
Renewed Facility Operating License
Nos. DPR–24 and DPR–27: Amendments
revised the Technical Specifications and
License.
Date of initial notice in Federal
Register: April 25, 2006 (71 FR 23958).
The December 19, 2006, supplement,
contained clarifying information and
did not change the staff’s initial
proposed finding of no significant
hazards consideration.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 21, 2007.
No significant hazards consideration
comments received: No.
Nuclear Management Company, LLC,
Docket Nos. 50–282 and 50–306, Prairie
Island Nuclear Generating Plant, Units
1 and 2, Goodhue County, Minnesota
Date of application for amendments:
February 16, 2006, supplemented by
letters dated July 21, and December 27,
2006.
Brief description of amendments: The
amendments consist of changes to the
Technical Specifications (TSs) related to
steam generator tube integrity. The
amendments are modeled after the U.S.
Nuclear Regulatory Commission
approved Technical Specification Task
Force (TSTF) Standard Technical
Specification Change Traveler, TSTF–
449, ‘‘Steam Generator Tube Integrity,’’
Revision 4 (ML0510902003).
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Date of issuance: March 20, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 90 days.
Amendment Nos.: 177 and 167.
Facility Operating License Nos. DPR–
42 and DPR–60: Amendments revised
the Technical Specifications.
Date of initial notice in Federal
Register: April 11, 2006 (71 FR 18376)
The supplemental letters contained
clarifying information and did not
change the initial no significant hazards
consideration determination, and did
not expand the scope of the original
Federal Register notice.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 20, 2007.
No significant hazards consideration
comments received: No.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of application for amendments:
May 30, 2006, as supplemented by
letters dated November 22, 2006, and
January 11, 2007.
Brief description of amendments: The
amendments revised the existing steam
generator (SG) tube surveillance
program. The changes were modeled
after Technical Specification Task Force
(TSTF) traveler TSTF–449, Revision 4,
‘‘Steam Generator Tube Integrity,’’ and
the model safety evaluation prepared by
the U.S. Nuclear Regulatory
Commission and published in the
Federal Register on March 2, 2005 (70
FR 10298). The scope of the application
included changes to the definition of
leakage, changes to the primary-tosecondary leakage requirements,
changes to the SG tube surveillance
program (SG tube integrity), changes to
the SG reporting requirements, and
associated changes to the Technical
Specification Bases.
Date of issuance: March 21, 2007.
Effective date: As of its date of
issuance and shall be implemented
within 120 days from the date of
issuance.
Amendment Nos.: Unit 1—194; Unit
2—195.
Facility Operating License Nos. DPR–
80 and DPR–82: The amendments
revised the Facility Operating Licenses
and Technical Specifications.
Date of initial notice in Federal
Register: July 18, 2006 (71 FR 40751).
The supplemental letters dated
November 22, 2006, and January 11,
2007, provided additional information
that clarified the application, did not
expand the scope of the application as
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originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 21, 2007.
No significant hazards consideration
comments received: No.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of application for amendments:
December 14, 2006.
Brief description of amendments: The
amendments deleted Section 2.G of
Facility Operating License Nos. DPR–80
and DPR–82, which require reporting of
violations of the requirements of
Sections 2.C, 2.E, and 2.F of the
operating license. This operating license
improvement was made available by the
U.S. Nuclear Regulatory Commission on
November 4, 2005, as part of the
consolidated line item improvement
process (CLIIP).
Date of issuance: March 19, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 90 days from the date of
issuance.
Amendment Nos.: Unit 1–193; Unit
2–194.
Facility Operating License Nos. DPR–
80 and DPR–82: The amendments
revised the Facility Operating Licenses.
Date of initial notice in Federal
Register: January 3, 2007 (72 FR 154).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 19, 2007.
No significant hazards consideration
comments received: No.
cprice-sewell on PROD1PC66 with NOTICES
PPL Susquehanna, LLC, Docket No. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1
and 2), Luzerne County, Pennsylvania
Date of application for amendments:
November 18, 2005, as supplemented on
November 29, 2006, December 1, 2006,
December 15, 2006, January 9, 2007, and
March 12, 2007 (PLA–6168 and PLA–
6169).
Brief description of amendments: The
amendments change the SSES 1 and 2
Technical Specifications (TSs) to
implement the Average Power Range
Monitor/Rod Block Monitor/TSs/
Maximum Load Line Limit Analysis by
revising TS 1.1, ‘‘Definitions,’’ TS 5.6.5,
‘‘Core Operating Limits Report,’’ and the
surveillance requirement sections of TS
3.3.1.1, ‘‘Reactor Protection System
Instrumentation,’’ and TS 3.3.2.1,
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15:22 Apr 09, 2007
Jkt 211001
‘‘Control Rod Block Instrumentation.’’
The amendments also delete TS 3.2.4,
‘‘Average Power Range Monitor Gain
and Setpoints,’’ and its associated
references in the TSs. Additionally, the
amendments change the method of
evaluation for the postulated
recirculation line break in the reactor
pressure vessel shield annulus region.
Date of issuance: March 23, 2007.
Effective date: As of the date of
issuance and to be implemented prior to
the startup following the SSES 1 spring
2008 15th refueling outage for Unit 1
and prior to the startup following the
SSES 2 spring 2007 13th refueling
outage for Unit 2.
Amendment Nos.: 242 and 220.
Facility Operating License Nos. NPF–
14 and NPF–22: The amendments
revised the TSs and the License.
Date of initial notice in Federal
Register: February 14, 2006 (71 FR
7810).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 23, 2007.
No significant hazards consideration
comments received: No.
PPL Susquehanna, LLC, Docket No. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1
and 2), Luzerne County, Pennsylvania
Date of application for amendments:
September 7, 2006.
Brief description of amendments: The
amendments revise the SSES 1 and 2
Technical Specifications (TSs) Section
5.5.6, ‘‘Inservice Testing Program,’’ and
TS 5.5.12, ‘‘Primary Containment
Leakage Rate Testing Program,’’ to be
consistent with the requirements of
Title 10 of the Code of Federal
Regulations (10 CFR) Section
50.55a(f)(4) and 10 CFR 50.55a(g)(4),
respectively. The amendments
implement TS Task Force (TSTF)–343,
Revision 1 and TSTF–479, Revision 0.
Date of issuance: March 19, 2007.
Effective date: As of the date of
issuance and to be implemented within
30 days.
Amendment Nos.: 241 and 219.
Facility Operating License Nos. NPF–
14 and NPF–22: The amendments
revised the License and Technical
Specifications.
Date of initial notice in Federal
Register: December 19, 2006 (71 FR
75997).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 19, 2007.
No significant hazards consideration
comments received: No.
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17957
PPL Susquehanna, LLC, Docket No. 50–
388, Susquehanna Steam Electric
Station, Unit 2 (SSES 2), Luzerne
County, Pennsylvania
Date of application for amendment:
November 16, 2006, as supplemented on
February 15, 2007.
Brief description of amendment: The
amendment changes the SSES 2
Technical Specification (TS) Section
2.1.1.2 by revising the Unit 2 Cycle 14
Minimum Critical Power Ratio Safety
Limit for two-loop and single-loop
operation and the references listed in TS
5.6.5.b.
Date of issuance: March 19, 2007.
Effective date: As of the date of
issuance and to be implemented within
30 days.
Amendment No.: 218.
Facility Operating License No. NPF–
22: The amendment revised the License
and Technical Specifications.
Date of initial notice in Federal
Register: December 19, 2006 (71 FR
75998).
The supplement dated February 15,
2007, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 19, 2007.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket Nos. 50–272
and 50–311, Salem Nuclear Generating
Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of application for amendments:
May 1, 2006.
Brief description of amendments: The
amendments eliminate the requirement
for a power range neutron flux high
negative rate trip and delete the
references to this trip in Salem Unit
Nos. 1 and 2 Technical Specification
(TS) Table 2.2–1, ‘‘Reactor Trip System
Instrumentation Trip Setpoints,’’ TS
Table 3.3–1, ‘‘Reactor Trip System
Instrumentation,’’ TS Table 3.3–2,
‘‘Reactor Trip System Instrumentation
Response Times,’’ and TS Table 4.3–1,
‘‘Reactor Trip System Instrumentation
Surveillance Requirements.’’ The
amendments also incorporate
administrative and editorial changes to
correct miscellaneous errors in the TSs
for Salem Units Nos. 1 and 2.
Date of issuance: March 19, 2007.
Effective date: As of the date of
issuance, to be implemented within 60
days.
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Amendment Nos.: 278 and 261
Facility Operating License Nos. DPR–
70 and DPR–75: The amendments
revised the TSs and the License.
Date of initial notice in Federal
Register: July 18, 2006 (71 FR 40752).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 19, 2007.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket Nos. 50–272
and 50–311, Salem Nuclear Generating
Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of application for amendments:
August 4, 2006, as supplemented by
letter dated February 20, 2007.
Brief description of amendments: The
amendments allow the use of blind
flanges for containment isolation in the
containment purge system supply and
exhaust lines, and make corresponding
changes to the Technical Specifications
(TSs). The amendments also consolidate
the containment isolation requirements
by moving the requirements of TS 3/4
6.1.7, ‘‘Containment Ventilation
System,’’ to TS 3/4 6.3.1 (TS 3/4 6.3 for
Unit No. 2), ‘‘Containment Isolation
Valves.’’
Date of issuance: March 19, 2007.
Effective date: As of the date of
issuance, to be implemented within 60
days.
Amendment Nos.: 277 and 260.
Facility Operating License Nos. DPR–
70 and DPR–75: The amendments
revised the License and the TSs.
cprice-sewell on PROD1PC66 with NOTICES
PSEG Nuclear LLC, Docket No. 50–272,
Salem Nuclear Generating Station, Unit
No. 1, Salem County, New Jersey
Date of application for amendment:
January 18, 2007, as supplemented on
February 23, March 9, and March 22,
2007.
Brief description of amendment: The
amendment approves a one-time change
to the Technical Specifications (TSs)
regarding the steam generator (SG) tube
inspection and repair required for the
portion of the SG tubes passing through
the tubesheet region. Specifically, for
Salem Unit No. 1 refueling outage 18
(planned for spring 2007) and the
subsequent operating cycle, the TS
changes limit the required inspection
(and repair if degradation is found) to
the portions of the SG tubes passing
through the upper 17 inches of the
approximate 21-inch tubesheet region.
Date of issuance: March 27, 2007.
Effective date: As of the date of
issuance, to be implemented within 60
days.
Amendment No.: 279.
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15:22 Apr 09, 2007
Jkt 211001
Facility Operating License No. DPR–
70: The amendment revised the TSs and
the License.
Date of initial notice in Federal
Register: January 25, 2007 (72 FR
3427).
The letters dated February 23, March
9, and March 22, 2007, provided
clarifying information that did not
change the initial proposed no
significant hazards consideration
determination or expand the application
beyond the scope of the original Federal
Register notice.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 27, 2007.
No significant hazards consideration
comments received: No.
R.E. Ginna Nuclear Power Plant, LLC,
Docket No. 50–244, R.E. Ginna Nuclear
Power Plant, Wayne County, New York
Date of application for amendment:
March 28, 2006, as supplemented by
letter dated October 24, 2006.
Brief description of amendment: The
amendment revises Technical
Specification Surveillance Requirement
3.5.1.4 to change the method and
frequency for verifying emergency core
cooling system accumulator boric acid
concentration.
Date of issuance: March 28, 2007.
Effective date: As of the date of
issuance to be implemented within 45
days.
Amendment No.: 101.
Renewed Facility Operating License
No. DPR–18: Amendment revised the
License and Technical Specifications.
Date of initial notice in Federal
Register: April 25, 2006 (71 FR 23960)
The October 24, 2006, letter provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 28, 2007.
No significant hazards consideration
comments received: No.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Unit Nos.
1 and 2, Somervell County, Texas
Date of amendment request: August
22, 2005, as supplemented by letters
dated September 18, 2006, October 23,
2006, and February 16, 2007.
Brief description of amendments:
These amendments modified Technical
Specification (TS) requirements related
to control room envelope habitability in
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TS 3.7.10, ‘‘Control Room Emergency
Filtration/Pressurization System
(CREFS)’’ and TS Section 5.5,
‘‘Administrative Controls—Programs
and Manuals.’’
Date of issuance: March 26, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 120 days from the date of
issuance.
Amendment Nos.: 136/136.
Facility Operating License Nos. NPF–
87 and NPF–89: The amendments
revised the Facility Operating Licenses
and Technical Specifications.
Date of initial notice in Federal
Register: November 8, 2005 (70 FR
67754). The supplemental letters dated
September 18 and October 23, 2006, and
February 16, 2007, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 26, 2007.
No significant hazards consideration
comments received: No.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Unit Nos.
1 and 2, Somervell County, Texas
Date of amendment request: March
31, 2006.
Brief description of amendments: The
amendments revised Technical
Specification 5.0 entitled,
‘‘ADMINISTRATIVE CONTROLS.’’
Specifically, the change deleted the Vice
President, Nuclear Operations, as an
alternative to the Plant Manager for
certain functions.
Date of Issuance: March 20, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 120 days from the date of
issuance.
Amendment Nos.: Unit 1–134; Unit
2–134.
Facility Operating License Nos. NPF–
87 and NPF–89: The amendments
revised the Facility Operating Licenses
and Technical Specifications.
Date of initial notice in Federal
Register: September 12, 2006 (71 FR
53722).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 20, 2007.
No significant hazards consideration
comments received: No.
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TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station (CPSES),
Unit Nos. 1 and 2, Somervell County,
Texas
Date of amendment request: February
21, 2006, as supplemented by letter
dated March 19, 2007.
Brief description of amendments: The
amendments revise TS 5.6.5 entitled,
‘‘Core Operating Limits Report (COLR),’’
by adding two reports providing Lossof-Coolant Accident (LOCA) and nonLOCA analysis methodologies for
CPSES Unit 1.
Date of issuance: March 26, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 120 days from the date of
issuance, but no later than the entry into
Mode 5 in the restart of Unit 1 from its
spring 2007 refueling outage.
Amendment Nos.: 135/135.
Facility Operating License Nos. NPF–
87 and NPF–89: The amendments
revised the Facility Operating Licenses
and Technical Specifications.
Date of initial notice in Federal
Register: June 6, 2006 (71 FR 32609).
The supplemental letter dated March
19, 2007, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 26, 2007.
No significant hazards consideration
comments received: No.
cprice-sewell on PROD1PC66 with NOTICES
Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of application for amendment:
May 25, 2006, as supplemented by letter
dated March 12, 2007.
Brief description of amendment: The
amendment revised Technical
Specifications 3.1.7, ‘‘Rod Position
Indication,’’ 3.2.1, ‘‘Heat Flux Hot
Channel Factor (FQ(Z)) (FQ
Methodology),’’ 3.2.4, ‘‘Quadrant Power
Tilt Ratio (QPTR),’’ and 3.3.1, ‘‘Reactor
Trip System (RTS) Instrumentation,’’ to
allow use of the Westinghouse
proprietary computer code, the Best
Estimate Analyzer for Core Operations—
Nuclear (BEACON). Certain required
actions, for when a limiting condition
for operation is not met, and certain
surveillance requirements are being
changed to refer to power distribution
measurements or measurement
information of the core.
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16:29 Apr 09, 2007
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Date of issuance: March 21, 2007.
Effective date: As of its date of
issuance and shall be implemented
before entry into Mode 2 in the plant
restart from the refueling outage
scheduled for the spring of 2007. This
includes the incorporation of the
identified changes to the Final Safety
Analysis Report (FSAR) in Attachment
6 of the licensee’s application dated
May 25, 2006, into the FSAR.
Amendment No.: 182.
Facility Operating License No. NPF–
30: The amendment revised the
Operating License and Technical
Specifications.
Date of initial notice in Federal
Register: July 18, 2006 (71 FR 40756)
The supplemental letter dated March
12, 2007, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the NRC staff’s
original proposed no significant hazards
consideration determination published
in the Federal Register on July 18, 2006.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 21, 2007.
No significant hazards consideration
comments received: No.
Dated at Rockville, Maryland, this 3rd day
of April 2007.
For the Nuclear Regulatory Commission.
Catherine Haney,
Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. E7–6632 Filed 4–9–07; 8:45 am]
BILLING CODE 7590–01–P
OVERSEAS PRIVATE INVESTMENT
CORPORATION
Submission for OMB Review;
Comment Request
Overseas Private Investment
Corporation (OPIC)
ACTION: Request for comments.
AGENCY:
SUMMARY: Under the provision of the
Paperwork Reduction Act (44 U.S.C.
Chapter 35), agencies are required to
publish a Notice in the Federal Register
notifying the public that Agency is
preparing an information collection
request for OMB review and approval
and to request public review and
comment on the submission.
Comments are being solicited on the
need for the information, its practical
utility, the accuracy of the Agency’s
burden estimate, and on ways to
minimize the reporting burden,
including automated collection
techniques and uses of other forms of
PO 00000
Frm 00144
Fmt 4703
Sfmt 4703
17959
technology. The proposed form under
review is summarized below.
DATES: Comments must be received
within 30 calendar days of this notice.
ADDRESSES: Copies of the subject form
and the request for review prepared for
submission to OMB may be obtained
from the Agency submitting officer.
Comments on the form should be
submitted to the Agency Submitting
Officer.
FOR FURTHER INFORMATION CONTACT:
OPIC Agency Submitting Officer: Essie
Bryant, Record Manager, Overseas
Private Investment Corporation, 1100
New York Avenue, NW., Washington,
DC 20527; 202–336–8563.
Summary Form Under Review
Type of Request: Revised form.
Title: OPIC Self-Monitoring
Questionnaire.
Form Number: OPIC–162.
Frequency of Use: Annually for
duration of project.
Type of Respondents: Business or
other institution (except farms);
individuals.
Standard Industrial Classification
Codes: All.
Description of Affected Public: U.S.
companies or citizens investing
overseas.
Reporting Hours: 6.5 hours per
project.
Number of Responses: 350 per year.
Federal Cost: $35,000.
Authority for Information Collection:
Sections 231, 234(a), 239(d), and 240A
of the Foreign Assistance Act of 1961,
as amended.
Abstract (Needs and Uses): The
questionnaire is completed by OPICassisted investors annually. The
questionnaire allows OPIC’s assessment
of effects of OPIC-assisted projects on
the U.S. economy and employment, as
well as on the environment and
economic development abroad.
Dated: April 5, 2007.
John P. Crowley, III,
Senior Administrative Counsel, Department
of Legal Affairs.
[FR Doc. 07–1771 Filed 4–9–07; 8:45 am]
BILLING CODE 3210–01–M
PENSION BENEFIT GUARANTY
CORPORATION
Approval of Exemption From the Bond/
Escrow Requirement Relating to the
Sale of Assets by an Employer Who
Contributes to a Multiemployer Plan;
Washington Nationals Baseball Club,
LLC
Pension Benefit Guaranty
Corporation.
AGENCY:
E:\FR\FM\10APN1.SGM
10APN1
Agencies
[Federal Register Volume 72, Number 68 (Tuesday, April 10, 2007)]
[Notices]
[Pages 17944-17959]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: E7-6632]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued, and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from March 16, 2007 to March 29, 2007. The last
biweekly notice was published on March 27, 2007 (72 FR 14303).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example, in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rulemaking,
Directives and Editing Branch, Division of Administrative Services,
Office of Administration, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, and should cite the publication date and
page number of this Federal Register notice. Written comments may also
be delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike,
Rockville, Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received may be examined at the Commission's
Public Document Room (PDR), located at One White Flint North, Public
File Area O1F21, 11555 Rockville Pike (first floor), Rockville,
Maryland. The filing of requests for a hearing and petitions for leave
to intervene is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of
[[Page 17945]]
which the petitioner is aware and on which the petitioner/requestor
intends to rely to establish those facts or expert opinion. The
petition must include sufficient information to show that a genuine
dispute exists with the applicant on a material issue of law or fact.
Contentions shall be limited to matters within the scope of the
amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket No. 50-461, Clinton Power Station,
Unit No. 1, DeWitt County, Illinois
Date of amendment request: November 13, 2006.
Description of amendment request: The proposed amendment changes
the technical specification (TS) testing frequency for the surveillance
requirement (SR) in TS 3.1.4, ``Control Rod Scram Times.'' The proposed
change revises the test frequency of SR 3.1.4.2, control rod scram time
testing, from ``120 days cumulative operation in MODE 1'' to ``200 days
cumulative operation in Mode 1.''
AmerGen has reviewed the proposed no significant hazards
consideration determination published in the Federal Register on August
23, 2004 (69 FR 51864), as part of the consolidated line item
improvement process (CLIIP) and has concluded that the proposed
determination presented in the notice is applicable to Clinton Power
Station, Unit No. 1.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below.
1. Does the change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
The proposed change extends the frequency for testing control
rod scram time testing from every 120 days of cumulative Mode 1
operation to 200 days of cumulative Mode 1 operation. The frequency
of surveillance testing is not an initiator of any accident
previously evaluated. The frequency of surveillance testing does not
affect the ability to mitigate any accident previously evaluated, as
the tested component is still required to be operable. Therefore,
the proposed change does not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. Does the change create the possibility of a new or different
kind of accident from any accident previously evaluated?
Response: No.
The proposed change extends the frequency for testing control
rod scram time testing from every 120 days of cumulative Mode 1
operation to 200 days of cumulative Mode 1 operation. The proposed
change does not result in any new or different modes of plant
operation. Therefore, the proposed change does not create the
possibility of a new or different kind of accident from any
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change extends the frequency for testing control
rod scram time testing from every 120 days of cumulative Mode 1
operation to 200 days of cumulative Mode 1 operation. The proposed
change continues to test the control rod scram time to ensure the
assumptions in the safety analysis are protected. Therefore, the
proposed change does not involve a significant reduction in a margin
of safety.
Based on the above, the proposed change presents no significant
hazards consideration under the standards set forth in 10 CFR 50.92(c),
and accordingly, a finding of ``no significant hazards consideration''
is justified.
Therefore, the NRC staff proposes to determine that the amendment
request involves no significant hazards consideration.
Attorney for licensee: Mr. Bradley J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Kennett
Square, PA 19348.
NRC Branch Chief: Russell Gibbs.
Detroit Edison Company, Docket No. 50-341, Fermi 2, Monroe County,
Michigan
Date of amendment request: January 26, 2007.
Description of amendment request: The proposed amendment would
revise technical specifications (TS) requirements for unavailable
barriers by
[[Page 17946]]
adding limiting condition for operation (LCO) 3.0.9. This would
establish conditions under which TS systems would remain operable when
required physical barriers are not capable of providing their related
support function. Also, the proposed amendment would make editorial
changes to LCO 3.0.8 to be consistent with the terminology in LCO
3.0.9.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration by a reference to a generic analysis published in the
Federal Register on October 3, 2006 (71 FR 58444), which is presented
below:
1. Does the proposed change involve a significant increase in
the probability or consequences of any accident previously
evaluated?
Response: No.
The proposed change allows a delay time for entering a supported
system technical specification (TS) when the inoperability is due
solely to an unavailable barrier if risk is assessed and managed.
The postulated initiating events which may require a functional
barrier are limited to those with low frequencies of occurrence, and
the overall TS system safety function would still be available for
the majority of anticipated challenges. Therefore, the probability
of an accident previously evaluated is not significantly increased,
if at all. The consequences of an accident while relying on the
allowance provided by proposed LCO 3.0.9 are no different than the
consequences of an accident while relying on the TS required actions
in effect without the allowance provided by proposed LCO 3.0.9.
Therefore, the consequences of an accident previously evaluated are
not significantly affected by this change. The addition of a
requirement to assess and manage the risk introduced by this change
will further minimize possible concerns.
Therefore, this change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change does not involve a physical alteration of
the plant (no new or different type of equipment will be installed).
Allowing delay times for entering supported system TS when
inoperability is due solely to an unavailable barrier, if risk is
assessed and managed, will not introduce new failure modes or
effects and will not, in the absence of other unrelated failures,
lead to an accident whose consequences exceed the consequences of
accidents previously evaluated. The addition of a requirement to
assess and manage the risk introduced by this change will further
minimize possible concerns. Thus, this change does not create the
possibility of a new or different kind of accident from an accident
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change allows a delay time for entering a supported
system TS when the inoperability is due solely to an unavailable
barrier, if risk is assessed and managed. The postulated initiating
events which may require a functional barrier are limited to those
with low frequencies of occurrence, and the overall TS system safety
function would still be available for the majority of anticipated
challenges. The risk impact of the proposed TS changes was assessed
following the three-tiered approach recommended in RG 1.177. A
bounding risk assessment was performed to justify the proposed TS
changes. This application of LCO 3.0.9 is predicated upon the
licensee's performance of a risk assessment and the management of
plant risk. The net change to the margin of safety is insignificant
as indicated by the anticipated low levels of associated risk (ICCDP
and ICLERP) as shown in Table 1 of Section 3.1.1 in the Safety
Evaluation.
Therefore, this change does not involve a significant reduction
in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David G. Pettinari, Legal Department, 688
WCB, Detroit Edison Company, 2000 2nd Avenue, Detroit, Michigan 48226-
1279.
NRC Branch Chief: L. Raghavan.
Entergy Nuclear Operations, Inc., Docket No. 50-286, Indian Point
Nuclear Generating Unit No. 3, Westchester County, New York
Date of amendment request: January 18, 2007.
Description of amendment request: The proposed amendment would
revise the expiration limit for the reactor coolant system Pressure/
Temperature (P/T) limit graphs in Technical Specifications (TS); revise
the adjusted reference temperature for the reactor vessel; and revise
the Low Temperature Overpressure Protection (LTOP) arming temperature
value specified in TSs. It would also make editorial changes in the use
of inequality signs in TSs associated with the LTOP arming temperature
in order to make them consistent.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No
The proposed change does not affect the accident initiators or
mitigation assumptions associated with any of the accidents
previously evaluated. Operating restrictions on pressure-temperature
conditions for the reactor pressure vessel provide assurance that
reactor vessel integrity will be maintained under accident or
transient conditions. The proposed change uses approved criteria and
analysis methods to update the time period for which the current
operating limits remain valid.
The LTOP system performs an automatic function by opening relief
valves if reactor coolant system pressure reaches a temperature-
dependent limit. The proposed change includes establishing a more
restrictive temperature limit for when this system must be in
service, to reflect the material condition of the reactor vessel at
the new EFPY limit proposed for the pressure-temperature graphs. The
mitigation function and capability of the LTOP system is not being
changed by this request.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No
There are no new accident initiators being introduced by this
proposed change. The proposed change does not involve installation
of new plant equipment, modification of existing equipment, or
changes in the way that plant equipment is operated. Pressure-
temperature operating limits depicted by graphs in the technical
specifications will not be changed and will continue to be used by
plant operators. A change in the LTOP system arming temperature will
assure that the graphs remain valid for the proposed new operating
period of 27.2 EFPY [effective full power years].
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No
Operating limits on pressure and temperature conditions for the
reactor coolant system (RCS) are important to assure that the RCS
pressure boundary stresses are within analyzed limits. Margins of
safety are inherent in the analysis methods, assumptions, and limits
specified in regulations and guidance documents. The proposed change
is based on NRC-accepted methods, assumptions and limits and
maintains the required margin of safety.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this
[[Page 17947]]
review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. John Fulton, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 440 Hamilton Avenue, White Plains, NY
10601.
NRC Acting Branch Chief: Douglas V. Pickett.
Entergy Nuclear Operations, Inc., Docket Nos. 50-247 and 50-286, Indian
Point Nuclear Generating Unit Nos. 2 (IP2) and 3 (IP3), Westchester
County, New York
Date of amendment request: March 13, 2007.
Description of amendment request: The amendment would revise
License Condition 2.K for IP2 and License Condition 2.H for IP3, which
require the implementation and maintenance of an approved Fire
Protection Program for each unit.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No
The proposed changes are strictly an administrative relocation
of the specific fire protection SER [safety evaluation report]
references and do not modify any requirements of the fire protection
programs.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes are strictly an administrative relocation
of the specific fire protection SER references and do not modify any
requirements of the fire protection programs.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed changes are strictly an administrative relocation
of the specific fire protection SER references and do not modify any
requirements of the fire protection programs.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. John Fulton, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 440 Hamilton Avenue, White Plains, NY
10601.
NRC Acting Branch Chief: Douglas V. Pickett.
Entergy Nuclear Operations, Inc., Docket No. 50-247, Indian Point
Nuclear Generating Unit No. 2, Westchester County, New York
Date of amendment request: March 22, 2007.
Description of amendment request: The proposed amendment will
revise the test acceptance criteria specified in Technical
Specification Surveillance Requirement (SR) 3.8.1.10 for the diesel
generator endurance test.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
No. The proposed change revises the acceptance criteria to be
applied to an existing surveillance test of the facility emergency
diesel generators (DGs). Performing a surveillance test is not an
accident initiator and does not increase the probability of an
accident occurring. The proposed new acceptance criteria will assure
that the DGs are capable of carrying the peak electrical loading
assumed in the various existing safety analyses which take credit
for the operation of the DGs. Establishing acceptance criteria that
bound existing analyses validates the related assumption used in
those analyses regarding the capability of equipment to mitigate
accident conditions. Therefore the proposed change does not involve
a significant increase in the probability or consequences of an
accident previously evaluated.
2. Does the change create the possibility of a new or different
kind of accident from any accident previously evaluated?
No. The proposed change revises the test acceptance criteria for
a specific performance test conducted on the existing DGs. The
proposed change does not involve installation of new equipment or
modification of existing equipment, so no new equipment failure
modes are introduced. The proposed revision to the DG surveillance
test acceptance criteria also is not a change to the way that the
equipment or facility is operated and no new accident initiators are
created. Therefore the proposed change does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
No. The conduct of performance tests on safety-related plant
equipment is a means of assuring that the equipment is capable of
maintaining the margin of safety established in the safety analyses
for the facility. The proposed change in the DG technical
specification surveillance test acceptance criteria is consistent
with values assumed in existing safety analyses and is consistent
with the design rating of the DGs. Therefore the proposed change
does not involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. John Fulton, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 440 Hamilton Avenue, White Plains, NY
10601.
NRC Acting Branch Chief: Douglas V. Pickett.
Entergy Nuclear Operations, Inc., Docket No. 50-333, James A.
FitzPatrick Nuclear Power Plant, Oswego County, New York
Date of amendment request: February 15, 2007.
Description of amendment request: The proposed changes would revise
Technical Specification (TS) 3.10.1 to expand its scope to include
provisions for reactor coolant temperature excursions greater than 212
[deg]F as a consequence of inservice leak and hydrostatic testing, and
as a consequence of scram time testing initiated in conjunction with an
inservice leak or hydrostatic test, while considering operational
conditions to be in Mode 4, which is defined to be reactor coolant
temperature less than or equal to 212 [deg]F.
This change was proposed by the industry's TS Task Force (TSTF) and
is designated TSTF-484. The NRC staff issued a notice of opportunity
for comment in the Federal Register on August 21, 2006 (71 FR 48561),
on possible amendments concerning TSTF-484, including a model safety
evaluation and model no significant hazards (NSHC) determination, using
the consolidated line item improvement process (CLIIP). The NRC staff
subsequently issued a notice of availability of the models for
referencing in license amendment applications in the Federal Register
on October 27,
[[Page 17948]]
2006 (71 FR 63050). The licensee affirmed the applicability of the
following NSHC determination in its application dated February 15,
2007.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
Criterion 1: The proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
Technical Specifications currently allow for operation at
greater than 212 [deg]F while imposing MODE 4 requirements in
addition to the secondary containment requirements required to be
met. Extending the activities that can apply this allowance will not
adversely impact the probability or consequences of an accident
previously evaluated. Therefore, the proposed change does not
involve a significant increase in the probability or consequences of
an accident previously evaluated.
Criterion 2: The proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
Technical Specifications currently allow for operation at
greater than 212 [deg]F while imposing MODE 4 requirements in
addition to the secondary containment requirements required to be
met. No new operational conditions beyond those currently allowed by
LCO 3.10.1 are introduced. The changes do not involve a physical
alteration of the plant (i.e., no new or different type of equipment
will be installed) or a change in the methods governing normal plant
operation. In addition, the changes do not impose any new or
different requirements or eliminate any existing requirements. The
changes do not alter assumptions made in the safety analysis. The
proposed changes are consistent with the safety analysis assumptions
and current plant operating practice. Therefore, the proposed change
does not create the possibility of a new or different kind of
accident from any accident previously evaluated.
Criterion 3: The proposed change does not involve a significant
reduction in a margin of safety.
Technical Specifications currently allow for operation at
greater than 212 [deg]F while imposing MODE 4 requirements in
addition to the secondary containment requirements required to be
met. Extending the activities that can apply this allowance will not
adversely impact any margin of safety. Allowing completion of
inspections and testing and supporting completion of scram time
testing initiated in conjunction with an inservice leak or
hydrostatic test prior to power operation results in enhanced safe
operations by eliminating unnecessary maneuvers to control reactor
temperature and pressure. Therefore, the proposed change does not
involve a significant reduction in a margin of safety.
Based on the above, the NRC staff concludes that the proposed
change presents no significant hazards consideration under the
standards set forth in 10 CFR 50.92(c), and, accordingly, a finding of
no significant hazards consideration is justified.
Attorney for licensee: Mr. John Fulton, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 440 Hamilton Avenue, White Plains, NY
10601.
NRC Acting Branch Chief: Douglas V. Pickett.
Exelon Generation Company, LLC (EGC), Docket Nos. 50-373 and 50-374,
LaSalle County Station (LSCS), Units 1 and 2, LaSalle County, Illinois
Date of amendment request: November 17, 2006.
Description of amendment request: The proposed amendments would
replace references to Section XI of the American Society of Mechanical
Engineers (ASME) Boiler and Pressure Vessel Code (Code) with a
reference to the ASME Code of Operation and Maintenance of Nuclear
Power Plants (OM Code) in Technical Specification (TS) 5.5.7,
``Inservice Testing Program [IST].'' These proposed changes are
consistent with the implementation of the LSCS, Units 1 and 2 third 10-
year IST program in accordance with the requirements of Title 10 of the
Code of Federal Regulations (10 CFR) Section 50.55a, ``Codes and
standards,'' paragraph (f), ``Inservice testing requirements.'' The
third 10-year interval for LSCS, Units 1 and 2 is scheduled to start on
October 12, 2007.
In addition to the replacement of the references, EGC is also
adding provisions in TS 5.5.7, item b, to only apply Surveillance
Requirement (SR) 3.0.2 to those inservice testing frequencies of two
years or less. These proposed changes are based on TS Task Force (TSTF)
Traveler No. 479-A (TSTF-479-A), Revision 0, ``Changes to Reflect
Revision of 10 CFR 50.55a,'' as modified by TSTF-497, Revision 0,
``Limit Inservice Testing Program SR 3.0.2 Application to Frequencies
of 2 Years or Less'' and approved by the NRC in December 6, 2005, and
October 4, 2006.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes revise TS 5.5.7 for LSCS Units 1 and 2 to
conform to the requirements of 10 CFR 50.55a, ``Codes and
standards,'' paragraph (f) regarding the inservice testing of pumps
and calves for the Third 10-year Interval. The current TS reference
the [American Society of Mechanical Engineers] ASME Boiler and
Pressure Vessel Code, Section XI, requirements for the inservice
testing of ASME Code Class 1, 2, and 3 pumps and valves. The
proposed changes would reference the ASME OM Code, which is
consistent with 10 CFR 50.55a, paragraph (f), ``Inservice testing
requirements,'' and approved for use by the NRC. In addition,
provisions modifying TS 5.5.7, item b, clarify that SR 3.0.2 is only
applied to those inservice testing frequencies of two years or less.
The definitions of the frequencies are not changed by this license
amendment request.
The proposed changes are administrative in nature, do not affect
any accident initiators, do not affect the ability of LSCS to
successfully respond to previously evaluated accidents and do not
affect radiological assumptions used in the evaluations. Thus, the
radiological consequences of any accident previously evaluated are
not increased.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the change create the possibility of a new or different
kind of accident from any accident previously evaluated?
Response: No.
The proposed changes revise TS 5.5.7 for LSCS Units 1 and 2 to
conform to the requirements of 10 CFR 50.55a(f) regarding the
inservice testing of pumps and valves for the Third 10-year
Interval. The current TS reference the ASME Boiler and Pressure
Vessel Code, Section XI, requirements for the inservice testing of
ASME Code Class 1, 2, and 3 pumps and valves. The proposed changes
would reference the ASME OM Code, which is consistent with the 10
CFR 50.55a(f) and approved for use by the NRC. In addition,
provisions modifying TS 5.5.7, item b, clarify that SR 3.0.2 is only
applied to those inservice testing frequencies of two years or less.
The definitions of the frequencies are not changed by this license
amendment request.
The proposed changes to TS Section 5.5.7 do not affect the
performance of any LSCS structure, system, or component credited
with mitigating any accident previously evaluated and do not
introduce any new modes of system operation or failure mechanisms.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Does the change involve a significant reduction in a margin
of safety?
Response: No.
The proposed changes revise TS 5.5.7 for LSCS Units 1 and 2 to
conform to the requirements of 10 CFR 50.55a(f) regarding the
inservice testing of pumps and valves for the Third 10-Year
Interval. The current TS reference the ASME Boiler and Pressure
Vessel Code, Section XI, requirements for the inservice testing of
ASME Code Class 1, 2,
[[Page 17949]]
and 3 pumps and valves. The proposed changes would reference the
ASME OM Code, which is consistent with the 10 CFR 50.55a(f) and
approved for use by the NRC. In addition, provisions modifying TS
5.5.7, item b, clarify that SR 3.0.2 is only applied to those
inservice testing frequencies of two years or less. The definitions
of the frequencies are not changed by this license amendment
request.
The proposed changes do not modify the safety limits setpoints
at which protective actions are initiated and do not change the
requirements governing operation or availability of safety equipment
assumed to operate to preserve the margin of safety.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Bradley J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Kennett
Square, PA 19348.
NRC Branch Chief: Russell Gibbs.
Exelon Generation Company, LLC, Docket Nos. 50-352 and 50-353, Limerick
Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
Date of amendment request: June 2, 2006.
Description of amendment request: The proposed amendments
incorporates revised 10 CFR Part 20 requirements for Limerick
Generating Station Units 1 and 2 technical specifications (TSs).
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
Updating the Technical Specifications (TS) to be consistent with
10 CFR Part 20 has no impact on plant structures, systems, or
components, does not affect any accident initiators, and does not
change any safety analysis. Therefore, the proposed changes do not
involve an increase in the probability or consequences of an
accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
Updating the TS to be consistent with 10 CFR Part 20 will not
change any equipment, require new equipment to be installed, or
change the way current equipment operates. No credible new failure
mechanisms, malfunctions, or accident initiators are created by the
proposed changes.
Therefore, the changes do not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
Updating the TS to be consistent with 10 CFR Part 20 does not
adversely affect existing plant safety margins or the reliability of
equipment assumed to operate in the safety analysis. As such, there
are no changes being made to safety analysis assumptions, safety
limits or limiting safety system settings that would adversely
affect plant safety as a result of the proposed changes. Therefore,
the proposed changes do not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. Brad Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200 Exelon Way, Kennett Square, PA
19348.
NRC Branch Chief: Harold K. Chernoff.
FirstEnergy Nuclear Operating Company, et al., Docket No. 50-346,
Davis-Besse Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
Date of amendment request: February 12, 2007.
Description of amendment request: The proposed license amendment
would revise Technical Specification (TS) Limiting Condition for
Operation 3.9.4, ``Containment Penetrations'', to allow penetrations
included under TS 3.9.4(c) to be opened during core alterations or
movement of irradiated fuel, under administrative controls. This change
is based on the TS Task Force Traveler No. 312-A, Revision 1.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change would allow containment penetrations
identified under Technical Specification 3.9.4(c) to remain open
during fuel movement and core alterations. These penetrations are
normally closed during this time period to prevent the release of
radioactive material in the event of a Fuel Handling Accident inside
containment. These penetrations are not initiators of any accident.
The probability of a Fuel Handling Accident is unaffected by the
status of these penetrations.
The Fuel Handling Accident analyses demonstrate that the maximum
offsite dose is well [within] the acceptance limits specified in SRP
[Standard Review Plan] 15.7.4, and the control room dose is within
the acceptance criteria specified in GDC [General Design Criterion]
19. Furthermore, the existing analysis results are independent of
the containment release path, and therefore are unaffected by the
proposed change.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed change does not involve the addition or
modification of any plant equipment. Also, the proposed change will
not alter the design, configuration, or method of operation of the
plant beyond the standard functional capabilities of the equipment.
The proposed change involves a Technical Specification change that
will allow containment penetrations identified under Technical
Specification 3.9.4(c) to remain open during fuel movement and core
alterations. Open penetrations are not accident initiators, and will
not create the possibility of a new kind of accident. Administrative
controls will be implemented to ensure the capability to close the
affected containment penetrations in the event of a Fuel Handling
Accident.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed change has the potential to slightly increase the
post-Fuel Handling Accident dose at the site boundary and in the
control room. However, the existing analyses take no credit for
containment of the release, so that the existing analysis results
will remain bounding.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David W. Jenkins, Attorney, FirstEnergy
Corporation, Mail Stop A-GO-18, 76 South Main Street, Akron, OH 44308.
NRC Branch Chief: Russell Gibbs.
[[Page 17950]]
FirstEnergy Nuclear Operating Company, et al., Docket No. 50-440, Perry
Nuclear Power Plant, Unit No. 1, Lake County, Ohio
Date of amendment request: January 19, 2007.
Description of amendment request: The proposed amendment would
modify Technical Specification (TS) 5.5.9, ``Diesel Fuel Oil Testing
Program,'' by relocating a reference to a specific American Society for
Testing and Materials (ASTM) international standard for fuel oil
testing to licensee-controlled documents, and by adding an alternate
criteria to the ``clear and bright'' acceptance test for new fuel oil,
per the consolidated line item improvement process (CLIIP).
The U.S. Nuclear Regulatory Commission (NRC) staff issued a notice
of opportunity for comment in the Federal Register on February 22, 2006
(71 FR 9179), on possible amendments concerning the CLIIP, including a
model safety evaluation and a model no significant hazards
consideration determination. The NRC staff subsequently issued a notice
of availability of the models for referencing in license amendment
applications in the Federal Register on April 21, 2006 (71 FR 20735),
as part of the CLIIP.
In its application dated January 19, 2007, the licensee affirmed
the applicability of the following determination.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of any accident previously
evaluated?
Response: No.
The proposed changes relocate the specific ASTM standard
references from the Administrative Controls Section of TS to a
licensee-controlled document. Requirements to perform testing in
accordance with applicable ASTM standards are retained in the TS as
are requirements to perform surveillances of both new and stored
diesel fuel oil. Future changes to the licensee-controlled document
will be evaluated pursuant to the requirements of 10 CFR 50.59,
``Changes, tests and experiments,'' to ensure that such changes do
not result in more than a minimal increase in the probability or
consequences of an accident previously evaluated. In addition, the
``clear and bright'' test used to establish the acceptability of new
fuel oil for use prior to addition to storage tanks has been
expanded to recognize more rigorous testing of water and sediment
content. Relocating the specific ASTM standard references from the
TS to a licensee-controlled document and allowing a water and
sediment content test to be performed to establish the acceptability
of new fuel oil will not affect nor degrade the ability of the
emergency diesel generators (DGs) to perform their specified safety
function. Fuel oil quality will continue to meet ASTM requirements.
The proposed changes do not adversely affect accident initiators
or precursors nor alter the design assumptions, conditions, and
configuration of the facility or the manner in which the plant is
operated and maintained. The proposed changes do not adversely
affect the ability of structures, systems, and components (SSCs) to
perform their intended safety function to mitigate the consequences
of an initiating event within the assumed acceptance limits. The
proposed changes do not affect the source term, containment
isolation, or radiological release assumptions used in evaluating
the radiological consequences of any accident previously evaluated.
Further, the proposed changes do not increase the types and amounts
of radioactive effluent that may be released offsite, nor
significantly increase individual or cumulative occupational/public
radiation exposures.
Therefore, the changes do not involve a significant increase in
the probability or consequences of any accident previously
evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes relocate the specific ASTM standard
references from the Administrative Controls Section of TS to a
licensee-controlled document. In addition, the ``clear and bright''
test used to establish the acceptability of new fuel oil for use
prior to addition to storage tanks has been expanded to allow a
water and sediment content test to be performed to establish the
acceptability of new fuel oil. The changes do not involve a physical
alteration of the plant (i.e., no new or different type of equipment
will be installed) or a change in the methods governing normal plant
operation. The requirements retained in the TS continue to require
testing of the diesel fuel oil to ensure the proper functioning of
the DGs.
Therefore, the changes do not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed changes relocate the specific ASTM standard
references from the Administrative Controls Section of TS to a
licensee-controlled document. Instituting the proposed changes will
continue to ensure the use of applicable ASTM standards to evaluate
the quality of both new and stored fuel oil designated for use in
the emergency DGs.
Changes to the licensee-controlled document are performed in
accordance with the provisions of 10 CFR 50.59. This approach
provides an effective level of regulatory control and ensures that
diesel fuel oil testing is conducted such that there is no
significant reduction in a margin of safety.
The ``clear and bright'' test used to establish the
acceptability of new fuel oil for use prior to addition to storage
tanks has been expanded to allow a water and sediment content test
to be performed to establish the acceptability of new fuel oil. The
margin of safety provided by the DGs is unaffected by the proposed
changes since there continue to be TS requirements to ensure fuel
oil is of the appropriate quality for emergency DG use. The proposed
changes provide the flexibility needed to improve fuel oil sampling
and analysis methodologies while maintaining sufficient controls to
preserve the current margins of safety.
The NRC staff proposes to determine that the amendment request
involves no significant hazards consideration.
Attorney for licensee: David W. Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street, Akron, OH 44308.
NRC Branch Chief: Russell A. Gibbs
Florida Power Corporation, et al., Docket No. 50-302, Crystal River
Unit 3 Nuclear Generating Plant (CR-3), Citrus County, Florida
Date of amendment request: December 14, 2006, as supplemented by
letter dated March 14, 2007.
Description of amendment request: The proposed amendment would
modify the technical specification (TS) requirements for inoperable
snubbers by adding Limiting Condition for Operation (LCO) 3.0.8. The
changes are consistent with NRC approved Industry/Technical
Specification Task Force (TSTF) standard TS change TSTF-372, Revision
4.
The proposed amendment includes an administrative change to LCO
3.0.1 that will clarify that LCO 3.0.7 allows specified TS requirements
to be suspended during physics tests performed in accordance with TSs
3.1.8 and 3.1.9. This administrative change will make the CR-3 TSs more
consistent with the standard TSs and with TSTF-372, Revision 4.
The NRC staff issued a notice of availability of a model safety
evaluation and model no significant hazards consideration (NSHC)
determination for referencing in license amendment applications in the
Federal Register on May 4, 2005 (70 FR 23252). The licensee affirmed
the applicability of the model NSHC determination in its application
dated April 26, 2006.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
[[Page 17951]]
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change allows a delay time before declaring
supported TS systems inoperable when the associated snubber(s)
cannot perform its required safety function. Entrance into Actions
or delaying entrance into Actions is not an initiator of any
accident previously evaluated. Consequently, the probability of an
accident previously evaluated is not significantly increased. The
consequences of an accident while relying on the delay time allowed
before declaring a TS supported system inoperable and taking its
Conditions and Required Actions are no different than the
consequences of an accident under the same plant conditions while
relying on the existing TS supported system Conditions and Required
Actions. Therefore, the consequences of an accident previously
evaluated are not significantly increased by this change. Therefore,
this change does not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change allows a delay time before declaring
supported TS systems inoperable when the associated snubber(s)
cannot perform its required safety function. The proposed change
does not involve a physical alteration of the plant (no new or
different type of equipment will be installed) or a change in the
methods governing normal plant operations. Thus, this change does
not create the possibility of a new or different kind of accident
from any accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change allows a delay time before declaring
supported TS systems inoperable when the associated snubber(s)
cannot perform its required safety function. The proposed change
restores an allowance in the pre-ISTS [improved Standard Technical
Specifications] conversion TS that was unintentionally eliminated by
the conversion. The pre-ISTS TSs were considered to provide an
adequate margin of safety for plant operation, as does the post-ISTS
conversion TS. Therefore, this change does not involve a significant
reduction in a margin of safety.
The NRC staff proposes to determine that the amendment request
involves no significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Branch Chief: Thomas H. Boyce.
PSEG Nuclear LLC, Docket Nos. 50-272 and 50-311, Salem Nuclear
Generating Station, Unit Nos. 1 and 2, Salem County, New Jersey
Date of amendment request: March 16, 2007.
Description of amendment request: The proposed amendment would add
new Technical Specification (TS) requirements for the response times
associated with a steam generator feedwater pump (SGFP) trip and
feedwater isolation valve (FIV) closure. The amendment would also
revise the TS requirements for the containment fan cooler unit (CFCU)
cooling water flow rate. These changes are associated with a revised
containment response analysis that credits a SGFP trip and FIV closure
(on a feedwater regulator valve failure) to reduce the mass/energy
release to the containment during a main steam line break (MSLB). The
containment analysis also credits a reduced heat removal capability for
the CFCUs, allowing a reduction in the required service water (SW) flow
to the CFCUs.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change does not involve a significant increase in
the probability or consequences of an accident previously evaluated.
The proposed change establishes response time requirements for
feedwater isolation and reduced CFCU flow rates to support
containment analyses to accommodate reduced CFCU heat removal
capacity. The changes in analysis input assumptions affect plant
response to an accident and are not accident initiators; therefore,
they have no bearing on the probability of an accident. The Salem
FSAR [Final Safety Analysis Report] Chapter 15 accidents which are
impacted by a change in the CFCU modeling parameters are LOCA [loss-
of-coolant accident] and MSLB mass and energy release Containment
analyses. The consequences of these postulated accidents are shown
to be acceptable using assumptions consistent with the proposed
changes.
For the LOCA transients, the containment cooling systems are
considered for three aspects: core response, containment response
and dose. The core response is most limiting when the containment
conditions minimize back pressure since this increases the blowdown
and reduces the effectiveness of the ECCS [emergency core cooling
system]. The LOCA core response (10 CFR 50.46 [Section 50.46 of
Title 10 of the Code of Federal Regulations]--PCT [peak cladding
temperature]) is conservatively biased to minimize the containment
backpressure such that any safety injection effectiveness is
minimized (the core becomes the highest resistance flow path). Thus,
any reduction in the accident capability of the CFCUs has no bearing
on the LOCA core response.
The bounding containment integrity analyses are the LBLOCA
[large-break LOCA] and the MSLB Inside Containment events. The
containment integrity analysis relies on two heat removal paths to
maintain containment pressure and temperature conditions. The CFCU
air-to-water heat exchangers reject containment energy to the SW
System and the Containment Spray System removes containment energy
by using spray droplet direct contact heat exchange to transfer the
energy from the containment ambient to the containment sump, where
it is transferred out of containment via the RHR [residual heat
removal] heat exchanger and CCW [component cooling water]/SW
Systems. Containment integrity analyses for both LOCA and MSLB,
using input assumptions consistent with the proposed changes, show
that containment integrity is maintained with reduced CFCU heat
removal capacity.
The potential dose impacts due to reduced CFCU heat removal
capacity are bounded as the design basis assumptions concerning the
number of operating CFCUs (three of five), and the thermal-hydraulic
transient operation of the Containment Spray System are unchanged.
The Salem design basis only credits Containment Spray iodine removal
effectiveness during the LOCA injection and recirculation phases
based on a single failure of an entire ESF [engineered safety
features] train. This assumption results in 3 of 5 CFCUs being
available to ensure adequate mixing of the containment ambient air
as well as operation of a single Containment Spray Train, which
controls containment spray droplet size and pH, as described in
UFSAR [updated FSAR] Section 6.2.3. As a further conservatism, the
current LOCA Alternate Source Term (AST) analysis (Calculation S-C-
ZZ-MDC-1945, an interim revision of which was sent to the NRC
[Nuclear Regulatory Commission] staff for review via letter dated
September 16, 2004) only credits two CFCUs for mixing. The
Containment Building and Auxiliary Building leakage rates are
unaffected by the revised containment analysis as the peak
containment pressure and temperatures are less than the design basis
values described in the Salem UFSAR. Therefore, there is no impact
on offsite dose rates due to the reduced CFCU heat removal capacity.
One other high energy line break for consideration is the
rupture of a feedwater line break. From a containment response
aspect, this event is bounded by the MSLB event, so it is not
explicitly analyzed (or even discussed in the Salem UFSAR).
A review of the Salem design basis for AST dose calculations
shows that the revised Containment Integrity Analysis, WCAP-16503,
does not challenge any of the assumptions that are part of the AST
design basis.
Section 6.2 of the UFSAR indicates that the Appendix J Type A
containment leak rate test
[[Page 17952]]
pressure is based on the containment design pressure of 47.0 psig,
not the calculated accident pressure. Since the design pressure
value bounds the peak pressure calculated in WCAP-16503 and is not
being changed, the Appendix J testing requirements are not impacted.
Thus, in conclusion, the proposed change does not involve a
significant increase in the probability or consequences of an
accident previously evaluated. The proposed change modifies response
time requirements for feedwater isolation, and reduces CFCU flow
rates and heat removal requirements consistent with the new
containment analysis.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change does no