Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 46929-46946 [06-6921]
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Federal Register / Vol. 71, No. 157 / Tuesday, August 15, 2006 / Notices
Program Directors (CRCPD) (Public
Meeting) (Contact: Shawn Smith,
301–415–2620).
This meeting will be webcast live at
the Web address—https://www.nrc.gov.
1 p.m. Discussion of Security Issues
(Closed—Ex. 1).
Week of September 18, 2006—Tentative
There are no meetings scheduled for
the Week of September 18, 2006.
* The schedule for Commission
meetings is subject to change on short
notice. To verify the status of meetings
call (recording)—(301) 415–1292.
Contact person for more information:
Michelle Schroll, (301) 415–1662.
The NRC Commission Meeting
Schedule can be found on the Internet
at: www.nrc.gov/what-we-do/policymaking/schedule.html.
The NRC provides reasonable
accommodation to individuals with
disabiloities where appropriate. If you
need a reasonable acommodation to
participate in these public meetings, or
need this meeting notice or the
transcript or other information from the
public meetings in another format (e.g.,
braille, large print), please notify the
NRC’s Disability Program Coordinator,
Deborah Chan, at 301–415–7041, TDD:
301–415–2100, or by E-mail at
DLC@nrc.gov. Determinations on
requests for reasonable accommodation
will be made on a case-by-case basis.
This notice is distributed by mail to
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In addition, distribution of this meeting
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receiving this Commission meeting
schedule electronically, please send an
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Dated: August 10, 2008.
R. Michelle Schroll,
Office of the Secretary.
[FR Doc. 06–6939 Filed 8–11–06; 9:59 am]
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NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
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staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from July 21,
2006, to August 3, 2006. The last
biweekly notice was published on
August 1, 2006 (71 FR 43528).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
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46929
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example,
in derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
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leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
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intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland 20852,
Attention: Rulemaking and
Adjudications Staff; (3) e-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
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For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket
No. 50–461, Clinton Power Station
(CPS), Unit 1, DeWitt County, Illinois
Date of amendment request: June 30,
2006.
Description of amendment request:
The proposed change would revise the
Note preceding Technical Specification
(TS) Surveillance Requirement (SR)
3.4.6.1 to be consistent with the
wording in NUREG–1434, ‘‘Standard
Technical Specifications General
Electric Plants, BWR/6,’’ Revision 3.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed amendment revises the note
associated with TS SR 3.4.6.1, which requires
verification that the leakage past the Reactor
Coolant System (RCS) Pressure Isolation
Valves (PIVs) is less than a specified limit.
The proposed revision provides clarification
that performance of this SR is allowed during
plant shutdown (i.e., a Mode other than
Modes 1 and 2).
The proposed change does not require
modification to the facility. The proposed
change does not affect the operation of any
facility equipment, the interface between
facility systems, or the reliability of any
equipment. In addition, the proposed change
does not alter the requirement to perform the
leakage testing of the RCS PIVs and does not
revise the leakage limits associated with this
SR. The function of the RCS PIVs is to
separate the high pressure RCS from an
attached low pressure system. Periodic
testing of PIVs can substantially reduce
intersystem Loss of Coolant Accident (LOCA)
probability. Since the proposed change does
not alter the method or limits associated with
the leak rate testing of the RCS PIVs there is
no significant increase in the probability of
a LOCA. Therefore, the proposed amendment
does not involve a significant increase in the
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probability of an accident previously
evaluated.
The consequences of a previously analyzed
event are dependent on the initial conditions
assumed in the analysis, the availability and
successful functioning of equipment assumed
to operate in response to the analyzed event,
and the setpoints at which these actions are
initiated. The method for performing the
leakage testing of the RCS PIVs and the
specified leakage limit for this testing will
not change as a result of the proposed
revision and, therefore, there is no change in
the consequences associated with the LOCA
analysis. The radiological consequences
remain within applicable regulatory limits.
The proposed change does not alter any
system’s performance measures or the ability
to perform its accident mitigation functions.
The radiological consequences associated
with any previously evaluated accident do
not change as a result of the proposed
revision. Therefore, the proposed change
does not involve a significant increase in the
consequences of an accident previously
evaluated.
Based on the above, the proposed change
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change to the wording of the
Note to TS SR 3.4.6.1 clarifies the plant
conditions for when the surveillance is
required to be performed. The proposed
change does not affect the design, functional
performance or operation of the facility. No
new equipment is being introduced and
installed equipment is not being operated in
a new or different manner. Similarly, the
proposed change does not affect the design
or operation of any structures, systems or
components involved in the mitigation of any
accidents, nor does it affect the design or
operation of any component in the facility
such that new equipment failure modes are
created. There are no setpoints at which
protective or mitigative actions are initiated
that are affected by this proposed action. No
change is being made to procedures relied
upon to respond to an off-normal event.
As such the proposed amendment will not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
Margins of safety are established in the
design of components, the configuration of
components to meet certain performance
parameters, and in the establishment of
setpoints to initiate alarms or actions. The
proposed change revises a note associated
with a surveillance requirement to clarify the
plant conditions for when the surveillance
needs to be performed. This change involves
an administrative clarification to reflect the
original intent of the TS. The equipment will
continue to be tested in a manner and at a
frequency necessary to provide confidence
that the equipment can perform its intended
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safety function. There is no change in the
design of the affected systems, no alteration
of the setpoints at which alarms or actions
are initiated, and no change in plant
configuration from original design. There is
no impact on the plant safety analyses.
Therefore, operation of CPS in accordance
with the proposed change will not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. Bradley J.
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
Entergy Operations Inc., Docket No. 50–
382, Waterford Steam Electric Station,
Unit 3, St. Charles Parish, Louisiana
Date of amendment request: June 14,
2006.
Description of amendment request:
The proposed change will delete
Waterford 3 Technical Specification
(TS) Surveillance Requirement (SR)
4.8.1.1.2.f. This SR requires that the
emergency diesel generator be subjected
to an inspection in accordance with
procedures prepared in conjunction
with its manufacturer’s
recommendations.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The ability of the emergency diesel
generator to perform its safety function is not
proven by the performance of the
manufacturer’s recommended inspections.
The inspections are not considered an
initiator or mitigating factor in any
previously evaluated accidents.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change results in the
deletion of the SR associated with the
performance of manufacturer’s inspections.
No modifications to plant structures,
systems, or components, or changes in the
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design of the plant structures, systems, or
components are required to support the
proposed TS change.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The ability of the emergency diesel
generator to perform its safety function is not
proven by the performance of the
manufacturer’s recommended inspections.
Inspection activities will continue to be
performed.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: N.S. Reynolds,
Esquire, Winston & Strawn, 1700 K
Street, NW., Washington, DC 20006–
3817.
NRC Branch Chief: David Terao.
Exelon Generation Company, LLC,
Docket Nos. 50–237 and 50–249,
Dresden Nuclear Power Station (DNPS),
Units 2 and 3, Grundy County, Illinois
Date of amendment request: June 2,
2006.
Description of amendment request:
The proposed amendments would
revise Technical Specification (TS)
Surveillance Requirement (SR) 3.4.3.1 to
increase the allowable as-found main
steam safety valve (MSSV) lift set point
tolerance from +/¥1 percent to +/¥3
percent. The proposed change would
also revise the SR 3.1.7.10 to increase
the enrichment of sodium pentaborate
used in the Standby Liquid Control
(SLC) system from greater than or equal
to 30 atom percent boron-10 to greater
than or equal to 45 atom percent boron10.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change increases the
allowable as-found MSSV lift setpoint
tolerance, determined by test after the valves
have been removed from service, from +/¥1
percent to +/¥3 percent. The proposed
change does not alter the TS requirements for
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the number of MSSVs required to be
operable, the nominal lift setpoints, the
allowable as-left lift setpoint tolerance, the
MSSV testing frequency, or the manner in
which the valves are operated.
Consistent with current TS requirements,
the proposed change continues to require
that the MSSVs be adjusted to within +/¥1
percent of their nominal lift setpoints
following testing. Since the proposed change
does not alter the manner in which the valves
are operated, there is no significant impact
on reactor operation.
The proposed change does not involve a
physical change to the valves, nor does it
change the safety function of the valves. The
proposed TS revision involves no significant
changes to the operation of any systems or
components in normal or accident operating
conditions and no changes to existing
structures, systems, or components, with the
exception of the SLC system enrichment
change. The proposed change to increase the
enrichment of sodium pentaborate used in
the SLC system by a design modification
using a single SLC pump will ensure that the
requirements of 10 CFR 50.62,
‘‘Requirements for reduction of risk from
anticipated transients without scram (ATWS)
events for light-water-cooled nuclear power
plants,’’ continue to be met. The SLC system
is not an initiator to an accident; rather, the
SLC system is used to mitigate a postulated
anticipated transient without scram (ATWS)
event. Therefore, these changes will not
increase the probability of an accident
previously evaluated.
Generic considerations related to the
change in setpoint tolerance were addressed
in NEDC–31753P, ‘‘BWROG In-Service
Pressure Relief Technical Specification
Revision Licensing Topical Report,’’ and
were reviewed and approved by the NRC in
a safety evaluation dated March 8, 1993. The
plant specific evaluations, required by the
NRC’s safety evaluation and performed to
support this proposed change, show that
there is no change to the design core thermal
limits and adequate margin to the reactor
vessel pressure limits using a +/¥3 percent
lift setpoint tolerance. These analyses also
show that operation of Emergency Core
Cooling Systems is not affected, and the
containment response following a loss-ofcoolant accident is acceptable. The plant
systems associated with these proposed
changes are capable of meeting applicable
design basis requirements and retain the
capability to mitigate the consequences of
accidents described in the Updated Final
Safety Analysis Report. Therefore, these
changes do not involve an increase in the
consequences of an accident previously
evaluated.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change increases the
allowable as-found lift setpoint tolerance for
the DNPS MSSVs, and increases the required
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enrichment of sodium pentaborate used in
the SLC system. The proposed change to
increase the enrichment of sodium
pentaborate used in the SLC system will
ensure that the requirements of 10 CFR 50.62
continue to be met.
The proposed change to increase the MSSV
tolerance was developed in accordance with
the provisions contained in the NRC safety
evaluation for NEDC–31753P. MSSVs
installed in the plant following testing or
refurbishment will continue to meet the
current tolerance as-left acceptance criteria of
+/¥1 percent of the nominal setpoint. The
proposed change does not affect the manner
in which the overpressure protection system
is operated; therefore, there are no new
failure mechanisms for the overpressure
protection system.
The proposed change to allow an increase
in the MSSV setpoint tolerance does not alter
the nominal MSSV lift setpoints or the
number of MSSVs currently required to be
operable by DNPS TS. The proposed change
does not involve physical changes to the
valves, nor does it change the safety function
of the valves. There is no alteration to the
parameters within which the plant is
normally operated. As a result, no new
failure modes are being introduced.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The margin of safety is established through
the design of the plant structures, systems,
and components, the parameters within
which the plant is operated, and the
establishment of the setpoints for the
actuation of equipment relied upon to
respond to an event. The proposed change
does not modify the safety limits or setpoints
at which protective actions are initiated, and
does not change the requirements governing
operation or availability of safety equipment
assumed to operate to preserve the margin of
safety.
Establishment of the ±3 percent MSSV
setpoint tolerance limit does not adversely
impact the operation of any safety-related
component or equipment. Evaluations
performed in accordance with the NRC safety
evaluation for NEDC–31753P have concluded
that all design limits will continue to be met.
The proposed change to increase the
enrichment of sodium pentaborate used in
the SLC system will ensure that the
requirements of 10 CFR 50.62 continue to be
met.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Bradley J.
Fewell, Assistant General Counsel,
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Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
Exelon Generation Company, LLC,
Docket Nos. 50–373 and 50–374, LaSalle
County Station (LSCS), Units 1 and 2,
LaSalle County, Illinois
Date of amendment request: March
16, 2006.
Description of amendment request:
The proposed amendment would
modify Technical Specification (TS)
3.3.6.1, ‘‘Primary Containment Isolation
Instrumentation,’’ Table 3.3.6.1–1 to
revise the allowable values (AVs) for the
reactor core isolation cooling (RCIC)
temperature-based leak detection. The
proposed change is a result of revising
the setpoint calculation for the subject
temperature instruments based on the
current reactor coolant leak detection
analytical limit. The temperature limits
correspond to a 25-gallon per minute
(gpm) leak as determined by LSCS
calculations. The proposed changes
would revise TS Table 3.3.6.1–1 AVs for
the following four RCIC system isolation
functions:
Item 3.e. RCIC Equipment Room
Temperature—High
Item 3.f. RCIC Equipment Room Differential
Temperature—High
Item 3.g. RCIC Steam Line Tunnel
Temperature—High
Item 3.h. RCIC Steam Line Tunnel
Differential Temperature—High
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed change does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated.
The proposed change is a result of revising
the setpoint calculation for the subject
temperature instruments based on the current
reactor coolant leak detection calculation
analytical limit. The proposed changes will
revise TS Table 3.3.6.1–1 Allowable Values
for the following four RCIC system isolation
functions as noted below.
• Increase the Allowable Value for Function
3.e., ‘‘RCIC Equipment Room
Temperature—High,’’ from ≤ 291.0 °F to ≤
297.0 °F
• Decrease the Allowable Value for Function
3.f., ‘‘RCIC Equipment Room Differential
Temperature—High,’’ from ≤ 189.0 °F to ≤
188.0 °F
• Decrease the Allowable Value for Function
3.g., ‘‘RCIC Steam Line Tunnel
Temperature—High,’’ from ≤ 277.0 °F to ≤
267.0 °F
• Increase the Allowable Value for Function
3.h., ‘‘RCIC Steam Line Tunnel Differential
Temperature—High,’’ from ≤ 155.0 °F to ≤
163.0 °F
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The function of the instrumentation listed
on TS Table 3.3.6.1–1, in combination with
other accident mitigation features, is to limit
fission product release during and following
postulated Design Basis Accidents to within
allowable limits. The Allowable Values
specified in TS Table 3.3.6.1–1 provide
assurance that the instrumentation will
perform as designed.
The Allowable Values for RCIC system
isolation are not a precursor to any accident
previously evaluated. Accidents are assumed
to be initiated by equipment failure. The
proposed change does not alter the initiation
conditions or operational parameters for the
system. There is no increase in the failure
probability of the system. As such, the
probability of occurrence for a previously
evaluated accident is not increased.
The Allowable Values specified in Table
3.3.6.1–1 provide assurance that the RCIC
system will perform as designed. The
proposed revision to the Allowable Values
does not change any of the RCIC system leak
detection isolation actuation setpoints. Thus,
the radiological consequences of any
accident previously evaluated are not
increased.
Based on the above information, the
proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. The proposed TS change does not create
the possibility of a new or different kind of
accident from any accident previously
evaluated.
The proposed change does not affect the
control parameters governing unit operation
or the response of plant equipment to
transient conditions. The proposed change
does not change or introduce any new
equipment, modes of system operation or
failure mechanisms.
The proposed change is based on revised
reactor coolant leak detection calculation
analytical limits determined by the most
current revision to the heat rise calculation.
Setpoint calculations have been performed to
determine the nominal trip setpoints and
Allowable Values for the instrumentation
associated with the leak detection function
based on the revised analytical limits
determined by the heat rise calculations. The
proposed revision to the Allowable Values
does not change any of the RCIC system leak
detection isolation actuation setpoints.
Based on the above information, the
proposed change does not create the
possibility of a new or different kind of
accident from any previously evaluated.
3. The proposed change does not involve
a significant reduction in the margin of
safety.
The proposed change will revise TS Table
3.3.6.1–1 Allowable Values for the
instrument functions associated with RCIC
Isolation.
The current Allowable Values for these
functions are:
≤ 291.0 °F for RCIC Equipment Room
Temperature—High
≤ 189.0 °F for RCIC Equipment Room
Differential Temperature—High
≤ 277.0 °F for the RCIC Steam Line Tunnel
Temperature—High
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≤ 155.0 °F for the RCIC Steam Line Tunnel
Differential Temperature—High
The proposed change revises the Allowable
Values to the following:
≤ 297.0 °F for RCIC Equipment Room
Temperature—High
≤ 188.0 °F for RCIC Equipment Room
Differential Temperature—High
≤ 267.0 °F for the RCIC Steam Line Tunnel
Temperature—High
≤ 163.0 °F for the RCIC Steam Line Tunnel
Differential Temperature—High
The proposed change is a result of revising
the setpoint calculation for the subject
temperature instruments based on the current
analytical limit. The proposed changes will
revise TS Table 3.3.6.1–1 Allowable Values
for the subject four RCIC system isolation
functions and will provide assurance that the
RCIC system will perform as designed. The
proposed revision to the Allowable Values
does not change any of the RCIC system leak
detection isolation actuation setpoints.
Margin of safety is established by the
design and qualification of plant equipment,
the operation of the plant within analyzed
limits, and the point at which protective or
mitigative actions are being initiated. The
proposed change does not alter these
considerations. The proposed allowable
values will still ensure that the results of the
accident analysis remain valid.
Based on this information, the proposed
changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Bradley J.
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
Exelon Generation Company, LLC,
Docket Nos. 50–373 and 50–374, LaSalle
County Station, Units 1 and 2, LaSalle
County, Illinois
Date of amendment request: April 4,
2006.
Description of amendment request:
The proposed amendment request will
add one NRC approved topical report
reference to the list of analytical
methods in Technical Specification (TS)
5.6.5, ‘‘Core Operating Limits Report
(COLR),’’ that can be used to determine
core operating limits, and will delete
seven obsolete references from the same
TS Section.
The proposed changes are:
1. Add an NRC previously approved
Topical Report ANF–1358(P)(A), Revision 3,
‘‘The Loss of Feedwater Heating Transient in
Boiling Water Reactors,’’ (LOFWH), which
will list FRA–ANP method for evaluating the
LOFWH transient.
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2. Delete seven references describing
previously approved Global Nuclear Fuel
(GNF) and FRA–ANP methodologies for the
analyses of ATRIUM–9B and GE9 fuel. Both
of these fuel types have been or will be
completely discharged from both Lasalle
County Station (LSCS) reactors after the
loading of ATRIUM–10 fuel during the LSCS
Unit 2 refuel outage currently scheduled to
begin in February 2007 (i.e., L2R11).
The proposed changes support the
continued irradiation of ATRIUM–10
fuel in the LSCS reactors and the use of
the NRC-approved analytical
methodology for evaluation of LOFWH
transients.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Technical Specification (TS) 5.6.5 lists
NRC-approved analytical methods used at
LaSalle County Station (LSCS) to determine
core operating limits. The proposed changes
will add an NRC-approved topical report
reference to the list of administratively
controlled analytical methods in TS 5.6.5,
‘‘Core Operating Limits Report (COLR),’’ that
can be used to determine core operating
limits, and delete seven obsolete references.
The addition of a Framatome ANP (FRA–
ANP) methodology to determine overall core
operating limits for future LSCS core
configurations was approved by the NRC in
Reference 2. LSCS Unit 2 will continue to
load Framatome ANP ATRIUM–10 fuel
during the Unit 2 Refueling Outage 11
currently scheduled for February 2007. The
proposed change to TS 5.6.5 will add a FRA–
ANP methodology as a reference to
determine core operating limits for loss of
feedwater heater (LOFWH) conditions. Thus,
the proposed change will allow LSCS to use
the most recent FRA–ANP methodology for
analysis of LOFWH conditions.
The addition and deletion of approved
analytical methods in TS Section 5.6.5 has no
effect on any accident initiator or precursor
previously evaluated and does not change the
manner in which the core is operated. The
NRC-approved methods ensure that the
output accurately models predicted core
behavior, have no effect on the type or
amount of radiation released, and have no
effect on predicted offsite doses in the event
of an accident. Additionally, the NRCapproved methods do not change any key
core parameters that influence any accident
consequences. Thus, the proposed changes
do not have any effect on the probability of
an accident previously evaluated.
The methodology conservatively
establishes acceptable core operating limits
such that the consequences of previously
analyzed events are not significantly
increased.
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The proposed changes in the list of
analytical methods do not affect the ability of
LSCS to successfully respond to previously
evaluated accidents and does not affect
radiological assumptions used in the
evaluations. Thus, the radiological
consequences of any accident previously
evaluated are not increased.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes to TS Section 5.6.5
do not affect the performance of any LSCS
structure, system, or component credited
with mitigating any accident previously
evaluated. The NRC-approved analytical
methodology for evaluating LOFWH
transients will not affect the control
parameters governing unit operation or the
response of plant equipment to transient
conditions. The proposed changes do not
introduce any new modes of system
operation or failure mechanism.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do the proposed changes involve a
significant reduction in the margin of safety?
Response: No.
The proposed changes will add a reference
to the list of analytical methods in TS 5.6.5
that can be used to determine core operating
limits and delete seven obsolete references.
The proposed changes do not modify the
safety limits or setpoints at which protective
actions are initiated and do not change the
requirements governing operation or
availability of safety equipment assumed to
operate to preserve the margin of safety.
Therefore, the proposed changes provide an
equivalent level of protection as that
currently provided.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
Based on the above information, EGC
concludes that the proposed amendment
presents no significant hazards consideration
under the standards set forth in 10 CFR
50.92(c), and, accordingly, a finding of ‘‘no
significant hazards consideration’’ is
justified.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Thomas S.
O’Neill, Associate General Counsel,
Exelon Generation Company, LLC, 4300
Winfield Road, Warrenville, IL 60555.
NRC Branch Chief: Daniel S. Collins.
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15:41 Aug 14, 2006
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Exelon Generation Company, LLC, and
PSEG Nuclear LLC, Docket Nos. 50–277
and 50–278, Peach Bottom Atomic
Power Station, Units 2 and 3, York and
Lancaster Counties, Pennsylvania
Date of application for amendments:
June 8, 2006.
Description of amendment request:
The proposed changes modify Technical
Specifications (TSs) 3.1.3, ‘‘Control Rod
OPERABILITY’’; 3.1.6, ‘‘Rod Pattern
Control’’; 3.3.2.1, ‘‘Control Rod Block
Instrumentation’’; 3.10.7, ‘‘Control Rod
Testing—Operating’’; and 3.10.8,
‘‘SHUTDOWN MARGIN (SDM) Test—
Refueling’’ to replace the current
references to banked position
withdrawal sequence (BPWS) with
references to ‘‘the analyzed rod position
sequence.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change modifies Technical
Specifications (TS) 3.1.3, ‘‘Control Rod
OPERABILITY’’; TS 3.1.6, ‘‘Rod Pattern
Control’’; TS 3.3.2.1, ‘‘Control Rod Block
Instrumentation’’; TS 3.10.7, ‘‘Control Rod
Testing—Operating’’, and; TS 3.10.8,
SHUTDOWN MARGIN (SDM) Test—
Refueling’’. The proposed change would
replace the current references to ‘‘Banked
Position Withdrawal Sequence (BPWS)’’ with
references to ‘‘the analyzed rod position
sequence’’. The use of the ‘‘the analyzed rod
position sequence’’ will continue to
minimize the consequences of an accident
previously evaluated including the Control
Rod Drop Accident (CRDA). Additionally,
the use of the words ‘‘the analyzed rod
position sequence’’ will provide an
equivalent level of protection during plant
startups and shutdowns and therefore will
not increase the consequences of an accident
previously evaluated.
Control rod patterns during startup and
shutdown conditions will continue to be
controlled by the operator and the Rod Worth
Minimizer (RWM) (LCO [limiting condition
of operation] 3.3.2.1, ‘‘Control Rod Block
Instrumentation’’), so that only specified
control rod sequences and relative positions
are allowed over the operating range of all
control rods inserted to 10% of Rated
Thermal Power. As a result of this change,
these sequences will continue to limit the
potential amount of reactivity addition that
could occur in the event of a Control Rod
Drop Accident (CRDA).
Accidents are initiated by the malfunction
of plant equipment, or the failure of plant
structures, systems, or components. The
proposed change will ensure that analyzed
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rod position sequences are developed to
minimize incremental control rod reactivity
worth in accordance with the ‘‘General
Electric Standard Application for Reactor
Fuel,’’ NEDE–24011–P–A–15 (GESTAR–II),
and U.S. Supplement, NEDE–24011–P–A–
15–US, September, 2005, NRC approved
methodology, and reviewed and approved in
accordance with the 10 CFR 50.59 process.
These analyzed rod position sequences will
limit the potential reactivity increase for a
postulated CRDA during reactor startups and
shutdowns below the Low Power Setpoint of
10% of Rated Thermal Power.
The proposed change will continue to
ensure that systems, structures and
components are capable of performing their
intended safety functions.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not affect the
assumed accident performance of the control
rods, nor any plant structure, system, or
component previously evaluated.
The proposed change does not involve the
installation of new equipment, and installed
equipment is not being operated in a new or
different manner. The change ensures that
control rods remain capable of performing
their safety functions. No set points are being
changed which would alter the dynamic
response of plant equipment. Accordingly,
no new failure modes are introduced.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change will ensure that
analyzed rod position sequences are
developed to minimize incremental control
rod reactivity worth in accordance with the
‘‘General Electric Standard Application for
Reactor Fuel,’’ NEDE–24011–P–A–15
(GESTAR–II), and U.S. Supplement, NEDE–
24011–P–A–15–US, September, 2005, NRC
approved methodology, and reviewed and
approved in accordance with the 10 CFR
50.59 process. The proposed change will not
adversely impact the plant’s response to an
accident or transient. All current safety
margins will be maintained. There are no
changes proposed which alter the set points
at which protective actions are initiated, and
there is no change to the operability
requirements for equipment assumed to
operate for accident mitigation.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
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amendment request involves no
significant hazards consideration.
Attorney for Licensee: Mr. Brad
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief (Acting): Brooke D.
Poole.
mstockstill on PROD1PC61 with NOTICES
FirstEnergy Nuclear Operating
Company, et al., Docket Nos. 50–334
and 50–412, Beaver Valley Power
Station, Unit Nos. 1 and 2 (BVPS–1
and 2), Beaver County, Pennsylvania
Date of amendment request: June 14,
2006.
Description of amendment request:
The amendments would incorporate the
results of a new spent fuel pool
criticality analysis documented in
WCAP–16518–P/WCAP–16518–NP,
‘‘Beaver Valley Unit 2 Spent Fuel Pool
Criticality Analysis,’’ Revision 1, May
2006 for the BVPS–2 spent fuel storage
pool. The revised criticality analysis
will permit utilization of vacant storage
locations dictated by the existing
Technical Specification (TS) storage
configurations in the BVPS–2 spent fuel
storage pool.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No. The relevant accidents
previously evaluated are limited to the fuel
handling and criticality accidents.
Administrative controls during fuel
fabrication ensure that the fuel is fabricated
to ensure proper loading of fuel in the fuel
assemblies. Administrative and operational
controls used to load fuel assemblies into the
spent fuel pool ensure the fuel assemblies are
stored in compliance with the allowed
storage configurations. Fuel handling is
performed under administrative controls and
physical limitations. These controls will
remain in effect and continue to protect
against criticality and fuel handling accidents
involving new storage configurations dictated
by the new analysis. There is therefore no
impact on the probability of fuel handling or
criticality accidents.
The new criticality analysis defines new
spent fuel storage configurations with new
enrichment and burnup limits. Integral Fuel
Burnable Absorber (IFBA) limits are used to
comply with the 1-out-of-4 configuration for
fresh fuel. The boron dilution evaluation that
supported Amendment [No.] 128 [February
11, 2002, Agencywide Documents Access
and Management System Accession No.
ML020020373], permitting credit for soluble
boron at BVPS Unit No. 2 continues to
remain valid. The new analysis demonstrates
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that keff remains below unity for the various
storage configurations considered with zero
soluble boron, and that keff remains less than
or equal to 0.95 for the entire pool with credit
for soluble boron under non-accident and
accident conditions with a 95% probability
at a 95% confidence level (95/95). Potential
consequences of accidents previously
analyzed remain unchanged.
The editorial changes made to the table
numbers and the LCO [Limiting Condition
for Operation] and Surveillance Requirement
wording do not impact probability or
consequences of an accident previously
evaluated.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No. The relevant types of
accidents previously evaluated are limited to
criticality and fuel handling accidents.
Although the new analysis will allow
utilization of additional storage capacity,
implementation of fuel loading
configurations and fuel handling activities
will continue to be performed under
administrative and operational controls. No
new or different activities are introduced as
a result of the proposed changes. The
utilization of additional storage capacity
within the allowances of the revised analysis
will introduce no new or other kind of
accident.
The editorial changes made to the table
numbers and the LCO and Surveillance
Requirement wording do not impact any
previously evaluated accident.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No. The margin to safety with
respect to analyzed accidents involves
maintaining keff through fuel storage
configurations and boron concentration
controls in the spent fuel pool. The boron
dilution evaluation that supported that
supported Amendment [No.] 128 permitting
credit for soluble boron at BVPS Unit No. 2
remains valid. The Amendment [No.] 128
evaluation concluded that a boron dilution
event is not credible for BVPS Unit No. 2.
The new analysis calculates the non-accident
soluble boron concentration to be less than
was determined in the Amendment [No.] 128
evaluation. Thus, there is no significant
reduction in a margin of safety because of the
new analysis and the conclusions of the
Amendment [No.] 128 dilution evaluation
remain valid.
Under accident conditions, the soluble
boron needed to maintain keff below 0.95
with the new storage configurations is less
than what is assumed in current analysis.
The proposed change does not involve a
significant reduction in a margin of safety for
accident conditions.
The editorial changes made to the table
numbers and the LCO and Surveillance
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46935
Requirement wording do not impact a margin
of safety.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mary O’Reilly,
FirstEnergy Nuclear Operating
Company, FirstEnergy Corporation, 76
South Main Street, Akron, OH 44308.
NRC Branch Chief: Richard J. Laufer.
FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–440,
Perry Nuclear Power Plant, Unit 1, Lake
County, Ohio
Date of amendment request: June 1,
2006.
Description of amendment request:
The proposed amendment would
modify Technical Specification 3.4.10,
‘‘Residual Heat Removal (RHR)
Shutdown Cooling System—Cold
Shutdown’’ by adding a default
Condition to address situations when an
RHR shutdown cooling subsystem
becomes inoperable in MODE 4 and,
within the completion time of 1 hour,
an alternate method of decay heat
removal can not be verified to be
available.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No. The proposed amendment
does not change the design of any structures,
systems or components (SSCs), and does not
affect the manner in which plant systems are
operated. It is a change to the Technical
Specifications only, to provide guidance to
plant operators on appropriate actions to
take, where no Technical Specification
guidance currently exists. Since the design of
plant SSCs is not changed and plant systems
and components are not operated in a
different manner, there is no change to
previously identified accident initiators, and
the proposed amendment would not impact
the probability of any of the previously
evaluated accidents in the Updated Safety
Analysis Report (USAR).
The USAR event that evaluates the
consequences of a loss of RHR Shutdown
Cooling is included in Section 15.2.9 entitled
‘‘Failure of RHR Shutdown Cooling’’. This
event examines the consequences of a loss of
not only an RHR shutdown cooling
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subsystem, but also the loss of the suction
source from the recirculation system leading
to both RHR Shutdown Cooling subsystems,
and a loss of offsite power. Even with these
multiple failures, this event is not one of the
limiting transients. As noted in Section
15.2.9.5, ‘‘Radiological Consequences,’’ there
are no fuel failures, and the consequences of
the event are much less than those for the
‘‘Main Steam Isolation Valve Closure’’
transient, which is evaluated with acceptable
results in USAR Section 15.2.4.5. Since the
proposed amendment only involves the
addition of a Required Action where no
guidance currently exists, and the design of
plant SSCs is not changed and plant systems
and components are not operated in a
different manner, the proposed amendment
does not affect the consequences of the
Section 15.2.9 analysis, nor does it affect the
ability of the installed RHR subsystems to
perform their shutdown cooling function.
The change adds a default Condition to
provide guidance to the operators in those
situations when a subsystem becomes
inoperable with the plant in MODE 4 and an
alternate cannot be verified to be available
within an hour, which does not impact the
consequences of the previously evaluated
accidents in the USAR.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No. This change to the required
Technical Specification actions does not
involve a change in the design function or
operation of plant SSCs. It does not introduce
credible new failure mechanisms,
malfunctions, or accident initiators not
considered in the existing plant design and
licensing basis.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No. This proposed amendment
only involves a change to the required
Technical Specification actions. It does not
involve a change in the evaluation and
analysis methods used to demonstrate
compliance with regulatory and licensing
requirements, and does not exceed or alter a
design basis or safety limit. The safety margin
before the change remains unchanged after
the proposed amendment.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David W.
Jenkins, Attorney, FirstEnergy
VerDate Aug<31>2005
15:41 Aug 14, 2006
Jkt 208001
Corporation, 76 South Main Street,
Akron, OH 44308.
NRC Branch Chief: Daniel S. Collins.
FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–440,
Perry Nuclear Power Plant, Unit 1, Lake
County, Ohio
Date of amendment request: June 1,
2006.
Description of amendment request:
The proposed amendment would
modify Technical Specification 3.4.9,
‘‘Residual Heat Removal (RHR)
Shutdown Cooling System—Hot
Shutdown,’’ to revise the Required
Actions when both RHR shutdown
cooling subsystems are inoperable in
MODE 3.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No. The proposed amendment
does not change the design of any structures,
systems or components (SSCs), and does not
affect the manner in which plant systems are
operated. It is a change to the Technical
Specifications only, to provide guidance to
plant operators on appropriate actions to
take, when both RHR shutdown cooling
subsystems are inoperable. Since the design
of plant SSCs is not changed and plant
systems and components are not operated in
a different manner, there is no change to
previously identified accident initiators, and
the proposed amendment would not impact
the probability of any of the previously
evaluated accidents in the Updated Safety
Analysis Report (USAR).
The USAR event that evaluates the
consequences of a loss of RHR Shutdown
Cooling is included in Section 15.2.9 entitled
‘‘Failure of RHR Shutdown Cooling.’’ This
event examines the consequences of a loss of
not only an RHR shutdown cooling
subsystem, but also the loss of the suction
source from the recirculation system leading
to both RHR Shutdown Cooling subsystems,
and a loss of offsite power. Even with these
multiple failures, this event is not one of the
limiting transients. As noted in Section
15.2.9.5, ‘‘Radiological Consequences,’’ there
are no fuel failures, and the consequences of
the event are much less than those for the
‘‘Main Steam Isolation Valve Closure’’
transient, which is evaluated with acceptable
results in USAR Section 15.2.4.5. Since the
proposed amendment only involves the
addition of a Required Action where no
guidance currently exists, and the design of
plant SSCs is not changed and plant systems
and components are not operated in a
different manner, the proposed amendment
does not affect the consequences of the
Section 15.2.9 analysis, nor does it affect the
ability of the installed RHR subsystems to
perform their shutdown cooling function.
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Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No. This change to the required
Technical Specification actions does not
involve a change in the design function or
operation of plant SSCs. It does not introduce
credible new failure mechanisms,
malfunctions, or accident initiators not
considered in the existing plant design and
licensing basis.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No. This proposed amendment
only involves a change to the required
Technical Specification actions. It does not
involve a change in the evaluation and
analysis methods used to demonstrate
compliance with regulatory and licensing
requirements, and does not exceed or alter a
design basis or safety limit. The safety margin
before the change remains unchanged after
the proposed amendment.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David W.
Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street,
Akron, OH 44308.
NRC Branch Chief: Daniel S. Collins.
PPL Susquehanna, LLC, Docket Nos. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1
and 2), Luzerne County, Pennsylvania
Date of amendment request: April 28,
2006.
Description of amendment request:
The proposed amendment would
change the SSES 1 and 2 Technical
Specifications (TSs) to modify the
standby liquid control system for single
loop pump operation and use of
enriched sodium pentaborate solution.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
Does the proposed change involve a
significant increase in the probability or
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consequences of an accident previously
evaluated?
Response: No.
The proposed changes revise Technical
Specification 3.1.7 for the Standby Liquid
Control (SLC) system to reflect new boron
weight-percent and enrichment
requirements. In addition, the change to
single pump operation reduces the required
SLC pump flow and discharge pressure
required to satisfy 10 CFR 50.62, thus
increasing the reliability of the system. The
changes do not otherwise alter the design or
operation of the SLC system, and the existing
design of the system is sufficient to support
operation with the enriched sodium
pentaborate solution. The SLC system is not
considered to be the initiator of any event
currently analyzed in the FSAR [Final Safety
Analysis Report]. Therefore, the proposed
changes do not increase the probability of a
previously evaluated accident.
The SSES ATWS [anticipated transient
without scram] analysis was performed using
standard accepted assumptions, inputs, and
codes. That analysis, which demonstrated
that the acceptance criteria for peak vessel
pressure, peak cladding temperature, peak
local cladding oxidation, peak suppression
pool temperature, and peak containment
pressure, established the requirements for the
proposed boron weight-percent and
concentration, and pump flow rate. The
analysis assumed the use of only a single
pump, versus two pumps. The results of the
analysis are that no fission product barriers
are adversely challenged, and the
radiological consequences of previously
evaluated accidents (i.e., ATWS) are not
increased.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes revise Technical
Specification 3.1.7 for the SLC system to
reflect new boron weight-percent and
enrichment requirements. In addition, the
change to single pump operation reduces the
required SLC pump flow and discharge
pressure required to satisfy 10 CFR 50.62,
thus increasing the reliability of the system.
A new Surveillance Requirement (SR
3.1.7.10) is also added to verify the correct
solution enrichment prior to addition of
inventory to the SLC tank. The changes do
not otherwise alter the design or operation of
the SLC system, and the existing design of
the system is sufficient to process the
enriched sodium pentaborate solution. With
the exception of these changes, no other
physical changes to plant structures or
systems are proposed. Thus, the proposed
changes do not create a new initiating event
for the spectrum of events currently
postulated in the FSAR.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
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Response: No.
The proposed changes revise Technical
Specification 3.1.7 for the SLC system to
reflect new boron weight-percent and
enrichment requirements. In addition, the
change to single pump operation reduces the
required SLC pump flow and discharge
pressure required to satisfy 10 CFR 50.62,
thus increasing the reliability of the system.
The changes do not otherwise alter the
design or operation of the SLC system, and
the existing design of the system is sufficient
to process the enriched sodium pentaborate
solution.
The analysis was performed using standard
accepted assumptions, inputs, and codes.
That analysis, which demonstrated that
ATWS acceptance criteria are satisfied,
established the requirements for the
proposed boron weight-percent and
concentration, and pump flow rate. Further,
the analysis assumed only a single pump is
in operation verses two pumps. The
evaluation demonstrated that the SLC system
meets this post-LOCA [loss-of-coolant
accident] suppression pool pH control design
function.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Bryan A. Snapp,
Esquire, Assoc. General Counsel, PPL
Services Corporation, 2 North Ninth St.,
GENTW3, Allentown, PA 18101–1179.
NRC Branch Chief: Richard J. Laufer.
Tennessee Valley Authority, Docket No.
50–259 , Browns Ferry Nuclear Plant,
Unit 1, Limestone County, Alabama
Date of amendment request: October
12, 2004.
Description of amendment request: As
part of Nuclear Regulatory
Commission’s (NRC) approval of the
Improved Technical Specifications for
Browns Ferry Nuclear Plant, Unit 1, by
Amendment No. 234, NRC imposed
License Condition 2.C(4) to ensure that
the required analyses and modifications
needed to support the Technical
Specification (TS) changes made by
License Amendment No. 234 and any
subsequent TS changes, were completed
by licensee prior to entering the mode
for which the TS applies. The proposed
amendment would remove this license
condition from the license.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
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1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed amendment does not affect
any precursors for accidents described in
Chapter 14 of the Browns Ferry Updated
Final Safety Analysis Report (UFSAR). The
proposed amendment does not change the
conditions, operating configurations, or
minimum amount of operating equipment
assumed in the safety analysis for accident
mitigation. No changes are proposed in plant
protection or which create new modes of
plant operation. Therefore, the proposed
amendment does not involve a significant
increase in the probability or consequences
of an accident previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed amendment does not
introduce new equipment, which could
create a new or different kind of accident. No
new external threats, release pathways, or
equipment failure modes are created.
Therefore, the implementation of the
proposed amendment will not create a
possibility for an accident of a new or
different type than those previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed amendment does not impact
the redundancy or availability of equipment
credited in the response to accidents
described in Chapter 14 of the UFSAR. For
these reasons, the proposed amendment does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: L. Raghavan.
Tennessee Valley Authority, Docket No.
50–259, Browns Ferry Nuclear Plant,
Unit 1, Limestone County, Alabama
Date of amendment request: May 1,
2006 (TS–455).
Description of amendment request:
The proposed amendment would revise
the numeric values of the safety limit
minimum critical power ratio (SLMCPR)
in the Technical Specification (TS)
Section 2.1.1.2 for single and two
reactor recirculation loop operation to
incorporate the results of the Browns
Ferry Nuclear Plant, Unit 1 Cycle 7
SLMCPR analysis.
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Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
fuel design and licensing criteria. The
SLMCPR remains high enough to ensure that
greater than 99.9 percent of all fuel rods in
the core are expected to avoid transition
boiling if the limit is not violated, thereby
preserving the fuel cladding integrity.
Therefore, the proposed TS change does not
involve a reduction in the margin of safety.
1. Does the proposed Technical
Specification change involve a significant
increase in the probability or consequences
of an accident previously evaluated?
Response: No.
The proposed amendment establishes a
revised SLMCPR value for single and two
recirculation loop operation. The probability
of an evaluated accident is derived from the
probabilities of the individual precursors to
that accident. The proposed SLMCPR values
preserve the existing margin to transition
boiling and the probability of fuel damage is
not increased. Since the change does not
require any physical plant modifications or
physically affect any plant components, no
individual precursors of an accident are
affected and the probability of an evaluated
accident is not increased by revising the
SLMCPR values.
The consequences of an evaluated accident
are determined by the operability of plant
systems designed to mitigate those
consequences. The revised SLMCPR values
have been determined using NRC-approved
methods and procedures. The basis of the
MCPR Safety Limit is to ensure no
mechanistic fuel damage is calculated to
occur if the limit is not violated. These
calculations do not change the method of
operating the plant and have no effect on the
consequences of an evaluated accident.
Therefore, the proposed TS change does not
involve an increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed Technical
Specification change create the possibility of
a new or different kind of accident from any
accident previously evaluated?
Response: No.
The proposed license amendment involves
a revision of the SLMCPR value for single
and two recirculation loop operation based
on the results of an analysis of the Unit 1
Cycle 7 core. Creation of the possibility of a
new or different kind of accident would
require the creation of one or more new
precursors of that accident. New accident
precursors may be created by modifications
of the plant configuration, including changes
in the allowable methods of operating the
facility. This proposed license amendment
does not involve any modifications of the
plant configuration or changes in the
allowable methods of operation. Therefore,
the proposed TS change does not create the
possibility of a new or different kind of
accident previously evaluated.
3. Does the proposed Technical
Specification change involve a significant
reduction in a margin of safety?
Response: No.
The margin of safety as defined in the TS
bases will remain the same. The new
SLMCPR values were calculated using
referenced fuel vendor methods and
procedures, which are in accordance with the
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC (Acting) Branch Chief: L.
Raghavan.
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Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton
County, Tennessee
Date of amendment request: July 6,
2006 (TS–06–04).
Description of amendment request:
The proposed amendment would revise
the Technical Specifications (TS) for the
Sequoyah Nuclear Plant, Units 1 and 2.
Action a.1 of TS 3.1.3.2, ‘‘Position
Indication Systems—Operating,’’
requires the verification of rod position
by use of the moveable incore detectors.
Tennessee Valley Authority (the
licensee, TVA) is proposing a revision to
TS 3.1.3.2 to allow the position of the
control and shutdown rods to be
monitored by a means other than the
moveable incore detectors. The
amendment will provide a less
burdensome monitoring method should
problems with the analog rod position
indication (ARPI) system be
experienced. When a recurring problem
in the system requires the monitoring of
a rod’s position by the alternate means,
TVA plans to continue unit operation
and to use the alternate means until the
unit enters Mode 5 and repairs to the
system can safely be implemented.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change provides an
alternative method for the monitoring of the
position of a rod once the position of the rod
is verified using the moveable incore detector
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system. The proposed monitoring of rod
control system parameters provides a
reasonably similar approach to rod position
monitoring as that provided by the movable
incore detector system. In particular, the
ability to immediately detect a rod drop or
misalignment is not directly provided by the
movable incore detector system or by the
monitoring of rod control system parameters.
Additionally, neither the movable incore
detector system, nor the monitoring of rod
control system parameters, provides the
capability to verify rod position following a
reactor trip or shutdown. Therefore, the
monitoring of rod control system parameters,
in lieu of the use of the movable incore
detector system, provides an equivalent and
acceptable method of monitoring rod
position while a position indicator is
inoperable.
The proposed change does not alter plant
equipment that is considered to have the
potential to alter the probability of an
accident. The affected components are for
monitoring only and do not actively affect
equipment that interacts with the control of
the reactor. Likewise, the affected
components are for monitoring and provide
an equivalent level of indication of rod
position as the current action. This maintains
an acceptable level of rod position indication
for normal plant operations, as well as post
accident mitigation actions. Therefore, the
proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
As described above, the proposed change
provides only an alternative method of
monitoring the position of a rod. No new
accident initiators are introduced by the
proposed alternative manner of performing
rod position monitoring. The proposed
change does not affect the reactor protection
system or the reactor control system. Hence,
no new failure modes are created that would
cause a new or different kind of accident
from any accident previously evaluated.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The rod position indicators are required to
determine control rod positions and thereby
ensure compliance with the control rod
alignment and insertion limits. The proposed
change does not alter the requirement to
determine rod position but provides an
alternative method for monitoring the
position of the affected rod after the position
of the rod is verified using the moveable
incore detector system. As a result, the initial
conditions of the accident analysis are
preserved. The components affected by the
alternate rod monitoring will not affect plant
setpoints utilized for automatic mitigation of
accident conditions or other equipment
necessary for accident mitigation.
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Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L.
Marshall, Jr.
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Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton
County, Tennessee
Date of amendment request: July 12,
2006 (TS–06–03).
Description of amendment request:
The proposed amendment would revise
the limiting condition for operation for
the Sequoyah Nuclear Plant, Units 1 and
2, Technical Specification (TS) Section
3.7.5, ‘‘Ultimate Heat Sink.’’ This
revision would change the minimum
ultimate heat sink (UHS) water
elevation in TS 3.7.5.a from 670 feet to
674 feet. The essential raw cooling
water (ERCW) temperature requirement
in TS 3.7.5.b would be increased from
83 degrees Fahrenheit (°F) to 87 °F. The
conditional requirements of TS 3.7.5.c
would no longer be required and would
be deleted by the proposed change. This
change would also delete a footnote that
established a temporary UHS
temperature limit of 87 °F through
September 30, 1995. These proposed
changes are supported by a combination
of design basis re-analysis, bounding
analysis, and sensitivity analysis of the
ERCW system, the UHS, and supported
systems.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change to increase the UHS
maximum temperature and the minimum
water level does not alter the function,
design, or operating practices for plant
systems or components. One exception is the
elimination of non-safety-related station air
compressor loads located in the turbine
building. The UHS is utilized to remove heat
loads from plant systems during normal and
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accident conditions. This function is not
expected or postulated to result in the
generation of any accident and continues to
adequately satisfy the associated safety
functions with the proposed changes.
Therefore, the probability of an accident
presently evaluated in the safety analyses
will not be increased because the UHS
function does not have the potential to be the
source of an accident. The heat loads that the
UHS is designed to accommodate have been
evaluated for functionality with the higher
temperature and elevation requirements. The
result of these evaluations is that there is
existing margins associated with the systems
that utilize the UHS for normal and accident
conditions. These margins are sufficient to
accommodate the postulated normal and
accident heat loads with the proposed
changes to the UHS. Since the safety
functions of the UHS are maintained, the
systems that ensure acceptable offsite dose
consequences will continue to operate as
designed. Therefore, the proposed change
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The UHS function is not an initiator of any
accident and only serves as a heat sink for
normal and upset plant conditions. By
allowing the proposed change in the UHS
temperature and elevation requirements, only
the parameters for UHS operation are
changed while the safety functions of the
UHS and systems that transfer the heat sink
capability continue to be maintained. The
UHS function provides accident mitigation
capabilities and does not reflect the potential
for accident generation. Therefore, the
possibility for creating a new or different
kind of accident is not created because the
UHS is only utilized for heat removal
functions that are not a potential source for
accident generation. Therefore, the proposed
change does not create the possibility of a
new or different kind of accident from any
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change has been evaluated
for systems that are needed to support
accident mitigation functions as well as
normal operational evolutions. Operational
margins were found to exist in the systems
that utilize the UHS capabilities such that
these proposed changes will not result in the
loss of any safety function necessary for
normal or accident conditions. The ERCW
system has excess flow margins that will
accommodate the increased flows necessary
for the proposed temperature increase. While
operating margins have been reduced by the
proposed changes, safety margins have been
maintained as assumed in the accident
analyses for postulated events.
Additionally, the proposed changes do not
require the modification of component
setpoints utilized for automatic mitigation of
accident conditions or other equipment
necessary for accident mitigation. Therefore,
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a significant reduction in the margin to safety
is not created by this proposed change.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: L. Raghavan.
Tennessee Valley Authority, Docket No.
50–390, Watts Bar Nuclear Plant, Unit 1,
Rhea County, Tennessee
Date of amendment request: June 16,
2006 (WBN–TS–06–04).
Description of amendment request:
The proposed amendment change
would revise Technical Specification
(TS) 5.7.2.11, ‘‘Inservice Testing
Program,’’ to remove ‘‘applicable
supports’’ from the Inservice Testing
(IST) Program and revise the IST
Program for pumps and valves to meet
the requirements of the latest Edition
and Addenda of the American Society
of Mechanical Engineers (ASME) Code
approved by the NRC for use on the date
12-months prior to the start of the 10year IST Interval. For the Watts Bar
Nuclear Plant (WBN), Unit 1, the second
10-year IST Interval will begin on
December 27, 2006. The ASME Code
that was approved in 10 CFR
50.55a(f)(4) for use on December 27,
2005, was ASME Operations and
Maintenance (OM) Code, 2001 Edition,
with Addenda through 2003. The
proposed change provides consistency
with the requirements in 10 CFR
50.55a(f)(4) by replacing the reference to
ASME Boiler and Pressure Vessel Code,
Section XI, with ASME OM Code. This
proposed change is based on Technical
Specification Task Force (TSTF)
Traveler 479, Revision 0, ‘‘Changes to
Reflect Revision of 10 CFR 50.55a.’’
TSTF 279–A, Revision 0, ‘‘Remove
‘applicable supports’ from Inservice
Testing Program,’’ was approved by
NRC and incorporated into Revision 2 of
NUREG–1431, ‘‘Standard Technical
Specification Westinghouse Plants.’’ In
addition, the proposed amendment
would add provisions to TS 5.7.2.11,
Item b, to only apply Surveillance
Requirement 3.0.2 to those IST
frequencies of 2 years or less.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
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licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change revises Technical
Specification Section 5.7.2.11 for WBN Unit
1 to conform to the requirements of 10 CFR
50.55a(f)(4) regarding the inservice testing of
pumps and valves which are classified as
ASME Code Class 1, 2, and 3.
ASME has in the last several years,
transitioned the requirements for inservice
testing of pumps and valves out of ASME
Section XI and into a separate, stand alone
code entitled the ‘‘Code for Operation and
Maintenance of Nuclear Power Plants,’’
(ASME OM Code). The ASME OM Code has
been endorsed by the NRC in 10 CFR 50.55a
and is the Code that will be required for
inservice testing of pumps and valves during
the WBN Second Inservice Interval. The
proposed change incorporates revisions to
the ASME Code that result in a net
improvement in the measures for testing
pumps and valves. The proposed change also
deletes the reference to supports from the
Inservice Testing Program as supports are
already inspected under the Inservice
Inspection Program.
The proposed changes do not involve any
hardware changes, nor do the changes affect
the probability of any event initiators. There
will be no change to normal plant operating
parameters, accident mitigation capabilities,
or accident analysis assumptions or inputs.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change revises the Technical
Specifications to delete the reference to
‘‘applicable supports’’ from the Inservice
Testing Program and to incorporate the latest
Code requirements in 10 CFR 50.55a(f)(4) for
Code Class 1, 2, and 3 pumps and valves for
WBN’s next ten year interval. The testing
requirements are similar and reflect the same
type testing. Valves are still stroke timed;
remote position indicators are still verified to
be accurate; seat leakage measurements of
critical valves are still performed; relief
valves still have their setpoints and seat
leakages verified; pumps are still tested for
hydraulic performance and mechanical
condition; check valves are verified to open
and close properly; and supports are still
inspected under the appropriate inspection
program.
The proposed changes do not involve a
modification to the physical configuration of
the plant or change methods governing
normal plant operation. No test methods are
added or deleted. Therefore, the proposed
change does not create the possibility of a
new or different kind of accident from any
previously evaluated.
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3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change revises the TS for
consistency with the Standard Technical
Specification and with the requirements in
10 CFR 50.55a(f)(4) regarding the inservice
testing of pumps and valves which are
classified as ASME Code Class 1, 2, and 3.
This change incorporates revisions to the
ASME Code that result in a net improvement
in the measures of testing. Incorporation of
the ASME OM Code does not alter the
limiting values and acceptance criteria used
to judge the continued acceptability of
components tested by the Inservice Testing
Program. Deletion of the reference to
supports in the Inservice Testing Program
does not alter the support inspection program
as the program is currently under the
Inservice Inspection Program. Since these
limits are not altered, the margin of safety is
not altered. Therefore, the proposed changes
do not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: L. Raghavan.
Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of amendment request: May 30,
2006.
Description of amendment request:
The amendment would revise
Surveillance Requirements (SRs) 3.5.2.8
and 3.6.7.1 in the Technical
Specifications (TSs), and delete the
footnote to the frequency for SR 3.5.2.5.
SR 3.5.2.8 would be revised by
replacing the phrase ‘‘trash racks and
screens’’ with the word ‘‘strainers.’’ This
reflects (1) the replacement of the
existing containment recirculation sump
suction inlet trash racks and screens
with strainers with significantly greater
effective surface area, and (2) the
resulting relocation of the recirculation
fluid pH control system in Refueling
Outage 15 schedule for the spring of
2007. The footnote to SR 3.5.2.5 would
be deleted because it is no longer
applicable to the TSs.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
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1. Do[es] the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
None of the changes impact the initiation
or probability of occurrence of any accident
[previously evaluated].
The consequences of accidents evaluated
in the FSAR [Final Safety Analysis Report for
the Callaway Plant] that could be affected by
this proposed change are those involving the
pressurization of the containment and
associated flooding of the containment and
recirculation of this fluid within the
Emergency Core Cooling System (ECCS) or
the Containment Spray System (CSS) (e.g.,
LOCAs [Loss-of-Coolant Accidents]). [The
containment sump trash racks and screens,
and the sump strainers that are replacing the
trash racks and screens are not initiators of
accidents.]
Although the configurations of the existing
sump screen and the replacement strainer
assemblies are different, they serve the same
fundamental purpose of passively removing
debris from the suction of the supported
system pumps. Removal of trash racks does
not impact the adequacy of the pump NPSH
[net positive suction head] assumed in the
safety analyses. Likewise the change does not
reduce the reliability of any supported
systems or introduce any new system
interactions. The greatly increased surface
area of the new strainer is designed to reduce
head loss [at the containment sump] and
reduce the approach velocity at the strainer
face significantly, decreasing the risk of
impact from large debris entrained in the
sump flow stream.
The recirculation fluid pH control system
storage baskets serve a passive function to
provide a buffering agent to neutralize the
sump solution. The redesign and relocation
of the storage baskets are considered a like
kind replacement. The baskets will be
located within the flood plain and will
continue to ensure that the buffering agent is
dissolved in the sump fluid to ensure an
equilibrium pH ≥ 7.1. Failure of a basket
would not initiate an accident. The ECCS and
CSS will continue to function in a manner
consistent with the plant design basis.
As such, the proposed change to the
Technical Specifications Surveillance
Requirements does not involve a significant
increase in the probability or consequences
of an accident previously evaluated. The
installed quantity of trisodium phosphate
Crystalline will provide a minimum
equilibrium sump pH of 7.1 following
dissolution and mixing. [Deleting the
footnote to SR 3.5.2.5 is an administrative
change to remove a one-time required
verification that has already been performed
and is no longer a requirement in the current
TSs.] Therefore, there is not a significant
increase in the probability or consequences
of an accident previously evaluated.
2. Do[es] the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The containment recirculation sump
strainers and recirculation fluid pH control
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system are passive systems used for accident
mitigation. As such, they cannot be accident
initiators. Therefore, there is no possibility
that this change could create any accident of
any kind. [The containment recirculation
sump suction inlet trash racks and screens
are being replaced with a complex strainer
design with significantly larger effective
surface area to reduce head loss and reduce
the approach velocity at the strainer face
significantly, decreasing the risk of impact
from large debris entrained in the sump flow
stream. This will result in the recirculation
fluid pH control system being relocated.]
No new accident scenarios, transient
precursors, or limiting single failures are
introduced as a result of these changes. There
will be no adverse effect[s] or challenges
imposed on any safety-related system as a
result of these changes. The quantity of
trisodium phosphate crystalline will provide
a minimum equilibrium sump pH of ≥ 7.1
following dissolution and mixing. Therefore,
the possibility of a new or different type of
accident is not created.
There are no changes which would cause
the malfunction of safety-related equipment,
assumed to be operable in the accident
analyses, as a result of the proposed
Technical Specification changes. No new
equipment performance burdens are
imposed. The possibility of a malfunction of
safety-related equipment with a different
result is not created. [Deleting the footnote to
SR 3.5.2.5 is an administrative change to
remove a one-time required verification that
has already been performed and is no longer
a requirement in the current TSs.] Therefore,
the proposed change does not create the
possibility of a new or different kind of
accident from any previously evaluated.
3. Do[es] the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes do not adversely
affect any plant safety limits, setpoints, or
design parameters. The changes also do not
adversely affect the fuel, fuel cladding,
Reactor Coolant System (RCS), or
containment integrity. [The radiological dose
consequence acceptance criteria in the
Standard Review Plan for accidents will
continue to be met. Deleting the footnote to
SR 3.5.2.5 is an administrative change to
remove a one-time required verification that
has already been performed and is no longer
a requirement in the current TSs.] Therefore,
the proposed TS change does not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: John O’Neill,
Esq., Pillsbury Winthrop Shaw Pittman
LLP, 2300 N Street, NW., Washington,
DC 20037.
NRC Branch Chief: David Terao.
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Virginia Electric and Power Company,
Docket Nos. 50–338 and 50–339, North
Anna Power Station, Units No. 1 and
No. 2, Louisa County, Virginia
Date of amendment request: May 30,
2006, as supplemented by letter dated
June 30, 2006.
Description of amendment request:
The proposed amendments would
relocate the American Society for
Testing and Materials (ASTM) standard
being used to test the total particulate
concentration of the stored fuel oil to
the TS Bases. This proposed change is
described in TS Task force (TSTF)
Standard TS Change Traveler TSTF–
374–A, Rev. 0, ‘‘Revision to TS 5.5.13
and Associated TS Bases for Diesel Fuel
Oil.’’ In addition, the licensee has
proposed to use a ‘‘water and sediment
test’’ instead of the ‘‘clear and bright’’
test provided in TSTF–374.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do changes involve a significant increase
in the probability or consequences of an
accident previously evaluated?
The proposed change relocates the specific
ASTM reference from the Administrative
Controls Section of Technical Specifications
(TS) to a licensee-controlled document.
Relocating the specific ASTM Standard
reference from the TS to a licensee-controlled
document will not affect nor degrade the
ability of the EDGs [emergency diesel
generators] to perform their specified safety
function. Fuel oil quality will continue to
meet the current ASTM requirements for
particulate concentration.
The proposed change is administrative in
nature and does not adversely affect accident
initiators or precursors nor alter the design
assumptions, conditions, and configuration
of the facility or the manner in which the
plant is operated and maintained. The
proposed change does not alter or prevent the
ability of structures, systems or components
from performing their intended function to
mitigate the consequences on an initiating
event with the assumed acceptance limits.
The proposed change does not affect the
source term, containment isolation, or
radiological release assumptions used in
evaluating the radiological consequences of
an accident previously evaluated. Further,
the proposed change does not increase the
types and amounts of radioactive effluent
that may be released offsite, nor significantly
increase individual or cumulative
occupational/public radiation exposure.
Therefore, the change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Do changes create the possibility of a
new or different kind of accident from any
accident previously evaluated?
PO 00000
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46941
The proposed change relocates the specific
ASTM reference from the Administrative
Controls Section of Technical Specifications
to a licensee-controlled document.
The change does not involve a physical
alteration of the plant or a change in the
methods governing normal plant conditions.
In addition, the change does not impose any
new or different requirements or eliminate
any existing requirements. The change does
not alter assumptions made in the safety
analysis and licensing basis. Therefore, the
change does not create the possibility of a
new or different kind of accident from any
accident previously evaluated.
3. Do changes involve a significant
reduction in the margin of safety?
The proposed change relocates the specific
ASTM reference from the Administrative
Controls Section of TS to a licenseecontrolled document. The detail associated
with the specific ASTM standard reference is
not required to be in the TS to provide
adequate protection of the public health and
safety, since the TS still retain the
requirement for compliance with the
applicable ASTM standard.
The level of safety of facility operation is
unaffected by the proposed change since
there is no change in the intent of the TS
requirements of assuring fuel oil is of the
appropriate quality for EDG use. The
proposed change provides the flexibility
needed to maintain state-of-the-art
technology in fuel oil sampling and analysis
methodology.
The proposed change does not reduce a
margin of safety since it has no impact on
any transient or safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 50.92(c) are satisfied.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Attorney for licensee: Lillian M.
Cuoco, Esq., Senior Counsel, Dominion
Resources Services, Inc., Millstone
Power Station, Building 475, 5th Floor,
Rope Ferry Road, Rt. 156, Waterford,
Connecticut 06385.
NRC Branch Chief: Evangelos C.
Marinos.
Virginia Electric and Power Company,
Docket Nos. 50–280 and 50–281, Surry
Power Station, Unit Nos. 1 and 2, Surry
County, Virginia
Date of amendment request: May 26,
2006.
Description of amendment request:
Item 1: The proposed amendments
would revise the Technical
Specification (TS) requirements related
to Reactor Coolant System (RCS) leakage
definitions and requirements and steam
generator tube integrity. The licensee
requested this change to implement TS
Task Force (TSTF) Standard TS Change
Traveler, TSTF–449, ‘‘Steam Generator
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Tube Integrity,’’ (TSTF–449, Rev. 4).
Item 2: In addition, in its submittal
dated May 26, 2006, the licensee
proposed minor deviations from the TS
changes described in TSTF–449, Rev. 4,
to provide consistency with Surry’s
custom TSs.
Basis for proposed no significant
hazards consideration determination:
Item 1: As required by 10 CFR 50.91(a),
an analysis of the issue of no significant
hazards consideration is presented
below:
1. The Proposed Change Does Not Involve
a Significant Increase in the Probability or
Consequences of an Accident Previously
Evaluated.
The proposed change requires a SG
Program that includes performance criteria
that will provide reasonable assurance that
the SG tubing will retain integrity over the
full range of operating conditions (including
startup, operation in the power range, hot
standby, cooldown and all anticipated
transients included in the design
specification). The SG performance criteria
are based on tube structural integrity,
accident induced leakage, and operational
leakage.
A SG tube rupture (TR) event is one of the
design basis accidents that are analyzed as
part of a plant’s licensing basis. In the
analysis of a SGTR event, a bounding
primary to secondary leakage rate equal to
the operational leakage rate limits in the
licensing basis plus the leakage rate
associated with a double-ended rupture of a
single tube is assumed.
For other design basis accidents such as
main steam line break (MSLB), rod ejection,
and reactor coolant pump locked rotor the
tubes are assumed to retain their structural
integrity (i.e., they are assumed not to
rupture). These analyses typically assume
that primary to secondary leakage for all SGs
is 1 gallon per minute or increases to 1 gallon
per minute as a result of accident induced
stresses. The accident induced leakage
criterion introduced by the proposed changes
accounts for tubes that may leak during
design basis accidents. The accident induced
leakage criterion limits this leakage to no
more than the value assumed in the accident
analysis.
The SG performance criteria proposed
change to the TS identify the standards
against which tube integrity is to be
measured. Meeting the performance criteria
provides reasonable assurance that the SG
tubing will remain capable of fulfilling its
specific safety function of maintaining
reactor coolant pressure boundary integrity
throughout each operating cycle and in the
unlikely event of a design basis accident. The
performance criteria are only a part of the SG
Program required by the proposed change to
the TS. The program, defined by NEI 97–06,
Steam Generator Program Guidelines,
includes a framework that incorporates a
balance of prevention, inspection, evaluation,
repair, and leakage monitoring. The proposed
changes do not, therefore, significantly
increase the probability of an accident
previously evaluated.
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Jkt 208001
The consequences of design basis accidents
are, in part, functions of the DOSE
EQUIVALENT 1–131 in the primary coolant
and the primary to secondary leakage rates
resulting from an accident. Therefore, limits
are included in the plant TS for operational
leakage and for DOSE EQUIVALENT 1–131
in primary coolant to ensure the plant is
operated within its analyzed condition. The
typical analysis of the limiting design basis
accident assumes that primary to secondary
leak rate after the accident is 1 gallon per
minute with no more than 500 gallons per
day in any one SG, and that the reactor
coolant activity levels of DOSE
EQUIVALENT 1–131 are at the TS values
before the accident.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary coolant chemistry controls. The
proposed approach updates the current TSs
and enhances the requirements for SG
inspections. The proposed change does not
adversely impact any other previously
evaluated design basis accident and is an
improvement over the current TSs.
Therefore, the proposed change does not
affect the consequences of a SGTR accident
and the probability of such an accident is
reduced. In addition, the proposed changes
do not affect the consequences of an MSLB,
rod ejection, or a reactor coolant pump
locked rotor event, or other previously
evaluated accident.
2. The Proposed Change Does Not Create
the Possibility of a New or Different Kind of
Accident from any Previously Evaluated.
The proposed performance based
requirements are an improvement over the
requirements imposed by the current [TS].
Implementation of the proposed SG Program
will not introduce any adverse changes to the
plant design basis or postulated accidents
resulting from potential tube degradation.
The result of the implementation of the SG
Program will be an enhancement of SG tube
performance. Primary to secondary leakage
that may be experienced during all plant
conditions will be monitored to ensure it
remains within current accident analysis
assumptions.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary or secondary coolant chemistry
controls. In addition, the proposed change
does not impact any other plant system or
component. The change enhances SG
inspection requirements.
Therefore, the proposed change does not
create the possibility of a new or different
type of accident from any accident
previously evaluated.
3. The Proposed Change Does Not Involve
a Significant Reduction in the Margin of
Safety.
The SG tubes in pressurized water reactors
are an integral part of the reactor coolant
pressure boundary and, as such, are relied
upon to maintain the primary system’s
pressure and inventory. As part of the reactor
coolant pressure boundary, the SG tubes are
unique in that they are also relied upon as
a heat transfer surface between the primary
and secondary systems such that residual
heat can be removed from the primary
system. In addition, the SG tubes isolate the
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radioactive fission products in the primary
coolant from the secondary system. In
summary, the safety function of an SG is
maintained by ensuring the integrity of its
tubes.
[SG] tube integrity is a function of the
design, environment, and the physical
condition of the tube. The proposed change
does not affect tube design or operating
environment. The proposed change is
expected to result in an improvement in the
tube integrity by implementing the SG
Program to manage SG tube inspection,
assessment, repair, and plugging. The
requirements established by the SG Program
are consistent with those in the applicable
design codes and standards and are an
improvement over the requirements in the
current TSs.
For the above reasons, the margin of safety
is not changed and overall plant safety will
be enhanced by the proposed change to the
TS.
The NRC staff has reviewed the
licensee’s incorporation of the above
analysis by reference and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Item 2: As required by 10 CFR
50.91(a), the licensee has provided its
analysis of the issue of no significant
hazards consideration, which is
presented below.
1. Involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The proposed changes involve adding a
new definition for RCS [reactor coolant
system] leakage and rewording certain [TSs]
for consistency with NUREG–1431, Revision
3. These changes do not involve any physical
plant modifications or changes in plant
operation; consequently, no technical
changes are being made to the existing TS.
As such, these changes are administrative in
nature and do not affect initiators of analyzed
events or assumed mitigation of accident or
transient events. Therefore, these changes do
not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Create the possibility of a new or
different kind of accident from any accident
previously evaluated.
The proposed changes involve adding a
new definition for RCS leakage and
rewording certain [TSs] for consistency with
NUREG–1431, Revision 3. These
administrative changes do not involve
physical alteration of the plant (no new or
different type of equipment will be installed)
or changes in methods governing normal
plant operation. The changes will not impose
any new or different requirements or
eliminate any existing requirements.
Therefore, these changes do not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
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3. Involve a significant reduction in a
margin of safety.
The proposed changes involve adding a
new definition for RCS leakage and
rewording certain [TS] for consistency with
NUREG–1431, Revision 3. The changes are
administrative in nature and will not involve
any technical changes. The changes will not
reduce a margin of safety because they have
no impact on any safety analysis
assumptions. Also, since these changes are
administrative in nature, no question of
safety is involved. Therefore, the changes do
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Lillian M.
Cuoco, Esq., Senior Counsel, Dominion
Resources Services, Inc., Millstone
Power Station, Building 475, 5th Floor,
Rope Ferry Road, Rt. 156, Waterford,
Connecticut 06385.
NRC Branch Chief: Evangelos C.
Marinos.
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Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
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15:41 Aug 14, 2006
Jkt 208001
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
Arizona Public Service Company, et al.,
Docket Nos. STN 50–528, STN 50–529,
and STN 50–530, Palo Verde Nuclear
Generating Station, Units Nos. 1, 2, and
3, Maricopa County, Arizona
Date of application for amendments:
May 26, 2005, as supplemented by
letters dated May 23 and June 20, 2006.
Brief description of amendments: The
amendments revised Technical
Specification (TS) 1.1, ‘‘Definitions,’’ TS
3.4.14, ‘‘RCS [reactor coolant system]
Operational Leakage,’’ TS 5.5.9, ‘‘Steam
Generator (SG) Program,’’ and TS 5.6.8,
‘‘Steam Generator Tube Inspection
Report,’’ and added a new specification,
TS 3.4.18, ‘‘Steam Generator (SG) Tube
Integrity.’’ The changes are consistent
with TS Task Force (TSTF) Change
TSTF–449, Revision 4, ‘‘Steam
Generator Tube Integrity.’’
Date of issuance: July 27, 2006.
Effective date: As of the date of
issuance to be implemented within 150
days from the date of issuance.
Amendment Nos.: Unit 1–161, Unit
2–161, Unit 3–161.
Facility Operating License Nos. NPF–
41, NPF–51, and NPF–74: The
amendments revised the Operating
Licenses and the Technical
Specifications for all three units.
Date of initial notice in Federal
Register: July 5, 2005 (70 FR 38714).
The May 23 and June 20, 2006,
supplemental letters provided
additional clarifying information, did
not expand the scope of the application
as originally noticed, and did not
change the NRC staff’s original proposed
no significant hazards consideration
determination.
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The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 27, 2006.
No significant hazards consideration
comments received: No.
Carolina Power & Light Company,
Docket No. 50–261, H. B. Robinson
Steam Electric Plant, Unit No. 2
(HBRSEP2), Darlington County, South
Carolina
Date of application for amendment:
January 21, 2005, as supplemented by
letters dated May 26, 2005, September
19, 2005, and March 31, 2006.
Brief description of amendment: The
amendment approves the
implementation of the alternative source
term methodology for a loss-of-coolant
accident at HBRSEP2.
Date of issuance: July 11, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No. 207.
Renewed Facility Operating License
No. DPR–23. Amendment does not
revise the Technical Specifications.
Date of initial notice in Federal
Register: May 24, 2005 (70 FR 29786).
The supplemental letters dated May 26,
2005, September 19, 2005, and March
31, 2006, provided clarifying
information that did not change the
initial proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 11, 2006.
No significant hazards consideration
comments received: No.
Dominion Energy Kewaunee, Inc. Docket
No. 50–305, Kewaunee Power Station,
Kewaunee County, Wisconsin
Date of application for amendment:
January 12, 2006, as supplemented by
letter dated June 2, 2006.
Brief description of amendment: The
amendment revises the existing steam
generator (SG) tube surveillance
program to be consistent with TS Task
Force (TSTF) Change TSTF–449,
Revision 4, ‘‘Steam Generator Tube
Integrity,’’ and the model safety
evaluation prepared by the Nuclear
Regulatory Commission (NRC) and
published in the Federal Register on
March 2, 2005 (70 FR 10298) under the
consolidated line item improvement
process (CLIIP).
Date of issuance: July 18, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 90 days.
Amendment No.: 188.
Facility Operating License No. DPR–
43: Amendment revised the Facility
Operating License and Technical
Specifications.
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Date of initial notice in Federal
Register: February 14, 2006 (71 FR
7806). The supplement letter contained
clarifying information and did not
change the initial no significant hazards
consideration determination, and did
not expand the scope of the orginal
Federal Register notice.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 18, 2006.
No significant hazards consideration
comments received: No.
Duke Power Company LLC, et al.,
Docket Nos. 50–413 and 50–414,
Catawba Nuclear Station, Units 1 and 2,
York County, South Carolina
Date of application for amendments:
October 27, 2004.
Brief description of amendments: The
amendments revised the facility
operating licenses by removal of license
condition 2.F, ‘‘Reporting
Requirements’’, with regard to
maximum power level, Updated Final
Safety Analysis Report, antitrust
conditions, fire protection, and
additional conditions.
Date of issuance: July 31, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 230, 226.
Renewed Facility Operating License
Nos. NPF–35 and NPF–52: Amendments
revised the licenses.
Date of initial notice in Federal
Register: July 5, 2005 (70 FR 38717).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated July 31, 2006.
No significant hazards consideration
comments received: No.
mstockstill on PROD1PC61 with NOTICES
Energy Northwest, Docket No. 50–397,
Columbia Generating Station, Benton
County, Washington
Date of application for amendment:
April 17, 2006.
Brief description of amendment: The
amendment allows a delay time for
entering a supported system Technical
Specification (TS) when the
inoperability is due solely to an
inoperable snubber, if risk is assessed
and managed consistent with the
program in place for complying with the
requirements of 10 CFR 50.65(a)(4).
Limiting Condition for Operation (LCO)
3.0.8 is added to the TS to provide this
allowance and define the requirements
and limitations for its use.
This change was proposed by the
industry’s Technical Specification Task
Force (TSTF) and is designated TSTF–
372, Revision 4. The NRC staff issued a
notice of opportunity for comment in
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15:41 Aug 14, 2006
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the Federal Register on November 24,
2004 (69 FR 68412), on possible
amendments concerning TSTF–372,
including a model safety evaluation and
model no significant hazards
consideration (NSHC) determination,
using the consolidated line item
improvement process. The NRC staff
subsequently issued a notice of
availability of the models for referencing
in license amendment applications in
the Federal Register on May 4, 2005 (70
FR 23252). The licensee affirmed the
applicability of the following NSHC
determination in its application dated
April 17, 2006.
Date of issuance: July 11, 2006.
Effective date: As of its date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment No.: 198.
Facility Operating License No. NPF–
21: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: May 9, 2006 (71 FR 26998).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 11, 2006.
No significant hazards consideration
comments received: No.
Entergy Nuclear Operations, Inc.,
Docket No. 50–247, Indian Point
Nuclear Generating Unit No. 2,
Westchester County, New York
Date of application for amendment:
September 26, 2005, as supplemented
by letter dated April 11, 2006.
Brief description of amendment: The
amendment revises the analysis method
used for the large-break loss-of-coolant
accident.
Date of issuance: July 24, 2006.
Effective date: As of the date of
issuance, and shall be implemented
within 60 days.
Amendment No.: 248.
Facility Operating License No. DPR–
26: The amendment revised the
Technical Specifications and License.
Date of initial notice in Federal
Register: November 8, 2005 (70 FR
67747). The April 11, 2006, supplement
provided additional information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the NRC
staff’s original proposed no significant
hazards consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 24, 2006.
No significant hazards consideration
comments received: No.
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Entergy Nuclear Operations, Inc.,
Docket No. 50–333, James A. FitzPatrick
Nuclear Power Plant (JAFNPP), Oswego
County, New York
Date of application for amendment:
January 26, 2006, as supplemented by
letter dated April 12, 2006.
Brief description of amendment: The
amendment approves the
implementation of the Boiling Water
Reactor Vessel and Internals Project
reactor pressure vessel integrated
surveillance program as the basis for
demonstrating the compliance of
JAFNPP with the requirements of
Appendix H to Title 10 of the Code of
Federal Regulations part 50.
Date of issuance: July 26, 2006.
Effective date: As of the date of
issuance, and shall be implemented
within 60 days.
Amendment No.: 285.
Facility Operating License No. DPR–
59: The amendment revised the
Updated Final Safety Analysis Report
and the License.
Date of initial notice in Federal
Register: March 14, 2006 (71 FR
13174). The April 12, 2006, supplement
provided additional information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the NRC
staff’s original proposed no significant
hazards consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 26, 2006.
No significant hazards consideration
comments received: No.
Entergy Operations, Inc., Docket No. 50–
368, Arkansas Nuclear One, Unit No. 2,
Pope County, Arkansas
Date of application for amendment:
September 19, 2005.
Brief description of amendment: The
amendment modified ANO–2
Surveillance Requirement TS 3.1.1.4,
‘‘Moderator Temperature Coefficient,’’
and allowed the use of WCAP–16011–
P–A, ‘‘Startup Test Activity Reduction
Program.’’
Date of issuance: August 2, 2006.
Effective date: As of the date of
issuance to be implemented within 30
days from the date of issuance.
Amendment No.: 265.
Renewed Facility Operating License
No. NPF–6: Amendment revised the
Technical Specifications/license.
Date of initial notice in Federal
Register: December 6, 2005 (70 FR
72671).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated August 2, 2006.
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No significant hazards consideration
comments received: No.
Entergy Operations, Inc., Docket No. 50–
368, Arkansas Nuclear One, Unit No. 2,
Pope County, Arkansas
Date of application for amendment:
September 19, 2005, as supplemented
by letters dated May 11 and June 19,
2006.
Brief description of amendment: The
amendment revised the existing steam
generator tube surveillance program to
be consistent with the U.S. Nuclear
Regulatory Commission’s approved
Technical Specification Task Force
Standard Technical Specification
Change Traveler, TSTF–449, ‘‘Steam
Generator Tube Integrity,’’ Revision 4.
TSTF–449 is part of the consolidated
line item improvement process.
Date of issuance: August 2, 2006.
Effective date: As of the date of
issuance to be implemented within 90
days from the date of issuance.
Amendment No.: 266.
Renewed Facility Operating License
No. NPF–6: Amendment revised the
Technical Specifications and Renewed
Facility Operating License.
Date of initial notice in Federal
Register: January 3, 2006 (71 FR 147).
The supplements dated May 11 and
June 19, 2006, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated August 2, 2006.
No significant hazards consideration
comments received: No.
mstockstill on PROD1PC61 with NOTICES
Exelon Generation Company, LLC,
Docket Nos. 50–254 and 50–265, Quad
Cities Nuclear Power Station, Units 1
and 2, Rock Island County, Illinois
Date of application for amendments:
January 25, 2006, as supplemented by
letter dated May 17, 2006.
Brief description of amendments: The
amendment revised the Quad Cities
licensing basis, as described in the
Updated Final Safety Analysis Report,
to allow the use of automatic load tap
changers to operate in automatic mode
on the reserve auxiliary transformers to
compensate for potential offsite power
voltage fluctuations, in order to ensure
that acceptable voltage is maintained for
safety-related equipment.
Date of issuance: July 24, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 30 days.
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15:41 Aug 14, 2006
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Amendment Nos.: 232 and 228.
Renewed Facility Operating License
Nos. DPR–29 and DPR–30: The
amendments revised the License.
Date of initial notice in Federal
Register: May 23, 2006 (71 FR 29678).
The May 17, 2006, supplement
contained clarifying information and
did not change the NRC staff’s initial
proposed finding of no significant
hazards consideration.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated July 24, 2006.
No significant hazards consideration
comments received: No.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of application for amendments:
August 23, 2005, as supplemented on
April 6, 2006.
Brief description of amendments: The
amendments extended the licensed lives
of the Diablo Canyon Power Plant, Unit
Nos. 1 and 2 reactors by the amount of
time the licensee had expended to
perform low-power testing of the
reactors prior to initial startup.
Date of issuance: July 17, 2006.
Effective date: As of its date of
issuance and shall be implemented
within 90 days of issuance.
Amendment Nos.: Unit 1–188; Unit
2–190.
Facility Operating License Nos. DPR–
80 and DPR–82: The amendments
revised the Facility Operating Licenses.
Date of initial notice in Federal
Register: October 11, 2005 (70 FR
59087). The April 6, 2006, supplemental
letter provided additional information
that clarified the application, and did
not expand the scope of the application
as originally noticed.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated July 17, 2006.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket No. 50–354,
Hope Creek Generating Station, Salem
County, New Jersey
Date of application for amendment:
August 4, 2005, as supplemented by
letters dated February 9, July 18, and
August 1, 2006.
Brief description of amendment: The
amendment revised Technical
Specification (TS) 3.7.1.3, ‘‘Ultimate
Heat Sink,’’ to permit continued plant
operation if the temperature of the
ultimate heat sink (UHS) exceeds 89 °F,
provided the UHS temperature averaged
over the previous 24-hour period is
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Fmt 4703
Sfmt 4703
46945
verified at least once per hour to be less
than or equal to 89 °F, and the UHS
temperature does not exceed a
maximum value of 91.4 °F.
Date of issuance: August 1, 2006.
Effective date: As of the date of
issuance, to be implemented within 60
days.
Amendment No.: 168.
Facility Operating License No. NPF–
57: This amendment revised the TSs.
Date of initial notice in Federal
Register: August 30, 2005 (70 FR
51382).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated August 1, 2006.
No significant hazards consideration
comments received: No.
R.E. Ginna Nuclear Power Plant, LLC,
Docket No. 50–244, R.E. Ginna Nuclear
Power Plant, Wayne County, New York
Date of application for amendment:
November 7, 2005, as supplemented on
May 5, 2006.
Brief description of amendment: The
amendment revises Technical
Specification 3.9.3, ‘‘Containment
Penetrations,’’ to allow an emergency
egress door, access door, or roll up door,
as associated with the equipment hatch
penetration, to be open, but capable of
being closed, during core alterations or
movement of irradiated fuel within
containment.
Date of issuance: July 26, 2006.
Effective date: As of the date of
issuance to be implemented within 60
days.
Amendment No.: 98.
Renewed Facility Operating License
No. DPR–18: Amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: January 3, 2006 (71 FR 154).
The May 5, 2006, letter provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 26, 2006.
No significant hazards consideration
comments received: No.
R.E. Ginna Nuclear Power Plant, LLC,
Docket No. 50–244, R.E. Ginna Nuclear
Power Plant, Wayne County, New York
Date of application for amendment:
November 18, 2005.
Brief description of amendment: The
amendment revises the frequency in
Technical Specification Surveillance
Requirement 3.6.6.15, which verifies
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that each containment spray nozzle is
unobstructed. The frequency is changed
from ‘‘10 years’’ to ‘‘following
maintenance which could result in
nozzle blockage.’’
Date of issuance: July 31, 2006.
Effective date: As of the date of
issuance to be implemented within 60
days.
Amendment No.: 99.
Renewed Facility Operating License
No. DPR–18: Amendment revised the
Technical Specifications and the
License.
Date of initial notice in Federal
Register: January 3, 2006 (71 FR 154).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 31, 2006.
No significant hazards consideration
comments received: No.
Tennessee Valley Authority, Docket No.
50–259 Browns Ferry Nuclear Plant,
Unit 1, Limestone County, Alabama
Date of application for amendment:
December 6, 2004 (TS 428) as
supplemented by letter dated June 16,
2005.
Brief description of amendment: The
amendment revised the reactor vessel
Pressure-Temperature curves depicted
in the Technical Specification (TS)
Figure 3.4.9–1 and adds a new TS
Figure 3.4.9–2.
Date of issuance: July 26, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment No.: 256.
Facility Operating License No. DPR–
33: Amendment revised the TS.
Date of initial notice in Federal
Register: January 18, 2005 (70 FR
2899). The supplement dated June 16,
2005, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 26, 2006.
No significant hazards consideration
comments received: No.
Specification Surveillance
Requirements to increase the minimum
required average ice basket weight, thus,
increasing the corresponding total
weight of the stored ice in the WBN ice
condenser. The changes to the ice basket
and total ice weights are due to the
additional energy associated with the
Replacement Steam Generators.
Date of issuance: July 25, 2006.
Effective date: As of the date of
issuance and shall be implemented
prior to Mode 4 at startup to begin Cycle
8 fuel cycle.
Amendment No. 62.
Facility Operating License No. NPF–
90: Amendment revises the Technical
Specifications.
Date of initial notice in Federal
Register: February 14, 2006 (71 FR
7814). The supplemental letter provided
clarifying information that was within
the scope of the initial notice and did
not change the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 25, 2006.
No significant hazards consideration
comments received: No.
in TS 5.65.b, ‘‘Core Operating Limits
Report (COLR),’’ to permit the use of an
alternate methodology to perform a
thermal-hydraulic analysis to predict
the critical heat flux and departure from
nucleate boiling ratio for the AREVA
Advanced Mark-BW fuel in the North
Anna 1 and 2 cores.
Date of issuance: July 21, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment Nos.: 247, 227.
Renewed Facility Operating License
Nos. NPF–4 and NPF–7: Amendments
changed the Licenses and the TSs.
Date of initial notice in Federal
Register: August 16, 2005 (70 FR
48208). The supplements dated March
30, April 13, and May 11, 2006,
contained clarifying information only
and did not change the initial no
significant hazards consideration
determination or expand the scope of
the initial application.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated July 21, 2006.
No significant hazards consideration
comments received: No.
Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Dated at Rockville, Maryland, this 8th day
of August, 2006.
For the Nuclear Regulatory Commission.
Catherine Haney,
Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. 06–6921 Filed 8–14–06; 8:45 am]
Date of application for amendment:
March 28, 2006.
Brief description of amendment: The
amendment revised Technical
Specification 5.0, ‘‘Administrative
Controls,’’ by changing a position title
and department name.
Date of issuance: July 11, 2006.
Effective date: As of its date of
issuance, and shall be implemented
within 90 days of the date of issuance.
Amendment No.: 173.
Facility Operating License No. NPF–
30: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: May 9, 2006 (71 FR 27005).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated July 11, 2006.
No significant hazards consideration
comments received: No.
mstockstill on PROD1PC61 with NOTICES
Tennessee Valley Authority, Docket No.
50–390, Watts Bar Nuclear Plant, Unit 1,
Rhea County, Tennessee
Virginia Electric and Power Company,
Docket Nos. 50–338 and 50–339, North
Anna Power Station, Units 1 and 2,
Louisa County, Virginia
Date of application for amendment:
December 15, 2005 (TS–05–09), as
supplemented by letter dated June 7,
2006.
Brief description of amendment: The
amendment revises the Watts Bar
Nuclear Plant (WBN) Technical
Date of application for amendment:
July 5, 2005, as supplemented by letters
dated March 30, April 13, and May 11,
2006.
Brief description of amendment: The
amendments revised the Technical
Specifications (TSs) to add a reference
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BILLING CODE 7590–01–P
SECURITIES AND EXCHANGE
COMMISSION
[Release No. 34–54296; File No. SR–ISE–
2006–30]
Self-Regulatory Organizations;
International Securities Exchange, Inc.;
Order Approving a Proposed Rule
Change, and Amendment No. 1
Thereto, Increasing the Linkage
Inbound Principal Order Fee
August 9, 2006.
On June 5, 2006, the International
Securities Exchange, Inc. (‘‘ISE’’ or
‘‘Exchange’’) filed with the Securities
and Exchange Commission
(‘‘Commission’’), pursuant to Section
19(b)(1) of the Securities Exchange Act
of 1934 (‘‘Act’’) 1 and Rule 19b–4
thereunder,2 a proposed rule change to
amend its Schedule of Fees in the
manner described below. On June 29,
1 15
2 17
E:\FR\FM\15AUN1.SGM
U.S.C. 78s(b)(1).
CFR 240.19b–4.
15AUN1
Agencies
[Federal Register Volume 71, Number 157 (Tuesday, August 15, 2006)]
[Notices]
[Pages 46929-46946]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: 06-6921]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from July 21, 2006, to August 3, 2006. The last
biweekly notice was published on August 1, 2006 (71 FR 43528).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example, in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The
filing of requests for a hearing and petitions for leave to intervene
is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for
[[Page 46930]]
leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland 20852, Attention: Rulemaking and
Adjudications Staff; (3) e-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket No. 50-461, Clinton Power Station
(CPS), Unit 1, DeWitt County, Illinois
Date of amendment request: June 30, 2006.
Description of amendment request: The proposed change would revise
the Note preceding Technical Specification (TS) Surveillance
Requirement (SR) 3.4.6.1 to be consistent with the wording in NUREG-
1434, ``Standard Technical Specifications General Electric Plants, BWR/
6,'' Revision 3.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed amendment revises the note associated with TS SR
3.4.6.1, which requires verification that the leakage past the
Reactor Coolant System (RCS) Pressure Isolation Valves (PIVs) is
less than a specified limit. The proposed revision provides
clarification that performance of this SR is allowed during plant
shutdown (i.e., a Mode other than Modes 1 and 2).
The proposed change does not require modification to the
facility. The proposed change does not affect the operation of any
facility equipment, the interface between facility systems, or the
reliability of any equipment. In addition, the proposed change does
not alter the requirement to perform the leakage testing of the RCS
PIVs and does not revise the leakage limits associated with this SR.
The function of the RCS PIVs is to separate the high pressure RCS
from an attached low pressure system. Periodic testing of PIVs can
substantially reduce intersystem Loss of Coolant Accident (LOCA)
probability. Since the proposed change does not alter the method or
limits associated with the leak rate testing of the RCS PIVs there
is no significant increase in the probability of a LOCA. Therefore,
the proposed amendment does not involve a significant increase in
the
[[Page 46931]]
probability of an accident previously evaluated.
The consequences of a previously analyzed event are dependent on
the initial conditions assumed in the analysis, the availability and
successful functioning of equipment assumed to operate in response
to the analyzed event, and the setpoints at which these actions are
initiated. The method for performing the leakage testing of the RCS
PIVs and the specified leakage limit for this testing will not
change as a result of the proposed revision and, therefore, there is
no change in the consequences associated with the LOCA analysis. The
radiological consequences remain within applicable regulatory
limits. The proposed change does not alter any system's performance
measures or the ability to perform its accident mitigation
functions. The radiological consequences associated with any
previously evaluated accident do not change as a result of the
proposed revision. Therefore, the proposed change does not involve a
significant increase in the consequences of an accident previously
evaluated.
Based on the above, the proposed change does not involve a
significant increase in the probability or consequences of an
accident previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed change to the wording of the Note to TS SR 3.4.6.1
clarifies the plant conditions for when the surveillance is required
to be performed. The proposed change does not affect the design,
functional performance or operation of the facility. No new
equipment is being introduced and installed equipment is not being
operated in a new or different manner. Similarly, the proposed
change does not affect the design or operation of any structures,
systems or components involved in the mitigation of any accidents,
nor does it affect the design or operation of any component in the
facility such that new equipment failure modes are created. There
are no setpoints at which protective or mitigative actions are
initiated that are affected by this proposed action. No change is
being made to procedures relied upon to respond to an off-normal
event.
As such the proposed amendment will not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
Margins of safety are established in the design of components,
the configuration of components to meet certain performance
parameters, and in the establishment of setpoints to initiate alarms
or actions. The proposed change revises a note associated with a
surveillance requirement to clarify the plant conditions for when
the surveillance needs to be performed. This change involves an
administrative clarification to reflect the original intent of the
TS. The equipment will continue to be tested in a manner and at a
frequency necessary to provide confidence that the equipment can
perform its intended safety function. There is no change in the
design of the affected systems, no alteration of the setpoints at
which alarms or actions are initiated, and no change in plant
configuration from original design. There is no impact on the plant
safety analyses.
Therefore, operation of CPS in accordance with the proposed
change will not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. Bradley J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Kennett
Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric
Station, Unit 3, St. Charles Parish, Louisiana
Date of amendment request: June 14, 2006.
Description of amendment request: The proposed change will delete
Waterford 3 Technical Specification (TS) Surveillance Requirement (SR)
4.8.1.1.2.f. This SR requires that the emergency diesel generator be
subjected to an inspection in accordance with procedures prepared in
conjunction with its manufacturer's recommendations.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The ability of the emergency diesel generator to perform its
safety function is not proven by the performance of the
manufacturer's recommended inspections. The inspections are not
considered an initiator or mitigating factor in any previously
evaluated accidents.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change results in the deletion of the SR associated
with the performance of manufacturer's inspections. No modifications
to plant structures, systems, or components, or changes in the
design of the plant structures, systems, or components are required
to support the proposed TS change.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The ability of the emergency diesel generator to perform its
safety function is not proven by the performance of the
manufacturer's recommended inspections. Inspection activities will
continue to be performed.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: N.S. Reynolds, Esquire, Winston & Strawn,
1700 K Street, NW., Washington, DC 20006-3817.
NRC Branch Chief: David Terao.
Exelon Generation Company, LLC, Docket Nos. 50-237 and 50-249, Dresden
Nuclear Power Station (DNPS), Units 2 and 3, Grundy County, Illinois
Date of amendment request: June 2, 2006.
Description of amendment request: The proposed amendments would
revise Technical Specification (TS) Surveillance Requirement (SR)
3.4.3.1 to increase the allowable as-found main steam safety valve
(MSSV) lift set point tolerance from +/-1 percent to +/-3 percent. The
proposed change would also revise the SR 3.1.7.10 to increase the
enrichment of sodium pentaborate used in the Standby Liquid Control
(SLC) system from greater than or equal to 30 atom percent boron-10 to
greater than or equal to 45 atom percent boron-10.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change increases the allowable as-found MSSV lift
setpoint tolerance, determined by test after the valves have been
removed from service, from +/-1 percent to +/-3 percent. The
proposed change does not alter the TS requirements for
[[Page 46932]]
the number of MSSVs required to be operable, the nominal lift
setpoints, the allowable as-left lift setpoint tolerance, the MSSV
testing frequency, or the manner in which the valves are operated.
Consistent with current TS requirements, the proposed change
continues to require that the MSSVs be adjusted to within +/-1
percent of their nominal lift setpoints following testing. Since the
proposed change does not alter the manner in which the valves are
operated, there is no significant impact on reactor operation.
The proposed change does not involve a physical change to the
valves, nor does it change the safety function of the valves. The
proposed TS revision involves no significant changes to the
operation of any systems or components in normal or accident
operating conditions and no changes to existing structures, systems,
or components, with the exception of the SLC system enrichment
change. The proposed change to increase the enrichment of sodium
pentaborate used in the SLC system by a design modification using a
single SLC pump will ensure that the requirements of 10 CFR 50.62,
``Requirements for reduction of risk from anticipated transients
without scram (ATWS) events for light-water-cooled nuclear power
plants,'' continue to be met. The SLC system is not an initiator to
an accident; rather, the SLC system is used to mitigate a postulated
anticipated transient without scram (ATWS) event. Therefore, these
changes will not increase the probability of an accident previously
evaluated.
Generic considerations related to the change in setpoint
tolerance were addressed in NEDC-31753P, ``BWROG In-Service Pressure
Relief Technical Specification Revision Licensing Topical Report,''
and were reviewed and approved by the NRC in a safety evaluation
dated March 8, 1993. The plant specific evaluations, required by the
NRC's safety evaluation and performed to support this proposed
change, show that there is no change to the design core thermal
limits and adequate margin to the reactor vessel pressure limits
using a +/-3 percent lift setpoint tolerance. These analyses also
show that operation of Emergency Core Cooling Systems is not
affected, and the containment response following a loss-of-coolant
accident is acceptable. The plant systems associated with these
proposed changes are capable of meeting applicable design basis
requirements and retain the capability to mitigate the consequences
of accidents described in the Updated Final Safety Analysis Report.
Therefore, these changes do not involve an increase in the
consequences of an accident previously evaluated.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change increases the allowable as-found lift
setpoint tolerance for the DNPS MSSVs, and increases the required
enrichment of sodium pentaborate used in the SLC system. The
proposed change to increase the enrichment of sodium pentaborate
used in the SLC system will ensure that the requirements of 10 CFR
50.62 continue to be met.
The proposed change to increase the MSSV tolerance was developed
in accordance with the provisions contained in the NRC safety
evaluation for NEDC-31753P. MSSVs installed in the plant following
testing or refurbishment will continue to meet the current tolerance
as-left acceptance criteria of +/-1 percent of the nominal setpoint.
The proposed change does not affect the manner in which the
overpressure protection system is operated; therefore, there are no
new failure mechanisms for the overpressure protection system.
The proposed change to allow an increase in the MSSV setpoint
tolerance does not alter the nominal MSSV lift setpoints or the
number of MSSVs currently required to be operable by DNPS TS. The
proposed change does not involve physical changes to the valves, nor
does it change the safety function of the valves. There is no
alteration to the parameters within which the plant is normally
operated. As a result, no new failure modes are being introduced.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The margin of safety is established through the design of the
plant structures, systems, and components, the parameters within
which the plant is operated, and the establishment of the setpoints
for the actuation of equipment relied upon to respond to an event.
The proposed change does not modify the safety limits or setpoints
at which protective actions are initiated, and does not change the
requirements governing operation or availability of safety equipment
assumed to operate to preserve the margin of safety.
Establishment of the 3 percent MSSV setpoint
tolerance limit does not adversely impact the operation of any
safety-related component or equipment. Evaluations performed in
accordance with the NRC safety evaluation for NEDC-31753P have
concluded that all design limits will continue to be met.
The proposed change to increase the enrichment of sodium
pentaborate used in the SLC system will ensure that the requirements
of 10 CFR 50.62 continue to be met.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Bradley J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Kennett
Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
Exelon Generation Company, LLC, Docket Nos. 50-373 and 50-374, LaSalle
County Station (LSCS), Units 1 and 2, LaSalle County, Illinois
Date of amendment request: March 16, 2006.
Description of amendment request: The proposed amendment would
modify Technical Specification (TS) 3.3.6.1, ``Primary Containment
Isolation Instrumentation,'' Table 3.3.6.1-1 to revise the allowable
values (AVs) for the reactor core isolation cooling (RCIC) temperature-
based leak detection. The proposed change is a result of revising the
setpoint calculation for the subject temperature instruments based on
the current reactor coolant leak detection analytical limit. The
temperature limits correspond to a 25-gallon per minute (gpm) leak as
determined by LSCS calculations. The proposed changes would revise TS
Table 3.3.6.1-1 AVs for the following four RCIC system isolation
functions:
Item 3.e. RCIC Equipment Room Temperature--High
Item 3.f. RCIC Equipment Room Differential Temperature--High
Item 3.g. RCIC Steam Line Tunnel Temperature--High
Item 3.h. RCIC Steam Line Tunnel Differential Temperature--High
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
The proposed change is a result of revising the setpoint
calculation for the subject temperature instruments based on the
current reactor coolant leak detection calculation analytical limit.
The proposed changes will revise TS Table 3.3.6.1-1 Allowable Values
for the following four RCIC system isolation functions as noted
below.
Increase the Allowable Value for Function 3.e., ``RCIC
Equipment Room Temperature--High,'' from <= 291.0 [deg]F to <= 297.0
[deg]F
Decrease the Allowable Value for Function 3.f., ``RCIC
Equipment Room Differential Temperature--High,'' from <= 189.0
[deg]F to <= 188.0 [deg]F
Decrease the Allowable Value for Function 3.g., ``RCIC
Steam Line Tunnel Temperature--High,'' from <= 277.0 [deg]F to <=
267.0 [deg]F
Increase the Allowable Value for Function 3.h., ``RCIC
Steam Line Tunnel Differential Temperature--High,'' from <= 155.0
[deg]F to <= 163.0 [deg]F
[[Page 46933]]
The function of the instrumentation listed on TS Table 3.3.6.1-
1, in combination with other accident mitigation features, is to
limit fission product release during and following postulated Design
Basis Accidents to within allowable limits. The Allowable Values
specified in TS Table 3.3.6.1-1 provide assurance that the
instrumentation will perform as designed.
The Allowable Values for RCIC system isolation are not a
precursor to any accident previously evaluated. Accidents are
assumed to be initiated by equipment failure. The proposed change
does not alter the initiation conditions or operational parameters
for the system. There is no increase in the failure probability of
the system. As such, the probability of occurrence for a previously
evaluated accident is not increased.
The Allowable Values specified in Table 3.3.6.1-1 provide
assurance that the RCIC system will perform as designed. The
proposed revision to the Allowable Values does not change any of the
RCIC system leak detection isolation actuation setpoints. Thus, the
radiological consequences of any accident previously evaluated are
not increased.
Based on the above information, the proposed change does not
involve a significant increase in the probability or consequences of
an accident previously evaluated.
2. The proposed TS change does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
The proposed change does not affect the control parameters
governing unit operation or the response of plant equipment to
transient conditions. The proposed change does not change or
introduce any new equipment, modes of system operation or failure
mechanisms.
The proposed change is based on revised reactor coolant leak
detection calculation analytical limits determined by the most
current revision to the heat rise calculation. Setpoint calculations
have been performed to determine the nominal trip setpoints and
Allowable Values for the instrumentation associated with the leak
detection function based on the revised analytical limits determined
by the heat rise calculations. The proposed revision to the
Allowable Values does not change any of the RCIC system leak
detection isolation actuation setpoints.
Based on the above information, the proposed change does not
create the possibility of a new or different kind of accident from
any previously evaluated.
3. The proposed change does not involve a significant reduction
in the margin of safety.
The proposed change will revise TS Table 3.3.6.1-1 Allowable
Values for the instrument functions associated with RCIC Isolation.
The current Allowable Values for these functions are:
<= 291.0 [deg]F for RCIC Equipment Room Temperature--High
<= 189.0 [deg]F for RCIC Equipment Room Differential Temperature--
High
<= 277.0 [deg]F for the RCIC Steam Line Tunnel Temperature--High
<= 155.0 [deg]F for the RCIC Steam Line Tunnel Differential
Temperature--High
The proposed change revises the Allowable Values to the
following:
<= 297.0 [deg]F for RCIC Equipment Room Temperature--High
<= 188.0 [deg]F for RCIC Equipment Room Differential Temperature--
High
<= 267.0 [deg]F for the RCIC Steam Line Tunnel Temperature--High
<= 163.0 [deg]F for the RCIC Steam Line Tunnel Differential
Temperature--High
The proposed change is a result of revising the setpoint
calculation for the subject temperature instruments based on the
current analytical limit. The proposed changes will revise TS Table
3.3.6.1-1 Allowable Values for the subject four RCIC system
isolation functions and will provide assurance that the RCIC system
will perform as designed. The proposed revision to the Allowable
Values does not change any of the RCIC system leak detection
isolation actuation setpoints.
Margin of safety is established by the design and qualification
of plant equipment, the operation of the plant within analyzed
limits, and the point at which protective or mitigative actions are
being initiated. The proposed change does not alter these
considerations. The proposed allowable values will still ensure that
the results of the accident analysis remain valid.
Based on this information, the proposed changes do not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Bradley J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Kennett
Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
Exelon Generation Company, LLC, Docket Nos. 50-373 and 50-374, LaSalle
County Station, Units 1 and 2, LaSalle County, Illinois
Date of amendment request: April 4, 2006.
Description of amendment request: The proposed amendment request
will add one NRC approved topical report reference to the list of
analytical methods in Technical Specification (TS) 5.6.5, ``Core
Operating Limits Report (COLR),'' that can be used to determine core
operating limits, and will delete seven obsolete references from the
same TS Section.
The proposed changes are:
1. Add an NRC previously approved Topical Report ANF-1358(P)(A),
Revision 3, ``The Loss of Feedwater Heating Transient in Boiling
Water Reactors,'' (LOFWH), which will list FRA-ANP method for
evaluating the LOFWH transient.
2. Delete seven references describing previously approved Global
Nuclear Fuel (GNF) and FRA-ANP methodologies for the analyses of
ATRIUM-9B and GE9 fuel. Both of these fuel types have been or will
be completely discharged from both Lasalle County Station (LSCS)
reactors after the loading of ATRIUM-10 fuel during the LSCS Unit 2
refuel outage currently scheduled to begin in February 2007 (i.e.,
L2R11).
The proposed changes support the continued irradiation of ATRIUM-10
fuel in the LSCS reactors and the use of the NRC-approved analytical
methodology for evaluation of LOFWH transients.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
Technical Specification (TS) 5.6.5 lists NRC-approved analytical
methods used at LaSalle County Station (LSCS) to determine core
operating limits. The proposed changes will add an NRC-approved
topical report reference to the list of administratively controlled
analytical methods in TS 5.6.5, ``Core Operating Limits Report
(COLR),'' that can be used to determine core operating limits, and
delete seven obsolete references.
The addition of a Framatome ANP (FRA-ANP) methodology to
determine overall core operating limits for future LSCS core
configurations was approved by the NRC in Reference 2. LSCS Unit 2
will continue to load Framatome ANP ATRIUM-10 fuel during the Unit 2
Refueling Outage 11 currently scheduled for February 2007. The
proposed change to TS 5.6.5 will add a FRA-ANP methodology as a
reference to determine core operating limits for loss of feedwater
heater (LOFWH) conditions. Thus, the proposed change will allow LSCS
to use the most recent FRA-ANP methodology for analysis of LOFWH
conditions.
The addition and deletion of approved analytical methods in TS
Section 5.6.5 has no effect on any accident initiator or precursor
previously evaluated and does not change the manner in which the
core is operated. The NRC-approved methods ensure that the output
accurately models predicted core behavior, have no effect on the
type or amount of radiation released, and have no effect on
predicted offsite doses in the event of an accident. Additionally,
the NRC-approved methods do not change any key core parameters that
influence any accident consequences. Thus, the proposed changes do
not have any effect on the probability of an accident previously
evaluated.
The methodology conservatively establishes acceptable core
operating limits such that the consequences of previously analyzed
events are not significantly increased.
[[Page 46934]]
The proposed changes in the list of analytical methods do not
affect the ability of LSCS to successfully respond to previously
evaluated accidents and does not affect radiological assumptions
used in the evaluations. Thus, the radiological consequences of any
accident previously evaluated are not increased.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes to TS Section 5.6.5 do not affect the
performance of any LSCS structure, system, or component credited
with mitigating any accident previously evaluated. The NRC-approved
analytical methodology for evaluating LOFWH transients will not
affect the control parameters governing unit operation or the
response of plant equipment to transient conditions. The proposed
changes do not introduce any new modes of system operation or
failure mechanism.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Do the proposed changes involve a significant reduction in
the margin of safety?
Response: No.
The proposed changes will add a reference to the list of
analytical methods in TS 5.6.5 that can be used to determine core
operating limits and delete seven obsolete references. The proposed
changes do not modify the safety limits or setpoints at which
protective actions are initiated and do not change the requirements
governing operation or availability of safety equipment assumed to
operate to preserve the margin of safety. Therefore, the proposed
changes provide an equivalent level of protection as that currently
provided.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
Based on the above information, EGC concludes that the proposed
amendment presents no significant hazards consideration under the
standards set forth in 10 CFR 50.92(c), and, accordingly, a finding
of ``no significant hazards consideration'' is justified.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Thomas S. O'Neill, Associate General
Counsel, Exelon Generation Company, LLC, 4300 Winfield Road,
Warrenville, IL 60555.
NRC Branch Chief: Daniel S. Collins.
Exelon Generation Company, LLC, and PSEG Nuclear LLC, Docket Nos. 50-
277 and 50-278, Peach Bottom Atomic Power Station, Units 2 and 3, York
and Lancaster Counties, Pennsylvania
Date of application for amendments: June 8, 2006.
Description of amendment request: The proposed changes modify
Technical Specifications (TSs) 3.1.3, ``Control Rod OPERABILITY'';
3.1.6, ``Rod Pattern Control''; 3.3.2.1, ``Control Rod Block
Instrumentation''; 3.10.7, ``Control Rod Testing--Operating''; and
3.10.8, ``SHUTDOWN MARGIN (SDM) Test--Refueling'' to replace the
current references to banked position withdrawal sequence (BPWS) with
references to ``the analyzed rod position sequence.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change modifies Technical Specifications (TS)
3.1.3, ``Control Rod OPERABILITY''; TS 3.1.6, ``Rod Pattern
Control''; TS 3.3.2.1, ``Control Rod Block Instrumentation''; TS
3.10.7, ``Control Rod Testing--Operating'', and; TS 3.10.8, SHUTDOWN
MARGIN (SDM) Test--Refueling''. The proposed change would replace
the current references to ``Banked Position Withdrawal Sequence
(BPWS)'' with references to ``the analyzed rod position sequence''.
The use of the ``the analyzed rod position sequence'' will continue
to minimize the consequences of an accident previously evaluated
including the Control Rod Drop Accident (CRDA). Additionally, the
use of the words ``the analyzed rod position sequence'' will provide
an equivalent level of protection during plant startups and
shutdowns and therefore will not increase the consequences of an
accident previously evaluated.
Control rod patterns during startup and shutdown conditions will
continue to be controlled by the operator and the Rod Worth
Minimizer (RWM) (LCO [limiting condition of operation] 3.3.2.1,
``Control Rod Block Instrumentation''), so that only specified
control rod sequences and relative positions are allowed over the
operating range of all control rods inserted to 10% of Rated Thermal
Power. As a result of this change, these sequences will continue to
limit the potential amount of reactivity addition that could occur
in the event of a Control Rod Drop Accident (CRDA).
Accidents are initiated by the malfunction of plant equipment,
or the failure of plant structures, systems, or components. The
proposed change will ensure that analyzed rod position sequences are
developed to minimize incremental control rod reactivity worth in
accordance with the ``General Electric Standard Application for
Reactor Fuel,'' NEDE-24011-P-A-15 (GESTAR-II), and U.S. Supplement,
NEDE-24011-P-A-15-US, September, 2005, NRC approved methodology, and
reviewed and approved in accordance with the 10 CFR 50.59 process.
These analyzed rod position sequences will limit the potential
reactivity increase for a postulated CRDA during reactor startups
and shutdowns below the Low Power Setpoint of 10% of Rated Thermal
Power.
The proposed change will continue to ensure that systems,
structures and components are capable of performing their intended
safety functions.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change does not affect the assumed accident
performance of the control rods, nor any plant structure, system, or
component previously evaluated.
The proposed change does not involve the installation of new
equipment, and installed equipment is not being operated in a new or
different manner. The change ensures that control rods remain
capable of performing their safety functions. No set points are
being changed which would alter the dynamic response of plant
equipment. Accordingly, no new failure modes are introduced.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change will ensure that analyzed rod position
sequences are developed to minimize incremental control rod
reactivity worth in accordance with the ``General Electric Standard
Application for Reactor Fuel,'' NEDE-24011-P-A-15 (GESTAR-II), and
U.S. Supplement, NEDE-24011-P-A-15-US, September, 2005, NRC approved
methodology, and reviewed and approved in accordance with the 10 CFR
50.59 process. The proposed change will not adversely impact the
plant's response to an accident or transient. All current safety
margins will be maintained. There are no changes proposed which
alter the set points at which protective actions are initiated, and
there is no change to the operability requirements for equipment
assumed to operate for accident mitigation.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
[[Page 46935]]
amendment request involves no significant hazards consideration.
Attorney for Licensee: Mr. Brad Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200 Exelon Way, Kennett Square, PA
19348.
NRC Branch Chief (Acting): Brooke D. Poole.
FirstEnergy Nuclear Operating Company, et al., Docket Nos. 50-334 and
50-412, Beaver Valley Power Station, Unit Nos. 1 and 2 (BVPS-1 and 2),
Beaver County, Pennsylvania
Date of amendment request: June 14, 2006.
Description of amendment request: The amendments would incorporate
the results of a new spent fuel pool criticality analysis documented in
WCAP-16518-P/WCAP-16518-NP, ``Beaver Valley Unit 2 Spent Fuel Pool
Criticality Analysis,'' Revision 1, May 2006 for the BVPS-2 spent fuel
storage pool. The revised criticality analysis will permit utilization
of vacant storage locations dictated by the existing Technical
Specification (TS) storage configurations in the BVPS-2 spent fuel
storage pool.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No. The relevant accidents previously evaluated are
limited to the fuel handling and criticality accidents.
Administrative controls during fuel fabrication ensure that the
fuel is fabricated to ensure proper loading of fuel in the fuel
assemblies. Administrative and operational controls used to load
fuel assemblies into the spent fuel pool ensure the fuel assemblies
are stored in compliance with the allowed storage configurations.
Fuel handling is performed under administrative controls and
physical limitations. These controls will remain in effect and
continue to protect against criticality and fuel handling accidents
involving new storage configurations dictated by the new analysis.
There is therefore no impact on the probability of fuel handling or
criticality accidents.
The new criticality analysis defines new spent fuel storage
configurations with new enrichment and burnup limits. Integral Fuel
Burnable Absorber (IFBA) limits are used to comply with the 1-out-
of-4 configuration for fresh fuel. The boron dilution evaluation
that supported Amendment [No.] 128 [February 11, 2002, Agencywide
Documents Access and Management System Accession No. ML020020373],
permitting credit for soluble boron at BVPS Unit No. 2 continues to
remain valid. The new analysis demonstrates that keff
remains below unity for the various storage configurations
considered with zero soluble boron, and that keff remains
less than or equal to 0.95 for the entire pool with credit for
soluble boron under non-accident and accident conditions with a 95%
probability at a 95% confidence level (95/95). Potential
consequences of accidents previously analyzed remain unchanged.
The editorial changes made to the table numbers and the LCO
[Limiting Condition for Operation] and Surveillance Requirement
wording do not impact probability or consequences of an accident
previously evaluated.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No. The relevant types of accidents previously
evaluated are limited to criticality and fuel handling accidents.
Although the new analysis will allow utilization of additional
storage capacity, implementation of fuel loading configurations and
fuel handling activities will continue to be performed under
administrative and operational controls. No new or different
activities are introduced as a result of the proposed changes. The
utilization of additional storage capacity within the allowances of
the revised analysis will introduce no new or other kind of
accident.
The editorial changes made to the table numbers and the LCO and
Surveillance Requirement wording do not impact any previously
evaluated accident.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No. The margin to safety with respect to analyzed
accidents involves maintaining keff through fuel storage
configurations and boron concentration controls in the spent fuel
pool. The boron dilution evaluation that supported that supported
Amendment [No.] 128 permitting credit for soluble boron at BVPS Unit
No. 2 remains valid. The Amendment [No.] 128 evaluation concluded
that a boron dilution event is not credible for BVPS Unit No. 2. The
new analysis calculates the non-accident soluble boron concentration
to be less than was determined in the Amendment [No.] 128
evaluation. Thus, there is no significant reduction in a margin of
safety because of the new analysis and the conclusions of the
Amendment [No.] 128 dilution evaluation remain valid.
Under accident conditions, the soluble boron needed to maintain
keff below 0.95 with the new storage configurations is
less than what is assumed in current analysis. The proposed change
does not involve a significant reduction in a margin of safety for
accident conditions.
The editorial changes made to the table numbers and the LCO and
Surveillance Requirement wording do not impact a margin of safety.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mary O'Reilly, FirstEnergy Nuclear Operating
Company, FirstEnergy Corporation, 76 South Main Street, Akron, OH
44308.
NRC Branch Chief: Richard J. Laufer.
FirstEnergy Nuclear Operating Company, et al., Docket No. 50-440, Perry
Nuclear Power Plant, Unit 1, Lake County, Ohio
Date of amendment request: June 1, 2006.
Description of amendment request: The proposed amendment would
modify Technical Specification 3.4.10, ``Residual Heat Removal (RHR)
Shutdown Cooling System--Cold Shutdown'' by adding a default Condition
to address situations when an RHR shutdown cooling subsystem becomes
inoperable in MODE 4 and, within the completion time of 1 hour, an
alternate method of decay heat removal can not be verified to be
available.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No. The proposed amendment does not change the design
of any structures, systems or components (SSCs), and does not affect
the manner in which plant systems are operated. It is a change to
the Technical Specifications only, to provide guidance to plant
operators on appropriate actions to take, where no Technical
Specification guidance currently exists. Since the design of plant
SSCs is not changed and plant systems and components are not
operated in a different manner, there is no change to previously
identified accident initiators, and the proposed amendment would not
impact the probability of any of the previously evaluated accidents
in the Updated Safety Analysis Report (USAR).
The USAR event that evaluates the consequences of a loss of RHR
Shutdown Cooling is included in Section 15.2.9 entitled ``Failure of
RHR Shutdown Cooling''. This event examines the consequences of a
loss of not only an RHR shutdown cooling
[[Page 46936]]
subsystem, but also the loss of the suction source from the
recirculation system leading to both RHR Shutdown Cooling
subsystems, and a loss of offsite power. Even with these multiple
failures, this event is not one of the limiting transients. As noted
in Section 15.2.9.5, ``Radiological Consequences,'' there are no
fuel failures, and the consequences of the event are much less than
those for the ``Main Steam Isolation Valve Closure'' transient,
which is evaluated with acceptable results in USAR Section 15.2.4.5.
Since the proposed amendment only involves the addition of a
Required Action where no guidance currently exists, and the design
of plant SSCs is not changed and plant systems and components are
not operated in a different manner, the proposed amendment does not
affect the consequences of the Section 15.2.9 analysis, nor does it
affect the ability of the installed RHR subsystems to perform their
shutdown cooling function. The change adds a default Condition to
provide guidance to the operators in those situations when a
subsystem becomes inoperable with the plant in MODE 4 and an
alternate cannot be verified to be available within an hour, which
does not impact the consequences of the previously evaluated
accidents in the USAR.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No. This change to the required Technical
Specification actions does not involve a change in the design
function or operation of plant SSCs. It does not introduce credible
new failure mechanisms, malfunctions, or accident initiators not
considered in the existing plant design and licensing basis.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No. This proposed amendment only involves a change to
the required Technical Specification actions. It does not involve a
change in the evaluation and analysis methods used to demonstrate
compliance with regulatory and licensing requirements, and does not
exceed or alter a design basis or safety limit. The safety margin
before the change remains unchanged after the proposed amendment.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David W. Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street, Akron, OH 44308.
NRC Branch Chief: Daniel S. Collins.
FirstEnergy Nuclear Operating Company, et al., Docket No. 50-440, Perry
Nuclear Power Plant, Unit 1, Lake County, Ohio
Date of amendment request: June 1, 2006.
Description of amendment request: The proposed amendment would
modify Technical Specification 3.4.9, ``Residual Heat Removal (RHR)
Shutdown Cooling System--Hot Shutdown,'' to revise the Required Actions
when both RHR shutdown cooling subsystems are inoperable in MODE 3.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No. The proposed amendment does not change the design
of any structures, systems or components (SSCs), and does not affect
the manner in which plant systems are operated. It is a change to
the Technical Specifications only, to provide guidance to plant
operators on appropriate actions to take, when both RHR shutdown
cooling subsystems are inoperable. Since the design of plant SSCs is
not changed and plant systems and components are not operated in a
different manner, there is no change to previously identified
accident initiators, and the proposed amendment would not impact the
probability of any of the previously evaluated accidents in the
Updated Safety Analysis Report (USAR).
The USAR event that evaluates the consequences of a loss of RHR
Shutdown Cooling is included in Section 15.2.9 entitled ``Failure of
RHR Shutdown Cooling.'' This event examines the consequences of a
loss of not only an RHR shutdown cooling subsystem, but also the
loss of the suction source from the recirculation system leading to
both RHR Shutdown Cooling subsystems, and a loss of offsite power.
Even with these multiple failures, this event is not one of the
limiting transients. As noted in Section 15.2.9.5, ``Radiological
Consequences,'' there are no fuel failures, and the consequences of
the event are much less than those for the ``Main Steam Isolation
Valve Closure'' transient, which is evaluated with acceptable
results in USAR Section 15.2.4.5. Since the proposed amendment only
involves the addition of a Required Action where no guidance
currently exists, and the design of plant SSCs is not changed and
plant systems and components are not operated in a different manner,
the proposed amendment does not affect the consequences of the
Section 15.2.9 analysis, nor does it affect the ability of the
installed RHR subsystems to perform their shutdown cooling function.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No. This change to the required Technical
Specification actions does not involve a change in the design
function or operation of plant SSCs. It does not introduce credible
new failure mechanisms, malfunctions, or accident initiators not
considered in the existing plant design and licensing basis.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No. This proposed amendment only involves a change to
the required Technical Specification actions. It does not involve a
change in the evaluation and analysis methods used to demonstrate
compliance with regulatory and licensing requirements, and does not
exceed or alter a design basis or safety limit. The safety margin
before the change remains unchanged after the proposed amendment.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David W. Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street, Akron, OH 44308.
NRC Branch Chief: Daniel S. Collins.
PPL Susquehanna, LLC, Docket Nos. 50-387 and 50-388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1 and 2), Luzerne County,
Pennsylvania
Date of amendment request: April 28, 2006.
Description of amendment request: The proposed amendment would
change the SSES 1 and 2 Technical Specifications (TSs) to modify the
standby liquid control system for single loop pump operation and use of
enriched sodium pentaborate solution.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
Does the proposed change involve a significant increase in the
probability or
[[Page 46937]]
consequences of an accident previously evaluated?
Response: No.
The proposed changes revise Technical Specification 3.1.7 for
the Standby Liquid Control (SLC) system to reflect new boron weight-
percent and enrichment requirements. In addition, the change to
single pump operation reduces the required SLC pump flow and
discharge pressure required to satisfy 10 CFR 50.62, thus increasing
the reliability of the system. The changes do not otherwise alter
the design or operation of the SLC system, and the existing design
of the system is sufficient to support operation with the enriched
sodium pentaborate solution. The SLC system is not considered to be
the initiator of any event currently analyzed in the FSAR [Final
Safety Analysis Report]. Therefore, the proposed changes do not
increase the probability of a previously evaluated accident.
The SSES ATWS [anticipated transient without scram] analysis was
performed using standard accepted assumptions, inputs, and codes.
That analysis, which demonstrated that the acceptance criteria for
peak vessel pressure, peak cladding temperature, peak local cladding
oxidation, peak suppression pool temperature, and peak containment
pressure, established the requirements for the proposed boron
weight-percent and concentration, and pump flow rate. The analysis
assumed the use of only a single pump, versus two pumps. The results
of the analy