Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 51222-51236 [06-7137]
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Federal Register / Vol. 71, No. 167 / Tuesday, August 29, 2006 / Notices
For the Nuclear Regulatory Commission.
NUCLEAR REGULATORY
COMMISSION
jlentini on PROD1PC65 with NOTICES
Southern Nuclear Operating Company;
Notice of Receipt and Availability of an
Application for an Early Site Permit for
the Vogtle ESP Site
On August 15, 2006, the Nuclear
Regulatory Commission (NRC, the
Commission) received an application
from Southern Nuclear Operating
Company filed pursuant to Section 103
of the Atomic Energy Act and 10 CFR
part 52, for an early site permit (ESP) for
a location in eastern Georgia (near
Waynesboro, Georgia) identified as the
Vogtle ESP site.
An applicant may seek an ESP in
accordance with Subpart A of 10 CFR
part 52 separate from the filing of an
application for a construction permit
(CP) or combined license (COL) for a
nuclear power facility. The ESP process
allows resolution of issues relating to
siting. At any time during the period of
an ESP (up to 20 years), the permit
holder may reference the permit in an
application for a CP or COL.
Subsequent Federal Register notices
will address the acceptability of the
tendered ESP application for docketing
and provisions for participation of the
public and other parties in the ESP
review process.
A copy of the application is available
for public inspection at the
Commission’s Public Document Room
(PDR), located at One White Flint North,
11555 Rockville Pike (first floor),
Rockville, Maryland and via the
Agencywide Documents Access and
Management System (ADAMS) Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html.
The accession number for the
application is ML062290246.
Future publicly available documents
related to the application will also be
posted in ADAMS. Persons who do not
have access to ADAMS or who
encounter problems in accessing the
documents located in ADAMS should
contact the NRC Public Document Room
staff by telephone at 1–800–397–4209 or
301–415–4737, or by e-mail to
pdr@nrc.gov. The application is also
available to local residents at the Burke
County Library, in Waynesboro,
Georgia, and it will be available on the
NRC Web page at https://www.nrc.gov/
reactors/new-licensing/esp.html.
Dated at Rockville, Maryland, this 21st day
of August, 2006.
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David B. Matthews,
Director, Division of New Reactor Licensing,
Office of Nuclear Reactor Regulation.
[FR Doc. E6–14285 Filed 8–28–06; 8:45 am]
BILLING CODE 7590–01–P
NUCLEAR REGULATORY
COMMISSION
Sunshine Act Notice
Weeks of August 28, September 4,
11, 18, 25, October 2, 2006.
PLACE: Commissioners’ Conference
Room, 1155 Rockville Pike, Rockville,
Maryland.
STATUS: Public and Closed.
MATTERS TO BE CONSIDERED:
DATE:
Week of August 28, 2006
There are no meetings scheduled for
the week of August 28, 2006.
Week of September 4, 2006—Tentative
Wednesday, September 6, 2006
1:50 p.m. Affirmation Session (Public)
(Tentative)
a. Pacific Gas & Elec. Co. (Diablo
Canyon ISFSI), Docket No. 72–26–
ISFSI ‘‘Motion by San Luis Obispo
Mothers for Peace, Sierra Club, and
Peg Pinard for Declaratory and
Injunctive Relief with respect to
Diablo Canyon ISFSI’’. (Tentative).
b. AmerGen Energy Company, LLC
(License Renewal for Oyster Creek
Nuclear Generating Station) Docket
No. 50–0219, Legal challenges to
LBP–06–07 and LBP–06–11.
(Tentative).
c. Pa’ina Hawaii, LLC, LBP–06–4, 63
NRC 99 (2006) and LBP–06–12, 63
NRC 409 (2006). (Tentative).
Week of September 11, 2006—Tentative
Monday, September 11, 2006
9:30 a.m. Discussion of Security Issues
(Closed—Ex. 1).
1:30 p.m. Discussion of Security Issues
(Closed—Ex. 1& 3).
Tuesday, September 12, 2006
9:30 a.m. Meeting with Organization of
Agreement States (OAS) and
Conference of Radiation Control
Program Directors (CRCPD) (Public
Meeting) (Contact: Shawn Smith,
301–415–2620).
This meeting will be webcast live at
the Web address https://www.nrc.gov.
1 p.m. Discussion of Security Issues
(Closed—Ex. 1).
Week of September 18, 2006—Tentative
There are no meetings scheduled for
the week of September 18, 2006.
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Week of September 25, 2006—Tentative
There are no meetings scheduled for
the week of September 25, 2006.
Week of October 2, 2006—Tentative
There are no meetings scheduled for
the week of October 2, 2006.
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*The schedule for Commission
meetings is subject to change on short
notice. To verify the status of meetings
call (recording)—(301) 415–1292.
Contact person for more information:
Michelle Schroll, (301) 415–1661.
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The NRC Commission Meeting
Schedule can be found on the Internet
at: https://www.nrc.gov/what-we-do/
policy-making/schedule.html.
*
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The NRC provides reasonable
accommodation to individuals with
disabilities where appropriate. If you
need a reasonable accommodation to
participate in these public meetings, or
need this meeting notice or the
transcript or other information from the
public meetings in another format (e.g.,
braille, large print), please notify the
NRC’s Disability Program Coordinator,
Deborah Chan, at 301–415–7041, TDD:
301–415–2100, or by e-mail at
DLC@nrc.gov. Determinations on
requests for reasonable accommodation
will be made on a case-by-case basis.
*
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This notice is distributed by mail to
several hundred subscribers; if you no
longer wish to receive it, or would like
to be added to the distribution, please
contact the Office of the Secretary,
Washington, DC 20555 (301–415–1969).
In addition, distribution of this meeting
notice over the Internet system is
available. If you are interested in
receiving this Commission meeting
schedule electronically, please send an
electronic message to dkw@nrc.gov.
Dated: August 24, 2006.
R. Michelle Schroll,
Office of the Secretary.
[FR Doc. 06–7236 Filed 8–25–06; 9:49 am]
BILLING CODE 7590–01–M
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
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Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from August 4,
2006 to August 17, 2006. The last
biweekly notice was published on
August 15, 2006 (71 FR 46929).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
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involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
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51223
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
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limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
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a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
Carolina Power & Light Company,
Docket No. 50–261, H. B. Robinson
Steam Electric Plant, Unit No. 2,
Darlington County, South Carolina
Date of amendment request: April 11,
2006.
Description of amendment request:
The proposed amendment would
modify Technical Specification 5.6.5
‘‘Core Operating Limits Report (COLR)’’
to add two U.S. Nuclear Regulatory
Commission-approved topical reports to
the COLR methodologies list. These
topical reports allow the use of S–
RELAP5 thermal-hydraulic analysis
code for accident safety analyses.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The Proposed Change Does Not Involve
a Significant Increase in the Probability or
Consequences of an Accident Previously
Evaluated.
The two topical reports have been
reviewed and approved by the NRC for use
in determining core operating limits. The
core operating limits to be developed using
the new methodologies for HBRSEP [H. B.
Robinson Steam Electric Plant], Unit No. 2,
will be established in accordance with the
applicable limitations as documented in the
NRC Safety Evaluation Reports. In a May 11,
2001, NRC Safety Evaluation Report, the NRC
concluded that the S–RELAP5 code is
capable of addressing the thermal-hydraulic
response of the target non-LOCA [loss-ofcoolant accident] events in a conservative
manner and is, therefore, an acceptable
replacement for the ANF–RELAP code. In the
May 19, 2004, Safety Evaluation Report for
Revision 1 to EMF–2310(P)(A), the NRC
concluded that the code remained acceptable
for use for the non-LOCA events. In a March
15, 2001, Safety Evaluation Report, the NRC
concluded that the code was acceptable for
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use for small break LOCA analyses at
Westinghouse pressurized water reactors.
The proposed change, by itself, does not
impact the current design bases. The
proposed change enables the use of new
methodologies to re-analyze certain events.
Revised analyses may either result in
continued conformance with design bases, or
may change the design bases. If design basis
changes result from a revised analysis, then
the specific design changes will be evaluated
in accordance with HBRSEP, Unit No. 2,
design change procedures and 10 CFR 50.59.
The proposed change does not involve
physical changes to any plant structure,
system, or component. Therefore, the
probability of occurrence for a previously
analyzed accident is not significantly
increased.
The consequences of a previously analyzed
accident are dependent on the initial
conditions assumed for the analysis, the
behavior of the fission product barriers
during the analyzed accident, the availability
and successful functioning of the equipment
assumed to operate in response to the
analyzed event, and the setpoints at which
these actions are initiated. The proposed
methodologies will ensure that the plant
continues to meet applicable design and
safety analyses acceptance criteria. The
proposed change does not affect the
performance of any equipment used to
mitigate the consequences of an analyzed
accident. As a result, no analysis
assumptions are impacted and there are no
adverse effects on the factors that contribute
to offsite or onsite dose as a result of an
accident. The proposed change does not
affect setpoints that initiate protective or
mitigative actions. The proposed change
ensures that plant structures, systems, and
components are maintained consistent with
the safety analysis and licensing bases. Based
on this evaluation, there is no significant
increase in the consequences of a previously
analyzed accident.
Therefore, this change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. The Proposed Change Does Not Create
the Possibility of a New or Different Kind of
Accident From Any Previously Evaluated.
The proposed change does not involve any
physical alteration of plant systems,
structures, or components, other than
allowing for fuel design in accordance with
NRC-approved methodologies. No new or
different equipment is being installed. No
installed equipment is being operated in a
different manner. There is no change to the
parameters within which the plant is
normally operated or in the setpoints that
initiate protective or mitigative actions. As a
result, no new failure modes are being
introduced. Therefore, the proposed change
does not create the possibility of a new or
different kind of accident from any accident
previously evaluated.
3. The Proposed Change Does Not Involve
a Significant Reduction in the Margin of
Safety.
There is no impact on any margin of safety
resulting from the incorporation of these new
topical reports into the Technical
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Specifications. If design basis changes result
from a revised analysis that uses these new
methodologies, the specific design changes
will be evaluated in accordance with
HBRSEP, Unit No. 2, design change
procedures and 10 CFR 50.59. Any potential
reduction in the margin of safety would be
evaluated for that specific design change.
Therefore, this change does not involve a
significant reduction in the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Branch Chief: L. Raghavan.
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Carolina Power & Light Company,
Docket No. 50–261, H. B. Robinson
Steam Electric Plant, Unit No. 2,
Darlington County, South Carolina
Date of amendment request: July 17,
2006.
Description of amendment request:
The proposed amendment would revise
the containment pressure requirements
specified in Surveillance Requirements
3.6.8 and 5.5.16 due to a revision in the
Loss-of-Coolant Accident (LOCA)
containment pressure analysis.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
No. The proposed change does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated. The revised post-LOCA
containment pressure and temperature
analysis used more conservative assumptions
and the increase in the calculated peak
pressure was approximately 1 psig. The
revised value of 41.49 psig remains less than
the containment design pressure of 42 psig.
The increase in the calculated peak
temperature was approximately 2 °F, which
was analyzed to have no impact on structures
or equipment. Although there is an increase
in the calculated pressure, the allowable
containment leakage rate, as measured at the
peak pressure, is not being changed. Since
there is no increase in the allowable leakage,
there is no increase in consequences. The
proposed change is related to containment
pressure analysis. There are no physical
changes being made to the plant, or to the
manner in which the plant is operated.
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Surveillance procedures for containment
leakage have been conservatively testing at
pressures in excess of 42 psig and
surveillance procedures for the Isolation
Valve Seal Water System have been
conservatively testing at pressures in excess
of 46.2 psig. The change can have no impact
on the probability of an accident occurring.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any previously evaluated?
No. The proposed change does not create
the possibility of a new or different kind of
accident from any previously evaluated.
There are no physical changes being made to
the plant or to the manner in which the plant
is operated. Surveillance procedures for
containment leakage have been
conservatively testing at pressures in excess
of 42 psig and surveillance procedures for the
Isolation Valve Seal Water System have been
conservatively testing at pressures in excess
of 46.2 psig. The revised containment
analysis results in a calculated peak
containment pressure that remains less than
the containment design pressure. The
increase in the calculated peak temperature
was analyzed to have no impact on structures
or equipment. Therefore, this change does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Do the proposed changes involve a
significant reduction in the margin of safety?
No. The proposed change does not involve
a significant reduction in the margin of
safety. The proposed change imposes more
conservative surveillance test requirements.
The calculated increase in post-LOCA peak
containment pressure is only 1 psig and the
revised value of 41.49 psig remains less than
the containment design pressure of 42 psig.
The increase in the calculated peak
temperature was approximately 2 °F, which
was analyzed to have no impact on structures
or equipment. Although there was an
increase in the calculated pressure, the
allowable containment leakage rate, as
measured at the peak pressure, is not being
changed. Therefore, this change does not
involve a significant reduction in any margin
of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Branch Chief: L. Raghavan.
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51225
Detroit Edison Company, Docket No.
50–341, Fermi 2, Monroe County,
Michigan
Date of amendment request: July 12,
2006.
Description of amendment request:
The proposed amendment would
modify Conditions, Required Actions
and Completion Times associated with
the inoperability of one or more
emergency diesel generators (EDGs) in
Technical Specification (TS) 3.8.1.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed change does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated.
This license amendment request proposes
a change to extend the Technical
Specification 3.8.1, ‘‘AC Sources-Operating,’’
Completion Time. This change allows a
single EDG to be inoperable for 7 days more
than Technical Specification 3.8.1 currently
provides. The Required Actions for CTG
[Combustion Turbine Generator] 11–1 are
also removed from Condition A and TSTF
[Technical Specification Task Force] -439 is
implemented for TS 3.8.1, removing the
second Completion Times.
The EDGs are safety related components
which provide backup electrical power
supply to the onsite ESF [Engineered Safety
Feature] power distribution system. CTG 11–
1 provides backup electrical power to the
Division 1 power distribution system.
Neither the EDGs nor CTG 11–1 are accident
initiators, thus these changes do not increase
the probability of a previously evaluated
accident.
The plant ESF power distribution systems
consist of two divisions for 100%
redundancy. Accident analyses demonstrate
that only one division is required for
accident mitigation. Thus, with one division
inoperable the other division is capable of
performing the required safety function.
Design basis analyses are not required to be
performed assuming extended loss of all
power supplies to the plant ESF power
distribution system. Thus, this change does
not involve a significant increase in the
consequences of a previously analyzed
accident.
The proposed change also eliminates the
second Completion Time from TS 3.8.1.
These second Completion Times are not an
initiator to any accident previously
evaluated. As a result, the probability of an
accident previously evaluated is not affected.
The consequences of an accident during the
revised Completion Times are no different
than the consequences of the same accident
during the existing Completion Times. As a
result, the consequences of an accident
previously evaluated are not affected by this
change. Therefore, the proposed change does
not involve a significant increase in the
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probability or consequences of an accident
previously evaluated.
2. The proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
The changes do not involve a physical
alteration of the plant (i.e., no new or
different type of equipment will be installed)
or a change in the methods governing normal
plant operation. The changes do not alter any
assumptions made in the safety analysis.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. The change does not involve a
significant reduction in the margin of safety.
This license amendment request proposes
Technical Specification changes to extend
the Technical Specification 3.8.1, ‘‘AC
Sources-Operating,’’ Completion Time for an
inoperable EDG to 14 days. These changes
allow an emergency diesel generator to be
inoperable for 7 days more than TS 3.8.1
currently provides.
Deterministic and probabilistic risk
assessments evaluated the effect of the
proposed TS changes on the availability of an
electrical power supply to the plant
emergency safeguards features systems.
These assessments concluded that the
proposed TS changes do not involve a
significant increase in the risk of power
supply unavailability.
This license amendment request proposes
TS changes to remove the Required Actions
for CTG 11–1 from TS 3.8.1 Condition A. If
CTG 11–1 is inoperable at the same time that
any single EDG is inoperable for the entire
proposed 14 day period with no other
equipment in maintenance, the risk remains
within RG [Regulatory Guide] 1.174
(Reference 2 [in the application]) thresholds
for a ‘‘very small’’ classification.
The proposed change to delete the second
Completion Time does not alter the manner
in which safety limits, limiting safety system
settings, or limiting conditions for operation
are determined. The safety analysis
acceptance criteria are not affected by this
change. The proposed changes will not result
in plant operation in a configuration outside
of the design basis.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David G.
Pettinari, Legal Department, 688 WCB,
Detroit Edison Company, 2000 2nd
Avenue, Detroit, Michigan 48226–1279.
NRC Acting Branch Chief: Martin
Murphy.
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Dominion Nuclear Connecticut, Inc.,
Docket No. 50–336, Millstone Power
Station, Unit No. 2, (MPS2) New London
County, Connecticut
Date of amendment request: June 13,
2006.
Description of amendment request:
The proposed amendment would allow
changes to the Technical Specifications
based on the radiological dose analysis
margins obtained by using an alternate
source term consistent with 10 CFR
50.67.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Involve a significant increase in the
probability or consequences of an accident
previously evaluated?
No.
The proposed amendment does not involve
a significant increase in the probability or
consequence of an accident previously
analyzed. The MPS2 control room emergency
ventilation system only functions following
the initiation of a design basis radiological
accident. Therefore, the change to the value
used for in-leakage rate test acceptance
criteria following a design basis accident will
not increase the probability of any previously
analyzed accident. The proposed 200 cfm
control room habitability envelope inleakage
surveillance acceptance criteria has no
adverse impact on control room habitability
analyses for postulated toxic chemical release
events. These habitability analyses do not
credit automatic or manual isolation of the
control room fresh air ventilation flow during
a toxic chemical release event. The control
room’s forced ventilation fresh air exchange
rate (e.g., 800 cfm) is much greater than the
proposed 200 cfm envelope inleakage rate
acceptance criteria. The MPS2 containment
purge valve isolation signal is not credited in
the accident analyses. The requirements
contained in this specification do not meet
any of 10 CFR 50.36(c)(2)(ii) criteria on items
for which technical specifications must be
established. Deletion of this technical
specification will not increase the probability
of any previously analyzed accident. The
MPS2 containment and the containment
systems function to prevent or control the
release of radioactive fission products
following a postulated accident. Therefore,
the change to the value used for primary to
secondary leak rate acceptance criteria, and
for all secondary containment bypass leakage
paths following a design basis accident, will
not increase the probability of any previously
analyzed accident.
These systems are not initiators of any
design bases accident. Revised dose
calculations, which take into account the
changes proposed by this amendment and
the use of the alternative source term, have
been performed for the MPS2 design basis
radiological accidents. The results of these
revised calculations indicate that public and
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control room doses will not exceed the limits
specified in 10 CFR 50.67 and Regulatory
Guide 1.183. There is not a significant
increase in predicted dose consequences for
any of the analyzed accidents. Therefore, the
proposed changes do not involve a
significant increase in the consequences of
any previously analyzed accident.
2. Create the possibility of a new or
different kind of accident from any accident
previously evaluated?
No.
The implementation of the proposed
changes does not create the possibility of an
accident of a different type than was
previously evaluated in the UFSAR.
Although the proposed changes could affect
the operation of the control room emergency
ventilation system, and the containment and
containment systems following a design basis
radiological accident, none of these changes
can initiate a new or different kind of
accident since they are only related to system
capabilities that provide protection from
accidents that have already occurred. These
changes do not alter the nature of events
postulated in the UFSAR nor do they
introduce any unique precursor mechanisms.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from those previously
analyzed.
3. Involve a significant reduction in the
margin of safety?
No.
The implementation of the proposed
changes does not reduce the margin of safety.
The proposed changes for the control room
ventilation system, and the containment and
containment systems do not affect the ability
of these systems to perform their intended
safety functions to maintain dose less than
the required limits during design basis
radiological events. The radiological analysis
results, when compared with the revised
TEDE [total effective dose equivalent]
acceptance criteria, meet the applicable
limits. These acceptance criteria have been
developed for application to analyses
performed with alternative source terms.
These acceptance criteria have been
developed for the purpose of use in design
basis accident analyses such that meeting the
stated limits demonstrates adequate
protection of public health and safety. It is
thus concluded that the margin of safety will
not be reduced by the implementation of the
changes.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Lillian M.
Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc.,
Rope Ferry Road, Waterford, CT 06385.
NRC Acting Branch Chief: Brooke D.
Poole.
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Dominion Nuclear Connecticut, Inc.,
Docket No. 50–423, Millstone Power
Station, Unit No. 3, New London
County, Connecticut
Date of amendment request: July 19,
2006.
Description of amendment request:
The proposed amendment will revise
reactor core safety limits Technical
Specifications (TSs) and relocate the
reactor core safety limit figure to the
Core Operating Limits Report (COLR) in
the Millstone Power Station, Unit 3,
Technical Requirements Manual.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
Criterion 1:
Does the proposed amendment involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The relocation of cycle-specific core
operating limits from the TS to the COLR and
the addition of the RCS [reactor coolant
system] total flow rate to the COLR has no
influence or impact on the probability or
consequences of a design basis accident.
Adherence to the COLR and methodologies
acceptable for establishing COLR parameters
continues to be controlled by TS. The
proposed amendment still requires exactly
the same actions to be taken when or if limits
are exceeded. Each accident analysis
addressed in the final safety analysis report
(FSAR) will be examined with respect to
changes in cycle-dependent parameters,
which are obtained from application of the
NRC-approved reload design methodologies,
to ensure that the transient evaluation of new
core designs are bounded by previously
accepted analyses. This examination, which
will be performed in accordance with the
requirements of 10 CFR 50.59, ensures that
future core designs will not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
Criterion 2:
Does the proposed amendment create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The relocation and addition of the cyclespecific variables to the COLR and adding
new document references in TS Section
6.9.1.6.b does not influence or impact, nor
does it contribute in any way to the
probability or consequences of an accident.
No safety-related equipment, safety function,
or plant operations will be altered as a result
of these proposed changes. The cycle-specific
variables are calculated using NRC-approved
methods and submitted to the NRC to allow
the staff to continue to trend the values of
these limits. The TS will continue to require
operation within the required core operating
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Jkt 208001
limits and appropriate actions will be taken
when or if limits are exceeded. Therefore the
proposed amendment does not in any way
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
Criterion 3:
Does the proposed amendment involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes have no impact on
plant equipment operation. The proposed
changes do not revise any setpoints or
acceptance criteria assumed in the accident
analyses. Therefore, the proposed changes
will not result in a reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Lillian M.
Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc.,
Rope Ferry Road, Waterford, CT 06385.
NRC Acting Branch Chief: Brooke D.
Poole.
Entergy Nuclear Operations, Inc.,
Docket No. 50–247, Indian Point
Nuclear Generating Unit No. 2 (IP2),
Westchester County, New York
Date of amendment request: July 10,
2006.
Description of amendment request:
Energy Nuclear Operations, Inc., is
planning to operate an Independent
Spent Fuel Storage Installation (ISFSI)
facility at IP2 using the HOLTEC HISTORM 100 Cask System. To support
this activity, the proposed amendment
adds Spent Fuel Cask loading
requirements to IP2 Technical
Specifications (TSs).
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change will revise the Indian
Point Unit 2 TSs associated with the SFP
[spent fuel pool] to assure that the regulatory
requirements related to criticality in the SFP
and applied to the Holtec HI-STORM 100
Multi-Purpose Canister MPC–32 when in the
SFP are reflected in the IP2 TS. The proposed
change does not require any physical changes
to Part 50 structures, systems, or
components, nor will their performance
requirements be altered. Therefore, the
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51227
response of the plant to previously analyzed
accidents and related radiological releases
will not be adversely impacted, and will
bound those postulated during cask loading
activities in the cask storage area.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
Existing fuel handling procedures and
associated administrative controls remain
applicable for cask loading operations within
the SFP. Additionally, the soluble boron
concentration required to maintain keff ≤
0.95 for postulated criticality accidents
associated with cask loading operations was
also evaluated. The results of the analyses,
using a methodology previously approved by
the NRC [Nuclear Regulatory Commission],
demonstrate that the amount of soluble boron
required to compensate for the positive
reactivity associated with these postulated
accidents (371 ppm [parts per million])
remains well below the existing spent fuel pit
minimum boron concentration limit of 2000
ppm. Accordingly, the same limit has been
proposed for cask loading operations in the
cask storage area.
Therefore, the possibility of a new or
different kind of accident from any accident
previously evaluated is not created.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
An NRC approved methodology was used
to perform the criticality analysis which
provides the basis to incorporate a new
family of burnup versus enrichment curves,
for various cooling times, into the plant
Technical Specifications to ensure criticality
requirements are met during spent fuel cask
loading. Accordingly, the existing minimum
boron concentration limit for the spent fuel
pit of 2000 ppm will continue to remain
bounding during cask loading operations.
This determination accounts for uncertainties
at a 95 percent probability, 95 percent
confidence level. Should it be postulated that
a boron dilution event does occur during this
time period, keff will remain less than 1.0
should the cask storage area become fully
flooded with unborated water.
Therefore, there will not be a
significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John Fulton,
Assistant General Counsel, Entergy
Nuclear Operations, Inc., 440 Hamilton
Avenue, White Plains, NY 10601.
NRC Branch Chief: Richard J. Laufer.
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Exelon Generation Company, LLC,
Docket No. 50–249, Dresden Nuclear
Power Station (DNPS), Unit 3, Grundy
County, Illinois
Date of amendment request: July 21,
2006.
Description of amendment request:
The proposed amendment would revise
the values of the safety limit minimum
critical power ratio (SLMCPR) in
Technical Specification Section 2.1.1,
‘‘Reactor Core SLs [Safety Limits].’’
Specifically, the proposed change
would require that for Unit 3, the
minimum critical power ratio (MCPR)
for Global Nuclear Fuel fuel shall be ≥
1.10 for two recirculation loop
operation, or ≥ 1.11 for single
recirculation loop operation.
Additionally, the proposed change
would require that MCPR for
Westinghouse fuel shall be ≥ 1.12 for
two recirculation loop operation, or ≥
1.14 for single recirculation loop
operation.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The probability of an evaluated accident is
derived from the probabilities of the
individual precursors to that accident. The
consequences of an evaluated accident are
determined by the operability of plant
systems designed to mitigate those
consequences. Limits have been established
consistent with NRC [Nuclear Regulatory
Commission]-approved methods to ensure
that fuel performance during normal,
transient, and accident conditions is
acceptable. The proposed change
conservatively establishes the SLMCPR for
DNPS, Unit 3, Cycle 20 such that the fuel is
protected during normal operation and
during plant transients or anticipated
operational occurrences (AOOs).
Changing the SLMCPR does not increase
the probability of an evaluated accident. The
change does not require any physical plant
modifications, physically affect any plant
components, or entail changes in plant
operation. Therefore, no individual
precursors of an accident are affected.
The proposed change revises the SLMCPR
to protect the fuel during normal operation
as well as during plant transients or AOOs.
Operational limits will be established based
on the proposed SLMCPR to ensure that the
SLMCPR is not violated. This will ensure
that the fuel design safety criterion (i.e., that
at least 99.9% of the fuel rods do not
experience transition boiling during normal
operation and AOOs) is met. Since the
proposed change does not affect operability
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of plant systems designed to mitigate any
consequences of accidents, the consequences
of an accident previously evaluated are not
expected to increase.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
Creation of the possibility of a new or
different kind of accident requires creating
one or more new accident precursors. New
accident precursors may be created by
modifications of plant configuration,
including changes in allowable modes of
operation. The proposed change does not
involve any plant configuration
modifications or changes to allowable modes
of operation. The proposed change to the
SLMCPR assures that safety criteria are
maintained for DNPS, Unit 3, Cycle 20.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The SLMCPR provides a margin of safety
by ensuring that at least 99.9% of the fuel
rods do not experience transition boiling
during normal operation and AOOs if the
MCPR limit is not violated. The proposed
change will ensure the current level of fuel
protection is maintained by continuing to
ensure that at least 99.9% of the fuel rods do
not experience transition boiling during
normal operation and AOOs if the MCPR
limit is not violated. The proposed SLMCPR
values were developed using NRC-approved
methods. Additionally, operational limits
will be established based on the proposed
SLMCPR to ensure that the SLMCPR is not
violated. This will ensure that the fuel design
safety criterion (i.e., that no more than 0.1%
of the rods are expected to be in boiling
transition if the MCPR limit is not violated)
is met.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Bradley J.
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
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FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–440,
Perry Nuclear Power Plant, Unit 1
(PNPP), Lake County, Ohio
Date of amendment request: June 6,
2006.
Description of amendment request:
The proposed amendment would revise
the Ventilation Filter Test Program
(VFTP) in Technical Specification (TS)
5.5.7. The license amendment is a
corrective action to revise the flow rate
units specified in the VFTP from
standard cubic feet per minute to cubic
feet per minute. This amendment will
ensure the PNPP TS are consistent with
plant design documentation, testing
criteria, and the industry.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response:
The ESF [Engineered Safety Feature]
Ventilation systems reduce the concentration
of airborne radioactive contaminants
following a design basis accident and
therefore are not initiators of design bases
accidents. The proposed amendment does
not change the manner in which the ESF
ventilation systems are operated or tested.
Implementation of the proposed amendment
will ensure the ESF ventilation systems
perform their function when called upon and
does not affect the plant operations, design
function or analysis that verifies the
capability of a [plant] structures, systems or
components.
The proposed amendment does not affect
the design of the ESF ventilation systems, the
operational characteristics of the ESF
ventilation systems, the interfaces between
the ESF ventilation systems and those plant
systems they support, or the reliability of the
ESF ventilation systems.
Therefore, the ESF ventilation systems will
be capable of performing their accident
mitigation function and there is no increase
in the probability or consequences of an
accident already evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response:
The proposed amendment introduces no
new mode of plant operation and does not
involve a physical modification to the plant.
New equipment is not installed with the
proposed amendment, nor does the proposed
amendment cause existing equipment to be
operated in a new or different manner.
Since the proposed changes do not involve
a change to the plant design or operation, no
new system interactions are created by this
change. The proposed amendment does not
produce any parameters or conditions that
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could contribute to the initiation of accidents
different from those already evaluated in the
Updated Safety Analysis Report.
The changes to the VFTP do not affect the
assumed accident performance of the ESF
Ventilation systems, nor [sic] any plant
structure, system or component previously
evaluated.
Therefore, the proposed amendment does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response:
The proposed amendment does not impact
the ESF ventilation systems performance,
including the capability for each ESF
ventilation system to attain and maintain
required air flow assumed in the plant safety
analysis.
The proposed amendment does not involve
a significant reduction in a margin of safety
since the operability of the ESF ventilations
[sic] systems continues to be determined as
required to support the capability of the ESF
ventilations [sic] systems to provide the
required ventilation, filtration and
temperature control to mitigate the
consequences of an accident.
jlentini on PROD1PC65 with NOTICES
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David W.
Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street,
Akron, OH 44308.
NRC Branch Chief: Daniel S. Collins.
Florida Power Corporation, et al.,
Docket No. 50–302, Crystal River Unit 3
Nuclear Generating Plant, Citrus
County, Florida
Date of amendment request: May 25,
2006.
Description of amendment request:
The proposed license amendment
revises the requirements in the Crystal
River Unit 3 Improved Technical
Specification related to steam generator
tube integrity. The licensee states that
the changes are consistent with NRCapproved Technical Specification (TS)
Task Force (TSTF) Change Traveler,
TSTF–449, ‘‘Steam Generator Tube
Integrity,’’ Revision 4. The availability
of this technical specification
improvement was announced in the
Federal Register on May 6, 2005, as part
of the consolidated line item
improvement process.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
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Criterion 1—The Proposed Change Does Not
Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated
The proposed change requires a SG [Steam
Generator] Program that includes
performance criteria that will provide
reasonable assurance that the SG tubing will
retain integrity over the full range of
operating conditions (including startup,
operation in the power range, hot standby,
cooldown and all anticipated transients
included in the design specification). The SG
performance criteria are based on tube
structural integrity, accident induced
leakage, and operational LEAKAGE.
A SGTR [steam generarator tube rupture]
event is one of the design basis accidents that
are analyzed as part of a plant’s licensing
basis. In the analysis of a SGTR event, a
bounding primary to secondary LEAKAGE
rate equal to the operational LEAKAGE rate
limits in the licensing basis plus the
LEAKAGE rate associated with a doubleended rupture of a single tube is assumed.
For other design basis accidents such as
MSLB [main steamline break], rod ejection,
and reactor coolant pump locked rotor the
tubes are assumed to retain their structural
integrity (i.e., they are assumed not to
rupture). These analyses typically assume
that primary to secondary LEAKAGE for all
SGs is 1 gallon per minute or increases to 1
gallon per minute as a result of accident
induced stresses. The accident induced
leakage criterion introduced by the proposed
changes accounts for tubes that may leak
during design basis accidents. The accident
induced leakage criterion limits this leakage
to no more than the value assumed in the
accident analysis.
The SG performance criteria proposed
change to the TS identify the standards
against which tube integrity is to be
measured. Meeting the performance criteria
provides reasonable assurance that the SG
tubing will remain capable of fulfilling its
specific safety function of maintaining
reactor coolant pressure boundary integrity
throughout each operating cycle and in the
unlikely event of a design basis accident. The
performance criteria are only a part of the SG
Program required by the proposed change to
the TS. The program, defined by NEI
[Nuclear Energy Institute] 97–06, Steam
Generator Program Guidelines, includes a
framework that incorporates a balance of
prevention, inspection, evaluation, repair,
and leakage monitoring. The proposed
changes do not, therefore, significantly
increase the probability of an accident
previously evaluated.
The consequences of design basis accidents
are, in part, functions of the DOSE
EQUIVALENT 1–131 in the primary coolant
and the primary to secondary LEAKAGE
rates resulting from an accident. Therefore,
limits are included in the plant technical
specifications for operational leakage and for
DOSE EQUIVALENT 1–131 in primary
coolant to ensure the plant is operated within
its analyzed condition. The typical analysis
of the limiting design basis accident assumes
that primary to secondary leak rate after the
accident is 1 gallon per minute with no more
than [500 gallons per day or 720 gallons per
PO 00000
Frm 00047
Fmt 4703
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51229
day] in any one SG, and that the reactor
coolant activity levels of DOSE
EQUIVALENT 1–131 are at the TS values
before the accident.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary coolant chemistry controls. The
proposed approach updates the current TSs
and enhances the requirements for SG
inspections. The proposed change does not
adversely impact any other previously
evaluated design basis accident and is an
improvement over the current TSs.
Therefore, the proposed change does not
affect the consequences of a SGTR accident
and the probability of such an accident is
reduced. In addition, the proposed changes
do not affect the consequences of an MSLB,
rod ejection, or a reactor coolant pump
locked rotor event, or other previously
evaluated accident.
Criterion 2—The Proposed Change Does Not
Create the Possibility of a New or Different
Kind of Accident from any Previously
Evaluated
The proposed performance based
requirements are an improvement over the
requirements imposed by the current
technical specifications. Implementation of
the proposed SG Program will not introduce
any adverse changes to the plant design basis
or postulated accidents resulting from
potential tube degradation. The result of the
implementation of the SG Program will be an
enhancement of SG tube performance.
Primary to secondary LEAKAGE that may be
experienced during all plant conditions will
be monitored to ensure it remains within
current accident analysis assumptions.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary or secondary coolant chemistry
controls. In addition, the proposed change
does not impact any other plant system or
component. The change enhances SG
inspection requirements.
Therefore, the proposed change does not
create the possibility of a new or different
type of accident from any accident
previously evaluated.
Criterion 3—The Proposed Change Does Not
Involve a Significant Reduction in the Margin
of Safety
The SG tubes in pressurized water reactors
are an integral part of the reactor coolant
pressure boundary and, as such, are relied
upon to maintain the primary system’s
pressure and inventory. As part of the reactor
coolant pressure boundary, the SG tubes are
unique in that they are also relied upon as
a heat transfer surface between the primary
and secondary systems such that residual
heat can be removed from the primary
system. In addition, the SG tubes isolate the
radioactive fission products in the primary
coolant from the secondary system. In
summary, the safety function of an SG is
maintained by ensuring the integrity of its
tubes.
Steam generator tube integrity is a function
of the design, environment, and the physical
condition of the tube. The proposed change
does not affect tube design or operating
environment. The proposed change is
expected to result in an improvement in the
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tube integrity by implementing the SG
Program to manage SG tube inspection,
assessment, repair, and plugging. The
requirements established by the SG Program
are consistent with those in the applicable
design codes and standards and are an
improvement over the requirements in the
current TSs.
For the above reasons, the margin of safety
is not changed and overall plant safety will
be enhanced by the proposed change to the
TS.
The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Branch Chief: L. Raghavan.
jlentini on PROD1PC65 with NOTICES
Nuclear Management Company, LLC,
Docket No. 50–266, Point Beach Nuclear
Plant (PBNP), Unit 1, Town of Two
Creeks, Manitowoc County, Wisconsin
Date of amendment request: July 11,
2006.
Description of amendment request:
The proposed amendment would revise
Technical Specification (TS) 5.5.8,
‘‘Steam Generator (SG) Program,’’ to
exclude the portion of the tube below 17
inches from the top of the tubesheet
from the SG tube inspection
requirements for Unit 1 on a one-time
basis for a single operating cycle. In
addition, administrative changes are
proposed to correct a page number in
the TS table of contents and delete two
blank pages in TS Section 5.
Basis for proposed no significant
hazards consideration determination:
As required by 10CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below.
1. Operation of the Point Beach Nuclear
Plant in accordance with the proposed
amendments does not result in a significant
increase in the probability or consequences
of any accident previously evaluated.
The proposed change revises Technical
Specification (TS) 5.5.8, ‘‘Steam Generator
(SG) Program’’ to redefine the PBNP Unit 1
primary pressure boundary for purposes of
the SG tube inspection requirements on a
one-time basis for Unit 1 Refueling Outage 30
and the subsequent operating cycle. The
redefined primary pressure boundary is
relocated from the seal weld at the bottom of
the SG tube to the tube-to-tubesheet
mechanical interface. The required structural
integrity margins of the SG tubes in this area
are unaffected by this change and will be
maintained by the SG tubesheet. SG tubes are
hydraulically expanded into the tubesheet.
Steam generator tube rupture is constrained
by the tubesheet for tubes with cracks in the
tubesheet. This constraint results from the
hydraulic expansion process which restricts
further expansion of the tube, thermal
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Jkt 208001
expansion mismatch between the tube and
tubesheet and from the differential pressure
between the primary and secondary side.
Thermal expansion and differential pressure
also restrain the tube axially. For
conservatism, hydraulic preload was not
factored into the analysis.
The proposed change continues to require
that the SG Program include performance
criteria that will provide reasonable
assurance that the SG tubing will retain
integrity over the full range of operating
conditions (including startup, operation in
the power range, hot standby, cooldown and
all anticipated transients included in the
design specification).
The SG performance criteria are based on
tube structural integrity, accident induced
leakage, and operational LEAKAGE. The
analysis shows that structural integrity
retains acceptable safety factors against burst
under normal steady state full power
operation primary-to-secondary pressure
differential and against burst applied to the
design basis accident primary-to-secondary
pressure differentials. The analysis also
shows that accident induced leakage is
bound by twice the normal operating leakage
and well below the accident analysis
assumption for each stream generator. The
primary to secondary operational LEAKAGE
limit is not changed.
The planned inspection and supporting
analysis provide reasonable assurance that
the SG tubing will remain capable of
fulfilling its specific safety function of
maintaining reactor coolant pressure
boundary integrity throughout the operating
cycle and in the unlikely event of a design
basis accident. The proposed change does
not, therefore, significantly increase the
probability of an accident previously
evaluated.
The consequences of design basis accidents
are, in part, functions of the DOSE
EQUIVALENT I–131 in the primary coolant
and the primary to secondary LEAKAGE
rates resulting from an accident. The plant
technical specification limits for operational
LEAKAGE and for DOSE EQUIVALENT I–
131 in primary coolant, which ensure the
plant is operated within its analyzed
condition, are unaffected by the proposed
change. Therefore, the proposed change does
not significantly increase the consequences
of any accident previously evaluated.
The proposed change does not significantly
affect the probability of any event initiators.
There will be no change to normal plant
operating parameters, engineered safety
feature actuation setpoints, accident
mitigation capabilities, or accident analysis
assumptions or inputs.
Therefore, the probability or consequences
of any accident previously evaluated will not
be significantly increased as a result of the
proposed change.
2. Operation of the Point Beach Nuclear
Plant in accordance with the proposed
amendments does not result in a new or
different kind of accident from any accident
previously evaluated.
Implementation of the proposed change
will not introduce any adverse changes to the
plant design basis or postulated accidents
resulting from potential tube degradation.
PO 00000
Frm 00048
Fmt 4703
Sfmt 4703
Primary to secondary leakage that may be
experienced during all plant conditions will
continue to be monitored to ensure it remains
within current accident analysis
assumptions. The proposed change does not
affect the method of operation of the SGs, or
primary or secondary coolant chemistry
controls. In addition, the proposed change
does not impact any other plant system or
component.
No new accident scenarios, transient
precursors, failure mechanisms, or limiting
single failures are introduced as a result of
the proposed change. Equipment important
to safety will continue to operate as designed.
The changes do not result in any event
previously deemed incredible being made
credible. The changes do not result in
adverse conditions or result in any increase
in the challenges to safety systems.
Therefore, the proposed change does not
create the possibility of a new or different
type of accident from any accident
previously evaluated.
3. Operation of the Point Beach Nuclear
Plant in accordance with the proposed
amendments does not result in a significant
reduction in a margin of safety.
The steam generators (SGs) are an integral
part of the reactor coolant pressure boundary
and, as such, are relied upon to maintain the
primary system’s pressure and inventory.
They are also relied upon to remove residual
heat from the primary system. The safety
function of an SG is maintained by ensuring
the integrity of its tubes. Steam generator
tube integrity is a function of the design,
environment, and the physical condition of
the tube. The proposed change redefines the
PBNP Unit 1 primary pressure boundary
from the tube end weld to 17 inches below
the top of the tubesheet and incorporates
revisions to the inspection criteria for SG
tube inspection in the tubesheet. The SG
operating environment is not affected by the
change. The proposed change maintains the
required structural margins of the SG tubes
for both normal and accident conditions.
For cracking located within the tubesheet,
steam generator tube rupture is constrained
by the tubesheet. For circumferentially
oriented cracking, the associated analysis for
the proposed change validates that 17 inches
of degradation free expanded tubing provides
the necessary resistance to tube pullout with
applicable safety factors applied.
The revised inspection criteria continue to
verify SG tube integrity. The safety function
of the affected components will be
maintained with the redefined primary
pressure boundary.
There are no new or significant changes to
the initial conditions contributing to accident
severity or consequences. The proposed
amendment will not otherwise affect the
plant protective boundaries, will not cause a
release of fission products to the public, nor
will it degrade the performance of any other
structures, systems or components (SSCs)
important to safety. Therefore, the requested
change will not result in a significant
reduction in the margin of safety.
The NRC staff has reviewed the licensee’s
analysis and, based on this review, it appears
that the three standards of 10 CFR 50.92(c)
are satisfied. Therefore, the NRC staff
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jlentini on PROD1PC65 with NOTICES
proposes to determine that the amendment
request involves no significant hazards
consideration.
Attorney for licensee: Jonathan Rogoff,
Esquire, Vice President, Counsel & Secretary,
Nuclear Management Company, LLC, 700
First Street, Hudson, WI 54016.
NRC Acting Branch Chief: Martin Murphy.
PPL Susquehanna, LLC, Docket Nos. 50–387
and 50–388, Susquehanna Steam Electric
Station, Units 1 and 2 (SSES 1 and 2),
Luzerne County, Pennsylvania
Date of amendment request: October 13,
2005.
Description of amendment request: The
proposed amendment would modify the
licensing bases of SSES 1 and 2 by adopting
the Alternative Source Term (AST)
methodology which replaces the current
accident source term with an AST. The AST
is characterized by the composition and
magnitude of the radioactive material, the
chemical and physical form of the
radionuclides, and the timing of the releases
of these radionuclides. The exceptions would
be that the current Technical Information
Document (TID)14844 accident source term
would remain the licensing basis for (1)
equipment qualification, (2) NUREG–0737
evaluations other than Control Room
Habitability Envelope (CRHE) doses, and (3)
Final Safety Analysis Report (FSAR)
accidents not included in Regulatory Guide
1.183.
Basis for proposed no significant hazards
consideration determination: As required by
10 CFR 50.91(a), the licensee has provided its
analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a
significant increase in the probability of
occurrence or consequences of an accident
previously evaluated?
Response: No.
Adoption of the AST and pursuant TS
[Technical Specification] changes, changes to
the TS’s to address NRC Generic Letter 2003–
01 (Reference 12.1) [see application dated
October 13, 2005] and the changes to the
atmospheric dispersion factors, have no
impact to the initiation of DBAs [design basis
accidents]. Once the occurrence of an
accident has been postulated, the new
accident source term and atmospheric
dispersion factors are an input to analyses
that evaluate the radiological consequences.
Some of the proposed changes do affect the
design or manner in which the facility is
operated following an accident; however, the
proposed changes do not involve a revision
to the design or manner in which the facility
is operated that could increase in the
probability of an accident previously
evaluated of a DBA discussed in Chapter 15
of the FSAR.
Therefore, the proposed change does not
involve an increase in the probability of an
accident previously evaluated.
The structures, systems and components
affected by the proposed changes act as
mitigators to the consequences of accidents.
Based on the revised analyses, the proposed
changes do revise certain performance
requirements; however, the proposed
changes do not involve a revision to the
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17:07 Aug 28, 2006
Jkt 208001
parameters or conditions that could
contribute to the initiation of a DBA
discussed in Chapter 15 of the FSAR.
Plant-specific radiological analyses have
been performed using the AST methodology
and new atmospheric dispersion factors.
Based on the results of these analyses, it had
been demonstrated that the CRHE dose
consequences of the limiting events
considered in the analyses meet the
regulatory guidance provided for use with
the AST, and the offsite doses are well within
acceptable limits. This guidance is presented
in 10 CFR 50.67, RG [Regulatory Guide]
1.183, and Standard Review Plan [SRP]
Section 15.0.1.
Therefore, the proposed amendment does
not result in a significant increase in the
consequences of any previously evaluated
accident.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
Implementation of AST and the associated
proposed TS changes and new atmospheric
dispersion factors do not alter or involve any
design basis accident initiators. These
changes do not affect the design function or
mode of operation of structures, systems and
components in the facility prior to a
postulated accident. Since structures,
systems and components are operated
essentially no differently after the AST
implementation, no new failure modes are
created by this proposed change.
Licensing basis changes are proposed and
justified to credit use of the SLC [Standby
Liquid Control] System to buffer suppression
pool pH to prevent iodine re-evolution
following a postulated design basis loss of
coolant accident. There are new required
manual operator actions associated with the
SLC System that are not currently considered
in the SSES design basis. Operator training
will be updated to reflect the new manual
operator actions for the pH control function
of the of the SLC System as defined in the
TS Section 3.1.7. These changes are not
significant because the operators are already
trained for the operation of the SLC System.
Procedural changes are mostly limited to the
timing of SLC initiation and termination. In
addition, no new hardware changes are
necessary to use SLC in this new functional
mode.
Licensing basis changes are proposed and
justified for the operation of the CREOASS
[control room emergency outside air supply
system] to respond to NRC Generic Letter
2003–01 and TSTF [Technical Specification
Task Force] 448. No new hardware changes
are necessary to implement these changes.
Since CREOASS will not be operated
differently as a result of these changes, no
new failure modes are created by these
changes.
Therefore, the proposed license
amendment will not create the possibility of
a new or different kind of accident from any
accident previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The results of the accident analyses revised
in support of the proposed change are subject
PO 00000
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Fmt 4703
Sfmt 4703
51231
to the acceptance criteria in 10 CFR 50.67.
The analyzed events have been carefully
selected, and the analyses supporting these
changes have been performed using approved
methodologies to ensure that analyzed events
are bounding and safety margin has not been
reduced. The dose consequences of these
limiting events are within the acceptance
criteria presented in 10 CFR 50.67, RG 1.183,
and SRP 15.0.1. Thus, by meeting the
applicable regulatory limits for AST, there is
no significant reduction in a margin of safety.
Changes to the SLC System to credit use of
the Standby Liquid Control (SLC) System to
buffer suppression pool pH to prevent iodine
re-evolution and the CREOASS to address
NRC Generic Letter 2003–01 and TSTF–448
[to] improve the margin of safety.
New offsite and Control Room atmospheric
dispersion factors (X/Qs) based on site
specific meteorological data, calculated in
accordance with the guidance of RGs 1.145
and 1.194, utilizes more recent data and
improved calculational methodologies.
Therefore, because the proposed changes
continue to result in dose consequences
within the applicable regulatory limits, the
changes are considered to not result in a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Bryan A. Snapp,
Esquire, Assoc. General Counsel, PPL
Services Corporation, 2 North Ninth St.,
GENTW3, Allentown, PA 18101–1179.
NRC Branch Chief: Richard J. Laufer.
PSEG Nuclear LLC, Docket Nos. 50–272
and 50–311, Salem Nuclear Generating
Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of amendment request: June 7,
2006.
Description of amendment request:
The proposed amendment would delete
Technical Specification (TS) 3/4.6.4,
‘‘Combustible Gas Control,’’ TS 3/
4.6.4.1, ‘‘Hydrogen Analyzers,’’ and TS
3/4.6.4.2, ‘‘Electric Hydrogen
Recombiners.’’ The changes would be
consistent with NRC-approved TS Task
Force (TSTF) Standard Technical
Specification (STS) Change Traveler
number TSTF–447, Revision 1,
‘‘Elimination of Hydrogen Recombiners
and Change to Hydrogen and Oxygen
Monitors,’’ as part of the Consolidated
Line Item Improvement Process (CLIIP).
The NRC staff issued a notice of
availability of ‘‘Model Application
Concerning Technical Specification
Improvement To Eliminate Hydrogen
Recombiner Requirement, and Relax the
Hydrogen and Oxygen Monitor
Requirements for Light Water Reactors
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Federal Register / Vol. 71, No. 167 / Tuesday, August 29, 2006 / Notices
jlentini on PROD1PC65 with NOTICES
Using the Consolidated Line Item
Improvement Process (CLIIP)’’, in the
Federal Register on September 25, 2003
(68 FR 55416). The notice included a
model safety evaluation (SE), a model
no significant hazards consideration
(NSHC) determination, and a model
application.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee presented an analysis of NSHC
by endorsing the model NSHC
determination for TSTF–447 which was
published in the Federal Register on
September 25, 2003 (68 FR 55416) as
follows:
Criterion 1—The Proposed Change Does
Not Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated.
The revised 10 CFR 50.44 no longer defines
a design-basis loss-of-coolant accident
(LOCA) hydrogen release, and eliminates
requirements for hydrogen control systems to
mitigate such a release. The installation of
hydrogen recombiners and/or vent and purge
systems required by 10 CFR 50.44(b)(3) was
intended to address the limited quantity and
rate of hydrogen generation that was
postulated from a design-basis LOCA. The
Commission has found that this hydrogen
release is not risk-significant because the
design basis LOCA hydrogen release does not
contribute to the conditional probability of a
large release up to approximately 24 hours
after the onset of core damage. In addition,
these systems were ineffective at mitigating
hydrogen releases from risk-significant
accident sequences that could threaten
containment integrity.
With the elimination of the design basis
LOCA hydrogen release, hydrogen monitors
are no longer required to mitigate designbasis accidents and, therefore, the hydrogen
monitors do not meet the definition of a
safety-related component as defined in 10
CFR 50.2. RG [Regulatory Guide] 1.97
Category 1, is intended for key variables that
most directly indicate the accomplishment of
a safety function for design-basis accident
events. The hydrogen monitors no longer
meet the definition of Category 1 in RG 1.97.
As part of the rulemaking to revise 10 CFR
50.44 the Commission found that Category 3,
as defined in RG 1.97, is an appropriate
categorization for the hydrogen monitors
because the monitors are required to
diagnose the course of beyond design-basis
accidents.
The regulatory requirements for the
hydrogen monitors can be relaxed without
degrading the plant emergency response. The
emergency response, in this sense, refers to
the methodologies used in ascertaining the
condition of the reactor core, mitigating the
consequences of an accident, assessing and
projecting offsite releases of radioactivity,
and establishing protective action
recommendations to be communicated to
offsite authorities. Classification of the
hydrogen monitors as Category 3, and
removal of the hydrogen monitors from TS
will not prevent an accident management
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17:07 Aug 28, 2006
Jkt 208001
strategy through the use of the SAMGs
[Severe Accident Management Guidelines],
the emergency plan (EP), the emergency
operating procedures (EOP), and site survey
monitoring that support modification of
emergency plan protective action
recommendations (PARs).
Therefore, the elimination of the hydrogen
recombiner requirements and relaxation of
the hydrogen monitor requirements,
including removal of these requirements
from TS, does not involve a significant
increase in the probability or the
consequences of any accident previously
evaluated.
Criterion 2—The Proposed Change Does
Not Create the Possibility of a New or
Different Kind of Accident From Any
Previously Evaluated.
The elimination of the hydrogen
recombiner requirements and relaxation of
the hydrogen monitor requirements,
including removal of these requirements
from TS, will not result in any failure mode
not previously analyzed. The hydrogen
recombiner and hydrogen monitor equipment
was intended to mitigate a design-basis
hydrogen release. The hydrogen recombiner
and hydrogen monitor equipment are not
considered accident precursors, nor does
their existence or elimination have any
adverse impact on the pre-accident state of
the reactor core or post accident confinement
of radionuclides within the containment
building.
Therefore, this change does not create the
possibility of a new or different kind of
accident from any previously evaluated.
Criterion 3—The Proposed Change Does
Not Involve a Significant Reduction in the
Margin of Safety.
The elimination of the hydrogen
recombiner requirements and relaxation of
the hydrogen monitor requirements,
including removal of these requirements
from TS, in light of existing plant equipment,
instrumentation, procedures, and programs
that provide effective mitigation of and
recovery from reactor accidents, results in a
neutral impact to the margin of safety.
The installation of hydrogen recombiners
and/or vent and purge systems required by
10 CFR 50.44(b)(3) was intended to address
the limited quantity and rate of hydrogen
generation that was postulated from a designbasis LOCA. The Commission has found that
this hydrogen release is not risk-significant
because the design-basis LOCA hydrogen
release does not contribute to the conditional
probability of a large release up to
approximately 24 hours after the onset of
core damage. Category 3 hydrogen monitors
are adequate to provide rapid assessment of
current reactor core conditions and the
direction of degradation while effectively
responding to the event in order to mitigate
the consequences of the accident. The intent
of the requirements established as a result of
the TMI, Unit 2 accident can be adequately
met without reliance on safety-related
hydrogen monitors.
Therefore, this change does not involve a
significant reduction in the margin of safety.
Removal of hydrogen monitoring from TS
will not result in a significant reduction in
their functionality, reliability, and
availability.
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Fmt 4703
Sfmt 4703
The NRC staff has reviewed the licensee’s
analysis and, based on this review, it appears
that the three standards of 10 CFR 50.92(c)
are satisfied. Therefore, the NRC staff
proposes to determine that the amendment
request involves no significant hazards
consideration.
Attorney for licensee: Jeffrie J. Keenan,
Esquire, Nuclear Business Unit—N21,
P.O. Box 236, Hancocks Bridge, NJ
08038.
NRC Acting Branch Chief: Brooke D.
Poole.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the internet at the
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Federal Register / Vol. 71, No. 167 / Tuesday, August 29, 2006 / Notices
Date of initial notice in Federal
Register: October 25, 2005 (70 FR
61656).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated August 15,
2006.
No significant hazards consideration
comments received: No.
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
Detroit Edison Company, Docket No.
50–341, Fermi 2, Monroe County,
Michigan
Date of application for amendment:
January 31, 2006, as supplemented by
letter dated July 12, 2006.
Brief description of amendment: The
amendment changed the technical
specifications to address issues related
to an inconsistency that was
inadvertently introduced during
conversion to improved technical
specifications when ‘‘1 per room’’
replaced ‘‘2’’ as the required channels
per trip system for the reactor water
cleanup area ventilation differential
temperature—high isolation function.
Date of issuance: August 7, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 90 days.
Amendment No.: 173.
Facility Operating License No. NPF–
43: Amendment revised the Technical
Specifications, Surveillance
Requirements, and License.
Date of initial notice in Federal
Register: March 14, 2006 (71 FR
13171). The July 12, 2006, supplement
contained clarifying information and
did not change the NRC staff’s initial
proposed finding of no significant
hazards consideration.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated August 7, 2006.
No significant hazards consideration
comments received: No.
jlentini on PROD1PC65 with NOTICES
Dominion Nuclear Connecticut, Inc., et
al., Docket No. 50–423, Millstone Power
Station, Unit No. 3, New London
County, Connecticut
Date of application for amendment:
September 13, 2005.
Brief description of amendment: The
amendment revised the Millstone Power
Station, Unit No. 3 Technical
Specification (TSs) temperature
requirement for the reactivity control
system rod drop time test.
Date of issuance: August 15, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment No.: 231.
Facility Operating License No. NPF–
49: The amendment revised the TSs.
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Entergy Nuclear Operations, Inc.,
Docket No. 50–293, Pilgrim Nuclear
Power Station, Plymouth County,
Massachusetts
Date of application for amendment:
May 24, 2005, revised by letter dated
May 2, 2006.
Brief description of amendment: The
Technical Specification amendment
deleted the requirements for NRC
approval of the engineering evaluation
justifying continued reactor operation
with safety relief valve (SRV) discharge
pipe temperature exceeding the limit.
Date of issuance: August 4, 2006.
Effective date: As of the date of
issuance, and shall be implemented
within 90 days.
Amendment No.: 222.
Facility Operating License No. DPR–
35: The amendment revised the Facility
Operating License and Technical
Specifications.
Date of initial notice in Federal
Register: August 16, 2005 (70 FR
48205).
The licensee originally requested for
deletion of TS 3.6.D.3 in their submittal
dated May 24, 2005. The NRC staff
found this unacceptable. Therefore, the
licensee revised the original application
by letter dated May 2, 2006, reducing
the scope of the application as originally
noticed. Hence, there is no change to the
NRC staff’s original proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated August 4, 2006.
No significant hazards consideration
comments received: No.
Entergy Operations, Inc., Docket No. 50–
382, Waterford Steam Electric Station,
Unit 3, St. Charles Parish, Louisiana
Date of amendment request: July 21,
2005, as supplemented on February 15,
May 3, and June 2, 2006.
Brief description of amendment: The
amendment modified the Waterford 3
Technical Specification (TS) to revise
the existing steam generator (SG) tube
surveillance program to be consistent
with TS Task Force (TSTF) Change
TSTF–449, ‘‘Steam Generator Tube
Integrity,’’ Revision 4, and the model
safety evaluation prepared by the NRC
and published in the Federal Register
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51233
notice on March 2, 2005 (70 FR 10298).
In this regard, the scope of the
application includes changes to the
definition of leakage, changes to the
primary-to-secondary leakage
requirements, changes to the SG tube
surveillance program, changes to the SG
reporting requirements, and associated
changes to the TS Bases.
Date of issuance: July 31, 2006.
Effective date: As of the date of
issuance and shall be implemented 90
days from the date of issuance.
Amendment No.: 204.
Facility Operating License No. NPF–
38: The amendment revised the
Technical Specifications and the
Facility Operating License.
Date of initial notice in Federal
Register: October 25, 2005 (70 FR
61659). The February 15, May 3, and
June 2, 2006, supplemental letters
contained additional information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the NRC
staff’s original proposed finding of no
significant hazards consideration.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 31, 2006.
No significant hazards consideration
comments received: No.
Entergy Operations, Inc., Docket No. 50–
382, Waterford Steam Electric Station,
Unit 3, St. Charles Parish, Louisiana
Date of amendment request: October
25, 2005.
Brief description of amendment: The
amendment modified the Waterford 3
Technical Specification 3.1.1.4,
‘‘Minimum Temperature for Criticality,’’
to raise the minimum temperature for
criticality from the current value of ≥520
°F to ≥533 °F. Changes were also
proposed to the associated Action
statement to reflect the increase in
temperature and to replace the current
statement in Surveillance Requirement
4.1.1.4 with wording consistent with
NUREG–1432, ‘‘Standard Technical
Specifications—Combustion
Engineering Plants.’’
Date of issuance: July 31, 2006.
Effective date: As of the date of
issuance and shall be implemented 30
days from the date of issuance.
Amendment No.: 205.
Facility Operating License No. NPF–
38: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: December 6, 2005 (70 FR
72672).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 31, 2006.
No significant hazards consideration
comments received: No.
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FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–346,
Davis-Besse Nuclear Power Station, Unit
1, Ottawa County, Ohio
Date of application for amendment:
May 5, 2004, as supplemented by letters
dated January 17, October 10, and
November 2, 2005 and May 30, 2006.
Brief description of amendment: This
amendment revised the technical
specifications (TSs) for instrumentation
setpoints, allowable values, and
calibration requirements based on
updated calculations and reviews, and
add a definition of ‘‘annual’’ frequency
for use in the TSs.
Date of issuance: August 9, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 120 days.
Amendment No.: 275.
Facility Operating License No. NPF–3:
Amendment revised the Technical
Specifications and License.
Date of initial notice in Federal
Register: June 8, 2004 (69 FR 32074).
The January 17, October 10, and
November 2, 2005 and May 30, 2006,
supplements contained clarifying
information and did not change the NRC
staff’s initial proposed finding of no
significant hazards consideration.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated August 9, 2006.
No significant hazards consideration
comments received: No.
jlentini on PROD1PC65 with NOTICES
Southern California Edison Company, et
al., Docket Nos. 50–361 and 50–362,
San Onofre Nuclear Generating Station,
Units 2 and 3, San Diego County,
California
Date of application for amendments:
January 28, 2005, as supplemented by
letter dated January 12, 2006.
Brief description of amendments: The
amendment revised Technical
Specifications (Tss) 1.1, ‘‘Definitions,’’
3.4, ‘‘Reactor Coolant System [RCS],’’
and 5.7, ‘‘Reporting Requirements,’’ to
relocate the RCS pressure-temperature
curves and limits from the TSs to a
licensee-controlled document identified
as the Pressure and Temperature Limit
Report.
Date of issuance: July 13, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment Nos.: Unit 2–203; Unit
3–195.
Facility Operating License Nos. NPF–
10 and NPF–15: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: March 1, 2005 (70 FR 9996).
The January 12, 2006, supplemental
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19:08 Aug 28, 2006
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letter provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated July 13, 2006.
No significant hazards consideration
comments received: No.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–424 and 50–425,
Vogtle Electric Generating Plant, Units 1
and 2, Burke County, Georgia
Date of application for amendments:
September 19, 2005, as supplemented
by letter dated June 9, 2006.
Brief description of amendments: The
amendments revised the Technical
Specifications (TSs) Limiting
Conditions for Operation 3.3.1, ‘‘Reactor
Trip System Instrumentation,’’ and TS
Surveillance Requirement (SR) 3.2.4.2,
‘‘Quadrant Power Tilt Ratio (QPTR).’’
The amendments revise TS 3.3.1,
Condition D and the note in SR 3.2.4.2
to clarify when a flux map for QTPR is
required.
Date of issuance: August 15, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 90 days from the date of
issuance.
Amendment Nos.: 143 and 123.
Facility Operating License Nos. NPF–
68 and NPF–81: Amendments revised
the licenses and the technical
specifications.
Date of initial notice in Federal
Register: March 14, 2005 (71 FR
13179). The supplement dated June 9,
2006, provided clarifying information
that did not change the scope of the
September 19, 2005, application nor the
initial proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated August 15,
2006.
No significant hazards consideration
comments received: No.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Unit Nos.
1 and 2, Somervell County, Texas
Date of amendment request: August
10, 2005.
Brief description of amendments: The
amendments revised the Technical
Specifications (TSs) to relocate diesel
fuel oil testing methods from TS 5.5.13
to a licensee-controlled document,
provided clarifications, and corrected
the format and typographical errors.
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Date of issuance: July 28, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 120 days from the date of
issuance.
Amendment Nos.: 127 and 127.
Facility Operating License Nos. NPF–
87 and NPF–89: The amendments
revised the Technical Specifications and
the Facility Operating Licenses.
Date of initial notice in Federal
Register: November 8, 2005 (70 FR
67754).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated July 28, 2006.
No significant hazards consideration
comments received: No.
Virginia Electric and Power Company, et
al., Docket Nos. 50–280 and 50–281,
Surry Power Station, Units 1 and 2,
Surry County, Virginia
Date of application for amendments:
September 13, 2005, as supplemented
on April 7 and May 23, 2006.
Brief Description of amendments:
These amendments revised Technical
Specification 5.1, ‘‘Site,’’ to redefine the
exclusion area boundary as the site
boundary.
Date of issuance: August 10, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 30 days.
Amendment Nos.: 249, 248.
Renewed Facility Operating License
Nos. DPR–32 and DPR–37: Amendments
changed the licenses and the technical
specifications.
Date of initial notice in Federal
Register: January 3, 2006 (71 FR 156).
The April 7 and May 23, 2006,
supplements contained clarifying
information only and did not change the
initial proposed no significant hazards
consideration determination or expand
the scope of the initial application.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated August 10,
2006.
No significant hazards consideration
comments received: No.
Notice of Issuance of Amendments to
Facility Operating Licenses and Final
Determination of No Significant
Hazards Consideration and
Opportunity for a Hearing (Exigent
Public Announcement or Emergency
Circumstances)
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application for the
amendment complies with the
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Federal Register / Vol. 71, No. 167 / Tuesday, August 29, 2006 / Notices
standards and requirements of the
Atomic Energy Act of 1954, as amended
(the Act), and the Commission’s rules
and regulations. The Commission has
made appropriate findings as required
by the Act and the Commission’s rules
and regulations in 10 CFR Chapter I,
which are set forth in the license
amendment.
Because of exigent or emergency
circumstances associated with the date
the amendment was needed, there was
not time for the Commission to publish,
for public comment before issuance, its
usual Notice of Consideration of
Issuance of Amendment, Proposed No
Significant Hazards Consideration
Determination, and Opportunity for a
Hearing.
For exigent circumstances, the
Commission has either issued a Federal
Register notice providing opportunity
for public comment or has used local
media to provide notice to the public in
the area surrounding a licensee’s facility
of the licensee’s application and of the
Commission’s proposed determination
of no significant hazards consideration.
The Commission has provided a
reasonable opportunity for the public to
comment, using its best efforts to make
available to the public means of
communication for the public to
respond quickly, and in the case of
telephone comments, the comments
have been recorded or transcribed as
appropriate and the licensee has been
informed of the public comments.
In circumstances where failure to act
in a timely way would have resulted, for
example, in derating or shutdown of a
nuclear power plant or in prevention of
either resumption of operation or of
increase in power output up to the
plant’s licensed power level, the
Commission may not have had an
opportunity to provide for public
comment on its no significant hazards
consideration determination. In such
case, the license amendment has been
issued without opportunity for
comment. If there has been some time
for public comment but less than 30
days, the Commission may provide an
opportunity for public comment. If
comments have been requested, it is so
stated. In either event, the State has
been consulted by telephone whenever
possible.
Under its regulations, the Commission
may issue and make an amendment
immediately effective, notwithstanding
the pendency before it of a request for
a hearing from any person, in advance
of the holding and completion of any
required hearing, where it has
determined that no significant hazards
consideration is involved.
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Jkt 208001
The Commission has applied the
standards of 10 CFR 50.92 and has made
a final determination that the
amendment involves no significant
hazards consideration. The basis for this
determination is contained in the
documents related to this action.
Accordingly, the amendments have
been issued and made effective as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the application for
amendment, (2) the amendment to
Facility Operating License, and (3) the
Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment, as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
The Commission is also offering an
opportunity for a hearing with respect to
the issuance of the amendment. Within
60 days after the date of publication of
this notice, the licensee may file a
request for a hearing with respect to
issuance of the amendment to the
subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
PO 00000
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51235
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland,
and electronically on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If there
are problems in accessing the document,
contact the PDR Reference staff at 1
(800) 397–4209, (301) 415–4737, or by email to pdr@nrc.gov. If a request for a
hearing or petition for leave to intervene
is filed by the above date, the
Commission or a presiding officer
designated by the Commission or by the
Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also identify the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner intends to
rely in proving the contention at the
hearing. The petitioner must also
provide references to those specific
sources and documents of which the
petitioner is aware and on which the
petitioner intends to rely to establish
those facts or expert opinion. The
petition must include sufficient
information to show that a genuine
dispute exists with the applicant on a
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jlentini on PROD1PC65 with NOTICES
material issue of law or fact.1
Contentions shall be limited to matters
within the scope of the amendment
under consideration. The contention
must be one which, if proven, would
entitle the petitioner to relief. A
petitioner/requestor who fails to satisfy
these requirements with respect to at
least one contention will not be
permitted to participate as a party.
Each contention shall be given a
separate numeric or alpha designation
within one of the following groups:
1. Technical—primarily concerns/
issues relating to technical and/or
health and safety matters discussed or
referenced in the applications.
2. Environmental—primarily
concerns/issues relating to matters
discussed or referenced in the
environmental analysis for the
applications.
3. Miscellaneous—does not fall into
one of the categories outlined above.
As specified in 10 CFR 2.309, if two
or more petitioners/requestors seek to
co-sponsor a contention, the petitioners/
requestors shall jointly designate a
representative who shall have the
authority to act for the petitioners/
requestors with respect to that
contention. If a petitioner/requestor
seeks to adopt the contention of another
sponsoring petitioner/requestor, the
petitioner/requestor who seeks to adopt
the contention must either agree that the
sponsoring petitioner/requestor shall act
as the representative with respect to that
contention, or jointly designate with the
sponsoring petitioner/requestor a
representative who shall have the
authority to act for the petitioners/
requestors with respect to that
contention.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing. Since the Commission has
made a final determination that the
amendment involves no significant
hazards consideration, if a hearing is
requested, it will not stay the
effectiveness of the amendment. Any
hearing held would take place while the
amendment is in effect.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
1 To the extent that the applications contain
attachments and supporting documents that are not
publicly available because they are asserted to
contain safeguards or proprietary information,
petitioners desiring access to this information
should contact the applicant or applicant’s counsel
and discuss the need for a protective order.
VerDate Aug<31>2005
17:07 Aug 28, 2006
Jkt 208001
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer or
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
Entergy Nuclear Operations, Inc.,
Docket No. 50–247, Indian Point
Nuclear Generating Unit No. 2,
Westchester County, New York
Date of amendment request: July 26,
2006.
Description of amendment request:
The amendment revised Function 6
[Containment Water Level (Containment
Sump)] of Table 3.3.3–1 (‘‘Post Accident
Monitoring Instrumentation’’),
referenced in the Technical
Specification (TS) Limiting Condition
for Operation (LCO) 3.3.3, ‘‘Post
Accident Monitoring Instrumentation.’’
The revision changed Function 6 to
specify 2 required channels for the
Containment Sump water level
instrumentation instead of 3 channels.
Date of issuance: July 28, 2006.
Effective date: As of its date of
issuance, and shall be implemented
prior to the expiration of the current 7day allowed outage time for inoperable
containment sump water level channels,
which was entered on July 24, 2006.
Amendment No.: 249.
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Sfmt 4703
Facility Operating License No. DPR–
26: The amendment revised the TS and
License.
Public comments requested as to
proposed no significant hazards
consideration (NSHC): No. The
Commission’s related evaluation of the
amendment, finding of emergency
circumstances, state consultation, and
final NSHC determination are contained
in a Safety Evaluation dated July 28,
2006.
Attorney for licensee: Mr. John Fulton,
Assistant General Counsel, Entergy
Nuclear Operations, Inc., 440 Hamilton
Avenue, White Plains, NY 10601.
NRC Branch Chief: Richard J. Laufer.
Dated at Rockville, Maryland, this 21st day
of August 2006.
For the Nuclear Regulatory Commission.
Cornelius F. Holden,
Deputy Director, Division of Operating
Reactor Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. 06–7137 Filed 8–28–06; 8:45 am]
BILLING CODE 7590–01–P
POSTAL RATE COMMISSION
Sunshine Act Meetings
NAME OF AGENCY:
Postal Rate
Commission.
Monday, August 28,
2006, at 3 p.m.
PLACE: Commission conference room,
901 New York Avenue, NW., Suite 200,
Washington, DC 20268–0001.
STATUS: Open.
Matters to be Considered: Consideration
of fiscal year 2007 budget and election
of vice chairman.
FOR FURTHER INFORMATION CONTACT:
Stephen L. Sharfman, General Counsel,
at 202–789–6820.
TIME AND DATE:
Dated: August 24, 2006.
Steven W. Williams,
Secretary.
[FR Doc. 06–7234 Filed 8–24–06; 4:37 pm]
BILLING CODE 7710–FW–M
RAILROAD RETIREMENT BOARD
Proposed Collection; Comment
Request
SUMMARY: In accordance with the
requirement of Section 3506(c)(2)(A) of
the Paperwork Reduction Act of 1995
which provides opportunity for public
comment on new or revised data
collections, the Railroad Retirement
Board (RRB) will publish periodic
summaries of proposed data collections.
Comments are invited on: (a) Whether
the proposed information collection is
E:\FR\FM\29AUN1.SGM
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Agencies
[Federal Register Volume 71, Number 167 (Tuesday, August 29, 2006)]
[Notices]
[Pages 51222-51236]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: 06-7137]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory
[[Page 51223]]
Commission (the Commission or NRC staff) is publishing this regular
biweekly notice. The Act requires the Commission publish notice of any
amendments issued, or proposed to be issued and grants the Commission
the authority to issue and make immediately effective any amendment to
an operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from August 4, 2006 to August 17, 2006. The last
biweekly notice was published on August 15, 2006 (71 FR 46929).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The
filing of requests for a hearing and petitions for leave to intervene
is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any
[[Page 51224]]
limitations in the order granting leave to intervene, and have the
opportunity to participate fully in the conduct of the hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland, 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam
Electric Plant, Unit No. 2, Darlington County, South Carolina
Date of amendment request: April 11, 2006.
Description of amendment request: The proposed amendment would
modify Technical Specification 5.6.5 ``Core Operating Limits Report
(COLR)'' to add two U.S. Nuclear Regulatory Commission-approved topical
reports to the COLR methodologies list. These topical reports allow the
use of S-RELAP5 thermal-hydraulic analysis code for accident safety
analyses.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The Proposed Change Does Not Involve a Significant Increase
in the Probability or Consequences of an Accident Previously
Evaluated.
The two topical reports have been reviewed and approved by the
NRC for use in determining core operating limits. The core operating
limits to be developed using the new methodologies for HBRSEP [H. B.
Robinson Steam Electric Plant], Unit No. 2, will be established in
accordance with the applicable limitations as documented in the NRC
Safety Evaluation Reports. In a May 11, 2001, NRC Safety Evaluation
Report, the NRC concluded that the S-RELAP5 code is capable of
addressing the thermal-hydraulic response of the target non-LOCA
[loss-of-coolant accident] events in a conservative manner and is,
therefore, an acceptable replacement for the ANF-RELAP code. In the
May 19, 2004, Safety Evaluation Report for Revision 1 to EMF-
2310(P)(A), the NRC concluded that the code remained acceptable for
use for the non-LOCA events. In a March 15, 2001, Safety Evaluation
Report, the NRC concluded that the code was acceptable for use for
small break LOCA analyses at Westinghouse pressurized water
reactors.
The proposed change, by itself, does not impact the current
design bases. The proposed change enables the use of new
methodologies to re-analyze certain events. Revised analyses may
either result in continued conformance with design bases, or may
change the design bases. If design basis changes result from a
revised analysis, then the specific design changes will be evaluated
in accordance with HBRSEP, Unit No. 2, design change procedures and
10 CFR 50.59.
The proposed change does not involve physical changes to any
plant structure, system, or component. Therefore, the probability of
occurrence for a previously analyzed accident is not significantly
increased.
The consequences of a previously analyzed accident are dependent
on the initial conditions assumed for the analysis, the behavior of
the fission product barriers during the analyzed accident, the
availability and successful functioning of the equipment assumed to
operate in response to the analyzed event, and the setpoints at
which these actions are initiated. The proposed methodologies will
ensure that the plant continues to meet applicable design and safety
analyses acceptance criteria. The proposed change does not affect
the performance of any equipment used to mitigate the consequences
of an analyzed accident. As a result, no analysis assumptions are
impacted and there are no adverse effects on the factors that
contribute to offsite or onsite dose as a result of an accident. The
proposed change does not affect setpoints that initiate protective
or mitigative actions. The proposed change ensures that plant
structures, systems, and components are maintained consistent with
the safety analysis and licensing bases. Based on this evaluation,
there is no significant increase in the consequences of a previously
analyzed accident.
Therefore, this change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
2. The Proposed Change Does Not Create the Possibility of a New
or Different Kind of Accident From Any Previously Evaluated.
The proposed change does not involve any physical alteration of
plant systems, structures, or components, other than allowing for
fuel design in accordance with NRC-approved methodologies. No new or
different equipment is being installed. No installed equipment is
being operated in a different manner. There is no change to the
parameters within which the plant is normally operated or in the
setpoints that initiate protective or mitigative actions. As a
result, no new failure modes are being introduced. Therefore, the
proposed change does not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3. The Proposed Change Does Not Involve a Significant Reduction
in the Margin of Safety.
There is no impact on any margin of safety resulting from the
incorporation of these new topical reports into the Technical
[[Page 51225]]
Specifications. If design basis changes result from a revised
analysis that uses these new methodologies, the specific design
changes will be evaluated in accordance with HBRSEP, Unit No. 2,
design change procedures and 10 CFR 50.59. Any potential reduction
in the margin of safety would be evaluated for that specific design
change.
Therefore, this change does not involve a significant reduction
in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Branch Chief: L. Raghavan.
Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam
Electric Plant, Unit No. 2, Darlington County, South Carolina
Date of amendment request: July 17, 2006.
Description of amendment request: The proposed amendment would
revise the containment pressure requirements specified in Surveillance
Requirements 3.6.8 and 5.5.16 due to a revision in the Loss-of-Coolant
Accident (LOCA) containment pressure analysis.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
No. The proposed change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated. The revised post-LOCA containment pressure and
temperature analysis used more conservative assumptions and the
increase in the calculated peak pressure was approximately 1 psig.
The revised value of 41.49 psig remains less than the containment
design pressure of 42 psig. The increase in the calculated peak
temperature was approximately 2 [deg]F, which was analyzed to have
no impact on structures or equipment. Although there is an increase
in the calculated pressure, the allowable containment leakage rate,
as measured at the peak pressure, is not being changed. Since there
is no increase in the allowable leakage, there is no increase in
consequences. The proposed change is related to containment pressure
analysis. There are no physical changes being made to the plant, or
to the manner in which the plant is operated. Surveillance
procedures for containment leakage have been conservatively testing
at pressures in excess of 42 psig and surveillance procedures for
the Isolation Valve Seal Water System have been conservatively
testing at pressures in excess of 46.2 psig. The change can have no
impact on the probability of an accident occurring. Therefore, the
proposed change does not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any previously evaluated?
No. The proposed change does not create the possibility of a new
or different kind of accident from any previously evaluated. There
are no physical changes being made to the plant or to the manner in
which the plant is operated. Surveillance procedures for containment
leakage have been conservatively testing at pressures in excess of
42 psig and surveillance procedures for the Isolation Valve Seal
Water System have been conservatively testing at pressures in excess
of 46.2 psig. The revised containment analysis results in a
calculated peak containment pressure that remains less than the
containment design pressure. The increase in the calculated peak
temperature was analyzed to have no impact on structures or
equipment. Therefore, this change does not create the possibility of
a new or different kind of accident from any accident previously
evaluated.
3. Do the proposed changes involve a significant reduction in
the margin of safety?
No. The proposed change does not involve a significant reduction
in the margin of safety. The proposed change imposes more
conservative surveillance test requirements. The calculated increase
in post-LOCA peak containment pressure is only 1 psig and the
revised value of 41.49 psig remains less than the containment design
pressure of 42 psig. The increase in the calculated peak temperature
was approximately 2 [deg]F, which was analyzed to have no impact on
structures or equipment. Although there was an increase in the
calculated pressure, the allowable containment leakage rate, as
measured at the peak pressure, is not being changed. Therefore, this
change does not involve a significant reduction in any margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Branch Chief: L. Raghavan.
Detroit Edison Company, Docket No. 50-341, Fermi 2, Monroe County,
Michigan
Date of amendment request: July 12, 2006.
Description of amendment request: The proposed amendment would
modify Conditions, Required Actions and Completion Times associated
with the inoperability of one or more emergency diesel generators
(EDGs) in Technical Specification (TS) 3.8.1.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
This license amendment request proposes a change to extend the
Technical Specification 3.8.1, ``AC Sources-Operating,'' Completion
Time. This change allows a single EDG to be inoperable for 7 days
more than Technical Specification 3.8.1 currently provides. The
Required Actions for CTG [Combustion Turbine Generator] 11-1 are
also removed from Condition A and TSTF [Technical Specification Task
Force] -439 is implemented for TS 3.8.1, removing the second
Completion Times.
The EDGs are safety related components which provide backup
electrical power supply to the onsite ESF [Engineered Safety
Feature] power distribution system. CTG 11-1 provides backup
electrical power to the Division 1 power distribution system.
Neither the EDGs nor CTG 11-1 are accident initiators, thus these
changes do not increase the probability of a previously evaluated
accident.
The plant ESF power distribution systems consist of two
divisions for 100% redundancy. Accident analyses demonstrate that
only one division is required for accident mitigation. Thus, with
one division inoperable the other division is capable of performing
the required safety function. Design basis analyses are not required
to be performed assuming extended loss of all power supplies to the
plant ESF power distribution system. Thus, this change does not
involve a significant increase in the consequences of a previously
analyzed accident.
The proposed change also eliminates the second Completion Time
from TS 3.8.1. These second Completion Times are not an initiator to
any accident previously evaluated. As a result, the probability of
an accident previously evaluated is not affected. The consequences
of an accident during the revised Completion Times are no different
than the consequences of the same accident during the existing
Completion Times. As a result, the consequences of an accident
previously evaluated are not affected by this change. Therefore, the
proposed change does not involve a significant increase in the
[[Page 51226]]
probability or consequences of an accident previously evaluated.
2. The proposed change does not create the possibility of a new
or different kind of accident from any accident previously
evaluated.
The changes do not involve a physical alteration of the plant
(i.e., no new or different type of equipment will be installed) or a
change in the methods governing normal plant operation. The changes
do not alter any assumptions made in the safety analysis.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. The change does not involve a significant reduction in the
margin of safety.
This license amendment request proposes Technical Specification
changes to extend the Technical Specification 3.8.1, ``AC Sources-
Operating,'' Completion Time for an inoperable EDG to 14 days. These
changes allow an emergency diesel generator to be inoperable for 7
days more than TS 3.8.1 currently provides.
Deterministic and probabilistic risk assessments evaluated the
effect of the proposed TS changes on the availability of an
electrical power supply to the plant emergency safeguards features
systems. These assessments concluded that the proposed TS changes do
not involve a significant increase in the risk of power supply
unavailability.
This license amendment request proposes TS changes to remove the
Required Actions for CTG 11-1 from TS 3.8.1 Condition A. If CTG 11-1
is inoperable at the same time that any single EDG is inoperable for
the entire proposed 14 day period with no other equipment in
maintenance, the risk remains within RG [Regulatory Guide] 1.174
(Reference 2 [in the application]) thresholds for a ``very small''
classification.
The proposed change to delete the second Completion Time does
not alter the manner in which safety limits, limiting safety system
settings, or limiting conditions for operation are determined. The
safety analysis acceptance criteria are not affected by this change.
The proposed changes will not result in plant operation in a
configuration outside of the design basis.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David G. Pettinari, Legal Department, 688
WCB, Detroit Edison Company, 2000 2nd Avenue, Detroit, Michigan 48226-
1279.
NRC Acting Branch Chief: Martin Murphy.
Dominion Nuclear Connecticut, Inc., Docket No. 50-336, Millstone Power
Station, Unit No. 2, (MPS2) New London County, Connecticut
Date of amendment request: June 13, 2006.
Description of amendment request: The proposed amendment would
allow changes to the Technical Specifications based on the radiological
dose analysis margins obtained by using an alternate source term
consistent with 10 CFR 50.67.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Involve a significant increase in the probability or
consequences of an accident previously evaluated?
No.
The proposed amendment does not involve a significant increase
in the probability or consequence of an accident previously
analyzed. The MPS2 control room emergency ventilation system only
functions following the initiation of a design basis radiological
accident. Therefore, the change to the value used for in-leakage
rate test acceptance criteria following a design basis accident will
not increase the probability of any previously analyzed accident.
The proposed 200 cfm control room habitability envelope inleakage
surveillance acceptance criteria has no adverse impact on control
room habitability analyses for postulated toxic chemical release
events. These habitability analyses do not credit automatic or
manual isolation of the control room fresh air ventilation flow
during a toxic chemical release event. The control room's forced
ventilation fresh air exchange rate (e.g., 800 cfm) is much greater
than the proposed 200 cfm envelope inleakage rate acceptance
criteria. The MPS2 containment purge valve isolation signal is not
credited in the accident analyses. The requirements contained in
this specification do not meet any of 10 CFR 50.36(c)(2)(ii)
criteria on items for which technical specifications must be
established. Deletion of this technical specification will not
increase the probability of any previously analyzed accident. The
MPS2 containment and the containment systems function to prevent or
control the release of radioactive fission products following a
postulated accident. Therefore, the change to the value used for
primary to secondary leak rate acceptance criteria, and for all
secondary containment bypass leakage paths following a design basis
accident, will not increase the probability of any previously
analyzed accident.
These systems are not initiators of any design bases accident.
Revised dose calculations, which take into account the changes
proposed by this amendment and the use of the alternative source
term, have been performed for the MPS2 design basis radiological
accidents. The results of these revised calculations indicate that
public and control room doses will not exceed the limits specified
in 10 CFR 50.67 and Regulatory Guide 1.183. There is not a
significant increase in predicted dose consequences for any of the
analyzed accidents. Therefore, the proposed changes do not involve a
significant increase in the consequences of any previously analyzed
accident.
2. Create the possibility of a new or different kind of accident
from any accident previously evaluated?
No.
The implementation of the proposed changes does not create the
possibility of an accident of a different type than was previously
evaluated in the UFSAR. Although the proposed changes could affect
the operation of the control room emergency ventilation system, and
the containment and containment systems following a design basis
radiological accident, none of these changes can initiate a new or
different kind of accident since they are only related to system
capabilities that provide protection from accidents that have
already occurred. These changes do not alter the nature of events
postulated in the UFSAR nor do they introduce any unique precursor
mechanisms. Therefore, the proposed changes do not create the
possibility of a new or different kind of accident from those
previously analyzed.
3. Involve a significant reduction in the margin of safety?
No.
The implementation of the proposed changes does not reduce the
margin of safety. The proposed changes for the control room
ventilation system, and the containment and containment systems do
not affect the ability of these systems to perform their intended
safety functions to maintain dose less than the required limits
during design basis radiological events. The radiological analysis
results, when compared with the revised TEDE [total effective dose
equivalent] acceptance criteria, meet the applicable limits. These
acceptance criteria have been developed for application to analyses
performed with alternative source terms. These acceptance criteria
have been developed for the purpose of use in design basis accident
analyses such that meeting the stated limits demonstrates adequate
protection of public health and safety. It is thus concluded that
the margin of safety will not be reduced by the implementation of
the changes.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Lillian M. Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc., Rope Ferry Road, Waterford, CT
06385.
NRC Acting Branch Chief: Brooke D. Poole.
[[Page 51227]]
Dominion Nuclear Connecticut, Inc., Docket No. 50-423, Millstone Power
Station, Unit No. 3, New London County, Connecticut
Date of amendment request: July 19, 2006.
Description of amendment request: The proposed amendment will
revise reactor core safety limits Technical Specifications (TSs) and
relocate the reactor core safety limit figure to the Core Operating
Limits Report (COLR) in the Millstone Power Station, Unit 3, Technical
Requirements Manual.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
Criterion 1:
Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The relocation of cycle-specific core operating limits from the
TS to the COLR and the addition of the RCS [reactor coolant system]
total flow rate to the COLR has no influence or impact on the
probability or consequences of a design basis accident. Adherence to
the COLR and methodologies acceptable for establishing COLR
parameters continues to be controlled by TS. The proposed amendment
still requires exactly the same actions to be taken when or if
limits are exceeded. Each accident analysis addressed in the final
safety analysis report (FSAR) will be examined with respect to
changes in cycle-dependent parameters, which are obtained from
application of the NRC-approved reload design methodologies, to
ensure that the transient evaluation of new core designs are bounded
by previously accepted analyses. This examination, which will be
performed in accordance with the requirements of 10 CFR 50.59,
ensures that future core designs will not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
Criterion 2:
Does the proposed amendment create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The relocation and addition of the cycle-specific variables to
the COLR and adding new document references in TS Section 6.9.1.6.b
does not influence or impact, nor does it contribute in any way to
the probability or consequences of an accident. No safety-related
equipment, safety function, or plant operations will be altered as a
result of these proposed changes. The cycle-specific variables are
calculated using NRC-approved methods and submitted to the NRC to
allow the staff to continue to trend the values of these limits. The
TS will continue to require operation within the required core
operating limits and appropriate actions will be taken when or if
limits are exceeded. Therefore the proposed amendment does not in
any way create the possibility of a new or different kind of
accident from any accident previously evaluated.
Criterion 3:
Does the proposed amendment involve a significant reduction in a
margin of safety?
Response: No.
The proposed changes have no impact on plant equipment
operation. The proposed changes do not revise any setpoints or
acceptance criteria assumed in the accident analyses. Therefore, the
proposed changes will not result in a reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Lillian M. Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc., Rope Ferry Road, Waterford, CT
06385.
NRC Acting Branch Chief: Brooke D. Poole.
Entergy Nuclear Operations, Inc., Docket No. 50-247, Indian Point
Nuclear Generating Unit No. 2 (IP2), Westchester County, New York
Date of amendment request: July 10, 2006.
Description of amendment request: Energy Nuclear Operations, Inc.,
is planning to operate an Independent Spent Fuel Storage Installation
(ISFSI) facility at IP2 using the HOLTEC HI-STORM 100 Cask System. To
support this activity, the proposed amendment adds Spent Fuel Cask
loading requirements to IP2 Technical Specifications (TSs).
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change will revise the Indian Point Unit 2 TSs
associated with the SFP [spent fuel pool] to assure that the
regulatory requirements related to criticality in the SFP and
applied to the Holtec HI-STORM 100 Multi-Purpose Canister MPC-32
when in the SFP are reflected in the IP2 TS. The proposed change
does not require any physical changes to Part 50 structures,
systems, or components, nor will their performance requirements be
altered. Therefore, the response of the plant to previously analyzed
accidents and related radiological releases will not be adversely
impacted, and will bound those postulated during cask loading
activities in the cask storage area.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
Existing fuel handling procedures and associated administrative
controls remain applicable for cask loading operations within the
SFP. Additionally, the soluble boron concentration required to
maintain keff <= 0.95 for postulated criticality accidents
associated with cask loading operations was also evaluated. The
results of the analyses, using a methodology previously approved by
the NRC [Nuclear Regulatory Commission], demonstrate that the amount
of soluble boron required to compensate for the positive reactivity
associated with these postulated accidents (371 ppm [parts per
million]) remains well below the existing spent fuel pit minimum
boron concentration limit of 2000 ppm. Accordingly, the same limit
has been proposed for cask loading operations in the cask storage
area.
Therefore, the possibility of a new or different kind of
accident from any accident previously evaluated is not created.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
An NRC approved methodology was used to perform the criticality
analysis which provides the basis to incorporate a new family of
burnup versus enrichment curves, for various cooling times, into the
plant Technical Specifications to ensure criticality requirements
are met during spent fuel cask loading. Accordingly, the existing
minimum boron concentration limit for the spent fuel pit of 2000 ppm
will continue to remain bounding during cask loading operations.
This determination accounts for uncertainties at a 95 percent
probability, 95 percent confidence level. Should it be postulated
that a boron dilution event does occur during this time period, keff
will remain less than 1.0 should the cask storage area become fully
flooded with unborated water.
Therefore, there will not be a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. John Fulton, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 440 Hamilton Avenue, White Plains, NY
10601.
NRC Branch Chief: Richard J. Laufer.
[[Page 51228]]
Exelon Generation Company, LLC, Docket No. 50-249, Dresden Nuclear
Power Station (DNPS), Unit 3, Grundy County, Illinois
Date of amendment request: July 21, 2006.
Description of amendment request: The proposed amendment would
revise the values of the safety limit minimum critical power ratio
(SLMCPR) in Technical Specification Section 2.1.1, ``Reactor Core SLs
[Safety Limits].'' Specifically, the proposed change would require that
for Unit 3, the minimum critical power ratio (MCPR) for Global Nuclear
Fuel fuel shall be >= 1.10 for two recirculation loop operation, or >=
1.11 for single recirculation loop operation. Additionally, the
proposed change would require that MCPR for Westinghouse fuel shall be
>= 1.12 for two recirculation loop operation, or >= 1.14 for single
recirculation loop operation.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The probability of an evaluated accident is derived from the
probabilities of the individual precursors to that accident. The
consequences of an evaluated accident are determined by the
operability of plant systems designed to mitigate those
consequences. Limits have been established consistent with NRC
[Nuclear Regulatory Commission]-approved methods to ensure that fuel
performance during normal, transient, and accident conditions is
acceptable. The proposed change conservatively establishes the
SLMCPR for DNPS, Unit 3, Cycle 20 such that the fuel is protected
during normal operation and during plant transients or anticipated
operational occurrences (AOOs).
Changing the SLMCPR does not increase the probability of an
evaluated accident. The change does not require any physical plant
modifications, physically affect any plant components, or entail
changes in plant operation. Therefore, no individual precursors of
an accident are affected.
The proposed change revises the SLMCPR to protect the fuel
during normal operation as well as during plant transients or AOOs.
Operational limits will be established based on the proposed SLMCPR
to ensure that the SLMCPR is not violated. This will ensure that the
fuel design safety criterion (i.e., that at least 99.9% of the fuel
rods do not experience transition boiling during normal operation
and AOOs) is met. Since the proposed change does not affect
operability of plant systems designed to mitigate any consequences
of accidents, the consequences of an accident previously evaluated
are not expected to increase.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
Creation of the possibility of a new or different kind of
accident requires creating one or more new accident precursors. New
accident precursors may be created by modifications of plant
configuration, including changes in allowable modes of operation.
The proposed change does not involve any plant configuration
modifications or changes to allowable modes of operation. The
proposed change to the SLMCPR assures that safety criteria are
maintained for DNPS, Unit 3, Cycle 20.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The SLMCPR provides a margin of safety by ensuring that at least
99.9% of the fuel rods do not experience transition boiling during
normal operation and AOOs if the MCPR limit is not violated. The
proposed change will ensure the current level of fuel protection is
maintained by continuing to ensure that at least 99.9% of the fuel
rods do not experience transition boiling during normal operation
and AOOs if the MCPR limit is not violated. The proposed SLMCPR
values were developed using NRC-approved methods. Additionally,
operational limits will be established based on the proposed SLMCPR
to ensure that the SLMCPR is not violated. This will ensure that the
fuel design safety criterion (i.e., that no more than 0.1% of the
rods are expected to be in boiling transition if the MCPR limit is
not violated) is met.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Bradley J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Kennett
Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
FirstEnergy Nuclear Operating Company, et al., Docket No. 50-440, Perry
Nuclear Power Plant, Unit 1 (PNPP), Lake County, Ohio
Date of amendment request: June 6, 2006.
Description of amendment request: The proposed amendment would
revise the Ventilation Filter Test Program (VFTP) in Technical
Specification (TS) 5.5.7. The license amendment is a corrective action
to revise the flow rate units specified in the VFTP from standard cubic
feet per minute to cubic feet per minute. This amendment will ensure
the PNPP TS are consistent with plant design documentation, testing
criteria, and the industry.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response:
The ESF [Engineered Safety Feature] Ventilation systems reduce
the concentration of airborne radioactive contaminants following a
design basis accident and therefore are not initiators of design
bases accidents. The proposed amendment does not change the manner
in which the ESF ventilation systems are operated or tested.
Implementation of the proposed amendment will ensure the ESF
ventilation systems perform their function when called upon and does
not affect the plant operations, design function or analysis that
verifies the capability of a [plant] structures, systems or
components.
The proposed amendment does not affect the design of the ESF
ventilation systems, the operational characteristics of the ESF
ventilation systems, the interfaces between the ESF ventilation
systems and those plant systems they support, or the reliability of
the ESF ventilation systems.
Therefore, the ESF ventilation systems will be capable of
performing their accident mitigation function and there is no
increase in the probability or consequences of an accident already
evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response:
The proposed amendment introduces no new mode of plant operation
and does not involve a physical modification to the plant. New
equipment is not installed with the proposed amendment, nor does the
proposed amendment cause existing equipment to be operated in a new
or different manner.
Since the proposed changes do not involve a change to the plant
design or operation, no new system interactions are created by this
change. The proposed amendment does not produce any parameters or
conditions that
[[Page 51229]]
could contribute to the initiation of accidents different from those
already evaluated in the Updated Safety Analysis Report.
The changes to the VFTP do not affect the assumed accident
performance of the ESF Ventilation systems, nor [sic] any plant
structure, system or component previously evaluated.
Therefore, the proposed amendment does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response:
The proposed amendment does not impact the ESF ventilation
systems performance, including the capability for each ESF
ventilation system to attain and maintain required air flow assumed
in the plant safety analysis.
The proposed amendment does not involve a significant reduction
in a margin of safety since the operability of the ESF ventilations
[sic] systems continues to be determined as required to support the
capability of the ESF ventilations [sic] systems to provide the
required ventilation, filtration and temperature control to mitigate
the consequences of an accident.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David W. Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street, Akron, OH 44308.
NRC Branch Chief: Daniel S. Collins.
Florida Power Corporation, et al., Docket No. 50-302, Crystal River
Unit 3 Nuclear Generating Plant, Citrus County, Florida
Date of amendment request: May 25, 2006.
Description of amendment request: The proposed license amendment
revises the requirements in the Crystal River Unit 3 Improved Technical
Specification related to steam generator tube integrity. The licensee
states that the changes are consistent with NRC-approved Technical
Specification (TS) Task Force (TSTF) Change Traveler, TSTF-449, ``Steam
Generator Tube Integrity,'' Revision 4. The availability of this
technical specification improvement was announced in the Federal
Register on May 6, 2005, as part of the consolidated line item
improvement process.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
Criterion 1--The Proposed Change Does Not Involve a Significant
Increase in the Probability or Consequences of an Accident Previously
Evaluated
The proposed change requires a SG [Steam Generator] Program that
includes performance criteria that will provide reasonable assurance
that the SG tubing will retain integrity over the full range of
operating conditions (including startup, operation in the power
range, hot standby, cooldown and all anticipated transients included
in the design specification). The SG performance criteria are based
on tube structural integrity, accident induced leakage, and
operational LEAKAGE.
A SGTR [steam generarator tube rupture] event is one of the
design basis accidents that are analyzed as part of a plant's
licensing basis. In the analysis of a SGTR event, a bounding primary
to secondary LEAKAGE rate equal to the operational LEAKAGE rate
limits in the licensing basis plus the LEAKAGE rate associated with
a double-ended rupture of a single tube is assumed.
For other design basis accidents such as MSLB [main steamline
break], rod ejection, and reactor coolant pump locked rotor the
tubes are assumed to retain their structural integrity (i.e., they
are assumed not to rupture). These analyses typically assume that
primary to secondary LEAKAGE for all SGs is 1 gallon per minute or
increases to 1 gallon per minute as a result of accident induced
stresses. The accident induced leakage criterion introduced by the
proposed changes accounts for tubes that may leak during design
basis accidents. The accident induced leakage criterion limits this
leakage to no more than the value assumed in the accident analysis.
The SG performance criteria proposed change to the TS identify
the standards against which tube integrity is to be measured.
Meeting the performance criteria provides reasonable assurance that
the SG tubing will remain capable of fulfilling its specific safety
function of maintaining reactor coolant pressure boundary integrity
throughout each operating cycle and in the unlikely event of a
design basis accident. The performance criteria are only a part of
the SG Program required by the proposed change to the TS. The
program, defined by NEI [Nuclear Energy Institute] 97-06, Steam
Generator Program Guidelines, includes a framework that incorporates
a balance of prevention, inspection, evaluation, repair, and leakage
monitoring. The proposed changes do not, therefore, significantly
increase the probability of an accident previously evaluated.
The consequences of design basis accidents are, in part,
functions of the DOSE EQUIVALENT 1-131 in the primary coolant and
the primary to secondary LEAKAGE rates resulting from an accident.
Therefore, limits are included in the plant technical specifications
for operational leakage and for DOSE EQUIVALENT 1-131 in primary
coolant to ensure the plant is operated within its analyzed
condition. The typical analysis of the limiting design basis
accident assumes that primary to secondary leak rate after the
accident is 1 gallon per minute with no more than [500 gallons per
day or 720 gallons per day] in any one SG, and that the reactor
coolant activity levels of DOSE EQUIVALENT 1-131 are at the TS
values before the accident.
The proposed change does not affect the design of the SGs, their
method of operation, or primary coolant chemistry controls. The
proposed approach updates the current TSs and enhances the
requirements for SG inspections. The proposed change does not
adversely impact any other previously evaluated design basis
accident and is an improvement over the current TSs.
Therefore, the proposed change does not affect the consequences
of a SGTR accident and the probability of such an accident is
reduced. In addition, the proposed changes do not affect the
consequences of an MSLB, rod ejection, or a reactor coolant pump
locked rotor event, or other previously evaluated accident.
Criterion 2--The Proposed Change Does Not Create the Possibility of a
New or Different Kind of Accident from any Previously Evaluated
The proposed performance based requirements are an improvement
over the requirements imposed by the current technical
specifications. Implementation of the proposed SG Program will not
introduce any adverse changes to the plant design basis or
postulated accidents resulting from potential tube degradation. The
result of the implementation of the SG Program will be an
enhancement of SG tube performance. Primary to secondary LEAKAGE
that may be experienced during all plant conditions will be
monitored to ensure it remains within current accident analysis
assumptions.
The proposed change does not affect the design of the SGs, their
method of operation, or primary or secondary coolant chemistry
controls. In addition, the proposed change does not impact any other
plant system or component. The change enhances SG inspection
requirements.
Therefore, the proposed change does not create the possibility
of a new or different type of accident from any accident previously
evaluated.
Criterion 3--The Proposed Change Does Not Involve a Significant
Reduction in the Margin of Safety
The SG tubes in pressurized water reactors are an integral part
of the reactor coolant pressure boundary and, as such, are relied
upon to maintain the primary system's pressure and inventory. As
part of the reactor coolant pressure boundary, the SG tubes are
unique in that they are also relied upon as a heat transfer surface
between the primary and secondary systems such that residual heat
can be removed from the primary system. In addition, the SG tubes
isolate the radioactive fission products in the primary coolant from
the secondary system. In summary, the safety function of an SG is
maintained by ensuring the integrity of its tubes.
Steam generator tube integrity is a function of the design,
environment, and the physical condition of the tube. The proposed
change does not affect tube design or operating environment. The
proposed change is expected to result in an improvement in the
[[Page 51230]]
tube integrity by implementing the SG Program to manage SG tube
inspection, assessment, repair, and plugging. The requirements
established by the SG Program are consistent with those in the
applicable design codes and standards and are an improvement over
the requirements in the current TSs.
For the above reasons, the margin of safety is not changed and
overall plant safety will be enhanced by the proposed change to the
TS.
The NRC staff proposes to determine that the amendment request
involves no significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Branch Chief: L. Raghavan.
Nuclear Management Company, LLC, Docket No. 50-266, Point Beach Nuclear
Plant (PBNP), Unit 1, Town of Two Creeks, Manitowoc County, Wisconsin
Date of amendment request: July 11, 2006.
Description of amendment request: The proposed amendment would
revise Technical Specification (TS) 5.5.8, ``Steam Generator (SG)
Program,'' to exclude the portion of the tube below 17 inches from the
top of the tubesheet from the SG tube inspection requirements for Unit
1 on a one-time basis for a single operating cycle. In addition,
administrative changes are proposed to correct a page number in the TS
table of contents and delete two blank pages in TS Section 5.
Basis for proposed no significant hazards consideration
determination: As required by 10CFR 50.91(a), the licensee has provided
its analysis of the issue of no significant hazards consideration which
is presented below.
1. Operation of the Point Beach Nuclear Plant in accordance with
the proposed amendments does not result in a significant increase in
the probability or consequences of any accident previously
evaluated.
The proposed change revises Technical Specification (TS) 5.5.8,
``Steam Generator (SG) Program'' to redefine the PBNP Unit 1 primary
pressure boundary for purposes of the SG tube inspection
requirements on a one-time basis for Unit 1 Refueling Outage 30 and
the subsequent operating cycle. The redefined primary pressure
boundary is relocated from the seal weld at the bottom of the SG
tube to the tube-to-tubesheet mechanical interface. The required
structural integrity margins of the SG tubes in this area are
unaffected by this change and will be maintained by the SG
tubesheet. SG tubes are hydraulically expanded into the tubesheet.
Steam generator tube rupture is constrained by the tubesheet for
tubes with cracks in the tubesheet. This constraint results from the
hydraulic expansion process which restricts further expansion of the
tube, thermal expansion mismatch between the tube and tubesheet and
from the differential pressure between the primary and secondary
side. Thermal expansion and differential pressure also restrain the
tube axially. For conservatism, hydraulic preload was not factored
into the analysis.
The proposed change continues to require that the SG Program
include performance criteria that will provide reasonable assurance
that the SG tubing will retain integrity over the full range of
operating conditions (including startup, operation in the power
range, hot standby, cooldown and all anticipated transients included
in the design specification).
The SG performance criteria are based on tube structural
integrity, accident induced leakage, and operational LEAKAGE. The
analysis shows that structural integrity retains acceptable safety
factors against burst under normal steady state full power operation
primary-to-secondary pressure differential and against burst applied
to the design basis accident primary-to-secondary pressure
differentials. The analysis also shows that accident induced leakage
is bound by twice the normal operating leakage and well below the
accident analysis assumption for each stream generator. The primary
to secondary operational LEAKAGE limit is not changed.
The planned inspection and supporting analysis provide
reasonable assurance that the SG tubing will remain capable of
fulfilling its specific safety function of maintaining reactor
coolant pressure boundary integrity throughout the operating cycle
and in the unlikely event of a design basis accident. The proposed
change does not, therefore, significantly increase the probability
of an accident previously evaluated.
The consequences of design basis accidents are, in part,
functions of the DOSE EQUIVALENT I-131 in the primary coolant and
the primary to secondary LEAKAGE rates resulting from an accident.
The plant technical specification limits for operational LEAKAGE and
for DOSE EQUIVALENT I-131 in primary coolant, which ensure the plant
is operated within its analyzed condition, are unaffected by the
proposed change. Therefore, the proposed change does not
significantly increase the consequences of any accident previously
evaluated.
The proposed change does not significantly affect the
probability of any event initiators. There will be no change to
normal plant operating parameters, engineered safety feature
actuation setpoints, accident mitigation capabilities, or accident
analysis assumptions or inputs.
Therefore, the probability or consequences of any accident
previously evaluated will not be significantly increased as a result
of the proposed change.
2. Operation of the Point Beach Nuclear Plant in accordance with
the proposed amendments does not result in a new or different kind
of accident from any accident previously evaluated.
Implementation of the proposed change will not introduce any
adverse changes to the plant design basis or postulated accidents
resulting from potential tube degradation. Primary to secondary
leakage that may be experienced during all plant conditions will
continue to be monitored to ensure it remains within current
accident analysis assumptions. The proposed change does not affect
the method of operation of the SGs, or primary or secondary coolant
chemistry controls. In addition, the proposed change does not impact
any other plant system or component.
No new accident scenarios, transient precursors, failure
mechanisms, or limiting single failures are introduced as a result
of the proposed change. Equipment important to safety will continue
to operate as designed. The changes do not result in any event
previously deemed incredible being made credible. The changes do not
result in adverse conditions or result in any increase in the
challenges to safety systems. Therefore, the proposed change does
not create the possibility of a new or different type of accident
from any accident previously evaluated.
3. Operation of the Point Beach Nuclear Plant in accordance with
the proposed amendments does not result in a significant reduction
in a margin of safety.
The steam generators (SGs) are an integral part of the reactor
coolant pressure boundary and, as such, are relied upon to maintain
the primar