Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 35456-35466 [E6-9434]
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Federal Register / Vol. 71, No. 118 / Tuesday, June 20, 2006 / Notices
General Counsel, Exelon Generation
Company, LLC, 200 Exelon Way,
Kennett Square, PA 19348, attorney for
the licensee.
For further details with respect to this
action, see the application for
amendment dated June 9, 2006, which
is available for public inspection at the
Commission’s Public Document Room
(PDR), located at One White Flint North,
Public File Area O1 F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible electronically from
the Agencywide Documents Access and
Management System’s (ADAMS) Public
Electronic Reading Room on the Internet
at the NRC Web site https://www.nrc.gov/
reading-rm.html. Persons who do not
have access to ADAMS or who
encounter problems in accessing the
documents located in ADAMS, should
contact the NRC PDR Reference staff by
telephone at 1–800–397–4209, 301–
415–4737, or by e-mail to pdr@nrc.gov.
Dated at Rockville, Maryland, this 14th day
of June 2006.
For the Nuclear Regulatory Commission.
Richard V. Guzman,
Project Manager, Plant Licensing Branch I–
2, Division of Operating Reactor Licensing,
Office of Nuclear Reactor Regulation.
[FR Doc. E6–9629 Filed 6–19–06; 8:45 am]
BILLING CODE 7590–01–P
NUCLEAR REGULATORY
COMMISSION
Notice of Sunshine Act Meetings
AGENCY HOLDING THE MEETINGS: Nuclear
Regulatory Commission.
DATE: Weeks of June 19, 26, July 3, 10,
17, 24, 2006.
PLACE: Commissioners’ Conference
room, 11555 Rockville Pike, Rockville,
Maryland.
STATUS: Public and Closed.
MATTERS TO BE CONSIDERED:
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Week of June 19, 2006
Friday, June 23, 2006
9 a.m. Affirmation Session (Public
Meeting) (Tentative).
a. AmerGen Energy Company, LLC
(License Renewal for Oyster Creek
Nuclear Generating Station) Docket
No. 50–0219, Legal challenges to
LBP–06–07 and LBP–06–11
(Tentative).
b. Nuclear Management Company,
LLC (Palisades Nuclear Plant,
license renewal application),
Appeal by Petitioners of LBP–06–10
(ruling on standing, contentions,
and other pending matters)
(Tentative).
9:30 Discussion of Security Issues
(Closed-Ex. 1).
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Week of June 6, 2006—Tentative
There are no meetings scheduled for
the Week of June 26, 2006.
Week of July 3, 2006—Tentative
There are no meetings scheduled for
the Week of July 3, 2006.
Week of July 10, 2006—Tentative
There are no meetings scheduled for
the Week of July 10, 2006.
Week of July 17, 2006—Tentative
There are no meetings scheduled for
the Week of July 17, 2006.
Week of July 24, 2006—Tentative
Thursday, July 27, 2006
9:30 a.m. Briefing on Office of
International Programs (OIP)
Programs, Performance, and Plans
(Public Meeting) (Contact: Karen
Henderson, 301–415;–0202). This
meeting will be Webcast live at the
Web address—https://www.nrc.gov.
1:30 p.m Briefing on Equal
Employment Opportunity (EEO)
Programs. (Public Meeting)
(Contact: Barbara Williams, 301–
415–7388). This meeting will be
Webcast live at the Web address—
https://www.nrc.gov.
*
*
*
*
*
*The schedule for Commission
meetings is subject to change on short
notice. To verify the status of meetings
call (recording)—(301) 415–1292.
Contact person for more information:
Michelle Schroll, (301) 415–1662.
*
*
*
*
*
*The NRC Commission Meeting
Schedule can be found on the Internet
at: https://www.nrc.gov/what-we-do/
policy-making/schedule.html.
*
*
*
*
*
The NRC provides reasonable
accommodation to individuals with
disabilities where appropriate. If you
need a reasonable accommodation to
participate in these public meetings, or
need this meeting notice or the
transcript or other information from the
public meetings in another format (e.g.,
braille, large print), please notify the
NRC’s Disability Program Coordinator,
Deborah Chan, at 301–415–7041, TDD:
301–415–2100, or by e-mail at
DLC@nrc.gov. Determinations on
requests for reasonable accommodation
will be made on a case-by-case basis.
*
*
*
*
*
This notice is distributed by mail to
several hundred subscribers; if you no
longer wish to receive it, or would like
to be added to the distribution, please
contact the Office of the Secretary,
Washington, DC 20555 (301–415–1969).
In addition, distribution of this meeting
notice over the Internet system is
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available. If you are interested in
receiving this Commission meeting
schedule electronically, please send an
electronic message to dkw@nrc.gov.
Dated: June 15, 2006.
R. Michelle Schroll,
Office of the Secretary.
[FR Doc. 06–5545 Filed 6–16–06; 10:34 am]
BILLING CODE 7590–01–M
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from May 25,
2006 to June 8, 2006. The last biweekly
notice was published on June 6, 2006
(71 FR 32603).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
Involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
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proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
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Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
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provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
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U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(I)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
Entergy Operations, Inc., System Energy
Resources, Inc., South Mississippi
Electric Power Association, and Entergy
Mississippi, Inc., Docket No. 50–416,
Grand Gulf Nuclear Station, Unit 1,
Claiborne County, Mississippi
Date of amendment request: May 8,
2006.
Description of amendment request:
The proposed change will add an NRCapproved topical report to the analytical
methods referenced in Technical
Specification (TS) Section 5.6.5, ‘‘Core
Operating Limits Report (COLR).’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
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1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Core operating limits are established each
operating cycle in accordance with TS 3.2,
‘‘Power Distribution’’ and TS 5.6.5, ‘‘Core
Operating Limits Report (COLR)’’. These core
operating limits ensure that the fuel design
limits are not exceeded during any
conditions of normal operation or in the
event of any Anticipated Operational
Occurrence (AOO). In addition, the Average
Planar Linear Heat Generation Rate
(APLHGR) operating limits imposed by
Technical Specification 3.2.1 also ensure that
the Peak Cladding Temperature (PCT) during
the postulated design[-]basis LOCA [loss-ofcoolant accident] does not exceed the 2200
°F limit specified in 10 CFR 50.46. The
APLHGR is a measure of the average linear
heat generation rate of all the fuel rods in a
fuel assembly at any axial location.
The methods used to determine the
operating limits are those previously found
acceptable by the NRC and listed in TS
Section 5.6.5.b. A change to TS Section
5.6.5.b is requested to include an updated
LOCA analysis method, EXEM BWR–2000.
The updated method will be used to
determine the APLHGR operating limits
imposed by Technical Specification 3.2.1.
EXEM BWR–2000 has been reviewed and
approved by the NRC and is applicable to the
GGNS [Grand Gulf Nuclear Station, Unit 1]
plant design and the FRA–ANP [FramatomeAdvance Nuclear Power] fuel being used at
GGNS. The application of the LOCA
analytical model will continue to ensure that
the APLHGR operating limits are established
to protect the fuel cladding integrity during
normal operation, AOOs, and the designbasis LOCA. The requested TS changes
concern the use of analytical methods and do
not involve any plant modifications or
operational changes that could affect any
postulated accident precursors or accident
mitigation systems and do not introduce any
new accident initiation mechanisms.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed TS amendment will not
change the design function, reliability,
performance, or operation of any plant
systems, components, or structures. It does
not create the possibility of a new failure
mechanism, malfunction, or accident
initiators not considered in the design and
licensing bases. Plant operation will continue
to be within the core operating limits that are
established using NRC[-]approved methods
that are applicable to the GGNS design and
the GGNS fuel.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
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Response: No.
The ECCS [emergency core cooling system]
performance analysis methods are used to
establish the APLHGR limits required by
Technical Specification 3.2.1. The APLHGR
limits are specified in the COLR and are the
result of fuel design, design[-]basis accident
(DBA), and transient analyses. Limits on the
APLHGR are specified to ensure that the fuel
design limits are not exceeded during
anticipated operational occurrences (AOOs)
and that the peak cladding temperature (PCT)
during the postulated design[-]basis LOCA
does not exceed the 2200 °F limit specified
in 10 CFR 50.46.
The EXEM BWR–2000 evaluation model is
an updated LOCA analytical method that has
been approved by the NRC and is applicable
to the GGNS plant design and the fuel being
used at GGNS. A GGNS plant[-]specific ECCS
performance analysis has been performed
with the EXEM BWR–2000 evaluation model.
This evaluation concluded that the resulting
PCT still afforded adequate margin to the
2200 °F limit of 10 CFR 50.46.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Nicholas S.
Reynolds, Esquire, Winston and Strawn
LLP, 1700 K Street, NW., Washington,
DC 20006
NRC Branch Chief: David Terao.
South Carolina Electric & Gas Company,
South Carolina Public Service
Authority, Docket No. 50–395, Virgil C.
Summer Nuclear Station, Unit No. 1,
Fairfield County, South Carolina
Date of amendment request: May 24,
2006.
Description of amendment request:
This amendment revises TS 1.0,
Definitions, TS 3/4.4.5, Steam Generator
Tube Integrity, TS 3/4.4.6.2, Reactor
Coolant System (RCS) Operational
LEAKAGE, adds a new specification TS
6.8.4.k for Steam Generator Program and
adds a new TS 6.9.1.12, Steam
Generator Tube Inspection Report. The
proposed changes are necessary in order
to implement the guidance for the
industry initiative on NEI 97–06,
‘‘Steam Generator Program Guidelines.’’
The NRC staff issued a notice of
availability of a model safety evaluation
and model no significant hazards
consideration (NSHC) determination for
referencing in license amendment
applications in the Federal Register on
March 2, 2005, (70 FR 10298). The
licensee affirmed the applicability of the
model NSHC determination in its
application dated May 24, 2006.
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Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
Criterion 1—The Proposed Change Does Not
Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated
The proposed change requires a SG
Program that includes performance criteria
that will provide reasonable assurance that
the SG tubing will retain integrity over the
full range of operating conditions (including
startup, operation in the power range, hot
standby, cooldown and all anticipated
transients included in the design
specification). The SG performance criteria
are based on tube structural integrity,
accident induced leakage, and operational
LEAKAGE.
A SGTR event is one of the design basis
accidents that are analyzed as part of a
plant’s licensing basis. In the analysis of a
SGTR event, a bounding primary to
secondary LEAKAGE rate equal to the
operational LEAKAGE rate limits in the
licensing basis plus the LEAKAGE rate
associated with a double-ended rupture of a
single tube is assumed.
For other design basis accidents such as
MSLB, rod ejection, and reactor coolant
pump locked rotor the tubes are assumed to
retain their structural integrity (i.e., they are
assumed not to rupture). These analyses
typically assume that primary to secondary
LEAKAGE for all SGs is 1 gallon per minute
or increases to 1 gallon per minute as a result
of accident induced stresses. The accident
induced leakage criterion introduced by the
proposed changes accounts for tubes that
may leak during design basis accidents. The
accident induced leakage criterion limits this
leakage to no more than the value assumed
in the accident analysis.
The SG performance criteria proposed
change to the TS identify the standards
against which tube integrity is to be
measured. Meeting the performance criteria
provides reasonable assurance that the SG
tubing will remain capable of fulfilling its
specific safety function of maintaining
reactor coolant pressure boundary integrity
throughout each operating cycle and in the
unlikely event of a design basis accident. The
performance criteria are only a part of the SG
Program required by the proposed change to
the TS. The program, defined by NEI 97–06,
Steam Generator Program Guidelines,
includes a framework that incorporates a
balance of prevention, inspection, evaluation,
repair, and leakage monitoring. The proposed
changes do not, therefore, significantly
increase the probability of an accident
previously evaluated.
The consequences of design basis accidents
are, in part, functions of the DOSE
EQUIVALENT 1–131 in the primary coolant
and the primary to secondary LEAKAGE
rates resulting from an accident. Therefore,
limits are included in the plant technical
specifications for operational leakage and for
DOSE EQUIVALENT 1–131 in primary
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coolant to ensure the plant is operated within
its analyzed condition. The typical analysis
of the limiting design basis accident assumes
that primary to secondary leak rate after the
accident is 1 gallon per minute with no more
than 150 gallons per day in any one SG, and
that the reactor coolant activity levels of
DOSE EQUIVALENT 1–131 are at the TS
values before the accident. The proposed
change does not affect the design of the SGs,
their method of operation, or primary coolant
chemistry controls. The proposed approach
updates the current TSs and enhances the
requirements for SG inspections. The
proposed change does not adversely impact
any other previously evaluated design basis
accident and is an improvement over the
current TSs.
Therefore, the proposed change does not
affect the consequences of a SGTR accident
and the probability of such an accident is
reduced. In addition, the proposed changes
do not affect the consequences of an MSLB,
rod ejection, or a reactor coolant pump
locked rotor event, or other previously
evaluated accident.
Criterion 2—The Proposed Change Does Not
Create the Possibility of a New or Different
Kind of Accident From Any Previously
Evaluated
The proposed performance based
requirements are an improvement over the
requirements imposed by the current
technical specifications. Implementation of
the proposed SG Program will not introduce
any adverse changes to the plant design basis
or postulated accidents resulting from
potential tube degradation. The result of the
implementation of the SG Program will be an
enhancement of SG tube performance.
Primary to secondary LEAKAGE that may be
experienced during all plant conditions will
be monitored to ensure it remains within
current accident analysis assumptions.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary or secondary coolant chemistry
controls. In addition, the proposed change
does not impact any other plant system or
component. The change enhances SG
inspection requirements.
Therefore, the proposed change does not
create the possibility of a new or different
type of accident from any accident
previously evaluated.
Criterion 3—The Proposed Change Does Not
Involve a Significant Reduction in the Margin
of Safety
The SG tubes in pressurized water reactors
are an integral part of the reactor coolant
pressure boundary and, as such, are relied
upon to maintain the primary system’s
pressure and inventory. As part of the reactor
coolant pressure boundary, the SG tubes are
unique in that they are also relied upon as
a heat transfer surface between the primary
and secondary systems such that residual
heat can be removed from the primary
system. In addition, the SG tubes isolate the
radioactive fission products in the primary
coolant from the secondary system. In
summary, the safety function of an SG is
maintained by ensuring the integrity of its
tubes.
Steam generator tube integrity is a function
of the design, environment, and the physical
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condition of the tube. The proposed change
does not affect tube design or operating
environment. The proposed change is
expected to result in an improvement in the
tube integrity by implementing the SG
Program to manage SG tube inspection,
assessment, repair, and plugging. The
requirements established by the SG Program
are consistent with those in the applicable
design codes and standards and are an
improvement over the requirements in the
current TSs.
For the above reasons, the margin of safety
is not changed and overall plant safety will
be enhanced by the proposed change to the
TS.
Based upon the reasoning presented above
and the previous discussion of the
amendment request, the requested change
does not involve a significant hazards
consideration.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: J. Hagood
Hamilton, South Carolina Electric & Gas
Company, Post Office Box 764,
Columbia, South Carolina 29218.
NRC Section Chief: Evangelos C.
Marinos.
Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton
County, Tennessee
Date of amendment request: May 1,
2006 (TS–05–10).
Description of amendment request:
The proposed amendment would extend
the burnup limit of the Mark-BW fuel
design with advanced alloy material
referred to as M5 alloy. This proposed
change affects Section 6.9.1.14.a of the
Sequoyah Nuclear Plant Technical
Specifications (TSs). The impact to
Section 6.9.1.14.a includes adding an
NRC-approved topical report (TR)
associated with M5 alloy fuel
assemblies. This TR will be utilized,
among others, in the determination of
core operating limits for each fuel cycle.
In addition, the proposed amendment
includes the adoption of Industry/
Technical Specification Task Force
(TSTF) Traveler, TSTF–363, Revision 0,
‘‘Revised Topical Report References in
Improved Technical Specification (ITS)
5.6.5, Core Operating Limits Report
(COLR),’’ which removes any references
to dates, revision numbers, and
supplements in the TS listing of TRs.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
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issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
In general, fuel assemblies and more
specifically fuel rod cladding, of any burnup
level, is not a precursor to accidents
previously evaluated. An evaluation has been
performed of the Mark-BW design fuel
assembly for all loss-of-coolant accidents
(LOCA) and non-LOCA transient events. This
evaluation confirmed and justified the use of
Mark-BW fuel for operation in Sequoyah
Nuclear Plant (SQN) Units 1 and 2.
The ability of the M5 fuel rod cladding
material to provide a barrier against the
release of radioactive fuel material has not
been reduced with respect to the Zircaloy-4
material. The approved TR evaluated
postulated accidents that involved adverse
core conditions and the release of
radionuclides, and found that higher burnup
limits have very little impact on the overall
radiological consequences. Radiological
consequences, as well as other safety limits,
are evaluated on a cycle-to-cycle basis to
confirm that the analyses of record remain
bounding. If a proposed extended burnup
core design exceeds bounding safety analysis
values, then either the core design would be
changed, or the safety values would be
changed.
Rod cladding failures are assumed to occur
in the fuel handling accident; however, the
consequences of this event are independent
of the properties of the fuel rod cladding.
This is based on the fuel handling event
assuming the rupture of all fuel rods
regardless of the rod cladding material.
No change is proposed to the established
safety analysis fuel assembly inputs,
specifically fuel assemblies are still limited
to a maximum 1500 effective full power day
(EFPD) burnup and the reactor core average
maximum burnup will remain at 1000 EFPD
burnup ensuring the present accident
analyses remain bounding. Based on above
discussion, the proposed revision to extend
the burnup limit of M5 fuel rod cladding
material will not significantly increase the
consequences of an accident and the
potential for the release of radioactive
material to the environment.
Removing revision numbers, dates, and
parenthetical information from the listed TRs
has no impact on the actual analytical
methods used to determine the core
operating limits, nor does the change have
impact on the calculations performed for the
current or future reloads. This change is
administrative in nature. This change has no
impact on plant equipment operation nor
does it affect the likelihood or consequences
of an accident previously evaluated.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
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Response: No.
Mark-BW fuel design with M5 alloy has
been demonstrated to have similar
characteristics to that of the Mark-B fuel
design. Extended burnup of the M5 material
has not been shown to alter the functions of
the rod cladding, which is to provide a
barrier against the release of radioactive
material. Initial plant conditions, which are
considered in the accident analysis, will also
be maintained such that no new plant
conditions will exist that could affect the
analysis results. Since plant functions and
conditions are not impacted by the proposed
revision and the higher burnup limit of the
Mark-BW fuel design with M5 alloy material
is not postulated to become an accident
initiator based on the similarity with MarkB fuel design and Zircaloy-4 material, the
possibility of a new or different kind of
accident is not created.
The proposed changes will not alter the
plant configuration or require any new or
unusual operator actions. They do not alter
the way any structure, system, or component
functions and do not alter the manner in
which the plant is operated. These changes
do not introduce any new failure modes.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The margin of safety is established by the
acceptance criteria used by NRC. Meeting the
acceptance criteria assures that the
consequences of accidents are within known
and acceptable limits. The emergency core
cooling system (ECCS) acceptance criteria are
not exceeded. Testing has been performed on
M5 alloy with respect to criteria for peak
cladding temperature (PCT) and maximum
cladding oxidation. These tests demonstrate
that M5 alloy rod cladding remains within
PCT of 2200 degrees Fahrenheit and
conservatively bounded by the 17 percent
limit for maximum cladding oxidation. M5
alloy oxidation rates are lower than that of
Zircaloy at temperatures less than 2200
degrees Fahrenheit and have similar rates for
temperatures up to about 2300 degrees
Fahrenheit. High-temperature oxidation rates
of M5 alloy remain equivalent to Zircaloy
and, as such, respond as hydrogen generators
to the same extent. Core geometry for
amenable cooling is not directly related to
rod cladding material; however, it applies
equally well to all materials. The
consequences of both thermal and
mechanical deformation of fuel assemblies
have been assessed, and the resultant
deformations have been shown to maintain
coolable core configurations. The ECCS is
evaluated against the thermal power
immediately after shutdown. The thermal
power is largely a function of short-lived
fission products which tend to saturate at
relatively low burnup limits and are not
appreciably affected by extended burnup.
Therefore, with no system changes being
proposed; long-term cooling is maintained.
Additionally, the fuel storage cooling system
is capable of supporting the long-term storage
of the extended burnup fuel assemblies’
decay heat.
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The changes to burnup limit have been
evaluated against Departure from Nucleate
Boiling (DNB) events and all applicable
acceptance criteria are met. In addition, the
proposed revision to allow an increase in the
burnup limit of the Mark-BW fuel design
with M5 alloy will not impact plant setpoints
that maintain the margin of safety. Based on
these results, it is concluded that the margin
of safety is not significantly reduced.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
Removing revision numbers, dates, and
parenthetical information from the listed TRs
will not reduce a margin of safety because
this information has no effect on any safety
analysis assumption nor does it revise any
setpoints assumed in the analysis of record.
The proposed change is consistent with
NUREG–1431, issued by the NRC staff,
revising the TSs to reflect the approved level
of detail, which indicates that there is no
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L.
Marshall, Jr.
Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton
County, Tennessee
Date of amendment request: May 25,
2006 (TSC 06–02).
Description of amendment request:
The proposed amendment would revise
Section 6.2.1.6 of the Sequoyah Nuclear
Plant (SQN) Updated Final Safety
Analysis Report (UFSAR). This change
would revise the methodology used for
containment sump debris transport
analysis and affects SQN’s current
design and licensing basis described in
Section 6.2.1.6 of the SQN UFSAR.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The design function of the sump during
accident conditions is to support emergency
core cooling systems (ECCS) and
containment spray system operation for
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recirculation. The sump is a passive feature
that does not act as an accident initiator, (i.e.,
failure of the sump would not initiate a
design basis accident).
The proposed change to the UFSAR
regarding debris transport analysis provides
an overall improvement in the analysis for
recirculation operation and does not change
the consequences of accidents previously
evaluated. The change in methodology is
neutral with regard to probability.
Consequently, the changes associated with
the enclosed license amendment do not affect
the frequency of occurrence for accidents
previously evaluated in the UFSAR.
Accident dose as previously evaluated in
the UFSAR is unaffected by the proposed
license amendment.
Based on the above discussion, the
proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The sump is a passive component and is
not an accident initiator; i.e., failure of the
sump will not initiate a design basis
accident. The sump transport methodology is
used to confirm the ability of the sump to
perform all safety functions during normal
and accident conditions. Consequently, this
activity does not create a possibility of a new
or different type of accident than any
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The changes addressed in TVA’s proposed
amendment are associated with methodology
for debris transport to the containment sump.
The change does not affect specific safety
limits, design limits, set points, or other
critical parameters. The transport
methodology is used to confirm that the
ECCS and containment spray systems will
perform their safety functions for all accident
conditions within existing equipment
performance capability margins.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L.
Marshall, Jr.
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Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of amendment request: May 9,
2006.
Description of amendment request:
The proposed amendment would revise
Technical Specifications (TSs) 1.1,
‘‘Definitions,’’ and 3.4.16, ‘‘RCS [reactor
coolant system] Specific Activity.’’ The
revisions would replace the current
Limiting Condition for Operation (LCO)
3.4.16 limit on RCS gross specific
activity with limits on RCS Dose
Equivalent I–131 and Dose Equivalent
Xe-133 (DEX). The conditions and
required actions for LCO 3.4.16 not
being met, and surveillance
requirements for LCO 3.4.16, are being
revised. The modes of applicability for
LCO 3.4.16 would be extended. The
¯
current definition of E—Average
Disintegration Energy in TS 1.1 would
be replaced by the definition of DEX. In
addition, the current definition of Dose
Equivalent I–131 in TS 1.1 would be
revised to allow alternate, NRCapproved thyroid dose conversion
factors.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. [Do] the proposed change[s] involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes would add new
thyroid dose conversion factor reference[s] to
the definition of DOSE EQUIVALENT I–131,
¯
eliminate the definition of E—AVERAGE
DISINTEGRATION ENERGY, add a new
definition of DOSE EQUIVALENT XE–133,
replace the Technical Specification (TS)
3.4.16 limit on reactor coolant system (RCS)
gross specific activity with a limit on noble
gas specific activity in the form of a Limiting
Condition for Operation (LCO) on DOSE
EQUIVALENT XE–133, increase the
Completion Time for Required Action B.1,
replace TS Figure 3.4.16–1 with a maximum
limit on DOSE EQUIVALENT I–131, extend
the Applicability of LCO 3.4.16, and make
corresponding changes to TS 3.4.16 to reflect
all of the above. The proposed changes are
not accident initiators and have no impact on
the probability of occurrence of any design
basis accidents.
The proposed changes will have no impact
on the consequences of a design basis
accident because they will limit the RCS
noble gas specific activity to be consistent
with the values assumed in the radiological
consequence analyses. The changes will also
limit the potential RCS [radio]iodine
concentration excursion to the value
currently associated with full power
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35461
operation, which is more restrictive on plant
operation than the existing allowable RCS
[radio]iodine specific activity at lower power
levels.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. [Do] the proposed change[s] create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes do not alter any
physical part of the plant nor do they affect
any plant operating parameters besides the
allowable specific activity in the RCS. The
changes which impact the allowable specific
activity in the RCS are consistent with the
assumptions assumed in the current
radiological consequence analyses. [The
proposed changes are also not accident
initiators.]
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. [Do] the proposed change[s] involve a
significant reduction in a margin of safety?
Response: No.
The acceptance criteria related to the
proposed changes involve the allowable
control room and offsite radiological
consequences following a design basis
accident. The proposed changes will have no
impact on the radiological consequences of a
design basis accident because they will limit
the RCS noble gas specific activity to be
consistent with the values assumed in the
radiological consequence analyses. The
changes will also limit the potential RCS
[radio]iodine specific activity excursion to
the value currently associated with full
power operation, which is more restrictive on
plant operation than the existing allowable
RCS [radio]iodine specific activity at lower
power levels.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: John O’Neill,
Esq., Shaw, Pittman, Potts &
Trowbridge, 2300 N Street, NW.,
Washington, DC 20037.
NRC Branch Chief: David Terao.
Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of amendment request: May 11,
2006.
Description of amendment request:
The proposed amendment would revise
Surveillance Requirements 3.7.2.1,
3.7.3.1, and 3.7.3.3 on verifying the
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closure time of the main steam isolation
valves (MSIVs), main feedwater
regulating valves (MFRVs), main
feedwater regulating valve bypass valves
(MFRVBVs), and main feedwater
isolation valves (MFIVs) in the
Technical Specifications (TSs). These
valves are the Main Steam and Main
Feedwater System isolation valves. The
revisions would replace (1) the specified
maximum acceptable valve closure time
for the MSIVs, MFRVs, and MFRVBVs,
and (2) TS Figure 3.7.3–1, which shows
acceptable valve closure times for the
MFIVs, by the reference to the valve
closure time, is verified to be ‘‘within
limits.’’ The maximum acceptable valve
closure times for the MFRVs and
MFRVBVs, and TS Figure 3.7.3–1 will
be relocated to the TS Bases. The
maximum acceptable valve closure time
for the MSIV is already in the TS Bases.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Because the proposed change[s remove]
specific isolation times from the TS and
[relocate] the specific values to the TS Bases,
there are no design or physical changes to the
facility or to the Main Steam and Main
Feedwater System isolation valves
themselves. The design and functional
performance requirements, operational
characteristics, and reliability of these
components remain unchanged. There is[,]
therefore[,] no impact on the design safety
function of the valves to close (as an accident
mitigator), nor is there any change with
respect to inadvertent closure (as a potential
transient initiator). Since no failure mode or
initiating condition that could cause an
accident (including any plant transient)
evaluated per the FSAR [Final Safety
Analysis Report]-described safety analyses is
created or affected, the change cannot
involve a significant increase in the
probability of an accident previously
evaluated. The probability of an accident is
not affected. The Main Steam and Main
Feedwater System isolation valves are
assumed to function to mitigate some
accidents (for example, SLB [steam line
break] and FWLB [main feedwater line
break]). The proposed change[s] only [affect]
the level of detail included in the TS. The TS
requirements continue to provide the same
level of assurance as before that the Main
Steam and Main Feedwater System isolation
valves are capable of performing their
intended safety function. These isolation
valves will continue to be verified operable
in the same manner as before. As such, the
proposed change[s do] not affect the ability
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of the isolation valves to perform their
assumed mitigation function.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change[s] only [affect] the
level of detail included in the TS. The TS
requirements [are not being changed and they
will] continue to provide the same level of
assurance as before that the Main Steam and
Main Feedwater System isolation valves are
capable of performing their intended safety
function. The Main Steam and Main
Feedwater System isolation valves will
continue to be verified operable in the same
manner. As such, the proposed change[s do]
not involve a modification to the physical
configuration of the plant (i.e., no new
equipment will be installed) or change in the
methods governing normal plant operation.
The proposed change[s] will not impose any
new or different requirements or introduce a
new accident initiator, accident precursor, or
malfunction mechanism. Additionally, there
is no change in the types or increases in the
amounts of any effluent that may be released
off-site and there is no increase in individual
or cumulative occupational exposure.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. [Do] the proposed change[s] involve a
significant reduction in a margin of safety?
Response: No.
The proposed change[s do] not reduce the
margin of safety. The proposed change[s]
only [affect] the level of detail included in
the TS. The TS requirements [are not being
changed and will] continue to provide the
same level of assurance as before that the
Main Steam and Main Feedwater System
isolation valves will continue to be verified
operable in the same manner as before. As
such, the proposed change[s do] not affect
the assumptions of any accident analysis or
the availability or operability of any plant
equipment.
Therefore, the proposed changes do not
involve a significant reduction in the margin
of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: John O’Neill,
Esq., Shaw, Pittman, Potts &
Trowbridge, 2300 N Street, NW.,
Washington, DC 20037.
NRC Branch Chief: David Terao.
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Previously Published Notices of
Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The following notices were previously
published as separate individual
notices. The notice content was the
same as above. They were published as
individual notices either because time
did not allow the Commission to wait
for this biweekly notice or because the
action involved exigent circumstances.
They are repeated here because the
biweekly notice lists all amendments
issued or proposed to be issued
involving no significant hazards
consideration.
For details, see the individual notice
in the Federal Register on the day and
page cited. This notice does not extend
the notice period of the original notice.
Virginia Electric and Power Company,
Docket Nos. 50–280 and 50–281, Surry
Power Station, Unit Nos. 1 and 2, Surry
County, Virginia
Date of amendment request: February
14, 2006.
Brief description of amendment
request: The proposed amendments
would add a requirement to the Title 10
of the Code of Federal Regulations, (10
CFR) part 50 license to restrict the
minimum cooling time and burnup of
spent fuel assemblies that will be placed
into storage in the NUHOMS HD spent
fuel dry storage system at Surry starting
in the summer of 2006.
Date of publication of individual
notice in Federal Register: May 16,
2006 (71 FR 28390).
Expiration date of individual notice:
30 day expiration date, June 15, 2006,
and 60 day expiration date, July 17,
2006.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
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Hazards Consideration Determination,
and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) The applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket
No. 50–461, Clinton Power Station, Unit
1, DeWitt County, Illinois
Date of application for amendment:
April 26, 2004, as supplemented April
18 and October 11, 2005, and May 19,
2006.
Brief description of amendment: The
amendment revised Technical
Specification 3.8.7, ‘‘Inverters—
Operating’’ to change the completion
time for restoration of an inoperable
Division 1 or 2 inverter from the current
24 hours to 7 days.
Date of issuance: May 26, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days of the date of issuance.
Amendment No.: 174.
Facility Operating License No. NPF–
62: The amendment revised the
Technical Specifications and License.
Date of initial notice in Federal
Register: June 8, 2004 (69 FR 32072).
The supplements dated April 18 and
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18:14 Jun 19, 2006
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October 11, 2005, and May 19, 2006,
provided additional information that
clarified the application, but did not
expand the scope of the application as
originally noticed, and did not change
the NRC staff’s original proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated May 26, 2006.
No significant hazards consideration
comments received: No.
Arizona Public Service Company, et al.,
Docket Nos. STN 50–528, STN 50–529,
and STN 50–530, Palo Verde Nuclear
Generating Station, Units Nos. 1, 2, and
3, Maricopa County, Arizona
Date of application for amendments:
June 3, 2005, as supplemented by letter
dated March 7, 2006.
Brief description of amendments: The
amendments revise the Updated Final
Safety Analysis Report (UFSAR) to
incorporate the description of the
approved changes associated with the
plant modifications made to the diesel
generator cooling water system for each
emergency diesel generator as described
in the amendment application of June 3,
2005, as supplemented by letter dated
March 7, 2006.
Date of issuance: May 25, 2006.
Effective date: As of the date of
issuance to be implemented within 90
days from the date of issuance.
Amendment Nos.: Unit 1–160, Unit
2—160, Unit 3 –160.
Facility Operating License Nos. NPF–
41, NPF–51, and NPF–74: The
amendments revise the Operating
Licenses and the UFSAR for all three
units.
Date of initial notice in Federal
Register: July 5, 2005 (70 FR 38715).
The March 7, 2006, supplemental letter
provided additional clarifying
information, did not expand the scope
of the application as originally noticed,
and did not change the NRC staff’s
original proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated May 25, 2006.
No significant hazards consideration
comments received: No.
Duke Energy Corporation, Docket Nos.
50–269, 50–270, and 50–287, Oconee
Nuclear Station, Units 1, 2, and 3,
Oconee County, South Carolina
Date of application of amendments:
August 20, 2004, supplemented January
31, 2006.
Brief description of amendments: The
amendments revised Technical
Specification (TS) 3.3.8, ‘‘Post Accident
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Sfmt 4703
35463
Monitoring (PAM) Instrumentation,’’ to
eliminate TS requirements associated
with the reactor building spray flow
instruments commensurate with the
importance of their post-accident
function.
Date of Issuance: June 1, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 90 days from the date of
issuance.
Amendment Nos.: 350/352/351.
Renewed Facility Operating License
Nos. DPR–38, DPR–47, and DPR–55:
Amendments revised the Licenses and
the Technical Specifications.
Date of initial notice in Federal
Register: September 28, 2004 (69 FR
57983).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated June 1, 2006.
No significant hazards consideration
comments received: No.
Entergy Operations, Inc., Docket No. 50–
368, Arkansas Nuclear One, Unit 2,
Pope County, Arkansas
Date of amendment request:
September 19, 2005.
Brief description of amendment: The
proposed changes would revise
Technical Specification (TS) 3.1.1.5,
‘‘Minimum Temperature for Criticality.’’
The request proposes to change the
current Limiting Condition for
Operation (LCO) for TS 3.1.1.5 by
raising the minimum temperature for
criticality from the current value of ≥
525 °F to ≥ 540 °F; to change the current
Action statement for LCO 3.1.1.5 to
reflect this change; and to delete the
current statement in Surveillance
Requirement 4.1.1.5 and replace the
statement with wording consistent with
NUREG–1432, ‘‘Standard Technical
Specifications Combustion Engineering
Plants.’’ Also, changes will be made to
the ANO–2 TS Bases in accordance with
the Technical Specifications (TS) Bases
Control Program (ANO–2 TS 6.5.14).
Date of issuance: May 30, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment No.: 264.
Renewed Facility Operating License
No. NPF–6: The amendment revised the
Technical Specifications and
Surveillance Requirements.
Date of initial notice in Federal
Register: December 6, 2005, (70 FR
72672).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated May 30, 2006.
No significant hazards consideration
comments received: No.
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Florida Power and Light Company,
Docket Nos. 50–250 and 50–251, Turkey
Point Plant, Units 3 and 4, Miami-Dade
County, Florida
Date of application for amendments:
January 20, 2005, as supplemented July
5, 2005.
Brief description of amendments: The
amendments revised several Technical
Specifications (TSs) using six TS Task
Force (TSTF) generic changes. The six
TSTFs (nos. 5, 93, 258, 299, 308, and
361) delete redundant safety limit
violation notification requirements;
extend the pressurizer heater
surveillance frequency from 92 days to
18 months; remove redundant
requirements and add other
requirements to the Administrative
Controls section of the TSs; clarify the
requirements regarding the frequency of
testing for cumulative and projected
dose contributions from radioactive
effluents; and add a note to the residual
heat removal requirements during Mode
6 low water level operations that allows
one required residual heat removal
(RHR) loop to be inoperable for up to 2
hours for surveillance testing provided
the other RHR loop is operable and in
operation.
The amendments represent partial
approval of the January 20, 2005,
application for the proposed
amendments. The Commission has
granted the request of Florida Power
and Light Company (the licensee) to
withdraw portions of its January 20,
2005, application for the proposed
amendment. The application also
included TSTF–95, which would extend
the completion time for reducing the
Power Range High trip setpoint from 8
to 72 hours and TSTF–101, which
would change the auxiliary feedwater
pump test frequency to be consistent
with the inservice test program
frequency. However, by letter dated
March 22, 2005, the licensee withdrew
the request to adopt TSTF–95 and by
letter dated October 13, 2005, the
licensee withdrew the request to adopt
TSTF–101.
Date of issuance: May 26, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment Nos: 229 and 225.
Renewed Facility Operating License
Nos. DPR–31 and DPR–41: Amendments
revised the TSs.
Date of initial notice in Federal
Register: March 15, 2005 (70 FR
12747). The supplement dated July 5,
2005, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
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17:31 Jun 19, 2006
Jkt 208001
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated May 26, 2006.
No significant hazards consideration
comments received: No.
No significant hazards consideration
comments received: No.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of application for amendments:
Nuclear Management Company, Docket October 19, 2005, as supplemented by
letter dated December 23, 2005.
No. 50–263, Monticello Nuclear
Brief description of amendments: The
Generating Plant (MNGP), Wright
amendments updated the Technical
County, Minnesota
Specification (TS)5.3, ‘‘Unit Staff
Date of application for amendment:
Qualifications,’’ operator minimum
June 29, 2005, as supplemented by
qualification requirements contained in
letters dated April 25 (two letters), May
the March 28, 1980, NRC letter to all
4, and May 12, 2006.
licensees with the more recent NRCBrief description of amendment: The
approved operator qualification
amendment converts the current
requirements contained in American
Technical Specifications (CTSs) to the
National Standards Institute/American
Improved Technical Specifications
Nuclear Society (ANSI/ANS) 3.1–1993.
(ITSs) format and relocates certain
In addition, the changes removed the TS
requirements to other licensee5.3.1 plant staff retraining and
controlled documents. The ITSs are
replacement training program
based on NUREG–1433, ‘‘Standard
requirements, which have been
Technical Specifications General
superseded by requirements contained
Electric Plants BWR/4,’’ Revision 3,
in 10 CFR 50.120.
dated June 2004; the Commission’s
Date of issuance: May 26, 2006.
Final Policy Statement, ‘‘NRC Final
Effective date: As of its date of
Policy Statement on Technical
issuance, and shall be implemented
Specification Improvements for Nuclear within 90 days of issuance.
Power Reactors,’’ dated July 22, 1993
Amendment Nos.: Unit 1—187 ; Unit
(58 FR 39132); and 10 CFR 50.36,
2—189.
‘‘Technical specifications.’’ The purpose
Facility Operating License Nos. DPR–
of the conversion is to provide clearer
80 and DPR–82: The amendments
and more readily understandable
revised the Technical Specifications.
requirements in the TSs for MNGP to
Date of initial notice in Federal
ensure safer operation of the unit. In
Register: December 20, 2005 (70 FR
addition, the amendment includes a
75495). The December 23, 2005,
number of issues that are considered
supplemental letter provided additional
beyond the scope of NUREG–1433.
information that clarified the
Date of issuance: June 5, 2006.
application, and did not expand the
Effective date: As of the date of
scope of the application as originally
issuance and shall be implemented by
noticed.
September 30, 2006.
The Commission’s related evaluation
Amendment No: 146.
of the amendments is contained in a
Facility Operating License No. DPR–22:
Safety Evaluation dated May 26, 2006.
Amendment revised the Facility
No significant hazards consideration
Operating License and Technical
comments received: No.
Specifications.
Date of initial notice in Federal
PPL Susquehanna, LLC, Docket No. 50–
Register: November 16, 2005 (70 FR
387 and 50–388, Susquehanna Steam
70889).
Electric Station, Units 1 and 2 (SSES 1
The Commission’s related evaluation
and 2), Luzerne County, Pennsylvania
of the amendments is contained in a
Date of application for amendments:
Safety Evaluation dated June 5, 2006.
February 28, 2006, as supplemented on
No significant hazards consideration
April 7, 2006.
comments received: No.
Brief description of amendments: The
Amendment No: 146.
amendments revise the SSES 1 and 2
Facility Operating License No. DPR–
Technical Specification (TS)
22: Amendment revised the Facility
Surveillance Requirements 3.8.4.7 and
Operating License and Technical
3.8.4.8 to clarify that Diesel Generator
Specifications.
‘‘E’’ (DG E) electrical power subsystem
Date of initial notice in Federal
testing does not require a mode
Register: November 16, 2005 (70 FR
restriction when the DG E diesel is not
70889).
The Commission’s related evaluation
aligned to the Class 1E distribution
of the amendment is contained in a
system.
Date of issuance: May 30, 2006.
Safety Evaluation dated June 5, 2006.
PO 00000
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Effective date: As of the date of
issuance and to be implemented within
30 days.
Amendment Nos.: 235 and 212.
Facility Operating License Nos. NPF–
14 and NPF–22: The amendments
revised the TSs and license.
Date of initial notice in Federal
Register: March 28, 2006 (71 FR
15485). The supplement dated April 7,
2006, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated May 30, 2006.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket Nos. 50–272
and 50 311, Salem Nuclear Generating
Station, Unit Nos. 1 and 2, Salem
County, New Jersey
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Date of application for amendments:
February 10, 2005, as supplemented by
letters dated July 14, 2005, and October
20, 2005.
Brief description of amendments: The
amendments modified Technical
Specification Surveillance Requirement
4.5.3.2 b to allow safety injection and
charging pumps to run in a recirculation
flow path, provided that two
independent means are used to prevent
injection into the reactor coolant
system.
Date of issuance: May 31, 2006.
Effective date: As of the date of
issuance, and shall be implemented in
60 days.
Amendment Nos.: 273 and 254.
Facility Operating License Nos. DPR–
70 and DPR–75: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: April 12, 2005 (70 FR 19116).
The supplements dated July 14, 2005
and October 20, 2005 provided
clarifying information only and did not
change the initial no significant hazards
consideration determination. The
Commission’s related evaluation of the
amendments is contained in a Safety
Evaluation dated May 31, 2006.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket Nos. 50–272
and 50–311, Salem Nuclear Generating
Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of application for amendments:
August 31, 2005, as supplemented by
letters dated December 8, 2005, and
April 10, 2006.
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17:31 Jun 19, 2006
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Brief description of amendments: The
amendments changed the Technical
Specifications (TSs) to move the
requirements for the containment area
high-range radiation monitors from TS
3/4.3.3.1, ‘‘Radiation Monitoring
Instrumentation,’’ to TS 3/4.3.3.7,
‘‘Accident Monitoring Instrumentation,’’
and correct a typographical error in
Surveillance Requirement 4.2.2.
Date of issuance: May 25, 2006.
Effective date: May 25, 2006.
Amendment Nos.: 272 and 253.
Facility Operating License Nos. DPR–
70 and DPR–75: The amendments
revised the TSs.
Date of initial notice in Federal
Register: January 17, 2006 (71 FR
2594). The April 10, 2006 supplement
did not expand the scope of the
application, as originally noticed, and
did not change the staff’s original
proposed no significant hazards
consideration.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated May 25, 2006.
No significant hazards consideration
comments received: No.
R.E. Ginna Nuclear Power Plant, LLC,
Docket No. 50–244, R.E. Ginna Nuclear
Power Plant, Wayne County, New York
Date of application for amendment:
April 29, 2005, as supplemented on
August 15 and December 9, 2005, and
January 11 and 25, and May 9, 2006.
Brief description of amendment: The
amendment revises Technical
Specification (TS) 3.5.1,
‘‘Accumulators,’’ and TS 3.5.4,
‘‘Refueling Water Storage Tank,’’ to
reflect the results of revised analyses
performed to accommodate the
proposed extended power uprate and
revises TS 5.6.4, ‘‘Core Operating Limits
Report,’’ to permit the use of approved
methodology for large-break and smallbreak loss-of-coolant accident analyses.
Date of issuance: May 31, 2006.
Effective date: As of the date of
issuance to be implemented prior to
restart from the fall 2006 refueling
outage.
Amendment No.: 96.
Renewed Facility Operating License
No. DPR–18: Amendment revised the
Technical Specifications and the
license.
Date of initial notice in Federal
Register: June 7, 2005 (70 FR 33219).
The August 15 and December 9, 2005,
and January 11 and 25, and May 9,
2006, letters provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
PO 00000
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Sfmt 4703
35465
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated May 31, 2006.
No significant hazards consideration
comments received: No.
Southern Nuclear Operating Company,
Inc., Georgia Power Company,
Oglethorpe Power Corporation,
Municipal Electric Authority of Georgia,
City of Dalton, Georgia, Docket Nos. 50–
321 and 50–366, Edwin I. Hatch Nuclear
Plant, Units 1 and 2, Appling County,
Georgia
Date of application for amendments:
March 17, 2006, as supplemented on
April 14, 2006. The supplemental letter
dated April 14, 2006, provided
clarifying information that did not
change the scope of the March 17, 2006,
application nor the initial proposed no
significant hazards consideration
determination.
Brief description of amendments: The
amendments authorized the licensee to
credit administering potassium iodide
(KI) to reduce the 30-day post-accident
thyroid dose to the occupants of the
main control room for an interim period
of 4 years. In addition, the design-basis
accident analysis section of the Updated
Final Safety Analysis Reports will be
updated to reflect crediting of KI.
Date of issuance: May 25, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 249 and 193.
Renewed Facility Operating License
Nos. DPR–57 and NPF–5: Amendments
revised the Operating Licenses.
Date of initial notice in Federal
Register: March 27, 2006 (71 FR
15223). The Commission’s related
evaluation of the amendments is
contained in a Safety Evaluation dated
May 25, 2006.
No significant hazards consideration
comments received: No.
Virginia Electric and Power Company, et
al., Docket Nos. 50–280 and 50–281,
Surry Power Station, Units 1 and 2,
Surry County, Virginia
Date of application for amendments:
July 21, 2005.
Brief Description of amendments:
These amendments revised the
Technical Specifications (TSs) to change
the accident monitoring instrumentation
listing, allowed outage times,
requirements, and surveillances to be
consistent with the requirements of the
Improved TSs for post-accident
monitoring instrumentation.
Date of issuance: May 31, 2006.
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Federal Register / Vol. 71, No. 118 / Tuesday, June 20, 2006 / Notices
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment Nos.: 247/246.
Renewed Facility Operating License
Nos. DPR–32 and DPR–37: Amendments
change the Technical Specifications.
Date of initial notice in Federal
Register: January 3, 2006 (71 FR 155).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated May 31, 2006.
No significant hazards consideration
comments received: No.
Dated at Rockville, Maryland, this June 12,
2006.
For the Nuclear Regulatory Commission.
Catherine Haney,
Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. E6–9434 Filed 6–19–06; 8:45 am]
BILLING CODE 7590–01–P
SECURITIES AND EXCHANGE
COMMISSION
[Rel. No. IC–27393; File No. 812–13263]
ING USA Annuity and Life Insurance
Company, et al.; Notice of Application
June 13, 2006.
Securities and Exchange
Commission (‘‘SEC’’ or ‘‘Commission’’).
ACTION: Notice of application for an
order under Section 6(c) of the
Investment Company Act of 1940 (the
‘‘Act’’) granting exemptions from the
provisions of Sections 2(a)(32), and
27(i)(2)(A) of the Act and Rule 22c–1
thereunder.
AGENCY:
ING USA Annuity and Life
Insurance Company (‘‘ING USA’’),
Separate Account B of ING USA
Annuity and Life Insurance Company
(‘‘Account B’’), ReliaStar Life Insurance
Company of New York (‘‘RLNY’’) (ING
USA and RLNY collectively, the ‘‘Life
Companies’’), Separate Account NY–B
of ReliaStar Life Insurance Company of
New York (‘‘Account NY–B’’) (Account
B and Account NY–B collectively, the
‘‘Accounts’’), and Directed Services, Inc.
(‘‘DSI’’).
SUMMARY OF THE APPLICATION: The
Applicants request an order pursuant to
Section 6(c) of the Act exempting them
from the provisions of Sections 2(a)(32)
and 27(i)(2)(A) of the Act and Rule 22c–
1 thereunder to the extent necessary to
permit recapture of certain bonuses
applied to purchase payments with
respect to: (1) The deferred variable
annuity contracts and certificates
described herein that the Life
Companies intend to issue (the ‘‘Current
rwilkins on PROD1PC63 with NOTICES
APPLICANTS:
VerDate Aug<31>2005
17:31 Jun 19, 2006
Jkt 208001
Contracts’’); (2) deferred variable
annuity contracts and certificates,
substantially similar to the Current
Contracts that the Life Companies may
issue in the future (the ‘‘Future
Contracts’’) (Current Contracts and
Future Contracts collectively, the
‘‘Contracts’’); (3) any other separate
accounts of the Life Companies and
their successors in interest (‘‘Future
Accounts’’) that support the Contracts;
and (4) any National Association of
Securities Dealers, Inc. (‘‘NASD’’)
member broker-dealers controlling,
controlled by, or under common control
with any Applicant, whether existing or
created in the future, that in the future,
may act as principle underwriter for the
Contracts (‘‘Future Underwriters’’). The
circumstances under which the
Contracts would allow the recapture of
all or a portion of certain bonus credits
(previously applied to premium
payments) are where the bonus credits
were applied and: (1) The contract
owner exercises his or her ‘‘free look’’
right; (2) the contract owner dies within
twelve months of the bonus credit being
applied (unless the Contract is
continued under the spousal benefit
continuation option); or (3) the contract
owner takes a partial withdrawal or
surrenders the contract in the first seven
or four contract years, as applicable,
pursuant to the bonus credit recapture
schedule set forth below.
FILING DATE: The application was filed
on February 28, 2006 and amended and
restated on May 3, 2006.
HEARING OR NOTIFICATION OF HEARING: An
order granting the application will be
issued unless the Commission orders a
hearing. Interested persons may request
a hearing by writing to the Secretary of
the Commission and serving the
Applicants with a copy of the request,
personally or by mail. Hearing requests
must be received by the Commission by
5:30 p.m. on July 7, 2006, and should
be accompanied by proof of service on
the Applicants in the form of an
affidavit or, for lawyers, a certificate of
service. Hearing requests should state
the nature of the writer’s interest, the
reason for the request, and the issues
contested. Persons may request
notification of a hearing by writing to
the Secretary of the Commission.
ADDRESSES: Secretary, Securities and
Exchange Commission, 100 F Street,
NE., Washington, DC 20549–1090.
Applicants, c/o Nicole J. Starr, Counsel,
ING USA Annuity and Life Insurance
Company, 1475 Dunwoody Drive, West
Chester, Pennsylvania 19380.
FOR FURTHER INFORMATION CONTACT:
Alison White, Senior Counsel, or Joyce
M. Pickholz, Branch Chief, Office of
PO 00000
Frm 00059
Fmt 4703
Sfmt 4703
Insurance Products, Division of
Investment Management, at (202) 551–
6795.
The
following is a summary of the
Application. The complete Application
is available for a fee from the Public
Reference Branch of the Commission,
100 F Street, NE., Room 1580,
Washington, DC 20549.
SUPPLEMENTARY INFORMATION:
Applicants’ Representations
1. ING USA is an Iowa stock life
insurance company, which was
originally incorporated in Minnesota on
January 2, 1973. ING USA is a wholly
owned subsidiary of Lion Connecticut
Holdings, Inc. (‘‘Lion Connecticut’’)
which in turn is an indirect wholly
owned subsidiary of ING Groep N.V.
(‘‘ING Group’’), a global financial
services holding company based in The
Netherlands. ING USA is authorized to
sell insurance and annuities in all
states, except New York, and the District
of Columbia. ING USA is the depositor
and sponsor for Account B. ING USA
also serves as depositor for several
currently existing Future Accounts, one
or more of which may support
obligations under the Contracts. ING
USA may establish one or more
additional Future Accounts for which it
will serve as depositor.
2. ING USA established Account B as
a segregated investment account under
Delaware law on July 14, 1988. Account
B is registered with the Commission as
a unit investment trust (File No. 811–
5626), and interests in Account B
offered through the Contracts will be
registered under the Securities Act of
1933 on form N–4.
3. RLNY is a New York stock life
insurance company originally
incorporated on June 11, 1917 under the
name, The Morris Plan Insurance
Society. RLNY is an indirect wholly
owned subsidiary of ING Group. RLNY
is authorized to transact business in all
states, the District of Columbia, the
Dominican Republic, and the Cayman
Islands and is principally engaged in the
business of providing individual life
insurance and annuities, employee
benefit products and services,
retirement plans, and life and health
reinsurance. RLNY is the depositor and
sponsor for Account NY–B. RLNY also
serves as depositor for several currently
existing Future Accounts, one or more
of which may support obligations under
the Contracts. RLNY may establish one
or more additional Future Accounts for
which it will serve as depositor.
4. Account NY–B was established as
a separate account of First Golden
American Life Insurance Company of
E:\FR\FM\20JNN1.SGM
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Agencies
[Federal Register Volume 71, Number 118 (Tuesday, June 20, 2006)]
[Notices]
[Pages 35456-35466]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: E6-9434]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from May 25, 2006 to June 8, 2006. The last
biweekly notice was published on June 6, 2006 (71 FR 32603).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
Involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this
[[Page 35457]]
proposed determination for each amendment request is shown below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The
filing of requests for a hearing and petitions for leave to intervene
is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland, 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary,
[[Page 35458]]
U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov; or (4)
facsimile transmission addressed to the Office of the Secretary, U.S.
Nuclear Regulatory Commission, Washington, DC, Attention: Rulemakings
and Adjudications Staff at (301) 415-1101, verification number is (301)
415-1966. A copy of the request for hearing and petition for leave to
intervene should also be sent to the Office of the General Counsel,
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, and it
is requested that copies be transmitted either by means of facsimile
transmission to (301) 415-3725 or by e-mail to OGCMailCenter@nrc.gov. A
copy of the request for hearing and petition for leave to intervene
should also be sent to the attorney for the licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(I)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
Entergy Operations, Inc., System Energy Resources, Inc., South
Mississippi Electric Power Association, and Entergy Mississippi, Inc.,
Docket No. 50-416, Grand Gulf Nuclear Station, Unit 1, Claiborne
County, Mississippi
Date of amendment request: May 8, 2006.
Description of amendment request: The proposed change will add an
NRC-approved topical report to the analytical methods referenced in
Technical Specification (TS) Section 5.6.5, ``Core Operating Limits
Report (COLR).''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
Core operating limits are established each operating cycle in
accordance with TS 3.2, ``Power Distribution'' and TS 5.6.5, ``Core
Operating Limits Report (COLR)''. These core operating limits ensure
that the fuel design limits are not exceeded during any conditions
of normal operation or in the event of any Anticipated Operational
Occurrence (AOO). In addition, the Average Planar Linear Heat
Generation Rate (APLHGR) operating limits imposed by Technical
Specification 3.2.1 also ensure that the Peak Cladding Temperature
(PCT) during the postulated design[-]basis LOCA [loss-of-coolant
accident] does not exceed the 2200 [deg]F limit specified in 10 CFR
50.46. The APLHGR is a measure of the average linear heat generation
rate of all the fuel rods in a fuel assembly at any axial location.
The methods used to determine the operating limits are those
previously found acceptable by the NRC and listed in TS Section
5.6.5.b. A change to TS Section 5.6.5.b is requested to include an
updated LOCA analysis method, EXEM BWR-2000. The updated method will
be used to determine the APLHGR operating limits imposed by
Technical Specification 3.2.1. EXEM BWR-2000 has been reviewed and
approved by the NRC and is applicable to the GGNS [Grand Gulf
Nuclear Station, Unit 1] plant design and the FRA-ANP [Framatome-
Advance Nuclear Power] fuel being used at GGNS. The application of
the LOCA analytical model will continue to ensure that the APLHGR
operating limits are established to protect the fuel cladding
integrity during normal operation, AOOs, and the design-basis LOCA.
The requested TS changes concern the use of analytical methods and
do not involve any plant modifications or operational changes that
could affect any postulated accident precursors or accident
mitigation systems and do not introduce any new accident initiation
mechanisms.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed TS amendment will not change the design function,
reliability, performance, or operation of any plant systems,
components, or structures. It does not create the possibility of a
new failure mechanism, malfunction, or accident initiators not
considered in the design and licensing bases. Plant operation will
continue to be within the core operating limits that are established
using NRC[-]approved methods that are applicable to the GGNS design
and the GGNS fuel.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The ECCS [emergency core cooling system] performance analysis
methods are used to establish the APLHGR limits required by
Technical Specification 3.2.1. The APLHGR limits are specified in
the COLR and are the result of fuel design, design[-]basis accident
(DBA), and transient analyses. Limits on the APLHGR are specified to
ensure that the fuel design limits are not exceeded during
anticipated operational occurrences (AOOs) and that the peak
cladding temperature (PCT) during the postulated design[-]basis LOCA
does not exceed the 2200 [deg]F limit specified in 10 CFR 50.46.
The EXEM BWR-2000 evaluation model is an updated LOCA analytical
method that has been approved by the NRC and is applicable to the
GGNS plant design and the fuel being used at GGNS. A GGNS plant[-
]specific ECCS performance analysis has been performed with the EXEM
BWR-2000 evaluation model. This evaluation concluded that the
resulting PCT still afforded adequate margin to the 2200 [deg]F
limit of 10 CFR 50.46.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and
Strawn LLP, 1700 K Street, NW., Washington, DC 20006
NRC Branch Chief: David Terao.
South Carolina Electric & Gas Company, South Carolina Public Service
Authority, Docket No. 50-395, Virgil C. Summer Nuclear Station, Unit
No. 1, Fairfield County, South Carolina
Date of amendment request: May 24, 2006.
Description of amendment request: This amendment revises TS 1.0,
Definitions, TS 3/4.4.5, Steam Generator Tube Integrity, TS 3/4.4.6.2,
Reactor Coolant System (RCS) Operational LEAKAGE, adds a new
specification TS 6.8.4.k for Steam Generator Program and adds a new TS
6.9.1.12, Steam Generator Tube Inspection Report. The proposed changes
are necessary in order to implement the guidance for the industry
initiative on NEI 97-06, ``Steam Generator Program Guidelines.'' The
NRC staff issued a notice of availability of a model safety evaluation
and model no significant hazards consideration (NSHC) determination for
referencing in license amendment applications in the Federal Register
on March 2, 2005, (70 FR 10298). The licensee affirmed the
applicability of the model NSHC determination in its application dated
May 24, 2006.
[[Page 35459]]
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
Criterion 1--The Proposed Change Does Not Involve a Significant
Increase in the Probability or Consequences of an Accident Previously
Evaluated
The proposed change requires a SG Program that includes
performance criteria that will provide reasonable assurance that the
SG tubing will retain integrity over the full range of operating
conditions (including startup, operation in the power range, hot
standby, cooldown and all anticipated transients included in the
design specification). The SG performance criteria are based on tube
structural integrity, accident induced leakage, and operational
LEAKAGE.
A SGTR event is one of the design basis accidents that are
analyzed as part of a plant's licensing basis. In the analysis of a
SGTR event, a bounding primary to secondary LEAKAGE rate equal to
the operational LEAKAGE rate limits in the licensing basis plus the
LEAKAGE rate associated with a double-ended rupture of a single tube
is assumed.
For other design basis accidents such as MSLB, rod ejection, and
reactor coolant pump locked rotor the tubes are assumed to retain
their structural integrity (i.e., they are assumed not to rupture).
These analyses typically assume that primary to secondary LEAKAGE
for all SGs is 1 gallon per minute or increases to 1 gallon per
minute as a result of accident induced stresses. The accident
induced leakage criterion introduced by the proposed changes
accounts for tubes that may leak during design basis accidents. The
accident induced leakage criterion limits this leakage to no more
than the value assumed in the accident analysis.
The SG performance criteria proposed change to the TS identify
the standards against which tube integrity is to be measured.
Meeting the performance criteria provides reasonable assurance that
the SG tubing will remain capable of fulfilling its specific safety
function of maintaining reactor coolant pressure boundary integrity
throughout each operating cycle and in the unlikely event of a
design basis accident. The performance criteria are only a part of
the SG Program required by the proposed change to the TS. The
program, defined by NEI 97-06, Steam Generator Program Guidelines,
includes a framework that incorporates a balance of prevention,
inspection, evaluation, repair, and leakage monitoring. The proposed
changes do not, therefore, significantly increase the probability of
an accident previously evaluated.
The consequences of design basis accidents are, in part,
functions of the DOSE EQUIVALENT 1-131 in the primary coolant and
the primary to secondary LEAKAGE rates resulting from an accident.
Therefore, limits are included in the plant technical specifications
for operational leakage and for DOSE EQUIVALENT 1-131 in primary
coolant to ensure the plant is operated within its analyzed
condition. The typical analysis of the limiting design basis
accident assumes that primary to secondary leak rate after the
accident is 1 gallon per minute with no more than 150 gallons per
day in any one SG, and that the reactor coolant activity levels of
DOSE EQUIVALENT 1-131 are at the TS values before the accident. The
proposed change does not affect the design of the SGs, their method
of operation, or primary coolant chemistry controls. The proposed
approach updates the current TSs and enhances the requirements for
SG inspections. The proposed change does not adversely impact any
other previously evaluated design basis accident and is an
improvement over the current TSs.
Therefore, the proposed change does not affect the consequences
of a SGTR accident and the probability of such an accident is
reduced. In addition, the proposed changes do not affect the
consequences of an MSLB, rod ejection, or a reactor coolant pump
locked rotor event, or other previously evaluated accident.
Criterion 2--The Proposed Change Does Not Create the Possibility of a
New or Different Kind of Accident From Any Previously Evaluated
The proposed performance based requirements are an improvement
over the requirements imposed by the current technical
specifications. Implementation of the proposed SG Program will not
introduce any adverse changes to the plant design basis or
postulated accidents resulting from potential tube degradation. The
result of the implementation of the SG Program will be an
enhancement of SG tube performance. Primary to secondary LEAKAGE
that may be experienced during all plant conditions will be
monitored to ensure it remains within current accident analysis
assumptions.
The proposed change does not affect the design of the SGs, their
method of operation, or primary or secondary coolant chemistry
controls. In addition, the proposed change does not impact any other
plant system or component. The change enhances SG inspection
requirements.
Therefore, the proposed change does not create the possibility
of a new or different type of accident from any accident previously
evaluated.
Criterion 3--The Proposed Change Does Not Involve a Significant
Reduction in the Margin of Safety
The SG tubes in pressurized water reactors are an integral part
of the reactor coolant pressure boundary and, as such, are relied
upon to maintain the primary system's pressure and inventory. As
part of the reactor coolant pressure boundary, the SG tubes are
unique in that they are also relied upon as a heat transfer surface
between the primary and secondary systems such that residual heat
can be removed from the primary system. In addition, the SG tubes
isolate the radioactive fission products in the primary coolant from
the secondary system. In summary, the safety function of an SG is
maintained by ensuring the integrity of its tubes.
Steam generator tube integrity is a function of the design,
environment, and the physical condition of the tube. The proposed
change does not affect tube design or operating environment. The
proposed change is expected to result in an improvement in the tube
integrity by implementing the SG Program to manage SG tube
inspection, assessment, repair, and plugging. The requirements
established by the SG Program are consistent with those in the
applicable design codes and standards and are an improvement over
the requirements in the current TSs.
For the above reasons, the margin of safety is not changed and
overall plant safety will be enhanced by the proposed change to the
TS.
Based upon the reasoning presented above and the previous
discussion of the amendment request, the requested change does not
involve a significant hazards consideration.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: J. Hagood Hamilton, South Carolina Electric
& Gas Company, Post Office Box 764, Columbia, South Carolina 29218.
NRC Section Chief: Evangelos C. Marinos.
Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
Date of amendment request: May 1, 2006 (TS-05-10).
Description of amendment request: The proposed amendment would
extend the burnup limit of the Mark-BW fuel design with advanced alloy
material referred to as M5 alloy. This proposed change affects Section
6.9.1.14.a of the Sequoyah Nuclear Plant Technical Specifications
(TSs). The impact to Section 6.9.1.14.a includes adding an NRC-approved
topical report (TR) associated with M5 alloy fuel assemblies. This TR
will be utilized, among others, in the determination of core operating
limits for each fuel cycle. In addition, the proposed amendment
includes the adoption of Industry/Technical Specification Task Force
(TSTF) Traveler, TSTF-363, Revision 0, ``Revised Topical Report
References in Improved Technical Specification (ITS) 5.6.5, Core
Operating Limits Report (COLR),'' which removes any references to
dates, revision numbers, and supplements in the TS listing of TRs.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the
[[Page 35460]]
issue of no significant hazards consideration, which is presented
below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
In general, fuel assemblies and more specifically fuel rod
cladding, of any burnup level, is not a precursor to accidents
previously evaluated. An evaluation has been performed of the Mark-
BW design fuel assembly for all loss-of-coolant accidents (LOCA) and
non-LOCA transient events. This evaluation confirmed and justified
the use of Mark-BW fuel for operation in Sequoyah Nuclear Plant
(SQN) Units 1 and 2.
The ability of the M5 fuel rod cladding material to provide a
barrier against the release of radioactive fuel material has not
been reduced with respect to the Zircaloy-4 material. The approved
TR evaluated postulated accidents that involved adverse core
conditions and the release of radionuclides, and found that higher
burnup limits have very little impact on the overall radiological
consequences. Radiological consequences, as well as other safety
limits, are evaluated on a cycle-to-cycle basis to confirm that the
analyses of record remain bounding. If a proposed extended burnup
core design exceeds bounding safety analysis values, then either the
core design would be changed, or the safety values would be changed.
Rod cladding failures are assumed to occur in the fuel handling
accident; however, the consequences of this event are independent of
the properties of the fuel rod cladding. This is based on the fuel
handling event assuming the rupture of all fuel rods regardless of
the rod cladding material.
No change is proposed to the established safety analysis fuel
assembly inputs, specifically fuel assemblies are still limited to a
maximum 1500 effective full power day (EFPD) burnup and the reactor
core average maximum burnup will remain at 1000 EFPD burnup ensuring
the present accident analyses remain bounding. Based on above
discussion, the proposed revision to extend the burnup limit of M5
fuel rod cladding material will not significantly increase the
consequences of an accident and the potential for the release of
radioactive material to the environment.
Removing revision numbers, dates, and parenthetical information
from the listed TRs has no impact on the actual analytical methods
used to determine the core operating limits, nor does the change
have impact on the calculations performed for the current or future
reloads. This change is administrative in nature. This change has no
impact on plant equipment operation nor does it affect the
likelihood or consequences of an accident previously evaluated.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
Mark-BW fuel design with M5 alloy has been demonstrated to have
similar characteristics to that of the Mark-B fuel design. Extended
burnup of the M5 material has not been shown to alter the functions
of the rod cladding, which is to provide a barrier against the
release of radioactive material. Initial plant conditions, which are
considered in the accident analysis, will also be maintained such
that no new plant conditions will exist that could affect the
analysis results. Since plant functions and conditions are not
impacted by the proposed revision and the higher burnup limit of the
Mark-BW fuel design with M5 alloy material is not postulated to
become an accident initiator based on the similarity with Mark-B
fuel design and Zircaloy-4 material, the possibility of a new or
different kind of accident is not created.
The proposed changes will not alter the plant configuration or
require any new or unusual operator actions. They do not alter the
way any structure, system, or component functions and do not alter
the manner in which the plant is operated. These changes do not
introduce any new failure modes.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The margin of safety is established by the acceptance criteria
used by NRC. Meeting the acceptance criteria assures that the
consequences of accidents are within known and acceptable limits.
The emergency core cooling system (ECCS) acceptance criteria are not
exceeded. Testing has been performed on M5 alloy with respect to
criteria for peak cladding temperature (PCT) and maximum cladding
oxidation. These tests demonstrate that M5 alloy rod cladding
remains within PCT of 2200 degrees Fahrenheit and conservatively
bounded by the 17 percent limit for maximum cladding oxidation. M5
alloy oxidation rates are lower than that of Zircaloy at
temperatures less than 2200 degrees Fahrenheit and have similar
rates for temperatures up to about 2300 degrees Fahrenheit. High-
temperature oxidation rates of M5 alloy remain equivalent to
Zircaloy and, as such, respond as hydrogen generators to the same
extent. Core geometry for amenable cooling is not directly related
to rod cladding material; however, it applies equally well to all
materials. The consequences of both thermal and mechanical
deformation of fuel assemblies have been assessed, and the resultant
deformations have been shown to maintain coolable core
configurations. The ECCS is evaluated against the thermal power
immediately after shutdown. The thermal power is largely a function
of short-lived fission products which tend to saturate at relatively
low burnup limits and are not appreciably affected by extended
burnup. Therefore, with no system changes being proposed; long-term
cooling is maintained. Additionally, the fuel storage cooling system
is capable of supporting the long-term storage of the extended
burnup fuel assemblies' decay heat.
The changes to burnup limit have been evaluated against
Departure from Nucleate Boiling (DNB) events and all applicable
acceptance criteria are met. In addition, the proposed revision to
allow an increase in the burnup limit of the Mark-BW fuel design
with M5 alloy will not impact plant setpoints that maintain the
margin of safety. Based on these results, it is concluded that the
margin of safety is not significantly reduced. Therefore, the
proposed change does not involve a significant reduction in a margin
of safety.
Removing revision numbers, dates, and parenthetical information
from the listed TRs will not reduce a margin of safety because this
information has no effect on any safety analysis assumption nor does
it revise any setpoints assumed in the analysis of record. The
proposed change is consistent with NUREG-1431, issued by the NRC
staff, revising the TSs to reflect the approved level of detail,
which indicates that there is no significant reduction in a margin
of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: General Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A, Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L. Marshall, Jr.
Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
Date of amendment request: May 25, 2006 (TSC 06-02).
Description of amendment request: The proposed amendment would
revise Section 6.2.1.6 of the Sequoyah Nuclear Plant (SQN) Updated
Final Safety Analysis Report (UFSAR). This change would revise the
methodology used for containment sump debris transport analysis and
affects SQN's current design and licensing basis described in Section
6.2.1.6 of the SQN UFSAR.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The design function of the sump during accident conditions is to
support emergency core cooling systems (ECCS) and containment spray
system operation for
[[Page 35461]]
recirculation. The sump is a passive feature that does not act as an
accident initiator, (i.e., failure of the sump would not initiate a
design basis accident).
The proposed change to the UFSAR regarding debris transport
analysis provides an overall improvement in the analysis for
recirculation operation and does not change the consequences of
accidents previously evaluated. The change in methodology is neutral
with regard to probability. Consequently, the changes associated
with the enclosed license amendment do not affect the frequency of
occurrence for accidents previously evaluated in the UFSAR.
Accident dose as previously evaluated in the UFSAR is unaffected
by the proposed license amendment.
Based on the above discussion, the proposed change does not
involve a significant increase in the probability or consequences of
an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The sump is a passive component and is not an accident
initiator; i.e., failure of the sump will not initiate a design
basis accident. The sump transport methodology is used to confirm
the ability of the sump to perform all safety functions during
normal and accident conditions. Consequently, this activity does not
create a possibility of a new or different type of accident than any
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The changes addressed in TVA's proposed amendment are associated
with methodology for debris transport to the containment sump.
The change does not affect specific safety limits, design
limits, set points, or other critical parameters. The transport
methodology is used to confirm that the ECCS and containment spray
systems will perform their safety functions for all accident
conditions within existing equipment performance capability margins.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: General Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A, Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L. Marshall, Jr.
Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of amendment request: May 9, 2006.
Description of amendment request: The proposed amendment would
revise Technical Specifications (TSs) 1.1, ``Definitions,'' and 3.4.16,
``RCS [reactor coolant system] Specific Activity.'' The revisions would
replace the current Limiting Condition for Operation (LCO) 3.4.16 limit
on RCS gross specific activity with limits on RCS Dose Equivalent I-131
and Dose Equivalent Xe-133 (DEX). The conditions and required actions
for LCO 3.4.16 not being met, and surveillance requirements for LCO
3.4.16, are being revised. The modes of applicability for LCO 3.4.16
would be extended. The current definition of [Emacr]--Average
Disintegration Energy in TS 1.1 would be replaced by the definition of
DEX. In addition, the current definition of Dose Equivalent I-131 in TS
1.1 would be revised to allow alternate, NRC-approved thyroid dose
conversion factors.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. [Do] the proposed change[s] involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes would add new thyroid dose conversion
factor reference[s] to the definition of DOSE EQUIVALENT I-131,
eliminate the definition of [Emacr]--AVERAGE DISINTEGRATION ENERGY,
add a new definition of DOSE EQUIVALENT XE-133, replace the
Technical Specification (TS) 3.4.16 limit on reactor coolant system
(RCS) gross specific activity with a limit on noble gas specific
activity in the form of a Limiting Condition for Operation (LCO) on
DOSE EQUIVALENT XE-133, increase the Completion Time for Required
Action B.1, replace TS Figure 3.4.16-1 with a maximum limit on DOSE
EQUIVALENT I-131, extend the Applicability of LCO 3.4.16, and make
corresponding changes to TS 3.4.16 to reflect all of the above. The
proposed changes are not accident initiators and have no impact on
the probability of occurrence of any design basis accidents.
The proposed changes will have no impact on the consequences of
a design basis accident because they will limit the RCS noble gas
specific activity to be consistent with the values assumed in the
radiological consequence analyses. The changes will also limit the
potential RCS [radio]iodine concentration excursion to the value
currently associated with full power operation, which is more
restrictive on plant operation than the existing allowable RCS
[radio]iodine specific activity at lower power levels.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. [Do] the proposed change[s] create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed changes do not alter any physical part of the plant
nor do they affect any plant operating parameters besides the
allowable specific activity in the RCS. The changes which impact the
allowable specific activity in the RCS are consistent with the
assumptions assumed in the current radiological consequence
analyses. [The proposed changes are also not accident initiators.]
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any accident previously
evaluated.
3. [Do] the proposed change[s] involve a significant reduction
in a margin of safety?
Response: No.
The acceptance criteria related to the proposed changes involve
the allowable control room and offsite radiological consequences
following a design basis accident. The proposed changes will have no
impact on the radiological consequences of a design basis accident
because they will limit the RCS noble gas specific activity to be
consistent with the values assumed in the radiological consequence
analyses. The changes will also limit the potential RCS
[radio]iodine specific activity excursion to the value currently
associated with full power operation, which is more restrictive on
plant operation than the existing allowable RCS [radio]iodine
specific activity at lower power levels.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: John O'Neill, Esq., Shaw, Pittman, Potts &
Trowbridge, 2300 N Street, NW., Washington, DC 20037.
NRC Branch Chief: David Terao.
Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of amendment request: May 11, 2006.
Description of amendment request: The proposed amendment would
revise Surveillance Requirements 3.7.2.1, 3.7.3.1, and 3.7.3.3 on
verifying the
[[Page 35462]]
closure time of the main steam isolation valves (MSIVs), main feedwater
regulating valves (MFRVs), main feedwater regulating valve bypass
valves (MFRVBVs), and main feedwater isolation valves (MFIVs) in the
Technical Specifications (TSs). These valves are the Main Steam and
Main Feedwater System isolation valves. The revisions would replace (1)
the specified maximum acceptable valve closure time for the MSIVs,
MFRVs, and MFRVBVs, and (2) TS Figure 3.7.3-1, which shows acceptable
valve closure times for the MFIVs, by the reference to the valve
closure time, is verified to be ``within limits.'' The maximum
acceptable valve closure times for the MFRVs and MFRVBVs, and TS Figure
3.7.3-1 will be relocated to the TS Bases. The maximum acceptable valve
closure time for the MSIV is already in the TS Bases.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
Because the proposed change[s remove] specific isolation times
from the TS and [relocate] the specific values to the TS Bases,
there are no design or physical changes to the facility or to the
Main Steam and Main Feedwater System isolation valves themselves.
The design and functional performance requirements, operational
characteristics, and reliability of these components remain
unchanged. There is[,] therefore[,] no impact on the design safety
function of the valves to close (as an accident mitigator), nor is
there any change with respect to inadvertent closure (as a potential
transient initiator). Since no failure mode or initiating condition
that could cause an accident (including any plant transient)
evaluated per the FSAR [Final Safety Analysis Report]-described
safety analyses is created or affected, the change cannot involve a
significant increase in the probability of an accident previously
evaluated. The probability of an accident is not affected. The Main
Steam and Main Feedwater System isolation valves are assumed to
function to mitigate some accidents (for example, SLB [steam line
break] and FWLB [main feedwater line break]). The proposed change[s]
only [affect] the level of detail included in the TS. The TS
requirements continue to provide the same level of assurance as
before that the Main Steam and Main Feedwater System isolation
valves are capable of performing their intended safety function.
These isolation valves will continue to be verified operable in the
same manner as before. As such, the proposed change[s do] not affect
the ability of the isolation valves to perform their assumed
mitigation function.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change[s] only [affect] the level of detail
included in the TS. The TS requirements [are not being changed and
they will] continue to provide the same level of assurance as before
that the Main Steam and Main Feedwater System isolation valves are
capable of performing their intended safety function. The Main Steam
and Main Feedwater System isolation valves will continue to be
verified operable in the same manner. As such, the proposed change[s
do] not involve a modification to the physical configuration of the
plant (i.e., no new equipment will be installed) or change in the
methods governing normal plant operation. The proposed change[s]
will not impose any new or different requirements or introduce a new
accident initiator, accident precursor, or malfunction mechanism.
Additionally, there is no change in the types or increases in the
amounts of any effluent that may be released off-site and there is
no increase in individual or cumulative occupational exposure.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any accident previously
evaluated.
3. [Do] the proposed change[s] involve a significant reduction
in a margin of safety?
Response: No.
The proposed change[s do] not reduce the margin of safety. The
proposed change[s] only [affect] the level of detail included in the
TS. The TS requirements [are not being changed and will] continue to
provide the same level of assurance as before that the Main Steam
and Main Feedwater System isolation valves will continue to be
verified operable in the same manner as before. As such, the
proposed change[s do] not affect the assumptions of any accident
analysis or the availability or operability of any plant equipment.
Therefore, the proposed changes do not involve a significant
reduction in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: John O'Neill, Esq., Shaw, Pittman, Potts &
Trowbridge, 2300 N Street, NW., Washington, DC 20037.
NRC Branch Chief: David Terao.
Previously Published Notices of Consideration of Issuance of Amendments
to Facility Operating Licenses, Proposed No Significant Hazards
Consideration Determination, and Opportunity for a Hearing
The following notices were previously published as separate
individual notices. The notice content was the same as above. They were
published as individual notices either because time did not allow the
Commission to wait for this biweekly notice or because the action
involved exigent circumstances. They are repeated here because the
biweekly notice lists all amendments issued or proposed to be issued
involving no significant hazards consideration.
For details, see the individual notice in the Federal Register on
the day and page cited. This notice does not extend the notice period
of the original notice.
Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281,
Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
Date of amendment request: February 14, 2006.
Brief description of amendment request: The proposed amendments
would add a requirement to the Title 10 of the Code of Federal
Regulations, (10 CFR) part 50 license to restrict the minimum cooling
time and burnup of spent fuel assemblies that will be placed into
storage in the NUHOMS HD spent fuel dry storage system at Surry
starting in the summer of 2006.
Date of publication of individual notice in Federal Register: May
16, 2006 (71 FR 28390).
Expiration date of individual notice: 30 day expiration date, June
15, 2006, and 60 day expiration date, July 17, 2006.
Notice of Issuance of Amendments to Facility Operating Licenses
During the period since publication of the last biweekly notice,
the Commission has issued the following amendments. The Commission has
determined for each of these amendments that the application complies
with the standards and requirements of the Atomic Energy Act of 1954,
as amended (the Act), and the Commission's rules and regulations. The
Commission has made appropriate findings as required by the Act and the
Commission's rules and regulations in 10 CFR chapter I, which are set
forth in the license amendment.
Notice of Consideration of Issuance of Amendment to Facility
Operating License, Proposed No Significant
[[Page 35463]]
Hazards Consideration Determination, and Opportunity for A Hearing in
connection with these actions was published in the Federal Register as
indicated.
Unless otherwise indicated, the Commission has determined that
these amendments satisfy the criteria for categorical exclusion in
accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b),
no environmental impact statement or environmental assessment need be
prepared for these amendments. If the Commission has prepared an
environmental assessment under the special circumstances provision in
10 CFR 51.12(b) and has made a determination based on that assessment,
it is so indicated.
For further details with respect to the action see (1) The
applications for amendment, (2) the amendment, and (3) the Commission's
related letter, Safety Evaluation and/or Environmental Assessment as
indicated. All of these items are available for public inspection at
the Commission's Public Document Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555 Rockville Pike (first floor),
Rockville, Maryland. Publicly available records will be accessible from
the Agencywide Documents Access and Management Systems (ADAMS) Public
Electronic Reading Room on the internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket No. 50-461, Clinton Power Station,
Unit 1, DeWitt County, Illinois
Date of application for amendment: April 26, 2004, as supplemented
April 18 and October 11, 2005, and May 19, 2006.
Brief description of amendment: The amendment revised Technical
Specification 3.8.7, ``Inverters--Operating'' to change the completion
time for restoration of an inoperable Division 1 or 2 inverter from the
current 24 hours to 7 days.
Date of issuance: May 26, 2006.
Effective date: As of the date of issuance and shall be implemented
within 60 days of the date of issuance.
Amendment No.: 174.
Facility Operating License No. NPF-62: The amendment revised the
Technical Specifications and License.
Date of initial notice in Federal Register: June 8, 2004 (69 FR
32072). The supplements dated April 18 and October 11, 2005, and May
19, 2006, provided additional information that clarified the
application, but did not expand the scope of the application as
originally noticed, and did not change the NRC staff's original
proposed no significant hazards consideration determination.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated May 26, 2006.
No significant hazards consideration comments received: No.
Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
529, and STN 50-530, Palo Verde Nuclear Generating Station, Units Nos.
1, 2, and 3, Maricopa County, Arizona
Date of application for amendments: June 3, 2005, as supplemented
by letter dated March 7, 2006.
Brief description of amendments: The amendments revise the Updated
Final Safety Analysis Report (UFSAR) to incorporate the description of
the approved changes associated with the plant modifications made to
the diesel generator cooling water system for each emergency diesel
generator as described in the amendment application of June 3, 2005, as
supplemented by letter dated March 7, 2006.
Date of issuance: May 25, 2006.
Effective date: As of the date of issuance to be implemented within
90 days from the date of issuance.
Amendment Nos.: Unit 1-160, Unit 2--160, Unit 3 -160.
Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The
amendments revise the Operating Licenses and the UFSAR for all three
units.
Date of initial notice in Federal Register: July 5, 2005 (70 FR
38715). The March 7, 2006, supplemental letter provided additional
clarifying information, did not expand the scope of the application as
originally noticed, and did not change the NRC staff's original
proposed no significant hazards consideration determination.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated May 25, 2006.
No significant hazards consideration comments received: No.
Duke Energy Corporation, Docket Nos. 50-269, 50-270, and 50-287, Oconee
Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
Date of application of amendments: August 20, 2004, supplemented
January 31, 2006.
Brief description of amendments: The amendments revised Technical
Specification (TS) 3.3.8, ``Post Accident Monitoring (PAM)
Instrumentation,'' to eliminate TS requirements associated with the
reactor building spray flow instruments commensurate with the
importance of their post-accident function.
Date of Issuance: June 1, 2006.
Effective date: As of the date of issuance and shall be implemented
within 90 days from the date of issuance.
Amendment Nos.: 350/352/351.
Renewed Facility Operating License Nos. DPR-38, DPR-47, and DPR-55:
Amendments revised the Licenses and the Technical Specifications.
Date of initial notice in Federal Register: September 28, 2004 (69
FR 57983).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated June 1, 2006.
No significant hazards consideration comments received: No.
Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit
2, Pope County, Arkansas
Date of amendment request: September 19, 2005.
Brief description of amendment: The proposed changes would revise
Technical Specification (TS) 3.1.1.5, ``Minimum Temperature for
Criticality.'' The request proposes to change the current Limiting
Condition for Operation (LCO) for TS 3.1.1.5 by raising the minimum
temperature for criticality from the current value of >= 525 [deg]F to
>= 540 [deg]F; to change the current Action statement for LCO 3.1.1.5
to reflect this change; and to delete the current statement in
Surveillance Requirement 4.1.1.5 and replace the statement with wording
consistent with NUREG-1432, ``Standard Technical Specifications
Combustion Engineering Plants.'' Also, changes will be made to the ANO-
2 TS Bases in accordance with the Technical Specifications (TS) Bases
Control Program (ANO-2 TS 6.5.14).
Date of issuance: May 30, 2006.
Effective date: As of the date of issuance and shall be implemented
within 30 days from the date of issuance.
Amendment No.: 264.
Renewed Facility Operating License No. NPF-6: The amendment revised
the Technical Specifications and Surveillance Requirements.
Date of initial notice in Federal Register: December 6, 2005, (70
FR 72672).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated May 30, 2006.
No significant hazards consideration comments received: No.
[[Page 35464]]
Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey
Point Plant, Units 3 and 4, Miami-Dade County, Florida
Date of application for amendments: January 20, 2005, as
supplemented July 5, 2005.
Brief description of amendments: The amendments revised several
Technical Specifications (TSs) using six TS Task Force (TSTF) generic
changes. The six TSTFs (nos. 5, 93, 258, 299, 308, and 361) delete
redundant safety limit violation notification requirements; extend the
pressurizer heater surveillance frequency from 92 days to 18 months;
remove redundant requirements and add other requirements to the
Administrative Controls section of the TSs; clarify the requirements
regarding the frequency of testing for cumulative and projected dose
contributions from radioactive effluents; and add a note to the
residual heat removal requirements during Mode 6 low water level
operations that allows one required residual heat removal (RHR) loop to
be inoperable for up to 2 hours for surveillance testing provided the
other RHR loop is operable and in operation.
The amendments represent partial approval of the January 20, 2005,
application for the proposed amendments. The Commission has granted the
request of Florida Power and Light Company (the licensee) to withdraw
portions of its January 20, 2005, application for the proposed
amendment. The application also included TSTF-95, which would extend
the completion time for reducing the Power Range High trip setpoint
from 8 to 72 hours and TSTF-101, which would change the auxiliary
feedwater pump test frequency to be consistent with the inservice test
program frequency. However, by letter dated March 22, 2005, the
licensee withdrew the request to adopt TSTF-95 and by letter dated
October 13, 2005, the licensee withdrew the request to adopt TSTF-101.
Date of issuance: May 26, 2006.
Effective date: As of the date of issuance and shall be implemented
within 60 days.
Amendment Nos: 229 and 225.
Renewed Facility Operating License Nos. DPR-31 and DPR-41:
Amendments revised the TSs.
Date of initial notice in Federal Register: March 15, 2005 (70 FR
12747). The supplement dated July 5, 2005, provided additional
information that clarified the application, did not expand the scope of
the application as originally noticed, and did not change the staff's
original proposed no significant hazards consideration determination as
published in the Federal Register.
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated May 26, 2006.
No significant hazards consideration comments received: No.
Nuclear Management Company, Docket No. 50-263, Monticello Nuclear
Generating Plant (MNGP), Wright County, Minnesota
Date of application for amendment: June 29, 2005, as supplemented
by letters dated April 25 (two letters), May 4, and May 12, 2006.
Brief description of amendment: The amendment converts the current
Technical Specifications (CTSs) to the Improved Technical
Specifications (ITSs) format and relocates certain requirements to
other licensee-controlled documents. The ITSs are based on NUREG-1433,
``Standard Technical Specifications General Electric Plants BWR/4,''
Revision 3, dated June 2004; the Commission's Final Policy Statement,
``NRC Final Policy Statement on Technical Specification Improvements
for Nuclear Power Reactors,'' dated July 22, 1993 (58 FR 39132); and 10
CFR 50.36, ``Technical specifications.'' The purpose of the conversion
is to provide clearer and more readily understandable requirements in
the TSs for MNGP to ensure safer operation of the unit. In addition,
the amendment includes a number of issues that are considered beyond
the scope of NUREG-1433.
Date of issuance: June 5, 2006.
Effective date: As of the date of issuance and shall be implemented
by September 30, 2006.
Amendment No: 146.
Facility Operating License No. DPR-22: Amendment revised the
Facility Operating License and Technical Specifications.
Date of initial notice in Federal Register: November 16, 2005 (70
FR 70889).
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated June 5, 2006.
No significant hazards consideration comments received: No.
Amendment No: 146.
Facility Operating License No. DPR-22: Amendment revised the
Facility Operating License and Technical Specifications.
Date of initial notice in Federal Register: November 16, 2005 (70
FR 70889).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated June 5, 2006.
No significant hazards consideration comments received: No.
Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo
Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County,
California
Date of application for amendments: October 19, 2005, as
supplemented by letter dated December 23, 2005.
Brief description of amendments: The amendments updated the
Technical Specification (TS)5.3, ``Unit Staff Qualifications,''
operator minimum qualification requirements contained in the March 28,
1980, NRC letter to all licensees with the more recent NRC-approved
operator qualification requirements contained in American National
Standards Institute/American Nuclear Society (ANSI/ANS) 3.1-1993. In
addition, the changes removed the TS 5.3.1 plant staff retraining and
replacement training program requirements, which have been superseded
by requirements contained in 10 CFR 50.120.
Date of issuance: May 26, 2006.
Effective date: As of its date of issuance, and shall be
implemented within 90 days of issuance.
Amendment Nos.: Unit 1--187 ; Unit 2--189.
Facility Operating License Nos. DPR-80 and DPR-82: The amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: December 20, 2005 (70
FR 75495). The December 23, 2005, supplemental letter provided
additional information that clarified the application, and did not
expand the scope of the application as originally noticed.
The Commission's related evaluation of the amendments is contained
in a Safety Evaluation dated May 26, 2006.
No significant hazards consideration comments received: No.
PPL Susquehanna, LLC, Docket No. 50-387 and 50-388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1 and 2), Luzerne County,
Pennsylvania
Date of application for amendments: February 28, 2006, as
supplemented on April 7, 2006.
Brief description of amendments: The amendments revise the SSES 1
and 2 Technical Specification (TS) Surveillance Requirements 3.8.4.7
and 3.8.4.8 to clarify that Diesel Generator ``E'' (DG E) electrical
power subsystem testing does not require a mode restriction when the DG
E diesel is not aligned to the Class 1E distribution system.
Date of issuance: May 30, 2006.
[[Page 35465]]
Effective date: As of the date of issuance and to be implemented
within 30 days.
Amendment Nos.: 235 and 212.
Facil