Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 6780-6795 [E7-2323]
Download as PDF
6780
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
ASSISTANCE PROVIDED UNDER SECTION 605—Continued
Projects
Obligated
Quarterly disbursements
Objectives
Access to Land .................
$36,020,000
Strengthen property rights
and increase investment in rural and urban
land.
$0
Access to Markets ............
$168,020,000
$0
Program Administration*,
Due Diligence, Monitoring and Evaluation.
To be allocated** ..............
$22,370,000
Improve Access to Markets through Improvements to the Port of
Cotonou.
..........................................
..........................................
Improve enterprise registration center.
Value of investments made to rural land parcels per
year; land investment data will come from self-reported data through EMICoV.
Value of investments made to urban land parcels
per year; land investment data will come from
self-reported data through EMICoV.
Total volume of exports and imports passing
through Port of Cotonou, per year in million metric
tons.
$0
$0
Measures
$2,097,000
619 Transfer Funds
U.S. Agency to which funds were
transferred
Amount
USAID ..................................................
Country
$149,670,094
Description of program or project
.....................................
Threshold Program.
*Program administration funds are used to pay items such as salaries, rent, and the cost of office equipment.
**These amounts represent disbursements made that will be allocated to individual projects in the subsequent quarter(s) and reported as such
in subsequent quarterly report(s).
Dated: February 7, 2007.
Frances C. McNaught,
Vice President, Congressional & Public
Affairs, Millennium Challenge Corporation.
[FR Doc. E7–2447 Filed 2–12–07; 8:45 am]
BILLING CODE 9211–01–P
NATIONAL TRANSPORTATION
SAFETY BOARD
NUCLEAR REGULATORY
COMMISSION
Sunshine Act Meeting
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
Agenda
9:30 a.m., Wednesday,
February 21, 2007.
TIME AND DATE:
NATIONAL CREDIT UNION
ADMINISTRATION
NTSB Conference Center, 429
L’Enfant Plaza SW., Washington, DC
20594.
PLACE:
Sunshine Act Meeting
10 a.m., Thursday,
February 15, 2007.
PLACE: Board Room, 7th Floor, Room
7047, 1775 Duke Street, Alexandria, VA
22314–3428.
STATUS: Open.
MATTERS TO BE CONSIDERED:
1. Quarterly Insurance Fund Report.
2. Report to Congress on the Study of
Possible Changes to the Deposit
Insurance System.
3. Appeal from Delaware Federal
Credit of the Regional Director’s Denial
of Conversion from a Multiple Common
Bond to a Community Charter.
4. Final Rule: Part 701 of NCUA’s
Rules and Regulations, General Lending
Maturity Limit and Other Financial
Services.
FOR FURTHER INFORMATION CONTACT:
Mary Rupp, Secretary of the Board,
Telephone: 703–518–6304.
jlentini on PROD1PC65 with NOTICES
TIME AND DATE:
STATUS:
The one item is open to the
public.
7774A:
Highway Accident Report—Motorcoach
Fire on Interstate 45 During Hurricane
Rita Evacuation, Near Wilmer, Texas,
September 23, 2005.
MATTER TO BE CONSIDERED:
Public Affairs,
Telephone: (202) 314–6100.
Individuals requesting specific
accommodations should contact Chris
Bisett at (202) 314–6305 by Friday,
February 16, 2007.
The public may view the meeting via
a live or archived webcast by accessing
a link under ‘‘News & Events’’ on the
NTSB home page at www.ntsb.gov.
NEWS MEDIA CONTACT:
FOR FURTHER INFORMATION CONTACT:
Vicky D’Onofrio, (202) 314–6410.
Mary Rupp,
Secretary of the Board.
[FR Doc. 07–653 Filed 2–8–07; 4:20 pm]
Dated: February 9, 2007.
Vicky D’Onofrio,
Federal Register Liaison Officer
[FR Doc. 07–682 Filed 2–9–07; 1:53 pm]
BILLING CODE 7535–01–M
BILLING CODE 7533–01–M
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
PO 00000
Frm 00073
Fmt 4703
Sfmt 4703
I. Background
Pursuant to section 189a. (2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from January 19,
2007, to February 1, 2007. The last
biweekly notice was published on
January 30, 2007 (72 FR 4304).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
E:\FR\FM\13FEN1.SGM
13FEN1
jlentini on PROD1PC65 with NOTICES
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rulemaking,
Directives and Editing Branch, Division
of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
PO 00000
Frm 00074
Fmt 4703
Sfmt 4703
6781
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
E:\FR\FM\13FEN1.SGM
13FEN1
6782
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
condensate flow switch from Technical
Specification (TS) 3.4.5.1, ‘‘Reactor
Coolant System Leakage—Leakage
Detection Instrumentation,’’ and to
modify or delete associated actions.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
jlentini on PROD1PC65 with NOTICES
(1) first class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)7ndash;(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The Reactor Coolant System (RCS) leakage
detection systems are passive monitoring
systems therefore the proposed changes do
not affect reactor operations or accident
analyses and have no radiological
consequences. The proposed change
continues to require diverse methods of
monitoring leakage. The gaseous
radioactivity monitor, although not included
in the TSs and the CFC condensate flow
switches, which are proposed for removal
from the TSs, will be maintained functional
and available.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change introduces no new
mode of plant operation or any plant
modification. The RCS leakage detection
instrumentation is used solely for monitoring
purposes and is not part of plant control
instruments or engineered safety feature
actuation circuits. The change does not vary
or affect any plant operating condition or
parameter.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change does not modify any
of the RCS leakage detection instrumentation.
The proposed change continues to require
diverse methods of monitoring leakage. In
addition, although not required by TS,
multiple means of diverse monitoring RCS
leakage will remain functional and available.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
Entergy Operations Inc., Docket No. 50–
382, Waterford Steam Electric Station,
Unit 3, St. Charles Parish, Louisiana
Date of amendment request:
September 26, 2006.
Description of amendment request:
The proposed change deletes reference
to the containment fan cooler (CFC)
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
PO 00000
Frm 00075
Fmt 4703
Sfmt 4703
Attorney for licensee: Terence A.
Burke, Associate General Council—
Nuclear Entergy Services, Inc., 1340
Echelon Parkway, Jackson, Mississippi
39213.
NRC Branch Chief: David Terao.
Entergy Operations, Inc., System Energy
Resources, Inc., South Mississippi
Electric Power Association, and Entergy
Mississippi, Inc., Docket No. 50–416,
Grand Gulf Nuclear Station, Unit 1,
Claiborne County, Mississippi
Date of amendment request: January
18, 2007.
Description of amendment request:
The proposed change will revise the
description of Grand Gulf Nuclear
Station Technical Specification 4.2.2,
‘‘Control Rod Assemblies,’’ to allow to
the use of hafnium as an additional type
of control material.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The NRC has specifically approved the use
of hafnium as neutron absorbing material for
use in BWR [boiling-water reactor] control
rod assemblies. The use of hafnium in
control rods as a neutron absorber material
does not significantly alter the neutronic or
mechanical functional characteristics of the
control rods. Control rod designs using
hafnium have been successfully used in other
BWRs. Since control rods that utilize
hafnium have a longer lifetime, the
probability of some accidents involving the
handling, on-site storage, and shipping of
irradiated rods will actually be reduced. The
proposed change does not alter the required
number of control rods nor does it affect any
of the specifications related to the control
rods (e.g., the shutdown margin and scram
timing requirements are unaffected).
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The application of a control rod design
using hafnium as an absorber material does
not produce any new mode of plant
operation or alter the control rods in such a
way as to affect their function or operability
since the new control rods are designed to be
compatible with the existing control rods.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
E:\FR\FM\13FEN1.SGM
13FEN1
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change does not significantly
affect the neutronic or mechanical
characteristics of the control rods since the
hafnium containing controls rods are
designed to be compatible with the existing
design and reload licensing criteria;
therefore, there is no significant change in
the margin of safety. It does not change the
required number of existing control rods. It
does not affect the existing Technical
Specifications related to control rods (e.g.,
required shutdown margin and scram time,
etc.).
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Terence A.
Burke, Associate General Council—
Nuclear Entergy Services, Inc., 1340
Echelon Parkway, Jackson, Mississippi
39213.
NRC Branch Chief: David Terao.
jlentini on PROD1PC65 with NOTICES
Florida Power Corporation, et al.,
Docket No. 50–302, Crystal River Unit 3
Nuclear Generating Plant (CR–3), Citrus
County, Florida
Date of amendment request: October
11, 2006.
Description of amendment request:
The proposed amendment would
modify the plant Improved Technical
Specifications (ITSs) to implement a
more conservative requirement in ITS
3.7.7, ‘‘Nuclear Services Closed Cycle
Cooling Water (SW) System.’’ The
current Action A allows the plant to
operate for up to 72 hours before
initiating a shutdown when one
required SW heat exchanger is
inoperable. The proposed revision will
only allow operation to continue for 8
hours before initiating a shutdown
when one required SW heat exchanger
is inoperable.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
(1) Does not involve a significant increase
in the probability or consequences of an
accident previously evaluated.
The limiting design basis accident for CR–
3 includes, as an assumption, adequate heat
removal capability by the SW system. The
amendment is being proposed to ensure the
SW system performs its design basis
function. Adequate heat removal is provided
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
by three OPERABLE SW heat exchangers.
The 8 hour completion time will reduce the
window that the plant can operate with only
two SW heat exchangers before a shutdown
is required. The proposed change does not
increase the probability of an accident
previously evaluated since the amendment is
not a modification to plant systems, nor a
change to plant operation that could initiate
an accident. Therefore, granting the LAR
[license amendment request] does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated. The dose consequences
of all design basis accidents are unchanged
by this proposed amendment.
(2) Does not create the possibility of a new
or different kind of accident from any
accident previously evaluated?
The function of the SW system considered
in the design basis is to remove process and
operating heat from safety-related
components during normal as well as
transient conditions. The proposed
amendment to limit the allowed ACTION
Completion Time to 8 hours will ensure the
function of the SW system is consistent with
the design basis and will not result in
changes to the design, physical configuration
of the plant or the assumptions made in the
safety analysis. The requirement does not
change the function of the system nor its
ability to perform its design function. No
alteration to plant configuration or operation
is proposed. Therefore, the proposed change
will not create the possibility of a new or
different kind of accident from any
previously evaluated.
(3) Does not involve a significant reduction
in a margin of safety?
CR–3’s design basis considers adequate
heat removal by the SW system to cool the
containment fan assembly cooling coils and
fan motors, spent fuel pool, SW pump motors
and other equipment which must function
following an accident. This proposed
amendment will not alter the current design
basis. By limiting the allowed ACTION
Completion Time to 8 hours, the proposed
amendment to ITS 3.7.7 will limit the time
the safety function of the SW system can be
compromised. Therefore, the amendment
does not result in a reduction of the margin
of safety.
The NRC staff has reviewed the
analysis provided for Florida Power
Corporation and, based on this review,
it appears that the three standards of 10
CFR 50.92(c) are satisfied. Therefore, the
NRC staff proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Branch Chief (Acting): Margaret
H. Chernoff.
PO 00000
Frm 00076
Fmt 4703
Sfmt 4703
6783
GPU Nuclear, Inc., Docket No. 50–320,
Three Mile Island Nuclear Station, Unit
2, Dauphin County, Pennsylvania
Date of amendment request:
December 13, 2006.
Description of amendment requests:
The amendment application proposes to
delete Technical Specification (TS)
6.8.1.3, which provides the requirement
for submittal of the annual occupational
radiation exposure report.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated? No
The proposed change eliminates the
Technical Specification reporting
requirement for occupational radiation
exposure information, which is in excess to
that required to be submitted by regulations.
The proposed change involves no changes to
plant systems or accident analyses. As such,
the change is administrative in nature and
does not affect initiators of analyzed events
or assumed mitigation of accidents.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated? No
The proposed change does not involve a
physical alteration of the plant, add any new
equipment, or require any existing
equipment to be operated in a manner
different from the present design. Therefore,
the proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
No
This change is an administrative change to
reporting requirements of occupational
radiation exposure data and will not reduce
a margin of safety because it has no effect on
any safety analyses assumptions. Hence, this
change is administrative in nature. For these
reasons, the proposed change does not
involve a significant reduction in the margin
of safety.
The NRC staff has reviewed the
licensee’s analysis, and based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
NRC Branch Chief: Claudia Craig.
E:\FR\FM\13FEN1.SGM
13FEN1
6784
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
jlentini on PROD1PC65 with NOTICES
Nuclear Management Company, LLC,
Docket Nos. 50–266 and 50–301, Point
Beach Nuclear Plant, Units 1 and 2,
Town of Two Creeks, Manitowoc
County, Wisconsin
Date of amendment request:
December 21, 2006.
Description of amendment request:
The proposed amendment revises the
licensing basis to reflect a revision to
the spent fuel pool criticality analysis
methodology and a new criticality
analysis. In addition, associated changes
are proposed to Technical
Specifications 3.7.12, ‘‘Spent Fuel
Storage,’’ and 4.3.1, ‘‘Criticality,’’ to
reflect the results of the new criticality
analysis.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
(1) Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No
Operation of the facility in accordance
with the proposed amendment request does
not involve a significant increase in the
probability or consequences of an accident
previously evaluated. The presence of
soluble boron in the Spent Fuel Pool (SFP)
water being used for criticality control does
not increase the probability of a dropped fuel
assembly accident within the pool. The
handling of the fuel assemblies in the SFP
has always been performed and will continue
to be performed in borated water.
There is no increase in the probability of
the accidental misloading of fuel assemblies
into the SFP fuel storage racks when
considering the presence of soluble boron in
the pool water for criticality control. Fuel
assembly placement will continue to be
controlled pursuant to approved fuel
handling procedures and in accordance with
the spent fuel storage rack limitations
specified in the Technical Specifications
(TS). There is no increase in the
consequences for an accidental misloading of
fuel assemblies in the SFP fuel storage racks
because the criticality analyses demonstrate
that the pool will remain subcritical
following an accidental misloading.
Soluble boron credit is used to provide
margin to offset uncertainties, tolerances, and
off-normal/accident conditions, and to
provide subcritical margin such that the SFP
keff [effective neutron multiplication
constant] is maintained less than or equal to
0.95. The plant-specific criticality analysis
results demonstrate that the spent fuel rack
keff will remain<1.0 (at a 95/95 percent
probability and confidence level) even with
the SFP flooded with unborated water.
There is no increase in the probability of
the loss of normal cooling to the SFP water
when considering the presence of soluble
boron in the pool water for subcriticality
control since a high concentration of soluble
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
boron has always been maintained in the SFP
water.
A loss of normal cooling to the SFP water
causes an increase in the temperature of the
water passing through the stored fuel
assemblies. This causes a decrease in water
density, which would result in a net increase
in reactivity when soluble boron is present in
the water. However, the additional negative
reactivity provided by the 2100 ppm [parts
per million] boron concentration limit, above
that provided by the concentration required
(805 ppm) to maintain keff less than or equal
to 0.95, will compensate for the increased
reactivity which could result from a loss of
SFP cooling event. Because adequate soluble
boron will be maintained in the SFP water
the consequences of a loss of normal cooling
to the SFP will not be increased.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
(2) Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No
Under the proposed amendment, no
changes are being made to the fuel storage
racks themselves, to any other systems, or to
the physical structures of the Primary
Auxiliary Building. Therefore, there are no
changes proposed to the plant configuration,
equipment design, or installed equipment.
Criticality accidents in the SFP are not new
or different types of accidents. They have
been analyzed in the FSAR [Final Safety
Analysis Report] and in fuel storage
criticality analysis reports associated with
specific licensing amendments. The
proposed new SFP storage limitations are
consistent with the assumptions made in the
new criticality analysis, and will not have
any significant effect on normal SFP
operations and maintenance, and do not
create the possibility of a new or different
kind of accident. Verifications will continue
to be performed to ensure that the SFP
loading configuration meets specified
requirements.
The current TS includes a SFP boron
concentration limit that conservatively
bounds the boration assumption of the new
criticality analysis. Since soluble boron has
always been maintained in the SFP water,
implementation of this requirement for SFP
criticality control purposes has have no effect
on normal pool operations and maintenance.
Also, since soluble boron has always been
present in the SFP, a dilution event has
always been a possibility. The loss of
substantial amounts of soluble boron from
the SFP that could lead to keff exceeding 0.95
was evaluated as part of the analyses in
support of this license amendment request.
The evaluation demonstrates that a dilution
of the SFP boron concentration from the
minimum TS concentration of 2100 to 805
ppm is not credible.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
(3) Does the proposed amendment result in
a significant reduction in a margin of safety?
PO 00000
Frm 00077
Fmt 4703
Sfmt 4703
Response: No
The proposed Technical Specification
changes providing the resulting spent fuel
storage operation limits provide adequate
safety margin to ensure that the stored fuel
assembly array always remains subcritical.
These limits are based on a plant-specific
criticality analysis performed in accordance
with the present Westinghouse spent fuel
rack criticality analysis methodology which
allows credit for soluble boron.
The criticality analysis takes credit for
soluble boron to ensure that keff will be less
than or equal to 0.95 under normal
circumstances. While the criticality analysis
used credit for soluble boron, storage
configurations have been defined using 95/95
keff calculations to ensure that the spent fuel
rack keff is less than unity (0.995) with no
soluble boron. Soluble boron credit is used
to provide safety margin to offset
uncertainties, tolerances, and off-normal/
accident conditions, and to provide
subcritical margin such that the SFP keff is
maintained less than or equal to 0.95.
The loss of substantial amounts of soluble
boron from the SFP that could lead to keff
exceeding 0.95 was evaluated as part of the
analyses in support of this license
amendment request. The evaluation
demonstrates that a dilution of the SFP boron
concentration from the minimum TS
concentration of 2100 to 805 ppm is not
credible. Also, the plant-specific criticality
analysis results demonstrate that even if a
complete dilution were to occur the spent
fuel rack keff would remain <1.0 (at a 95/95
percent probability and confidence level)
with the SFP flooded with unborated water.
The plant-specific criticality analysis
performed in accordance with the
conservative analysis methodology of the
Westinghouse licensing topical report
demonstrates that the requirements of 10 CFR
50.68 and 10 CFR 50, Appendix A, General
Design Criterion 62 will be satisfied.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jonathan Rogoff,
Esquire, Vice President, Counsel &
Secretary, Nuclear Management
Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Acting Branch Chief: Patrick D.
Milano.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of amendment request:
December 29, 2006.
Description of amendment request:
The proposed amendments would
E:\FR\FM\13FEN1.SGM
13FEN1
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
jlentini on PROD1PC65 with NOTICES
revise Technical Specification (TS) 5.5.8
to indicate that the Inservice Testing
Program shall include testing
frequencies applicable to the American
Society of Mechanical Engineers Code
for Operations and Maintenance (ASME
OM Code), and to indicate that there
may be some non-standard frequencies
specified as 2 years or less in the
Inservice Testing Program to which the
provisions of Surveillance Requirement
(SR) 3.0.2 are applicable. The proposed
changes are consistent with NRCapproved Technical Specification Task
Force (TSTF) Travelers TSTF–479,
Revision 0, ‘‘Changes to Reflect Revision
of 10 CFR 50.55a,’’ and TSTF–497,
Revision 0, ‘‘Limit Inservice Testing
Program SR 3.0.2 Application to
Frequencies of 2 Years or Less.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes revise TS 5.5.8,
‘‘lnservice Testing Program,’’ for consistency
with 10 CFR 50.55a(f)(4) requirements
regarding inservice testing of pumps and
valves. The proposed change incorporates
revisions to the ASME Code that result in a
net improvement in the measures for testing
pumps and valves.
The proposed changes do not impact any
accident initiators or analyzed events or
assumed mitigation of accident or transient
events. They do not involve the addition or
removal of any equipment, or any design
changes to the facility. Therefore, the
proposed changes do not represent a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. [Do] the proposed change[s] create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No
The proposed changes do not involve a
modification to the physical configuration of
the plant (i.e., no new equipment will be
installed) or change in the methods
governing normal plant operation. The
proposed change will not impose any new or
different requirements or introduce a new
accident initiator, accident precursor, or
malfunction mechanism. Additionally, there
is no change in the types or increases in the
amounts of any effluent that may be released
off-site and there is no increase in individual
or cumulative occupational exposure.
Therefore, this proposed change does not
create the possibility of an accident of a
different kind than previously evaluated.
3. [Do] the proposed change[s] involve a
significant reduction in a margin of safety?
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
Response: No
The proposed changes revise TS 5.5.8,
‘‘lnservice Testing Program,’’ for consistency
with the requirements of 10 CFR 50.55a(f)(4)
regarding the inservice testing of pumps and
valves. The proposed change incorporates
revisions to the ASME Code that result in a
net improvement in the measures for testing
pumps and valves. The safety function of the
affected pumps and valves will be
maintained. Therefore, this proposed change
does not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Antonio
Fernandez, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of amendment requests:
December 29, 2006.
Description of amendment requests:
The proposed amendments will revise
Technical Specification (TS) 5.5.16 for
consistency with the requirements of 10
CFR 50.55a(g)(4) for components
classified as Code Class CC. This
regulation requires licensees to update
their containment inservice inspection
requirements in accordance with
Subsections IWE and IWL of Section XI,
Division I of the American Society of
Mechanical Engineers (ASME) Boiler
and Pressure Vessel Code as limited by
10 CFR 50.55a(b)(2)(vi) and modified by
10 CFR 50.55a(b)(2)(viii) and 10 CFR
50.55a(b)(2)(ix). This license
amendment request is consistent with
NRC-approved Industry/Technical
Specification Task Force (TSTF)
Traveler number TSTF–343,
‘‘Containment Structural Integrity.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change revises the Technical
Specification (TS) administrative controls
programs for consistency with the
PO 00000
Frm 00078
Fmt 4703
Sfmt 4703
6785
requirements of 10 CFR [Part] 50, paragraph
55a(g)(4) for components classified as Code
Class CC.
The proposed change affects the frequency
of visual examinations that will be performed
for the concrete surfaces of the containment
for the purpose of the Containment Leakage
Rate Testing Program. In addition, the
proposed change allows those examinations
to be performed during power operation as
opposed to during a refueling outage. The
frequency of visual examinations of the
concrete surfaces of the containment and the
mode of operation during which those
examinations are performed has no
relationship to or adverse impact on the
probability of any of the initiating events
assumed in the accident analyses. The
proposed change would allow visual
examinations that are performed pursuant to
NRC-approved ASME [Code,] Section XI
requirements (except where relief has been
granted by the NRC) to meet the intent of
visual examinations required by Regulatory
Guide 1.163, without requiring additional
visual examinations pursuant to the
Regulatory Guide. The intent of early
detection of deterioration will continue to be
met by the more rigorous requirements of the
Code-required visual examinations. As such,
the safety function of the containment as a
fission product barrier is maintained.
The proposed change does not impact any
accident initiators or analyzed events or
assumed mitigation of accident or transient
events. It does not involve the addition or
removal of any equipment, or any design
changes to the facility.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different accident
from any accident previously evaluated?
Response: No.
The proposed change revises the TS
Administrative Controls programs for
consistency with the requirements of 10 CFR
[Part] 50, paragraph 55a(g)(4) for components
classified as Code Class CC.
The change affects the frequency of visual
examinations that will be performed for the
concrete surfaces of the containments. In
addition, the proposed change allows those
examinations to be performed during power
operation as opposed to during a refueling
outage. The proposed change does not
involve a modification to the physical
configuration of the plant (i.e., no new
equipment will be installed) or a change in
the methods governing normal plant
operation. The proposed change will not
impose any new or different requirements or
introduce a new accident initiator, accident
precursor, or a malfunction mechanism.
Additionally, there is no change in the types
or increases in the amounts of any effluent
that may be released offsite and there is no
increase in individual or cumulative
occupational exposure.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
E:\FR\FM\13FEN1.SGM
13FEN1
6786
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
Response: No.
The proposed change revises the TS
Administrative Controls programs for
consistency with the requirements of 10 CFR
[Part] 50, paragraph 55a(g)(4) for components
classified as Code Class CC.
The change affects the frequency of visual
examinations that will be performed for the
concrete surfaces of the containments. In
addition, the proposed change allows those
examinations to be performed during power
operation as opposed to during a refueling
outage. The safety function of the
containment as a fission product barrier will
be maintained.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
jlentini on PROD1PC65 with NOTICES
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Antonio
´
Fernandez, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of amendment requests:
December 29, 2006.
Description of amendment requests:
The proposed amendments will revise
Technical Specification (TS) 3.4.1, ‘‘RCS
[Reactor Coolant System] Pressure,
Temperature, and Flow Departure from
Nucleate Boiling (DNB) Limits,’’ and TS
5.6.5, ‘‘CORE OPERATING LIMITS
REPORT (COLR). This license
amendment request proposes to relocate
the RCS DNB parameters for pressurizer
pressure and RCS average temperature
to the COLR. This relocation is
consistent with Technical Specification
Task Force Traveler TSTF–339,
Revision 2, ‘‘Relocate TS Parameters to
COLR.’’ TS 5.6.5 is revised to add
topical reports WCAP–8567–P–A,
‘‘Improved Thermal Design Procedure,’’
and WCAP–11596–P–A, ‘‘Qualification
of the PHOENIX–P/ANC Nuclear Design
System for Pressurized Water Reactor
Cores,’’ by name and title only. These
changes are consistent with TSTF–363,
Revision 0, ‘‘Revise Topical Report
References in ITS 5.6.5, COLR.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
1. [Do] the proposed change[s] involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes are programmatic
and administrative in nature, and do not
physically alter safety-related systems or
affect the way in which safety-related
systems perform their functions. The
proposed changes relocate cycle-specific
parameters from Technical Specification (TS)
3.4.1 to the Core Operating Limits Report
(COLR). This does not change plant design or
affect system operating parameters. The
proposed changes do not, by themselves,
alter any of the parameters. Removal of the
cycle-specific parameters from the TS does
not eliminate existing requirements to
comply with the parameters. Also, TS 5.6.5
is revised to add topical reports WCAP–
8567–P–A, ‘‘Improved Thermal Design
Procedure,’’ and WCAP–11596–P–A,
‘‘Qualification of the PHOENIX–P/ANC
Nuclear Design System for Pressurized Water
Reactor Cores,’’ as they are approved
analytical methods for determining core
operating limits.
Although relocation of the cycle-specific
parameters to the COLR would allow revision
of the affected parameters without prior NRC
approval, there is no significant effect on the
probability or consequences of an accident
previously evaluated. Future changes to the
COLR parameters could result in event
consequences that are either slightly less or
slightly more severe than the consequences
for the same event using the present
parameters. The differences would not be
significant and would be bounded by the
existing requirement of TS 5.6.5c to meet the
applicable limits of the safety analyses.
The cycle-specific parameters being
transferred from the TS to the COLR will
continue to be controlled under existing
programs and procedures. The Final Safety
Analysis Report Update (FSARU) accident
analyses will continue to be examined with
respect to changes in the cycle-dependent
parameters obtained using NRC reviewed and
approved reload design methodologies to
ensure that the transient evaluation of new
reload designs are bounded by previously
accepted analyses. This examination will
continue to be performed pursuant to 10 CFR
50.59 requirements, ensuring that future
reload designs use NRC-approved
methodologies and do not involve more than
a minimal increase in the probability or
consequences of an accident previously
evaluated in the FSARU.
The proposed changes do not allow for an
increase in plant power levels, do not
increase the production, and do not alter the
flow path or method of disposal of
radioactive waste or byproducts. Therefore,
the proposed changes do not change the type
or increase the amount of effluents released
offsite.
The proposed changes to TS 5.6.5b to
reference only the topical report number and
title for five of the topical reports do not alter
the analytical methods that have been
previously reviewed and approved by the
NRC. This method of referencing topical
reports would allow the use of current
PO 00000
Frm 00079
Fmt 4703
Sfmt 4703
topical reports to support limits in the COLR
without having to submit a request for an
amendment to the operating license.
Implementation of revisions to these topical
reports would still be reviewed in accordance
with 10 CFR 50.59 and, where required,
revisions would be submitted to the NRC for
approval prior to implementation.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. [Do] the proposed change[s] create the
possibility of a new or different accident
from any accident previously evaluated?
Response: No.
The proposed changes that relocate cyclespecific parameters from the TS to the COLR,
thus removing the requirement for prior NRC
approval of revisions to those parameters, do
not involve a physical change to the plant.
No new equipment is being introduced, and
installed equipment is not being operated in
a new or different manner. No changes are
being made to the parameters within which
the plant is operated, other than their
relocation to the COLR. No protective or
mitigative action setpoints are affected by the
proposed changes. The proposed changes
will not alter the manner in which
equipment operation is initiated, nor will the
functional demands on credited equipment
be changed. No change to procedures that
ensure the plant remains within analyzed
limits are being proposed, and no change is
being made to procedures relied upon to
respond to an off-normal event. As such, no
new failure modes are being introduced.
Relocation of cycle-specific parameters
does not influence, impact, or contribute in
any way to the possibility of a new or
different kind of accident. The relocated
cycle-specific parameters will continue to be
calculated using the NRC-reviewed and
approved methodology. The proposed
changes do not alter assumptions made in the
safety analysis, and operation within the core
operating limits will continue.
The proposed changes to reference only the
topical report number and title do not alter
the use of the analytical methods that have
been previously reviewed and approved by
the NRC. This method of referencing topical
reports would allow the use of current
topical reports to support limits in the COLR
without having to submit a request for an
amendment to the operating license.
Implementation of revisions to topical
reports would still be reviewed in accordance
with 10 CFR 50.59 and, where required,
would receive NRC review and approval.
The addition of WCAP–8567–P–A and
WCAP–11596–P–A to TS 5.6.5 is a
clarification to provide a complete listing of
approved analytical methods used for
determining core operating limits.
Therefore, the proposed change does not
create the possibility of a new or different
accident from any accident previously
evaluated.
3. [Do] the proposed change[s] involve a
significant reduction in a margin of safety?
Response: No.
The margin of safety is established through
equipment design, operating parameters, and
the setpoints at which automatic actions are
E:\FR\FM\13FEN1.SGM
13FEN1
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
initiated. The proposed changes do not
physically alter safety-related systems, nor do
they affect the way in which safety-related
systems perform their functions. No
protective or mitigative action setpoints are
affected by the proposed changes. Therefore,
sufficient equipment remains available to
actuate upon demand for the purpose of
mitigating an analyzed event. As the
proposed changes to relocate cycle-specific
parameters to the COLR will not affect plant
design or system operating parameters, there
is no detrimental impact on any equipment
design parameter, and the plant will continue
to be operated within prescribed limits.
The development of cycle-specific
parameters for future reload designs will
continue to conform to NRC-reviewed and
approved methodologies, and will be
performed pursuant to 10 CFR 50.59 to
assure that the plant operates within cyclespecific parameters.
The proposed changes to reference only the
topical report number and title do not alter
the use of the analytical methods used to
determine core operating limits that have
been reviewed and approved by the NRC.
This method of referencing topical reports
would allow the use of current NRCapproved topical reports to support limits in
the COLR without having to submit a request
for an amendment to the operating license.
Implementation of revisions to topical
reports would still be reviewed in accordance
with 10 CFR 50.59 and, where required,
receive NRC review and approval.
The addition of WCAP–8567–P–A and
WCAP–11596–P–A to TS 5.6.5 is a
clarification to provide a complete listing of
approved analytical methods used for
determining core operating limits.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
jlentini on PROD1PC65 with NOTICES
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Antonio
´
Fernandez, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of amendment requests: January
11, 2007.
Description of amendment requests:
The proposed amendments would
revise the Technical Specifications
(TSs) to support replacement of the
steam generators (SGs) at Diablo Canyon
Power Plant, Unit Nos. 1 and 2.
Revisions are proposed to TS 3.3.2,
‘‘Engineered Safety Feature Actuation
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
System (ESFAS) Instrumentation,’’ TS
5.5.9, ‘‘Steam Generator (SG) Program,’’
and TS 5.6.10, ‘‘Steam Generator (SG)
Tube Inspection Report.’’ The
replacement SGs are to be installed
during the Diablo Canyon Power Plant,
Unit No. 2, 14th refueling outage (2R14),
currently scheduled for February 2008,
and the Unit No. 1, 15th refueling
outage (1R15), currently scheduled for
January 2009.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. [Do] the proposed change[s] involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The revised engineered safety feature
actuation system (ESFAS) steam generator
(SG) Water Level-High High feedwater
isolation Nominal Trip Setpoint and
Allowable Value have been determined using
the existing setpoint methodology approved
for Diablo Canyon Power Plant. The setpoint
analysis for the replacement steam generators
(RSGs) accounts for the setpoint uncertainties
specific to the RSG design. The revised
Feedwater Isolation SG Water Level-High
High (P–14) Nominal Trip Setpoint and
Allowable Value are applied using a
conservative surveillance requirement
methodology. The function of the ESFAS
instrumentation is unchanged. The
Feedwater Isolation SG Water Level-High
High (P–14) ESFAS instrumentation will
continue to function in a manner consistent
with the plant design basis and satisfy all the
requirements of the safety analyses.
The probability and consequences of
accidents previously evaluated in the Final
Safety Analysis Report (FSAR) Update are
not adversely affected because the revised
Feedwater Isolation SG Water Level-High
High (P–14) Nominal Trip Setpoint and
Allowable Value continue to assure a
conservative plant response to high SG level,
consistent with the safety analyses and
licensing basis.
The proposed changes revise and clarify
the surveillance requirements for ESFAS
Function 5.b, Feedwater Isolation SG Water
Level-High High (P–14). These changes
ensure that this function will actuate as
assumed in the safety analyses.
The proposed changes to TS 5.5.9 delete
the alternate repair criteria (ARC) for the
existing SGs, incorporate tube inspection
periods applicable to Alloy 690 thermally
treated tubes, and delete the TS 5.6.10
reporting requirements for ARC. The TS 5.5.9
SG structural integrity, accident induced
leakage, and operational leakage performance
criteria will continue to be met for the RSGs.
Meeting the SG performance criteria provides
reasonable assurance that the SG tubes will
remain capable of maintaining reactor
coolant pressure boundary integrity
throughout each operating cycle and in the
PO 00000
Frm 00080
Fmt 4703
Sfmt 4703
6787
unlikely event of a design basis accident.
Removal of the ARC for the existing SGs will
ensure that all tubes found by inservice
inspection to contain flaws with a depth
equal to or exceeding 40 percent of the
nominal tube wall thickness will be plugged
as required by TS 5.5.9.c. With the revised
SG tube inspection period, the SGs will
continue to meet the SG program defined by
NEI [Nuclear Energy Institute] 97–06, ‘‘Steam
Generator Program Guidelines,’’ which
incorporates a balance of prevention,
inspection, evaluation, repair, and leakage
monitoring.
Removal of the ARC will reduce the
allowable accident induced leakage following
a main steamline break accident. The
proposed changes do not have any impact on
the accident induced leakage assumed in the
other design basis accidents. The changes do
not have any impact on the allowable SG
operational leakage, allowable reactor coolant
system activity, or the allowable SG
secondary activity.
The proposed changes will not affect the
probability of any accident initiators. There
will be no degradation in the performance of,
or an increase in the number of challenges
imposed on, safety-related equipment
assumed to function during an accident.
There will be no change to accident
mitigation performance. The proposed
changes will not alter any assumptions or
change any mitigation actions in the
radiological consequence evaluations in the
FSAR Update.
Therefore the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. [Do] the proposed change[s] create the
possibility of a new or different accident
from any accident previously evaluated?
Response: No.
The proposed changes will not affect the
normal method of plant operation or create
new methods of plant operation related to the
Feedwater Isolation SG Water Level-High
High (P–14) ESFAS setpoints. The proposed
changes to the Feedwater Isolation SG Water
Level-High High (P–14) instrumentation
surveillance requirements will provide
assurance that the plant will operate within
the limits assumed in the safety analyses.
The assumptions made in the setpoint
analyses for the Feedwater Isolation SG
Water Level-High High (P–14) ESFAS
instrument do not create any new accidents,
accident initiators, or failure mechanisms.
The proposed changes, which delete the
TS 5.5.9 ARC for the existing SGs,
incorporate tube inspection periods for Alloy
690 thermally-treated tubes in TS 5.5.9, and
delete the ARC reporting requirements in TS
5.6.10, will not introduce any adverse
changes to the plant design basis or
postulated accidents resulting from potential
tube degradation. The primary-to-secondary
leakage that may be experienced during all
plant conditions will be monitored to ensure
it remains within current safety analysis
assumptions. The proposed changes do not
adversely affect the method of operation of
the SGs or the primary or secondary coolant
controls and do not impact other plant
systems or components.
E:\FR\FM\13FEN1.SGM
13FEN1
6788
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
Therefore, the proposed changes do not
create the possibility of a new or different
accident from any accident previously
evaluated.
3. [Do] the proposed change[s] involve a
significant reduction in a margin of safety?
Response: No.
The FSAR Update Excessive Heat Removal
due to Feedwater System Malfunctions event
credits the Feedwater Isolation SG Water
Level-High High (P–14) ESFAS
instrumentation. The safety analysis limit
assumed for the Feedwater Isolation SG
Water Level-High High (P–14) ESFAS
instrumentation for this event has not
changed for the safety analyses for the RSGs.
None of the acceptance criteria for Excessive
Heat Removal due to Feedwater System
Malfunctions event are changed as a result of
the revised Feedwater Isolation SG Water
Level-High High (P–14) Nominal Trip
Setpoint and Allowable Value. The
instrument surveillance requirement changes
for the Feedwater Isolation SG Water LevelHigh High (P–14) function ensure that the
instrumentation will actuate as assumed in
the safety analysis.
The safety function of the SGs is
maintained by ensuring the integrity of the
tubes. SG tube integrity is a function of the
design, environment, and the physical
condition of the SG tubes. The proposed
changes, which delete the TS 5.5.9 ARCs for
the existing SGs, incorporate tube inspection
periods for Alloy 690 thermally treated tubes
in TS 5.5.9, and delete the ARC reporting
requirements in TS 5.6.10, do not adversely
impact the SG tube design or operating
environment. SG tube integrity will continue
to be maintained by implementing the SG
Program to manage SG tube inspection,
assessment, and repair. The requirements
established by the SG program are consistent
with those in the applicable design codes and
standards.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
jlentini on PROD1PC65 with NOTICES
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Antonio
´
Fernandez, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Co., Docket No.
50–133, Humboldt Bay Power Plant
(HBPP), Unit 3 Humboldt County,
California
Date of amendment request: May 17,
2006.
Description of amendment request:
The licensee has proposed to modify the
Physical Security Plan (PSP) to allow
leaving certain security posts
temporarily under emergency
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
conditions requiring personnel to
evacuate occupied plant areas for their
health and safety.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
(1) Does the change involve a significant
increase in the probability or consequences
of an accident previously evaluated?
Response: No.
Allowing the security posts and monitoring
requirements of PSP, Sections 3.1.4 and 4.3,
and Table 7–1, to not be continuously
maintained has no impact on the probability
of an accident from occurring, especially acts
of nature such as earthquakes and tsunamis.
The HBPP Defueled Safety Analysis
Report, Appendix A, and NRC Safety
Evaluation Report (SER), Section 10, dated
April 29, 1987, evaluate various accidents at
HBPP. Because all fuel has been removed
from the reactor vessel and stored in the
spent fuel pool, the majority of accidents
analyzed pertain to events that could only
affect spent fuel or the spent fuel pool. All
accidents affecting spent fuel or the spent
fuel pool do not require security personnel
action to protect the public health and safety,
or to maintain offsite radiological doses well
within regulatory limits. In addition, NRC
SER, Section 10.7, ‘‘Impact of Tsunami
Flooding,’’ analyzes the impact of tsunami
flooding. That analysis identifies a likely
impact of the tsunami to be a release of the
radwaste tank radionuclide contents to the
bay and some damage to the reactor building.
For both situations, no security personnel
action is required to maintain offsite
radiological doses well within regulatory
limits.
Allowing the security posts and monitoring
requirements of PSP, Sections 3.1.4 and 4.3,
and Table 7–1, to not be continuously
maintained temporarily, under emergency
conditions, does not create problems that
could increase the consequences of an
accident. The primary function of the
manning and monitoring requirements of
PSP, Sections 3.1.4 and 4.3, and Table 7–1,
is to monitor, detect and assess unauthorized
intrusion into the protected area, and has
nothing to do with the probability or
consequences of plant accidents.
If security personnel evacuate PSP, Section
3.1.4 and Table 7–1, security posts during a
tsunami, those security personnel will be
able to return to the PSP, Section 3.1.4 and
Table 7–1, security posts after the tsunami
and assess damage or intrusion by observing
alarms and/or physical conditions as well as
resume implementation of security post and
monitoring requirements of PSP, Sections
3.1.4 and 4.3, and Table 7–1. In addition,
upon evacuation, security personnel notify
offsite security backup personnel of the
evacuation and the need for the offsite
personnel to remotely monitor HBPP security
system alarms. Conversely, if security
personnel remain at the PSP, Section 3.1.4
and Table 7–1, security posts during a
tsunami and become injured, those security
PO 00000
Frm 00081
Fmt 4703
Sfmt 4703
personnel would be unable to assist in the
resumption of implementation of security
post and monitoring requirements of PSP,
Sections 3.1.4 and 4.3, and Table 7–1.
Therefore, not continually manning the PSP,
Section 3.1.4 and Table 7–1, security posts
during a tsunami does not increase the
consequences of the tsunami.
(2) Does the change create the possibility
of a new or different kind of accident from
any accident evaluated?
Response: No.
As discussed in the response to Question
1 above, none of the analyzed accidents
require security personnel action to keep
offsite radiological doses well within
regulatory limits. In addition, allowing
security personnel to not continuously
maintain security post and monitoring
requirements of PSP, Sections 3.1.4 and 4.3,
and Table 7–1, after an emergency situation
has occurred has no impact on the possibility
of a new or different kind of accident from
occurring. The primary function of the
manning and monitoring requirements of
PSP, Sections 3.1.4 and 4.3, and Table 7–1,
is to monitor, detect, and assess unauthorized
intrusion into the protected area, and has
nothing to do with the possibility of a
different kind of plant accident occurring.
(3) Does the change involve a significant
reduction in a margin of safety?
Response: No.
NRC SER, Section 10.8, ‘‘Accident
Analysis Conclusions,’’ summarizes the
consequences from accidents in terms of
offsite radiological doses. SER, Section 10.8,
includes the statement, ‘‘The (NRC) staff has
determined that offsite radiological
consequences due to a tsunami are within
acceptable dose guideline values.’’ As
discussed in the response to Question 1
above, none of the analyzed accidents require
security personnel action to keep offsite
radiological doses well within regulatory
limits. Therefore, allowing security personnel
to not continuously maintain security post
and monitoring requirements of PSP,
Sections 3.1.4 and 4.3, and Table 7–1, after
an emergency situation has occurred has no
impact on the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. Antonio
´
Fernandez, Esquire, Pacific Gas &
Electric Company, Post Office Box 7442,
San Francisco, CA 94120.
NRC Branch Chief: Claudia Craig.
Pacific Gas and Electric Co., Docket No.
50–133, Humboldt Bay Power Plant
(HBPP), Unit 3 Humboldt County,
California
Date of amendment request:
December 20, 2006.
Description of amendment request:
The licensee has proposed to amend the
E:\FR\FM\13FEN1.SGM
13FEN1
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
jlentini on PROD1PC65 with NOTICES
Facility Operating License by deleting
paragraph 2.B.3(c), and replacing it with
a new paragraph 2.B.4 to read as
follows: ‘‘Pursuant to the Act and Title
10, CFR, Chapter I, Parts 30, 40, and 70,
to receive, possess, and use in amounts
as required any byproduct, source, or
special nuclear material without
restriction to chemical or physical form,
for sample analysis or instrument
calibration or associated with
radioactive apparatus or components.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the change involve a significant
increase in the probability or consequences
of an accident previously evaluated?
Response: No.
The proposed change eliminates a
restriction regarding the type and limits of
byproduct and special nuclear material to be
received, possessed, and used onsite.
However, in the proposed change, the type or
amount of byproduct, source, or special
nuclear material to be received, possessed, or
used would not change plant systems or
accident analysis, and as such, would not
affect initiators of analyzed events or
assumed mitigation of accidents. Therefore,
the proposed change does not increase the
probability or consequences of an accident
previously evaluated.
2. Does the change create the possibility of
a new or different kind of accident from any
accident evaluated?
Response: No.
The proposed change eliminates a
restriction regarding the limits and type of
byproduct and special nuclear material to be
received, possessed, and used onsite. The
proposed change does not involve a physical
alteration to the plant or require existing
equipment to be operated in a manner
different from the present design. Temporary
equipment brought onsite for
decommissioning activities would still be
required to be operated in accordance with
plant procedures and licensing bases
documents, regardless of the byproduct
material content. Therefore, the proposed
change does not create the possibility of a
new or different kind of accident from any
accident evaluated.
3. Does the change involve a significant
reduction in a margin of safety?
Response: No.
The proposed change eliminates a
restriction regarding the limit and type of
byproduct and special nuclear material to be
received, possessed, and used onsite. The
proposed change has no effect on existing
plant equipment, operating practices, or
safety analysis assumptions. Temporary
equipment brought onsite for
decommissioning activities would still be
required to be operated in accordance with
plant procedures and licensing bases
documents, regardless of the byproduct
material content. Therefore, the proposed
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
change does not involve a significant
reduction in a margin of safety.
The U.S. Nuclear Regulatory
Commission staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. Antonio
´
Fernandez, Esquire, Pacific Gas &
Electric Company, Post Office Box 7442,
San Francisco, CA 94120.
NRC Branch Chief: Claudia Craig.
PSEG Nuclear LLC, Docket No. 50–354,
Hope Creek Generating Station, Salem
County, New Jersey
Date of amendment request:
November 15, 2006.
Description of amendment request:
The proposed amendment would delete
Technical Specification (TS) Table
3.6.3–1, ‘‘Primary Containment Isolation
Valves,’’ and relocate the information to
the Technical Requirements Manual.
The amendment would also revise other
TS sections that reference TS Table
3.6.3–1. The proposed changes are
based on the guidance in Generic Letter
91–08, ‘‘Removal of Component Lists
from Technical Specifications.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed relocation of Technical
Specification component lists of primary
containment isolation valves does not alter
the requirements for component operability
or surveillance currently in the Technical
Specifications. The proposed change to
remove the component lists from TS and
relocate the information to an
administratively controlled document will
have no impact on any safety related
structures, systems or components.
The probability of occurrence of a
previously evaluated accident is not
increased because this change does not
introduce any new potential accident
initiating conditions. The consequences of
accidents previously evaluated in the UFSAR
[Updated Final Safety Analysis Report] are
not affected because the ability of the
components to perform their required
function is not affected.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
PO 00000
Frm 00082
Fmt 4703
Sfmt 4703
6789
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes are administrative
in nature, conform to the guidance in Generic
Letter 91–08 and do not result in physical
alterations or changes in the method by
which any safety related system performs its
intended function. The proposed changes do
not affect any safety analysis assumptions.
The proposed changes do not create any new
accident initiators or involve an activity that
could be an initiator of an accident of a
different type.
All components will continue to be tested
to the same requirements as defined in the
Technical Specification Surveillance
Requirements. The proposed revision does
not make changes in any method of testing
or how any safety related system performs its
safety functions.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed change to remove Technical
Specification Table 3.6.3–1 from the
Technical Specifications and relocate it to
the Technical Requirements Manual does not
alter the Technical Specification
requirements for containment integrity and
containment isolation and will not affect the
containment isolation capability. Future
revisions to the Technical Requirements
Manual Table will be subject to evaluation
pursuant to 10 CFR 50.59 [Title 10 of the
Code of Federal Regulations (10 CFR),
Section 50.59].
The proposed change will not affect the
current Technical Specification requirements
or the components to which they apply.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jeffrie J. Keenan,
Esquire, Nuclear Business Unit—N21,
P.O. Box 236, Hancocks Bridge, NJ
08038.
NRC Branch Chief: Harold K.
Chernoff.
Sacramento Municipal Utility District,
Docket No. 50–312, Rancho Seco
Nuclear Generating Station, Sacramento
County, California
Date of amendment request: April 12,
2006, and supplemented November 21,
2006.
Description of amendment request:
The licensee has proposed to amend its
E:\FR\FM\13FEN1.SGM
13FEN1
6790
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
jlentini on PROD1PC65 with NOTICES
license to incorporate a new license
condition addressing the license
termination plan (LTP). This
amendment will document the approval
of the LTP, document the criteria for
making changes to the LTP which will
and will not require pre-approval by the
NRC, and will document any conditions
imposed with the approval of the LTP.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed license amendment
involve a significant increase in the
probability or consequences of an accident
previously evaluated?
No. The proposed change is administrative.
The change allows for the approval of the
LTP and provides the criteria for when
changes to the LTP require prior U.S. Nuclear
Regulatory Commission (NRC) approval. This
change does not affect possible initiating
events for accidents previously evaluated or
alter the configuration or operation of the
facility. Safety limits, limiting safety system
settings, and limiting control systems are no
longer applicable to Rancho Seco in the
permanently defueled mode, and are
therefore not relevant.
The proposed change does not affect the
boundaries used to evaluate compliance with
liquid or gaseous effluent limits, and has no
impact on plant operations. Therefore, the
proposed license amendment does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed license amendment
create the possibility of a new or different
kind of accident from any accident
previously evaluated?
No. As described above, the proposed
change is administrative and provides the
criteria for when changes to the LTP require
prior NRC approval. The safety analysis for
the facility remains complete and accurate.
There are no physical changes to the facility
as a result of the proposed amendment and
the plant conditions for which the design
basis accidents have been evaluated are still
valid.
The operating procedures and emergency
procedures are not affected. The proposed
changes do not affect the emergency planning
zone, the boundaries used to evaluate
compliance with liquid or gaseous effluent
limits, and have no impact on plant
operations. Consequently, no new failure
modes are introduced as the result of the
proposed changes. Therefore, the proposed
changes will not create the possibility of a
new or different kind of accident from any
accident previously evaluated.
3. Does the proposed license amendment
involve a significant reduction in a margin of
safety?
No. As described above, the proposed
changes are administrative. There are no
changes to the design or operation of the
facility. The proposed changes do not affect
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
the emergency planning zone, the boundaries
used to evaluate compliance with liquid or
gaseous effluent limits, and have no impact
on plant operations. Accordingly, neither the
design basis nor the accident assumptions in
the Defueled Safety Analysis Report, nor the
Technical Specification Bases are affected.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s significant hazards analysis
and, based on this review, it appears
that the three standards of 10 CFR
50.92(c) are satisfied. Therefore, the
NRC staff proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Arlen Orchard,
Esq., General Counsel, Sacramento
Municipal Utility District, 6201 S Street,
P.O. Box 15830, Sacramento, CA 95817–
1899.
NRC Branch Chief: Claudia M. Craig.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–348 and 50–364,
Joseph M. Farley Nuclear Plant (FNP),
Units 1 and 2, Houston County,
Alabama
Date of amendment request: January
30, 2007.
Description of amendment request:
The proposed amendment would revise
the Farley Nuclear Plant, Units 1 and 2,
Technical Specifications (TSs) to reflect
a change to a site vice president
organizational structure. The resulting
structure places a vice president at the
plant site. The proposed amendment
describes changes in titles and
administrative duties that accompany
the reorganization.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
The proposed change to [the] FNP TS
involves SNC moving to a site vice president
organizational structure. Since the proposed
change is administrative in nature, it does
not involve any physical changes to any
structures, systems, or components, nor will
their performance requirements be altered.
The proposed change also does not affect the
operation, maintenance, or testing of the
plant. Therefore, the response of the plant to
previously analyzed accidents will not be
affected. Consequently, the proposed change
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any previously evaluated?
PO 00000
Frm 00083
Fmt 4703
Sfmt 4703
As a result of the proposed change to the
FNP TS, the qualification requirements for
the unit staff position[s] will remain
unchanged and the plant staff will continue
to meet applicable regulatory requirements.
Also, since no change is being made to the
design, operation, maintenance, or testing of
the plant, no new methods of operation or
failure modes are introduced by the proposed
change. Therefore, the possibility of a new or
different kind of accident from any
previously evaluated is not created.
3. Does the proposed change involve a
significant decrease in the margin of safety?
The proposed change to the FNP TS will
have no adverse impact on the onsite
organizational features necessary to assure
safe operation of the plant since the
qualification requirements for the unit staff
remains unchanged. Since the proposed
change is administrative in nature, it does
not involve any physical changes to any
structures, systems, or components, nor will
their performance requirements be altered.
Therefore, the proposed change does not
involve a significant decrease in the margin
of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M. Stanford
Blanton, Esq., Balch and Bingham, Post
Office Box 306, 1710 Sixth Avenue
North, Birmingham, Alabama 35201.
NRC Branch Chief: Evangelos C.
Marinos.
Southern Nuclear Operating Company,
Inc., Georgia Power Company,
Oglethorpe Power Corporation,
Municipal Electric Authority of Georgia,
City of Dalton, Georgia, Docket Nos. 50–
321 and 50–366, Edwin I. Hatch Nuclear
Plant (HNP), Units 1 and 2, Appling
County, Georgia
Date of amendment request: January
30, 2007.
Description of amendment request:
The proposed amendments would
revise the Hatch Nuclear Plant, Units 1
and 2, Technical Specifications (TSs) to
reflect a change to a site vice president
organizational structure. The resulting
structure places a vice president at the
plant site. The proposed amendment
describes changes in titles and
administrative duties that accompany
the reorganization.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
E:\FR\FM\13FEN1.SGM
13FEN1
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
The proposed change to [the] HNP TS
involves SNC moving to a site vice president
organizational structure. Since the proposed
change is administrative in nature, it does
not involve any physical changes to any
structures, systems, or components, nor will
their performance requirements be altered.
The proposed change also does not affect the
operation, maintenance, or testing of the
plant. Therefore, the response of the plant to
previously analyzed accidents will not be
affected. Consequently, the proposed change
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any previously evaluated?
As a result of the proposed change to the
HNP TS, the qualification requirements for
the unit staff position[s] will remain
unchanged and the plant staff will continue
to meet applicable regulatory requirements.
Also, since no change is being made to the
design, operation, maintenance, or testing of
the plant, no new methods of operation or
failure modes are introduced by the proposed
change. Therefore, the possibility of a new or
different kind of accident from any
previously evaluated is not created.
3. Does the proposed change involve a
significant decrease in the margin of safety?
The proposed change to the HNP TS will
have no adverse impact on the onsite
organizational features necessary to assure
safe operation of the plant since the
qualification requirements for the unit staff
remains unchanged. Since the proposed
change is administrative in nature, it does
not involve any physical changes to any
structures, systems, or components, nor will
their performance requirements be altered.
Therefore, the proposed change does not
involve a significant decrease in the margin
of safety.
jlentini on PROD1PC65 with NOTICES
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Ernest L. Blake,
Jr., Esquire, Shaw, Pittman, Potts and
Trowbridge, 2300 N Street, NW.,
Washington, DC 20037.
NRC Branch Chief: Evangelos C.
Marinos.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–424 and 50–425,
Vogtle Electric Generating Plant (VEGP),
Units 1 and 2, Burke County, Georgia
Date of amendment request: January
30, 2007.
Description of amendment request:
The proposed amendment would revise
the Vogle Electric Generating Plant,
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
Units 1 and 2, Technical Specifications
(TSs) to reflect a change to a site vice
president organizational structure. The
resulting structure places a vice
president at the plant site. The proposed
amendment describes changes in titles
and administrative duties that
accompany the reorganization. Basis for
proposed no significant hazards
consideration determination: As
required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
The proposed change to [the] VEGP TS
involves SNC moving to a site vice president
organizational structure. Since the proposed
change is administrative in nature, it does
not involve any physical changes to any
structures, systems, or components, nor will
their performance requirements be altered.
The proposed change also does not affect the
operation, maintenance, or testing of the
plant. Therefore, the response of the plant to
previously analyzed accidents will not be
affected. Consequently, the proposed change
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any previously evaluated?
As a result of the proposed change to the
VEGP TS, the qualification requirements for
the unit staff position[s] will remain
unchanged and the plant staff will continue
to meet applicable regulatory requirements.
Also, since no change is being made to the
design, operation, maintenance, or testing of
the plant, no new methods of operation or
failure modes are introduced by the proposed
change. Therefore, the possibility of a new or
different kind of accident from any
previously evaluated is not created.
3. Does the proposed change involve a
significant decrease in the margin of safety?
The proposed change to the VEGP TS will
have no adverse impact on the onsite
organizational features necessary to assure
safe operation of the plant since the
qualification requirements for the unit staff
remains unchanged. Since the proposed
change is administrative in nature, it does
not involve any physical changes to any
structures, systems, or components, nor will
their performance requirements be altered.
Therefore, the proposed change does not
involve a significant decrease in the margin
of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
PO 00000
Frm 00084
Fmt 4703
Sfmt 4703
6791
Attorney for licensee: Mr. Arthur H.
Domby, Troutman Sanders,
NationsBank Plaza, Suite 5200, 600
Peachtree Street, NE., Atlanta, Georgia
30308–2216.
NRC Branch Chief: Evangelos C.
Marinos.
Tennessee Valley Authority, Docket
Nos. 50–259, 50–260 and 50–296,
Browns Ferry Nuclear Plant, Units 1, 2
and 3, Limestone County, Alabama
Date of amendment request:
December 21, 2006 (TS–456).
Description of amendment request:
The proposed amendment would revise
Technical Specification (TS) Limiting
Condition for Operation (LCO) 3.10.1
and the associated TS Bases to expand
its scope to include provisions for
temperature excursions greater than
212 °F as a consequence of inservice
leak and hydrostatic testing, and as a
consequence of scram time testing
initiated in conjunction with inservice
leak or hydrostatic testing, while
considering operational conditions to be
in Mode 4.
The NRC staff issued a notice of
opportunity for comment in the Federal
Register on August 21, 2006 (71 FR
48561), on possible amendments to
revise the plant-specific TS, to expand
the scope of TS LCO 3.10.1, to include
provisions for temperature excursions
greater than 200 °F as a consequence of
inservice leak and hydrostatic testing,
and as a consequence of scram time
testing initiated in conjunction with an
inservice leak or hydrostatic test, while
considering operational conditions to be
in MODE 4, including a model safety
evaluation and model No Significant
Hazards Consideration (NSHC)
Determination, using the consolidated
line item improvement process. The
NRC staff subsequently issued a notice
of availability of the models for
referencing in license amendment
applications in the Federal Register on
October 27, 2006 (71 FR 63050). The
licensee affirmed the applicability of the
model NSHC determination in its
application dated December 21, 2006.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of NSHC is
presented below:
Criterion 1: The proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
Technical Specifications currently allow
for operation at greater than [200] °F while
imposing MODE 4 requirements in addition
to the secondary containment requirements
required to be met. Extending the activities
that can apply this allowance will not
E:\FR\FM\13FEN1.SGM
13FEN1
6792
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
adversely impact the probability or
consequences of an accident previously
evaluated. Therefore, the proposed change
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
Criterion 2: The proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
Technical Specifications currently allow
for operation at greater than [200] °F while
imposing MODE 4 requirements in addition
to the secondary containment requirements
required to be met. No new operational
conditions beyond those currently allowed
by LCO 3.10.1 are introduced. The changes
do not involve a physical alteration of the
plant (i.e., no new or different types of
equipment will be installed) or a change in
the methods governing normal plant
operation. In addition, the changes
requirements or eliminate any existing
requirements. The changes do not alter
assumptions made in the safety analysis. The
proposed changes are consistent with the
safety analysis assumptions and current plant
operating practice. Therefore the proposed
change does not create the possibility of a
new or different kind of accident from any
accident previously evaluated.
Criterion 3: The proposed change does not
involve a significant reduction in a margin of
safety.
Technical Specifications currently allow
for operation at greater than [200] °F while
imposing MODE 4 requirements in addition
to the secondary containment requirements
required to be met. Extending the activities
that can apply this allowance will not
adversely impact any margin of safety.
Allowing completion of inspections and
testing and supporting completion of scram
time testing in conjunction with an inservice
leak or hydrostatic test prior to power
operation results in enhanced safe operations
by eliminating unnecessary maneuvers to
control reactor temperature and pressure.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: L. Raghavan.
jlentini on PROD1PC65 with NOTICES
Previously Published Notices of
Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The following notices were previously
published as separate individual
notices. The notice content was the
same as above. They were published as
individual notices either because time
did not allow the Commission to wait
for this biweekly notice or because the
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
action involved exigent circumstances.
They are repeated here because the
biweekly notice lists all amendments
issued or proposed to be issued
involving no significant hazards
consideration.
For details, see the individual notice
in the Federal Register on the day and
page cited. This notice does not extend
the notice period of the original notice.
Entergy Operations, Inc., Docket No. 50–
313, Arkansas Nuclear One, Unit No. 1,
Pope County, Arkansas
Date of amendment request: July 27,
2006, as supplemented by letters dated
October 4 and October 9, 2006.
Brief description of amendment
request: The proposed amendment
would revise Technical Specification
(TS) 3.7.14, ‘‘Spent Fuel Pool Boron
Concentration,’’ TS 3.7.15, ‘‘Spent Fuel
Pool Storage,’’ and the associated Figure
3.7.15–1, and TS 4.3, ‘‘Fuel Storage,’’
and the associated Figure 4.3.1.2–1. In
addition, this amendment would add TS
5.5.17, ‘‘Metamic Coupon Sampling
Program,’’ and Surveillance
Requirement 3.7.15.2 that directs the
performance of the coupon sampling
program. The proposed TS changes
support a modification to the ANO–1
spent fuel pool (SFP) that would utilize
Metamic poison insert assemblies. In
addition to the proposed plant
modification, the licensee would
increase the SFP boron concentration
and credit boron to ensure that a 5percent subcriticality margin is
maintained during normal and accident
conditions. This proposed amendment
also would increase the allowable initial
fuel assembly uranium-235 (U-235)
enrichment from 4.1 weight percent
(wt%) to a maximum U-235 enrichment
of 4.95 wt%.
Date of publication of individual
notice in Federal Register: December
26, 2006 (71 FR 77414).
Expiration date of individual notice:
February 26, 2007.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
PO 00000
Frm 00085
Fmt 4703
Sfmt 4703
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
Dominion Nuclear Connecticut, Inc.,
Docket No. 50–336, Millstone Power
Station, Unit No. 2, New London
County, Connecticut
Date of application for amendment:
January 26, 2006, as supplemented by
letter dated December 20, 2006.
Brief description of amendment: The
amendment revised the Millstone Power
Station, Unit No. 2 Technical
Specifications (TSs) to update the list of
NRC-approved documents specified in
the TSs that describe the analytical
methods used to determine the core
operating limits. The proposed change
also corrects a typographical error in TS
5.3.1, ‘‘Reactor Core, Fuel Assembly,’’
which was introduced in the retyped
pages provided to the NRC for issuance
of Amendment No. 280, dated
September, 25, 2003.
Date of issuance: January 23, 2007.
E:\FR\FM\13FEN1.SGM
13FEN1
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 295.
Facility Operating License Nos. DPR–
65: The Amendment revised the TSs.
Date of initial notice in Federal
Register: May 9, 2006 (71 FR 26997).
The supplement dated December 20,
2006, provided clarifying information
that did not change the scope of the
proposed amendment as described in
the original notice of proposed action
published in the Federal Register, and
did not change the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated January 23,
2007.
No significant hazards consideration
comments received: No.
Dominion Nuclear Connecticut, Inc.,
Docket No. 50–336, Millstone Power
Station, Unit No. 2, New London
County, Connecticut
Date of application for amendment:
March 17, 2006.
Brief description of amendment: The
amendment changed the Millstone
Power Station, Unit No. 2, Technical
Specifications by replacing the existing
maximum and minimum pressurizer
water volume and water level limits
with a maximum water level limit. The
associated TS bases were updated to
address the proposed changes.
Date of issuance: January 30, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 296.
Facility Operating License No. DPR–
65: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: November 11, 2006 (71 FR
65141).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated January 30,
2007.
No significant hazards consideration
comments received: No.
jlentini on PROD1PC65 with NOTICES
Entergy Operations, Inc., Docket No. 50–
313, Arkansas Nuclear One, Unit No. 1
(ANO–1), Pope County, Arkansas
Date of amendment request: July 27,
2006, as supplemented by letters dated
October 4, October 9, and December 14,
2006.
Brief description of amendment: The
amendment revised Technical
Specification (TS) 3.7.14, ‘‘Spent Fuel
Pool Boron Concentration,’’ TS 3.7.15,
‘‘Spent Fuel Pool Storage,’’ and the
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
associated Figure 3.7.15–1, and TS 4.3,
‘‘Fuel Storage,’’ and the associated
Figure 4.3.1.2–1. In addition, this
amendment added TS 5.5.17, ‘‘Metamic
Coupon Sampling Program,’’ and
Surveillance Requirement 3.7.15.2 that
directs the performance of the coupon
sampling program. The TS changes
support a modification to the ANO–1
spent fuel pool (SFP) that utilize
Metamic poison insert assemblies. In
addition to the proposed plant
modification, the licensee increased the
SFP boron concentration and credited
boron to ensure that a 5-percent
subcriticality margin is maintained
during normal and accident conditions.
This amendment also increased the
allowable initial fuel assembly uranium235 (U–235) enrichment from 4.1 weight
percent (wt%) to a maximum U–235
enrichment of 4.95 wt%.
Date of issuance: January 26, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment No.: 228.
Renewed Facility Operating License
No. DPR–51: Amendment revised the
Technical Specifications/license.
Date of initial notice in Federal
Register: December 26, 2006 (71 FR
77414). The supplement dated
December 14, 2006, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register. The
Commission’s related evaluation of the
amendment is contained in a Safety
Evaluation dated January 26, 2007.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket No. 50–374, LaSalle County
Station, Unit 2, LaSalle County, Illinois
Date of application for amendments:
April 21, 2006.
Brief description of amendment: The
amendment revised Technical
Specification (TS) 5.5.13, ‘‘Primary
Containment Leakage Testing Program,’’
to reflect a one-time extension of the
LaSalle, Unit 2 primary containment
Type A integrated leak rate test (ILRT)
from the current requirement of no later
than December 7, 2008, to prior to
startup following the 12th LaSalle, Unit
2 refueling outage.
Date of issuance: January 24, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 166.
PO 00000
Frm 00086
Fmt 4703
Sfmt 4703
6793
Facility Operating License No. NPF–
18: The amendment revised the
Technical Specifications and License.
Date of initial notice in Federal
Register: June 6, 2006 (71 FR 32605).
The Commission’s related evaluation of
the amendments is contained in a Safety
Evaluation dated January 24, 2007.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket Nos. 50–373 and 50–374, LaSalle
County Station, Units 1 and 2, LaSalle
County, Illinois
Date of application for amendments:
April 13, 2005, as supplemented by
letters dated December 22, 2005, June
12, 2006, and January 4, 2007.
Brief description of amendments: The
proposed amendment would extend, on
a one-time basis, the completion time
(CT) for required action C.4, ‘‘Restore
required Diesel Generators (DGs)
OPERABLE status,’’ associated with
Technical Specification (TS) Section
3.8.1 from 72 hours to 6 days. This
proposed change would only be used
during the upcoming Unit 2—spring
2007 refueling outage, and later during
the Unit 1—spring 2008 refueling
outage. The amendment would also
extend the CT from 2 hours to 6 hours
in TS Section 3.8.1, Required Action
F.1, ‘‘Restore one required DG to
OPERABLE status.’’ This proposed
change to be used during the upcoming
Unit 2—spring 2007 refueling outage,
and later during the subsequent Unit
1—spring 2008 refueling outage.
Date of issuance: January 29, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 30 days.
Amendment Nos.: 180/167.
Facility Operating License Nos. NPF–
11 and NPF–18: The amendments
revised the Technical Specifications/
License.
Date of initial notice in Federal
Register: June 7, 2005 (70 FR 33210).
The Commission’s related evaluation of
the amendments is contained in a Safety
Evaluation dated January 29, 2007.
No significant hazards consideration
comments received: No.
Florida Power and Light Company,
Docket No. 50–335, St. Lucie Plant, Unit
No. 1, St. Lucie County, Florida
Date of application for amendment:
April 24, 2006, as supplemented
September 14, 2006.
Brief description of amendment: The
amendment revised the Technical
Specifications (TSs) consistent with the
NRC-approved Revision 4 to TS Task
Force (TSTF) Standard TS Change
E:\FR\FM\13FEN1.SGM
13FEN1
6794
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
Traveler, TSTF–449, ‘‘Steam Generator
Tube Integrity.’’
Date of Issuance: January 30, 2007.
Effective Date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment No.: 200.
Renewed Facility Operating License
No. DPR–67: Amendment revised the
TSs.
Date of initial notice in Federal
Register: July 18, 2006 (71 FR 40746).
The September 14, 2006, supplement
did not affect the original proposed no
significant hazards determination, or
expand the scope of the request as
noticed in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated: January 30,
2007.
No significant hazards consideration
comments received: No.
Nine Mile Point Nuclear Station, LLC,
Docket No. 50–220, Nine Mile Point
Nuclear Station, Unit No. 1, Oswego
County, New York
jlentini on PROD1PC65 with NOTICES
Date of application for amendment:
December 16, 2005, as supplemented by
letter dated October 25, 2006.
Brief description of amendment: The
amendment relocates Technical
Specification Surveillance Requirement
4.1.4d for core spray header differential
pressure instrumentation to the Updated
Final Safety Analysis Report.
Date of issuance: January 31, 2007.
Effective date: January 31, 2007.
Amendment No.: 192.
Facility Operating License No. DPR–
63: Amendment revised the License and
Technical Specifications.
Date of initial notice in Federal
Register: March 28, 2006 (71 FR
15484). The supplemental letter dated
October 25, 2006, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the NRC staff’s
original proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated January 31,
2007.
No significant hazards consideration
comments received: No.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of application for amendments:
January 25, 2006.
Brief description of amendments: The
amendments revised Technical
VerDate Aug<31>2005
16:55 Feb 12, 2007
Jkt 211001
Specification (TS) 1.1, ‘‘Definitions,’’
and TS 3.4.16, ‘‘RCS [Reactor Coolant
System] Specific Activity.’’ The
amendments replaced the current TS
3.4.16 limit on RCS gross specific
activity with a new limit on RCS noble
gas specific activity. The noble gas
specific activity limit is based on a new
dose equivalent Xe–133 definition that
would replace the current E-Bar average
disintegration energy definition. In
addition, the current dose equivalent I–
131 definition is revised to allow the
use of alternate thyroid dose conversion
factors.
Date of issuance: January 19, 2007.
Effective date: As of the date of
issuance and shall be implemented
within 90 days from the date of
issuance.
Amendment Nos.: Unit 1–192; Unit
2–193.
Facility Operating License Nos. DPR–
80 and DPR–82: The amendments
revised the Technical Specifications and
Operating Licenses.
Date of initial notice in Federal
Register: March 14, 2006 (71 FR
13176). The Commission’s related
evaluation of the amendments is
contained in a Safety Evaluation dated
January 19, 2007.
No significant hazards consideration
comments received: No.
PPL Susquehanna, LLC, Docket No. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1
and 2), Luzerne County, Pennsylvania
Date of application for amendments:
October 13, 2005, as supplemented on
May 18, September 15 (PLA–6112 and
PLA–6114), September 29, October 20,
November 14, December 13, and
December 14, 2006.
Brief description of amendments: The
amendments revise the SSES 1 and 2
Technical Specifications (TSs) to
incorporate a full-scope application of
an alternate source term methodology in
accordance with Title 10 of the Code of
Federal Regulations, section 50.67.
Date of issuance: January 31, 2007.
Effective date: As of the date of
issuance and to be implemented by
October 30, 2007.
Amendment Nos.: 239 and 216.
Facility Operating License Nos. NPF–
14 and NPF–22: The amendments
revised the TSs and license.
Date of initial notice in Federal
Register: August 29, 2006 (71 FR
51231). The Commission’s related
evaluation of the amendments is
contained in a Safety Evaluation dated
January 31, 2007.
The supplements dated September 15
(PLA–6112 and PLA–6114), September
29, October 20, November 14, December
PO 00000
Frm 00087
Fmt 4703
Sfmt 4703
13, and December 14, 2006, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination.
No significant hazards consideration
comments received: No.
Tennessee Valley Authority, Docket
Nos. 50–260 and 50–296, Browns Ferry
Nuclear Plant, Units 2 and 3, Limestone
County, Alabama
Date of application for amendments:
October 26, 2006 (TS–457).
Brief description of amendments: The
amendments revise Technical
Specification (TS) Action 3.8.1.B.4 for
Browns Ferry Nuclear Plant Units 2 and
3. The revision changes the restoration
time of an inoperable Emergency Diesel
Generator from 14 to 7 days.
Date of issuance: January 26, 2007.
Effective date: Within 60 days of NRC
approval or prior to changing Unit 1
reactor mode to startup, whichever is
earlier.
Amendment Nos.: 298 and 256.
Renewed Facility Operating License
Nos. DPR–52 and DPR–68: Amendments
revised the TSs.
Date of initial notice in Federal
Register: November 21, 2006 (71 FR
67398).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated January 26,
2007.
No significant hazards consideration
comments received: No.
Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of application for amendment:
May 25, 2006.
Brief description of amendment: The
amendment revised TSs by adding
Limiting Condition for Operation (LCO)
3.0.8. This change is consistent with
NRC-approved Revision 4 to Technical
Specification Task Force (TSTF)
Standard Technical Specification
Traveler, TSTF–372, ‘‘Addition of LCO
3.0.8, Inoperability of Snubbers.’’
Date of issuance: January 31, 2007.
Effective date: As of its date of
issuance, and shall be implemented
within 90 days of the date of issuance.
Amendment No.: 179.
Facility Operating License No. NPF–
30: The amendment revised the Facility
Operating License and Technical
Specifications.
Date of initial notice in Federal
Register: July 18, 2006 (71 FR 40755).
The Commission’s related evaluation
of the amendment is contained in a
E:\FR\FM\13FEN1.SGM
13FEN1
Federal Register / Vol. 72, No. 29 / Tuesday, February 13, 2007 / Notices
Safety Evaluation dated January 31,
2007.
No significant hazards consideration
comments received: No.
Virginia Electric and Power Company,
Docket Nos. 50–338 and 50–339, North
Anna Power Station, Units 1 and 2,
Louisa County, Virginia
Date of application for amendment:
May 22, 2006.
Brief description of amendment:
These amendments revise the existing
steam generator tube surveillance
program to be consistent with the
Technical Specification Task Force
(TSTF) Standard TS Change Traveler,
TSTF–449, ‘‘Steam Generator Tube
Integrity.’’
Date of issuance: October 16, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 180 days from the date of
issuance.
Amendment Nos.: 248, 228.
Renewed Facility Operating License
Nos. NPF–4 and NPF–7: Amendments
change the licenses and the technical
specifications.
Date of initial notice in Federal
Register: August 1, 2006 (71 FR 43537)
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 16,
2006.
No significant hazards consideration
comments received: No.
Dated at Rockville, Maryland, this 6th day
of February 2007.
For the Nuclear Regulatory Commission.
John W. Lubinski,
Acting Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. E7–2323 Filed 2–12–07; 8:45 am]
BILLING CODE 7590–01–P
SECURITIES AND EXCHANGE
COMMISSION
[Release No. 34–55248; File No. SR–Amex–
2006–90]
Self-Regulatory Organizations;
American Stock Exchange LLC; Order
Approving Proposed Rule Change, as
Modified by Amendment Nos. 1 and 2
Thereto, To List and Trade Notes
Linked to the Performance of the Hang
Seng China Enterprises Index
jlentini on PROD1PC65 with NOTICES
February 6, 2007.
1 15
On September 22, 2006, the American
Stock Exchange LLC (‘‘Amex’’ or
‘‘Exchange’’) submitted to the Securities
and Exchange Commission
(‘‘Commission’’), pursuant to Section
19(b)(1) of the Securities Exchange Act
VerDate Aug<31>2005
16:55 Feb 12, 2007
of 1934 (‘‘Act’’) 1 and Rule 19b–4
thereunder,2 a proposed rule change to
list and trade notes linked to the
performance of the Hang Seng China
Enterprises Index (‘‘Index’’). Amex
amended the proposal on November 15,
2006 and subsequently on December 12,
2006.3 The proposed rule change, as
amended, was published for comment
in the Federal Register on December 26,
2006.4 No comments were received on
the proposal. This order approves the
proposed rule change, as amended.
Under Section 107A of its Company
Guide (‘‘Company Guide’’), Amex
proposes to list notes issued by
Citigroup Funding, Inc. (the ‘‘Issuer’’)
under the name ‘‘Stock Market Upturn
Notes’’ that are based on the value of the
Index (the ‘‘Notes’’). The Index is
currently based on 37 common stocks
that are listed and traded on the Stock
Exchange of Hong Kong and are among
the largest companies in the 200-stock
Hang Seng Composite Index (‘‘HSCI’’).
The Index is compiled by HSI Services
Limited (the ‘‘Index Calculator’’), a
wholly owned subsidiary of Hang Seng
Bank. The Index is capitalizationweighted and revised twice each year to
eliminate any components whose
weight might exceed 15% of the Index.
The Notes would offer investors
exposure to certain stocks traded on the
Stock Exchange of Hong Kong. The
Notes would be cash-settled in U.S.
dollars, must be held to maturity, and
would pay out according to a formula
set forth in the notice of Amex’s
proposal.5 Unlike traditional debt
securities, the Notes would not have a
minimum principal amount that would
be repaid at maturity and thus the
return could be less than the original
issue price. The Notes would entitle the
holder at maturity to receive an amount
based on the percentage change of the
Index, subject to a maximum payment
determined at the time of issuance.
The Notes would be senior nonconvertible debt securities of the Issuer.
Like traditional debt securities,
therefore, the Notes are dependent upon
the creditworthiness of the Issuer. This
credit risk is addressed by the listing
standards in Amex Rule 107A, which
provide that a security may not be listed
on the Exchange unless its issuer
satisfies certain financial requirements.
Section 107A of the Company Guide
also requires a market value of $4
Jkt 211001
U.S.C. 78s(b)(l).
CFR 240. 19b–4.
3 Amendment No. 2 replaced and superseded the
original rule filing and Amendment No. 1 in their
entirety.
4 Securities Exchange Act Release No. 54943
(December 15, 2006), 71 FR 77422 (‘‘Notice’’).
5 See Notice, supra note 4, 71 FR at 77423–24.
2 17
PO 00000
Frm 00088
Fmt 4703
Sfmt 4703
6795
million for initial listing. In addition,
the Notes would have to comply with
continued listing standards in Sections
1001–1003 of the Amex Company
Guide. Under Section 1002(b) of the
Company Guide, the Exchange would
consider removing from listing any
security where, in the opinion of the
Exchange, it appears that the extent of
public distribution or aggregate market
value has become so reduced to make
further dealings on the Exchange
inadvisable.6
The Notes would trade as equity
securities subject to Amex rules
governing, among other things, priority,
parity, and precedence of orders;
specialist responsibilities; margin; and
customer suitability requirements. In
addition, the Exchange would halt
trading in the Notes if the circuit
breaker parameters of Exchange Rule
117 are reached. In exercising its
discretion to halt or suspend trading in
the Notes, the Exchange may consider
the factors set forth in Exchange Rule
918C(b), and other factors that may be
relevant. In particular, if the Index value
is not being disseminated as required,
the Exchange may halt trading during
the day in which the interruption to the
dissemination of the Index value occurs.
If the interruption to the dissemination
of the Index value persists past the
trading day in which it occurred, the
Exchange would halt trading no later
than the beginning of the trading day
following the interruption.
Amex has represented that it would
rely on its existing surveillance
procedures governing index-linked
securities, which Amex represents are
adequate to properly monitor trading in
the Notes. The Exchange has an
information-sharing agreement with the
Stock Exchange of Hong Kong for the
purpose of providing information in
connection with trading in or related to
the components comprising the Index.
After careful consideration, the
Commission finds that the proposed
rule change is consistent with the
requirements of the Act and the rules
and regulations thereunder applicable to
a national securities exchange.7 In
particular the Commission finds that the
proposed rule change is consistent with
the requirements of section 6(b)(5) of the
6 In this case, the Exchange would look for
guidance to Section 1003(b)(iv)(A) (relating to
bonds) which states that the Exchange would
normally consider suspending dealings in, or
removing from the list, a security if the aggregate
market value or the principal amount of the bonds
publicly held is less than $400,000.
7 In approving the rule, the Commission notes
that it has considered the proposed rule’s impact on
efficiency, competition and capital formation. See
15 U.S.C. 78c(f).
E:\FR\FM\13FEN1.SGM
13FEN1
Agencies
[Federal Register Volume 72, Number 29 (Tuesday, February 13, 2007)]
[Notices]
[Pages 6780-6795]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: E7-2323]
=======================================================================
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from January 19, 2007, to February 1, 2007. The
last biweekly notice was published on January 30, 2007 (72 FR 4304).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the
[[Page 6781]]
following amendment requests involve no significant hazards
consideration. Under the Commission's regulations in 10 CFR 50.92, this
means that operation of the facility in accordance with the proposed
amendment would not (1) involve a significant increase in the
probability or consequences of an accident previously evaluated; or (2)
create the possibility of a new or different kind of accident from any
accident previously evaluated; or (3) involve a significant reduction
in a margin of safety. The basis for this proposed determination for
each amendment request is shown below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rulemaking,
Directives and Editing Branch, Division of Administrative Services,
Office of Administration, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, and should cite the publication date and
page number of this Federal Register notice. Written comments may also
be delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike,
Rockville, Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received may be examined at the Commission's
Public Document Room (PDR), located at One White Flint North, Public
File Area O1F21, 11555 Rockville Pike (first floor), Rockville,
Maryland. The filing of requests for a hearing and petitions for leave
to intervene is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by:
[[Page 6782]]
(1) first class mail addressed to the Office of the Secretary of the
Commission, U.S. Nuclear Regulatory Commission, Washington, DC 20555-
0001, Attention: Rulemaking and Adjudications Staff; (2) courier,
express mail, and expedited delivery services: Office of the Secretary,
Sixteenth Floor, One White Flint North, 11555 Rockville Pike,
Rockville, Maryland 20852, Attention: Rulemaking and Adjudications
Staff; (3) E-mail addressed to the Office of the Secretary, U.S.
Nuclear Regulatory Commission, HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of the Secretary, U.S. Nuclear
Regulatory Commission, Washington, DC, Attention: Rulemakings and
Adjudications Staff at (301) 415-1101, verification number is (301)
415-1966. A copy of the request for hearing and petition for leave to
intervene should also be sent to the Office of the General Counsel,
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, and it
is requested that copies be transmitted either by means of facsimile
transmission to (301) 415-3725 or by e-mail to OGCMailCenter@nrc.gov. A
copy of the request for hearing and petition for leave to intervene
should also be sent to the attorney for the licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)7ndash;(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric
Station, Unit 3, St. Charles Parish, Louisiana
Date of amendment request: September 26, 2006.
Description of amendment request: The proposed change deletes
reference to the containment fan cooler (CFC) condensate flow switch
from Technical Specification (TS) 3.4.5.1, ``Reactor Coolant System
Leakage--Leakage Detection Instrumentation,'' and to modify or delete
associated actions.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The Reactor Coolant System (RCS) leakage detection systems are
passive monitoring systems therefore the proposed changes do not
affect reactor operations or accident analyses and have no
radiological consequences. The proposed change continues to require
diverse methods of monitoring leakage. The gaseous radioactivity
monitor, although not included in the TSs and the CFC condensate
flow switches, which are proposed for removal from the TSs, will be
maintained functional and available.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change introduces no new mode of plant operation or
any plant modification. The RCS leakage detection instrumentation is
used solely for monitoring purposes and is not part of plant control
instruments or engineered safety feature actuation circuits. The
change does not vary or affect any plant operating condition or
parameter.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change does not modify any of the RCS leakage
detection instrumentation. The proposed change continues to require
diverse methods of monitoring leakage. In addition, although not
required by TS, multiple means of diverse monitoring RCS leakage
will remain functional and available.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Terence A. Burke, Associate General
Council--Nuclear Entergy Services, Inc., 1340 Echelon Parkway, Jackson,
Mississippi 39213.
NRC Branch Chief: David Terao.
Entergy Operations, Inc., System Energy Resources, Inc., South
Mississippi Electric Power Association, and Entergy Mississippi, Inc.,
Docket No. 50-416, Grand Gulf Nuclear Station, Unit 1, Claiborne
County, Mississippi
Date of amendment request: January 18, 2007.
Description of amendment request: The proposed change will revise
the description of Grand Gulf Nuclear Station Technical Specification
4.2.2, ``Control Rod Assemblies,'' to allow to the use of hafnium as an
additional type of control material.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The NRC has specifically approved the use of hafnium as neutron
absorbing material for use in BWR [boiling-water reactor] control
rod assemblies. The use of hafnium in control rods as a neutron
absorber material does not significantly alter the neutronic or
mechanical functional characteristics of the control rods. Control
rod designs using hafnium have been successfully used in other BWRs.
Since control rods that utilize hafnium have a longer lifetime, the
probability of some accidents involving the handling, on-site
storage, and shipping of irradiated rods will actually be reduced.
The proposed change does not alter the required number of control
rods nor does it affect any of the specifications related to the
control rods (e.g., the shutdown margin and scram timing
requirements are unaffected).
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The application of a control rod design using hafnium as an
absorber material does not produce any new mode of plant operation
or alter the control rods in such a way as to affect their function
or operability since the new control rods are designed to be
compatible with the existing control rods.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
[[Page 6783]]
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change does not significantly affect the neutronic
or mechanical characteristics of the control rods since the hafnium
containing controls rods are designed to be compatible with the
existing design and reload licensing criteria; therefore, there is
no significant change in the margin of safety. It does not change
the required number of existing control rods. It does not affect the
existing Technical Specifications related to control rods (e.g.,
required shutdown margin and scram time, etc.).
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Terence A. Burke, Associate General
Council--Nuclear Entergy Services, Inc., 1340 Echelon Parkway, Jackson,
Mississippi 39213.
NRC Branch Chief: David Terao.
Florida Power Corporation, et al., Docket No. 50-302, Crystal River
Unit 3 Nuclear Generating Plant (CR-3), Citrus County, Florida
Date of amendment request: October 11, 2006.
Description of amendment request: The proposed amendment would
modify the plant Improved Technical Specifications (ITSs) to implement
a more conservative requirement in ITS 3.7.7, ``Nuclear Services Closed
Cycle Cooling Water (SW) System.'' The current Action A allows the
plant to operate for up to 72 hours before initiating a shutdown when
one required SW heat exchanger is inoperable. The proposed revision
will only allow operation to continue for 8 hours before initiating a
shutdown when one required SW heat exchanger is inoperable.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
(1) Does not involve a significant increase in the probability
or consequences of an accident previously evaluated.
The limiting design basis accident for CR-3 includes, as an
assumption, adequate heat removal capability by the SW system. The
amendment is being proposed to ensure the SW system performs its
design basis function. Adequate heat removal is provided by three
OPERABLE SW heat exchangers. The 8 hour completion time will reduce
the window that the plant can operate with only two SW heat
exchangers before a shutdown is required. The proposed change does
not increase the probability of an accident previously evaluated
since the amendment is not a modification to plant systems, nor a
change to plant operation that could initiate an accident.
Therefore, granting the LAR [license amendment request] does not
involve a significant increase in the probability or consequences of
an accident previously evaluated. The dose consequences of all
design basis accidents are unchanged by this proposed amendment.
(2) Does not create the possibility of a new or different kind
of accident from any accident previously evaluated?
The function of the SW system considered in the design basis is
to remove process and operating heat from safety-related components
during normal as well as transient conditions. The proposed
amendment to limit the allowed ACTION Completion Time to 8 hours
will ensure the function of the SW system is consistent with the
design basis and will not result in changes to the design, physical
configuration of the plant or the assumptions made in the safety
analysis. The requirement does not change the function of the system
nor its ability to perform its design function. No alteration to
plant configuration or operation is proposed. Therefore, the
proposed change will not create the possibility of a new or
different kind of accident from any previously evaluated.
(3) Does not involve a significant reduction in a margin of
safety?
CR-3's design basis considers adequate heat removal by the SW
system to cool the containment fan assembly cooling coils and fan
motors, spent fuel pool, SW pump motors and other equipment which
must function following an accident. This proposed amendment will
not alter the current design basis. By limiting the allowed ACTION
Completion Time to 8 hours, the proposed amendment to ITS 3.7.7 will
limit the time the safety function of the SW system can be
compromised. Therefore, the amendment does not result in a reduction
of the margin of safety.
The NRC staff has reviewed the analysis provided for Florida Power
Corporation and, based on this review, it appears that the three
standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff
proposes to determine that the amendment request involves no
significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Branch Chief (Acting): Margaret H. Chernoff.
GPU Nuclear, Inc., Docket No. 50-320, Three Mile Island Nuclear
Station, Unit 2, Dauphin County, Pennsylvania
Date of amendment request: December 13, 2006.
Description of amendment requests: The amendment application
proposes to delete Technical Specification (TS) 6.8.1.3, which provides
the requirement for submittal of the annual occupational radiation
exposure report.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
No
The proposed change eliminates the Technical Specification
reporting requirement for occupational radiation exposure
information, which is in excess to that required to be submitted by
regulations. The proposed change involves no changes to plant
systems or accident analyses. As such, the change is administrative
in nature and does not affect initiators of analyzed events or
assumed mitigation of accidents. Therefore, the proposed change does
not involve a significant increase in the probability or
consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
No
The proposed change does not involve a physical alteration of
the plant, add any new equipment, or require any existing equipment
to be operated in a manner different from the present design.
Therefore, the proposed change does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety? No
This change is an administrative change to reporting
requirements of occupational radiation exposure data and will not
reduce a margin of safety because it has no effect on any safety
analyses assumptions. Hence, this change is administrative in
nature. For these reasons, the proposed change does not involve a
significant reduction in the margin of safety.
The NRC staff has reviewed the licensee's analysis, and based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
NRC Branch Chief: Claudia Craig.
[[Page 6784]]
Nuclear Management Company, LLC, Docket Nos. 50-266 and 50-301, Point
Beach Nuclear Plant, Units 1 and 2, Town of Two Creeks, Manitowoc
County, Wisconsin
Date of amendment request: December 21, 2006.
Description of amendment request: The proposed amendment revises
the licensing basis to reflect a revision to the spent fuel pool
criticality analysis methodology and a new criticality analysis. In
addition, associated changes are proposed to Technical Specifications
3.7.12, ``Spent Fuel Storage,'' and 4.3.1, ``Criticality,'' to reflect
the results of the new criticality analysis.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
(1) Does the proposed amendment involve a significant increase
in the probability or consequences of an accident previously
evaluated?
Response: No
Operation of the facility in accordance with the proposed
amendment request does not involve a significant increase in the
probability or consequences of an accident previously evaluated. The
presence of soluble boron in the Spent Fuel Pool (SFP) water being
used for criticality control does not increase the probability of a
dropped fuel assembly accident within the pool. The handling of the
fuel assemblies in the SFP has always been performed and will
continue to be performed in borated water.
There is no increase in the probability of the accidental
misloading of fuel assemblies into the SFP fuel storage racks when
considering the presence of soluble boron in the pool water for
criticality control. Fuel assembly placement will continue to be
controlled pursuant to approved fuel handling procedures and in
accordance with the spent fuel storage rack limitations specified in
the Technical Specifications (TS). There is no increase in the
consequences for an accidental misloading of fuel assemblies in the
SFP fuel storage racks because the criticality analyses demonstrate
that the pool will remain subcritical following an accidental
misloading.
Soluble boron credit is used to provide margin to offset
uncertainties, tolerances, and off-normal/accident conditions, and
to provide subcritical margin such that the SFP keff
[effective neutron multiplication constant] is maintained less than
or equal to 0.95. The plant-specific criticality analysis results
demonstrate that the spent fuel rack keff will remain<1.0
(at a 95/95 percent probability and confidence level) even with the
SFP flooded with unborated water.
There is no increase in the probability of the loss of normal
cooling to the SFP water when considering the presence of soluble
boron in the pool water for subcriticality control since a high
concentration of soluble boron has always been maintained in the SFP
water.
A loss of normal cooling to the SFP water causes an increase in
the temperature of the water passing through the stored fuel
assemblies. This causes a decrease in water density, which would
result in a net increase in reactivity when soluble boron is present
in the water. However, the additional negative reactivity provided
by the 2100 ppm [parts per million] boron concentration limit, above
that provided by the concentration required (805 ppm) to maintain
keff less than or equal to 0.95, will compensate for the
increased reactivity which could result from a loss of SFP cooling
event. Because adequate soluble boron will be maintained in the SFP
water the consequences of a loss of normal cooling to the SFP will
not be increased.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
(2) Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No
Under the proposed amendment, no changes are being made to the
fuel storage racks themselves, to any other systems, or to the
physical structures of the Primary Auxiliary Building. Therefore,
there are no changes proposed to the plant configuration, equipment
design, or installed equipment.
Criticality accidents in the SFP are not new or different types
of accidents. They have been analyzed in the FSAR [Final Safety
Analysis Report] and in fuel storage criticality analysis reports
associated with specific licensing amendments. The proposed new SFP
storage limitations are consistent with the assumptions made in the
new criticality analysis, and will not have any significant effect
on normal SFP operations and maintenance, and do not create the
possibility of a new or different kind of accident. Verifications
will continue to be performed to ensure that the SFP loading
configuration meets specified requirements.
The current TS includes a SFP boron concentration limit that
conservatively bounds the boration assumption of the new criticality
analysis. Since soluble boron has always been maintained in the SFP
water, implementation of this requirement for SFP criticality
control purposes has have no effect on normal pool operations and
maintenance. Also, since soluble boron has always been present in
the SFP, a dilution event has always been a possibility. The loss of
substantial amounts of soluble boron from the SFP that could lead to
keff exceeding 0.95 was evaluated as part of the analyses
in support of this license amendment request. The evaluation
demonstrates that a dilution of the SFP boron concentration from the
minimum TS concentration of 2100 to 805 ppm is not credible.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
(3) Does the proposed amendment result in a significant
reduction in a margin of safety?
Response: No
The proposed Technical Specification changes providing the
resulting spent fuel storage operation limits provide adequate
safety margin to ensure that the stored fuel assembly array always
remains subcritical. These limits are based on a plant-specific
criticality analysis performed in accordance with the present
Westinghouse spent fuel rack criticality analysis methodology which
allows credit for soluble boron.
The criticality analysis takes credit for soluble boron to
ensure that keff will be less than or equal to 0.95 under
normal circumstances. While the criticality analysis used credit for
soluble boron, storage configurations have been defined using 95/95
keff calculations to ensure that the spent fuel rack
keff is less than unity (0.995) with no soluble boron.
Soluble boron credit is used to provide safety margin to offset
uncertainties, tolerances, and off-normal/accident conditions, and
to provide subcritical margin such that the SFP keff is
maintained less than or equal to 0.95.
The loss of substantial amounts of soluble boron from the SFP
that could lead to keff exceeding 0.95 was evaluated as
part of the analyses in support of this license amendment request.
The evaluation demonstrates that a dilution of the SFP boron
concentration from the minimum TS concentration of 2100 to 805 ppm
is not credible. Also, the plant-specific criticality analysis
results demonstrate that even if a complete dilution were to occur
the spent fuel rack keff would remain <1.0 (at a 95/95
percent probability and confidence level) with the SFP flooded with
unborated water. The plant-specific criticality analysis performed
in accordance with the conservative analysis methodology of the
Westinghouse licensing topical report demonstrates that the
requirements of 10 CFR 50.68 and 10 CFR 50, Appendix A, General
Design Criterion 62 will be satisfied. Therefore, the proposed
changes do not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Jonathan Rogoff, Esquire, Vice President,
Counsel & Secretary, Nuclear Management Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Acting Branch Chief: Patrick D. Milano.
Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo
Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County,
California
Date of amendment request: December 29, 2006.
Description of amendment request: The proposed amendments would
[[Page 6785]]
revise Technical Specification (TS) 5.5.8 to indicate that the
Inservice Testing Program shall include testing frequencies applicable
to the American Society of Mechanical Engineers Code for Operations and
Maintenance (ASME OM Code), and to indicate that there may be some non-
standard frequencies specified as 2 years or less in the Inservice
Testing Program to which the provisions of Surveillance Requirement
(SR) 3.0.2 are applicable. The proposed changes are consistent with
NRC-approved Technical Specification Task Force (TSTF) Travelers TSTF-
479, Revision 0, ``Changes to Reflect Revision of 10 CFR 50.55a,'' and
TSTF-497, Revision 0, ``Limit Inservice Testing Program SR 3.0.2
Application to Frequencies of 2 Years or Less.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes revise TS 5.5.8, ``lnservice Testing
Program,'' for consistency with 10 CFR 50.55a(f)(4) requirements
regarding inservice testing of pumps and valves. The proposed change
incorporates revisions to the ASME Code that result in a net
improvement in the measures for testing pumps and valves.
The proposed changes do not impact any accident initiators or
analyzed events or assumed mitigation of accident or transient
events. They do not involve the addition or removal of any
equipment, or any design changes to the facility. Therefore, the
proposed changes do not represent a significant increase in the
probability or consequences of an accident previously evaluated.
2. [Do] the proposed change[s] create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No
The proposed changes do not involve a modification to the
physical configuration of the plant (i.e., no new equipment will be
installed) or change in the methods governing normal plant
operation. The proposed change will not impose any new or different
requirements or introduce a new accident initiator, accident
precursor, or malfunction mechanism. Additionally, there is no
change in the types or increases in the amounts of any effluent that
may be released off-site and there is no increase in individual or
cumulative occupational exposure. Therefore, this proposed change
does not create the possibility of an accident of a different kind
than previously evaluated.
3. [Do] the proposed change[s] involve a significant reduction
in a margin of safety?
Response: No
The proposed changes revise TS 5.5.8, ``lnservice Testing
Program,'' for consistency with the requirements of 10 CFR
50.55a(f)(4) regarding the inservice testing of pumps and valves.
The proposed change incorporates revisions to the ASME Code that
result in a net improvement in the measures for testing pumps and
valves. The safety function of the affected pumps and valves will be
maintained. Therefore, this proposed change does not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Attorney for licensee: Antonio Fernandez, Esq., Pacific Gas and
Electric Company, P.O. Box 7442, San Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo
Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County,
California
Date of amendment requests: December 29, 2006.
Description of amendment requests: The proposed amendments will
revise Technical Specification (TS) 5.5.16 for consistency with the
requirements of 10 CFR 50.55a(g)(4) for components classified as Code
Class CC. This regulation requires licensees to update their
containment inservice inspection requirements in accordance with
Subsections IWE and IWL of Section XI, Division I of the American
Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code
as limited by 10 CFR 50.55a(b)(2)(vi) and modified by 10 CFR
50.55a(b)(2)(viii) and 10 CFR 50.55a(b)(2)(ix). This license amendment
request is consistent with NRC-approved Industry/Technical
Specification Task Force (TSTF) Traveler number TSTF-343, ``Containment
Structural Integrity.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change revises the Technical Specification (TS)
administrative controls programs for consistency with the
requirements of 10 CFR [Part] 50, paragraph 55a(g)(4) for components
classified as Code Class CC.
The proposed change affects the frequency of visual examinations
that will be performed for the concrete surfaces of the containment
for the purpose of the Containment Leakage Rate Testing Program. In
addition, the proposed change allows those examinations to be
performed during power operation as opposed to during a refueling
outage. The frequency of visual examinations of the concrete
surfaces of the containment and the mode of operation during which
those examinations are performed has no relationship to or adverse
impact on the probability of any of the initiating events assumed in
the accident analyses. The proposed change would allow visual
examinations that are performed pursuant to NRC-approved ASME
[Code,] Section XI requirements (except where relief has been
granted by the NRC) to meet the intent of visual examinations
required by Regulatory Guide 1.163, without requiring additional
visual examinations pursuant to the Regulatory Guide. The intent of
early detection of deterioration will continue to be met by the more
rigorous requirements of the Code-required visual examinations. As
such, the safety function of the containment as a fission product
barrier is maintained.
The proposed change does not impact any accident initiators or
analyzed events or assumed mitigation of accident or transient
events. It does not involve the addition or removal of any
equipment, or any design changes to the facility.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different accident from any accident previously evaluated?
Response: No.
The proposed change revises the TS Administrative Controls
programs for consistency with the requirements of 10 CFR [Part] 50,
paragraph 55a(g)(4) for components classified as Code Class CC.
The change affects the frequency of visual examinations that
will be performed for the concrete surfaces of the containments. In
addition, the proposed change allows those examinations to be
performed during power operation as opposed to during a refueling
outage. The proposed change does not involve a modification to the
physical configuration of the plant (i.e., no new equipment will be
installed) or a change in the methods governing normal plant
operation. The proposed change will not impose any new or different
requirements or introduce a new accident initiator, accident
precursor, or a malfunction mechanism. Additionally, there is no
change in the types or increases in the amounts of any effluent that
may be released offsite and there is no increase in individual or
cumulative occupational exposure.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
[[Page 6786]]
Response: No.
The proposed change revises the TS Administrative Controls
programs for consistency with the requirements of 10 CFR [Part] 50,
paragraph 55a(g)(4) for components classified as Code Class CC.
The change affects the frequency of visual examinations that
will be performed for the concrete surfaces of the containments. In
addition, the proposed change allows those examinations to be
performed during power operation as opposed to during a refueling
outage. The safety function of the containment as a fission product
barrier will be maintained.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Attorney for licensee: Antonio Fern[aacute]ndez, Esq., Pacific Gas
and Electric Company, P.O. Box 7442, San Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo
Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County,
California
Date of amendment requests: December 29, 2006.
Description of amendment requests: The proposed amendments will
revise Technical Specification (TS) 3.4.1, ``RCS [Reactor Coolant
System] Pressure, Temperature, and Flow Departure from Nucleate Boiling
(DNB) Limits,'' and TS 5.6.5, ``CORE OPERATING LIMITS REPORT (COLR).
This license amendment request proposes to relocate the RCS DNB
parameters for pressurizer pressure and RCS average temperature to the
COLR. This relocation is consistent with Technical Specification Task
Force Traveler TSTF-339, Revision 2, ``Relocate TS Parameters to
COLR.'' TS 5.6.5 is revised to add topical reports WCAP-8567-P-A,
``Improved Thermal Design Procedure,'' and WCAP-11596-P-A,
``Qualification of the PHOENIX-P/ANC Nuclear Design System for
Pressurized Water Reactor Cores,'' by name and title only. These
changes are consistent with TSTF-363, Revision 0, ``Revise Topical
Report References in ITS 5.6.5, COLR.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. [Do] the proposed change[s] involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes are programmatic and administrative in
nature, and do not physically alter safety-related systems or affect
the way in which safety-related systems perform their functions. The
proposed changes relocate cycle-specific parameters from Technical
Specification (TS) 3.4.1 to the Core Operating Limits Report (COLR).
This does not change plant design or affect system operating
parameters. The proposed changes do not, by themselves, alter any of
the parameters. Removal of the cycle-specific parameters from the TS
does not eliminate existing requirements to comply with the
parameters. Also, TS 5.6.5 is revised to add topical reports WCAP-
8567-P-A, ``Improved Thermal Design Procedure,'' and WCAP-11596-P-A,
``Qualification of the PHOENIX-P/ANC Nuclear Design System for
Pressurized Water Reactor Cores,'' as they are approved analytical
methods for determining core operating limits.
Although relocation of the cycle-specific parameters to the COLR
would allow revision of the affected parameters without prior NRC
approval, there is no significant effect on the probability or
consequences of an accident previously evaluated. Future changes to
the COLR parameters could result in event consequences that are
either slightly less or slightly more severe than the consequences
for the same event using the present parameters. The differences
would not be significant and would be bounded by the existing
requirement of TS 5.6.5c to meet the applicable limits of the safety
analyses.
The cycle-specific parameters being transferred from the TS to
the COLR will continue to be controlled under existing programs and
procedures. The Final Safety Analysis Report Update (FSARU) accident
analyses will continue to be examined with respect to changes in the
cycle-dependent parameters obtained using NRC reviewed and approved
reload design methodologies to ensure that the transient evaluation
of new reload designs are bounded by previously accepted analyses.
This examination will continue to be performed pursuant to 10 CFR
50.59 requirements, ensuring that future reload designs use NRC-
approved methodologies and do not involve more than a minimal
increase in the probability or consequences of an accident
previously evaluated in the FSARU.
The proposed changes do not allow for an increase in plant power
levels, do not increase the production, and do not alter the flow
path or method of disposal of radioactive waste or byproducts.
Therefore, the proposed changes do not change the type or increase
the amount of effluents released offsite.
The proposed changes to TS 5.6.5b to reference only the topical
report number and title for five of the topical reports do not alter
the analytical methods that have been previously reviewed and
approved by the NRC. This method of referencing topical reports
would allow the use of current topical reports to support limits in
the COLR without having to submit a request for an amendment to the
operating license. Implementation of revisions to these topical
reports would still be reviewed in accordance with 10 CFR 50.59 and,
where required, revisions would be submitted to the NRC for approval
prior to implementation.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. [Do] the proposed change[s] create the possibility of a new
or different accident from any accident previously evaluated?
Response: No.
The proposed changes that relocate cycle-specific parameters
from the TS to the COLR, thus removing the requirement for prior NRC
approval of revisions to those parameters, do not involve a physical
change to the plant. No new equipment is being introduced, and
installed equipment is not being operated in a new or different
manner. No changes are being made to the parameters within which the
plant is operated, other than their relocation to the COLR. No
protective or mitigative action setpoints are affected by the
proposed changes. The proposed changes will not alter the manner in
which equipment operation is initiated, nor will the functional
demands on credited equipment be changed. No change to procedures
that ensure the plant remains within analyzed limits are being
proposed, and no change is being made to procedures relied upon to
respond to an off-normal event. As such, no new failure modes are
being introduced.
Relocation of cycle-specific parameters does not influence,
impact, or contribute in any way to the possibility of a new or
different kind of accident. The relocated cycle-specific parameters
will continue to be calculated using the NRC-reviewed and approved
methodology. The proposed changes do not alter assumptions made in
the safety analysis, and operation within the core operating limits
will continue.
The proposed changes to reference only the topical report number
and title do not alter the use of the analytical methods that have
been previously reviewed and approved by the NRC. This method of
referencing topical reports would allow the use of current topical
reports to support limits in the COLR without having to submit a
request for an amendment to the operating license. Implementation of
revisions to topical reports would still be reviewed in accordance
with 10 CFR 50.59 and, where required, would receive NRC review and
approval.
The addition of WCAP-8567-P-A and WCAP-11596-P-A to TS 5.6.5 is
a clarification to provide a complete listing of approved analytical
methods used for determining core operating limits.
Therefore, the proposed change does not create the possibility
of a new or different accident from any accident previously
evaluated.
3. [Do] the proposed change[s] involve a significant reduction
in a margin of safety?
Response: No.
The margin of safety is established through equipment design,
operating parameters, and the setpoints at which automatic actions
are
[[Page 6787]]
initiated. The proposed changes do not physically alter safety-
related systems, nor do they affect the way in which safety-related
systems perform their functions. No protective or mitigative action
setpoints are affected by the proposed changes. Therefore,
sufficient equipment remains available to actuate upon demand for
the purpose of mitigating an analyzed event. As the proposed changes
to relocate cycle-specific parameters to the COLR will not affect
plant design or system operating parameters, there is no detrimental
impact on any equipment design parameter, and the plant will
continue to be operated within prescribed limits.
The development of cycle-specific parameters for future reload
designs will continue to conform to NRC-reviewed and approved
methodologies, and will be performed pursuant to 10 CFR 50.59 to
assure that the plant operates within cycle-specific parameters.
The proposed changes to reference only the topical report number
and title do not alter the use of the analytical methods used to
determine core operating limits that have been reviewed and approved
by the NRC. This method of referencing topical reports would allow
the use of current NRC-approved topical reports to support limits in
the COLR without having to submit a request for an amendment to the
operating license. Implementation of revisions to topical reports
would still be reviewed in accordance with 10 CFR 50.59 and, where
required, receive NRC review and approval.
The addition of WCAP-8567-P-A and WCAP-11596-P-A to TS 5.6.5 is
a clarification to provide a complete listing of approved analytical
methods used for determining core operating limits.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Attorney for licensee: Antonio Fern[aacute]ndez, Esq., Pacific Gas
and Electric Company, P.O. Box 7442, San Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo
Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County,
California
Date of amendment requests: January 11, 2007.
Description of amendment requests: The proposed amendments would
revise the Technical Specifications (TSs) to support replacement of the
steam generators (SGs) at Diablo Canyon Power Plant, Unit Nos. 1 and 2.
Revisions are proposed to TS 3.3.2, ``Engineered Safety Feature
Actuation System (ESFAS) Instrumentation,'' TS 5.5.9, ``Steam Generator
(SG) Program,'' and TS 5.6.10, ``Steam Generator (SG) Tube Inspection
Report.'' The replacement SGs are to be installed during the Diablo
Canyon Power Plant, Unit No. 2, 14th refueling outage (2R14), currently
scheduled for February 2008, and the Unit No. 1, 15th refueling outage
(1R15), currently scheduled for January 2009.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. [Do] the proposed change[s] involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The revised engineered safety feature actuation system (ESFAS)
steam generator (SG) Water Level-High High feedwater isolation
Nominal Trip Setpoint and Allowable Value have been determined using
the existing setpoint methodology approved for Diablo Canyon Power
Plant. The setpoint analysis for the replacement steam generators
(RSGs) accounts for the setpoint uncertainties specific to the RSG
design. The revised Feedwater Isolation SG Water Level-High High (P-
14) Nominal Trip Setpoint and Allowable Value are applied using a
conservative surveillance requirement methodology. The function of
the ESFAS instrumentation is unchanged. The Feedwater Isolation SG
Water Level-High High (P-14) ESFAS instrumentation will continue to
function in a manner consistent with the plant design basis and
satisfy all the requirements of the safety analyses.
The probability and consequences of accidents previously
evaluated in the Final Safety Analysis Report (FSAR) Update are not
adversely affected because the revised Feedwater Isolation SG Water
Level-High High (P-14) Nominal Trip Setpoint and Allowable Value
continue to assure a conservative plant response to high SG level,
consistent with the safety analyses and licensing basis.
The proposed changes revise and clarify the surveillance
requirements for ESFAS Function 5.b, Feedwater Isolation SG Water
Level-High High (P-14). These changes ensure that this function will
actuate as assumed in the safety analyses.
The proposed changes to TS 5.5.9 delete the alternate repair
criteria (ARC) for the existing SGs, incorporate tube inspection
periods applicable to Alloy 690 thermally treated tubes, and delete
the TS 5.6.10 reporting requirements for ARC. The TS 5.5.9 SG
structural integrity, accident induced leakage, and operational
leakage performance criteria will continue to be met for the RSGs.
Meeting the SG performance criteria provides reasonable assurance
that the SG tubes will remain capable of maintaining reactor coolant
pressure boundary integrity throughout each operating cycle and in
the unlikely event of a design basis accident. Removal of the ARC
for the existing SGs will ensure that all tubes found by inservice
inspection to contain flaws with a depth equal to or exceeding 40
percent of the nominal tube wall thickness will be plugged as
required by TS 5.5.9.c. With the revised SG tube inspection period,
the SGs will continue to meet the SG program defined by NEI [Nuclear
Energy Institute] 97-06, ``Steam Generator Program Guidelines,''
which incorporates a balance of prevention, inspection, evaluation,
repair, and leakage monitoring.
Removal of the ARC will reduce the allowable accident induced
leakage following a main steamline break accident. The proposed
changes do not have any impact on the accident induced leakage
assumed in the other design basis accidents. The changes do not have
any impact on the allowable SG operational leakage, allowable
reactor coolant system activity, or the allowable SG secondary
activity.
The proposed changes will not affect the probability of any
accident initiators. There will be no degradation in the performance
of, or an increase in the number of challenges imposed on, safety-
related equipment assumed to function during an accident. There will
be no change to accident mitigation performance. The proposed
changes will not alter any assumptions or change any mitigation
actions in the radiological consequence evaluations in the FSAR
Update.
Therefore the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. [Do] the proposed change[s] create the possibility of a new
or different accident from any accident previously evaluated?
Response: No.
The proposed changes will not affect the normal method of plant
operation or create new methods of plant operation related to the
Feedwater Isolation SG Water Level-High High (P-14) ESFAS setpoints.
The proposed changes to the Feedwater Isolation SG Water Level-High
High (P-14) instrumentation surveillance requirements will provide
assurance that the plant will operate within the limits assumed in
the safety analyses. The assumptions made in the setpoint analyses
for the Feedwater Isolation SG Water Level-High High (P-14) ESFAS
instrument do not create any new accidents, accident initiators, or
failure mechanisms.
The proposed changes, which delete the TS 5.5.9 ARC for the
existing SGs, incorporate tube inspection periods for Alloy 690
thermally-treated tubes in TS 5.5.9, and delete the ARC reporting
requirements in TS 5.6.10, will not introduce any adverse changes to
the plant design basis or postulated accidents resulting from
potential tube degradation. The primary-to-secondary leakage that
may be experienced during all plant conditions will be monitored to
ensure it remains within current safety analysis assumptions. The
proposed changes do not adversely affect the method of operation of
the SGs or the primary or secondary coolant controls and do not
impact other plant systems or components.
[[Page 6788]]
Therefore, the proposed changes do not create the possibility of
a new or different accident from any accident previously evaluated.
3. [Do] the proposed change[s] involve a significant reduction
in a margin of safety?
Response: No.
The FSAR Update Excessive Heat Removal due to Feedwater System
Malfunctions event credits the Feedwater Isolation SG Water Level-
High High (P-14) ESFAS instrumentation. The safety analysis limit
assumed for the Feedwater Isolation SG Water Level-High High (P-14)
ESFAS instrumentation for this event has not changed for the safety
analyses for the RSGs. None of the acceptance criteria for Excessive
Heat Removal due to Feedwater System Malfunctions event are changed
as a result of the revised Feedwater Isolation SG Water Level-High
High (P-14) Nominal Trip Setpoint and Allowable Value. The
instrument surveillance requirement changes for the Feedwater
Isolation SG Water Level-High High (P-14) function ensure that the
instrumentation will actuate as assumed in the safety analysis.
The safety function of the SGs is maintained by ensuring the
integrity of the tubes. SG tube integrity is a function of the
design, environment, and the physical condition of the SG tubes. The
proposed changes, which delete the TS 5.5.9 ARCs for the existing
SGs, incorporate tube inspection periods for Alloy 690 thermally
treated tubes in TS 5.5.9, and delete the ARC reporting requirements
in TS 5.6.10, do not adversely impact the SG tube design or
operating environment. SG tube integrity will continue to be
maintained by implementing the SG Program to manage SG tube
inspection, assessment, and repair. The requirements established by
the SG program are consistent with those in the applicable design
codes and standards.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Attorney for licensee: Antonio Fern[aacute]ndez, Esq., Pacific Gas
and Electric Company, P.O. Box 7442, San Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Co., Docket No. 50-133, Humboldt Bay Power
Plant (HBPP), Unit 3 Humboldt County, California
Date of amendment request: May 17, 2006.
Description of amendment request: The licensee has proposed to
modify the Physical Security Plan (PSP) to allow leaving certain
security posts temporarily under emergency conditions requiring
personnel to evacuate occupied plant areas for their health and safety.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
(1) Does the change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
Allowing the security posts and monitoring requirements of PSP,
Sections 3.1.4 and 4.3, and Table 7-1, to not be continuously
maintained has no impact on the probability of an accident from
occurring, especially acts of nature such as earthquakes and
tsunamis.
The HBPP Defueled Safety Analysis Report, Appendix A, and NRC
Safety Evaluation Report (SER), Section 10, dated April 29, 1987,
evaluate various accidents at HBPP. Because all fuel has been
removed from the reactor vessel and stored in the spent fuel pool,
the majority of accidents analyzed pertain to events that could only
affect spent fuel or the spent fuel pool. All accidents affecting
spent fuel or the spent fuel pool do not require security personnel
action to protect the public health and safety, or to maintain
offsite radiological doses well within regulatory limits. In
addition, NRC SER, Section 10.7, ``Impact of Tsunami Flooding,''
analyzes the impact of tsunami flooding. That analysis identifies a
likely impact of the tsunami to be a release of the radwaste tank
radionuclide contents to the bay and some damage to the reactor
building. For both situations, no security personnel action is
required to maintain offsite radiological doses well within
regulatory limits.
Allowing the security posts and monitoring requirements of PSP,
Sections 3.1.4 and 4.3, and Table 7-1, to not be continuously
maintained temporarily, under emergency conditions, does not create
problems that could increase the consequences of an accident. The
primary function of the manning and monitoring requirements of PSP,
Sections 3.1.4 and 4.3, and Table 7-1, is to monitor, detect and
assess unauthorized intrusion into the protected area, and has
nothing to do with the probability or consequences of plant
accidents.
If security personnel evacuate PSP, Section 3.1.4 and Table 7-1,
security posts during a tsunami, those security personnel will be
able to return to the PSP, Section 3.1.4 and Table 7-1, security
posts after the tsunami and assess damage or intrusion by observing
alarms and/or physical conditions as well as resume implementation
of security post and monitoring requirements of PSP, Sections 3.1.4
and 4.3, and Table 7-1. In addition, upon evacuation, security
personnel notify offsite security backup pe