Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 29671-29686 [06-4736]
Download as PDF
rmajette on PROD1PC67 with NOTICES
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
describes the function of the Board.
Notice of the meeting is required under
the Sunshine in Government Act.
TIME AND DATE: Monday, June 5, 2006
from 10:30 a.m. to 12 p.m.
AGENDA: Committee Meetings of the
Eighth National Museum and Library
Service Board Meeting:
10:30 a.m.–12 p.m. Joint Meeting of
the Committees on Partnerships &
Government Affairs and the
Committee on Policy & Planning.
(Open to the Public)
I. Staff Reports.
II. Other Business.
2 p.m.–3:30 p.m. Jury Meeting to
consider the National Awards for
Museum Services.
(Closed to the Public)
4 p.m.–5:30 p.m. Jury Meeting to
consider the National Awards for
Library Services.
(Closed to the Public)
PLACE: The meetings will be held at the
Institute of Museum and Library
Services, 1800 M Street, NW., 9th Floor,
Washington, DC 20036. Telephone:
(202) 653–4676.
TIME AND DATE: Tuesday, June 6, 2006,
from 9 a.m. to 1 p.m.
AGENDA: Eighth National Museum and
Library Services Board Meeting: (Open
to the Public)
I. Welcome.
II. Approval of Minutes.
III. Program Reports.
IV. Committee Reports.
V. Board Program: Big Read Initiative.
VI. Other Business.
VII. Adjournment.
PLACE: The meeting will be held at the
Institute of Museum and Library
Services, 1800 M Street, NW., 9th Floor,
Washington, DC 20036. Telephone:
(202) 653–4676.
STATUS: Parts of this meeting will be
closed to the public as identified in the
meeting agenda and SUPPLEMENTARY
INFORMATION. The rest of the meeting
will be open to the public.
FOR FURTHER INFORMATION CONTACT:
Elizabeth Lyons, Special Assistant to the
Director, Institute of Museum and
Library Services, 1800 M Street, NW.,
9th Floor, Washington, DC 20036.
Telephone: (202) 653–4676.
SUPPLEMENTARY INFORMATION: The
National Museum and Library Services
Board is established under the Museum
and Library Services Act, 20 U.S.C. 9101
et seq. The Board advises the Director of
the Institute on general policies with
respect to the duties, powers, and
authorities related to Museum and
Library Services.
The Jury Meetings to Consideration
the National Awards for Museum and
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
Library Services, on Monday, June 5,
2006, will be closed pursuant to
subsections (c)(4) and (c)(9) of section
552b of Title 5, United States Code
because the Board will consider
information that may disclose: Trade
secrets and commercial or financial
information obtained from a person and
privileged or confidential; and
information the premature disclosure of
which would be likely to significantly
frustrate implementation of a proposed
agency action. The meetings from 10:30
a.m. until 12 p.m. on Monday, June 5,
2006 and the meeting from 9 a.m. to 1
p.m. on Tuesday, June 6, 2006, are open
to the public. If you need special
accommodations due to a disability,
please contact: Institute of Museum and
Library Services, 1100 Pennsylvania
Avenue, NW., Washington, DC 20506.
Telephone: (202) 653–4676; TDD (202)
653–4699 at least seven (7) days prior to
the meeting date.
Dated: May 17, 2006.
Kate Fernstrom,
Chief of Staff.
[FR Doc. 06–4804 Filed 5–19–06; 10:22 am]
BILLING CODE 7036–01–M
NATIONAL TRANSPORTATION
SAFETY BOARD
Notice of Sunshine Act Meeting
9:30 a.m., Wednesday,
May 31, 2006.
PLACE: NTSB Conference Center, 429
L’Enfant Plaza, SW., Washington, DC
20594.
STATUS: This one item is open to the
public.
MATTER TO BE CONSIDERED: 7794,
Highway Accident Brief—Passenger
Vehicle Collison with a Fallen Overhead
Girder Eastbound on Interstate 70 at the
Colorado State Route 470 Overpass,
Golden, Colorado, May 15, 2004.
NEWS MEDIA CONTACT: Ted Lopatkiewicz,
Telephone: (202) 314–6100.
Individuals requesting specific
accommodations should contact Chris
Bisett at (202) 314–6305 by Friday, May
26, 2006.
The public may view the meeting via
a live or archived Webcast by accessing
a link under ‘‘News & Events’’ on the
NTSB home page at https://
www.ntsb.gov.
FOR FURTHER INFORMATION CONTACT:
Vicky D’Onofrio, (202) 314–6410.
TIME AND DATE:
Dated: May 19, 2006.
Vicky D’Onofrio,
Federal Register Liaison Officer.
[FR Doc. 06–4836 Filed 5–19–06; 2:41 pm]
BILLING CODE 7533–01–M
PO 00000
Frm 00066
Fmt 4703
Sfmt 4703
29671
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from April 28,
2006 to May 11, 2006. The last biweekly
notice was published on May 9, 2006
(71 FR 26995).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
E:\FR\FM\23MYN1.SGM
23MYN1
rmajette on PROD1PC67 with NOTICES
29672
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR Part 2. Interested persons should
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
PO 00000
Frm 00067
Fmt 4703
Sfmt 4703
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by e-
E:\FR\FM\23MYN1.SGM
23MYN1
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
mail to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
Dominion Energy Kewaunee, Inc. Docket
No. 50–305, Kewaunee Power Station,
Kewaunee County, Wisconsin
rmajette on PROD1PC67 with NOTICES
Date of amendment request: April 6,
2006.
Description of amendment request:
The proposed amendment would allow
the use of a different methodology for
determining the design requirements
necessary for protecting safety-related
equipment from damage by tornado
generated missiles.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The probability of occurrence of an
accident previously evaluated is not
significantly increased by the proposed
change to permit probabilistic evaluation of
missiles generated by natural phenomena.
The actual frequency of tornado occurrence
at Kewaunee is unaffected by the proposed
change in assessment methodology.
Furthermore, the projected frequency of
tornado occurrence, as specified in the USAR
[Updated Safety Analysis Report], is not
significantly affected by this change. The
value for the probability of tornado
occurrence in the updated study is in general
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
agreement with the original value in the
USAR (i.e. 3.97E–4 vs. 4.86E–4). Similarly,
the probability of a tornado-generated missile
is not significantly affected by this change.
Likewise, the consequences of an accident
previously evaluated are not significantly
increased by the proposed change. The actual
probability of a tornado missile onsite
remains unchanged. The actual probability of
a tornado missile strike remains unchanged.
For the limited number of components
affected by this proposed change (i.e. exhaust
ducts and fuel vent), the missile strike
probability is approximately 5.75 x 10¥7 per
year, which is significantly lower than the
SRP [Standard Review Plan] acceptance
criteria of 1 x 10¥6 per year. Therefore, the
proposed change is not considered to
constitute a significant increase in the
consequences of an accident due to the low
probability of occurrence.
In addition, use of a probabilistic versus a
deterministic methodology to assess missile
hazard acceptability has no impact on
accident initiation or consequence.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes involve use of an
evaluation methodology to determine
protection requirements for two specific
support components for safety-related
equipment, which may be adversely affected
by missiles during a tornado. A tornado at
Kewaunee is considered in the USAR as a
separate event and not occurring coincident
with any of the design basis accidents in the
USAR. As such, no new or different kind of
accident is created by the proposed change
to permit probabilistic evaluation of missiles
generated by natural phenomena.
This change involves recognition of the
acceptability of performing tornado missile
strike probability calculations in accordance
with established regulatory guidance in lieu
of using deterministic methodology alone.
Therefore, the change would not create the
possibility of, or be the initiator for, any new
or different kind of accident. The acceptance
criterion of the SRP guidance establishes a
threshold for tornado missile damage to
system components that is consistent with
this conclusion.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The request does not involve a significant
reduction in a margin of safety. The existing
design basis for Kewaunee, with respect to a
tornado affecting safety related equipment, is
to provide positive missile barriers for all
safety-related systems and components. The
proposed change recognizes that for
probability of occurrences below the SRP
established acceptance limit, the extremely
low probability associated with an
PO 00000
Frm 00068
Fmt 4703
Sfmt 4703
29673
‘‘important’’ system or component being
struck by a tornado missile does not
represent a significant reduction in the
margin of safety provided by use of the
deterministic methodology. The change from
‘‘protecting all safety-related systems and
components’’ to ‘‘an extremely low
probability of occurrence of tornado
generated missile strikes on portions of
important systems and components’’ is not
considered to constitute a significant
reduction in the margin of safety.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Bradley D.
Jackson, Esq., Foley and Lardner, P.O.
Box 1497, Madison, WI 53701–1497.
NRC Branch Chief: L. Raghavan.
Dominion Nuclear Connecticut, Inc.,
Docket No. 50–423 Millstone Power
Station, Unit No. 3 New London County,
Connecticut
Date of amendment request: March
28, 2006.
Description of amendment request:
The proposed amendment would
eliminate redundant surveillance
requirements [SRs] pertaining to postmaintenance/post-modification testing.
The associated TS bases will be updated
to address the proposed changes.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes do not modify any
plant equipment and do not impact any
failure modes that could lead to an accident.
Testing in accordance with the requirements
of SR 4.0.1 will continue to provide the
necessary assurance that the associated
systems will function consistent with the
assumptions used in the accident analyses.
On this basis, the proposed amendment does
not increase the probability or consequences
of an accident previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes do not involve any
physical changes to systems, structures, or
components, or involve a change to the
E:\FR\FM\23MYN1.SGM
23MYN1
29674
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
method of plant operation. The requirement
to perform post maintenance/post
modification testing will continue to be
implemented consistent with SR 4.0.1,
through existing plant programs and
procedures. As such, the proposed
amendment does not introduce any new
failure modes, accident initiators or
malfunctions that would cause a new or
different kind of accident. Therefore, the
proposed amendment does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The TS changes do not involve a
significant reduction in a margin of safety
because the requirements described in SR
4.0.1, as implemented through existing plant
programs and procedures, will continue to
ensure that post maintenance/post
modification testing will be performed when
necessary. The proposed change does not
affect any of the assumptions used in the
accident analyses, nor does it affect
operability requirements for equipment
important to plant safety. Therefore, the
margin of safety is not impacted by the
proposed amendment.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Lillian M.
Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc.,
Rope Ferry Road, Waterford, CT 06385.
NRC Branch Chief: Darrell J. Roberts.
rmajette on PROD1PC67 with NOTICES
Energy Northwest, Docket No. 50–397,
Columbia Generating Station, Benton
County, Washington
Date of amendment request: April 17,
2006.
Description of amendment request:
The proposed amendment would
change the method for calculating fuel
pool decay heat load from the original
licensing basis methodology of ORIGEN
and the Auxiliary Systems Branch
Technical Position (ASBTP) 9–2,
‘‘Residual Decay Heat Energy for Light
Water Reactors for Long-Term Cooling,’’
to ORIGEN–ARP.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration is presented below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
The adoption of ORIGEN–ARP does not
affect the probability or consequences of an
accident previously evaluated. The
calculation of the fuel pool decay heat load
is used to evaluate and demonstrate the
ability of the fuel pool cooling system to
maintain the fuel pool temperatures within
the acceptance limits specified in the
Columbia Final Safety Analysis Report
[FSAR]. The proposed change to the
methodology used to calculate the fuel pool
[decay] heat load has no bearing on the
probability or consequences of any
previously evaluated accident. Therefore,
this change does not involve a significant
increase in the probability or consequences
of an accident previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The change involves the use of a different
methodology for calculating fuel pool decay
heat load. This change does not involve any
new equipment, it does not change any
previously approved acceptance limits, and it
does not affect or alter the operation of any
equipment. Therefore[,] this change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The margin of safety provided by the fuel
pool cooling system is primarily defined by
the difference between the maximum
allowed fuel pool temperature and the
boiling point of water. The margin of safety
is supplemented by the ability to make up
water to the spent fuel pool if boiling were
to occur. The proposed change in
methodology for calculating the fuel pool
[decay] heat load does not alter the current
temperature limits or acceptance criteria
specified in the FSAR and has no effect on
the ability to provide make-up water if
boiling were to occur. This change will allow
Energy Northwest to more accurately
calculate the fuel pool [decay] heat load to
provide added confidence in the ability of
the fuel pool cooling system to accommodate
the heat load added to the spent fuel pool
during refueling activities. Therefore, this
change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: William A.
Horin, Esq., Winston & Strawn, 1700 K
Street, NW., Washington, DC 20006–
3817.
NRC Branch Chief: David Terao.
PO 00000
Frm 00069
Fmt 4703
Sfmt 4703
Energy Northwest, Docket No. 50–397,
Columbia Generating Station, Benton
County, Washington
Date of amendment request: April 18,
2006.
Description of amendment request:
The proposed change would modify
technical specification surveillance
requirement 3.6.1.1.2 by changing the
test frequency of the drywell-tosuppression chamber bypass leakage
test from 24 to 120 months. This
proposed amendment also includes
testing the suppression chamber-todrywell vacuum breakers on a 24-month
frequency.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the operation of Columbia
Generating Station in accordance with the
proposed amendment involve a significant
increase in the probability or consequences
of an accident previously evaluated?
Response: No.
The proposed changes would modify
Technical Specification (TS) Surveillance
Requirement (SR) 3.6.1.1.2 and add two new
SRs, SR 3.6.1.1.3 and SR 3.6.1.1.4. The
proposed changes will extend the frequency
for the drywell-to-suppression chamber
bypass leakage test while maintaining the
current leakage testing frequency for the
suppression chamber-to-drywell vacuum
breakers, and establish leakage acceptance
criteria for the suppression chamber-todrywell vacuum breakers when the valves are
tested individually.
The performance of a drywell-tosuppression chamber bypass leakage test or
suppression chamber-to-drywell vacuum
breaker leakage test is not a precursor to any
accident previously evaluated. Thus, the
proposed changes to the performance of the
leakage tests do not have any affect on the
probability of an accident previously
evaluated.
The performance of a drywell-tosuppression chamber bypass leakage test or
a suppression chamber-to-drywell vacuum
breaker leakage test continues to provide
assurance that the containment will perform
as designed. Thus, the radiological
consequences of any accident previously
evaluated are not impacted.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the operation of Columbia
Generating Station in accordance with the
proposed amendment create the possibility of
a new or different kind of accident from any
accident previously evaluated?
Response: No.
The proposed changes to TS SR 3.6.1.1.2,
and the addition of SR 3.6.1.1.3, and SR
3.6.1.1.4 do not affect the assumed
performance of any Columbia Generating
E:\FR\FM\23MYN1.SGM
23MYN1
rmajette on PROD1PC67 with NOTICES
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
Station structure, system or component
previously evaluated. The proposed changes
do not introduce any new modes of system
operation or any new failure mechanisms.
This is an administrative change and does
not involve the modification, addition or
removal of any plant equipment.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the operation of Columbia
Generating Station in accordance with the
proposed amendment involve a significant
reduction in the margin of safety?
Response: No.
The current frequency associated with a
drywell-to-suppression chamber bypass
leakage test in TS SR 3.6.1.1.2 is 24 months
or 12 months if two consecutive tests fail and
continues at this frequency until two
consecutive tests pass. The proposed change
will modify this leakage test frequency to 120
months, or 48 months following one test
failure or 24 months if two consecutive tests
fail and continues at this frequency until two
consecutive tests pass. The proposed change
in SR 3.6.1.1.2 frequency is acceptable as the
results from previous tests show that the
measured drywell-to-suppression chamber
bypass leakage at the current TS frequency
has been a small percentage of the allowable
leakage. Acceptability is further
demonstrated by the design requirements
applied to the primary containment
components and other periodically
performed primary containment inspections.
The proposed SR 3.6.1.1.3 will establish a
leakage test frequency of 24 months for each
suppression chamber-to-drywell vacuum
breaker except when the leakage test of SR
3.6.1.1.2 has been performed within the past
24 months. SR 3.6.1.1.3 specifies a leakage
limit for each suppression chamber-todrywell vacuum breaker pathway of less than
or equal to 12 percent of the bypass leakage
limit of SR 3.6.1.1.2. The proposed SR
3.6.1.1.4 will establish a total leakage limit of
less than or equal to 30 percent of the bypass
leakage limit of SR 3.6.1.1.2 when the
suppression chamber-to-drywell vacuum
breakers are tested in accordance with SR
3.6.1.1.3.
TS SR 3.6.1.1.2 drywell-to-suppression
chamber bypass leakage test monitors the
combined leakage of three types of pathways:
(1) The drywell floor and downcomers, (2)
piping externally connected to both the
drywell and suppression chamber air space,
and (3) the suppression chamber-to-drywell
vacuum breakers. This amendment would
extend the surveillance interval on the
passive components of the test (the first two
types of pathways), while retaining the
current surveillance interval on the active
components (suppression chamber-todrywell vacuum breakers). The proposed
changes establish leakage limits for both
individual suppression chamber-to-drywell
vacuum breakers and the total leakage.
Additional testing is required if acceptable
results are not achieved.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 50.92(c) are satisfied.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Attorney for licensee: William A.
Horin, Esq., Winston & Strawn, 1700 K
Street, NW., Washington, DC 20006–
3817.
NRC Branch Chief: David Terao.
Entergy Nuclear Operations, Inc.,
Docket No. 50–293, Pilgrim Nuclear
Power Station, Plymouth County,
Massachusetts
Date of amendment request: April 12,
2006.
Description of amendment request:
The proposed amendment would revise
the Technical Specification reactor
pressure vessel Pressure and
Temperature (P–T) curves.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed License Amendment (LA)
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated. There are no physical
changes to the plant being introduced by the
proposed changes to the pressuretemperature curves. The proposed change
does not modify the reactor coolant pressure
boundary, (i.e., there are no changes in
operating pressure, materials, or seismic
loading). The proposed change does not
adversely affect the integrity of the reactor
coolant pressure boundary such that its
function in the control of radiological
consequences is affected.
The proposed pressure-temperature curves
are generated in accordance with the fracture
toughness requirements of 10 CFR 50
Appendix G, and American Society of
Mechanical Engineers (ASME) Boiler and
Pressure Vessel (B&PV) Code, Section Xl,
Appendix G and Regulatory Guide (R.G.)
1.99, Revision 2[,] ‘‘Radiation Embrittlement
of Reactor Vessel Materials.’’ A best-estimate
calculation of reactor vessel 34 effective full
power years (EFPYs) neutron fluence and
associated uncertainty has been completed
for Pilgrim using the Radiation Analysis
Modeling Application (RAMA) methodology.
This methodology was previously approved
by the NRC. The resulting reactor vessel
neutron fluence value was then used in
conjunction with R.G. 1.99, [Revision] 2 to
determine the adjusted reference temperature
(ART) and with ASME Section Xl Appendix
G to develop revised P-T curves.
PO 00000
Frm 00070
Fmt 4703
Sfmt 4703
29675
This provides sufficient assurance that the
Pilgrim reactor vessel will be operated in a
manner that will protect it from brittle
fracture under all operating conditions. This
proposed license amendment provides
compliance with the intent of 10 CFR [Part
50] Appendix G and provides margins of
safety that assure reactor vessel integrity.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. [Does] the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed license amendment does not
create the possibility of new or different kind
of accident from any accident previously
evaluated. The revised pressure-temperature
curves are generated in accordance with the
fracture toughness requirements of 10 CFR
Part 50 Appendix G and ASME Section Xl
Appendix G. Compliance with the proposed
pressure-temperature curves will ensure the
avoidance of conditions in which brittle
fracture of primary coolant pressure
boundary materials is possible because such
compliance with the pressure-temperature
curves provides sufficient protection against
a non-ductile-type fracture of the reactor
pressure vessel. No new modes of operation
are introduced by the proposed change. The
proposed change will not create any failure
mode not bounded by previously evaluated
accidents. Further, the proposed change does
not affect any activities or equipment and is
not assumed in any safety analysis to initiate
any accident sequence. This provides
sufficient assurance that Pilgrim reactor
vessel will be operated in a manner that will
protect it from brittle fracture under all
operating conditions.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. [Does] the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed license amendment requests
the use of revised P-T curves that are based
on established NRC and ASME
methodologies. A best-estimate calculation of
reactor vessel neutron fluence and associated
uncertainty has been completed for Pilgrim
through 34 EFPY using the NRC approved
RAMA methodology. The 34 EFPY reactor
vessel neutron fluence value was used in
conjunction with R.G. 1.99, [Revision 2] to
compute reference temperature shift, and
with ASME Section Xl Appendix G to
develop revised P-T curves. This provides
sufficient margin such that the Pilgrim
reactor vessel will be operated in a manner
that will protect it from brittle fracture under
all operating conditions. Operation within
the proposed limits ensures that the reactor
vessel materials will continue to behave in a
non-brittle manner, thereby preserving the
original safety design bases. No plant
safetylimits, set points, or design parameters
are adversely affected by the proposed
changes.
E:\FR\FM\23MYN1.SGM
23MYN1
29676
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 50.92(c) are satisfied.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Attorney for licensee: Travis C.
McCullough, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 400
Hamilton Avenue, White Plains, NY
10601.
Branch Chief: Richard Laufer.
rmajette on PROD1PC67 with NOTICES
Entergy Nuclear Operations, Inc.,
Docket No. 50–293, Pilgrim Nuclear
Power Station, Plymouth County,
Massachusetts
Date of amendment request: June 2,
2005.
Description of amendment request:
The proposed amendment would revise
the Technical Specification (TS) reactor
coolant system leakage detection
instrumentation requirements and
actions.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No. The proposed relocation is
administrative in nature and does not involve
the modification of any plant equipment or
affect basic plant operation. The associated
instrumentation and surveillances are not
assumed to be an initiator of any analyzed
event, nor are these functions assumed in the
mitigation of consequences of accidents.
Additionally, the associated required actions
for inoperable components do not impact the
initiation or mitigation of any accident.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No. The proposed change does
not involve any physical alteration of plant
equipment and does not change the method
by which any safety-related system performs
its function. As such, no new or different
types of equipment will be installed, and the
basic operation of installed equipment is
unchanged. The methods governing plant
operation and testing remain consistent with
current safety analysis assumptions.
Therefore, the proposed change does not
create the possibility of a new or different
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No. The proposed change to
relocate current TS requirements to the FSAR
[Final Safety Analysis Report], consistent
with regulatory guidance and previously
approved changes for other stations, are
administrative in nature. These changes do
not negate any existing requirement, and do
not adversely affect existing plant safety
margins or the reliability of the equipment
assumed to operate in the safety analysis. As
such, there are no changes being made to
safety analysis assumptions, safety limits or
safety system settings that would adversely
affect plant safety as a result of the proposed
change. Margins of safety are unaffected by
requirements that are retained, but relocated
from the Technical Specifications to the
FSAR. Additionally, the changes being made
to allow additional repair time for inoperable
instrumentation will not affect the required
leakage limits, which will continue to be
monitored at the same required frequency.
These compensatory measures, operational
limitations, and administrative functions that
will be modified are not credited in any
design-basis event and do not reflect a
margin of safety. Therefore, the proposed
change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 50.92(c) are satisfied.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Attorney for licensee: Travis C.
McCullough, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 400
Hamilton Avenue, White Plains, NY
10601.
Branch Chief: Richard Laufer.
Exelon Generation Company, LLC,
Docket Nos. STN 50–454 and STN 50–
455, Byron Station, Unit Nos. 1 and 2,
Ogle County, Illinois
Docket Nos. STN 50–456 and STN 50–
457, Braidwood Station, Unit Nos. 1 and
2, Will County, Illinois.
Date of amendment request:
November 18, 2005.
Description of amendment request:
The proposed amendment would revise
the Technical Specifications (TS) to
adopt NRC-approved Revision 4 to
Technical Specification Task Force
(TSTF) Standard Technical
Specification Change Traveler, TSTF–
449, ‘‘Steam Generator Tube Integrity.’’
The proposed amendment would also
include changes to the TS definition of
Leakage, TS 3.4.13, ‘‘RCS [Reactor
Coolant System] Operational
LEAKAGE,’’ TS 5.5.9, ‘‘Steam Generator
(SG) Program,’’ TS 5.6.9, Steam
Generator Tube Inspection Report,’’ and
PO 00000
Frm 00071
Fmt 4703
Sfmt 4703
would add TS 3.4.19, ‘‘Steam Generator
(SG) Tube Integrity.’’ The proposed
changes are necessary in order to
implement the guidance for the industry
initiative on Nuclear Energy Institute
(NEI) 97–06, ‘‘Steam Generator Program
Guidelines.’’
The NRC staff issued a notice of
opportunity for comment in the Federal
Register on March 2, 2005 (70 FR
10298), on possible amendments
adopting TSTF–449, including a model
safety evaluation and model no
significant hazards consideration
(NSHC) determination, using the
consolidated line item improvement
process. The NRC staff subsequently
issued a notice of availability of the
models for referencing in license
amendment applications in the Federal
Register on May 6, 2005 (70 FR 24126).
The licensee affirmed the applicability
of the published NSHC determination in
its application dated November 18,
2005.
The licensee included a variation
from TSTF–449 for Braidwood, Unit 2
and Byron, Unit 2 in that the proposed
amendment would also include an
effective change to the definition of
primary pressure boundary from the
hot-leg tube end weld to 17 inches
below the top of the hot-leg tube sheet.
The proposed amendment would also
delete the current TS allowance to use
Westinghouse laser welded sleeves as a
SG tube repair method. The licensee
provided an analyses of the NSHC issue
in its application for the plant-specific
variations from TSTF–449.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
Exelon Generation Company, LLC, (EGC)
has reviewed the proposed no significant
hazards consideration determination
published on March 2, 2005 (i.e., 70 FR
10298) as part of the consolidated line item
improvement process (CLIIP) item. EGC has
concluded that the proposed determination
presented in the notice is applicable to
Braidwood Station, Units 1 and 2, and Byron
Station, Units 1 and 2, and the determination
is hereby incorporated by reference to satisfy
the requirements of 10 CFR 50.91 (a), except
as discussed below.
The proposed amendment also revises the
Technical Specification Task Force (TSTF)
Standard Technical Specification Change
Traveler, TSTF–449, ‘‘Steam Generator Tube
Integrity,’’ Revision 4, version of TS 5.5.9,
Steam Generator Program, to exclude the
portion of the tube below 17 inches from the
top of the hot leg tubesheet in the Braidwood
Station, Unit 2, and Byron Station, Unit 2,
steam generators from TS 5.5.9.d, ‘‘Provisions
for SG tube inspections.’’ This proposed
E:\FR\FM\23MYN1.SGM
23MYN1
rmajette on PROD1PC67 with NOTICES
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
license amendment request, in effect,
redefines the Braidwood Station, Unit 2, and
Byron Station, Unit 2, primary pressure
boundary from the hot leg tube end weld to
17 inches below the top of the hot leg tube
sheet. This proposed license amendment also
deletes the current TS 5.5.9.e.6 and TS
5.5.9.e.10 allowance to use Westinghouse
laser welded sleeves as a SG tube repair
method.
EGC has evaluated whether or not a
significant hazards consideration is involved
with the proposed TS change by focusing on
the three criteria set forth in 10 CFR 50.92
as discussed below:
Criterion 1.—Does the proposed change
involve a significant increase in the
probability or consequences of an accident
previously evaluated?
Response: No.
The previously analyzed accidents are
initiated by the failure of plant structures,
systems, or components. The proposed
changes that alter the SG inspection criteria
and delete the allowance to repair SG tubes
using Westinghouse laser welded sleeves do
not have a detrimental impact on the
integrity of any plant structure, system, or
component that initiates an analyzed event.
The proposed changes will not alter the
operation of, or otherwise increase the failure
probability of any plant equipment that
initiates an analyzed accident. Therefore, the
proposed change does not involve a
significant increase in the probability of an
accident previously evaluated.
Of the applicable accidents previously
evaluated, the limiting transients with
consideration to the proposed changes to the
SG tube inspection criteria, are the SG tube
rupture (SGTR) event and the steam line
break (SLB) accident.
During the SGTR event, the required
structural integrity margins of the SG tubes
will be maintained by the presence of the SG
tubesheet. SG tubes are hydraulically
expanded in the tubesheet area. Tube rupture
in tubes with cracks in the tubesheet is
precluded by the constraint provided by the
tubesheet. This constraint results from the
hydraulic expansion process, thermal
expansion mismatch between the tube and
tubesheet and from the differential pressure
between the primary and secondary side.
Based on this design, the structural margins
against burst, discussed in Regulatory Guide
(RG) 1.121, ‘‘Bases for Plugging Degraded
PWR [Pressurized Water Reactor] SG Tubes,’’
are maintained for both normal and
postulated accident conditions.
The proposed changes do not affect other
systems, structures, components or
operational features. Therefore, the proposed
changes result in no significant increase in
the probability of the occurrence of a SGTR
accident.
At normal operating pressures, leakage
from primary water stress corrosion cracking
(PWSCC) below the proposed limited
inspection depth is limited by both the tubeto-tubesheet crevice and the limited crack
opening permitted by the tubesheet
constraint. Consequently, negligible normal
operating leakage is expected from cracks
within the tubesheet region. The
consequences of an SGTR event are affected
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
by the primary-to-secondary leakage flow
during the event. Primary-to-secondary
leakage flow through a postulated broken
tube is not affected by the proposed change
since the tubesheet enhances the tube
integrity in the region of the hydraulic
expansion by precluding tube deformation
beyond its initial hydraulically expanded
outside diameter.
The probability of a SLB is unaffected by
the potential failure of a SG tube as this
failure is not an initiator for a SLB.
The consequences of a SLB are also not
significantly affected by the proposed
changes. During a SLB accident, the
reduction in pressure above the tubesheet on
the shell side of the SG creates an axially
uniformly distributed load on the tubesheet
due to the reactor coolant system pressure on
the underside of the tubesheet. The resulting
bending action constrains the tubes in the
tubesheet thereby restricting primary-tosecondary leakage below the midplane.
Primary-to-secondary leakage from tube
degradation in the tubesheet area during the
limiting accident (i.e., SLB) is limited by flow
restrictions resulting from the crack and tubeto-tubesheet contact pressures that provide a
restricted leakage path above the indications
and also limit the degree of potential crack
face opening as compared to free span
indications. The primary-to-secondary leak
rate during postulated SLB accident
conditions would be expected to be less than
that during normal operation for indications
near the bottom of the tubesheet (i.e.,
including indications in the tube end welds).
This conclusion is based on the observation
that while the driving pressure causing
leakage increases by approximately a factor
of two, the flow resistance associated with an
increase in the tube-to-tubesheet contact
pressure, during a SLB, increases by up to
approximately a factor of three. While such
a leakage decrease is logically expected, the
postulated accident leak rate could be
conservatively bounded by twice the normal
operating leak rate if the increase in contact
pressure is ignored. Since normal operating
leakage is limited to less than 0.104 gpm
[gallons per minute] (150 gpd [gallons per
day]) per TS 3.4.13, ‘‘RCS Operational
Leakage,’’ the associated accident condition
leak rate, assuming all leakage to be from
lower tubesheet indications, would be
bounded by approximately 0.2 gpm. This
value is well within the assumed accident
leakage rate of 0.5 gpm discussed in Updated
Final Safety Analysis Table 15.1–3,
‘‘Parameters Used in Steam Line Break
Analyses.’’ Hence it is reasonable to omit any
consideration of inspection of the tube, tube
end weld, bulges/overexpansions or other
anomalies below 17 inches from the top of
the hot leg tubesheet. Therefore, the
consequences of a SLB accident remain
unaffected.
Based on the above discussion, the
proposed changes do not involve an increase
in the consequences of an accident
previously evaluated.
Criterion 2.—Does the proposed change
create the possibility of a new or different
kind of accident from any accident
previously evaluated?
Response: No.
PO 00000
Frm 00072
Fmt 4703
Sfmt 4703
29677
The proposed changes do not involve the
use or installation of new equipment and the
currently installed equipment will not be
operated in a new or different manner. No
new or different system interactions are
created and no new processes are introduced.
The proposed changes will not introduce any
new failure mechanisms, malfunctions, or
accident initiators not already considered in
the design and licensing bases.
Based on this evaluation, the proposed
change does not create the possibility of a
new or different kind of accident from any
accident previously evaluated.
Criterion 3.—Does the proposed change
involve a significant reduction in a margin of
safety?
Response: No.
The proposed changes maintain the
required structural margins of the SG tubes
for both normal and accident conditions.
Nuclear Energy Institute (NEI) 97–06, ‘‘Steam
Generator Program Guidelines,’’ Revision 1
and Regulatory Guide (RG) 1.121, ‘‘Bases for
Plugging Degraded PWR Steam Generator
Tubes,’’ are used as the bases in the
development of the limited hot leg tubesheet
inspection depth methodology for
determining that SG tube integrity
considerations are maintained within
acceptable limits. RG 1.121 describes a
method acceptable to the NRC for meeting
General Design Criteria (GDC) 14, ‘‘Reactor
coolant pressure boundary,’’ GDC 15,
‘‘Reactor coolant system design,’’ GDC 31,
‘‘Fracture prevention of reactor coolant
pressure boundary,’’ and GDC 32,
‘‘Inspection of reactor coolant pressure
boundary,’’ by reducing the probability and
consequences of a SGTR. RG 1.121 concludes
that by determining the limiting safe
conditions for tube wall degradation the
probability and consequences of a SGTR are
reduced. This RG uses safety factors on loads
for tube burst that are consistent with the
requirements of Section III of the American
Society of Mechanical Engineers (ASME)
Code.
For axially oriented cracking located
within the tubesheet, tube burst is precluded
due to the presence of the tubesheet. For
circumferentially oriented cracking,
Westinghouse letter LTR–CDME–05–32,
‘‘Limited Inspection of the Steam Generator
Tube Portion Within the Tubesheet at Byron
Unit 2 and Braidwood Unit 2,’’ Revision 2,
dated August 2005, defines a length of
degradation free expanded tubing that
provides the necessary resistance to tube
pullout due to the pressure induced forces,
with applicable safety factors applied.
Application of the limited hot leg tubesheet
inspection depth criteria will preclude
unacceptable primary-to-secondary leakage
during all plant conditions. The methodology
for determining leakage provides for large
margins between calculated and actual
leakage values in the proposed limited hot
leg tubesheet inspection depth criteria.
Therefore, the proposed changes do not
involve a significant hazards consideration
under the criteria set forth in 10 CFR
50.92(c).
The NRC staff has reviewed the
licensee’s analysis and, based on this
E:\FR\FM\23MYN1.SGM
23MYN1
29678
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Brad J.
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
rmajette on PROD1PC67 with NOTICES
Exelon Generation Company, LLC,
Docket Nos. 50–254 and 50–265, Quad
Cities Nuclear Power Station, Units 1
and 2, Rock Island County, Illinois
Date of amendment request: January
25, 2006.
Description of amendment request:
The proposed amendment would revise
the Updated Final Safety Analysis
Report (UFSAR) to allow the use of
automatic load tap changers (LTCs) to
operate in automatic mode on the
reserve auxiliary transformers (RATs) to
compensate for potential offsite power
voltage fluctuations, in order to ensure
that acceptable voltage is maintained for
safety related equipment.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The requested change allows the automatic
operation mode of the LTC. The only
accident previously evaluated for which the
probability is potentially affected by the
change is the loss of offsite power (LOOP).
A failure of the LTC while in automatic
operation mode that results in decreased
voltage to the ESS [essential service system]
buses could cause a LOOP. This could occur
in two ways. A failure of the LTC controller
that results in rapidly decreasing the voltage
to the emergency buses is the most severe
failure mode. However, a backup controller
is provided with the LTC that makes this
failure unlikely. A failure of the LTC
controller to respond to decreasing grid
voltage is less severe, since grid voltage
changes occur slowly. In both of the above
potential failure modes, operators will take
manual control of the LTC to mitigate the
effects of the failure. Thus, the probability of
a LOOP is not significantly increased.
The proposed change has no effect on the
consequences of a LOOP, since the
emergency diesel generators provide power
to safety related equipment following a
LOOP. The emergency diesel generators are
not affected by the proposed change.
The probability of other accidents
previously evaluated is not affected, since the
proposed change does not affect the way
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
plant equipment is operated and thus does
not contribute to the initiation of any of the
previously evaluated accidents.
The LTC is equipped with a backup
controller, which controls the LTC in the
event of primary controller failure.
Additionally, operator action is available to
prevent a sustained high voltage condition
from occurring. Damage due to over-voltage
is time-dependent. Therefore, damage of
safety related equipment is extremely
unlikely, and the consequences of these
accidents are not significantly increased. The
only way in which the consequences of other
previously evaluated accidents could be
affected is if a failure of the LTC, while in
automatic operation mode, led to a sustained
high voltage condition, which resulted in
damage to safety related equipment that is
used to mitigate an accident.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change involves functions
that provide offsite power to safety related
equipment for accident mitigation. Thus, the
proposed change potentially affects the
consequences of previously evaluated
accidents (as addressed in Question 1), but
does not result in any new mechanisms that
could initiate damage to the reactor and its
principal safety barriers (i.e., fuel cladding,
reactor coolant system, or primary
containment).
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change does not affect the
inputs or assumptions of any of the analyses
that demonstrate the integrity of the fuel
cladding, reactor coolant system, or
containment during accident conditions. The
allowable values for the degraded voltage
protection function are unchanged and will
continue to ensure that the degraded voltage
protection function actuates when required,
but does not actuate prematurely to cause a
LOOP. Automatic operation of the LTC
increases margin by reducing the potential
for transferring to the EDGs [emergency
diesel generators] during an event.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Bradley J.
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
PO 00000
Frm 00073
Fmt 4703
Sfmt 4703
Exelong Way, Kennett Square, PA
19348.
NRC Branch Chief: Daniel S. Collins.
FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–440,
Perry Nuclear Power Plant, Unit 1, Lake
County, Ohio
Date of amendment request: February
10, 2006.
Description of amendment request:
The proposed amendment would
modify Technical Specification (TS)
3.3.5.1, ‘‘Emergency Core Cooling
System (ECCS) Instrumentation,’’ to
correct a Perry Nuclear Power Plant
(PNPP)-specific issue and establish
consistency with the improved standard
technical specifications (ISTS).
Specifically, Sub-actions B.1.2.1 and
B.1.2.2, which were added into PNPP
TS 3.3.5.1 during the ISTS conversion
process, will be deleted. PNPP Required
Action B.1 will then match the ISTS
Required Action B.1. As a result, actions
with a 1-hour completion time will only
be required for the annulus exhaust gas
treatment (AEGT) system if a loss of
initiation capability in both divisions
actually exists for an AEGT initiation
function, as originally intended.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
1. The proposed change does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated.
There are no physical modifications being
made to any plant system or component. The
only change is to a Required Action within
the Technical Specifications. The revised
Technical Specification requirements do not
impact initiators of previously evaluated
accidents or transients.
The specification being revised is
associated with a system used to mitigate the
consequences of accidents. The change does
not affect how the AEGT system is
controlled, operated, or tested. The intent of
Required Action B.1 for the ECCS
Instrumentation, specifically, a loss of
initiation capability check, is maintained by
the changes being proposed. The wording of
Required Action B.1 ensures appropriate
actions are taken when a loss of initiation
capability exists, by declaring the supported
systems inoperable. This action is consistent
with the current requirements.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. The proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
There are no physical modifications being
made to any plant system or component, and
E:\FR\FM\23MYN1.SGM
23MYN1
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
the proposed change introduces no new
method of operation for the plant, or its
systems or components. Therefore, the
proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. The proposed change does not involve
a significant reduction in a margin of safety.
The change to the ECCS Instrumentation
Required Action continues to ensure that a
check is performed to determine if one or
more of the ECCS Instrumentation Functions
has lost its capability to actuate the Division
1 and 2 low-pressure ECCS, the AEGT
subsystems, and the associated diesel
generators. It continues to direct appropriate
actions if such a loss of initiation capability
is found. Therefore, the necessary function of
the Technical Specification requirements is
maintained, and the proposed changes do not
involve a significant reduction in a margin of
safety.
rmajette on PROD1PC67 with NOTICES
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David W.
Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street,
Akron, OH 44308.
NRC Branch Chief: Daniel S. Collins.
Nuclear Management Company, LLC,
Docket No. 50–255, Palisades Plant, Van
Buren County, Michigan
Date of amendment request: February
16, 2006.
Description of amendment request:
The proposed amendment would revise
the Technical Specification (TS)
requirements related to steam generator
(SG) tube integrity. The change is
consistent with NRC-approved Revision
4 to Technical Specification Task Force
(TSTF) Standard Technical
Specification Change Traveler, TSTF–
449, ‘‘Steam Generator Tube Integrity.’’
The availability of this TS improvement
was announced in the Federal Register
on May 6, 2005 (70 FR 24126) as part
of the consolidated line item
improvement process (CLIIP).
The NRC staff issued a notice of
availability of a model no significant
hazards consideration (NSHC)
determination for referencing in license
amendment applications in the Federal
Register on March 2, 2005 (70 FR
10298) as part of the CLIIP. The licensee
affirmed the applicability of the model
NSHC determination in its application
dated February 16, 2006.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
issue of no significant hazards
consideration, which is presented
below:
Criterion 1.—The Proposed Change Does Not
Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated
The proposed change requires a SG
Program that includes performance criteria
that will provide reasonable assurance that
the SG tubing will retain integrity over the
full range of operating conditions (including
startup, operation in the power range, hot
standby, cooldown and all anticipated
transients included in the design
specification). The SG performance criteria
are based on tube structural integrity,
accident induced leakage, and operational
LEAKAGE.
A SGTR [steam generator tube rupture]
event is one of the design basis accidents that
are analyzed as part of a plant’s licensing
basis. In the analysis of a SGTR event, a
bounding primary to secondary LEAKAGE
rate equal to the operational LEAKAGE rate
limits in the licensing basis plus the
LEAKAGE rate associated with a doubleended rupture of a single tube is assumed.
For other design basis accidents such as
MSLB [main steamline break], rod ejection,
and reactor coolant pump locked rotor the
tubes are assumed to retain their structural
integrity (i.e., they are assumed not to
rupture). These analyses typically assume
that primary to secondary LEAKAGE for all
SGs is 1 gallon per minute or increases to 1
gallon per minute as a result of accident
induced stresses. The accident induced
leakage criterion introduced by the proposed
changes accounts for tubes that may leak
during design basis accidents. The accident
induced leakage criterion limits this leakage
to no more than the value assumed in the
accident analysis.
The SG performance criteria proposed
change to the TS identify the standards
against which tube integrity is to be
measured. Meeting the performance criteria
provides reasonable assurance that the SG
tubing will remain capable of fulfilling its
specific safety function of maintaining
reactor coolant pressure boundary integrity
throughout each operating cycle and in the
unlikely event of a design basis accident. The
performance criteria are only a part of the SG
Program required by the proposed change to
the TS. The program, defined by NEI
[Nuclear Energy Institute] 97–06, Steam
Generator Program Guidelines, includes a
framework that incorporates a balance of
prevention, inspection, evaluation, repair,
and leakage monitoring. The proposed
changes do not, therefore, significantly
increase the probability of an accident
previously evaluated.
The consequences of design basis accidents
are, in part, functions of the DOSE
EQUIVALENT I–131 in the primary coolant
and the primary to secondary LEAKAGE
rates resulting from an accident. Therefore,
limits are included in the plant technical
specifications for operational leakage and for
DOSE EQUIVALENT I–131 in primary
coolant to ensure the plant is operated within
its analyzed condition. The typical analysis
PO 00000
Frm 00074
Fmt 4703
Sfmt 4703
29679
of the limiting design basis accident assumes
that primary to secondary leak rate after the
accident is 1 gallon per minute with no more
than [500 gallons per day or 720 gallons per
day] in any one SG, and that the reactor
coolant activity levels of DOSE
EQUIVALENT I–131 are at the TS values
before the accident.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary coolant chemistry controls. The
proposed approach updates the current TSs
and enhances the requirements for SG
inspections. The proposed change does not
adversely impact any other previously
evaluated design basis accident and is an
improvement over the current TSs.
Therefore, the proposed change does not
affect the consequences of a SGTR accident
and the probability of such an accident is
reduced. In addition, the proposed changes
do not affect the consequences of an MSLB,
rod ejection, or a reactor coolant pump
locked rotor event, or other previously
evaluated accident.
Criterion 2.—The Proposed Change Does Not
Create the Possibility of a New or Different
Kind of Accident From Any Previously
Evaluated
The proposed performance based
requirements are an improvement over the
requirements imposed by the current
technical specifications. Implementation of
the proposed SG Program will not introduce
any adverse changes to the plant design basis
or postulated accidents resulting from
potential tube degradation. The result of the
implementation of the SG Program will be an
enhancement of SG tube performance.
Primary to secondary LEAKAGE that may be
experienced during all plant conditions will
be monitored to ensure it remains within
current accident analysis assumptions.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary or secondary coolant chemistry
controls. In addition, the proposed change
does not impact any other plant system or
component. The change enhances SG
inspection requirements.
Therefore, the proposed change does not
create the possibility of a new or different
type of accident from any accident
previously evaluated.
Criterion 3.—The Proposed Change Does
Not Involve a Significant Reduction in the
Margin of Safety.
The SG tubes in pressurized water reactors
are an integral part of the reactor coolant
pressure boundary and, as such, are relied
upon to maintain the primary system’s
pressure and inventory. As part of the reactor
coolant pressure boundary, the SG tubes are
unique in that they are also relied upon as
a heat transfer surface between the primary
and secondary systems such that residual
heat can be removed from the primary
system. In addition, the SG tubes isolate the
radioactive fission products in the primary
coolant from the secondary system. In
summary, the safety function of an SG is
maintained by ensuring the integrity of its
tubes.
Steam generator tube integrity is a function
of the design, environment, and the physical
condition of the tube. The proposed change
E:\FR\FM\23MYN1.SGM
23MYN1
29680
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
does not affect tube design or operating
environment. The proposed change is
expected to result in an improvement in the
tube integrity by implementing the SG
Program to manage SG tube inspection,
assessment, repair, and plugging. The
requirements established by the SG Program
are consistent with those in the applicable
design codes and standards and are an
improvement over the requirements in the
current TSs.
For the above reasons, the margin of safety
is not changed and overall plant safety will
be enhanced by the proposed change to the
TS.
Based upon the reasoning presented above
and the previous discussion of the
amendment request, the requested change
does not involve a significant hazards
consideration.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jonathan Rogoff,
Esquire, Vice President, Counsel &
Secretary, Nuclear Management
Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Branch Chief: L. Raghavan.
Tennessee Valley Authority, Docket No.
50–259 , Browns Ferry Nuclear Plant,
Unit 1, Limestone County, Alabama
rmajette on PROD1PC67 with NOTICES
Date of amendment request: July 9,
2004 (TS–436).
Description of amendment request:
The proposed amendment would revise
Technical Specification Surveillance
Requirement 3.6.1.3.10 to increase the
allowed main steam isolation valve
(MSIV) leak rate from 11.5 standard
cubic feet per hour (scfh) per valve, to
100 scfh for individual MSIVs with a
150 scfh combined leakage for all four
main steam lines.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
TVA proposes to utilize the main steam
drain lines to preferentially direct MSIV
leakage to the main condenser. This drain
path takes advantage of the large volume of
the steam lines and condenser to provide
holdup and plate-out of fission products that
may leak through the closed MSIVs. In this
approach, the main steam lines, steam drain
piping, and the main condenser are used to
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
mitigate the consequences of an accident to
limit potential doses below the limits
prescribed in 10 CFR 50.67(b)(2)(i) for the
exclusion area, 10 CFR 50.67(b)(2)(ii) for the
low population zone, and in 10 CFR
50.67(b)(2)(iii) for control room personnel.
Seismic verification walkdowns and
evaluations of bounding piping/supports
were performed to demonstrate the main
steam line piping and components that
comprise the Alternate Leakage Treatment
(ALT) path were rugged and able to perform
the safety function of MSIV leakage control
following a Design Basis Earthquake (DBE).
Thus, it has been concluded the components
in the MSIV alternate leakage treatment flow
path can be relied upon to maintain
structural integrity.
Therefore, the proposed amendment does
not involve changes to structures,
components, or systems which would affect
the probability of an accident previously
evaluated in the Browns Ferry Updated Final
Safety Analysis Report (UFSAR).
A plant-specific radiological analysis has
been performed to assess the effects of the
proposed increase in MSIV leakage
acceptance criteria in terms of off-site doses
and main control room dose. The analysis
shows the dose contribution from the
proposed increase in leakage acceptance
criteria is acceptable compared to doses
limits prescribed in 10 CFR 50.67(b)(2)(i) for
the exclusion area, 10 CFR 50.67(b)(2)(ii) for
the low population zone, and in 10 CFR
50.67(b)(2)(iii) for control room personnel.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes require the use of
the main steam piping and the condenser to
process MSIV leakage. This additional
function does not compromise the reliability
of these systems. They will continue to
function as intended and not be subject to a
failure of a different kind than previously
considered. In addition, MSIV functionality
will not be adversely impacted by the
increased leakage limit. Therefore, the
proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change to Surveillance
Requirement 3.6.1.3.10, to increase the
allowable MSIV leakage, does not involve a
significant reduction in the margin of safety.
The allowable leak rate specified for the
MSIVs is used to quantify a maximum
amount of leakage assumed to bypass
containment. The results of the re-analysis
supporting these changes were evaluated
against the dose limits contained in 10 CFR
50.67(b)(2)(i) for the exclusion area, 10 CFR
50.67(b)(2)(ii) for the low population zone,
and in 10 CFR 50.67(b)(2)(iii) for control
room personnel. Sufficient margin relative to
the regulatory limits is maintained even
when conservative assumptions and methods
are utilized. Therefore, the proposed change
does not involve a significant reduction in a
margin of safety.
PO 00000
Frm 00075
Fmt 4703
Sfmt 4703
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L.
Marshall, Jr.
Tennessee Valley Authority, Docket
Nos. 50–259, 50–260 and 50–296,
Browns Ferry Nuclear Plant, Units 1, 2
and 3, Limestone County, Alabama
Date of amendment request: August
16, 2004 (TS—447).
Description of amendment request:
The proposed amendment would extend
the channel calibration frequency
requirements for instrumentation in the
high pressure coolant injection, reactor
core isolation cooling, and reactor water
core isolation cooling systems.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes extend the channel
calibration surveillance frequency of
instrumentation used for the high area
temperature isolation of the high pressure
coolant injection (HPCI), reactor core
isolation cooling (RCIC), and the reactor
water clean-up (RWCU) systems. The
allowable trip point value for three sets of
RCIC instruments on each unit and for two
sets of RWCU instruments on Unit 1 are also
revised. The calibration surveillance
frequency is extended to 24 months from 92
days (for the HPCI and RCIC high area
temperature instrumentation) and from 122
days (for the RWCU high area temperature
instrumentation). Under certain
circumstances, Technical Specifications (TS)
SR [Surveillance Requirement] 3.0.2 would
allow a maximum surveillance interval of 30
months for an SR having a nominal 24-month
performance frequency. Instrumentation
scaling and setpoint calculations performed
in accordance with the guidelines of Generic
Letter 91–04 have shown that the reliability
of the affected protection instrumentation
will be preserved for the maximum allowable
calibration surveillance interval. The Unit 1
instrumentation will be physically modified
to be essentially identical to that installed on
Unit 2 and Unit 3 prior to restart of Unit 1.
Therefore, the proposed change does not
involve a significant increase in the
E:\FR\FM\23MYN1.SGM
23MYN1
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes extend the channel
calibration surveillance frequency of
instrumentation used for the high area
temperature isolation of the high pressure
coolant injection (HPCI), reactor core
isolation cooling (RCIC), and the reactor
water clean-up (RWCU) systems. The
allowable trip point value for three sets of
RCIC instruments on each unit and for two
sets of RWCU instruments on Unit 1 are also
revised. The instrumentation will function in
the same way following the amendment as it
functions currently. Hence, the changes do
not create the possibility of any new failure
mechanisms. Note that the Unit 1
instrumentation will be modified to be
essentially identical to that installed on Unit
2 and Unit 3 prior to restart of Unit 1.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes extend the channel
calibration surveillance frequency of
instrumentation used for the high area
temperature isolation of the high pressure
coolant injection (HPCI), reactor core
isolation cooling (RCIC), and the reactor
water clean-up (RWCU) systems. The
allowable trip point value for three sets of
RCIC instruments on each unit and for two
sets of RWCU instruments on Unit 1 are also
revised. Instrumentation scaling and setpoint
calculations performed in accordance with
the guidelines of Generic Letter 91–04 have
shown safety margins are preserved with the
extended surveillance frequency and the
revised TS allowable values. Therefore, the
proposed change does not involve a
significant reduction in a margin of safety.
rmajette on PROD1PC67 with NOTICES
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L.
Marshall, Jr.
Tennessee Valley Authority (TVA),
Docket No. 50–390, Watts Bar Nuclear
Plant (WBN), Unit 1, Rhea County,
Tennessee
Date of amendment request: May 8,
2006 (TS–06–09).
Description of amendment request:
The proposed amendment would revise
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
the limiting condition for operation for
Technical Specification (TS) Section
3.7.9, ‘‘Ultimate Heat Sink.’’ The
maximum essential raw cooling water
(ERCW) temperature limit associated
with Surveillance Requirement 3.7.9.1
would increase from 85 degrees
Fahrenheit (°F) to 88 °F. This proposed
change is based on evaluations of the
ERCW system and the ultimate heat sink
(UHS) functions and maximum
temperatures that will satisfy the
associated safety functions.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change to increase the UHS
maximum temperature will not adversely
alter the function, design, or operating
practices for plant systems or components.
The UHS is utilized to remove heat loads
from plant systems during normal and
accident conditions. This function is not
expected or postulated to result in the
generation of any accident and continues to
adequately satisfy the associated safety
functions with the proposed changes.
Therefore, the probability of an accident
presently evaluated in the safety analyses
will not be increased. The heat loads, that the
UHS is designed to accommodate, have been
evaluated with the higher temperature limit.
The result of these evaluations is that there
is existing margin associated with the
systems that utilize the UHS for normal and
accident conditions. These margins are
sufficient to accommodate the postulated
normal and accident heat loads with the
proposed changes to the UHS. Since the
safety functions of the UHS are maintained,
the systems that ensure acceptable offsite
dose consequences will continue to operate
as designed. The change in the maximum
calculated containment pressure associated
with the design basis loss-of-coolant-accident
(LOCA) remains below the American Society
of Mechanical Engineers (ASME) Code
design internal pressure. Therefore, the
consequence of any accident will be the same
as those previously analyzed.
Since the UHS safety function will
continue to meet accident mitigation
requirements and limit dose consequences to
acceptable levels, TVA has concluded that
the proposed TS change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The UHS function provides accident
mitigation capabilities and serves as a heat
PO 00000
Frm 00076
Fmt 4703
Sfmt 4703
29681
sink for normal and upset plant conditions;
the UHS is not an initiator of any accident.
By allowing the proposed change in the UHS
temperature requirements, only the
parameters for UHS operation are changed
while the safety functions of the UHS and
systems that transfer the heat sink capability
continue to be maintained. The proposed
change does not impact the response of the
systems and components assumed in the
safety analysis. Therefore, the proposed
change does not create the possibility of a
new or different kind of accident from any
accident evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change has been evaluated
for systems that are needed to support
accident mitigation functions as well as
normal operational evolutions. Operational
margins were found to exist in the systems
that utilize the UHS capabilities such that
these proposed changes will not result in the
loss of any safety function necessary for
normal or accident conditions. The ERCW
system has excess flow capacity that will
accommodate the increased flows necessary
for the proposed temperature increase. While
operating margins have been reduced by the
proposed changes, safety margins have been
maintained as assumed in the accident
analyses for postulated events. The proposed
change results in an increase in the
maximum calculated containment peak
pressure. However, the change in the
maximum calculated containment peak
pressure associated with the design basis
LOCA is a small percentage of the margin
between the current maximum calculated
containment peak pressure and the ASME
Code design internal pressure. This aspect of
the proposed change does not involve a
significant reduction in a margin of safety.
Additionally, the proposed changes do not
require any further modification of
component setpoints or operating provisions
that are necessary to maintain margins of
safety established by the WBN design (the
shutdown board room chillers were
physically modified to operate properly at
the 88 degree F UHS temperature). Therefore,
the proposed change does not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L.
Marshall, Jr.
E:\FR\FM\23MYN1.SGM
23MYN1
29682
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
rmajette on PROD1PC67 with NOTICES
Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of amendment request: April 14,
2005, as supplemented by letter dated
December 21, 2005.
Description of amendment request:
The amendment would revise the
Technical Specifications (TSs) by (1)
adding a new TS 3.1.9, ‘‘RCS [Reactor
Coolant System] Boron Limitations <500
°F,’’ and (2) revising TS 3.3.1, ‘‘Reactor
Trip System (RTS) Instrumentation.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Overall protection system performance will
remain within the bounds of the previously
performed accident analyses since there are
no design changes. The design of the reactor
trip system (RTS) instrumentation and
engineered safety feature actuation system
(ESFAS) instrumentation will be unaffected
and these protection systems will continue to
function in a manner consistent with the
plant design basis. All design, material, and
construction standards that were applicable
prior to this amendment request will be
maintained.
The proposed changes will not adversely
affect accident initiators or precursors nor
alter the design assumptions, conditions, and
configuration of the facility or the manner in
which the plant is operated and maintained
other than extending the OPERABILITY
requirements for RTS trip Function 2.b
(Power Range Neutron Flux—Low) to the
upper portion of MODE 3. The proposed
changes will not alter or prevent the ability
of structures, systems, and components
(SSCs) from performing their intended
functions to mitigate the consequences of an
initiating event within the assumed
acceptance limits.
As discussed previously [in the
application,] the proposed change[s] will add
more restrictive requirements in the form of
a new LCO [limiting condition for operation]
3.1.9 and an expanded LCO Applicability for
RTS trip Function 2.b, Power Range Neutron
Flux—Low, to provide mitigative capability
in the event of an uncontrolled RCCA [rod
cluster control assembly] bank withdrawal
event postulated to occur during low power
or subcritical (startup) conditions.
There will be no change[s] to normal plant
operating parameters or accident mitigation
performance. None of the proposed changes
will initiate any accidents; therefore, the
probability of an accident will not be
increased. There will be no degradation in
the performance of, nor an increase in the
number of challenges imposed on, safetyrelated equipment assumed to function
during an accident situation.
VerDate Aug<31>2005
16:41 May 22, 2006
Jkt 208001
All accident analysis acceptance criteria
will continue to be met with the proposed
changes. The proposed changes will not
affect the source term, containment isolation,
or radiological release assumptions used in
evaluating the radiological consequences of
an accident previously evaluated. The
proposed changes will not alter any
assumptions or change any mitigation actions
in the radiological consequence evaluations
in the FSAR [Final Safety Analysis Report for
Callaway]. The applicable radiological dose
acceptance criteria will continue to be met.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
There are no proposed design changes nor
are there any changes in the method by
which any safety-related plant SSC performs
its safety function. [These changes] will not
affect the normal method of plant operation
or change any operating parameters. No
equipment performance requirements will be
affected other than the more restrictive
Applicability requirements being imposed on
RTS trip Function 2.b, Power Range Neutron
Flux—Low, in the upper portion of MODE 3.
The proposed changes will not alter any
assumptions made in the safety analyses.
No new accident scenarios, transient
precursors, failure mechanisms, or limiting
single failures will be introduced as a result
of this amendment. There will be no adverse
effect or challenges imposed on any safetyrelated system as a result of this amendment.
The proposed amendment will not alter the
design or performance of the 7300 Process
Protection System, Nuclear Instrumentation
System, or Solid State Protection System
used in the plant protection systems.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
There will be no effect on the manner in
which safety limits or limiting safety system
settings are determined nor will there be any
effect on those plant systems necessary to
assure the accomplishment of protection
functions. There will be no impact on the
overpower limit, departure from nucleate
boiling ratio (DNBR) limits, heat flux hot
channel factor (FQ), nuclear enthalpy rise hot
channel factor (FDH), loss of coolant accident
peak cladding temperature (LOCA PCT), peak
local power density, or any other margin of
safety. The applicable radiological dose
consequence acceptance criteria will
continue to be met.
The proposed changes do not eliminate
any RTS or ESFAS surveillances or alter the
Frequency of surveillances required by the
Technical Specifications. More restrictive
changes are proposed by virtue of a new LCO
3.1.9 on [RCS] boron requirements when the
RCS temperature is below 500 °F and by
virtue of extending the Applicability of RTS
PO 00000
Frm 00077
Fmt 4703
Sfmt 4703
trip Function 2.b, Power Range Neutron
Flux—Low, to the upper portion of MODE 3.
The nominal RTS and ESFAS trip setpoints
will remain unchanged. None of the
acceptance criteria for any accident analysis
will be changed.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: John O’Neill,
Esq., Shaw, Pittman, Potts &
Trowbridge, 2300 N Street, NW.,
Washington, DC 20037
NRC Branch Chief: David Terao.
Previously Published Notices of
Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The following notices were previously
published as separate individual
notices. The notice content was the
same as above. They were published as
individual notices either because time
did not allow the Commission to wait
for this biweekly notice or because the
action involved exigent circumstances.
They are repeated here because the
biweekly notice lists all amendments
issued or proposed to be issued
involving no significant hazards
consideration.
For details, see the individual notice
in the Federal Register on the day and
page cited. This notice does not extend
the notice period of the original notice.
Virginia Electric and Power Company,
Docket Nos. 50–280 and 50–281, Surry
Power Station, Unit Nos. 1 and 2, Surry
County, Virginia
Date of amendment request: April 20,
2006.
Brief description of amendment
request: The proposed amendments
would reinstate the previous reactor
coolant system pressure and
temperature limits, low temperature
overpressure protection system (LTOPS)
setpoint, and (LTOPS) enable
temperature basis that were approved by
the NRC staff on December 28, 1995, as
License Amendments Nos. 207 and 207
for Surry 1 and 2.
Date of publication of individual
notice in Federal Register: April 28,
2006 (71 FR 25249)
Expiration date of individual notice:
30 day expiration date, May 30, 2006,
E:\FR\FM\23MYN1.SGM
23MYN1
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
and 60 day expiration date, June 27,
2006.
rmajette on PROD1PC67 with NOTICES
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) The applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
Carolina Power & Light Company,
Docket Nos. 50–325 and 50–324,
Brunswick Steam Electric Plant, Units 1
and 2, Brunswick County, North
Carolina
Date of application for amendments:
June 20, 2005.
Brief Description of amendments: The
amendments revise the Technical
Specification (TS) Surveillance
Requirement 3.6.1.6.2 of 3.6.1.6,
‘‘Suppression Chamber-to-Drywell
Vacuum Breakers’’ for the frequency of
functionally testing the suppression
chamber-to-drywell vacuum breakers.
Date of issuance: May 5, 2006.
Effective date: May 5, 2006.
Amendment Nos.: 240 and 268.
Facility Operating License Nos. DPR–
71 and DPR–62: Amendments change
the TS.
Date of initial notice in Federal
Register: August 16, 2005 (70 FR
48202).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated May 5, 2006.
No significant hazards consideration
comments received: No.
Carolina Power & Light Company, et al.,
Docket No. 50–400, Shearon Harris
Nuclear Power Plant, Unit 1, Wake and
Chatham Counties, North Carolina
Date of application for amendment:
August 18, 2005, as supplemented by
letter dated February 15, 2006.
Brief description of amendment: This
amendment authorizes the use of fireresistive electrical cables in lieu of the
alternatives specified in Section C5.b.2
of Branch Technical Position Chemical
Engineering Branch 9.5–1 (NUREG–
0800), ‘‘ Guidelines for Fire Protection
for Nuclear Power Plants,’’ dated July
1981, for Fire Areas 12–A–CR, 1–A–
CSRA, 1–A–CSRB, 1–A–SWGRA, 1–A–
SWGRB, and 1–A–BAL–B.
Date of issuance: May 1, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment No. 123.
Facility Operating License No. NPF–
63: Amendment revises the License.
Date of initial notice in Federal
Register: November 8, 2005.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated May 1, 2006.
No significant hazards consideration
comments received: No.
Dominion Nuclear Connecticut, Inc.,
Docket No. 50–336, Millstone Power
Station, Unit No. 2, New London
County, Connecticut
Date of application for amendment:
July 14, 2005, as supplemented January
11, 2006.
PO 00000
Frm 00078
Fmt 4703
Sfmt 4703
29683
Brief description of amendment: The
proposed change modifies the Millstone
Power Station, Unit No. 2 reactor
coolant system heatup and cooldown
limits Technical Specification (TS)
3.4.9.1, ‘‘Reactor Coolant System’’. The
associated TS bases will be updated to
address the proposed change.
Date of issuance: May 3, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 292.
Facility Operating License No. DPR–
65: The amendment revised the TSs.
Date of initial notice in Federal
Register: August 30, 2005 (70 FR
51379). The supplement dated January
11, 2006, provided clarifying
information that did not change the
scope of the proposed amendment as
described in the original notice, and did
not change the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated May 3, 2006.
No significant hazards consideration
comments received: No.
Duke Power Company, LLC Docket No.
50–287, Oconee Nuclear Station, Unit 3,
Oconee County, South Carolina
Date of application of amendment:
August 18, 2005, supplemented
September 15, 2005, and January 5 and
April 6, 2006.
Brief description of amendment: The
amendment revised Technical
Specifications 3.5.2.6 and 3.5.3.6 to
accommodate the replacement of the
reactor building emergency sump
suction inlet trash racks and screens
with strainers. Similar amendments
were issued for Units 1 and 2 on
November 1, 2005; however, the
amendment for Unit 3 was not issued at
that time since the licensee had not
completed its evaluation of the impact
of pipe whip, jet impingement and
internally generated missiles for Unit 3.
Date of Issuance: May 4, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment No.: 350.
Renewed Facility Operating License
No. DPR–55: Amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: August 31, 2005 (70 FR
51852).
The supplemental letters contained
clarifying information and did not
change the initial no significant hazards
consideration determination and did not
expand the scope of the initial Federal
E:\FR\FM\23MYN1.SGM
23MYN1
29684
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
rmajette on PROD1PC67 with NOTICES
Register notice. The Commission’s
related evaluation of the amendment is
contained in a Safety Evaluation dated
May 4, 2006.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC, and
PSEG Nuclear LLC, Docket Nos. 50–277
and 50–278, Peach Bottom Atomic
Power Station, Units 2 and 3, York and
Lancaster Counties, Pennsylvania
Date of application for amendments:
June 24, 2004.
Brief description of amendments:
These amendments implement 25
generic Technical Specification (TS)
changes previously approved by the
NRC staff as part of the Technical
Specifications Task Force (TSTF). The
TSTF change travelers and proposed
changes are:
1. TSTF–5, an administrative change
to TS 2.2 to remove reporting
requirements that are already in the
regulations 10 CFR, Sections 50.36 and
50.73;
2. TSTF–208, an extension of the time
allowed to reach MODE 2 once a TS
3.0.3 condition is identified, from the
current 7 hours to 10 hours;
3. TSTFs–222 and 229, changes to TS
3.1.4 to allow scram time testing on only
affected rods when an outage is short
and only a limited number of fuel
assemblies are moved and to require the
Minimum Critical Power Ratio to be
determined after scram time testing;
4. TSTFs–297 and 227, changes to TSs
3.3.2.2, 3.3.4.1, and 3.3.4.2 to allow
reactor feedwater pumps and main
turbine valves to be removed from
service if their trip function is
compromised;
5. TSTF–295, a clarification in Table
3.3.3.1–1 that penetration flow paths,
not just valve positions, are to be
considered;
6. TSTF–275, a clarification Table
3.3.5.1–1 that certain emergency core
cooling system (ECCS) instrumentation
needs to be operable when ECCS and
ECCS support systems are required to be
operable;
7. TSTF–306, changes to TS 3.3.6.1 to
allow penetration flow paths to be
opened intermittently under
administrative controls and to set apart
the Traversing In-core Probe system
isolation as a separate function;
8. TSTF–416, changes to TSs 3.5.1
and 3.5.2 to allow the low pressure
coolant injection subsystems to be
considered operable during alignment
and operation in the decay heat removal
mode;
9. TSTF–17, a change to TS 3.6.1.2 to
extend the containment air lock
interlock mechanism testing frequency
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
from 6 months to 2 years to coincide
with refueling outage frequency;
10. TSTFs–30, 323, 45, 46, and 269,
changes to TSs 3.6.1.3 and 3.6.4.2
related to primary and secondary
containment isolation valve completion
times, isolation times, and status
verification;
11. TSTF–322, a clarification in TS
3.6.4.1 of the intent of secondary
containment drawdown tests;
12. TSTF–276, Revision 2, a change to
TS 3.8.1 to allow certain emergency
diesel generator (EDG) testing to
continue even if the stated power factor
cannot be attained;
13. TSTF–404, a change to TS 3.1.8 to
revise required actions when one valve
is inoperable in one or more scram
discharge volume vent and drain lines,
as part of the consolidated line item
improvement process;
14. TSTF–65 Revision 1, a change to
allow the use of generic organizational
titles in the TSs, as opposed to plantspecific titles;
15. TSTF–299, a clarification in TS
5.2.2 of the intent of refueling cycle
intervals with respect to system leak test
requirements;
16. TSTF–279, a deletion in TS 5.5.6
of the reference to ‘‘applicable
supports’’ as part of the description of
the Inservice Testing Program;
17. TSTF–118, a change to TS 5.5.9 to
apply the provisions of Surveillance
Requirement (SR) 3.0.2 (25% extension
interval) and SR 3.0.3 (missed
surveillance actions) to EDG fuel oil
testing surveillances;
18. TSTF–106, Revision 1, a
clarification in TS 5.5.9 that the
American Society for Testing and
Materials standard for EDG fuel oil
applies only to new fuel being received;
and
19. TSTF–152, a change to the
Radioactive Effluent Release Report to
ensure that a common report for both
units combines sections common to
both units.
Date of issuance: May 10, 2006.
Effective date: As of the date of
issuance, to be implemented within 90
days.
Amendments Nos.: 259 and 262.
Renewed Facility Operating License
Nos. DPR–44 and DPR–56: The
amendments revised the TSs.
Date of initial notice in Federal
Register: September 28, 2004 (69 FR
57985) and October 26, 2004 (69 FR
62476).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated May 10, 2006.
No significant hazards consideration
comments received: No.
PO 00000
Frm 00079
Fmt 4703
Sfmt 4703
FPL Energy Seabrook, LLC, Docket No.
50–443, Seabrook Station, Unit No. 1,
Rockingham County, New Hampshire
Date of amendment request:
December 19, 2006.
Description of amendment request:
The amendment deletes Technical
Specification (TS) 6.8.1.2a,
‘‘Occupational Radiation Exposure
Report [ORER],’’ TS 6.8.1.2.c, regarding
challenges to pressurizer relief and
safety valves and TS 6.8.1.5, ‘‘Monthly
Operating Report [MOR],’’ as described
in the Notice of Availability published
in the Federal Register on June 23, 2004
(69 FR 35067).
Date of issuance: May 5, 2006.
Effective date: As of its date of
issuance, and shall be implemented
within 90 days.
Amendment No.: 109.
Facility Operating License No. NPF–
86: The amendment revised the TSs.
Date of initial notice in Federal
Register: February 14, 2006 (71 FR
7808).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated May 5, 2006.
No significant hazards consideration
comments received: No.
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request: October
12, 2005.
Brief description of amendment: The
amendment revised Technical
Specification (TS) Section 3.4.9, ‘‘RCS
[reactor coolant system] Pressure and
Temperature (P/T) Limits,’’ curves
3.4.9–1, ‘‘Pressure/Temperature Limits
for Non-Nuclear Heatup or Cooldown
Following Nuclear Shutdown,’’ 3.4.9–2,
‘‘Pressure/Temperature Limits for
Inservice Hydrostatic and Inservice
Leakage Tests, and 3.4.9–3, ‘‘Pressure/
Temperature Limits for Criticality,’’ to
remove the cycle operating restriction
and replace it with a limitation of 30
effective full-power years (EFPY).
Date of issuance: April 27, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment No.: 219.
Facility Operating License No. DPR–
46: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: January 3, 2006 (71 FR 150).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 27, 2006.
No significant hazards consideration
comments received: No.
E:\FR\FM\23MYN1.SGM
23MYN1
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request:
December 30, 2005.
Brief description of amendment: The
amendment established a combined
leakage rate limit for the sum of the four
main steam line leakage rates that is
equal to four times the current
individual main steam isolation valve
leakage rate limit.
Date of issuance: May 2, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 30 days of issuance.
Amendment No.: 220.
Facility Operating License No. DPR–
46: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: February 28, 2006 (71 FR
10073)
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated May 2, 2006.
No significant hazards consideration
comments received: No.
rmajette on PROD1PC67 with NOTICES
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request: January
30, 2006.
Brief description of amendment: The
amendment allows a delay time for
entering a supported system Technical
Specification (TS) when the
inoperability is due solely to an
inoperable snubber, if risk is assessed
and managed consistent with the
program in place for complying with the
requirements of 10 CFR 50.65(a)(4).
Limiting Condition for Operation (LCO)
3.0.8 is added to the TS to provide this
allowance and define the requirements
and limitations for its use.
This change was proposed by the
industry’s Technical Specification Task
Force (TSTF) and is designated TSTF–
372, Revision 4. The NRC staff issued a
notice of opportunity for comment in
the Federal Register on November 24,
2004 (69 FR 68412), on possible
amendments concerning TSTF–372,
including a model safety evaluation and
model no significant hazards
consideration (NSHC) determination,
using the consolidated line item
improvement process. The NRC staff
subsequently issued a notice of
availability of the models for referencing
in license amendment applications in
the Federal Register on May 4, 2005 (70
FR 23252). The licensee affirmed the
applicability of the following NSHC
determination in its application dated
January 30, 2006.
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
Date of issuance: May 2, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment No.: 221.
Facility Operating License No. DPR–
46: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: February 28, 2006 (71 FR
10074).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated May 2, 2006.
No significant hazards consideration
comments received: No.
Nuclear Management Company, LLC,
Docket No. 50–263, Monticello Nuclear
Generating Plant (MNGP), Wright
County, Minnesota
Date of application for amendment:
April 29, 2004, as supplemented on
November 23, 2004; January 20,
February 28, April 12, 2005; and March
10, 2006.
Brief description of amendment: The
amendment revised the MNGP licensing
basis by selectively implementing the
alternative source term for the
postulated fuel handling accident,
leading to revision of portions of the
Technical Specifications to reflect this
change in licensing basis.
Date of issuance: April 24, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 145.
Facility Operating License No. DPR–
22. Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: January 18, 2005 (70 FR 2891)
The supplemental letters contained
clarifying information and did not
change the initial no significant hazards
consideration determination and did not
expand the scope of the original Federal
Register notice.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 24, 2006.
No significant hazards consideration
comments received: No.
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1, Washington County, Nebraska
Date of amendment request: August
11, 2005.
Brief description of amendment: The
change allows a delay time for entering
a supported system Technical
Specification (TS) when the
inoperability is due solely to an
inoperable snubber, if risk is assessed
and managed consistent with the
program in place for complying with the
PO 00000
Frm 00080
Fmt 4703
Sfmt 4703
29685
requirements of 10 CFR 50.65(a)(4).
Limiting Condition for Operation (LCO)
3.0.8 is added to the TS to provide this
allowance and define the requirements
and limitations for its use.
Date of issuance: March 1, 2006.
Effective date: As of its date of
issuance and shall be implemented
within 120 days of issuance.
Amendment No.: 238.
Renewed Facility Operating License
No. DPR–40: The amendment revised
the Technical Specifications.
Date of initial notice in Federal
Register: December 6, 2005 (70 FR
72674)
The Commission’s related evaluation
of the amendment is contained in a
safety evaluation dated March 1, 2006.
No significant hazards consideration
comments received: No.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of application for amendments:
October 19, 2005.
Brief description of amendments: The
change allows a delay time for entering
a supported system Technical
Specification (TS) when the
inoperability is due solely to an
inoperable snubber, if risk is assessed
and managed consistent with the
program in place for complying with the
requirements of 10 CFR 50.65(a)(4).
Limiting Condition for Operation (LCO)
3.0.8 is added to the TS to provide this
allowance and define the requirements
and limitations for its use.
Date of issuance: March 7, 2006.
Effective date: As of its date of
issuance and shall be implemented
within 90 days of issuance.
Amendment Nos.: Unit 1—185; Unit
2—187
Facility Operating License Nos. DPR–
80 and DPR–82: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: December 20, 2005 (70 FR
75495).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 7, 2006.
No significant hazards consideration
comments received: No.
Tennessee Valley Authority, Docket No.
50–390, Watts Bar Nuclear Plant, Unit 1,
Rhea County, Tennessee
Date of application for amendment:
December 9, 2004, as supplemented by
letters dated November 18 and
December 5, 2005.
Brief description of amendment: The
amendment authorizes modification to
E:\FR\FM\23MYN1.SGM
23MYN1
29686
Federal Register / Vol. 71, No. 99 / Tuesday, May 23, 2006 / Notices
rmajette on PROD1PC67 with NOTICES
the Updated Final Safety Analysis
Report (UFSAR) to include a revision to
the methodology for splicing reinforcing
steel bars during restoration of the Unit
1 concrete shield building dome as part
of the steam generator replacement
project.
Date of issuance: April 27, 2006.
Effective date: As of the date of
issuance and shall be implemented as
part of the next UFSAR update made in
accordance with 10 CFR 50.71(e).
Amendment No. 60.
Facility Operating License No. NPF–
90: Amendment authorizes revision of
the Updated Final Safety Analysis
Report.
Date of initial notice in the Federal
Register: January 4, 2005 (70 FR 405).
The supplemental letters provided
clarifying information that was within
the scope of the initial notice and did
not change the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 27, 2006.
No significant hazards consideration
comments received: No.
Wolf Creek Nuclear Operating
Corporation, Docket No. 50–482, Wolf
Creek Generating Station, Coffey
County, Kansas
Date of amendment request: October
30, 2003, as supplemented by letters
dated August 31 and November 18,
2005, and March 6, 2006.
Brief description of amendment: The
amendment increases the completion
times (CTs) for Technical Specification
(TS) 3.8.1, ‘‘AC Sources—Operating,’’
and adds requirements on the diesel
generators at the Sharpe Station when a
diesel generator at Wolf Creek
Generating Station is in an extended CT
greater than 72 hours. The proposed
changes to TS 3.8.9, ‘‘Distribution
Systems—Operating,’’ are withdrawn.
The amendment also revises a page in
the license and adds conditions to
Appendix D, ‘‘Additional Conditions,’’
of the license.
Date of issuance: April 26, 2006.
Effective date: As of its date of
issuance and shall be implemented
within 90 days of the date of issuance.
Amendment No.: 163.
Facility Operating License No. NPF–
42. The amendment revised the license
including Appendix D, ‘‘Additional
Conditions,’’ and Appendix A,
‘‘Technical Specifications.’’
Date of initial notice in Federal
Register: January 6, 2004 (69 FR 700).
The supplemental letters dated
August 31 and November 18, 2005, and
March 2, 2006, provided additional
VerDate Aug<31>2005
15:14 May 22, 2006
Jkt 208001
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the NRC staff’s
original proposed no significant hazards
consideration determination published
in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 26, 2006.
No significant hazards consideration
comments received: No
Wolf Creek Nuclear Operating
Corporation, Docket No. 50–482, Wolf
Creek Generating Station, Coffey
County, Kansas
Date of amendment request:
November 3, 2005, and supplemental
letters dated February 21 and March 28,
2006.
Brief description of amendment: The
amendment revised the Technical
Specifications associated with steam
generator tube integrity consistent with
Revision 4 to Technical Specification
Task Force (TSTF) Standard Technical
Specification Change Traveler, TSTF–
449, ‘‘Steam Generator Tube Integrity.’’
A notice of availability for this TS
improvement using the consolidated
line item improvement process was
published in the Federal Register on
May 6, 2005 (70 FR 24126).
Date of issuance: May 8, 2006.
Effective date: The license
amendment is effective as of its date of
issuance and shall be implemented
prior to the entry into Mode 5 in the
restart from Refueling Outage 15, which
is scheduled to begin in October 2006.
Amendment No.: 164.
Facility Operating License No. NPF–
42. The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: December 6, 2005 (70 FR
72676) The supplemental letters dated
February 21 and March 28, 2006,
provided additional clarifying
information, did not expand the scope
of the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination published
in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated May 8, 2006.
No significant hazards consideration
comments received: No.
Dated at Rockville, Maryland, this 15th day
of May 2006.
PO 00000
Frm 00081
Fmt 4703
Sfmt 4703
For the Nuclear Regulatory Commission
Catherine Haney,
Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. 06–4736 Filed 5–22–06; 8:45 am]
BILLING CODE 7590–01–P
OFFICE OF THE UNITED STATES
TRADE REPRESENTATIVE
Trade Policy Staff Committee; Initiation
of Environmental Review of Proposed
Free Trade Agreement Between the
United States and Malaysia; Public
Comments on Scope of Environmental
Review
Office of the United States
Trade Representative.
ACTION: Notice and request for
comments.
AGENCY:
SUMMARY: This publication gives notice
that, pursuant to the Trade Act of 2002,
and consistent with Executive Order
13141 (64 FR 63169) (Nov. 18, 1999)
and its implementing guidelines (65 FR
79442), the Office of the United States
Trade Representative (USTR), through
the Trade Policy Staff Committee
(TPSC), is initiating an environmental
review of the proposed free trade
agreement (FTA) between the United
States and Malaysia. The TPSC is
requesting written comments from the
public on what should be included in
the scope of the environmental review,
including the potential environmental
effects that might flow from the free
trade agreement and the potential
implications for U.S. environmental
laws and regulations, and identification
of complementarities between trade and
environmental objectives such as the
promotion of sustainable development.
The TPSC also welcomes public views
on appropriate methodologies and
sources of data for conducting the
review. Persons submitting written
comments should provide as much
detail as possible on the degree to which
the subject matter they propose for
inclusion in the review may raise
significant environmental issues in the
context of the negotiation.
DATES: Public comments should be
received no later than July 7, 2006.
ADDRESSES:
Submissions by electronic mail:
FR06017@ustr.eop.gov.
Submissions by facsimile: Gloria Blue,
Executive Secretary, Trade Policy Staff
Committee, at (202) 395–6143.
FOR FURTHER INFORMATION CONTACT: For
procedural questions concerning public
comments, contact Gloria Blue,
E:\FR\FM\23MYN1.SGM
23MYN1
Agencies
[Federal Register Volume 71, Number 99 (Tuesday, May 23, 2006)]
[Notices]
[Pages 29671-29686]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: 06-4736]
=======================================================================
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from April 28, 2006 to May 11, 2006. The last
biweekly notice was published on May 9, 2006 (71 FR 26995).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this
[[Page 29672]]
proceeding and who wishes to participate as a party in the proceeding
must file a written request for a hearing and a petition for leave to
intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The
filing of requests for a hearing and petitions for leave to intervene
is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland, 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-
[[Page 29673]]
mail to OGCMailCenter@nrc.gov. A copy of the request for hearing and
petition for leave to intervene should also be sent to the attorney for
the licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
Dominion Energy Kewaunee, Inc. Docket No. 50-305, Kewaunee Power
Station, Kewaunee County, Wisconsin
Date of amendment request: April 6, 2006.
Description of amendment request: The proposed amendment would
allow the use of a different methodology for determining the design
requirements necessary for protecting safety-related equipment from
damage by tornado generated missiles.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The probability of occurrence of an accident previously
evaluated is not significantly increased by the proposed change to
permit probabilistic evaluation of missiles generated by natural
phenomena. The actual frequency of tornado occurrence at Kewaunee is
unaffected by the proposed change in assessment methodology.
Furthermore, the projected frequency of tornado occurrence, as
specified in the USAR [Updated Safety Analysis Report], is not
significantly affected by this change. The value for the probability
of tornado occurrence in the updated study is in general agreement
with the original value in the USAR (i.e. 3.97E-4 vs. 4.86E-4).
Similarly, the probability of a tornado-generated missile is not
significantly affected by this change.
Likewise, the consequences of an accident previously evaluated
are not significantly increased by the proposed change. The actual
probability of a tornado missile onsite remains unchanged. The
actual probability of a tornado missile strike remains unchanged.
For the limited number of components affected by this proposed
change (i.e. exhaust ducts and fuel vent), the missile strike
probability is approximately 5.75 x 10-7 per year, which
is significantly lower than the SRP [Standard Review Plan]
acceptance criteria of 1 x 10-6 per year. Therefore, the
proposed change is not considered to constitute a significant
increase in the consequences of an accident due to the low
probability of occurrence.
In addition, use of a probabilistic versus a deterministic
methodology to assess missile hazard acceptability has no impact on
accident initiation or consequence. Therefore, the proposed change
does not involve a significant increase in the probability or
consequences of an accident previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed changes involve use of an evaluation methodology to
determine protection requirements for two specific support
components for safety-related equipment, which may be adversely
affected by missiles during a tornado. A tornado at Kewaunee is
considered in the USAR as a separate event and not occurring
coincident with any of the design basis accidents in the USAR. As
such, no new or different kind of accident is created by the
proposed change to permit probabilistic evaluation of missiles
generated by natural phenomena.
This change involves recognition of the acceptability of
performing tornado missile strike probability calculations in
accordance with established regulatory guidance in lieu of using
deterministic methodology alone. Therefore, the change would not
create the possibility of, or be the initiator for, any new or
different kind of accident. The acceptance criterion of the SRP
guidance establishes a threshold for tornado missile damage to
system components that is consistent with this conclusion.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The request does not involve a significant reduction in a margin
of safety. The existing design basis for Kewaunee, with respect to a
tornado affecting safety related equipment, is to provide positive
missile barriers for all safety-related systems and components. The
proposed change recognizes that for probability of occurrences below
the SRP established acceptance limit, the extremely low probability
associated with an ``important'' system or component being struck by
a tornado missile does not represent a significant reduction in the
margin of safety provided by use of the deterministic methodology.
The change from ``protecting all safety-related systems and
components'' to ``an extremely low probability of occurrence of
tornado generated missile strikes on portions of important systems
and components'' is not considered to constitute a significant
reduction in the margin of safety.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner,
P.O. Box 1497, Madison, WI 53701-1497.
NRC Branch Chief: L. Raghavan.
Dominion Nuclear Connecticut, Inc., Docket No. 50-423 Millstone Power
Station, Unit No. 3 New London County, Connecticut
Date of amendment request: March 28, 2006.
Description of amendment request: The proposed amendment would
eliminate redundant surveillance requirements [SRs] pertaining to post-
maintenance/post-modification testing. The associated TS bases will be
updated to address the proposed changes.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes do not modify any plant equipment and do
not impact any failure modes that could lead to an accident. Testing
in accordance with the requirements of SR 4.0.1 will continue to
provide the necessary assurance that the associated systems will
function consistent with the assumptions used in the accident
analyses. On this basis, the proposed amendment does not increase
the probability or consequences of an accident previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed changes do not involve any physical changes to
systems, structures, or components, or involve a change to the
[[Page 29674]]
method of plant operation. The requirement to perform post
maintenance/post modification testing will continue to be
implemented consistent with SR 4.0.1, through existing plant
programs and procedures. As such, the proposed amendment does not
introduce any new failure modes, accident initiators or malfunctions
that would cause a new or different kind of accident. Therefore, the
proposed amendment does not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The TS changes do not involve a significant reduction in a
margin of safety because the requirements described in SR 4.0.1, as
implemented through existing plant programs and procedures, will
continue to ensure that post maintenance/post modification testing
will be performed when necessary. The proposed change does not
affect any of the assumptions used in the accident analyses, nor
does it affect operability requirements for equipment important to
plant safety. Therefore, the margin of safety is not impacted by the
proposed amendment.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Lillian M. Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc., Rope Ferry Road, Waterford, CT
06385.
NRC Branch Chief: Darrell J. Roberts.
Energy Northwest, Docket No. 50-397, Columbia Generating Station,
Benton County, Washington
Date of amendment request: April 17, 2006.
Description of amendment request: The proposed amendment would
change the method for calculating fuel pool decay heat load from the
original licensing basis methodology of ORIGEN and the Auxiliary
Systems Branch Technical Position (ASBTP) 9-2, ``Residual Decay Heat
Energy for Light Water Reactors for Long-Term Cooling,'' to ORIGEN-ARP.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The adoption of ORIGEN-ARP does not affect the probability or
consequences of an accident previously evaluated. The calculation of
the fuel pool decay heat load is used to evaluate and demonstrate
the ability of the fuel pool cooling system to maintain the fuel
pool temperatures within the acceptance limits specified in the
Columbia Final Safety Analysis Report [FSAR]. The proposed change to
the methodology used to calculate the fuel pool [decay] heat load
has no bearing on the probability or consequences of any previously
evaluated accident. Therefore, this change does not involve a
significant increase in the probability or consequences of an
accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The change involves the use of a different methodology for
calculating fuel pool decay heat load. This change does not involve
any new equipment, it does not change any previously approved
acceptance limits, and it does not affect or alter the operation of
any equipment. Therefore[,] this change does not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The margin of safety provided by the fuel pool cooling system is
primarily defined by the difference between the maximum allowed fuel
pool temperature and the boiling point of water. The margin of
safety is supplemented by the ability to make up water to the spent
fuel pool if boiling were to occur. The proposed change in
methodology for calculating the fuel pool [decay] heat load does not
alter the current temperature limits or acceptance criteria
specified in the FSAR and has no effect on the ability to provide
make-up water if boiling were to occur. This change will allow
Energy Northwest to more accurately calculate the fuel pool [decay]
heat load to provide added confidence in the ability of the fuel
pool cooling system to accommodate the heat load added to the spent
fuel pool during refueling activities. Therefore, this change does
not involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: William A. Horin, Esq., Winston & Strawn,
1700 K Street, NW., Washington, DC 20006-3817.
NRC Branch Chief: David Terao.
Energy Northwest, Docket No. 50-397, Columbia Generating Station,
Benton County, Washington
Date of amendment request: April 18, 2006.
Description of amendment request: The proposed change would modify
technical specification surveillance requirement 3.6.1.1.2 by changing
the test frequency of the drywell-to-suppression chamber bypass leakage
test from 24 to 120 months. This proposed amendment also includes
testing the suppression chamber-to-drywell vacuum breakers on a 24-
month frequency.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the operation of Columbia Generating Station in
accordance with the proposed amendment involve a significant
increase in the probability or consequences of an accident
previously evaluated?
Response: No.
The proposed changes would modify Technical Specification (TS)
Surveillance Requirement (SR) 3.6.1.1.2 and add two new SRs, SR
3.6.1.1.3 and SR 3.6.1.1.4. The proposed changes will extend the
frequency for the drywell-to-suppression chamber bypass leakage test
while maintaining the current leakage testing frequency for the
suppression chamber-to-drywell vacuum breakers, and establish
leakage acceptance criteria for the suppression chamber-to-drywell
vacuum breakers when the valves are tested individually.
The performance of a drywell-to-suppression chamber bypass
leakage test or suppression chamber-to-drywell vacuum breaker
leakage test is not a precursor to any accident previously
evaluated. Thus, the proposed changes to the performance of the
leakage tests do not have any affect on the probability of an
accident previously evaluated.
The performance of a drywell-to-suppression chamber bypass
leakage test or a suppression chamber-to-drywell vacuum breaker
leakage test continues to provide assurance that the containment
will perform as designed. Thus, the radiological consequences of any
accident previously evaluated are not impacted.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the operation of Columbia Generating Station in
accordance with the proposed amendment create the possibility of a
new or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed changes to TS SR 3.6.1.1.2, and the addition of SR
3.6.1.1.3, and SR 3.6.1.1.4 do not affect the assumed performance of
any Columbia Generating
[[Page 29675]]
Station structure, system or component previously evaluated. The
proposed changes do not introduce any new modes of system operation
or any new failure mechanisms. This is an administrative change and
does not involve the modification, addition or removal of any plant
equipment.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Does the operation of Columbia Generating Station in
accordance with the proposed amendment involve a significant
reduction in the margin of safety?
Response: No.
The current frequency associated with a drywell-to-suppression
chamber bypass leakage test in TS SR 3.6.1.1.2 is 24 months or 12
months if two consecutive tests fail and continues at this frequency
until two consecutive tests pass. The proposed change will modify
this leakage test frequency to 120 months, or 48 months following
one test failure or 24 months if two consecutive tests fail and
continues at this frequency until two consecutive tests pass. The
proposed change in SR 3.6.1.1.2 frequency is acceptable as the
results from previous tests show that the measured drywell-to-
suppression chamber bypass leakage at the current TS frequency has
been a small percentage of the allowable leakage. Acceptability is
further demonstrated by the design requirements applied to the
primary containment components and other periodically performed
primary containment inspections.
The proposed SR 3.6.1.1.3 will establish a leakage test
frequency of 24 months for each suppression chamber-to-drywell
vacuum breaker except when the leakage test of SR 3.6.1.1.2 has been
performed within the past 24 months. SR 3.6.1.1.3 specifies a
leakage limit for each suppression chamber-to-drywell vacuum breaker
pathway of less than or equal to 12 percent of the bypass leakage
limit of SR 3.6.1.1.2. The proposed SR 3.6.1.1.4 will establish a
total leakage limit of less than or equal to 30 percent of the
bypass leakage limit of SR 3.6.1.1.2 when the suppression chamber-
to-drywell vacuum breakers are tested in accordance with SR
3.6.1.1.3.
TS SR 3.6.1.1.2 drywell-to-suppression chamber bypass leakage
test monitors the combined leakage of three types of pathways: (1)
The drywell floor and downcomers, (2) piping externally connected to
both the drywell and suppression chamber air space, and (3) the
suppression chamber-to-drywell vacuum breakers. This amendment would
extend the surveillance interval on the passive components of the
test (the first two types of pathways), while retaining the current
surveillance interval on the active components (suppression chamber-
to-drywell vacuum breakers). The proposed changes establish leakage
limits for both individual suppression chamber-to-drywell vacuum
breakers and the total leakage. Additional testing is required if
acceptable results are not achieved.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: William A. Horin, Esq., Winston & Strawn,
1700 K Street, NW., Washington, DC 20006-3817.
NRC Branch Chief: David Terao.
Entergy Nuclear Operations, Inc., Docket No. 50-293, Pilgrim Nuclear
Power Station, Plymouth County, Massachusetts
Date of amendment request: April 12, 2006.
Description of amendment request: The proposed amendment would
revise the Technical Specification reactor pressure vessel Pressure and
Temperature (P-T) curves.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed License Amendment (LA) does not involve a
significant increase in the probability or consequences of an
accident previously evaluated. There are no physical changes to the
plant being introduced by the proposed changes to the pressure-
temperature curves. The proposed change does not modify the reactor
coolant pressure boundary, (i.e., there are no changes in operating
pressure, materials, or seismic loading). The proposed change does
not adversely affect the integrity of the reactor coolant pressure
boundary such that its function in the control of radiological
consequences is affected.
The proposed pressure-temperature curves are generated in
accordance with the fracture toughness requirements of 10 CFR 50
Appendix G, and American Society of Mechanical Engineers (ASME)
Boiler and Pressure Vessel (B&PV) Code, Section Xl, Appendix G and
Regulatory Guide (R.G.) 1.99, Revision 2[,] ``Radiation
Embrittlement of Reactor Vessel Materials.'' A best-estimate
calculation of reactor vessel 34 effective full power years (EFPYs)
neutron fluence and associated uncertainty has been completed for
Pilgrim using the Radiation Analysis Modeling Application (RAMA)
methodology. This methodology was previously approved by the NRC.
The resulting reactor vessel neutron fluence value was then used in
conjunction with R.G. 1.99, [Revision] 2 to determine the adjusted
reference temperature (ART) and with ASME Section Xl Appendix G to
develop revised P-T curves.
This provides sufficient assurance that the Pilgrim reactor
vessel will be operated in a manner that will protect it from
brittle fracture under all operating conditions. This proposed
license amendment provides compliance with the intent of 10 CFR
[Part 50] Appendix G and provides margins of safety that assure
reactor vessel integrity.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. [Does] the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed license amendment does not create the possibility
of new or different kind of accident from any accident previously
evaluated. The revised pressure-temperature curves are generated in
accordance with the fracture toughness requirements of 10 CFR Part
50 Appendix G and ASME Section Xl Appendix G. Compliance with the
proposed pressure-temperature curves will ensure the avoidance of
conditions in which brittle fracture of primary coolant pressure
boundary materials is possible because such compliance with the
pressure-temperature curves provides sufficient protection against a
non-ductile-type fracture of the reactor pressure vessel. No new
modes of operation are introduced by the proposed change. The
proposed change will not create any failure mode not bounded by
previously evaluated accidents. Further, the proposed change does
not affect any activities or equipment and is not assumed in any
safety analysis to initiate any accident sequence. This provides
sufficient assurance that Pilgrim reactor vessel will be operated in
a manner that will protect it from brittle fracture under all
operating conditions.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. [Does] the proposed change involve a significant reduction in
a margin of safety?
Response: No.
The proposed license amendment requests the use of revised P-T
curves that are based on established NRC and ASME methodologies. A
best-estimate calculation of reactor vessel neutron fluence and
associated uncertainty has been completed for Pilgrim through 34
EFPY using the NRC approved RAMA methodology. The 34 EFPY reactor
vessel neutron fluence value was used in conjunction with R.G. 1.99,
[Revision 2] to compute reference temperature shift, and with ASME
Section Xl Appendix G to develop revised P-T curves. This provides
sufficient margin such that the Pilgrim reactor vessel will be
operated in a manner that will protect it from brittle fracture
under all operating conditions. Operation within the proposed limits
ensures that the reactor vessel materials will continue to behave in
a non-brittle manner, thereby preserving the original safety design
bases. No plant safetylimits, set points, or design parameters are
adversely affected by the proposed changes.
[[Page 29676]]
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Travis C. McCullough, Assistant General
Counsel, Entergy Nuclear Operations, Inc., 400 Hamilton Avenue, White
Plains, NY 10601.
Branch Chief: Richard Laufer.
Entergy Nuclear Operations, Inc., Docket No. 50-293, Pilgrim Nuclear
Power Station, Plymouth County, Massachusetts
Date of amendment request: June 2, 2005.
Description of amendment request: The proposed amendment would
revise the Technical Specification (TS) reactor coolant system leakage
detection instrumentation requirements and actions.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No. The proposed relocation is administrative in
nature and does not involve the modification of any plant equipment
or affect basic plant operation. The associated instrumentation and
surveillances are not assumed to be an initiator of any analyzed
event, nor are these functions assumed in the mitigation of
consequences of accidents. Additionally, the associated required
actions for inoperable components do not impact the initiation or
mitigation of any accident. Therefore, the proposed change does not
involve a significant increase in the probability or consequences of
an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No. The proposed change does not involve any physical
alteration of plant equipment and does not change the method by
which any safety-related system performs its function. As such, no
new or different types of equipment will be installed, and the basic
operation of installed equipment is unchanged. The methods governing
plant operation and testing remain consistent with current safety
analysis assumptions. Therefore, the proposed change does not create
the possibility of a new or different kind of accident from any
accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No. The proposed change to relocate current TS
requirements to the FSAR [Final Safety Analysis Report], consistent
with regulatory guidance and previously approved changes for other
stations, are administrative in nature. These changes do not negate
any existing requirement, and do not adversely affect existing plant
safety margins or the reliability of the equipment assumed to
operate in the safety analysis. As such, there are no changes being
made to safety analysis assumptions, safety limits or safety system
settings that would adversely affect plant safety as a result of the
proposed change. Margins of safety are unaffected by requirements
that are retained, but relocated from the Technical Specifications
to the FSAR. Additionally, the changes being made to allow
additional repair time for inoperable instrumentation will not
affect the required leakage limits, which will continue to be
monitored at the same required frequency. These compensatory
measures, operational limitations, and administrative functions that
will be modified are not credited in any design-basis event and do
not reflect a margin of safety. Therefore, the proposed change does
not involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Travis C. McCullough, Assistant General
Counsel, Entergy Nuclear Operations, Inc., 400 Hamilton Avenue, White
Plains, NY 10601.
Branch Chief: Richard Laufer.
Exelon Generation Company, LLC, Docket Nos. STN 50-454 and STN 50-455,
Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois
Docket Nos. STN 50-456 and STN 50-457, Braidwood Station, Unit Nos.
1 and 2, Will County, Illinois.
Date of amendment request: November 18, 2005.
Description of amendment request: The proposed amendment would
revise the Technical Specifications (TS) to adopt NRC-approved Revision
4 to Technical Specification Task Force (TSTF) Standard Technical
Specification Change Traveler, TSTF-449, ``Steam Generator Tube
Integrity.'' The proposed amendment would also include changes to the
TS definition of Leakage, TS 3.4.13, ``RCS [Reactor Coolant System]
Operational LEAKAGE,'' TS 5.5.9, ``Steam Generator (SG) Program,'' TS
5.6.9, Steam Generator Tube Inspection Report,'' and would add TS
3.4.19, ``Steam Generator (SG) Tube Integrity.'' The proposed changes
are necessary in order to implement the guidance for the industry
initiative on Nuclear Energy Institute (NEI) 97-06, ``Steam Generator
Program Guidelines.''
The NRC staff issued a notice of opportunity for comment in the
Federal Register on March 2, 2005 (70 FR 10298), on possible amendments
adopting TSTF-449, including a model safety evaluation and model no
significant hazards consideration (NSHC) determination, using the
consolidated line item improvement process. The NRC staff subsequently
issued a notice of availability of the models for referencing in
license amendment applications in the Federal Register on May 6, 2005
(70 FR 24126). The licensee affirmed the applicability of the published
NSHC determination in its application dated November 18, 2005.
The licensee included a variation from TSTF-449 for Braidwood, Unit
2 and Byron, Unit 2 in that the proposed amendment would also include
an effective change to the definition of primary pressure boundary from
the hot-leg tube end weld to 17 inches below the top of the hot-leg
tube sheet. The proposed amendment would also delete the current TS
allowance to use Westinghouse laser welded sleeves as a SG tube repair
method. The licensee provided an analyses of the NSHC issue in its
application for the plant-specific variations from TSTF-449.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
Exelon Generation Company, LLC, (EGC) has reviewed the proposed
no significant hazards consideration determination published on
March 2, 2005 (i.e., 70 FR 10298) as part of the consolidated line
item improvement process (CLIIP) item. EGC has concluded that the
proposed determination presented in the notice is applicable to
Braidwood Station, Units 1 and 2, and Byron Station, Units 1 and 2,
and the determination is hereby incorporated by reference to satisfy
the requirements of 10 CFR 50.91 (a), except as discussed below.
The proposed amendment also revises the Technical Specification
Task Force (TSTF) Standard Technical Specification Change Traveler,
TSTF-449, ``Steam Generator Tube Integrity,'' Revision 4, version of
TS 5.5.9, Steam Generator Program, to exclude the portion of the
tube below 17 inches from the top of the hot leg tubesheet in the
Braidwood Station, Unit 2, and Byron Station, Unit 2, steam
generators from TS 5.5.9.d, ``Provisions for SG tube inspections.''
This proposed
[[Page 29677]]
license amendment request, in effect, redefines the Braidwood
Station, Unit 2, and Byron Station, Unit 2, primary pressure
boundary from the hot leg tube end weld to 17 inches below the top
of the hot leg tube sheet. This proposed license amendment also
deletes the current TS 5.5.9.e.6 and TS 5.5.9.e.10 allowance to use
Westinghouse laser welded sleeves as a SG tube repair method.
EGC has evaluated whether or not a significant hazards
consideration is involved with the proposed TS change by focusing on
the three criteria set forth in 10 CFR 50.92 as discussed below:
Criterion 1.--Does the proposed change involve a significant increase
in the probability or consequences of an accident previously evaluated?
Response: No.
The previously analyzed accidents are initiated by the failure
of plant structures, systems, or components. The proposed changes
that alter the SG inspection criteria and delete the allowance to
repair SG tubes using Westinghouse laser welded sleeves do not have
a detrimental impact on the integrity of any plant structure,
system, or component that initiates an analyzed event. The proposed
changes will not alter the operation of, or otherwise increase the
failure probability of any plant equipment that initiates an
analyzed accident. Therefore, the proposed change does not involve a
significant increase in the probability of an accident previously
evaluated.
Of the applicable accidents previously evaluated, the limiting
transients with consideration to the proposed changes to the SG tube
inspection criteria, are the SG tube rupture (SGTR) event and the
steam line break (SLB) accident.
During the SGTR event, the required structural integrity margins
of the SG tubes will be maintained by the presence of the SG
tubesheet. SG tubes are hydraulically expanded in the tubesheet
area. Tube rupture in tubes with cracks in the tubesheet is
precluded by the constraint provided by the tubesheet. This
constraint results from the hydraulic expansion process, thermal
expansion mismatch between the tube and tubesheet and from the
differential pressure between the primary and secondary side. Based
on this design, the structural margins against burst, discussed in
Regulatory Guide (RG) 1.121, ``Bases for Plugging Degraded PWR
[Pressurized Water Reactor] SG Tubes,'' are maintained for both
normal and postulated accident conditions.
The proposed changes do not affect other systems, structures,
components or operational features. Therefore, the proposed changes
result in no significant increase in the probability of the
occurrence of a SGTR accident.
At normal operating pressures, leakage from primary water stress
corrosion cracking (PWSCC) below the proposed limited inspection
depth is limited by both the tube-to-tubesheet crevice and the
limited crack opening permitted by the tubesheet constraint.
Consequently, negligible normal operating leakage is expected from
cracks within the tubesheet region. The consequences of an SGTR
event are affected by the primary-to-secondary leakage flow during
the event. Primary-to-secondary leakage flow through a postulated
broken tube is not affected by the proposed change since the
tubesheet enhances the tube integrity in the region of the hydraulic
expansion by precluding tube deformation beyond its initial
hydraulically expanded outside diameter.
The probability of a SLB is unaffected by the potential failure
of a SG tube as this failure is not an initiator for a SLB.
The consequences of a SLB are also not significantly affected by
the proposed changes. During a SLB accident, the reduction in
pressure above the tubesheet on the shell side of the SG creates an
axially uniformly distributed load on the tubesheet due to the
reactor coolant system pressure on the underside of the tubesheet.
The resulting bending action constrains the tubes in the tubesheet
thereby restricting primary-to-secondary leakage below the midplane.
Primary-to-secondary leakage from tube degradation in the
tubesheet area during the limiting accident (i.e., SLB) is limited
by flow restrictions resulting from the crack and tube-to-tubesheet
contact pressures that provide a restricted leakage path above the
indications and also limit the degree of potential crack face
opening as compared to free span indications. The primary-to-
secondary leak rate during postulated SLB accident conditions would
be expected to be less than that during normal operation for
indications near the bottom of the tubesheet (i.e., including
indications in the tube end welds). This conclusion is based on the
observation that while the driving pressure causing leakage
increases by approximately a factor of two, the flow resistance
associated with an increase in the tube-to-tubesheet contact
pressure, during a SLB, increases by up to approximately a factor of
three. While such a leakage decrease is logically expected, the
postulated accident leak rate could be conservatively bounded by
twice the normal operating leak rate if the increase in contact
pressure is ignored. Since normal operating leakage is limited to
less than 0.104 gpm [gallons per minute] (150 gpd [gallons per day])
per TS 3.4.13, ``RCS Operational Leakage,'' the associated accident
condition leak rate, assuming all leakage to be from lower tubesheet
indications, would be bounded by approximately 0.2 gpm. This value
is well within the assumed accident leakage rate of 0.5 gpm
discussed in Updated Final Safety Analysis Table 15.1-3,
``Parameters Used in Steam Line Break Analyses.'' Hence it is
reasonable to omit any consideration of inspection of the tube, tube
end weld, bulges/overexpansions or other anomalies below 17 inches
from the top of the hot leg tubesheet. Therefore, the consequences
of a SLB accident remain unaffected.
Based on the above discussion, the proposed changes do not
involve an increase in the consequences of an accident previously
evaluated.
Criterion 2.--Does the proposed change create the possibility of a new
or different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes do not involve the use or installation of
new equipment and the currently installed equipment will not be
operated in a new or different manner. No new or different system
interactions are created and no new processes are introduced. The
proposed changes will not introduce any new failure mechanisms,
malfunctions, or accident initiators not already considered in the
design and licensing bases.
Based on this evaluation, the proposed change does not create
the possibility of a new or different kind of accident from any
accident previously evaluated.
Criterion 3.--Does the proposed change involve a significant reduction
in a margin of safety?
Response: No.
The proposed changes maintain the required structural margins of
the SG tubes for both normal and accident conditions. Nuclear Energy
Institute (NEI) 97-06, ``Steam Generator Program Guidelines,''
Revision 1 and Regulatory Guide (RG) 1.121, ``Bases for Plugging
Degraded PWR Steam Generator Tubes,'' are used as the bases in the
development of the limited hot leg tubesheet inspection depth
methodology for determining that SG tube integrity considerations
are maintained within acceptable limits. RG 1.121 describes a method
acceptable to the NRC for meeting General Design Criteria (GDC) 14,
``Reactor coolant pressure boundary,'' GDC 15, ``Reactor coolant
system design,'' GDC 31, ``Fracture prevention of reactor coolant
pressure boundary,'' and GDC 32, ``Inspection of reactor coolant
pressure boundary,'' by reducing the probability and consequences of
a SGTR. RG 1.121 concludes that by determining the limiting safe
conditions for tube wall degradation the probability and
consequences of a SGTR are reduced. This RG uses safety factors on
loads for tube burst that are consistent with the requirements of
Section III of the American Society of Mechanical Engineers (ASME)
Code.
For axially oriented cracking located within the tubesheet, tube
burst is precluded due to the presence of the tubesheet. For
circumferentially oriented cracking, Westinghouse letter LTR-CDME-
05-32, ``Limited Inspection of the Steam Generator Tube Portion
Within the Tubesheet at Byron Unit 2 and Braidwood Unit 2,''
Revision 2, dated August 2005, defines a length of degradation free
expanded tubing that provides the necessary resistance to tube
pullout due to the pressure induced forces, with applicable safety
factors applied. Application of the limited hot leg tubesheet
inspection depth criteria will preclude unacceptable primary-to-
secondary leakage during all plant conditions. The methodology for
determining leakage provides for large margins between calculated
and actual leakage values in the proposed limited hot leg tubesheet
inspection depth criteria.
Therefore, the proposed changes do not involve a significant
hazards consideration under the criteria set forth in 10 CFR
50.92(c).
The NRC staff has reviewed the licensee's analysis and, based on
this
[[Page 29678]]
review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Brad J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Kennett
Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
Exelon Generation Company, LLC, Docket Nos. 50-254 and 50-265, Quad
Cities Nuclear Power Station, Units 1 and 2, Rock Island County,
Illinois
Date of amendment request: January 25, 2006.
Description of amendment request: The proposed amendment would
revise the Updated Final Safety Analysis Report (UFSAR) to allow the
use of automatic load tap changers (LTCs) to operate in automatic mode
on the reserve auxiliary transformers (RATs) to compensate for
potential offsite power voltage fluctuations, in order to ensure that
acceptable voltage is maintained for safety related equipment.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The requested change allows the automatic operation mode of the
LTC. The only accident previously evaluated for which the
probability is potentially affected by the change is the loss of
offsite power (LOOP). A failure of the LTC while in automatic
operation mode that results in decreased voltage to the ESS
[essential service system] buses could cause a LOOP. This could
occur in two ways. A failure of the LTC controller that results in
rapidly decreasing the voltage to the emergency buses is the most
severe failure mode. However, a backup controller is provided with
the LTC that makes this failure unlikely. A failure of the LTC
controller to respond to decreasing grid voltage is less severe,
since grid voltage changes occur slowly. In both of the above
potential failure modes, operators will take manual control of the
LTC to mitigate the effects of the failure. Thus, the probability of
a LOOP is not significantly increased.
The proposed change has no effect on the consequences of a LOOP,
since the emergency diesel generators provide power to safety
related equipment following a LOOP. The emergency diesel generators
are not affected by the proposed change.
The probability of other accidents previously evaluated is not
affected, since the proposed change does not affect the way plant
equipment is operated and thus does not contribute to the initiation
of any of the previously evaluated accidents.
The LTC is equipped with a backup controller, which controls the
LTC in the event of primary controller failure. Additionally,
operator action is available to prevent a sustained high voltage
condition from occurring. Damage due to over-voltage is time-
dependent. Therefore, damage of safety related equipment is
extremely unlikely, and the consequences of these accidents are not
significantly increased. The only way in which the consequences of
other previously evaluated accidents could be affected is if a
failure of the LTC, while in automatic operation mode, led to a
sustained high voltage condition, which resulted in damage to safety
related equipment that is used to mitigate an accident.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change involves functions that provide offsite
power to safety related equipment for accident mitigation. Thus, the
proposed change potentially affects the consequences of previously
evaluated accidents (as addressed in Question 1), but does not
result in any new mechanisms that could initiate damage to the
reactor and its principal safety barriers (i.e., fuel cladding,
reactor coolant system, or primary containment).
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change does not affect the inputs or assumptions of
any of the analyses that demonstrate the integrity of the fuel
cladding, reactor coolant system, or containment during accident
conditions. The allowable values for the degraded voltage protection
function are unchanged and will continue to ensure that the degraded
voltage protection function actuates when required, but does not
actuate prematurely to cause a LOOP. Automatic operation of the LTC
increases margin by reducing the potential for transferring to the
EDGs [emergency diesel generators] during an event.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Bradley J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelong Way, Kennett
Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
FirstEnergy Nuclear Operating Company, et al., Docket No. 50-440, Perry
Nuclear Power Plant, Unit 1, Lake County, Ohio
Date of amendment request: February 10, 2006.
Description of amendment request: The proposed amendment would
modify Technical Specification (TS) 3.3.5.1, ``Emergency Core Cooling
System (ECCS) Instrumentation,'' to correct a Perry Nuclear Power Plant
(PNPP)-specific issue and establish consistency with the improved
standard technical specifications (ISTS). Specifically, Sub-actions
B.1.2.1 and B.1.2.2, which were added into PNPP TS 3.3.5.1 during the
ISTS conversion process, will be deleted. PNPP Required Action B.1 will
then match the ISTS Required Action B.1. As a result, actions with a 1-
hour completion time will only be required for the annulus exhaust gas
treatment (AEGT) system if a loss of initiation capability in both
divisions actually exists for an AEGT initiation function, as
originally intended.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. The proposed change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
There are no physical modifications being made to any plant
system or component. The only change is to a Required Action within
the Technical Specifications. The revised Technical Specification
requirements do not impact initiators of previously evaluated
accidents or transients.
The specification being revised is associated with a system used
to mitigate the consequences of accidents. The change does not
affect how the AEGT system is controlled, operated, or tested. The
intent of Required Action B.1 for the ECCS Instrumentation,
specifically, a loss of initiation capability check, is maintained
by the changes being proposed. The wording of Required Action B.1
ensures appropriate actions are taken when a loss of initiation
capability exists, by declaring the supported systems inoperable.
This action is consistent with the current requirements.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. The proposed change does not create the possibility of a new
or different kind of accident from any accident previously
evaluated.
There are no physical modifications being made to any plant
system or component, and
[[Page 29679]]
the proposed change introduces no new method of operation for the
plant, or its systems or components. Therefore, the proposed change
does not create the possibility of a new or different kind of
accident from any accident previously evaluated.
3. The proposed change does not involve a significant reduction
in a margin of safety.
The change to the ECCS Instrumentation Required Action continues
to ensure that a check is performed to determine if one or more of
the ECCS Instrumentation Functions has lost its capability to
actuate the Division 1 and 2 low-pressure ECCS, the AEGT subsystems,
and the associated diesel generators. It continues to direct
appropriate actions if such a loss of initiation capability is
found. Therefore, the necessary function of the Technical
Specification requirements is maintained, and the proposed changes
do not involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David W. Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street, Akron, OH 44308.
NRC Branch Chief: Daniel S. Collins.
Nuclear Management Company, LLC, Docket No. 50-255, Palisades Plant,
Van Buren County, Michigan
Date of amendment request: February 16, 2006.
Description of amendment request: The proposed amendment would
revise the Technical Specification (TS) requirements related to steam
generator (SG) tube integrity. The change is consistent with NRC-
approved Revision 4 to Technical Specification Task Force (TSTF)
Standard Technical Specification Change Traveler, TSTF-449, ``Steam
Generator Tube Integrity.'' The availability of this TS improvement was
announced in the Federal Register on May 6, 2005 (70 FR 24126) as part
of the consolidated line item improvement process (CLIIP).
The NRC staff issued a notice of availability of a model no
significant hazards consideration (NSHC) determination for referencing
in license amendment applications in the Federal Register on March 2,
2005 (70 FR 10298) as part of the CLIIP. The licensee affirmed the
applicability of the model NSHC determination in its application dated
February 16, 2006.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
Criterion 1.--The Proposed Change Does Not Involve a Significant
Increase in the Probability or Consequences of an Accident Previously
Evaluated
The proposed change requires a SG Program that includes
performance criteria that will provide reasonable assurance that the
SG tubing will retain integrity over the full range of operating
conditions (including startup, operation in the power range, hot
standby, cooldown and all anticipated transients included in the
design specification). The SG performance criteria are based on tube
structural integrity, accident induced leakage, and operational
LEAKAGE.
A SGTR [steam generator tube rupture] event is one of the design
basis accidents that are analyzed as part of a plant's licensing
basis. In the analysis of a SGTR event, a bounding primary to
secondary LEAKAGE rate equal to the operational LEAKAGE rate limits
in the licensing basis plus the LEAKAGE rate associated with a
double-ended rupture of a single tube is assumed.
For other design basis accidents such as MSLB [main steamline
break], rod ejection, and reactor coolant pump locked rotor the
tubes are assumed to retain their structural integrity (i.e., they
are assumed not to rupture). These analyses typically assume that
primary to secondary LEAKAGE for all SGs is 1 gallon per minute or
increases to 1 gallon per minute as a result of accident induced
stresses. The accident induced leakage criterion introduced by the
proposed changes accounts for tubes that may leak during design
basis accidents. The accident induced leakage criterion limits this
leakage to no more than the value assumed in the accident analysis.
The SG performance criteria proposed change to the TS identify
the st