Biweekly Notice, 67391-67403 [E6-19434]
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Federal Register / Vol. 71, No. 224 / Tuesday, November 21, 2006 / Notices
(c) NASA, Glenn Research Center at
Lewis Field, Cleveland, OH 44135 (866–
404–3642);
(d) NASA, Goddard Space Flight
Center, Greenbelt, MD 20771 (301–286–
4721);
(e) NASA, Johnson Space Center,
Houston, TX 77058 (281–483–8612);
(f) NASA, Kennedy Space Center, FL
32899 (321–867–2745);
(g) NASA, Langley Research Center,
Hampton, VA 23681 (757–864–2497);
(h) NASA, Marshall Space Flight
Center, Huntsville, AL 35812 (256–544–
1837); and
(i) NASA, Stennis Space Center, MS
39529 (228–688–2118).
NASA published a Notice of
Availability (NOA) of the Draft EIS
(DEIS) for the MSL mission in the
Federal Register on September 5, 2006,
(71 FR 52347) and made the DEIS
available in electronic format on its Web
site. The EPA published its NOA in the
Federal Register on September 8, 2006,
(71 FR 53093). In addition, NASA
published its NOA in local newspapers
in the Cape Canaveral, Florida regional
area, and in Washington, DC, and held
public meetings in Cocoa, Florida on
September 27, 2006, and in Washington,
DC on October 10, 2006, during which
attendees were invited to present both
oral and written comments on the DEIS.
Three comments relevant to the DEIS
were presented at these meetings. NASA
received 44 written comment
submissions, both hardcopy and
electronic, during the comment period
ending October 23, 2006. The comments
are addressed in the FEIS.
Olga M. Dominguez,
Assistant Administrator for Infrastructure
and Administration.
[FR Doc. E6–19610 Filed 11–20–06; 8:45 am]
BILLING CODE 7510–13–P
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice
Applications and Amendments to
Facility Operating Licenses Involving
No Significant Hazards Considerations
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I. Background
Pursuant to section 189a. (2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
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immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from October 27,
2006, to November 8, 2006. The last
biweekly notice was published on
November 7, 2006 (71 FR 65139).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
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67391
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rulemaking,
Directives and Editing Branch, Division
of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
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petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
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significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
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Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
AmerGen Energy Company, LLC, et al.,
Docket No. 50–219, Oyster Creek
Nuclear Generating Station (Oyster
Creek), Ocean County, New Jersey
Date of amendment request:
September 28, 2006.
Description of amendment request:
The amendment would revise the
Oyster Creek Technical Specifications
definition of Channel Calibration,
Channel Check, and Channel Functional
Test in accordance with the NUREG–
1433, Revision 3, ‘‘Standard Technical
Specifications, General Electric Plants—
BWR [boiling water reactor]/4.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Will operation of the facility in
accordance with the proposed amendment
involve a significant increase in the
probability or consequences of an accident
previously evaluated?
Response: No.
The definitions of Channel Check, Channel
Calibration[,] and Channel Functional Test
specified in Technical Specifications (TS)
provide basic information regarding what the
test involves, the components involved in the
test, and general information regarding how
the test is to be performed. Instrument
channel checking, calibrating, and testing are
not initiators of any accident previously
evaluated. Furthermore, the proposed
changes will not affect the ability of the
channel being checked, calibrated[,] or tested
to respond as assumed in any accident
previously evaluated. Therefore, these
revised definitions result in no increase in
the probability of an accident previously
evaluated.
The proposed revisions of these
definitions, corresponding administrative
changes (capitalization of definitions), and
the proposed alternate testing and calibrating
methodology using sequential, overlapping
testing, and/or actual channel input signals
and/or in place qualitative assessments of
resistance temperature detectors (RTD’s) and
thermocouples (TC’s) involve no changes to
plant design, equipment, or operation related
to mitigation of accidents. The qualitative
evaluation of sensor behavior for nonadjustable sensors will provide an accurate
indication of sensor operation and will
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assure that [the evaluated] portion of the
channel is operating properly, ensuring that
the consequences of an accident will remain
as previously evaluated. Therefore, these
revised definitions result in no increase in
the consequences of an accident previously
identified.
Based on the above, AmerGen concludes
that the proposed changes do not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Will operation of the facility in
accordance of the proposed amendment
create the possibility of a new or different
kind of accident from any accident
previously evaluated?
Response: No.
The proposed revisions of the instrument
surveillance definitions, corresponding
administrative changes (capitalization of
definitions), and the proposed alternate
testing and calibrating methodology using
sequential, overlapping testing, and/or actual
channel input signals and/or in place
qualitative assessments of RTD’s and TC’s do
not involve a physical alteration of the plant
or a change in the methods governing normal
plant operation. No new or different type[s]
of equipment will be installed. The proposed
changes also do not adversely affect the
operation or operability of existing plant
equipment. The proposed revisions will
allow a change in testing and calibrating
methodology. Allowing an alternate testing
and calibrating methodology will not change
how the plant is operated. Each instrument
channel will be tested one sub channel at a
time, as is currently performed, and will not
create the possibility of a new or different
kind of accident.
Based on the above discussion, AmerGen
concludes that the proposed changes do not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Will operation of the facility in
accordance with the proposed amendment
involve a significant reduction in a margin of
safety?
Response: No.
The affected definitions involve checking,
calibrating[,] and testing of instrumentation
used in the mitigation of accidents to ensure
that the instrumentation will perform as
assumed in safety analyses. The proposed
revisions of these definitions, corresponding
administrative changes (capitalization of
definitions), and the proposed alternate
testing and calibrating methodology using
sequential, overlapping testing, and/or actual
channel input signals and/or in place
qualitative assessments of RTD’s and TC’s
does not alter the ability of the instrument
channel to respond as designed or assumed
in the safety analyses. As a result[,] the
ability of the plant to respond to[,] and
mitigate[,] accidents is unchanged by the
revised definitions. Therefore, this change
does not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
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satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Thomas S.
O’Neill, Associate General Counsel,
Exelon Generation Company, LCC, 4300
Winfield Road, Warrenville, IL 60555.
NRC Branch Chief: Harold K.
Chernoff.
Exelon Generation Company, LLC,
Docket Nos. STN 50–454 and STN 50–
455, Byron Station, Unit Nos. 1 and 2,
Ogle County, Illinois
Date of amendment request: June 16,
2006, as supplemented by letter dated
September 14, 2006.
Description of amendment request:
The proposed amendment would revise
the Byron Station Updated Final Safety
Analysis Report (UFSAR) to incorporate
changes concerning the requirements for
physical protection from tornadogenerated missiles (TGM) for safetyrelated and non-safety related systems
and components.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The probability of occurrence of the design
basis tornado remains the same as originally
established in the Byron Station Updated
Final Safety Analysis Report (UFSAR). The
request involves the use of a probabilitybased assessment of the need for physical
tornado missile protection of specific existing
features at Byron Station.
The request is to utilize an NRC approved
methodology (i.e., the Electric Power
Research Institute (EPRI) Topical Report
‘‘Tornado Missile Risk Evaluation
Methodology’’) to conclude that the
acceptance criteria of NUREG–0800,
‘‘Standard Review Plan,’’ (SRP) Section 2.2.3,
‘‘Evaluation of Potential Accidents,’’
Revision 2, July 1981, has been met for Byron
Station and that tornado missile damage of
selected components at Byron Station need
not be considered as a credible event.
Per Item 2 in Section III of SRP 3.5.1.4,
probability methods can be used to accept
tornado missile effects provided damage to
all important structures, systems and
components, as discussed in Regulatory
Guide 1.117 are considered. Per Section II of
the SRP, the acceptance criterion of SRP 2.2.3
is applicable. Section II of SRP 2.2.3 states
that the expected rate of occurrence of
potential exposure in excess of 10 CFR Part
100, ‘‘Reactor Site Criteria,’’ guidelines of
approximately 1.0E–06 per reactor year is
acceptable, if when combined with
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67393
reasonable qualitative arguments, that the
realistic probability can be shown to be
smaller.
[The licensee in its September 14, 2006,
letter stated the following in regards to the
consequences of an accident previously
evaluated:
The acceptance criteria for the TORMIS
analysis has been established as 1.0 E–06 per
year cumulative probability of a TGM
striking/damaging an unprotected essential
SSC [system, structure or component]
required for safe shutdown in the event of a
tornado, which is the same value found to be
acceptable by the NRC based on the accepted
rates of occurrence of potential exposures in
excess of 10 CFR 100 guidelines. This criteria
in combination with conservative qualitative
assumptions show that the realistic
probability of a potential exposure in excess
of the 10 CFR Part 100 guidelines is lower
than 1.0 E–06 per year. The conservative
qualitative assumptions are the same as
previously found to be acceptable by the NRC
as described below:
It is assumed that an essential SSC being
struck/damaged by a tornado missile will
result in damage sufficient to preclude it
from performing its safety function.
It is assumed that the damage to the
essential SSC results in damage to fuel
sufficient to result in conservatively
calculated radiological release values in
excess of 10 CFR 100 guidelines.
There are no missiles that can directly
impact irradiated fuel, even the spent fuel
stored in the Spent Fuel Pool.]
The proposed change is not considered to
constitute a significant increase in the
probability or occurrence or the
consequences of an accident due to the
extremely low probability of damage due to
tornado-generated missiles and therefore an
extremely low probability of a radiological
release. Therefore, the proposed changes do
not involve a significant increase in the
probability or consequences of previously
evaluated accidents.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
This change involves the use of an
alternative methodology to assess the need
for tornado missile protection on selected
Byron Station components. The use of this
methodology and the changes to the Byron
Station UFSAR will be limited to design
basis tornado applications and do not
contribute to the possibility of a new or
different kind of accident from those
previously analyzed.
No new or different system interactions are
created and no new processes are introduced.
The proposed change does not introduce any
new failure mechanisms, malfunctions, or
accident initiators not already considered in
the design and licensing bases. Based on this
evaluation, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
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The changes, allowing for no additional
physical protection for tornado-generated
missiles for certain Byron Sation
components, is based on successfully
meeting the acceptance criteria of NUREG–
0800, ‘‘Standard Review Plan,’’ (SRP) Section
2.2.3, ‘‘Evaluation of Potential Accidents,’’
Revision 2, July 1981. Because of the
extremely low probability of damage to these
components from tornado-generated missiles,
the change is not considered to constitute a
significant decrease in the margin of safety.
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The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Bradley J.
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–440,
Perry Nuclear Power Plant, Unit 1, Lake
County, Ohio
Date of amendment request: October
13, 2006.
Description of amendment request:
The proposed amendment would
eliminate License Condition 2.F, which
requires reporting violations of
Operating License Section 2.C, and
eliminates Technical Specification
5.6.6, which contains a reporting
condition similar to Operating License
Section 2.C.(6).
The availability of this operating
license improvement was announced in
the Federal Register on November 4,
2005 (70 FR 67202), as part of the
consolidated line item improvement
process (CLIIP). The NRC staff issued a
notice of opportunity for comment in
the Federal Register on August 29, 2005
(70 FR 51098), on possible amendments
concerning this CLIIP, including a
model safety evaluation and a model no
significant hazards consideration
(NSHC) determination. The NRC staff
subsequently issued a notice of
availability of the models for referencing
in license amendment applications in
the Federal Register on November 4,
2005 (70 FR 67202). In its application
dated October 13, 2006, the licensee
affirmed the applicability of the
following determination.
Basis for proposed no significant
hazards consideration determination: As
required by 10 CFR 50.91(a), an analysis
of the issue of no significant hazards
consideration is presented below:
1. Does the change involve a significant
increase in the probability or consequences
of an accident previously evaluated?
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Response: No.
The proposed change involves the deletion
of a reporting requirement. The change does
not affect plant equipment or operating
practices and therefore does not significantly
increase the probability or consequences of
an accident previously evaluated.
2. Does the change create the possibility of
a new or different kind of accident from any
accident previously evaluated?
Response: No.
The proposed change is administrative in
that it deletes a reporting requirement. The
change does not add new plant equipment,
change existing plant equipment, or affect the
operating practices of the facility. Therefore,
the change does not create the possibility of
a new or different kind of accident from any
accident previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change deletes a reporting
requirement. The change does not affect
plant equipment or operating practices and
therefore does not involve a significant
reduction in a margin of safety.
The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorney for licensee: David W.
Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street,
Akron, OH 44308.
NRC Branch Chief: Daniel S. Collins.
Florida Power Corporation, et al.,
Docket No. 50–302, Crystal River Unit 3
Nuclear Generating Plant, Citrus
County, Florida
Date of amendment request: October
5, 2006.
Description of amendment request:
The proposed amendment to the
Improved Technical Specification will
revise the defined pool burnupenrichment requirements, storage
configuration for fresh fuel and low
burnup/high enriched fuel, the
definition of a peripheral assembly, and
will include minor editorial changes.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
(1) Involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The LAR proposes to revise the fresh fuel
loading configuration. PEF [Progress Energy
Florida, Inc.] has reanalyzed the criticality of
the revised storage configuration for fresh
fuel checkerboarded with spent fuel in Pool
A, and surrounded by empty water cells in
Pool B. Similarly, storage of spent fuel in
peripheral storage locations, given the new
definition, was also reanalyzed. The revised
fuel storage configuration does not affect any
structure, system, component or process
related to the operation of Crystal River Unit
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3 (CR–3). As a result, the proposed LAR will
not change the probability or consequences
of any accidents previously evaluated that
are related to operation of the plant. Thus,
only those accidents that are related to
movement and storage of fuel assemblies
could be potentially affected by the proposed
LAR.
Fuel Handling Accidents (FHAs) are
analyzed in Section 14.2.2.3 of the CR–3
Final Safety Analysis Report (FSAR). These
include a FHA inside the Reactor Building
(RB) and outside the RB. This LAR involves
storage of fuel assemblies, an activity
conducted outside the RB only. Therefore,
only the FHA outside the RB event needs to
be considered.
The FHA outside the RB event is described
as the dropping of a fuel assembly into the
spent fuel storage pool that results in damage
to a fuel assembly and the release of the
gaseous fission products. The current FHA
assumes all 208 fuel pins in the dropped
assembly are damaged and the gas gap
activity released. The results of that analysis
demonstrate that the applicable dose
acceptance criteria, 10 CFR 50.67 and
Regulatory Guide 1.183, ‘‘Alternative
Radiological Source Terms for Evaluating
Design Basis Accidents at Nuclear Power
Reactors,’’ are satisfied. Thus, the
consequences of a FHA are not increased by
the allowed change in the fresh fuel
configuration. The fresh fuel storage
configurations permit more effective use of
already existing storage locations. They do
not change the frequency or method for
handling fuel assemblies. Fuel handling
equipment is unaffected. As such, the
probability of a FHA has not increased. Since
only one fuel assembly is handled at a time,
the consequences of a FHA have not
increased.
The current limiting heat load for the spent
fuel pool is from the combined impact of
stored spent fuel and a full core off-load.
These changes do not increase spent fuel
storage capacity over that for which the racks
are currently analyzed and it does not
increase the amount of heat ejected from an
off-loaded core. Consequently, current
analyses for spent fuel pool cooling remain
valid. The configuration change allows fresh
fuel to be checkerboarded with spent fuel.
Since these changes do not increase the
storage capacity over that already analyzed
for the racks, filling the empty water cells in
the checkerboard pattern with spent fuel will
not increase the heat load over that already
analyzed. The Pool B allowance to surround
a higher enriched/lower burnup fuel
assembly in Pool B with empty water cells
or changing the definition of a periphery rack
cell does not increase the number of spent
fuel assembly rack locations over that
previously analyzed. Therefore, there is no
increase in the pool heat load over that
already analyzed.
A change in storage configurations in
storage Pools A and B does not increase the
probability of a full core off-load or the
frequency of establishing maximum heat load
conditions.
The FSAR specifies the normal upper limit
of the fuel pool cooling system as 160 °F.
Administrative controls are implemented to
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control when fuel may be moved from the
reactor to the fuel pool to prevent reaching
this limit.
Because neither the probability nor the
consequences of a FHA are increased, and
because there is not additional heat input to
the spent fuel pools, it is concluded that the
LAR does not involve a significant increase
in the probability or consequences of an
accident previously evaluated.
(2) Create the possibility of a new or
different kind of accident from any accident
previously evaluated?
Onsite storage of spent fuel assemblies in
the spent fuel pools is a normal activity for
which CR–3 has been designed and licensed.
As part of assuring that this normal activity
can be performed without endangering
public health and safety, the ability of CR–
3 to safely accommodate different possible
accidents in the spent fuel pools, such as
dropping a fuel assembly or the misloading
of a fuel assembly, have been analyzed. The
revised fuel storage configurations proposed
by the LAR does not change the methods of
fuel movement or fuel storage. No structural
or mechanical change to racks or fuel
handling equipment is being proposed. The
proposed revisions allow for more effective
use of existing, unmodified rack locations
when fresh or highly enriched, low burnup
fuel is stored in the pool. The proposed
revisions are a modification to the criticality
analysis only, and therefore the proposed
LAR does not create any new or different
kind of accident from those previously
evaluated.
(3) Involve a significant reduction in a
margin of safety?
The CR–3 Improved Technical
Specification (ITS) ensures the effective
neutron multiplication factor, Keff, of the
spent fuel storage racks is maintained less
than or equal to 0.95 when fully loaded and
flooded with unborated water. The revisions
proposed by the LAR likewise ensure Keff is
maintained less than this requirement.
Analyses for the proposed fuel storage
configurations have shown that sufficient
margin exists for fuel enriched to the
maximum allowed by the CR–3 license, and
for all fuel that is or has been in use at CR–
3. Maintaining this margin is assured by
remaining within the limits on initial
enrichment and fuel burnup that are
specified in the CR–3 ITS and, in the case of
highly enriched, low burnup fuel in Pool B,
by water hole spacing. The LAR proposes
allowing fresh fuel to be checkerboarded
with Category B type fuel in Pool A rather
than with empty water cells. It also allows
fresh fuel with high initial enrichment which
does not meet current burnup requirements
to be placed in Pool B if surrounded by eight
empty water cells. It also proposes to change
the definition of a periphery rack location for
storing Category BP type fuel. Analyses show
that the new proposed limits ensure that Keff
remains less than 0.95. Attachment E [not
included in this FR notice] provides an
analysis summary.
The current CR–3 licensing basis allows
the use of administrative controls, e.g.,
curves of initial fuel assembly enrichment
versus burnup, as a means of preventing
criticality in the spent fuel pools. The use of
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these curves would be continued under this
proposed amendment. The changes to these
curves proposed by this LAR consist of
revising the values of burnup and adding
notes to restrict loading of certain fuel
assemblies to specific configurations. These
types of curves and administrative controls
have been included in the CR–3 operating
license and their use implemented by site
procedures for many operating cycles. From
this previous use, CR–3 personnel are
familiar with the practice of using
administrative controls, such as curves of
fuel assembly enrichment versus burnup, to
prevent criticality events when placing fuel
assemblies in the spent fuel pool.
Misloaded and mislocated fuel assemblies
were analyzed. The analysis demonstrated
that misloading of a fresh fuel assembly,
assuming no soluble poison (boron) in the
water does result in exceeding the criticality
margin regulatory limit of Keff = 0.95. The
analysis further shows that a concentration of
165 ppm boron in the Pool A and a
concentration of 46 ppm boron in Pool B is
sufficient to ensure Keff < 0.95. LCO 3.7.14
currently requires a minimum boron
concentration of 1925 ppm in the spent fuel
pools until fuel is verified as having been
loaded in accordance with the enrichment
and burnup requirements of LCO 3.7.15. The
soluble boron assumed in the analysis for
this proposed change is substantially less
than the 1925 ppm required by the existing
license. Therefore, existing license
requirements for soluble boron remain
conservative.
The NRC staff has reviewed the
analysis provided for Florida Power
Corporation and, based on this review,
it appears that the three standards of 10
CFR 50.92(c) are satisfied. Therefore, the
NRC staff proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Branch Chief (Acting): L.
Raghavan.
FPL Energy Duane Arnold, LLC, Docket
No. 50–331, Duane Arnold Energy
Center (DAEC), Linn County, Iowa
Date of amendment request: July 17,
2006.
Description of amendment request:
The proposed amendment would revise
the Limiting Condition for Operation
(LCO) 3.6.3.1 to eliminate the
requirement for the Containment
Atmospheric Dilution (CAD) system,
allowing its removal from the DAEC.
LCO 3.6.3.2 would also be revised to
allow an additional 48 hours on plant
start-up or shutdown sequences for the
primary containment to be de-inerted.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
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67395
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The Containment Atmosphere Dilution
(CAD) system and primary containment
oxygen concentration are not initiators to any
accident previously evaluated in the DAEC
Updated Final Safety Analysis Report
(UFSAR). The CAD system and containment
oxygen concentration were previously relied
upon to mitigate the consequences of a
design basis accident (DBA) combustible gas
mixture. However, the revised 10 CFR 50.44
(68 FR 54123) no longer defines a DBA
hydrogen release (i.e., combustible gas
mixture) and the Commission has
subsequently found that the DBA loss of
coolant accident (LOCA) hydrogen release is
not risk significant. In addition, hydrogen
control systems, such as CAD, have been
determined to be ineffective at mitigating
hydrogen releases from the more risk
significant beyond design basis accidents that
could threaten containment integrity.
Therefore, elimination of the CAD system
will not significantly increase the
consequences of any accident previously
evaluated. The consequences of an accident
while relying on the revised Required
Actions for primary containment oxygen
concentration are no different than the
consequences of the same accidents under
the current Required Actions. As a result, the
consequences of any accident previously
evaluated are not significantly increased.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
No new or different accidents result from
utilizing the proposed change. The changes
do not involve a physical alteration of the
plant, except for the elimination of the CAD
system (i.e., no new or different type of
equipment will be installed) or a change in
the methods governing normal plant
operation. The CAD system is not considered
an accident precursor, nor does its existence
or elimination have any adverse impact on
the pre-accident state of the reactor core or
post accident confinement of radionuclides
within the containment building from any
DBA. In addition, the changes do not impose
any new or different requirements. The
changes to the Technical Specifications for
oxygen concentration do not alter
assumptions made in the safety analysis, but
reflect changes to the safety analysis
requirements allowed under the revised 10
CFR 50.44. Specifically that an inerted
containment is no[t] required to mitigate any
DBA, but has been found to be helpful in
mitigating certain beyond design basis events
(i.e., severe accidents) that could generate
combustible levels of hydrogen.
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Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The installation of combustible gas control
systems, such as CAD, required by the
original § 50.44(b)(3) was intended to address
the limited quantity and rate of hydrogen
generation that was postulated from a designbasis LOCA. The Commission has found that
this hydrogen release is not risk-significant
because the design-basis LOCA hydrogen
release does not contribute to the conditional
probability of a large release up to
approximately 24 hours after the onset of
core damage. In addition, these systems were
ineffective at mitigating hydrogen releases
from risk-significant accident sequences that
could threaten containment integrity. (68 FR
54123). The proposed changes to CAD and
primary containment oxygen concentration
reflect this new regulatory position and, in
light of the remaining plant equipment,
instrumentation, procedures, and programs
that provide effective mitigation of and
recovery from reactor accidents, including
postulated beyond design basis events, does
not result in a significant reduction in a
margin of safety.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. R. E.
Helfrich, Florida Power & Light
Company, P. O. Box 14000, Juno Beach,
FL 33408–0420.
NRC Branch Chief: L. Raghavan.
sroberts on PROD1PC70 with NOTICES
Indiana Michigan Power Company
(I&M), Docket No. 50–316, Donald C.
Cook Nuclear Plant, Unit 2, Berrien
County, Michigan
Date of amendment request:
September 15, 2006.
Description of amendment request:
The proposed amendment would
replace the current control system and
it will increase the nominal control
fluid oil operating pressure from 114
pounds per square inch gauge (psig) to
1600 psig. The control fluid oil pressure
provides an input to the reactor
protection system via three pressure
switches connected to the control fluid
header. Due to the change in the
operating pressure, I&M is proposing a
revision to the allowable low fluid oil
pressure value from greater than or
equal to 57 psig to greater than or equal
to 750 psig.
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Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change reflects a design
change to the turbine control system that
increases the control oil pressure,
necessitating a change to the value at which
a low fluid oil pressure initiates a reactor
trip. The turbine control oil pressure is an
input to the reactor trip instrumentation, and
the reactor trip is a response to an event that
trips the turbine. A change in the nominal
control oil pressure does not introduce any
mechanisms that would increase the
probability of an accident previously
analyzed. The reactor trip on turbine trip
function is an anticipatory trip, and the
safety analysis does not credit this trip for
protecting the reactor core. Thus, the
consequences of previously analyzed
accidents are not impacted.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The control fluid oil pressure decreases in
response to a turbine trip. The value at which
the low control fluid oil initiates a reactor
trip is not an accident initiator. The change
in the value reflects the higher pressure of
the turbine control system that will be
installed during the Unit 2 Cycle 17 refueling
outage.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The change involves a parameter that
initiates an anticipatory reactor trip following
a turbine trip. The safety analyses do not
credit this anticipatory trip for reactor core
protection.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The Nuclear Regulatory Commission
(NRC) staff has reviewed the licensee’s
analysis and, based on this review, it
appears that the three standards of 10
CFR 50.92(c) are satisfied. Therefore, the
NRC staff proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: James M. Petro,
Jr., Esquire, One Cook Place, Bridgman,
MI 49106.
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NRC Acting Branch Chief: Martin C.
Murphy.
Indiana Michigan Power Company,
Docket Nos. 50–315 and 50–316, Donald
C. Cook Nuclear Plant, Unit 1 and 2,
Berrien County, Michigan
Date of amendment request:
September 15, 2006.
Description of amendment request:
The proposed amendment would
modify the Technical Specifications
(TS) to change Required Action Notes in
TS 3.3.1, ‘‘Reactor Trip System
Instrumentation,’’ and TS 3.3.2,
‘‘Engineered Safety Features Actuation
System Instrumentation,’’ to reflect
installed bypass test capability, as well
as correct one administrative error in TS
3.3.1 Condition Q. The proposed
changes to the Required Action Notes
are consistent with wording in Standard
Technical Specifications (NUREG–1431,
Revision 3) for plants with installed
bypass test capability.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability of
occurrence or consequences of an accident
previously evaluated?
Response: No.
The proposed change reflects NUREG–
1431, Revision 3, ‘‘Standard Technical
Specifications, Westinghouse Plants,’’ (STS)
wording for plants with installed bypass test
capability and aligns Technical Specification
(TS) Condition entry requirements with other
portions of the TS. The proposed changes do
not modify how the reactor trip system (RTS)
and engineered safety features actuation
systems (ESFAS) functions respond to an
accident condition. The proposed changes to
the TS Required Action Notes prevent
unnecessary TS Action entry during
performance of surveillance testing. The
probability of accidents previously evaluated
remains unchanged since the proposed
change does not affect any accident initiators.
The consequences of accidents previously
evaluated are unaffected by this change
because no change to any accident mitigation
scenario has resulted and there are no
additional challenges to fission product
barrier integrity.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
No changes are being made to the plant
that would introduce any new accident
causal mechanisms. The proposed change to
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the Required Action Notes and Condition
entry requirements does not adversely affect
previously identified accident initiators and
does not create any new accident initiators.
The change does not affect how the RTS and
ESFAS functions operate. No new single
failure or accident scenarios are created by
the proposed change and the proposed
change does not result in any event
previously deemed incredible being made
credible.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
No safety analyses were changed or
modified as a result of the proposed TS
changes to reflect STS wording for plants
with installed bypass test capability or for
aligning TS Condition entry requirements.
All margins associated with the current
safety analyses acceptance criteria are
unaffected. The current safety analyses
remain bounding. The safety systems
credited in the safety analyses will continue
to be available to perform their mitigation
functions. The proposed change does not
affect the availability or operability of safetyrelated systems and components.
Therefore, the proposed change does not
involve a significant reduction in the margin
of safety.
sroberts on PROD1PC70 with NOTICES
The Nuclear Regulatory Commission
(NRC) staff has reviewed the licensee’s
analysis and, based on this review, it
appears that the three standards of 10
CFR 50.92(c) are satisfied. Therefore, the
NRC staff proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: James M. Petro,
Jr., Esquire, One Cook Place, Bridgman,
MI 49106
NRC Acting Branch Chief: M.
Murphy.
Nuclear Management Company, LLC,
Docket Nos. 50–282 and 50–306, Prairie
Island Nuclear Generating Plant, Units
1 and 2, Goodhue County, Minnesota
Date of amendment request: August
14, 2006.
Description of amendment request:
The proposed amendments would make
miscellaneous improvements to the
Technical Specifications (TS) for Prairie
Island Nuclear Generating Plant (PINGP)
Units 1 and 2. The proposed
amendments would revise TS 1.3,
‘‘Completion Times’’; TS 3.1.4, ‘‘Rod
Group Alignment Limits’’; TS 3.3.7,
‘‘Spent Fuel Pool Special Ventilation
System (SFPSVS) Actuation
Instrumentation’’; TS 3.7.10, ‘‘Control
Room Special Ventilation System
(CRSVS)’’; and TS Chapter 4.0, ‘‘Design
Features’’.
Basis for proposed no significant
hazards consideration determination:
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As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
This license amendment request proposes
changes to the Prairie Island Nuclear
Generating Plant Technical Specifications as
follows: Technical Specification 1.3,
‘‘Completion Times’’, revise a text header
and add a new text header; Technical
Specification 3.1.4, ‘‘Rod Group Alignment
Limits’’, remove a Surveillance Note which
cross-references another Technical
Specification and may cause confusion;
Technical Specification 3.3.7, ‘‘Spent Fuel
Pool Special Ventilation System (SFPSVS)
Actuation Instrumentation’’, revises the
Modes of Applicability consistent with plant
design and the Technical Specifications for
the Spent Fuel Pool Special Ventilation
System, the supported system; Technical
Specification 3.7.10, ‘‘Control Room Special
Ventilation System (CRSVS)’’, revises the
applicability of Condition C and clarifies the
requirements of the Surveillance to verify
train filtration flow; and Technical
Specification Chapter 4.0, ‘‘Design Features’’,
revises Reference 1 to the most recent version
of the document.
Revising and adding text headers in
Technical Specification 1.3 are
administrative changes because the revised
document does not change any basis for the
current Technical Specifications. Since these
are administrative changes, they do not
involve a significant increase in the
probability or consequences of a previously
evaluated accident. Technical Specification
3.1.4 assures that the control rod positions
are within the limits assumed in the safety
analysis and that the assumed shutdown
margin is available when needed. This
license amendment request proposes to
remove a Note from a surveillance
requirement that cross-references to
Technical Specification 3.1.7. Removal of
this Note does not change plant operations,
testing or maintenance; therefore the
proposed change does not involve a
significant increase in the probability of an
accident. Since plant operations, testing and
maintenance are not changed, the proposed
changes do not involve a significant increase
in the consequences of an accident
previously evaluated.
The Spent Fuel Pool Special Ventilation
System filters radioactive materials in the
fuel pool enclosure atmosphere released
following a fuel handling accident. This
license amendment request proposes to
revise the Modes and Other Specified
Conditions of Applicability for the actuation
instrumentation.
Technical Specification to be consistent
with the Modes and Other Specified
Conditions of Applicability in the Technical
Specification for the supported system. The
Spent Fuel Pool Special Ventilation System
and its actuation instrumentation are not
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67397
accident initiators; therefore, the proposed
changes do not affect the probability of an
accident. With the proposed change, the
Technical Specifications will continue to
require the system actuation instrumentation
to be operable when irradiated fuel is moved
in the fuel pool enclosure which is also the
required Applicability in the supported
system Technical Specification. Since the
instrumentation will be required to actuate
the supported system when it is required to
operate, the accident consequences will
continue to be mitigated with this proposed
Technical Specification change. Thus, the
proposed Technical Specification change
does not involve a significant increase in the
consequences of an accident previously
evaluated.
The Control Room Special Ventilation
System provides an enclosed control room
environment from which the plant can be
operated following an uncontrolled release of
radioactivity. This system is not an accident
initiator, thus the proposed changes do not
increase the probability of an accident. This
license amendment proposes changes which
will: (1) Reduce the time to shut down the
plant when Technical Specification required
actions or completion time is not met; and (2)
clarifies surveillance requirements to assure
that the system performs as designed. These
changes do not impact the performance of the
system; thus this change does not involve a
significant increase in the consequences of an
accident previously evaluated.
Updating the reference in Technical
Specification Chapter 4.0 is an administrative
change because the revised document does
not change any basis for the current
Technical Specifications. Since this is an
administrative change, it does not involve a
significant increase in the probability or
consequences of a previously evaluated
accident.
The changes proposed in this license
amendment do not involve a significant
increase the probability or consequences of
an accident previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
This license amendment request proposes
changes to the Prairie Island Nuclear
Generating Plant Technical Specifications as
follows: Technical Specification 1.3,
‘‘Completion Times’’, revise a text header
and add a new text header; Technical
Specification 3.1.4, ‘‘Rod Group Alignment
Limits’’, remove a Surveillance Note which
cross-references another Technical
Specification and may cause confusion;
Technical Specification 3.3.7, ‘‘Spent Fuel
Pool Special Ventilation System (SFPSVS)
Actuation Instrumentation’’, revises the
Modes of Applicability consistent with plant
design and the Technical Specifications for
the Spent Fuel Pool Special Ventilation
System, the supported system; Technical
Specification 3.7.10, ‘‘Control Room Special
Ventilation System (CRSVS)’’, revises the
applicability of Condition C and clarifies the
requirements of the Surveillance to verify
train filtration flow; and Technical
Specification Chapter 4.0, ‘‘Design Features’’,
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revises Reference 1 to the most recent version
of the document.
Revising and adding text headers in
Technical Specification 1.3 are
administrative changes because the revised
document does not change any basis for the
current Technical Specifications. Since these
are administrative changes, they do not
create the possibility of a new or different
kind of accident.
Removal of a surveillance note from
Technical Specification 3.1.4 that crossreferences another Technical Specification
does not change any plant operations,
maintenance activities or testing
requirements. The Limiting Conditions for
Operation will continue to be met and the
proper control rod positions will continue to
be maintained. There are no new failure
modes or mechanisms created through the
removal of the Surveillance Requirements
Note, nor are new accident precursors
generated by this change. This proposed
change does not create the possibility of a
new or different kind of accident from any
previously evaluated.
The proposed revision of Modes of
Applicability for the Spent Fuel Pool Special
Ventilation System actuation instrumentation
makes operation of the actuation
instrumentation consistent with the
Technical Specification requirements for the
supported system and does not change the
operation of the supported system for
accident mitigation. The Limiting Conditions
for Operation will continue to be met, no
new failure modes or mechanisms are created
and no new accident precursors are
generated by this change. This proposed
change does not create the possibility of a
new or different kind of accident from any
previously evaluated.
The changes proposed for the Control
Room Special Ventilation System Technical
Specifications do not change any the system
operations, maintenance activities or testing
requirements. The Limiting Conditions for
Operation will continue to be met, no new
failure modes or mechanisms are created and
no new accident precursors are generated by
this change. This proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
Updating the reference in Technical
Specification Chapter 4.0 is an administrative
change because the revised document does
not change any basis for the current
Technical Specifications. Since this is an
administrative change, it does not create the
possibility of a new or different kind of
accident.
The Technical Specification changes
proposed in this license amendment do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
This license amendment request proposes
changes to the Prairie Island Nuclear
Generating Plant Technical Specifications as
follows: Technical Specification 1.3,
‘‘Completion Times’’, revise a text header
and add a new text header; Technical
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Specification 3.1.4, ‘‘Rod Group Alignment
Limits’’, remove a Surveillance Note which
cross-references another Technical
Specification and may cause confusion;
Technical Specification 3.3.7, ‘‘Spent Fuel
Pool Special Ventilation System (SFPSVS)
Actuation Instrumentation’’, revises the
Modes of Applicability consistent with plant
design and the Technical Specifications for
the Spent Fuel Pool Special Ventilation
System, the supported system; Technical
Specification 3.7.10, ‘‘Control Room Special
Ventilation System (CRSVS)’’, revises the
applicability of Condition C and clarifies the
requirements of the Surveillance to verify
train filtration flow; and Technical
Specification Chapter 4.0, ‘‘Design Features’’,
revises Reference 1 to the most recent version
of the document.
Revising and adding text headers in
Technical Specification 1.3 are
administrative changes because the revised
document does not change any basis for the
current Technical Specifications. Since these
are administrative changes, they do not
involve a significant reduction in a margin of
safety.
Plant operations are required to meet all
Technical Specifications for which the
Applicability is met; therefore, removal of the
cross-reference Note from a Technical
Specification 3.1.4 surveillance requirement
does not change how the plant is operated
and therefore, this change does not involve
a significant reduction in a margin of safety.
Technical Specification 3.3.7 provides
requirements for actuation instrument which
supports the operation of the Spent Fuel Pool
Special Ventilation System as required by
Technical Specification 3.7.13. The current
Applicability for Technical Specification
3.3.7 requires the actuation instrumentation
to be operable in Modes which are not
required by Technical Specification 3.7.13.
This license amendment proposes to make
Technical Specification 3.3.7 Applicability
the same as Technical Specification 3.7.13.
This change does not reduce the conditions
or Modes when the Spent Fuel Pool Special
Ventilation System will operate and perform
its accident mitigation function; thus this
change does not involve a significant
reduction in a margin of safety.
This license amendment proposes changes
to the Control Room Special Ventilation
System Technical Specifications which will:
(1) Reduce the time to shut down the plant
when Technical Specification required
actions or completion time is not met; and (2)
clarifies surveillance requirements to assure
that the system performs as designed. The
proposed time to shut down the plant is
consistent with other Technical
Specifications for shutting down the plant
and allows adequate time for an orderly shut
down of the plant; thus this change does not
involve a significant reduction in a margin of
safety. The surveillance requirement
clarifications do not reduce any testing
requirements and will continue to
demonstrate that the system can perform its
required safety function and satisfy the
Limiting Conditions for Operation. Thus this
change does not involve a significant
reduction in a margin of safety.
Updating the reference in Technical
Specification Chapter 4.0 is an administrative
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change because the revised document does
not change any basis for the current
Technical Specifications. Since this is an
administrative change, it does not involve a
significant reduction in a margin of safety.
The Technical Specification changes
proposed in this license amendment do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92 (c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Jonathan Rogoff,
Esquire, Vice President, Counsel &
Secretary, Nuclear Management
Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Branch Chief: M. Murphy (A).
Tennessee Valley Authority, Docket
Nos. 50–260 and 50–296, Browns Ferry
Nuclear Plant (BFN), Units 2 and 3,
Limestone County, Alabama
Date of amendment request: October
26, 2006.
Description of amendment request:
The proposed request would revise the
Units 2 and 3 emergency diesel
generator (EDG) Technical Specification
(TS) Completion Time (CT) from 14
days to 7 days for restoration of an
inoperable EDG. The current 14-day CT
was based on the assumption that Unit
1 was shut down. The near-term restart
of Unit 1 will invalidate this
assumption, therefore, the affected CTs
are being returned to their original
duration of 7 days.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed Technical
Specification change involve a significant
increase in the probability or consequences
of an accident previously evaluated?
Response: No.
The EDGs are designed as backup
alternating current (AC) power sources in the
event of a loss of offsite power. The proposed
restoration of the EDG CT to its original TS
duration does not change the conditions,
operating configurations, or minimum
amount of operating equipment assumed in
the safety analysis for accident mitigation. No
changes are proposed in the manner in which
the EDGs provide plant protection or which
create new modes of plant operation.
Therefore, the proposed amendment does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed Technical
Specification change create the possibility of
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a new or different kind of accident from any
accident previously evaluated?
Response: No.
The proposed amendment does not
introduce new equipment which could create
a new or different kind of accident. Existing
equipment will not be operated in any new
modes or for purposes different than it is
now utilized. No new external threats,
release pathways, or equipment failure
modes are created. Therefore, the
implementation of the proposed amendment
will not create a possibility for an accident
of a new or different type than those
previously evaluated.
3. Does the proposed Technical
Specification change involve a significant
reduction in a margin of safety?
Response: No.
BFN’s emergency AC [alternating current]
system is designed with sufficient
redundancy such that an EDG may be
removed from service for maintenance or
testing. The remaining EDGs are capable of
carrying sufficient electrical loads to satisfy
the UFSAR [Updated Final Safety Analysis
Report] requirements for accident mitigation
or unit safe shutdown. The proposed change
does not impact the redundancy or
availability requirements of offsite power
supplies or change the ability of the plant to
cope with station blackout events.
sroberts on PROD1PC70 with NOTICES
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: L. Raghavan.
U.S. Department of Transportation
(USDOT), United States Maritime
Administration (MARAD), License No.
NS–1, Docket No. 50–238, Nuclear Ship
Savannah (NSS)
Date of amendment request: August 7,
2006.
Description of amendment request:
The proposed license amendment
would modify the Technical
Specification (TS) requirements to
prepare for decommissioning the NSS.
Five TS changes are proposed. Three of
the proposed changes are related to
allowing the NSS to be berthed at
locations other than the James River
Reserve Fleet (JRRF), Newport News,
Virginia. The fourth proposed change
eliminates the need to utilize
administrative controls to remove the
Containment Vessel (CV) Entry Shield
Plugs to perform activities such as
surveys, system walkdowns and
inspections required for developing a
detailed decommissioning plan,
schedule and cost estimate.
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The fifth proposed change clarifies
the TS and eliminates redundancies,
subtle differences and inefficiencies in
the current TS regarding preventing
unauthorized access into the Reactor
Compartment and Radiation Control
Areas. In addition, MARAD is
enhancing the numbering of the TSs to
remove ambiguities that exist in the
current numbering (e.g., TS 2.2 is found
on pages 3 and 11 of the current TSs).
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
(1) Does the change involve a significant
increase in the probability or consequences
of an accident previously evaluated?
Response: No.
Proposed changes (1) Ship’s Location, (2)
Review and Audit Committee Membership,
(3) Qualification to perform Surveys and
Surveillances, (4) CV Entry Shield Plugs and
(5) RC and RCA Entrances are administrative
in nature and do not involve the modification
of any plant equipment or affect basic plant
operation.
The NSS’s reactor is not operational and
the level of radioactivity in the NSS has
significantly decreased from the levels that
existed when the 1976 Possession-only
License was issued. No aspect of any of
proposed changes is an initiator of any
accident previously evaluated. Consequently,
the probability of an accident previously
evaluated is not significantly increased.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
(2) Does the change create the possibility
of a new or different kind of accident from
any accident evaluated?
Response: No.
Proposed changes (1) Ship’s Location, (2)
Review and Audit Committee Membership,
(3) Qualification to perform Surveys and
Surveillances, (4) CV Entry Shield Plugs and
(5) RC and RCA Entrances are administrative
and do not involve any physical alteration of
plant equipment that was not previously
allowed by Technical Specifications. These
proposed changes do not change the method
by which any safety-related system performs
its function. As such, no new or different
types of equipment will be installed, and the
basic operation of installed equipment is
unchanged. The methods governing plant
operation and testing remain consistent with
current safety analysis assumptions.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
(3) Does the change involve a significant
reduction in a margin of safety?
Response: No.
Proposed changes (1) Ship’s Location, (2)
Review and Audit Committee Membership,
(3) Qualification to perform Surveys and
Surveillances, (4) CV Entry Shield Plugs and
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67399
(5) RC and RCA Entrances are administrative
in nature. No margins of safety exist that are
relevant to the ship’s defueled and partially
dismantled reactor. As such, there are no
changes being made to safety analysis
assumptions, safety limits or safety system
settings that would adversely affect plant
safety as a result of the proposed changes.
The proposed changes involve movement of
the ship, changes in the performance of
responsibilities and significantly improved
radiological conditions since 1976.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based upon the
staff’s review of the licensee’s analysis,
as well as the staff’s own evaluation, the
staff concludes that the three standards
of 10 CFR 50.92(c) are satisfied.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Senior Technical Advisor, N.S.
Savannah: Erhard W. Koehler, MARAD,
Office of Ship Operations.
NRC Branch Chief: Claudia Craig.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
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sroberts on PROD1PC70 with NOTICES
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
Arizona Public Service Company, et al.,
Docket Nos. STN 50–528, STN 50–529,
and STN 50–530, Palo Verde Nuclear
Generating Station, Units Nos. 1, 2, and
3, Maricopa County, Arizona
Date of application for amendments:
September 29, 2005, as supplemented
by letter dated July 5, 2006.
Brief description of amendments:
These amendments modified the
Security Plan, Training and
Qualification Plan, Safeguards
Contingency Plan, and Independent
Spent Fuel Security Program.
Date of issuance: October 31, 2006.
Effective date: As of the date of
issuance to be implemented within 30
days from the date of issuance.
Amendment Nos.: Unit 1–162, Unit
2–162, Unit 3–162.
Facility Operating License Nos. NPF–
41, NPF–51, and NPF–74: The
amendments revised the Operating
Licenses for all three units.
Date of initial notice in Federal
Register: August 1, 2006 (71 FR 43530).
The July 5, 2006, letter contained the
no significant hazards consideration
determination for the September 29,
2005, letter that was published in the
August 1, 2006, notice. The July 5, 2006,
supplemental letter provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
no significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 31,
2006.
No significant hazards consideration
comments received: No.
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14:17 Nov 20, 2006
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Letter contained the no significant
hazards consideration determination for
the September 29, 2005, letter that was
published in the August 1, 2006, notice.
The July 5, 2006, supplemental letter
provided additional information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the staff’s
original no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 31,
2006.
No significant hazards consideration
comments received: No.
Dominion Nuclear Connecticut, Inc.,
Docket No. 50–336, Millstone Power
Station, Unit No. 2, New London
County, Connecticut
Amendment No.: 139.
Facility Operating License No. NPF–
58: This amendment revised the
Technical Specification Surveillance
Requirements and License.
Date of initial notice in Federal
Register: January 31, 2006 (71 FR
5081).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 27,
2006.
No significant hazards consideration
comments received: No.
Florida Power and Light Company,
Docket Nos. 50–250 and 50–251, Turkey
Point Plant, Units 3 and 4, Miami-Dade
County, Florida
Date of application for amendment:
January 4, 2006.
Brief description of amendment: The
proposed amendment changed the
Millstone Power Station, Unit No. 2
Technical Specification (TS) 3/4 3.3.8,
‘‘Instrumentation, Accident
Monitoring,’’ to modify the description
of the pressurizer power operated relief
valves and pressurizer safety valves
position indicators.
Date of issuance: November 7, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment No.: 294.
Facility Operating License No. DPR–
65: The amendment revised the TSs.
Date of initial notice in Federal
Register: February 28, 2006 (71 FR
10073).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated November 7,
2006.
No significant hazards consideration
comments received: No.
Date of application for amendments:
April 27, 2006, as supplemented
October 3, 2006.
Brief description of amendments: The
amendments revise, on a one-time basis,
Technical Specification 3/4.4.5, Steam
Generator (SG) Surveillance
Requirements, to exclude the region of
the SG tubes below 17 inches from the
top of the hot leg tube sheet from the
inspection requirements. The
amendments also permanently revise
the limit for primary-to-secondary
leakage in TS 3/4.4.6, Reactor Coolant
System Leakage.
Date of issuance: November 1, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 30 days of issuance.
Amendment Nos: 231 and 226.
Renewed Facility Operating License
Nos. DPR–31 and DPR–41: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: August 1, 2006 (71 FR 43532).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated November 1,
2006.
No significant hazards consideration
comments received: No.
FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–440,
Perry Nuclear Power Plant, Unit 1, Lake
County, Ohio
Indiana Michigan Power Company,
Docket Nos. 50–315 and 50–316, Donald
C. Cook Nuclear Plant, Units 1 and 2,
Berrien County, Michigan
Date of application for amendment:
November 15, 2005.
Brief description of amendment: The
amendment modified the technical
specifications to clarify the wording of
the emergency closed cooling water
(ECCW) Surveillance Requirement
3.7.10.2 that verified actuation of the
entire ECCW system rather than just
verifying ‘‘valve’’ actuation.
Date of issuance: October 27, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 90 days.
Date of application for amendments:
March 7, 2006, as supplemented by
letter dated August 3, 2006.
Brief description of amendments: The
amendment revised Section 3.3.1,
‘‘Reactor Trip System (RTS)
Instrumentation,’’ of the DCCNP–1 and
DCCNP–2 Technical Specifications,
changing the reactor trip on turbine trip
interlock from the P–7 setpoint (10
percent rated thermal power) to the P–
8 setpoint (31 percent rated thermal
power).
Date of issuance: October 30, 2006.
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Effective date: As of the date of
issuance and shall be implemented
prior to entry into Mode 1 from the
Cycle 21 refueling outage for DCCNP–1,
and prior to entry into Mode 1 from the
Cycle 17 refueling outage for DCCNP–2.
Amendment Nos.: 297 and 298.
Facility Operating License Nos. DPR–
58 and DPR–74: Amendments revise the
Technical Specifications.
Date of initial notice in Federal
Register: April 25, 2006 (71 FR 23956).
The supplemental letter contained
clarifying information and did not
change the initial no significant hazards
consideration determination, and did
not expand the scope of the original
Federal Register notice.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 30,
2006.
No significant hazards consideration
comments received: No.
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
sroberts on PROD1PC70 with NOTICES
Date of amendment request: March
15, 2006.
Brief description of amendment: The
amendment revised the Cooper Nuclear
Station Technical Specification 5.5.12,
‘‘Primary Containment Leakage Rate
Testing Program,’’ by adding two subparagraphs to note exemptions from
Section III.A and Section llI.B of 10 CFR
Part 50, Appendix J, Option B. These
two sub-paragraphs allow the leakage
contribution from the four main steam
line penetrations, referred to as the
Main Steam Isolation Valve leakage, to
be excluded.
Date of issuance: October 31, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 30 days of issuance.
Amendment No.: 226.
Facility Operating License No. DPR–
46: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: April 25, 2006 (71 FR 23958).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 31,
2006.
No significant hazards consideration
comments received: No.
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1 (FCS), Washington County,
Nebraska
Date of amendment request: October
31, 2005, as supplemented on July 25,
2006.
Brief description of amendment: The
amendment revised the FCS Updated
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14:17 Nov 20, 2006
Jkt 211001
Safety Analysis Report Sections related
to the radiological consequences of
events affected by the planned 2006
replacement of the steam generators and
pressurizer.
Date of issuance: October 27, 2006.
Effective date: As of its date of
issuance and shall be implemented
within 90 days of its issuance.
Amendment No.: 243.
Renewed Facility Operating License
No. DPR–40: The amendment revised
the Updated Safety Analysis Report.
Date of initial notice in Federal
Register: December 20, 2005 (70 FR
75493).
The July 25, 2006, supplemental letter
provided information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
safety evaluation dated October 27,
2006.
No significant hazards consideration
comments received: No.
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1, Washington County, Nebraska
Date of amendment request:
December 19, 2005, as supplemented on
May 30, 2006.
Brief description of amendment: The
amendment modified Fort Calhoun
Station, Unit No. 1’s Technical
Specification 2.4, ‘‘Containment
Cooling,’’ (and the associated Bases) to
reduce the required number of operable
containment spray (CS) pumps from
three to two in order to enhance net
positive suction head margins. The
proposed change was implemented by
disabling the CS actuation signal
automatic start feature of one of the two
CS pumps that share the same diesel
generator and a common suction line.
Date of issuance: October 27, 2006.
Effective date: The license
amendment is effective as of its date of
issuance.
Amendment No.: 244.
Renewed Facility Operating License
No. DPR–40: The amendment revised
the Technical Specifications.
Date of initial notice in Federal
Register: February 28, 2006 (71 FR
10075).
The May 30, 2006, supplemental
letter provided information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the staff’s
original proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
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67401
safety evaluation dated October 27,
2006.
No significant hazards consideration
comments received: No.
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1, Washington County, Nebraska
Date of amendment request:
September 30, 2005, as supplemented
by letters dated May 23 and August 16,
2006.
Brief description of amendment:
Omaha Public Power District proposed
to change the licensing basis by
replacing EMF–2087(P)(A), Revision 0,
‘‘SEM/PWR–98: ECCS [Emergency Core
Cooling System] Evaluation Model for
PWR [Pressurized-Water Reactor]
LBLOCA [Large Break Loss-of-Coolant
Accident] Applications,’’ Siemens
Power Corporation, June 1999, with the
AREVA NP, Inc. Topical Report EMF–
2103(P)(A), ‘‘Realistic Large Break
LOCA Methodology,’’ Framatome ANP,
Inc., in the Fort Calhoun Station, Unit
1 (FCS), Core Operating Limit Report
(COLR). This change is necessary since
the EMF–2087(P)(A) methodology is not
approved for analyzing M5 clad fuel,
which will be used in the FCS reactor
core starting in Cycle 24. As part of this
approval, the NRC staff reviewed the
AREVA NP, Inc. FCS-specific LBLOCA
analysis using EMF–2103(P)(A). EMF–
2103(P)(A) will be used for Cycle 24 and
beyond.
Date of issuance: November 3, 2006.
Effective date: Effective as of its date
of issuance and shall be implemented
within 90 days of issuance.
Amendment No.: 245.
Renewed Facility Operating License
No. DPR–40: The amendment revised
the COLR.
Date of initial notice in Federal
Register: January 3, 2006 (71 FR 152).
The May 23 and August 16, 2006,
supplemental letters provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
safety evaluation dated November 3,
2006.
No significant hazards consideration
comments received: No.
Omaha Public Power District (OPPD),
Docket No. 50–285, Fort Calhoun
Station, Unit No. 1, Washington County,
Nebraska
Date of amendment request: May 30,
2006, as supplemented by two letters
dated on August 30, 2006.
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Brief description of amendment: The
amendment revised the Fort Calhoun
Station, Unit No. 1 (FCS) Technical
Specification (TS) requirements related
to steam generator tube integrity. The
change is consistent with NRC-approved
Revision 4 to Technical Specification
Task Force (TSTF) Standard Technical
Specification Change Traveler TSTF–
449, ‘‘Steam Generator Tube Integrity.’’
The availability of this TS improvement
was announced in the Federal Register
on May 6, 2005 (70 FR 24126) as part
of the consolidated line item
improvement process (CLIIP).
OPPD also changed the FCS TS by
deleting the sleeving repair alternative
to plugging for steam generator tubes.
The FCS replacement steam generators
(RSGs) to be installed during the fall of
2006 are manufactured by Mitsubishi
Heavy Industries, Ltd. (MHI). OPPD has
stated that the sleeving repair
alternative to plugging will not be used
for the MHI RSGs.
Date of issuance: November 7, 2006.
Effective date: As of its date of
issuance and shall be implemented
within 120 days of issuance.
Amendment No.: 246.
Renewed Facility Operating License
No. DPR–40: The amendment revised
the Technical Specifications.
Date of initial notice in Federal
Register: July 18, 2006 (71 FR 40750).
The two August 30, 2006,
supplemental letters provided
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination. The
Commission’s related evaluation of the
amendment is contained in a safety
evaluation dated November 7, 2006.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket No. 50–354,
Hope Creek Generating Station, Salem
County, New Jersey
Date of application for amendment:
October 7, 2005, as supplemented by
letter dated September 8, 2006.
Brief description of amendment: The
proposed amendment revised the
Technical Specifications (TSs) to clarify
certain requirements during fuel
movement, core alterations, and
operations with the potential for
draining the reactor vessel. The
amendment better aligns the TSs with
the NRC-approved Revision 2 to
Technical Specification Task Force
(TSTF) Traveler TSTF–51, ‘‘Revise
Containment Requirements During
Handling Irradiated Fuel and Core
Alterations,’’ and NUREG–1433,
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14:17 Nov 20, 2006
Jkt 211001
‘‘Standard Technical Specifications
General Electric Plants, BWR [boiling
water reactor]/4.’’
Date of issuance: October 31, 2006.
Effective date: As of the date of
issuance, to be implemented within 60
days.
Amendment No.: 170.
Facility Operating License No. NPF–
57: This amendment revised the TSs.
Date of initial notice in Federal
Register: May 9, 2006 (71 FR 27002).
The licensee’s September 8, 2006,
supplement provided clarifying
information that did not change the
scope of the proposed amendment as
described in the original notice of
proposed action published in the
Federal Register, and did not change
the initial proposed no significant
hazards consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 31,
2006.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket Nos. 50–272
and 50–311, Salem Nuclear Generating
Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of application for amendments:
April 25, 2006.
Brief description of amendments: The
amendments revised the Technical
Specifications to adopt the provisions in
Technical Specification Task Force
(TSTF) Traveler TSTF–359, ‘‘Increased
Flexibility in Mode Restraints,’’
Revision 9. The availability of TSTF–
359 for adoption by licensees was
announced in the Federal Register on
April 4, 2003 (68 FR 16579).
Date of issuance: October 27, 2006.
Effective date: As of the date of
issuance, to be implemented within 60
days.
Amendment Nos.: 276, 258.
Facility Operating License Nos. DPR–
70 and DPR–75: The amendments
revised the Technical Specifications and
License.
Date of initial notice in Federal
Register: July 5, 2006 (71 FR 38185).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 27,
2006.
No significant hazards consideration
comments received: No.
South Carolina Electric & Gas Company,
South Carolina Public Service
Authority, Docket No. 50–395, Virgil C.
Summer Nuclear Station, Unit No. 1,
Fairfield County, South Carolina
Date of application for amendment:
October 28, 2005, as supplemented on
April 2, June 15, and August 31, 2006.
PO 00000
Frm 00077
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Sfmt 4703
Brief description of amendment: The
amendment revises the Virgil C.
Summer Nuclear Station Technical
Specifications and provides associated
Bases to permit the implementation of
an alternate alternating current power
supply.
Date of issuance: November 2, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 30 days.
Amendment No. 178.
Renewed Facility Operating License
No. NPF–12: Amendment revises the
Technical Specifications.
Date of initial notice in Federal
Register: March 14, 2006 (71 FR
13176).
The supplemental letter provided
clarifying information that was within
the scope of the initial notice and did
not change the initial proposed no
significant hazards consideration.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated November 2,
2006.
No significant hazards consideration
comments received: No.
Wolf Creek Nuclear Operating
Corporation, Docket No. 50–482, Wolf
Creek Generating Station, Coffey
County, Kansas
Date of amendment request: October
27, 2005.
Brief description of amendment: The
amendment revised Technical
Specifications (TSs) 1.1, ‘‘Definitions,’’
and 3.4.16, ‘‘RCS [reactor coolant
system] Specific Activity,’’ to replace
the current Limiting Condition for
Operation (LCO) 3.4.16 limits on RCS
specific activity with limits on RCS
Dose Equivalent I–131 (DEI) and Dose
Equivalent Xe-133 (DEX). In TS 1.1, the
´
definition of (1) E—Average
Disintegration Energy is replaced by the
definition of DEX and (2) DEI is revised
to allow the use of alternate thyroid
dose conversion factors. The modes of
applicability, conditions and required
actions, and surveillance requirements
for TS 3.4.16 are revised.
Date of issuance: October 31, 2006.
Effective date: As of its date of
issuance and shall be implemented
within 90 days of the date of issuance.
Amendment No.: 170.
Facility Operating License No. NPF–
42. The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: January 3, 2006 (71 FR 156).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 31,
2006.
No significant hazards consideration
comments received: No.
E:\FR\FM\21NON1.SGM
21NON1
Federal Register / Vol. 71, No. 224 / Tuesday, November 21, 2006 / Notices
Wolf Creek Nuclear Operating
Corporation, Docket No. 50–482, Wolf
Creek Generating Station, Coffey
County, Kansas
Date of amendment request: August
25, 2006, as supplemented by letter
dated October 25, 2006.
Brief description of amendment: The
amendment revised Technical
Specification (TS) 3.7.2, ‘‘Main Steam
Isolation Valves (MSIVs),’’ and TS 3.7.3,
‘‘Main Feedwater Isolation Valves
(MFIVs),’’ to add the associated actuator
trains to (1) the limiting condition for
operation (LCO), (2) the conditions,
required actions, and completion times
for the LCO, and (3) the surveillance
requirements. The Table of Contents for
the TSs is changed to account for the
resulting renumbering of TS pages.
Date of issuance: November 7, 2006.
Effective date: As of its date of
issuance and shall be implemented
within 30 days of the date of issuance.
Amendment No.: 171.
Facility Operating License No. NPF–
42. The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: September 1, 2006 (71 FR
52173).
The supplemental letter dated
October 25, 2006, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the NRC staff’s
original proposed no significant hazards
consideration determination published
in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated November 7,
2006.
No significant hazards consideration
comments received: No.
Dated at Rockville, Maryland, this 9th day
of November, 2006.
For The Nuclear Regulatory Commission.
Catherine Haney,
Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. E6–19434 Filed 11–20–06; 8:45 am]
BILLING CODE 7590–01–P
NUCLEAR REGULATORY
COMMISSION
[NUREG–1852]
Extension of comment period
for NUREG–1852, ‘‘Demonstrating the
Feasibility and Reliability of Operator
Manual Actions in Response to Fire,
Draft Report for Comment.’’
ACTION:
SUMMARY: On October 12, 2006 (71 FR
60200), the Nuclear Regulatory
Commission (NRC) issued for public
comment NUREG 1852, ‘‘Demonstrating
the Feasibility and Reliability of
Operator Manual Actions in Response to
Fire, Draft Report for Comment.’’ Due to
an error in the previous notice of
comment period extension, a request
has been made to extend the public
comment period to allow the public 60
days to review the document. Currently,
the Federal Register specifies that the
public comment period ends on
December 12, 2006.
The comment period has been
extended and now expires on January
30, 2007. Comments received after this
date will be considered if it is practical
to do so, but the Commission is able to
ensure consideration only for comments
received before this date.
DATES:
Members of the public are
invited and encouraged to submit
written comments to Michael Lesar,
Chief, Rules and Directives Branch,
Office of Administration, Mail Stop T6–
D59, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001. Hand-deliver comments attention
to Michael Lesar, 11545 Rockville Pike,
Rockville, MD, between 7:30 a.m. and
4:15 p.m. on Federal workdays.
Comments may also be sent
electronically to NRCREP@nrc.gov.
This document, NUREG–1852, is
available at the Agencywide Documents
Access and Management System
(ADAMS) Public Electronic Reading
Room on the Internet at the NRC Web
site at https://www.nrc.gov/reading-rm/
adams.html under Accession No.
ML062350292; on the NRC Web site at
https://www.nrc.gov/reading-rm/doccollections/nuregs/docs4comment.html;
and at the NRC Public Document Room,
11555 Rockville Pike, Rockville, MD.
The PDR’s mailing address is USNRC
PDR, Washington, DC 20555; telephone
(301) 415–4737 or (800) 397–4205; fax
(301) 415–3548; e-mail PDR@NRC.GOV.
ADDRESSES:
sroberts on PROD1PC70 with NOTICES
FOR FURTHER INFORMATION CONTACT:
Demonstrating the Feasibility and
Reliability of Operator Manual Actions
in Response to Fire, Draft Report for
Comment
Erasmia Lois, Human Factors and
Reliability Branch, Office of Nuclear
Regulatory Research, telephone: (301)
415–6560; e-mail: exl1@nrc.gov.
Nuclear Regulatory
Commission.
Dated at Rockville, Maryland, this 15th day
of November, 2006.
AGENCY:
VerDate Aug<31>2005
14:17 Nov 20, 2006
Jkt 211001
PO 00000
Frm 00078
Fmt 4703
Sfmt 4703
67403
For the Nuclear Regulatory Commission.
Jose Ibarra,
Chief, Human Factors and Reliability Branch,
Probabilistic Risk and Applications, Division
of Risk Assessment and Special Projects,
Office of Nuclear Regulatory Research.
[FR Doc. E6–19626 Filed 11–20–06; 8:45 am]
BILLING CODE 7590–01–P
OFFICE OF PERSONNEL
MANAGEMENT
General Schedule Locality Pay Areas
Office of Personnel
Management.
ACTION: Notice.
AGENCY:
SUMMARY: On behalf of the President’s
Pay Agent, the Office of Personnel
Management (OPM) is providing notice
about two changes in locality pay area
boundaries in 2007 under the locality
pay program for General Schedule and
certain other employees. Grayson
County, TX, will be added to the Dallas
locality pay area, and Berks County, PA,
will be added to the Philadelphia
locality pay area. These changes will
occur automatically under existing
regulations. OPM also plans to issue a
notice later about changes in the
regulations needed to update the official
descriptions of the Boston-WorcesterManchester, MA-NH-ME-RI locality pay
area and the Denver-Aurora-Boulder,
CO locality pay area. As required by
OPM regulations, the additions to
locality pay areas are effective as of the
first pay period beginning on or after
January 1, 2007. Both the additions and
the planned description changes are the
result of changes made by the Office of
Management and Budget in
Metropolitan Statistical Areas and
Combined Statistical Areas.
DATES: The additions to locality pay
areas are applicable on the first day of
the first pay period beginning on or after
January 1, 2007.
FOR FURTHER INFORMATION CONTACT:
Allan Hearne, (202) 606–2838; FAX:
(202) 606–4264; e-mail: payperformance-policy@opm.gov.
Section 5304 of title 5, United States
Code, authorizes locality pay for
General Schedule (GS) employees with
duty stations in the contiguous United
States and the District of Columbia.
Section 5304(f) of title 5, United
States Code, authorizes the President’s
Pay Agent (the Secretary of Labor, the
Director of the Office of Management
and Budget (OMB), and the Director of
the Office of Personnel Management
(OPM) to determine locality pay areas.
The boundaries of locality pay areas
must be based on appropriate factors,
E:\FR\FM\21NON1.SGM
21NON1
Agencies
[Federal Register Volume 71, Number 224 (Tuesday, November 21, 2006)]
[Notices]
[Pages 67391-67403]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: E6-19434]
=======================================================================
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice Applications and Amendments to Facility Operating
Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from October 27, 2006, to November 8, 2006. The
last biweekly notice was published on November 7, 2006 (71 FR 65139).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rulemaking,
Directives and Editing Branch, Division of Administrative Services,
Office of Administration, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, and should cite the publication date and
page number of this Federal Register notice. Written comments may also
be delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike,
Rockville, Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received may be examined at the Commission's
Public Document Room (PDR), located at One White Flint North, Public
File Area O1F21, 11555 Rockville Pike (first floor), Rockville,
Maryland. The filing of requests for a hearing and petitions for leave
to intervene is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or
[[Page 67392]]
petition; and the Secretary or the Chief Administrative Judge of the
Atomic Safety and Licensing Board will issue a notice of a hearing or
an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland, 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
AmerGen Energy Company, LLC, et al., Docket No. 50-219, Oyster Creek
Nuclear Generating Station (Oyster Creek), Ocean County, New Jersey
Date of amendment request: September 28, 2006.
Description of amendment request: The amendment would revise the
Oyster Creek Technical Specifications definition of Channel
Calibration, Channel Check, and Channel Functional Test in accordance
with the NUREG-1433, Revision 3, ``Standard Technical Specifications,
General Electric Plants--BWR [boiling water reactor]/4.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Will operation of the facility in accordance with the
proposed amendment involve a significant increase in the probability
or consequences of an accident previously evaluated?
Response: No.
The definitions of Channel Check, Channel Calibration[,] and
Channel Functional Test specified in Technical Specifications (TS)
provide basic information regarding what the test involves, the
components involved in the test, and general information regarding
how the test is to be performed. Instrument channel checking,
calibrating, and testing are not initiators of any accident
previously evaluated. Furthermore, the proposed changes will not
affect the ability of the channel being checked, calibrated[,] or
tested to respond as assumed in any accident previously evaluated.
Therefore, these revised definitions result in no increase in the
probability of an accident previously evaluated.
The proposed revisions of these definitions, corresponding
administrative changes (capitalization of definitions), and the
proposed alternate testing and calibrating methodology using
sequential, overlapping testing, and/or actual channel input signals
and/or in place qualitative assessments of resistance temperature
detectors (RTD's) and thermocouples (TC's) involve no changes to
plant design, equipment, or operation related to mitigation of
accidents. The qualitative evaluation of sensor behavior for non-
adjustable sensors will provide an accurate indication of sensor
operation and will
[[Page 67393]]
assure that [the evaluated] portion of the channel is operating
properly, ensuring that the consequences of an accident will remain
as previously evaluated. Therefore, these revised definitions result
in no increase in the consequences of an accident previously
identified.
Based on the above, AmerGen concludes that the proposed changes
do not involve a significant increase in the probability or
consequences of an accident previously evaluated.
2. Will operation of the facility in accordance of the proposed
amendment create the possibility of a new or different kind of
accident from any accident previously evaluated?
Response: No.
The proposed revisions of the instrument surveillance
definitions, corresponding administrative changes (capitalization of
definitions), and the proposed alternate testing and calibrating
methodology using sequential, overlapping testing, and/or actual
channel input signals and/or in place qualitative assessments of
RTD's and TC's do not involve a physical alteration of the plant or
a change in the methods governing normal plant operation. No new or
different type[s] of equipment will be installed. The proposed
changes also do not adversely affect the operation or operability of
existing plant equipment. The proposed revisions will allow a change
in testing and calibrating methodology. Allowing an alternate
testing and calibrating methodology will not change how the plant is
operated. Each instrument channel will be tested one sub channel at
a time, as is currently performed, and will not create the
possibility of a new or different kind of accident.
Based on the above discussion, AmerGen concludes that the
proposed changes do not create the possibility of a new or different
kind of accident from any accident previously evaluated.
3. Will operation of the facility in accordance with the
proposed amendment involve a significant reduction in a margin of
safety?
Response: No.
The affected definitions involve checking, calibrating[,] and
testing of instrumentation used in the mitigation of accidents to
ensure that the instrumentation will perform as assumed in safety
analyses. The proposed revisions of these definitions, corresponding
administrative changes (capitalization of definitions), and the
proposed alternate testing and calibrating methodology using
sequential, overlapping testing, and/or actual channel input signals
and/or in place qualitative assessments of RTD's and TC's does not
alter the ability of the instrument channel to respond as designed
or assumed in the safety analyses. As a result[,] the ability of the
plant to respond to[,] and mitigate[,] accidents is unchanged by the
revised definitions. Therefore, this change does not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Thomas S. O'Neill, Associate General
Counsel, Exelon Generation Company, LCC, 4300 Winfield Road,
Warrenville, IL 60555.
NRC Branch Chief: Harold K. Chernoff.
Exelon Generation Company, LLC, Docket Nos. STN 50-454 and STN 50-455,
Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois
Date of amendment request: June 16, 2006, as supplemented by letter
dated September 14, 2006.
Description of amendment request: The proposed amendment would
revise the Byron Station Updated Final Safety Analysis Report (UFSAR)
to incorporate changes concerning the requirements for physical
protection from tornado-generated missiles (TGM) for safety-related and
non-safety related systems and components.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The probability of occurrence of the design basis tornado
remains the same as originally established in the Byron Station
Updated Final Safety Analysis Report (UFSAR). The request involves
the use of a probability-based assessment of the need for physical
tornado missile protection of specific existing features at Byron
Station.
The request is to utilize an NRC approved methodology (i.e., the
Electric Power Research Institute (EPRI) Topical Report ``Tornado
Missile Risk Evaluation Methodology'') to conclude that the
acceptance criteria of NUREG-0800, ``Standard Review Plan,'' (SRP)
Section 2.2.3, ``Evaluation of Potential Accidents,'' Revision 2,
July 1981, has been met for Byron Station and that tornado missile
damage of selected components at Byron Station need not be
considered as a credible event.
Per Item 2 in Section III of SRP 3.5.1.4, probability methods
can be used to accept tornado missile effects provided damage to all
important structures, systems and components, as discussed in
Regulatory Guide 1.117 are considered. Per Section II of the SRP,
the acceptance criterion of SRP 2.2.3 is applicable. Section II of
SRP 2.2.3 states that the expected rate of occurrence of potential
exposure in excess of 10 CFR Part 100, ``Reactor Site Criteria,''
guidelines of approximately 1.0E-06 per reactor year is acceptable,
if when combined with reasonable qualitative arguments, that the
realistic probability can be shown to be smaller.
[The licensee in its September 14, 2006, letter stated the
following in regards to the consequences of an accident previously
evaluated:
The acceptance criteria for the TORMIS analysis has been
established as 1.0 E-06 per year cumulative probability of a TGM
striking/damaging an unprotected essential SSC [system, structure or
component] required for safe shutdown in the event of a tornado,
which is the same value found to be acceptable by the NRC based on
the accepted rates of occurrence of potential exposures in excess of
10 CFR 100 guidelines. This criteria in combination with
conservative qualitative assumptions show that the realistic
probability of a potential exposure in excess of the 10 CFR Part 100
guidelines is lower than 1.0 E-06 per year. The conservative
qualitative assumptions are the same as previously found to be
acceptable by the NRC as described below:
It is assumed that an essential SSC being struck/damaged by a
tornado missile will result in damage sufficient to preclude it from
performing its safety function.
It is assumed that the damage to the essential SSC results in
damage to fuel sufficient to result in conservatively calculated
radiological release values in excess of 10 CFR 100 guidelines.
There are no missiles that can directly impact irradiated fuel,
even the spent fuel stored in the Spent Fuel Pool.]
The proposed change is not considered to constitute a
significant increase in the probability or occurrence or the
consequences of an accident due to the extremely low probability of
damage due to tornado-generated missiles and therefore an extremely
low probability of a radiological release. Therefore, the proposed
changes do not involve a significant increase in the probability or
consequences of previously evaluated accidents.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
This change involves the use of an alternative methodology to
assess the need for tornado missile protection on selected Byron
Station components. The use of this methodology and the changes to
the Byron Station UFSAR will be limited to design basis tornado
applications and do not contribute to the possibility of a new or
different kind of accident from those previously analyzed.
No new or different system interactions are created and no new
processes are introduced. The proposed change does not introduce any
new failure mechanisms, malfunctions, or accident initiators not
already considered in the design and licensing bases. Based on this
evaluation, the proposed change does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
[[Page 67394]]
The changes, allowing for no additional physical protection for
tornado-generated missiles for certain Byron Sation components, is
based on successfully meeting the acceptance criteria of NUREG-0800,
``Standard Review Plan,'' (SRP) Section 2.2.3, ``Evaluation of
Potential Accidents,'' Revision 2, July 1981. Because of the
extremely low probability of damage to these components from
tornado-generated missiles, the change is not considered to
constitute a significant decrease in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Bradley J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Kennett
Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
FirstEnergy Nuclear Operating Company, et al., Docket No. 50-440, Perry
Nuclear Power Plant, Unit 1, Lake County, Ohio
Date of amendment request: October 13, 2006.
Description of amendment request: The proposed amendment would
eliminate License Condition 2.F, which requires reporting violations of
Operating License Section 2.C, and eliminates Technical Specification
5.6.6, which contains a reporting condition similar to Operating
License Section 2.C.(6).
The availability of this operating license improvement was
announced in the Federal Register on November 4, 2005 (70 FR 67202), as
part of the consolidated line item improvement process (CLIIP). The NRC
staff issued a notice of opportunity for comment in the Federal
Register on August 29, 2005 (70 FR 51098), on possible amendments
concerning this CLIIP, including a model safety evaluation and a model
no significant hazards consideration (NSHC) determination. The NRC
staff subsequently issued a notice of availability of the models for
referencing in license amendment applications in the Federal Register
on November 4, 2005 (70 FR 67202). In its application dated October 13,
2006, the licensee affirmed the applicability of the following
determination.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
1. Does the change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
The proposed change involves the deletion of a reporting
requirement. The change does not affect plant equipment or operating
practices and therefore does not significantly increase the
probability or consequences of an accident previously evaluated.
2. Does the change create the possibility of a new or different
kind of accident from any accident previously evaluated?
Response: No.
The proposed change is administrative in that it deletes a
reporting requirement. The change does not add new plant equipment,
change existing plant equipment, or affect the operating practices
of the facility. Therefore, the change does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change deletes a reporting requirement. The change
does not affect plant equipment or operating practices and therefore
does not involve a significant reduction in a margin of safety.
The NRC staff proposes to determine that the amendment request
involves no significant hazards consideration.
Attorney for licensee: David W. Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street, Akron, OH 44308.
NRC Branch Chief: Daniel S. Collins.
Florida Power Corporation, et al., Docket No. 50-302, Crystal River
Unit 3 Nuclear Generating Plant, Citrus County, Florida
Date of amendment request: October 5, 2006.
Description of amendment request: The proposed amendment to the
Improved Technical Specification will revise the defined pool burnup-
enrichment requirements, storage configuration for fresh fuel and low
burnup/high enriched fuel, the definition of a peripheral assembly, and
will include minor editorial changes.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
(1) Involve a significant increase in the probability or
consequences of an accident previously evaluated.
The LAR proposes to revise the fresh fuel loading configuration.
PEF [Progress Energy Florida, Inc.] has reanalyzed the criticality
of the revised storage configuration for fresh fuel checkerboarded
with spent fuel in Pool A, and surrounded by empty water cells in
Pool B. Similarly, storage of spent fuel in peripheral storage
locations, given the new definition, was also reanalyzed. The
revised fuel storage configuration does not affect any structure,
system, component or process related to the operation of Crystal
River Unit 3 (CR-3). As a result, the proposed LAR will not change
the probability or consequences of any accidents previously
evaluated that are related to operation of the plant. Thus, only
those accidents that are related to movement and storage of fuel
assemblies could be potentially affected by the proposed LAR.
Fuel Handling Accidents (FHAs) are analyzed in Section 14.2.2.3
of the CR-3 Final Safety Analysis Report (FSAR). These include a FHA
inside the Reactor Building (RB) and outside the RB. This LAR
involves storage of fuel assemblies, an activity conducted outside
the RB only. Therefore, only the FHA outside the RB event needs to
be considered.
The FHA outside the RB event is described as the dropping of a
fuel assembly into the spent fuel storage pool that results in
damage to a fuel assembly and the release of the gaseous fission
products. The current FHA assumes all 208 fuel pins in the dropped
assembly are damaged and the gas gap activity released. The results
of that analysis demonstrate that the applicable dose acceptance
criteria, 10 CFR 50.67 and Regulatory Guide 1.183, ``Alternative
Radiological Source Terms for Evaluating Design Basis Accidents at
Nuclear Power Reactors,'' are satisfied. Thus, the consequences of a
FHA are not increased by the allowed change in the fresh fuel
configuration. The fresh fuel storage configurations permit more
effective use of already existing storage locations. They do not
change the frequency or method for handling fuel assemblies. Fuel
handling equipment is unaffected. As such, the probability of a FHA
has not increased. Since only one fuel assembly is handled at a
time, the consequences of a FHA have not increased.
The current limiting heat load for the spent fuel pool is from
the combined impact of stored spent fuel and a full core off-load.
These changes do not increase spent fuel storage capacity over that
for which the racks are currently analyzed and it does not increase
the amount of heat ejected from an off-loaded core. Consequently,
current analyses for spent fuel pool cooling remain valid. The
configuration change allows fresh fuel to be checkerboarded with
spent fuel. Since these changes do not increase the storage capacity
over that already analyzed for the racks, filling the empty water
cells in the checkerboard pattern with spent fuel will not increase
the heat load over that already analyzed. The Pool B allowance to
surround a higher enriched/lower burnup fuel assembly in Pool B with
empty water cells or changing the definition of a periphery rack
cell does not increase the number of spent fuel assembly rack
locations over that previously analyzed. Therefore, there is no
increase in the pool heat load over that already analyzed.
A change in storage configurations in storage Pools A and B does
not increase the probability of a full core off-load or the
frequency of establishing maximum heat load conditions.
The FSAR specifies the normal upper limit of the fuel pool
cooling system as 160 [deg]F. Administrative controls are
implemented to
[[Page 67395]]
control when fuel may be moved from the reactor to the fuel pool to
prevent reaching this limit.
Because neither the probability nor the consequences of a FHA
are increased, and because there is not additional heat input to the
spent fuel pools, it is concluded that the LAR does not involve a
significant increase in the probability or consequences of an
accident previously evaluated.
(2) Create the possibility of a new or different kind of
accident from any accident previously evaluated?
Onsite storage of spent fuel assemblies in the spent fuel pools
is a normal activity for which CR-3 has been designed and licensed.
As part of assuring that this normal activity can be performed
without endangering public health and safety, the ability of CR-3 to
safely accommodate different possible accidents in the spent fuel
pools, such as dropping a fuel assembly or the misloading of a fuel
assembly, have been analyzed. The revised fuel storage
configurations proposed by the LAR does not change the methods of
fuel movement or fuel storage. No structural or mechanical change to
racks or fuel handling equipment is being proposed. The proposed
revisions allow for more effective use of existing, unmodified rack
locations when fresh or highly enriched, low burnup fuel is stored
in the pool. The proposed revisions are a modification to the
criticality analysis only, and therefore the proposed LAR does not
create any new or different kind of accident from those previously
evaluated.
(3) Involve a significant reduction in a margin of safety?
The CR-3 Improved Technical Specification (ITS) ensures the
effective neutron multiplication factor, Keff, of the spent fuel
storage racks is maintained less than or equal to 0.95 when fully
loaded and flooded with unborated water. The revisions proposed by
the LAR likewise ensure Keff is maintained less than this
requirement.
Analyses for the proposed fuel storage configurations have shown
that sufficient margin exists for fuel enriched to the maximum
allowed by the CR-3 license, and for all fuel that is or has been in
use at CR-3. Maintaining this margin is assured by remaining within
the limits on initial enrichment and fuel burnup that are specified
in the CR-3 ITS and, in the case of highly enriched, low burnup fuel
in Pool B, by water hole spacing. The LAR proposes allowing fresh
fuel to be checkerboarded with Category B type fuel in Pool A rather
than with empty water cells. It also allows fresh fuel with high
initial enrichment which does not meet current burnup requirements
to be placed in Pool B if surrounded by eight empty water cells. It
also proposes to change the definition of a periphery rack location
for storing Category BP type fuel. Analyses show that the new
proposed limits ensure that Keff remains less than 0.95. Attachment
E [not included in this FR notice] provides an analysis summary.
The current CR-3 licensing basis allows the use of
administrative controls, e.g., curves of initial fuel assembly
enrichment versus burnup, as a means of preventing criticality in
the spent fuel pools. The use of these curves would be continued
under this proposed amendment. The changes to these curves proposed
by this LAR consist of revising the values of burnup and adding
notes to restrict loading of certain fuel assemblies to specific
configurations. These types of curves and administrative controls
have been included in the CR-3 operating license and their use
implemented by site procedures for many operating cycles. From this
previous use, CR-3 personnel are familiar with the practice of using
administrative controls, such as curves of fuel assembly enrichment
versus burnup, to prevent criticality events when placing fuel
assemblies in the spent fuel pool.
Misloaded and mislocated fuel assemblies were analyzed. The
analysis demonstrated that misloading of a fresh fuel assembly,
assuming no soluble poison (boron) in the water does result in
exceeding the criticality margin regulatory limit of Keff = 0.95.
The analysis further shows that a concentration of 165 ppm boron in
the Pool A and a concentration of 46 ppm boron in Pool B is
sufficient to ensure Keff < 0.95. LCO 3.7.14 currently requires a
minimum boron concentration of 1925 ppm in the spent fuel pools
until fuel is verified as having been loaded in accordance with the
enrichment and burnup requirements of LCO 3.7.15. The soluble boron
assumed in the analysis for this proposed change is substantially
less than the 1925 ppm required by the existing license. Therefore,
existing license requirements for soluble boron remain conservative.
The NRC staff has reviewed the analysis provided for Florida Power
Corporation and, based on this review, it appears that the three
standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff
proposes to determine that the amendment request involves no
significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Branch Chief (Acting): L. Raghavan.
FPL Energy Duane Arnold, LLC, Docket No. 50-331, Duane Arnold Energy
Center (DAEC), Linn County, Iowa
Date of amendment request: July 17, 2006.
Description of amendment request: The proposed amendment would
revise the Limiting Condition for Operation (LCO) 3.6.3.1 to eliminate
the requirement for the Containment Atmospheric Dilution (CAD) system,
allowing its removal from the DAEC. LCO 3.6.3.2 would also be revised
to allow an additional 48 hours on plant start-up or shutdown sequences
for the primary containment to be de-inerted.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The Containment Atmosphere Dilution (CAD) system and primary
containment oxygen concentration are not initiators to any accident
previously evaluated in the DAEC Updated Final Safety Analysis
Report (UFSAR). The CAD system and containment oxygen concentration
were previously relied upon to mitigate the consequences of a design
basis accident (DBA) combustible gas mixture. However, the revised
10 CFR 50.44 (68 FR 54123) no longer defines a DBA hydrogen release
(i.e., combustible gas mixture) and the Commission has subsequently
found that the DBA loss of coolant accident (LOCA) hydrogen release
is not risk significant. In addition, hydrogen control systems, such
as CAD, have been determined to be ineffective at mitigating
hydrogen releases from the more risk significant beyond design basis
accidents that could threaten containment integrity. Therefore,
elimination of the CAD system will not significantly increase the
consequences of any accident previously evaluated. The consequences
of an accident while relying on the revised Required Actions for
primary containment oxygen concentration are no different than the
consequences of the same accidents under the current Required
Actions. As a result, the consequences of any accident previously
evaluated are not significantly increased.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
No new or different accidents result from utilizing the proposed
change. The changes do not involve a physical alteration of the
plant, except for the elimination of the CAD system (i.e., no new or
different type of equipment will be installed) or a change in the
methods governing normal plant operation. The CAD system is not
considered an accident precursor, nor does its existence or
elimination have any adverse impact on the pre-accident state of the
reactor core or post accident confinement of radionuclides within
the containment building from any DBA. In addition, the changes do
not impose any new or different requirements. The changes to the
Technical Specifications for oxygen concentration do not alter
assumptions made in the safety analysis, but reflect changes to the
safety analysis requirements allowed under the revised 10 CFR 50.44.
Specifically that an inerted containment is no[t] required to
mitigate any DBA, but has been found to be helpful in mitigating
certain beyond design basis events (i.e., severe accidents) that
could generate combustible levels of hydrogen.
[[Page 67396]]
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The installation of combustible gas control systems, such as
CAD, required by the original Sec. 50.44(b)(3) was intended to
address the limited quantity and rate of hydrogen generation that
was postulated from a design-basis LOCA. The Commission has found
that this hydrogen release is not risk-significant because the
design-basis LOCA hydrogen release does not contribute to the
conditional probability of a large release up to approximately 24
hours after the onset of core damage. In addition, these systems
were ineffective at mitigating hydrogen releases from risk-
significant accident sequences that could threaten containment
integrity. (68 FR 54123). The proposed changes to CAD and primary
containment oxygen concentration reflect this new regulatory
position and, in light of the remaining plant equipment,
instrumentation, procedures, and programs that provide effective
mitigation of and recovery from reactor accidents, including
postulated beyond design basis events, does not result in a
significant reduction in a margin of safety.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. R. E. Helfrich, Florida Power & Light
Company, P. O. Box 14000, Juno Beach, FL 33408-0420.
NRC Branch Chief: L. Raghavan.
Indiana Michigan Power Company (I&M), Docket No. 50-316, Donald C. Cook
Nuclear Plant, Unit 2, Berrien County, Michigan
Date of amendment request: September 15, 2006.
Description of amendment request: The proposed amendment would
replace the current control system and it will increase the nominal
control fluid oil operating pressure from 114 pounds per square inch
gauge (psig) to 1600 psig. The control fluid oil pressure provides an
input to the reactor protection system via three pressure switches
connected to the control fluid header. Due to the change in the
operating pressure, I&M is proposing a revision to the allowable low
fluid oil pressure value from greater than or equal to 57 psig to
greater than or equal to 750 psig.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change reflects a design change to the turbine
control system that increases the control oil pressure,
necessitating a change to the value at which a low fluid oil
pressure initiates a reactor trip. The turbine control oil pressure
is an input to the reactor trip instrumentation, and the reactor
trip is a response to an event that trips the turbine. A change in
the nominal control oil pressure does not introduce any mechanisms
that would increase the probability of an accident previously
analyzed. The reactor trip on turbine trip function is an
anticipatory trip, and the safety analysis does not credit this trip
for protecting the reactor core. Thus, the consequences of
previously analyzed accidents are not impacted.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The control fluid oil pressure decreases in response to a
turbine trip. The value at which the low control fluid oil initiates
a reactor trip is not an accident initiator. The change in the value
reflects the higher pressure of the turbine control system that will
be installed during the Unit 2 Cycle 17 refueling outage.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The change involves a parameter that initiates an anticipatory
reactor trip following a turbine trip. The safety analyses do not
credit this anticipatory trip for reactor core protection.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The Nuclear Regulatory Commission (NRC) staff has reviewed the
licensee's analysis and, based on this review, it appears that the
three standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC
staff proposes to determine that the amendment requests involve no
significant hazards consideration.
Attorney for licensee: James M. Petro, Jr., Esquire, One Cook
Place, Bridgman, MI 49106.
NRC Acting Branch Chief: Martin C. Murphy.
Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald
C. Cook Nuclear Plant, Unit 1 and 2, Berrien County, Michigan
Date of amendment request: September 15, 2006.
Description of amendment request: The proposed amendment would
modify the Technical Specifications (TS) to change Required Action
Notes in TS 3.3.1, ``Reactor Trip System Instrumentation,'' and TS
3.3.2, ``Engineered Safety Features Actuation System Instrumentation,''
to reflect installed bypass test capability, as well as correct one
administrative error in TS 3.3.1 Condition Q. The proposed changes to
the Required Action Notes are consistent with wording in Standard
Technical Specifications (NUREG-1431, Revision 3) for plants with
installed bypass test capability.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability of occurrence or consequences of an accident
previously evaluated?
Response: No.
The proposed change reflects NUREG-1431, Revision 3, ``Standard
Technical Specifications, Westinghouse Plants,'' (STS) wording for
plants with installed bypass test capability and aligns Technical
Specification (TS) Condition entry requirements with other portions
of the TS. The proposed changes do not modify how the reactor trip
system (RTS) and engineered safety features actuation systems
(ESFAS) functions respond to an accident condition. The proposed
changes to the TS Required Action Notes prevent unnecessary TS
Action entry during performance of surveillance testing. The
probability of accidents previously evaluated remains unchanged
since the proposed change does not affect any accident initiators.
The consequences of accidents previously evaluated are unaffected by
this change because no change to any accident mitigation scenario
has resulted and there are no additional challenges to fission
product barrier integrity.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
No changes are being made to the plant that would introduce any
new accident causal mechanisms. The proposed change to
[[Page 67397]]
the Required Action Notes and Condition entry requirements does not
adversely affect previously identified accident initiators and does
not create any new accident initiators. The change does not affect
how the RTS and ESFAS functions operate. No new single failure or
accident scenarios are created by the proposed change and the
proposed change does not result in any event previously deemed
incredible being made credible.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
No safety analyses were changed or modified as a result of the
proposed TS changes to reflect STS wording for plants with installed
bypass test capability or for aligning TS Condition entry
requirements. All margins associated with the current safety
analyses acceptance criteria are unaffected. The current safety
analyses remain bounding. The safety systems credited in the safety
analyses will continue to be available to perform their mitigation
functions. The proposed change does not affect the availability or
operability of safety-related systems and components.
Therefore, the proposed change does not involve a significant
reduction in the margin of safety.
The Nuclear Regulatory Commission (NRC) staff has reviewed the
licensee's analysis and, based on this review, it appears that the
three standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC
staff proposes to determine that the amendment requests involve no
significant hazards consideration.
Attorney for licensee: James M. Petro, Jr., Esquire, One Cook
Place, Bridgman, MI 49106
NRC Acting Branch Chief: M. Murphy.
Nuclear Management Company, LLC, Docket Nos. 50-282 and 50-306, Prairie
Island Nuclear Generating Plant, Units 1 and 2, Goodhue County,
Minnesota
Date of amendment request: August 14, 2006.
Description of amendment request: The proposed amendments would
make miscellaneous improvements to the Technical Specifications (TS)
for Prairie Island Nuclear Generating Plant (PINGP) Units 1 and 2. The
proposed amendments would revise TS 1.3, ``Completion Times''; TS
3.1.4, ``Rod Group Alignment Limits''; TS 3.3.7, ``Spent Fuel Pool
Special Ventilation System (SFPSVS) Actuation Instrumentation''; TS
3.7.10, ``Control Room Special Ventilation System (CRSVS)''; and TS
Chapter 4.0, ``Design Features''.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
This license amendment request proposes changes to the Prairie
Island Nuclear Generating Plant Technical Specifications as follows:
Technical Specification 1.3, ``Completion Times'', revise a text
header and add a new text header; Technical Specification 3.1.4,
``Rod Group Alignment Limits'', remove a Surveillance Note which
cross-references another Technical Specification and may cause
confusion; Technical Specification 3.3.7, ``Spent Fuel Pool Special
Ventilation System (SFPSVS) Actuation Instrumentation'', revises the
Modes of Applicability consistent with plant design and the
Technical Specifications for the Spent Fuel Pool Special Ventilation
System, the supported system; Technical Specification 3.7.10,
``Control Room Special Ventilation System (CRSVS)'', revises the
applicability of Condition C and clarifies the requirements of the
Surveillance to verify train filtration flow; and Technical
Specification Chapter 4.0, ``Design Features'', revises Reference 1
to the most recent version of the document.
Revising and adding text headers in Technical Specification 1.3
are administrative changes because the revised document does not
change any basis for the current Technical Specifications. Since
these are administrative changes, they do not involve a significant
increase in the probability or consequences of a previously
evaluated accident. Technical Specification 3.1.4 assures that the
control rod positions are within the limits assumed in the safety
analysis and that the assumed shutdown margin is available when
needed. This license amendment request proposes to remove a Note
from a surveillance requirement that cross-references to Technical
Specification 3.1.7. Removal of this Note does not change plant
operations, testing or maintenance; therefore the proposed change
does not involve a significant increase in the probability of an
accident. Since plant operations, testing and maintenance are not
changed, the proposed changes do not involve a significant increase
in the consequences of an accident previously evaluated.
The Spent Fuel Pool Special Ventilation System filters
radioactive materials in the fuel pool enclosure atmosphere released
following a fuel handling accident. This license amendment request
proposes to revise the Modes and Other Specified Conditions of
Applicability for the actuation instrumentation.
Technical Specification to be consistent with the Modes and
Other Specified Conditions of Applicability in the Technical
Specification for the supported system. The Spent Fuel Pool Special
Ventilation System and its actuation instrumentation are not
accident initiators; therefore, the proposed changes do not affect
the probability of an accident. With the proposed change, the
Technical Specifications will continue to require the system
actuation instrumentation to be operable when irradiated fuel is
moved in the fuel pool enclosure which is also the required
Applicability in the supported system Technical Specification. Since
the instrumentation will be required to actuate the supported system
when it is required to operate, the accident consequences will
continue to be mitigated with this proposed Technical Specification
change. Thus, the proposed Technical Specification change does not
involve a significant increase in the consequences of an accident
previously evaluated.
The Control Room Special Ventilation System provides an enclosed
control room environment from which the plant can be operated
following an uncontrolled release of radioactivity. This system is
not an accident initiator, thus the proposed changes do not increase
the probability of an accident. This license amendment proposes
changes which will: (1) Reduce the time to shut down the plant when
Technical Specification required actions or completion time is not
met; and (2) clarifies surveillance requirements to assure that the
system performs as designed. These changes do not impact the
performance of the system; thus this change does not involve a
significant increase in the consequences of an accident previously
evaluated.
Updating the reference in Technical Specification Chapter 4.0 is
an administrative change because the revised document does not
change any basis for the current Technical Specifications. Since
this is an administrative change, it does not involve a significant
increase in the probability or consequences of a previously
evaluated accident.
The changes proposed in this license amendment do not involve a
significant increase the probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
This license amendment request proposes changes to the Prairie
Island Nuclear Generating Plant Technical Specifications as follows:
Technical Specification 1.3, ``Completion Times'', revise a text
header and add a new text header; Technical Specification 3.1.4,
``Rod Group Alignment Limits'', remove a Surveillance Note which
cross-references another Technical Specification and may cause
confusion; Technical Specification 3.3.7, ``Spent Fuel Pool Special
Ventilation System (SFPSVS) Actuation Instrumentation'', revises the
Modes of Applicability consistent with plant design and the
Technical Specifications for the Spent Fuel Pool Special Ventilation
System, the supported system; Technical Specification 3.7.10,
``Control Room Special Ventilation System (CRSVS)'', revises the
applicability of Condition C and clarifies the requirements of the
Surveillance to verify train filtration flow; and Technical
Specification Chapter 4.0, ``Design Features'',
[[Page 67398]]
revises Reference 1 to the most recent version of the document.
Revising and adding text headers in Technical Specification 1.3
are administrative changes because the revised document does not
change any basis for the current Technical Specifications. Since
these are administrative changes, they do not create the possibility
of a new or different kind of accident.
Removal of a surveillance note from Technical Specification
3.1.4 that cross-references another Technical Specification does not
change any plant operations, maintenance activities or testing
requirements. The Limiting Conditions for Operation will continue to
be met and the proper control rod positions will continue to be
maintained. There are no new failure modes or mechanisms created
through the removal of the Surveillance Requirements Note, nor are
new accident precursors generated by this change. This proposed
change does not create the possibility of a new or different kind of
accident from any previously evaluated.
The proposed revision of Modes of Applicability for the Spent
Fuel Pool Special Ventilation System actuation instrumentation makes
operation of the actuation instrumentation consistent with the
Technical Specification requirements for the supported system and
does not change the operation of the supported system for accident
mitigation. The Limiting Conditions for Operation will continue to
be met, no new failure modes or mechanisms are created and no new
accident precursors are generated by this change. This proposed
change does not create the possibility of a new or different kind of
accident from any previously evaluated.
The changes proposed for the Control Room Special Ventilation
System Technical Specifications do not change any the system
operations, maintenance activities or testing requirements. The
Limiting Conditions for Operation will continue to be met, no new
failure modes or mechanisms are created and no new accident
precursors are generated by this change. This proposed change does
not create the possibility of a new or different kind of accident
from any previously evaluated.
Updating the reference in Technical Specification Chapter 4.0 is
an administrative change because the revised document does not
change any basis for the current Technical Specifications. Since
this is an administrative change, it does not create the possibility
of a new or different kind of accident.
The Technical Specification changes proposed in this license
amendment do not create the possibility of a new or different kind
of accident from any previously evaluated.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
Response: No.
This license amendment request proposes changes to the Prairie
Island Nuclear Generating Plant Technical Specifications as follows:
Technical Specification 1.3, ``Completion Times'', revise a text
header and add a new text header; Technical Specification 3.1.4,
``Rod Group Alignment Limits'', remove a Surveillance Note which
cross-references another Technical Specification and may cause
confusion; Technical Specification 3.3.7, ``Spent Fuel Pool Special
Ventilation System (SFPSVS) Actuation Instrumentation'', revises the
Modes of Applicability consistent with plant design and the
Technical Specifications for the Spent Fuel Pool Special Ventilation
System, the supported system; Technical Specification 3.7.10,
``Control Room Special Ventilation System (CRSVS)'', revises the
applicability of Condition C and clarifies the requirements of the
Surveillance to verify train filtration flow; and Technical
Specification Chapter 4.0, ``Design Features'', revises Reference 1
to the most recent version of the document.
Revising and adding text headers in Technical Specification 1.3
are administrative changes because the revised document does not
change any basis for the current Technical Specifications. Since
these are administrative changes, they do not involve a significant
reduction in a margin of safety.
Plant operations are required to meet all Technical
Specifications for which the Applicability is met; therefore,
removal of the cross-reference Note from a Technical Specification
3.1.4 surveillance requirement does not change how the plant is
operated and therefore, this change does not involve a significant
reduction in a margin of safety.
Technical Specification 3.3.7 provides requirements for
actuation instrument which supports the operation of the Spent Fuel
Pool Special Ventilation System as required by Technical
Specification 3.7.13. The current Applicability for Technical
Specification 3.3.7 requires the actuation instrumentation to be
operable in Modes which are not required by Technical Specification
3.7.13. This license amendment proposes to make Technical
Specification 3.3.7 Applicability the same as Technical
Specification 3.7.13. This change does not reduce the conditions or
Modes when the Spent Fuel Pool Special Ventilation System will
operate and perform its accident mitigation function; thus this
change does not involve a significant reduction in a margin of
safety.
This license amendment proposes changes to the Control Room
Special Ventilation System Technical Specifications which will: (1)
Reduce the time to shut down the plant when Technical Specification
required actions or completion time is not met; and (2) clarifies
surveillance requirements to assure that the system performs as
designed. The proposed time to shut down the plant is consistent
with other Technical Specifications for shutting down the plant and
allows adequate time for an orderly shut down of the plant; thus
this change does not involve a significant reduction in a margin of
safety. The surveillance requirement clarifications do not reduce
any testing requirements and will continue to demonstrate that the
system can perform its required safety function and satisfy the
Limiting Conditions for Operation. Thus this change does not involve
a significant reduction in a margin of safety.
Updating the reference in Technical Specification Chapter 4.0 is
an administrative change because the revised document does not
change any basis for the current Technical Specifications. Since
this is an administrative change, it does not involve a significant
reduction in a margin of safety.
The Technical Specification changes proposed in this license
amendment do not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92 (c)
are satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Attorney for licensee: Jonathan Rogoff, Esquire, Vice President,
Counsel & Secretary, Nuclear Management Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Branch Chief: M. Murphy (A).
Tennessee Valley Authority, Docket Nos. 50-260 and 50-296, Browns Ferry
Nuclear Plant (BFN), Units 2 and 3, Limestone County, Alabama
Date of amendment request: October 26, 2006.
Description of amendment request: The proposed request would revise
the Units 2 and 3 emergency diesel generator (EDG) Technical
Specification (TS) Completion Time (CT) from 14 days to 7 days for
restoration of an inoperable EDG. The current 14-day CT was based on
the assumption that Unit 1 was shut down. The near-term restart of Unit
1 will invalidate this assumption, therefore, the affected CTs are
being returned to their original duration of 7 days.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed Technical Specification change involve a
significant increase in the probability or consequences of an
accident previously evaluated?
Response: No.
The EDGs are designed as backup alternating current (AC) power
sources in the event of a loss of offsite power. The proposed
restoration of the EDG CT to its original TS duration does not
change the conditions, operating configurations, or minimum amount
of operating equipment assumed in the safety analysis for accident
mitigation. No changes are proposed in the manner in which the EDGs
provide plant protection or which create new modes of plant
operation. Therefore, the proposed amendment does not involve a
significant increase in the probability or consequences