Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 23952-23970 [06-3901]
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23952
Federal Register / Vol. 71, No. 79 / Tuesday, April 25, 2006 / Notices
7778 Aircraft Accident Report—
Crash During Approach to Landing,
Air Tahoma, Inc., Flight 185,
Convair 580, N586P, Covington,
Kentucky, August 13, 2004.
NEWS MEDIA CONTACT: Ted Lopatkiewicz,
Telephone: (202) 314–6100.
Individuals requesting specific
accommodations should contact Chris
Bisett at (202) 314–6305 by Friday,
April 28, 2006.
The public may view the meeting via
a live or archived Web cast by accessing
a link under ‘‘News & Events’’ on the
NTSB home page at https://
www.ntsb.gov.
FOR FURTHER INFORMATION CONTACT:
Vicky D’Onofrio, (202) 314–6410.
Dated: April 21, 2006.
Vicky D’Onofrio,
Federal Register Liaison Officer.
[FR Doc. 06–3944 Filed 4–21–06; 1:51 pm]
BILLING CODE 7533–01–M
2334).
1 p.m.: Briefing on Status of
Emergency Planning Activities—
Afternoon Session (Public Meeting).
These meetings will be webcast live at
the Web address—https://www.nrc.gov.
Wednesday, May 3, 2006
8:55 a.m.: Affirmation Session (Public
Meeting) (Tentative). a. ANDREW
SIEMASZKO, Docket No. IA–05–
021, unpublished Licensing Board
Order (Dec. 22, 2005) (Tentative). b.
ANDREW SIEMASZKO, Docket No.
IA–05–021, unpublished Licensing
Board Order (March 2, 2006)
(Tentative).
9 a.m.: Briefing on Status of RiskInformed, Performance-Based
Regulation (Public Meeting)
(Contact: Eileen McKenna, 301–
415–2189).
This meeting will be webcast live at
the Web address—https://www.nrc.gov.
Week of May 8, 2006—Tentative
NUCLEAR REGULATORY
COMMISSION
There are no meetings scheduled for
the Week of May 8, 2006.
Sunshine Act Meetings
Week of May 15, 2006—Tentative
Weeks of April 24, May 1, 8, 15,
22, 29, 2006.
PLACE: Commissioners’ Conference
Room, 11555 Rockville Pike, Rockville,
Maryland.
STATUS: Public and Closed.
MATTERS TO BE CONSIDERED:
DATE:
Monday, May 15, 2006
1 p.m.: Briefing on Status of
Implementation of Energy Policy
Act of 2005 (Public Meeting)
(Contact: Scott Moore, 301–415–
7278).
This meeting will be Web cast live at
the Web address—https://www.nrc.gov.
Tuesday, May 16, 2006
Week of April 24, 2006
9:30 a.m.: Briefing on Results of the
Agency Action Review Meeting—
Reactors/Materials (Public Meeting)
(Contact: Mark Tonacci, 301–415–
4045).
Monday, April 24, 2006
2 p.m.: Meeting with Federal Energy
Regulatory Commission (FERC),
FERC Headquarters, 888 First St.,
NE., Washington, DC 20426, Room
2C (Public Meeting), (Contact: Mike
Mayfield, 301–415–3298).
This meeting will be webcast live at
the Web address—https://www.ferc.gov.
Wednesday, April 26, 2006
This meeting will be Web cast live at
the Web address—https://www.nrc.gov.
Week of May 22, 2006—Tentative
Wednesday, May 24, 2006
9:30 a.m.: Discussion of Security
Issues (Closed—Ex. 1).
1:30 p.m.: All Employees Meeting
(Public Meetings), Marriott
Bethesda North Hotel, Salons, D–H,
5701 Marinelli Road, Rockville, MD
20852.
1 p.m.: Discussion of Management
Issues (Closed—Ex. 2).
Thursday, April 27, 2006
1:30 p.m.: Meeting with Department
of Energy (DOE) on New Reactor
Issues (Public Meeting).
This meeting will be webcast live at
the Web address—https://www.nrc.gov.
Week of May 29, 2006–Tentative
Wednesday, May 31, 2006
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Week of May 1, 2006—Tentative
1 p.m.: Discussion of Security Issues
(Closed—Ex. 1).
Tuesday, May 2, 2006
9:30 a.m.: Briefing on Status of
Emergency Planning Activities—
Morning Session (Public Meeting)
(Contact: Eric Leeds, 301–415–
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Additional Information
The Briefing on Equal Employment
Opportunity (EEO) Programs (Public
Meeting) previously scheduled on May
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22, 2006, has been postponed and will
be rescheduled.
*The schedule for Commission meetings is
subject to change on short notice. To verify
the status of meetings call (recording)—(301)
415–1292. Contact person for more
information: Michelle Schroll, (301) 415–
1662.
The NRC Commission Meeting
Schedule can be found on the Internet
at: https://www.nrc.gov/what-we-do/
policy-making/schedule.html.
The NRC provides reasonable
accommodation to individuals with
disabilities where appropriate. If you
need a reasonable accommodation to
participate in these public meetings, or
need this meeting notice or the
transcript or other information from the
public meetings in another format (e.g.,
braille, large print), TDD: 301–415–
2100, or by e-mail at DLC@nrc.gov.
Determinations on requests for
reasonable accommodation will be
made on a case-by-case basis.
This notice is distributed by mail to
several hundred subscribers; if you no
longer wish to receive it, or would like
to be added to the distribution, please
contact the Office of the Secretary,
Washington, DC 20555 (301–415–1969).
In addition, distribution of this meeting
notice over the Internet system is
available. If you are interested in
receiving this Commission meeting
schedule electronically, please send an
electronic message to dkw@nrc.gov.
Dated: April 20, 2006.
R. Michelle Schroll,
Office of the Secretary.
[FR Doc. 06–3945 Filed 4–21–06; 2:01 pm]
BILLING CODE 7590–01–M
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
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the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from March 31,
2006 to April 13, 2006. The last
biweekly notice was published on April
11, 2006 (71 FR 18371).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
Involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
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will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
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As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
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when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) e-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
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www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
Dominion Energy Kewaunee, Inc.,
Docket No. 50–305, Kewaunee Power
Station, Kewaunee County, Wisconsin
Date of amendment request: March
17, 2006.
Description of amendment request:
The proposed amendment would
change the design criteria described in
the Kewaunee Power Station (KPS)
Updated Safety Analysis Report
(USAR). The change would add new
design criteria associated with internal
flooding to the current licensing basis
for KPS.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change provides clarification
to the existing functional requirements in the
USAR by including specific design criteria
for analyzing internal flooding in order to
verify the capability of an SSC [structure,
systems and components] to perform its
design function. The proposed change does
not affect any of the previously evaluated
accidents in the KPS updated safety analysis
report (USAR). No SSCs, operating
procedures, or administrative controls that
have the function of preventing or mitigating
any of these accidents are affected.
This proposed change to incorporate
design criteria into the USAR provides added
administrative assurance that internal
flooding will be appropriately addressed,
consistent with existing functional
requirements, and that safety related SSCs
will not be affected by a potential failure of
a non-safety related SSC. The change does
not affect any accident initiators or the
facility accident analysis. Thus, the
probability and the consequences of an
accident remain unchanged.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change to incorporate design
criteria consistent with existing functional
requirements into the USAR does not change
the design function or operation of any safety
related SSCs. The proposed change
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documents design criteria in use and
therefore does not involve a physical change
to the facility. The change, therefore, does
not create the possibility of a new or different
kind of accident due to credible new failure
mechanisms, malfunctions, or accident
initiators not considered in the design and
licensing bases.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
This proposed change does not affect any
margin of safety as established in the
Kewaunee USAR because it documents the
design criteria presently used and is
consistent with the functional requirements
in the USAR. This proposed change provides
added administrative assurance that safety
related SSCs will not be affected by a
potential failure of a non-safety related SSC
due to a postulated internal flooding event.
The proposed change adds criteria for the
evaluation of internal flooding events that are
more detailed than the existing functional
requirements in the USAR. Therefore, the
protection and subsequent availability of
safety related SSCs is maintained consistent
with previously assumed accident mitigation
capabilities.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Bradley D.
Jackson, Esq., Foley and Lardner, P.O.
Box 1497, Madison, WI 53701–1497.
NRC Branch Chief: L. Raghavan.
Exelon Generation Company, LLC,
Docket Nos. STN 50–454 and STN 50–
455, Byron Station, Unit Nos. 1 and 2,
Ogle County, Illinois; Docket Nos. STN
50–456 and STN 50–457, Braidwood
Station, Unit Nos. 1 and 2, Will County,
Illinois
Date of amendment request: January
12, 2006.
Description of amendment request:
The proposed amendment would
correctly modify the wording in
Technical Specification Surveillance
Requirement (SR) 3.6.6.3 Containment
Cooling train cooling water flow rate to
accurately reflect the plant
configuration. The current SR is to
verify flow to each train. The proposed
revision to SR 3.6.6.3 would verify flow
to each cooler (plant configuration is
two coolers per train).
Basis for proposed no significant
hazards consideration determination:
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As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed TS change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The proposed change will revise Technical
Specifications (TS) Surveillance Requirement
(SR) 3.6.6.3 containment cooling train
cooling water flow rate to accurately reflect
the existing plant configuration as described
in the Updated Final Safety Analysis Report
(UFSAR) Sections 6.2, ‘‘Containment
Systems,’’ and 9.4, ‘‘Air Conditioning,
Heating, Cooling, and Ventilation Systems.’’
The revision will specify the appropriate
testing requirements for verification that each
Containment Cooling System train Essential
Service Water (SX) flow rate to each cooling
unit is ≥ 2660 gpm [gallons per minute] and
will therefore provide assurance that the
design flow rate assumed in the safety
analyses will be achieved and the Limited
Conditions for Operation (LCO) will be met.
This change is in the conservative direction,
i.e., verification of flow rate to each cooling
unit 3 2660 gpm is more conservative than
verification of the same flow rate to each
cooling train that consists of two cooling
units. The performance of TS surveillance
testing is not a precursor to any accident
previously evaluated. Thus, the proposed
change does not have any effect on the
probability of an accident previously
evaluated.
The function of the Containment Cooling
System in conjunction with the Containment
Spray System is to provide containment
atmosphere cooling to limit post accident
pressure and temperature in containment to
less than design values. There is no change
to the design of the Containment Cooling
System. Furthermore, the surveillance testing
specified in SR 3.6.6.3 will provide assurance
that the Containment Cooling System will
perform as designed. Thus, the radiological
consequences of any accident previously
evaluated are not increased.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. The proposed TS change does not create
the possibility of a new or different kind of
accident from any accident previously
evaluated.
The proposed change does not affect the
control parameters governing unit operation
or the response of plant equipment to
transient conditions. The proposed change
does not change or introduce any new
equipment, modes of system operation or
failure mechanisms.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. The proposed TS change does not
involve a significant reduction in a margin of
safety.
Prior to conversion to ITS [Improved
Technical Specifications], the SR equivalent
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to SR 3.6.6.3 required that each system of
containment cooling fans be demonstrated
OPERABLE by ‘‘verifying an essential service
water flow rate of greater than or equal to
2660 gpm to each cooler.’’ During the ITS
conversion, standard verbiage for SR 3.6.6.3
was adopted; however, the specific plant
design of two Reactor Containment Fan
Coolers (RCFCs) per Containment Cooling
train was inadvertently overlooked.
This proposed amendment would correctly
modify the wording in Technical
Specifications (TS) Surveillance Requirement
(SR) 3.6.6.3 Containment Cooling System to
accurately reflect the Braidwood and Byron
existing plant design. The revision will
provide the appropriate testing requirements
for verification that each Containment
Cooling System train SX cooling flow rate to
each cooling unit is ≥ 2660 gpm. This
verification provides assurance that the
design flow rate assumed in the safety
analyses will be achieved; and, therefore the
LCO will be met. The change for verification
of SX cooling flow rate from each cooling
train to each cooling unit is in the
conservative direction and will revise the
existing non-conservative TS SR to be
consistent with the plant design as described
in the UFSAR.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change involves the deletion
of a reporting requirement. The change does
not affect plant equipment or operating
practices and, therefore, does not
significantly increase the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change is administrative in
that it deletes a reporting requirement. The
change does not add new plant equipment,
change existing plant equipment, or affect the
operating practices of the facility. Therefore,
the change does not create the possibility of
a new of different kind of accident from any
accident previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change deletes a reporting
requirement. The change does not affect
plant equipment or operation practices and,
therefore, does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Bradley J.
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
Based upon the reasoning presented
above, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M.S. Ross,
Florida Power & Light Company, P.O.
Box 14000, Juno Beach, FL 33408–0420.
NRC Branch Chief: Darrell J. Roberts.
FAL Energy Seabrook LLC, Docket No.
50–443, Seabrook Station, Unit No. 1,
Rockingham County, New Hampshire
Date of amendment request: March
23, 2006.
Description of amendment request:
The proposed amendment would revise
the Seabrook Station, Unit No. 1
(Seabrook) Operating License and
Technical Specifications (TSs) to delete
the license condition requiring reporting
of violations of other requirements (e.g.,
conditions listed in Section 2.C of the
operating license). The change is
consistent with the notice published in
the Federal Register on November 4,
2005, as part of the consolidated line
item improvement process.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
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FPL Energy Seabrook LLC, Docket No.
50–443, Seabrook Station, Unit No. 1,
Rockingham County, New Hampshire
Date of amendment request: March
23, 2006.
Description of amendment request:
The proposed amendment would revise
the Seabrook Station Unit No. 1
(Seabrook) Technical Specifications
(TSs) consistent with the NRC-approved
Revision 4 to Technical Specification
Task Force (TSTF) Standard Technical
Specification Change Traveler, TSTF–
449, ‘‘Steam Generator Tube Integrity.’’
Additionally, the proposed
amendment would revise Seabrook TS
Surveillance Requirement 4.4.6.2.1 to be
consistent with NUREG–1431, Revision
3, Improved Standard Technical
Specifications Westinghouse Plants.
The NRC staff issued a notice of
opportunity for comment in the Federal
Register on March 2, 2005 (70 FR
10298), on possible amendments
adopting TSTF–449, including a model
safety evaluation and model no
significant hazards consideration
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(NSHC) determination, using the
consolidated line item improvement
process. The NRC staff subsequently
issued a notice of availability of the
models for referencing in license
amendment applications in the Federal
Register on May 6, 2005 (70 FR 24126).
The licensee affirmed the applicability
of the following NSHC determination in
its application dated March 23, 2006.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
Criterion 1—The proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The proposed change requires a SG [Steam
Generator] Program that includes
performance criteria that will provide
reasonable assurance that the SG tubing will
retain integrity over the full range of
operating conditions (including startup,
operation in the power range, hot standby,
cooldown and all anticipated transients
included in the design specification). The SG
performance criteria are based on tube
structural integrity, accident induced
leakage, and operational LEAKAGE.
A SGTR [steam generator tube rupture]
event is one of the design basis accidents that
are analyzed as part of a plant’s licensing
basis. In the analysis of a[n] SGTR event, a
bounding primary to secondary LEAKAGE
rate equal to the operational LEAKAGE rate
limits in the licensing basis plus the
LEAKAGE rate associated with a doubleended rupture of a single tube is assumed.
For other design basis accidents such as
MSLB [main steamline break], rod ejection,
and reactor coolant pump locked rotor the
tubes are assumed to retain their structural
integrity (i.e., they are assumed not to
rupture). These analyses typically assume
that primary to secondary LEAKAGE for all
SGs is 1 gallon per minute or increases to 1
gallon per minute as a result of accident
induced stresses. The accident induced
leakage criterion introduced by the proposed
changes accounts for tubes that may leak
during design basis accidents. The accident
induced leakage criterion limits this leakage
to no more than the value assumed in the
accident analysis.
The SG performance criteria proposed
change[s] to the TS[s] to identify the
standards against which tube integrity is to
be measured. Meeting the performance
criteria provides reasonable assurance that
the SG tubing will remain capable of
fulfilling its specific safety function of
maintaining reactor coolant pressure
boundary integrity throughout each operating
cycle and in the unlikely event of a design
basis accident. The performance criteria are
only a part of the SG Program required by the
proposed change to the TS[s]. The program,
defined by NEI [Nuclear Energy Institute] 97–
06, Steam Generator Program Guidelines,
includes a framework that incorporates a
balance of prevention, inspection, evaluation,
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repair, and leakage monitoring. The proposed
changes do not, therefore, significantly
increase the probability of an accident
previously evaluated.
The consequences of design basis accidents
are, in part, functions of the DOSE
EQUIVALENT I–131 in the primary coolant
and the primary to secondary LEAKAGE
rates resulting from an accident. Therefore,
limits are included in the plant technical
specifications for operational leakage and for
DOSE EQUIVALENT I–131 in primary
coolant to ensure the plant is operated within
its analyzed condition. The typical analysis
of the limiting design basis accident assumes
that primary to secondary leak rate after the
accident is 1 gallon per minute with no more
than [500 gallons per day or 720 gallons per
day] in any one SG, and that the reactor
coolant activity levels of DOSE
EQUIVALENT I–131 are at the TS values
before the accident.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary coolant chemistry controls. The
proposed approach updates the current TSs
and enhances the requirements for SG
inspections. The proposed change does not
adversely impact any other previously
evaluated design basis accident and is an
improvement over the current TSs.
Therefore, the proposed change does not
affect the consequences of a SGTR accident
and the probability of such an accident is
reduced. In addition, the proposed changes
do not affect the consequences of an MSLB,
rod ejection, or a reactor coolant pump
locked rotor event, or other previously
evaluated accident.
Criterion 2—The proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
The proposed performance based
requirements are an improvement over the
requirements imposed by the current
technical specifications. Implementation of
the proposed SG Program will not introduce
any adverse changes to the plant design basis
or postulated accidents resulting from
potential tube degradation. The result of the
implementation of the SG Program will be an
enhancement of SG tube performance.
Primary to secondary LEAKAGE that may be
experienced during all plant conditions will
be monitored to ensure it remains within
current accident analysis assumptions.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary or secondary coolant chemistry
controls. In addition, the proposed change
does not impact any other plant system or
component. The change enhances SG
inspection requirements.
Therefore, the proposed change does not
create the possibility of a new or different
type of accident from any accident
previously evaluated.
Criterion 3—The proposed change does not
involve a significant reduction in the margin
of safety.
The SG tubes in pressurized water reactors
are an integral part of the reactor coolant
pressure boundary and, as such, are relied
upon to maintain the primary system’s
pressure and inventory. As part of the reactor
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coolant pressure boundary, the SG tubes are
unique in that they are also relied upon as
a heat transfer surface between the primary
and secondary systems such that residual
heat can be removed from the primary
system. In addition, the SG tubes isolate the
radioactive fission products in the primary
coolant from the secondary system. In
summary, the safety function of an SG is
maintained by ensuring the integrity of its
tubes.
Steam generator tube integrity is a function
of the design, environment, and the physical
condition of the tube. The proposed change
does not affect tube design or operating
environment. The proposed change is
expected to result in an improvement in the
tube integrity by implementing the SG
Program to manage SG tube inspection,
assessment, repair, and plugging. The
requirements established by the SG Program
are consistent with those in the applicable
design codes and standards and are an
improvement over the requirements in the
current TSs.
For the above reasons, the margin of safety
is not changed and overall plant safety will
be enhanced by the proposed change to the
TS.
Based upon the reasoning presented
above, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M.S. Ross,
Florida Power & Light Company, P.O.
Box 14000, Juno Beach, FL 33408–0420.
NRC Branch Chief: Darrell J. Roberts.
Indiana Michigan Power Company,
Docket Nos. 50–315 and 50–316, Donald
C. Cook Nuclear Plant, Units 1 and 2,
Berrien County, Michigan
Date of amendment requests: March
7, 2006.
Description of amendment requests:
The proposed amendments would
modify the Technical Specifications
(TS) of the units to change the reactor
trip on turbine trip from the P–7
interlock to the P–8 interlock.
Specifically, the amendment would
effect changes in TS Table 3.3.1–1,
‘‘Reactor Trip System Instrumentation,’’
for Function 16, ‘‘Turbine Trip.’’ The
purpose of the proposed amendment is
to decrease potentially unnecessary
transients on the reactor and to increase
plant availability when the cause of a
turbine trip is readily correctable.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration as follows:
(1) Does the proposed change involve a
significant increase in the probability of
occurrence or consequences of an accident
previously evaluated?
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Response: No.
The proposed change revises the setpoint
at which a reactor trip will occur by changing
the interlock at which it is enabled from the
P–7 interlock, at approximately 10 percent
power, to the P–8 interlock, at less than or
equal to 31 percent power. The P–7 and P–
8 interlocks are not accident initiators and
the change to the reactor trip setpoint does
not create any new credible single failure. An
analysis has shown that a turbine trip
without a reactor trip at 31 percent power or
below does not challenge the pressurizer
power operated relief valves (PORVs),
thereby not adversely affecting the
probability of a small[-]break loss[-]of
[-]coolant accident due to a stuck open
PORV. The consequences of accidents
previously evaluated are unaffected by this
change because no change to any accident
mitigation scenario has resulted and there are
no additional challenges to fission product
barrier integrity.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
(2) Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
No changes are being made to the plant
that would introduce any new accident
causal mechanisms. The proposed change to
the power level at which a reactor trip on
turbine trip is enabled does not adversely
affect previously identified accident
initiators and does not create any new
accident initiators. The change does not
affect how the associated trip function
operates. No new single failures or accident
scenarios are created by the proposed change
and the proposed change does not result in
any event previously deemed incredible
being made credible.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
(3) Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
No safety analyses [will be] changed or
modified as a result of the proposed change
in reactor trip setpoint. All margins
associated with the current safety analyses
acceptance criteria are unaffected. The
current safety analyses remain binding. The
safety systems credited in the safety analyses
will continue to be available to perform their
mitigation functions. The proposed change
does not affect the availability or operability
of safety-related systems and components.
Therefore, the proposed change does not
involve a significant reduction in the margin
of safety.
Based on the licensee’s analysis, it
appears that the three standards of 10
CFR 50.92(c) are satisfied. Therefore, the
NRC staff proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: James M. Petro,
Jr., Esquire, One Cook Place, Bridgman,
MI 49106.
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NRC Branch Chief: L. Raghavan.
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request: January
30, 2006.
Description of amendment request:
The proposed change would revise
Cooper Nuclear Station (CNS) Technical
Specification section 5.5.12, ‘‘Primary
Containment Leakage Rate Testing
Program,’’ to allow a one-time extension
of no more than 5 years for the Type A,
Integrated Leakage Rate Test (ILRT)
interval. This revision is a one-time
exception to the 10-year frequency of
the performance-based leakage rate
testing program for Type A tests as
defined in Nuclear Energy Institute
(NEI) document NEI 94–01, Revision 0,
‘‘Industry Guideline for Implementing
Performance-Based Option of 10 CFR
part 50, appendix J,’’ pursuant to 10
CFR 50, appendix J, option B. The
requested exception is to allow the ILRT
to be performed within 15 years from
the last ILRT, last performed on
December 7, 1998.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
This license amendment proposes to revise
the Technical Specifications to allow for a
one-time extension of the ILRT interval from
10 years to 15 years. The containment
function is solely to mitigate the
consequences of an accident. No design basis
accident is initiated by a failure of the
containment leakage mitigation function. The
extension of the ILRT will not create any
adverse interactions with other systems that
could result in initiation of a design basis
accident. Continued containment integrity is
also assured by the established programs for
local leakage rate testing and inservice
inspections which are unaffected by the
proposed change. Therefore, the probability
of occurrence of an accident previously
evaluated is not significantly increased.
The potential consequences of the
proposed change have been quantified by
analyzing the changes in risk that would
result from extending the ILRT interval from
10 to 15 years. The increase in risk in terms
of person-rem per year within 50 miles
resulting from accidents was determined to
be of a magnitude that NUREG–1493
indicates is imperceptible. NPPD [Nebraska
Public Power District] has also analyzed the
increase in risk in terms of the frequency of
large early releases from accidents. The
increase in the large early release frequency
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resulting from the proposed extension was
determined to be within the guidelines
published in Nuclear Regulatory Commission
(NRC) Regulatory Guide 1.174. Additionally,
the proposed change maintains defense-indepth by preserving a reasonable balance
among prevention of core damage,
prevention of containment failure, and
consequence mitigation. NPPD has
determined that the increase in conditional
containment failure probability from
reducing the ILRT frequency from one test in
10 years to one test in 15 years would be
insignificant.
Therefore, the probability of occurrence or
the consequences of an accident previously
analyzed are not significantly increased.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed extension of the current
interval for the ILRT does not involve any
change to the design or operation of any
plant structure, system, or component (SSC).
The plant will continue to be operated in the
same manner. Since no changes to the design
or operation of the plant are being made, the
proposed one-time extension of the ILRT
does not result in a new failure mode for an
accident.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any accident
previously analyzed.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The proposed extension to the ILRT test
interval will not result in a change to the
design or operation of any plant SSC used to
shut down the plant, initiate Emergency Core
Cooling Systems, or isolate the primary or
secondary containment. Thus, the change
will not impact the ability of CNS to mitigate
any accident or transient. NUREG–1493, a
generic study of the effects of extending
containment leakage testing, documented
that an extension in the ILRT interval from
three per 10 years to one per 20 years
resulted in an imperceptible increase in risk
to the public. NUREG–1493 generically
concluded that the design containment
leakage rate contributes about 0.1 percent to
the individual risk, and that the decrease in
the ILRT frequency would have a minimal
effect on this risk since 95% of the potential
leakage paths are detected by Type B and
Type C testing. A risk assessment using the
current CNS Probabilistic Safety Assessment
internal events model concluded that the risk
associated with this change is very small and
not risk significant.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
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Attorney for licensee: Mr. John C.
McClure, Nebraska Public Power
District, Post Office Box 499, Columbus,
NE 68602–0499.
NRC Branch Chief: David Terao.
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Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request: March
15, 2006.
Description of amendment request:
The proposed amendment would revise
Cooper Nuclear Station (CNS) Technical
Specification 5.5.12, ‘‘Primary
Containment Leakage Rate Testing
Program,’’ by adding two subparagraphs to note exemptions from
Section III.A and Section III.B of Part 50
of Title 10 of the Code of Federal
Regulations, Appendix J, Option B.
These two sub-paragraphs allow the
leakage contribution from the four main
steam line penetrations, referred to as
the Main Steam Isolation Valve (MSIV)
leakage, to be excluded.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
This proposed change to TS 5.5.12 does
not modify existing structures, systems or
components (SSC’s) of the plant, and it does
not introduce new SSC’s. It does not change
assumptions, methodology or results of
previously evaluated accidents in the
Updated Safety Analysis Report.
It does not change operating procedures or
administrative controls that affect the
functions of SSC’s. By excluding MSIV
leakage from Type A and Type B and C test
results, this change will make the CNS
Primary Containment Leakage Rate Testing
Program more closely aligned with the
assumptions used in associated accident
consequence analyses. Therefore, the
proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
This proposed change to TS 5.5.12.a does
not modify existing SSC’s of the plant, and
it does not introduce new SSC’s. Thus, it
does not affect the design function or
operation of SSC’s involved, and it does not
introduce a new accident initiator. Therefore,
the proposed change does not create the
possibility of a new or different kind of
accident from any previously evaluated.
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3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
Since MSIV leakage bypasses the
containment and its filtration system
(Standby Gas Treatment System) during a
Loss-of-Coolant Accident (LOCA), the effects
on release to the environment [are] analyzed
and specifically accounted for in the CNS
dose analysis methodology approved by
Amendments 196 and 206. This proposed
change to exclude MSIV leakage from Type
A and Type B and C test results does not
change dose analysis values, and thus, does
not affect actual margin in the dose analysis.
Therefore, the proposed change does not
involve a significant reduction in an actual
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John C.
McClure, Nebraska Public Power
District, Post Office Box 499, Columbus,
NE 68602–0499.
NRC Branch Chief: David Terao.
Nine Mile Point Nuclear Station, LLC,
Docket No. 50–410, Nine Mile Point
Nuclear Station, Unit 2, Oswego County,
New York
Date of amendment request:
December 29, 2005.
Description of amendment request:
The proposed change would delete
Section 2.F of the Nine Mile Point, Unit
2 Facility Operating License (FOL),
NPF–69, which requires the licensee
report violations of the requirements
contained in Section 2.C of this license.
The NRC staff issued a notice of
opportunity for comment in the Federal
Register on August 29, 2005 (70 FR
51098), on possible amendments to
delete this reporting requirement,
including a model safety evaluation and
model no significant hazards
consideration (NSHC) determination,
using the consolidated line item
improvement process. The NRC staff
subsequently issued a notice of
availability of the models for referencing
in license amendment applications in
the Federal Register on November 4,
2005 (70 FR 67202). The licensee
affirmed the applicability of the
following NSHC determination in its
application dated December 29, 2005.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
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1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change involves the deletion
of a reporting requirement. The change does
not affect any plant equipment or operating
practices and therefore does not significantly
increase the probability or consequences of
an accident previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change is administrative in
that it deletes a reporting requirement. The
change does not add new plant equipment,
change existing plant equipment, or affect the
operating practices of the facility. Therefore,
the change will not create the possibility of
a new or different kind of accident from any
accident previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change deletes a reporting
requirement. The change does not affect
plant equipment or operating practices and
therefore does not involve a significant
reduction in a margin of safety.
Based on the above, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mark J.
Wetterhahn, Esquire, Winston & Strawn,
1700 K Street, NW., Washington, DC
20006.
NRC Branch Chief: Richard J. Laufer.
Nuclear Management Company, LLC,
Docket Nos. 50–266 and 50–301, Point
Beach Nuclear Plant, Units 1 and 2,
Town of Two Creeks, Manitowoc
County, Wisconsin
Date of amendment request: March
23, 2006.
Description of amendment request:
The proposed amendment would revise
Technical Specification (TS) 3.3.4,
‘‘Loss of Power (LOP) Diesel Generator
(DG) Start and Load Sequence
Instrumentation’’. The revision modifies
the section title and corrects a
nonconservatism in the degraded
voltage time delay values in TS
Surveillance Requirement (SR) 3.3.4.3.b.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
1. Operation of the Point Beach Nuclear
Plant in accordance with the proposed
amendments does not result in a significant
increase in the probability or consequences
of any accident previously evaluated.
The diesel generators (DGs) provide
emergency electrical power to the safeguard
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buses in support of equipment required to
mitigate the consequences of design basis
accidents and anticipated operational
occurrences, including an assumed loss of all
offsite power. SR 3.3.4.3 verifies that the loss
of power (LOP) DG start instrumentation
channels respond to measured parameters
within the necessary range and accuracy. The
proposed amendment revises the section title
and corrects nonconservative values in the
allowed time delays for the degraded voltage
protection function. The revised values are
more restrictive than the previously allowed
values.
Reducing the time delays for the degraded
voltage function as proposed does not
significantly increase the probability of a loss
of offsite power event. The degraded voltage
analysis established both maximum time
delay limits for a degraded voltage condition
and minimum time delays to prevent
premature disconnection from offsite power.
The analyzed time delay limits considered
prevention of premature disconnection from
offsite power such that the probability of an
unnecessary loss of offsite power is not
significantly increased.
The proposed change does not involve any
hardware changes, nor does it affect the
probability of any event initiators. There will
be no change to normal plant operating
parameters, accident mitigation capabilities,
or accident analysis assumptions or inputs.
Therefore, the probability or consequences
of any accident previously evaluated will not
be significantly increased as a result of the
proposed change.
2. Operation of the Point Beach Nuclear
Plant in accordance with the proposed
amendments does not result in a new or
different kind of accident from any accident
previously evaluated.
No new accident scenarios, transient
precursors, failure mechanisms, or limiting
single failures are introduced as a result of
the proposed change. The revised
surveillance requirements are more
restrictive and will continue to assure
equipment reliability such that plant safety is
maintained or will be enhanced.
Equipment important to safety will
continue to operate as designed. The changes
do not result in any event previously deemed
incredible being made credible. The changes
do not result in adverse conditions or result
in any increase in the challenges to safety
systems. Therefore, operation of the Point
Beach Nuclear Plant in accordance with the
proposed amendment will not create the
possibility of a new or different type of
accident from any accident previously
evaluated.
3. Operation of the Point Beach Nuclear
Plant in accordance with the proposed
amendments does not result in a significant
reduction in a margin of safety.
The diesel generators (DGs) provide
emergency electrical power to the safeguard
buses in support of equipment required to
mitigate the consequences of design basis
accidents and anticipated operational
occurrences, including an assumed loss of all
offsite power. SR 3.3.4.3 verifies that the loss
of power (LOP) DG start instrumentation
channels respond to measured parameters
within the necessary range and accuracy. The
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proposed amendment corrects
nonconservative values in the allowed time
delays for the degraded voltage protection
function. The revised values are more
restrictive than the previously allowed
values. The proposed change to this SR
assures that design requirements of the
emergency electrical power system continue
to be met.
There are no new or significant changes to
the initial conditions contributing to accident
severity or consequences. The proposed
amendment will not otherwise affect the
plant protective boundaries, will not cause a
release of fission products to the public, nor
will it degrade the performance of any other
structures, systems or components (SSCs)
important to safety. Therefore, the requested
change will not result in a significant
reduction in the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jonathan Rogoff,
Esquire, Vice President, Counsel &
Secretary, Nuclear Management
Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Branch Chief: L. Raghavan.
PPL Susquehanna, LLC, Docket Nos. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1
and 2), Luzerne County, Pennsylvania
Date of amendment request: February
1, 2006.
Description of amendment request:
The proposed amendment would
modify Technical Specification (TS)
requirements for inoperable snubbers by
adding Limiting Condition for
Operation (LCO) 3.0.8 for SSES 1 and 2.
This change is based on the TS Task
Force (TSTF) change traveler TSTF–372,
Revision 4. A notice of availability for
this TS improvement using the
consolidated line item improvement
process was published in the Federal
Register on November 24, 2004, and
May 4, 2005.
The Nuclear Regulatory Commission
(NRC) staff issued a notice of
availability of a model no significant
hazards consideration (NSHC)
determination for referencing license
amendment applications in the Federal
Register on November 24, 2004 (69 FR
68412), and May 4, 2005 (70 FR 23252).
The licensee affirmed the applicability
of the model NSHC determination in its
application dated February 1, 2006.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
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issue of no significant hazards
consideration, which is presented
below:
1. Criterion 1—The Proposed Change Does
Not Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated.
The proposed change allows a delay time
for entering a supported system technical
specification (TS) when the inoperability is
due solely to an inoperable snubber if risk is
assessed and managed. The postulated
seismic event requiring snubbers is a lowprobability occurrence and the overall TS
system safety function would still be
available for the vast majority of anticipated
challenges. Therefore, the probability of an
accident previously evaluated is not
significantly increased, if at all. The
consequences of an accident while relying on
allowance provided by proposed LCO 3.0.8
are no different than the consequences of an
accident while relying on the TS required
actions in effect without the allowance
provided by proposed LCO 3.0.8. Therefore
the consequences of an accident previously
evaluated are not significantly affected by
this change. The addition of a requirement to
assess and manage the risk introduced by this
change will further minimize possible
concerns. Therefore, this change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Criterion 2—The Proposed Change Does
Not Create the Possibility of a New or
Different Kind of Accident From Any
Previously Evaluated.
The proposed change does not involve a
physical alteration of the plant (no new or
different type of equipment will be installed).
Allowing delay times for entering supported
system TS when inoperability is due solely
to inoperable snubbers, if risk is assessed and
managed, will not introduce new failure
modes or effects and will not, in the absence
of other unrelated failures, lead to an
accident whose consequences exceed the
consequences of accidents previously
evaluated. The addition of a requirement to
assess and manage the risk introduced by this
change will further minimize possible
concerns.
Thus, this change does not create the
possibility of a new or different kind of
accident from an accident previously
evaluated.
3. Criterion 3—The Proposed Change Does
Not Involve a Significant Reduction in the
Margin of Safety.
The proposed change allows a delay time
for entering a supported system TS when the
inoperability is due solely to an inoperable
snubber, if risk is assessed and managed. The
postulated seismic event requiring snubbers
is a low-probability occurrence and the
overall TS system safety function would still
be available for the vast majority of
anticipated challenges. The risk impact of the
proposed TS changes was assessed following
the three-tiered approach recommended in
RG 1.177. A bounding risk assessment was
performed to justify the proposed TS
changes. This application of LCO 3.0.8 is
predicated upon the licensee’s performance
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of a risk assessment and the management of
plant risk. The net change to the margin of
safety is insignificant. Therefore, this change
does not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Bryan A. Snapp,
Esquire, Assoc. General Counsel, PPL
Services Corporation, 2 North Ninth St.,
GENTW3, Allentown, PA 18101–1179.
NRC Branch Chief: Richard J. Laufer.
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R.E. Ginna Nuclear Power Plant, LLC,
Docket No. 50–244, R.E. Ginna Nuclear
Power Plant, Wayne County, New York
Date of amendment request: March
28, 2006.
Description of amendment request:
The proposed amendment would revise
Technical Specification Surveillance
Requirement 3.5.1.4 by changing the
method and sample frequency for boron
concentration verification for the
emergency core cooling system (ECCS)
accumulators.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The ECCS Accumulators are used only to
respond to an accident and are not an
accident initiator. Therefore, the probability
of an accident has not increased.
Boron concentration is controlled in the
ECCS Accumulators to prevent either
excessive boron concentrations or
insufficient boron concentrations. Post-lossof-coolant accident (LOCA) emergency
procedures directing the operator to establish
simultaneous hot and cold leg injection are
based on the worst case minimum boron
precipitation time. Maintaining the
maximum ECCS Accumulator boron
concentration within the upper limit ensures
that the ECCS Accumulators do not
invalidate these steps. The minimum boron
requirements of 2100 (2550 after EPU
[extended power uprate]) ppm [parts per
million] ppm are based on beginning-of-life
reactivity values and are selected to ensure
that the reactor will remain subcritical during
the reflood stage of a large break LOCA.
During a large break LOCA, all control
element assemblies are assumed not to insert
into the core, and the initial reactor
shutdown is accomplished by void formation
during blowdown. Sufficient boron
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concentration must be maintained in the
ECCS Accumulators to prevent a return to
criticality during reflood. Level and pressure
instrumentation is provided to monitor the
availability of the ECCS Accumulators during
plant operation.
The Technical Specification Surveillance
Requirement (SR 3.5.1.4) verifies that the
boron concentration remains within the
required range by sampling. Currently, the
boron concentration in each ECCS
Accumulator is required to be verified by
taking a sample of the water in the ECCS
Accumulator every 31 days on a staggered
test basis. A containment entry is required to
take a sample from each of the two ECCS
Accumulators. In addition, the makeup water
source for the ECCS Accumulators is from
the RWST [refueling water storage tank],
which is maintained between 2300 ppm and
2600 ppm (2750 and 3050 after EPU) by SR
3.5.4.2, ensuring the ECCS Accumulators are
not diluted during makeup/fill evolutions.
However, the Reactor Coolant System boron
concentration is lower during power
operation than the boron concentration in the
ECCS Accumulators. Two check valves in
series prevent leakage from the Reactor
Coolant System into the ECCS Accumulators.
This proposed amendment would require
inleakage monitoring to be done every twelve
hours in addition to taking samples from
each ECCS Accumulator every six months.
Samples would continue to be taken to verify
the inleakage observations remain
conservative.
The engineering analysis and risk insights
combine to demonstrate that the method of
ECCS Accumulator boron concentration
verification can be changed from sampling
every 31 days on a staggered test basis to
monitoring inleakage every twelve hours and
sampling each ECCS Accumulator every six
months. The inleakage monitoring is based
on a calculational method that has sufficient
conservatism to predict the boron
concentration of the ECCS Accumulator as
shown by sample. Therefore, the ECCS
Accumulator would remain capable of
responding to an accident as described above
and the consequences of an accident
previously evaluated are not increased.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not alter the
function of any equipment, nor cause it to
operate differently than it was designed to
operate. All equipment required to mitigate
the consequences of an accident would
continue to operate as before. The proposed
change alters the method of verification of
the ECCS Accumulator boron concentration,
but not the boron concentration requirements
themselves.
Therefore, this change does not create the
possibility of a new or different [kind] of
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
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Response: No.
The inleakage monitoring done to verify
the concentration of boron in the ECCS
Accumulators, is sufficiently conservative to
ensure that a decrease in boron concentration
would be detected, leading to attempts to
increase the boron concentration or a need to
sample the affected ECCS Accumulator.
Sampling of the ECCS Accumulators every
six months will continue to be done to
ensure that the inleakage monitoring remains
conservative and representative. If the boron
concentration is maintained in the ECCS
Accumulators, the system operates as
assumed in the Updated Final Safety
Analysis Report Chapter 15 analyses and the
analyses continues to meet the dose
consequences acceptance criteria given in the
Updated Final Safety Analysis Report.
Therefore, this proposed change does not
involve a significant reduction in [a] margin
of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Daniel F.
Stenger, Ballard Spahr Andrews &
Ingersoll, LLP, 601 13th Street, NW.,
Suite 1000 South, Washington, DC
20005.
NRC Branch Chief: Richard J. Laufer.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–348 and 50–364,
Joseph M. Farley Nuclear Plant (FNP),
Units 1 and 2, Houston County,
Alabama; Docket Nos. 50–321 and 50–
366, Edwin I. Hatch Nuclear Plant
(HNP), Units 1 and 2, Appling County,
Georgia; and Docket Nos. 50–424 and
50–425, Vogtle Electric Generating Plant
(VEGP), Units 1 and 2, Burke County,
Georgia
Date of amendment request: February
17, 2006.
Description of amendment request:
The proposed amendment would add
Technical Specification (TS) Limiting
Condition for Operation (LCO) 3.0.8
(and renumber existing LCO 3.0.8 to
LCO 3.0.9 for VEGP) to allow a delay
time for entering a supported system TS
when the inoperability is due solely to
an inoperable snubber, if risk is assessed
and managed consistent with the
program in place for complying with the
requirements of 10 CFR 50.65(a)(4).
The NRC staff issued a notice of
availability of a model safety evaluation
and model no significant hazards
consideration (NSHC) determination for
referencing in license amendment
applications in the Federal Register on
November 24, 2004 (69 FR 68412). The
licensee affirmed the applicability of the
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model NSHC determination in its
application dated February 17, 2006.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
The proposed change allows a delay time
for entering a supported system technical
specification (TS) when the inoperability is
due solely to an inoperable snubber if risk is
assessed and managed. The postulated
seismic event requiring snubbers is a lowprobability occurrence and the overall TS
system safety function would still be
available for the vast majority of anticipated
challenges. Therefore, the probability of an
accident previously evaluated is not
significantly increased, if at all. The
consequences of an accident while relying on
allowance provided by proposed LCO 3.0.8
are no different than the consequences of an
accident while relying on the TS required
actions in effect without the allowance
provided by proposed LCO 3.0.8. Therefore,
the consequences of an accident previously
evaluated are not significantly affected by
this change. The addition of a requirement to
assess and manage the risk introduced by this
change will further minimize possible
concerns. Therefore, this change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any previously evaluated?
The proposed change does not involve a
physical alteration of the plant (no new or
different type of equipment will be installed).
Allowing delay times for entering supported
system TS when inoperability is due solely
to inoperable snubbers, if risk is assessed and
managed, will not introduce new failure
modes or effects and will not, in the absence
of other unrelated failures, lead to an
accident whose consequences exceed the
consequences of accidents previously
evaluated. The addition of a requirement to
assess and manage the risk introduced by this
change will further minimize possible
concerns. Thus, this change does not create
the possibility of a new or different kind of
accident from an accident previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
The proposed change allows a delay time
for entering a supported system TS when the
inoperability is due solely to an inoperable
snubber, if risk is assessed and managed. The
postulated seismic event requiring snubbers
is a low-probability occurrence and the
overall TS system safety function would still
be available for the vast majority of
anticipated challenges. The risk impact of the
proposed TS changes was assessed following
the three-tiered approach recommended in
RG 1.177. A bounding risk assessment was
performed to justify the proposed TS
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changes. This application of LCO 3.0.8 is
predicated upon the licensee’s performance
of a risk assessment and the management of
plant risk. The net change to the margin of
safety is insignificant. Therefore, this change
does not involve a significant reduction in a
margin of safety. Based upon the reasoning
presented above and the previous discussion
of the amendment request, the requested
change does not involve a no-significanthazards consideration.
Register on May 6, 2005 (70 FR 24126).
The licensee affirmed the applicability
of the following NSHC determination in
its application dated March 29, 2006.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorneys for licensee: M. Stanford
Blanton, Esq., Balch and Bingham, Post
Office Box 306, 1710 Sixth Avenue
North, Birmingham, Alabama 35201;
Mr. Ernest L. Blake, Jr., Esquire, Shaw,
Pittman, Potts and Trowbridge, 2300 N
Street, NW., Washington, DC 20037; Mr.
Arthur H. Domby, Troutman Sanders,
Nations Bank Plaza, Suite 5200, 600
Peachtree Street, NE., Atlanta, Georgia
30308–2216.
NRC Branch Chief: Evangelos C.
Marinos.
Criterion 1—The Proposed Change Does
Not Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated.
The proposed change requires a SG
Program that includes performance criteria
that will provide reasonable assurance that
the SG tubing will retain integrity over the
full range of operating conditions (including
startup, operation in the power range, hot
standby, cooldown and all anticipated
transients included in the design
specification). The SG performance criteria
are based on tube structural integrity,
accident induced leakage, and operational
LEAKAGE.
A Steam Generator Tube Rupture (SGTR)
event is one of the design basis accidents that
are analyzed as part of a plant’s licensing
basis. In the analysis of a SGTR event, a
bounding primary to secondary LEAKAGE
rate equal to the operational LEAKAGE rate
limits in the licensing basis plus the
LEAKAGE rate associated with a doubleended rupture of a single tube is assumed.
For other design basis accidents such as
Main Steam Line Break (MSLB), rod ejection,
and reactor coolant pump locked rotor the
tubes are assumed to retain their structural
integrity (i.e., they are assumed not to
rupture). These analyses typically assume
that primary to secondary LEAKAGE for all
SGs is 1 gallon per minute or increases to 1
gallon per minute as a result of accident
induced stresses. The accident induced
leakage criterion introduced by the proposed
changes accounts for tubes that may leak
during design basis accidents. The accident
induced leakage criterion limits this leakage
to no more than the value assumed in the
accident analysis.
The SG performance criteria proposed
change to the TSs identifies the standards
against which tube integrity is to be
measured. Meeting the performance criteria
provides reasonable assurance that the SG
tubing will remain capable of fulfilling its
specific safety function of maintaining
reactor coolant pressure boundary integrity
throughout each operating cycle and in the
unlikely event of a design-basis accident. The
performance criteria are only a part of the SG
Program required by the proposed change to
the TSs. The program, defined by NEI 97–06,
Steam Generator Program Guidelines,
includes a framework that incorporates a
balance of prevention, inspection, evaluation,
repair, and leakage monitoring. The proposed
changes do not, therefore, significantly
increase the probability of an accident
previously evaluated.
The consequences of design-basis
accidents are, in part, functions of the DOSE
EQUIVALENT I–131 in the primary coolant
and the primary to secondary LEAKAGE
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–424 and 50–425,
Vogtle Electric Generating Plant, Units 1
and 2, Burke County, Georgia
Date of amendment request: March
29, 2006.
Description of amendment request:
The amendment would revise the
Technical Specifications (TS) to adopt
Nuclear Regulatory Commission (NRC)approved Revision 4 to Technical
Specification Task Force (TSTF)
Standard Technical Specification
Change Traveler, TSTF–449, ‘‘Steam
Generator Tube Integrity.’’ The
proposed amendment includes changes
to the TS definition of Leakage; TS
3.4.13, ‘‘Reactor Coolant System,
Operational Leakage’’; TS 5.5.9, ‘‘Steam
Generator (SG) Tube Surveillance
Program’’; and TS 5.6.10, ‘‘Steam
Generator Tube Inspection Report’’; and
adds TS 3.4.17, ‘‘Steam Generator (SG)
Tube Integrity.’’ The proposed changes
are necessary in order to implement the
guidance for the industry initiative on
NEI (Nuclear Energy Institute) 97–06,
‘‘Steam Generator Program Guidelines.’’
The NRC staff published a notice of
opportunity for comment in the Federal
Register on March 2, 2005 (70 FR
10298), on possible amendments
adopting TSTF–449, including a model
safety evaluation and model no
significant hazards consideration
(NSHC) determination, using the
consolidated line-item improvement
process. The NRC staff subsequently
issued a notice of availability of the
models for referencing in license
amendment applications in the Federal
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rates resulting from an accident. Therefore,
limits are included in the plant technical
specifications for operational leakage and for
DOSE EQUIVALENT I–131 in primary
coolant to ensure the plant is operated within
its analyzed condition. The typical analysis
of the limiting design basis accident assumes
that primary to secondary leak rate after the
accident is 1 gallon per minute with no more
than 500 gallons per day in any one SG, and
that the reactor coolant activity levels of
DOSE EQUIVALENT I–131 are at the TS
values before the accident.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary coolant chemistry controls. The
proposed approach updates the current TSs
and enhances the requirements for SG
inspections. The proposed change does not
adversely impact any other previously
evaluated design basis accident and is an
improvement over the current TSs.
Therefore, the proposed change does not
affect the consequences of a SGTR accident
and the probability of such an accident is
reduced. In addition, the proposed change
does not affect the consequences of an MSLB,
rod ejection, or a reactor coolant pump
locked rotor event, or other previously
evaluated accident.
Criteria 2—The Proposed Change Does Not
Create the Possibility of a New or Different
Kind of Accident From Any Previously
Evaluated.
The proposed performance-based
requirements are an improvement over the
requirements imposed by the current
technical specifications. Implementation of
the proposed SG Program will not introduce
any adverse changes to the plant design basis
or postulated accidents resulting from
potential tube degradation. The result of the
implementation of the SG Program will be an
enhancement of SG tube performance.
Primary to secondary LEAKAGE that may be
experienced during all plant conditions will
be monitored to ensure it remains within
current accident analysis assumptions.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary or secondary coolant chemistry
controls. In addition, the proposed change
does not impact any other plant system or
component. The change enhances SG
inspection requirements.
Therefore, the proposed change does not
create the possibility of a new or different
type of accident from any accident
previously evaluated.
Criterion 3—The Proposed Change Does
Not Involve a Significant Reduction in the
Margin of Safety.
The SG tubes in pressurized water reactors
are an integral part of the reactor coolant
pressure boundary and, as such, are relied
upon to maintain the primary system’s
pressure and inventory. As part of the reactor
coolant pressure boundary, the SG tubes are
unique in that they are also relied upon as
a heat transfer surface between the primary
and secondary systems such that residual
heat can be removed from the primary
system. In addition, the SG tubes isolate the
radioactive fission products in the primary
coolant from the secondary system. In
summary, the safety function of an SG is
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maintained by ensuring the integrity of its
tubes.
Steam generator tube integrity is a function
of the design, environment, and the physical
condition of the tube. The proposed change
does not affect tube design or operating
environment. The proposed change is
expected to result in an improvement in the
tube integrity by implementing the SG
Program to manage SG tube inspection,
assessment, repair, and plugging. The
requirements established by the SG Program
are consistent with those in the applicable
design codes and standards and are an
improvement over the requirements in the
current TSs.
For the above reasons, the margin of safety
is not changed and overall plant safety will
be enhanced by the proposed change to the
TSs.
The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. Arthur H.
Domby, Troutman Sanders,
NationsBank Plaza, Suite 5200, 600
Peachtree Street, NE., Atlanta, Georgia
30308–2216.
NRC Branch Chief: Evangelos C.
Marinos.
Tennessee Valley Authority, Docket No.
50–259, Browns Ferry Nuclear Plant,
Unit 1, Limestone County, Alabama
Date of amendment request: January
6, 2006 (TS–443).
Description of amendment request:
The proposed amendment involves the
activation of thermal-hydraulic stability
monitoring instrumentation and would
allow for the operation of the Oscillating
Power Range Monitor (OPRM) module
in the ‘‘armed’’ mode when the unit
returns to power operations. The OPRM
module of the Power Range Neutron
Monitoring System is designed to
provide the licensee’s solution regarding
reactor stability.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No
Operating in the region of the power-toflow map where instabilities can occur may
cause a slight, but not significant, increase in
the possibility that an instability will occur.
This slight increase is acceptable because the
OPRM Upscale trip function automatically
detects and suppresses design basis thermalhydraulic power oscillations prior to
challenging the fuel MCPR [Minimum
Critical Power Ratio] Safety Limit. Thus, the
proposed changes do not significantly
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increase the probability of an accident
previously evaluated.
Since the OPRM Upscale trip function
precludes challenges to the fuel MCPR Safety
Limit, the proposed changes do not involve
a significant increase in the consequences of
an accident previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No
The proposed changes do not modify the
basic functional requirements of the affected
equipment nor create any new system failure
modes or sequence of events that could lead
to an accident. The worst case failure of the
affected equipment is failure to perform a
mitigation action. Failure of this equipment
to perform a mitigating action does not create
the possibility of a new or different kind of
accident.
No new external threats or release
pathways are created. Therefore, the
proposed changes do not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No
The proposed changes do not revise any
safety margin requirements. The OPRM
Upscale trip function is designed to meet all
requirements of General Design Criteria
(GDC) 10 and 12 by automatically detecting
and suppressing design basis thermalhydraulic power oscillations prior to
challenging the fuel MCPR Safety Limit.
Thus, the new equipment improves the
ability of the equipment to automatically
enforce compliance with margins of safety.
Therefore, the proposed changes do not
involve a reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L.
Marshall, Jr.
Tennessee Valley Authority, Docket No.
50–390, Watts Bar Nuclear Plant, Unit 1,
Rhea County, Tennessee
Date of amendment request: February
24, 2006 (TS–06–02).
Description of amendment request:
The proposed amendment would revise
the Updated Final Safety Analysis
Report (UFSAR) Section 15.5 dose
analysis inputs and results for the steam
generator tube rupture (SGTR) accident.
This analysis is being revised for both
the current steam generators and the
revised primary and secondary side
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mass releases associated with the new
replacement steam generators, which
are scheduled to be installed during the
Unit 1, Cycle 7 Refueling Outage in the
Fall 2006. The analysis for the current
steam generators was revised as a result
of an error identified in the computer
model used to calculate the dose
consequences to the Main Control Room
subsequent to an accident.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The postulated SGTR analysis was revised
to determine the control room operator and
offsite dose due to correction of computer
model input errors and for primary and
secondary side mass releases associated with
the replacement steam generators. The
COROD and Control Room Emergency
Ventilating System (CREVS) computer model
input errors are software issues which affect
analysis results but do not affect operation of
plant systems. Consequently, correction of
these errors does not have an affect on the
probability of occurrence of an accident. The
change in the primary and secondary side
mass releases associated with the
replacement steam generators results in
changes to the input to the current SGTR
accident analysis. The revised analysis
results in an increase the calculated Main
Control Room (MCR) SGTR doses. However,
the changes in primary and secondary side
mass releases and associated release time
sequence does not increase the probability of
an accident previously evaluated.
The COROD and CREVS computer model
input errors and revised primary and
secondary side mass releases associated with
the replacement steam generators will result
in an increase in the calculated MCR preaccident iodine spike thyroid dose; however
the resulting calculated MCR dose does not
exceed 10 CFR 50, Appendix A, General
Design Criteria (GDC) 19, ‘‘Control Room,’’
dose limits as specified in NUREG–0800,
‘‘Standard Review Plan.’’ Other offsite and
MCR doses (gamma, beta, and thyroid)
associated with the SGTR accident for the
current steam generators and the replacement
steam generators either remain the same,
decrease slightly or increase slightly. These
changes are within the ten percent allowable
increase criteria of NEI [Nuclear Energy
Institute] 96–07, Revision 1. These doses
remain within a small fraction of the 10 CFR
100, ‘‘Reactor Site Criteria,’’ and 10 CFR 50
Appendix A, GDC 19 as specified in NUREG–
0800. Consequently, the changes do not
involve a significant increase in the
consequences of an accident previously
evaluated.
Based on the above, the proposed change
does not involve a significant increase in the
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16:59 Apr 24, 2006
Jkt 208001
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The COROD and CREVS computer model
input errors are software issues which affect
analysis results but do not result in new
accident initiators since operation of plant
systems and equipment are not affected.
Thus, these input changes do not create the
possibility of new or different kind of
accident from those previously evaluated.
The change in the primary and secondary
side mass releases associated with the
replacement steam generators result in
changes to the input to the current SGTR
accident analysis. The revised analysis
results in an increase in the calculated MCR
doses. However, the changes in primary and
secondary side mass releases and associated
release time sequence do not create the
possibility of a new or different kind of
accident than previously evaluated.
Based on the above, the changes will not
initiate an accident nor create any new
failure mechanisms. The changes do not
result in any event previously deemed
incredible being made credible. In addition;
the changes will not result in any increase in
the challenges to safety systems. Therefore,
the proposed changes do not create the
possibility of a new or different kind of
accident from any previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes to the affected
UFSAR tables revise the calculation input for
offsite and MCR dose values for the SGTR
accident. The MCR thyroid dose (21 µCi/gm
case) for the current steam generators and the
revised mass releases associated with the
replacement steam generators exceeds the ten
percent allowable increase criteria of NEI 96–
07, Revision 1. Offsite doses for the current
steam generators remain the same and then
decrease slightly for the replacement steam
generators. The MCR gamma and beta doses
(21 µCi/gm case) increase slightly for the
current steam generators and then decrease
slightly for the replacement steam generators.
The MCR gamma, beta and thyroid doses
(0.265 µCi/gm case) increase slightly for the
current steam generators and then decrease
slightly for the revised mass releases
associated with the replacement steam
generators.
The above changes in SGTR accident doses
are acceptable since the MCR doses do not
exceed the requirements in 10 CFR 50,
Appendix A, GDC 19 and the whole body
and thyroid doses at the exclusion area and
the lower population zone outer boundaries
remain the same or decrease relative to the
UFSAR values. Therefore, the proposed
changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
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23963
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902
NRC Branch Chief: Michael L.
Marshall, Jr.
Notice of Issuance of Amendments To
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) The applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
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located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
59084). The supplemental letters
provided clarifying information that was
within the scope of the initial notice
and did not change the initial proposed
no significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 30, 2006.
No significant hazards consideration
comments received: No.
wwhite on PROD1PC65 with NOTICES
Carolina Power & Light Company,
Docket Nos. 50–325 and 50–324,
Brunswick Steam Electric Plant, Units 1
and 2, Brunswick County, North
Carolina
Date of application for amendments:
August 11, 2005, as supplemented by
letters dated October 11, November 16,
and December 12, 2005, and February 7,
2006.
Brief Description of amendments: The
amendments revise Technical
Specification (TS) Surveillance
Requirement 3.6.1.3.9 with respect to
the allowed leakage rate through each
Main Steam Isolation Valve.
Date of issuance: March 2, 2006.
Effective date: March 2, 2006.
Amendment Nos.: 239 and 267.
Facility Operating License Nos. DPR–
71 and DPR–62: Amendments change
the TS.
Date of initial notice in Federal
Register: September 13, 2005 (70 FR
54087). The letters dated October 11,
November 16, and December 12, 2005,
and February 7, 2006, provided
clarifying information that was within
the scope of the initial notice and did
not change the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 2, 2006.
No significant hazards consideration
comments received: No.
Dairyland Power Cooperative, Docket
No. 50–409, La Crosse Boiling Water
Reactor, Genoa, Wisconsin
Date of amendment request:
December 13, 2005.
Brief description of amendment: The
amendment revises Technical
Specifications to allow waste processing
components or fixtures to be handled
over the Fuel Element Storage Well
(FESW), limiting the weight of such
items to 50 tons (the weight of the heavy
load drop found acceptable in the cask
drop analyses performed for the La
Crosse Boiling Water Reactor FESW).
Date of issuance: April 3, 2006.
Effective date: April 3, 2006.
Amendment No.: 70.
Possession Only License No. DPR–45:
The amendment revises the Technical
Specifications.
Date of initial notice in Federal
Register: February 14, 2006 (71 FR
7804).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation Report, dated April 3,
2006.
No significant hazards consideration
comments received: No.
Carolina Power & Light Company, et al.,
Docket No. 50–400, Shearon Harris
Nuclear Power Plant, Unit 1, Wake and
Chatham Counties, North Carolina
Date of application for amendment:
April 6, 2005, as supplemented by
letters dated August 8, and December 9,
2005.
Brief description of amendment: This
amendment revises Technical
Specification (TS) 6.8.4.k, ‘‘Containment
Leakage Rate Testing Program’’ and TS
Surveillance Requirement 4.6.1.6.1,
‘‘Containment Vessel Surfaces.’’
Specifically, the amendment allows a
one-time extension of Appendix J to
Part 50 of Title 10 of the Code of Federal
Regulation, Type A, Containment
Integrated Leak Rate Test interval from
once in 10 years to once in 15 years.
Date of issuance: March 30, 2006.
Effective date: March 30, 2006.
Amendment No.: 122.
Facility Operating License No. NPF–
63: Amendment revises the TS.
Date of initial notice in Federal
Register: October 11, 2005 (70 FR
Entergy Nuclear Operations, Inc.,
Docket No. 50–293, Pilgrim Nuclear
Power Station, Plymouth County,
Massachusetts
Date of application for amendment:
May 24, 2005.
Brief description of amendment: The
amendment revised the applicability
requirements of Technical Specification
3.7.A.5.a. and 3.7.A.i. related to primary
containment oxygen concentration and
drywell-to-suppression chamber
differential pressure limits.
Date of issuance: April 10, 2006.
Effective date: As of the date of
issuance, and shall be implemented
within 60 days.
Amendment No.: 218.
Facility Operating License No. DPR–
35: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: August 30, 2005 (70 FR
51380).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 10, 2006.
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16:59 Apr 24, 2006
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No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket Nos. 50–237 and 50–249,
Dresden Nuclear Power Station, Units 2
and 3, Grundy County, Illinois; Docket
Nos. 50–254 and 50–265, Quad Cities
Nuclear Power Station, Units 1 and 2,
Rock Island County, Illinois
Date of application for amendments:
June 15, 2005, as supplemented by
letters dated January 26, January 31,
February 22, March 3, and March 23,
2006.
Brief description of amendments: The
amendment allows a transition to
Westinghouse SVEA–96 Optima2 fuel at
Dresden Nuclear Power Station (DNPS)
and Quad Cities Nuclear Power Station
(QCNPS) beginning with the QCNPS,
Unit 2 refueling outage in March 2006.
Specifically, the amendment revised
Technical Specifications (TSs) Section
3.1.4, ‘‘Control Rod Scram Times,’’ TS
Section 4.2.1, ‘‘Fuel Assemblies,’’ and
TS Section 5.6.5, ‘‘Core Operating limits
Report (COLR),’’ to support this
transition. Additionally, a new
surveillance requirement was added to
verify sodium pentaborate enrichment.
The core reload analyses using the new
Westinghouse analytical methods for
the affected units may result in the need
for additional TS changes to support the
transition to Westinghouse SVEA–96
Optima2 fuel, such as a change to the
safety limit minimum critical power
ratio.
Date of issuance: April 4, 2006.
Effective date: As of the date of
issuance and shall be implemented
prior to unit startup with a reactor core
containing Westinghouse SVEA–96
Optima2 fuel.
Amendment Nos.: 220/211, 231/227.
Facility Operating License Nos. DPR–
19, DPR–25, DPR–29 and DPR–30. The
amendments revised the Technical
Specifications and Surveillance
Requirements.
Date of initial notice in Federal
Register: July 19, 2005 (70 FR 41445).
The January 26, January 31, February
22, March 3, and March 23, 2006,
supplements, contained clarifying
information and did not change the NRC
staff’s initial proposed finding of no
significant hazards consideration.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 4, 2006.
No significant hazards consideration
comments received: No.
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Exelon Generation Company, LLC,
Docket No. 50–265, Quad Cities Nuclear
Power Station, Unit 2, Rock Island
County, Illinois
Date of application for amendments:
December 15, 2005, as supplemented by
letters dated February 13 and March 3,
2006.
Brief description of amendments: The
amendment revised the safety limit
minimum critical power ratio values in
Technical Specification (TS) Section
2.1.1, ‘‘Reactor Core SLs.’’ Specifically,
the change required that for Quad Cities,
Unit 2, the minimum critical power
ratio (MCPR) for Global Nuclear Fuel
fuel shall be ≥ 1.09 for two recirculation
loop operation or ≥ 1.10 for single
recirculation loop operation.
Additionally, the change required that
the MCPR for Westinghouse fuel shall
be ≥ 1.11 for two recirculation loop
operation or ≥ 1.13 for single loop
operation.
Date of issuance: March 31, 2006.
Effective date: As of the date of
issuance and shall be implemented
prior to unit startup with a reactor core
containing Westinghouse Optima2 fuel.
Amendment No.: 226.
Facility Operating License No. DPR–
30: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: January 17, 2006 (71 FR
2591).
The February 13, 2006, and March 3,
2006, supplements, contained clarifying
information and did not change the NRC
staff’s initial proposed finding of no
significant hazards consideration.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 31, 2006.
No significant hazards consideration
comments received: No.
wwhite on PROD1PC65 with NOTICES
Florida Power and Light Company, et
al., Docket No. 50–389, St. Lucie Plant,
Unit No. 2, St. Lucie County, Florida
Date of application for amendment:
November 8, 2004, as supplemented
March 31, 2005, and February 13, 2006.
Brief description of amendment: The
amendment revises Technical
Specification (TS) Section 4.4.5.4 to
modify the definitions of steam
generator tube ‘‘Plugging Limit’’ and
‘‘Tube Inspection.’’ The purpose of
these modifications is to define the
depth of the required tube inspections
and to clarify the plugging criteria
within the tubesheet region. The
amendment also modifies TS Section
4.4.5.5, ‘‘Reports,’’ to require a Special
Report of indications found in the
tubesheet region following each
inspection.
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16:59 Apr 24, 2006
Jkt 208001
Date of Issuance: April 11, 2006.
Effective Date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment No.: 143.
Renewed Facility Operating License
No. NPF–16: Amendment revised the
TS.
Date of initial notice in Federal
Register: November 24, 2004 (69 FR
68404).
The March 31, 2005, and February 13,
2006, Supplements did not affect the
original proposed no significant hazards
determination, or expand the scope of
the request as noticed in the Federal
Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 11, 2006.
No significant hazards consideration
comments received: No.
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request: April 13,
2005, as supplemented by letter dated
September 29, 2005.
Brief description of amendment: The
amendment incorporated several
Technical Specification Task Force
(TSTF) changes to the licensee’s
Technical Specifications (TSs). The
specific TSTF changes that were
incorporated are:
1. TSTF–222–A, Revision 1, ‘‘Control
Rod Scram Time Testing’’—This change
modifies TS Section 3.1.4, ‘‘Control Rod
Scram Times,’’ to clarify that control rod
scram time testing is required only for
core cells in which work on the control
rod or drive has been performed or fuel
has been moved or replaced.
2. TSTF–275–A, Revision 0, ‘‘Clarify
Requirement for EDG [emergency diesel
generator] start signal on RPV [reactor
pressure vessel] Level—Low, Low, Low
during RPV cavity flood-up’’—This
change modifies the TS Section 3.3.5.1,
‘‘ECCS [emergency core cooling system]
Instrumentation,’’ to clarify that the
ECCS initiation instrumentation,
identified as being required in modes 4
and 5, is required to be operable only
when the associated ECCS subsystems
are required to be operable as defined in
limiting condition of operation (LCO)
3.5.2, ‘‘ECCS—Shutdown.’’
3. TSTF–300–A, Revision 0,
‘‘Eliminate DG [diesel generator] LOCA
[loss-of-coolant accident]-Start SRs
[surveillance requirements] while in S/
D [shutdown] when no ECCS is
Required’’—This change modifies the
TS Section 3.8.2, ‘‘AC [alternating
current] Sources—Shutdown,’’ to add
an additional note to the surveillance
that verifies automatic start of the
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23965
emergency diesel generators and
automatic load shedding from the
emergency buses, is considered to be
met without the ECCS initiation signals
operable when ECCS initiation signals
are not required to be operable per Table
3.3.5.1–1, ECCS Instrumentation.
4. TSTF–225, Revision 2, ‘‘Fuel
movement with inoperable refueling
equipment interlocks’’—This change
modifies TS Section 3.9.1, ‘‘Refueling
Equipment Interlocks,’’ to add required
actions to allow insertion of a control
rod withdrawal block and verification
that all control rods are fully inserted as
alternate actions to suspending in-vessel
fuel movement in the event that one or
more required refueling equipment
interlocks are inoperable.
Date of issuance: March 30, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment No.: 218.
Facility Operating License No. DPR–
46: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: June 7, 2005 (70 FR 33216).
The supplement dated September 29,
2005, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 30, 2006.
No significant hazards consideration
comments received: No.
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1, Washington County, Nebraska
Date of amendment request:
November 8, 2005, as supplemented by
letters dated March 17 and 27, 2006.
Brief description of amendment: The
amendment adds limits and controls for
the spent fuel cask loading and
unloading operations in the spent fuel
pool (SFP). The change modifies the
technical specifications (TSs) by adding
a new Limiting Condition for Operation
(LCO) 2.8.3(6) that establishes (1) A
boron concentration requirement during
cask loading operations in the SFP, and
(2) a spent fuel burnup-initial
enrichment limit in the spent fuel cask
to ensure subcritical conditions are
maintained during spent fuel cask
loading operations in the SFP. In
addition, the change modifies TS Tables
3–4 and 3–5, and adds a new subsection
4.3.1.3 in Design Features 4.3.1 to
describe the spent fuel cask design
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features. In addition, editorial changes
were made mostly to make the TSs
consistent with the proposed changes
and to conform pagination.
Date of issuance: April 10, 2006.
Effective date: The license
amendment is effective as of its date of
issuance.
Amendment No.: 239.
Renewed Facility Operating License
No. DPR–40: The amendment revised
the Technical Specifications.
Date of initial notice in Federal
Register: December 20, 2005 (70 FR
75494).
The March 17 and 27, 2006,
supplemental letters provided
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination. The
Commission’s related evaluation of the
amendment is contained in a safety
evaluation dated April 10, 2006.
No significant hazards consideration
comments received: No.
wwhite on PROD1PC65 with NOTICES
PPL Susquehanna, LLC, Docket No. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1
and 2), Luzerne County, Pennsylvania
Date of application for amendments:
October 5, 2005.
Brief description of amendments: The
amendments change the SSES 1 and 2
Technical Specifications (TSs) 3.4.10,
‘‘RCS [Reactor Coolant System] Pressure
and Temperature (P/T) Limits,’’ by
removing the valid P/T curve limit date
and replacing it with the effective fullpower years (EFPY) of radiation
exposure on each of the P/T limit curves
for SSES 1 and 2. The new P/T limit
will be 35.7 EFPY for SSES 1 and 30.2
EFPY for SSES 2.
Date of issuance: March 30, 2006.
Effective date: As of the date of
issuance and to be implemented within
30 days.
Amendment Nos.: 232 and 209.
Facility Operating License Nos. NPF–
14 and NPF–22: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: January 17, 2006 (71 FR
2595).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 30, 2006.
No significant hazards consideration
comments received: No.
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Jkt 208001
PPL Susquehanna, LLC, Docket Nos. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2, Luzerne
County, Pennsylvania
Date of application for amendments:
October 5, 2005, as supplemented on
March 31, 2006.
Brief description of amendments:
These amendments revise the Technical
Specifications by eliminating the
requirements to submit monthly
operating reports and occupational
radiation exposure reports.
Date of issuance: April 6, 2006.
Effective date: April 6, 2006.
Amendment Nos.: 233 and 210.
Facility Operating License Nos. NPF–
14 and NPF–22: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: January 3, 2006 (71 FR 153).
The supplement dated March 31,
2006, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 6, 2006.
No significant hazards consideration
comments received: No.
PPL Susquehanna, LLC, Docket Nos. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2, Luzerne
County, Pennsylvania
Date of application for amendments:
October 5, 2005, as supplemented on
March 31, 2006.
Brief description of amendments:
These amendments revise the Technical
Specifications by eliminating the
requirements associated with hydrogen
recombiners, and hydrogen and oxygen
monitors.
Date of issuance: April 6, 2006.
Effective date: As of the date of
issuance and to be implemented within
60 days of the date of issuance.
Amendment Nos.: 234 and 211.
Facility Operating License Nos. NPF–
14 and NPF 22: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: January 3, 2006 (71 FR 152).
The supplement dated March 31,
2006, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 6, 2006.
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No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket No. 50–354,
Hope Creek Generating Station, Salem
County, New Jersey
Date of application for amendment:
October 11, 2005.
Brief description of amendment: The
amendment revises certain 18-month
Technical Specification (TS)
surveillance requirements to eliminate
the condition that testing be conducted
during shutdown conditions.
Date of issuance: April 4, 2006.
Effective date: As of the date of
issuance, to be implemented within 60
days.
Amendment No.: 165.
Facility Operating License No. NPF–
57: This amendment revised the TSs.
Date of initial notice in Federal
Register: January 17, 2006 (71 FR
2593).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 4, 2006.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket No. 50–354,
Hope Creek Generating Station, Salem
County, New Jersey
Date of application for amendment:
October 11, 2005.
Brief description of amendment: The
amendment removes the Technical
Specification (TS) 3.1.5 requirement for
the standby liquid control (SLC) system
to be operable in Operational Condition
5 (refueling) with any control rod
withdrawn. Corresponding changes are
also made to the SLC initiation sections
of TS Tables 3.3.2–1 and 4.3.2–1.
Date of issuance: April 7, 2006.
Effective date: As of the date of
issuance, to be implemented within 60
days.
Amendment No.: 166.
Facility Operating License No. NPF–
57: This amendment revised the TSs.
Date of initial notice in Federal
Register: January 31, 2006 (71 FR
5083).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 7, 2006.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket No. 50–354,
Hope Creek Generating Station, Salem
County, New Jersey
Date of application for amendment:
October 11, 2005.
Brief description of amendment: The
amendment changes the Technical
Specifications (TSs) to relocate the
component identification of the
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overcurrent protective devices from TS
3/4.8.4.1 and TS 3/4.8.4.5 to the
Updated Final Safety Analysis Report.
Date of issuance: April 10, 2006.
Effective date: As of the date of
issuance, to be implemented within 60
days.
Amendment No.: 167.
Facility Operating License No. NPF–
57: The amendment revised the TSs.
Date of initial notice in Federal
Register: March 6, 2006 (71 FR 11233).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 10, 2006.
No significant hazards consideration
comments received: No.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–348 and 50–364,
Joseph M. Farley Nuclear Plant, Units 1
and 2, Houston County, Alabama
Date of amendments request:
September 27, 2005.
Brief Description of amendments: The
amendments revise the Technical
Specifications to eliminate the power
range neutron high-flux negative rate
reactor trip function.
Date of issuance: February 27, 2006.
Effective date: As of the date of
issuance and shall be implemented
prior to startup following refueling
outage 21 for Unit 1 and prior to startup
following refueling outage 18 for Unit 2.
Amendment Nos.: 171 and 164.
Renewed Facility Operating License
Nos. NPF–2 and NPF–8: Amendments
revise the Technical Specifications.
Date of initial notice in Federal
Register: November 8, 2005 (70 FR
67750).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated February 27,
2006.
No significant hazards consideration
comments received: No.
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STP Nuclear Operating Company,
Docket Nos. 50–498 and 50–499, South
Texas Project, Units 1 and 2, Matagorda
County, Texas
Date of amendment request: August
30, 2005.
Brief description of amendments: The
amendments revise Technical
Specifications to reflect incorporation of
the Westinghouse Electric Company
Best Estimate Analyzer for Core
Operations—Nuclear power distribution
monitoring as described in Topical
Report WCAP–124–P–A, ‘‘BEACON—
Core Monitoring and Operations
Support System.’’
Date of issuance: March 31, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 90 days of issuance.
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Amendment Nos.: Unit 1–175; Unit
2–163.
Facility Operating License Nos. NPF–
76 and NPF–80: The amendments
revised the Technical Specifications and
Surveillance Requirements.
Date of initial notice in Federal
Register: October 11, 2005 (70 FR
59088).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 31, 2006.
No significant hazards consideration
comments received: No.
STP Nuclear Operating Company,
Docket Nos. 50–498 and 50–499, South
Texas Project, Units 1 and 2, Matagorda
County, Texas
Date of amendment request: August
30, 2005.
Brief description of amendments: The
amendments revise Technical
Specifications to reflect incorporation of
the Westinghouse Electric Company
Best Estimate Analyzer for Core
Operations—Nuclear power distribution
monitoring as described in Topical
Report WCAP–124–P–A, ‘‘BEACON—
Core Monitoring and Operations
Support System.’’
Date of issuance: March 31, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 90 days of issuance.
Amendment Nos.: Unit 1–175; Unit
2–163.
Facility Operating License Nos. NPF–
76 and NPF–80: The amendments
revised the Technical Specifications and
Surveillance Requirements.
Date of initial notice in Federal
Register: October 11, 2005 (70 FR
59088).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 31, 2006.
No significant hazards consideration
comments received: No.
Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton
County, Tennessee
Date of application for amendments:
September 1, 2005, as supplemented by
letters dated March 16 and 30, 2006.
Brief description of amendments: The
amendments temporarily revise the
reactor protection system turbine trip
allowable value for low trip system
pressure from greater than or equal to 43
pounds per square inch gauge (psig) to
39.5 psig for Operating Cycle 15.
The amendments revise Technical
Specification 2.2.1, Functional Unit
17.A allowable value in Table 2.2–1
‘‘Reactor Trip System Instrumentation
Setpoints.’’
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23967
Date of issuance: April 6, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 45 days.
Amendment Nos. 307 and 296.
Facility Operating License Nos. DPR–
77 and DPR–79: Amendments revised
the technical specifications.
Date of initial notice in Federal
Register: October 25, 2005 (70 FR
61662). The supplemental letters
provided clarifying information that did
not change the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 6, 2006.
No significant hazards consideration
comments received: No.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Unit Nos.
1 and 2, Somervell County, Texas
Date of amendment request: April 13,
2004, as supplemented by letters dated
March 18 and August 31, 2005, and
January 6, 2006.
Description of amendment: The
amendments revise the Technical
Specification (TS) 3.3.2, ‘‘Engineered
Safety Features Actuation System
Instrumentation, ‘‘ Function 7.b,
‘‘Refueling Water Storage Tank Level—
Low Low’’ trip setpoint, and revise the
frequency of calibration of the level
transmitters from every 9 months to
every 18 months.
Date of issuance: March 30, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment Nos.: 125 and 125.
Facility Operating License Nos. NPF–
87 and NPF–89: The amendments
revised the Technical Specifications and
Surveillance Requirements.
Date of initial notice in Federal
Register: May 11, 2004 (69 FR 26193).
The March 18 and August 31, 2005, and
January 6, 2006, supplemental letters
provided additional information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the staff’s
original proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 30, 2006.
No significant hazards consideration
comments received: No.
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23968
Federal Register / Vol. 71, No. 79 / Tuesday, April 25, 2006 / Notices
Notice of Issuance of Amendments to
Facility Operating Licenses and Final
Determination of No Significant
Hazards Consideration and
Opportunity for a Hearing (Exigent
Public Announcement or Emergency
Circumstances)
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application for the
amendment complies with the
standards and requirements of the
Atomic Energy Act of 1954, as amended
(the Act), and the Commission’s rules
and regulations. The Commission has
made appropriate findings as required
by the Act and the Commission’s rules
and regulations in 10 CFR Chapter I,
which are set forth in the license
amendment.
Because of exigent or emergency
circumstances associated with the date
the amendment was needed, there was
not time for the Commission to publish,
for public comment before issuance, its
usual Notice of Consideration of
Issuance of Amendment, Proposed No
Significant Hazards Consideration
Determination, and Opportunity for a
Hearing.
For exigent circumstances, the
Commission has either issued a Federal
Register notice providing opportunity
for public comment or has used local
media to provide notice to the public in
the area surrounding a licensee’s facility
of the licensee’s application and of the
Commission’s proposed determination
of no significant hazards consideration.
The Commission has provided a
reasonable opportunity for the public to
comment, using its best efforts to make
available to the public means of
communication for the public to
respond quickly, and in the case of
telephone comments, the comments
have been recorded or transcribed as
appropriate and the licensee has been
informed of the public comments.
In circumstances where failure to act
in a timely way would have resulted, for
example, in derating or shutdown of a
nuclear power plant or in prevention of
either resumption of operation or of
increase in power output up to the
plant’s licensed power level, the
Commission may not have had an
opportunity to provide for public
comment on its no significant hazards
consideration determination. In such
case, the license amendment has been
issued without opportunity for
comment. If there has been some time
for public comment but less than 30
days, the Commission may provide an
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16:59 Apr 24, 2006
Jkt 208001
opportunity for public comment. If
comments have been requested, it is so
stated. In either event, the State has
been consulted by telephone whenever
possible.
Under its regulations, the Commission
may issue and make an amendment
immediately effective, notwithstanding
the pendency before it of a request for
a hearing from any person, in advance
of the holding and completion of any
required hearing, where it has
determined that no significant hazards
consideration is involved.
The Commission has applied the
standards of 10 CFR 50.92 and has made
a final determination that the
amendment involves no significant
hazards consideration. The basis for this
determination is contained in the
documents related to this action.
Accordingly, the amendments have
been issued and made effective as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) The application for
amendment, (2) the amendment to
Facility Operating License, and (3) the
Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment, as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
The Commission is also offering an
opportunity for a hearing with respect to
the issuance of the amendment. Within
60 days after the date of publication of
this notice, the licensee may file a
request for a hearing with respect to
PO 00000
Frm 00075
Fmt 4703
Sfmt 4703
issuance of the amendment to the
subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland,
and electronically on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If there
are problems in accessing the document,
contact the PDR Reference staff at 1
(800) 397–4209, (301) 415–4737, or by email to pdr@nrc.gov. If a request for a
hearing or petition for leave to intervene
is filed by the above date, the
Commission or a presiding officer
designated by the Commission or by the
Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also identify the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
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opinion which support the contention
and on which the petitioner intends to
rely in proving the contention at the
hearing. The petitioner must also
provide references to those specific
sources and documents of which the
petitioner is aware and on which the
petitioner intends to rely to establish
those facts or expert opinion. The
petition must include sufficient
information to show that a genuine
dispute exists with the applicant on a
material issue of law or fact.1
Contentions shall be limited to matters
within the scope of the amendment
under consideration. The contention
must be one which, if proven, would
entitle the petitioner to relief. A
petitioner/requestor who fails to satisfy
these requirements with respect to at
least one contention will not be
permitted to participate as a party.
Each contention shall be given a
separate numeric or alpha designation
within one of the following groups:
1. Technical—primarily concerns/
issues relating to technical and/or
health and safety matters discussed or
referenced in the applications.
2. Environmental—primarily
concerns/issues relating to matters
discussed or referenced in the
environmental analysis for the
applications.
3. Miscellaneous—does not fall into
one of the categories outlined above.
As specified in 10 CFR 2.309, if two
or more petitioners/requestors seek to
co-sponsor a contention, the petitioners/
requestors shall jointly designate a
representative who shall have the
authority to act for the petitioners/
requestors with respect to that
contention. If a petitioner/requestor
seeks to adopt the contention of another
sponsoring petitioner/requestor, the
petitioner/requestor who seeks to adopt
the contention must either agree that the
sponsoring petitioner/requestor shall act
as the representative with respect to that
contention, or jointly designate with the
sponsoring petitioner/requestor a
representative who shall have the
authority to act for the petitioners/
requestors with respect to that
contention.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing. Since the Commission has
1 To the extent that the applications contain
attachments and supporting documents that are not
publicly available because they are asserted to
contain safeguards or proprietary information,
petitioners desiring access to this information
should contact the applicant or applicant’s counsel
and discuss the need for a protective order.
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16:59 Apr 24, 2006
Jkt 208001
made a final determination that the
amendment involves no significant
hazards consideration, if a hearing is
requested, it will not stay the
effectiveness of the amendment. Any
hearing held would take place while the
amendment is in effect.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) e-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer or
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
AmerGen Energy Company, Docket No.
50–289, Three Mile Island, Unit 1,
Dauphin County, Pennsylvania
Date of amendment request: April 6,
2006.
Description of amendment request:
The amendment revised Technical
Specification (TS) 3.7.2.c, ‘‘Unit Electric
Power System,’’ to increase the TS
allowed outage time with one
inoperable emergency diesel generator
EDG–Y–1A from 7 days to 10 days, on
a one-time basis.
Date of issuance: April 8, 2006.
Effective date: As of the date of
issuance and is applicable until the
emergency diesel generator EG–Y–1A is
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23969
returned to operable status or until
April 12, 2006, at 21:00 hours,
whichever occurs first.
Amendment No.: 258.
Facility Operating License No. DPR–
50: The amendment revised the TSs.
Public comments requested as to
proposed no significant hazards
consideration (NSHC): No. The
Commission’s related evaluation of the
amendment, finding of emergency
circumstances, State consultation, and
final NSHC determination are contained
in a safety evaluation dated April 8,
2006.
Attorney for licensee: Assistant
General Counsel, AmerGen Energy
Company, LLC 200 Exelon Way,
Kennett Square, PA 19348.
NRC Branch Chief: Darrell J. Roberts.
Arizona Public Service Company, et al.,
Docket No. STN 50–528, Palo Verde
Nuclear Generating Station, Unit No. 1,
Maricopa County, Arizona
Date of application for amendment:
March 31, 2006, as supplemented by
letters dated March 31 and April 4,
2006.
Brief description of amendment: The
amendment to the Updated Final Safety
Analysis Report allows the use of an
operator action as a compensatory
measure to prevent exceeding the Train
A shutdown cooling (SDC) system
design basis vibration limit if a Loop 2
reactor coolant pump (RCP) should trip
or have a sheared shaft during four-RCP
operation. This compensatory measure
would only be used during a one-time
12-hour period for root cause data
collection in Mode 3. After the root
cause data collection is completed, a
modification will be implemented to
reduce the SDC system vibration.
Date of issuance: April 6, 2006.
Effective date: April 6, 2006, and shall
be implemented within 5 days of the
date of issuance.
Amendment No.: Unit 1–159.
Facility Operating License No. NPF–
41: The amendment revises the Updated
Final Safety Analysis Report as set forth
in the application for amendment by
licensee letter dated March 31, 2006, as
supplemented.
Public comments requested as to
proposed no significant hazards
consideration (NSHC): Yes. A public
notice was published in the April 3 and
4, 2006, editions of the Arizona
Republic. The notice provided an
opportunity to submit comments on the
Commission’s proposed NSHC
determination. No comments have been
received. The Commission’s related
evaluation of the amendment, finding of
exigent circumstances, state
consultation, and final NSHC
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Federal Register / Vol. 71, No. 79 / Tuesday, April 25, 2006 / Notices
determination are contained in a safety
evaluation dated April 6, 2006. The
March 31 and April 4, 2006,
supplemental letters provided
additional clarifying information, did
not expand the scope of the application
as originally noticed, and did not
change the NRC staff’s original proposed
no significant hazards consideration
determination.
Attorney for licensee: Kenneth C.
Manne, Senior Attorney, Arizona Public
Service Company, P.O. Box 52034, Mail
Station 7636, Phoenix, Arizona 85072–
2034.
NRC Branch Chief: David Terao.
Description of amendment request:
The amendment revised TS 3.7.6,
‘‘Condensate Storage Tank (CST),’’ to
require two CSTs to be OPERABLE and
to increase the combined safety-related
minimum volume. The amendment also
revised Surveillance Requirement 3.7.6
to reflect the additional limit for CST
volume. This amendment is needed to
resume power operation at the Vogtle
Electric Generating Plant, Unit 2.
Date of issuance: March 31, 2006.
Effective date: As of the date of
issuance, and shall be implemented
within 30 days.
Amendment No.: 120.
Facility Operating License No. NPF–
81: Amendment revises the technical
specifications.
Public comments requested as to
proposed no significant hazards
consideration (NSHC): No. The
Commission’s related evaluation of the
amendment, finding of emergency
circumstances, State consultation, and
final NSHC determination are contained
in a safety evaluation dated March 31,
2006.
Attorney for licensee: Mr. Arthur H.
Domby, Troutman Sanders,
NationsBank Plaza, Suite 5200, 600
Peachtree Street, NE., Atlanta, Georgia
30308–2216.
NRC Branch Chief: Evangelos C.
Marinos.
5. Personnel Matters and
Compensation Issues.
Wednesday, May 3, at 8:30 a.m. (Open)
1. Minutes of the Previous Meetings,
February 7–8; and March 22–23, 2006.
2. Remarks of the Postmaster General
and CEO Jack Potter.
3. Committee Reports and Committee
Charters.
4. Capital Investments.
a. Automated Flat Sorting Machine
100—Auto Induction Phase 2.
b. Additional Delivery Barcode
Sorter Equipment.
c. Oklahoma City, Oklahoma,
Regional Distribution Center.
5. Quarterly Report on Service
Performance.
6. Quarterly Report on Financial
Performance.
7. 2006 Privacy Trust Study of the
U.S. Government.
8. Tentative Agenda for the June 6–7,
2006 meeting in Indianapolis, Indiana.
wwhite on PROD1PC65 with NOTICES
Florida Power and Light, et al., Docket
No. 50–389, St. Lucie Nuclear Plant,
Unit 2, St. Lucie County, Florida
Date of amendment request: February
21, 2006.
Description of amendment request:
The amendment revises the Technical
Specifications (TSs) for the Containment
Ventilation System to allow additional
corrective actions for inoperable
containment purge supply and exhaust
valves. These corrective actions are
consistent with the Standard TSs for
Combustion Engineering plants.
Date of issuance: March 17, 2006.
Effective date: March 17, 2006.
Amendment No.: 142.
Facility Operating License No. NPF–
16: Amendment revises the TSs.
Public comments requested as to
proposed no significant hazards
consideration (NSHC): Yes. 71 FR 10566
dated March 1, 2006. The notice
provided an opportunity to submit
comments on the Commission’s
proposed NSHC determination. No
comments have been received. The
notice also provided an opportunity to
request a hearing by May 1, 2006, but
indicated that if the Commission makes
a final NSHC determination, any such
hearing would take place after issuance
of the amendment.
The Commission’s related evaluation
of the amendment, finding of exigent
circumstances, state consultation, and
final NSHC determination are contained
in a safety evaluation dated March 17,
2006.
Attorney for licensee: M.S. Ross,
Managing Attorney, Florida Power &
Light Company, P.O. Box 14000, Juno
Beach, FL 33408–0420.
NRC Branch Chief: Michael L.
Marshall, Jr.
Dated at Rockville, Maryland, this 17th day
of April 2006.
For the Nuclear Regulatory Commission.
Catherine Haney,
Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. 06–3901 Filed 4–24–06; 8:45 am]
Wendy A. Hocking,
Secretary.
[FR Doc. 06–3950 Filed 4–21–06; 3:32 pm]
BILLING CODE 7590–01–P
Actuarial Advisory Committee With
Respect to the Railroad Retirement
Account; Notice of Public Meeting
Southern Nuclear Operating Company,
Inc., Docket No. 50–425, Vogtle Electric
Generating Plant, Unit 2, Burke County,
Georgia
Tuesday, May 2, at 10:30 a.m. (Closed)
POSTAL SERVICE
Board of Governors; Sunshine Act
Meeting
10:30 a.m., Tuesday,
May 2, 2006; 8:30 a.m. and 10 a.m.,
Wednesday, May 3, 2006.
PLACE: Washington, DC, at U.S. Postal
Service Headquarters, 475 L’Enfant
Plaza, SW., in the Benjamin Franklin
Room.
STATUS: May 2, 10:30 a.m. (Closed); May
3, 8:30 a.m. (Open); May 3, 10 a.m.
(Closed).
MATTERS TO BE CONSIDERED:
TIMES AND DATES:
Date of amendment request: March
29, 2006.
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1. Strategic Planning.
2. Financial Update.
3. Rate Case Planning.
4. Labor Negotiations Planning.
Frm 00077
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Wednesday, May 3 at 10 a.m.
(Closed)—(If Needed)
1. Continuation of Tuesday’s closed
session agenda.
FOR FURTHER INFORMATION CONTACT:
Wendy A. Hocking, Secretary of the
Board, U.S. Postal Service, 475 L’Enfant
Plaza, SW., Washington, DC 20260–
1000. Telephone (202) 268–4800.
BILLING CODE 7710–12–M
RAILROAD RETIREMENT BOARD
Notice is hereby given in accordance
with Public Law 92–463 that the
Actuarial Advisory Committee will hold
a meeting on May 24, 2006, at 10 a.m.
at the office of the Chief Actuary of the
U.S. Railroad Retirement Board, 844
North Rush Street, Chicago, Illinois, on
the conduct of the 23rd Actuarial
Valuation of the Railroad Retirement
System. The agenda for this meeting
will include a discussion of the results
and presentation of the 23rd Actuarial
Valuation. The text and tables which
constitute the Valuation will have
prepared in draft form for review by the
Committee. It is expected that this will
be the last meeting of the Committee
before publication of the Valuation.
The meeting will be open to the
public. Persons wishing to submit
written statements or make oral
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Agencies
[Federal Register Volume 71, Number 79 (Tuesday, April 25, 2006)]
[Notices]
[Pages 23952-23970]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: 06-3901]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding
[[Page 23953]]
the pendency before the Commission of a request for a hearing from any
person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from March 31, 2006 to April 13, 2006. The last
biweekly notice was published on April 11, 2006 (71 FR 18371).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
Involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The
filing of requests for a hearing and petitions for leave to intervene
is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide
[[Page 23954]]
when the hearing is held. If the final determination is that the
amendment request involves no significant hazards consideration, the
Commission may issue the amendment and make it immediately effective,
notwithstanding the request for a hearing. Any hearing held would take
place after issuance of the amendment. If the final determination is
that the amendment request involves a significant hazards
consideration, any hearing held would take place before the issuance of
any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland, 20852, Attention: Rulemaking and
Adjudications Staff; (3) e-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
Dominion Energy Kewaunee, Inc., Docket No. 50-305, Kewaunee Power
Station, Kewaunee County, Wisconsin
Date of amendment request: March 17, 2006.
Description of amendment request: The proposed amendment would
change the design criteria described in the Kewaunee Power Station
(KPS) Updated Safety Analysis Report (USAR). The change would add new
design criteria associated with internal flooding to the current
licensing basis for KPS.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change provides clarification to the existing
functional requirements in the USAR by including specific design
criteria for analyzing internal flooding in order to verify the
capability of an SSC [structure, systems and components] to perform
its design function. The proposed change does not affect any of the
previously evaluated accidents in the KPS updated safety analysis
report (USAR). No SSCs, operating procedures, or administrative
controls that have the function of preventing or mitigating any of
these accidents are affected.
This proposed change to incorporate design criteria into the
USAR provides added administrative assurance that internal flooding
will be appropriately addressed, consistent with existing functional
requirements, and that safety related SSCs will not be affected by a
potential failure of a non-safety related SSC. The change does not
affect any accident initiators or the facility accident analysis.
Thus, the probability and the consequences of an accident remain
unchanged.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed change to incorporate design criteria consistent
with existing functional requirements into the USAR does not change
the design function or operation of any safety related SSCs. The
proposed change documents design criteria in use and therefore does
not involve a physical change to the facility. The change,
therefore, does not create the possibility of a new or different
kind of accident due to credible new failure mechanisms,
malfunctions, or accident initiators not considered in the design
and licensing bases.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
This proposed change does not affect any margin of safety as
established in the Kewaunee USAR because it documents the design
criteria presently used and is consistent with the functional
requirements in the USAR. This proposed change provides added
administrative assurance that safety related SSCs will not be
affected by a potential failure of a non-safety related SSC due to a
postulated internal flooding event. The proposed change adds
criteria for the evaluation of internal flooding events that are
more detailed than the existing functional requirements in the USAR.
Therefore, the protection and subsequent availability of safety
related SSCs is maintained consistent with previously assumed
accident mitigation capabilities.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner,
P.O. Box 1497, Madison, WI 53701-1497.
NRC Branch Chief: L. Raghavan.
Exelon Generation Company, LLC, Docket Nos. STN 50-454 and STN 50-455,
Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois; Docket Nos.
STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will
County, Illinois
Date of amendment request: January 12, 2006.
Description of amendment request: The proposed amendment would
correctly modify the wording in Technical Specification Surveillance
Requirement (SR) 3.6.6.3 Containment Cooling train cooling water flow
rate to accurately reflect the plant configuration. The current SR is
to verify flow to each train. The proposed revision to SR 3.6.6.3 would
verify flow to each cooler (plant configuration is two coolers per
train).
Basis for proposed no significant hazards consideration
determination:
[[Page 23955]]
As required by 10 CFR 50.91(a), the licensee has provided its analysis
of the issue of no significant hazards consideration, which is
presented below:
1. The proposed TS change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
The proposed change will revise Technical Specifications (TS)
Surveillance Requirement (SR) 3.6.6.3 containment cooling train
cooling water flow rate to accurately reflect the existing plant
configuration as described in the Updated Final Safety Analysis
Report (UFSAR) Sections 6.2, ``Containment Systems,'' and 9.4, ``Air
Conditioning, Heating, Cooling, and Ventilation Systems.'' The
revision will specify the appropriate testing requirements for
verification that each Containment Cooling System train Essential
Service Water (SX) flow rate to each cooling unit is >= 2660 gpm
[gallons per minute] and will therefore provide assurance that the
design flow rate assumed in the safety analyses will be achieved and
the Limited Conditions for Operation (LCO) will be met. This change
is in the conservative direction, i.e., verification of flow rate to
each cooling unit 3 2660 gpm is more conservative than
verification of the same flow rate to each cooling train that
consists of two cooling units. The performance of TS surveillance
testing is not a precursor to any accident previously evaluated.
Thus, the proposed change does not have any effect on the
probability of an accident previously evaluated.
The function of the Containment Cooling System in conjunction
with the Containment Spray System is to provide containment
atmosphere cooling to limit post accident pressure and temperature
in containment to less than design values. There is no change to the
design of the Containment Cooling System. Furthermore, the
surveillance testing specified in SR 3.6.6.3 will provide assurance
that the Containment Cooling System will perform as designed. Thus,
the radiological consequences of any accident previously evaluated
are not increased.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. The proposed TS change does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
The proposed change does not affect the control parameters
governing unit operation or the response of plant equipment to
transient conditions. The proposed change does not change or
introduce any new equipment, modes of system operation or failure
mechanisms.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. The proposed TS change does not involve a significant
reduction in a margin of safety.
Prior to conversion to ITS [Improved Technical Specifications],
the SR equivalent to SR 3.6.6.3 required that each system of
containment cooling fans be demonstrated OPERABLE by ``verifying an
essential service water flow rate of greater than or equal to 2660
gpm to each cooler.'' During the ITS conversion, standard verbiage
for SR 3.6.6.3 was adopted; however, the specific plant design of
two Reactor Containment Fan Coolers (RCFCs) per Containment Cooling
train was inadvertently overlooked.
This proposed amendment would correctly modify the wording in
Technical Specifications (TS) Surveillance Requirement (SR) 3.6.6.3
Containment Cooling System to accurately reflect the Braidwood and
Byron existing plant design. The revision will provide the
appropriate testing requirements for verification that each
Containment Cooling System train SX cooling flow rate to each
cooling unit is >= 2660 gpm. This verification provides assurance
that the design flow rate assumed in the safety analyses will be
achieved; and, therefore the LCO will be met. The change for
verification of SX cooling flow rate from each cooling train to each
cooling unit is in the conservative direction and will revise the
existing non-conservative TS SR to be consistent with the plant
design as described in the UFSAR.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Bradley J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Kennett
Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
FAL Energy Seabrook LLC, Docket No. 50-443, Seabrook Station, Unit No.
1, Rockingham County, New Hampshire
Date of amendment request: March 23, 2006.
Description of amendment request: The proposed amendment would
revise the Seabrook Station, Unit No. 1 (Seabrook) Operating License
and Technical Specifications (TSs) to delete the license condition
requiring reporting of violations of other requirements (e.g.,
conditions listed in Section 2.C of the operating license). The change
is consistent with the notice published in the Federal Register on
November 4, 2005, as part of the consolidated line item improvement
process.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change involves the deletion of a reporting
requirement. The change does not affect plant equipment or operating
practices and, therefore, does not significantly increase the
probability or consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change is administrative in that it deletes a
reporting requirement. The change does not add new plant equipment,
change existing plant equipment, or affect the operating practices
of the facility. Therefore, the change does not create the
possibility of a new of different kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change deletes a reporting requirement. The change
does not affect plant equipment or operation practices and,
therefore, does not involve a significant reduction in a margin of
safety.
Based upon the reasoning presented above, it appears that the three
standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff
proposes to determine that the amendment request involves no
significant hazards consideration.
Attorney for licensee: M.S. Ross, Florida Power & Light Company,
P.O. Box 14000, Juno Beach, FL 33408-0420.
NRC Branch Chief: Darrell J. Roberts.
FPL Energy Seabrook LLC, Docket No. 50-443, Seabrook Station, Unit No.
1, Rockingham County, New Hampshire
Date of amendment request: March 23, 2006.
Description of amendment request: The proposed amendment would
revise the Seabrook Station Unit No. 1 (Seabrook) Technical
Specifications (TSs) consistent with the NRC-approved Revision 4 to
Technical Specification Task Force (TSTF) Standard Technical
Specification Change Traveler, TSTF-449, ``Steam Generator Tube
Integrity.''
Additionally, the proposed amendment would revise Seabrook TS
Surveillance Requirement 4.4.6.2.1 to be consistent with NUREG-1431,
Revision 3, Improved Standard Technical Specifications Westinghouse
Plants.
The NRC staff issued a notice of opportunity for comment in the
Federal Register on March 2, 2005 (70 FR 10298), on possible amendments
adopting TSTF-449, including a model safety evaluation and model no
significant hazards consideration
[[Page 23956]]
(NSHC) determination, using the consolidated line item improvement
process. The NRC staff subsequently issued a notice of availability of
the models for referencing in license amendment applications in the
Federal Register on May 6, 2005 (70 FR 24126). The licensee affirmed
the applicability of the following NSHC determination in its
application dated March 23, 2006.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
Criterion 1--The proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
The proposed change requires a SG [Steam Generator] Program that
includes performance criteria that will provide reasonable assurance
that the SG tubing will retain integrity over the full range of
operating conditions (including startup, operation in the power
range, hot standby, cooldown and all anticipated transients included
in the design specification). The SG performance criteria are based
on tube structural integrity, accident induced leakage, and
operational LEAKAGE.
A SGTR [steam generator tube rupture] event is one of the design
basis accidents that are analyzed as part of a plant's licensing
basis. In the analysis of a[n] SGTR event, a bounding primary to
secondary LEAKAGE rate equal to the operational LEAKAGE rate limits
in the licensing basis plus the LEAKAGE rate associated with a
double-ended rupture of a single tube is assumed.
For other design basis accidents such as MSLB [main steamline
break], rod ejection, and reactor coolant pump locked rotor the
tubes are assumed to retain their structural integrity (i.e., they
are assumed not to rupture). These analyses typically assume that
primary to secondary LEAKAGE for all SGs is 1 gallon per minute or
increases to 1 gallon per minute as a result of accident induced
stresses. The accident induced leakage criterion introduced by the
proposed changes accounts for tubes that may leak during design
basis accidents. The accident induced leakage criterion limits this
leakage to no more than the value assumed in the accident analysis.
The SG performance criteria proposed change[s] to the TS[s] to
identify the standards against which tube integrity is to be
measured. Meeting the performance criteria provides reasonable
assurance that the SG tubing will remain capable of fulfilling its
specific safety function of maintaining reactor coolant pressure
boundary integrity throughout each operating cycle and in the
unlikely event of a design basis accident. The performance criteria
are only a part of the SG Program required by the proposed change to
the TS[s]. The program, defined by NEI [Nuclear Energy Institute]
97-06, Steam Generator Program Guidelines, includes a framework that
incorporates a balance of prevention, inspection, evaluation,
repair, and leakage monitoring. The proposed changes do not,
therefore, significantly increase the probability of an accident
previously evaluated.
The consequences of design basis accidents are, in part,
functions of the DOSE EQUIVALENT I-131 in the primary coolant and
the primary to secondary LEAKAGE rates resulting from an accident.
Therefore, limits are included in the plant technical specifications
for operational leakage and for DOSE EQUIVALENT I-131 in primary
coolant to ensure the plant is operated within its analyzed
condition. The typical analysis of the limiting design basis
accident assumes that primary to secondary leak rate after the
accident is 1 gallon per minute with no more than [500 gallons per
day or 720 gallons per day] in any one SG, and that the reactor
coolant activity levels of DOSE EQUIVALENT I-131 are at the TS
values before the accident.
The proposed change does not affect the design of the SGs, their
method of operation, or primary coolant chemistry controls. The
proposed approach updates the current TSs and enhances the
requirements for SG inspections. The proposed change does not
adversely impact any other previously evaluated design basis
accident and is an improvement over the current TSs.
Therefore, the proposed change does not affect the consequences
of a SGTR accident and the probability of such an accident is
reduced. In addition, the proposed changes do not affect the
consequences of an MSLB, rod ejection, or a reactor coolant pump
locked rotor event, or other previously evaluated accident.
Criterion 2--The proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
The proposed performance based requirements are an improvement
over the requirements imposed by the current technical
specifications. Implementation of the proposed SG Program will not
introduce any adverse changes to the plant design basis or
postulated accidents resulting from potential tube degradation. The
result of the implementation of the SG Program will be an
enhancement of SG tube performance. Primary to secondary LEAKAGE
that may be experienced during all plant conditions will be
monitored to ensure it remains within current accident analysis
assumptions.
The proposed change does not affect the design of the SGs, their
method of operation, or primary or secondary coolant chemistry
controls. In addition, the proposed change does not impact any other
plant system or component. The change enhances SG inspection
requirements.
Therefore, the proposed change does not create the possibility
of a new or different type of accident from any accident previously
evaluated.
Criterion 3--The proposed change does not involve a significant
reduction in the margin of safety.
The SG tubes in pressurized water reactors are an integral part
of the reactor coolant pressure boundary and, as such, are relied
upon to maintain the primary system's pressure and inventory. As
part of the reactor coolant pressure boundary, the SG tubes are
unique in that they are also relied upon as a heat transfer surface
between the primary and secondary systems such that residual heat
can be removed from the primary system. In addition, the SG tubes
isolate the radioactive fission products in the primary coolant from
the secondary system. In summary, the safety function of an SG is
maintained by ensuring the integrity of its tubes.
Steam generator tube integrity is a function of the design,
environment, and the physical condition of the tube. The proposed
change does not affect tube design or operating environment. The
proposed change is expected to result in an improvement in the tube
integrity by implementing the SG Program to manage SG tube
inspection, assessment, repair, and plugging. The requirements
established by the SG Program are consistent with those in the
applicable design codes and standards and are an improvement over
the requirements in the current TSs.
For the above reasons, the margin of safety is not changed and
overall plant safety will be enhanced by the proposed change to the
TS.
Based upon the reasoning presented above, it appears that the three
standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff
proposes to determine that the amendment request involves no
significant hazards consideration.
Attorney for licensee: M.S. Ross, Florida Power & Light Company,
P.O. Box 14000, Juno Beach, FL 33408-0420.
NRC Branch Chief: Darrell J. Roberts.
Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald
C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
Date of amendment requests: March 7, 2006.
Description of amendment requests: The proposed amendments would
modify the Technical Specifications (TS) of the units to change the
reactor trip on turbine trip from the P-7 interlock to the P-8
interlock. Specifically, the amendment would effect changes in TS Table
3.3.1-1, ``Reactor Trip System Instrumentation,'' for Function 16,
``Turbine Trip.'' The purpose of the proposed amendment is to decrease
potentially unnecessary transients on the reactor and to increase plant
availability when the cause of a turbine trip is readily correctable.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration as follows:
(1) Does the proposed change involve a significant increase in
the probability of occurrence or consequences of an accident
previously evaluated?
[[Page 23957]]
Response: No.
The proposed change revises the setpoint at which a reactor trip
will occur by changing the interlock at which it is enabled from the
P-7 interlock, at approximately 10 percent power, to the P-8
interlock, at less than or equal to 31 percent power. The P-7 and P-
8 interlocks are not accident initiators and the change to the
reactor trip setpoint does not create any new credible single
failure. An analysis has shown that a turbine trip without a reactor
trip at 31 percent power or below does not challenge the pressurizer
power operated relief valves (PORVs), thereby not adversely
affecting the probability of a small[-]break loss[-]of [-]coolant
accident due to a stuck open PORV. The consequences of accidents
previously evaluated are unaffected by this change because no change
to any accident mitigation scenario has resulted and there are no
additional challenges to fission product barrier integrity.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
(2) Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
No changes are being made to the plant that would introduce any
new accident causal mechanisms. The proposed change to the power
level at which a reactor trip on turbine trip is enabled does not
adversely affect previously identified accident initiators and does
not create any new accident initiators. The change does not affect
how the associated trip function operates. No new single failures or
accident scenarios are created by the proposed change and the
proposed change does not result in any event previously deemed
incredible being made credible.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
(3) Does the proposed change involve a significant reduction in
a margin of safety?
Response: No.
No safety analyses [will be] changed or modified as a result of
the proposed change in reactor trip setpoint. All margins associated
with the current safety analyses acceptance criteria are unaffected.
The current safety analyses remain binding. The safety systems
credited in the safety analyses will continue to be available to
perform their mitigation functions. The proposed change does not
affect the availability or operability of safety-related systems and
components.
Therefore, the proposed change does not involve a significant
reduction in the margin of safety.
Based on the licensee's analysis, it appears that the three
standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff
proposes to determine that the requested amendments involve no
significant hazards consideration.
Attorney for licensee: James M. Petro, Jr., Esquire, One Cook
Place, Bridgman, MI 49106.
NRC Branch Chief: L. Raghavan.
Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear
Station, Nemaha County, Nebraska
Date of amendment request: January 30, 2006.
Description of amendment request: The proposed change would revise
Cooper Nuclear Station (CNS) Technical Specification section 5.5.12,
``Primary Containment Leakage Rate Testing Program,'' to allow a one-
time extension of no more than 5 years for the Type A, Integrated
Leakage Rate Test (ILRT) interval. This revision is a one-time
exception to the 10-year frequency of the performance-based leakage
rate testing program for Type A tests as defined in Nuclear Energy
Institute (NEI) document NEI 94-01, Revision 0, ``Industry Guideline
for Implementing Performance-Based Option of 10 CFR part 50, appendix
J,'' pursuant to 10 CFR 50, appendix J, option B. The requested
exception is to allow the ILRT to be performed within 15 years from the
last ILRT, last performed on December 7, 1998.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
This license amendment proposes to revise the Technical
Specifications to allow for a one-time extension of the ILRT
interval from 10 years to 15 years. The containment function is
solely to mitigate the consequences of an accident. No design basis
accident is initiated by a failure of the containment leakage
mitigation function. The extension of the ILRT will not create any
adverse interactions with other systems that could result in
initiation of a design basis accident. Continued containment
integrity is also assured by the established programs for local
leakage rate testing and inservice inspections which are unaffected
by the proposed change. Therefore, the probability of occurrence of
an accident previously evaluated is not significantly increased.
The potential consequences of the proposed change have been
quantified by analyzing the changes in risk that would result from
extending the ILRT interval from 10 to 15 years. The increase in
risk in terms of person-rem per year within 50 miles resulting from
accidents was determined to be of a magnitude that NUREG-1493
indicates is imperceptible. NPPD [Nebraska Public Power District]
has also analyzed the increase in risk in terms of the frequency of
large early releases from accidents. The increase in the large early
release frequency resulting from the proposed extension was
determined to be within the guidelines published in Nuclear
Regulatory Commission (NRC) Regulatory Guide 1.174. Additionally,
the proposed change maintains defense-in-depth by preserving a
reasonable balance among prevention of core damage, prevention of
containment failure, and consequence mitigation. NPPD has determined
that the increase in conditional containment failure probability
from reducing the ILRT frequency from one test in 10 years to one
test in 15 years would be insignificant.
Therefore, the probability of occurrence or the consequences of
an accident previously analyzed are not significantly increased.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed extension of the current interval for the ILRT does
not involve any change to the design or operation of any plant
structure, system, or component (SSC). The plant will continue to be
operated in the same manner. Since no changes to the design or
operation of the plant are being made, the proposed one-time
extension of the ILRT does not result in a new failure mode for an
accident.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any accident previously
analyzed.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
Response: No.
The proposed extension to the ILRT test interval will not result
in a change to the design or operation of any plant SSC used to shut
down the plant, initiate Emergency Core Cooling Systems, or isolate
the primary or secondary containment. Thus, the change will not
impact the ability of CNS to mitigate any accident or transient.
NUREG-1493, a generic study of the effects of extending containment
leakage testing, documented that an extension in the ILRT interval
from three per 10 years to one per 20 years resulted in an
imperceptible increase in risk to the public. NUREG-1493 generically
concluded that the design containment leakage rate contributes about
0.1 percent to the individual risk, and that the decrease in the
ILRT frequency would have a minimal effect on this risk since 95% of
the potential leakage paths are detected by Type B and Type C
testing. A risk assessment using the current CNS Probabilistic
Safety Assessment internal events model concluded that the risk
associated with this change is very small and not risk significant.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
[[Page 23958]]
Attorney for licensee: Mr. John C. McClure, Nebraska Public Power
District, Post Office Box 499, Columbus, NE 68602-0499.
NRC Branch Chief: David Terao.
Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear
Station, Nemaha County, Nebraska
Date of amendment request: March 15, 2006.
Description of amendment request: The proposed amendment would
revise Cooper Nuclear Station (CNS) Technical Specification 5.5.12,
``Primary Containment Leakage Rate Testing Program,'' by adding two
sub-paragraphs to note exemptions from Section III.A and Section III.B
of Part 50 of Title 10 of the Code of Federal Regulations, Appendix J,
Option B. These two sub-paragraphs allow the leakage contribution from
the four main steam line penetrations, referred to as the Main Steam
Isolation Valve (MSIV) leakage, to be excluded.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
This proposed change to TS 5.5.12 does not modify existing
structures, systems or components (SSC's) of the plant, and it does
not introduce new SSC's. It does not change assumptions, methodology
or results of previously evaluated accidents in the Updated Safety
Analysis Report.
It does not change operating procedures or administrative
controls that affect the functions of SSC's. By excluding MSIV
leakage from Type A and Type B and C test results, this change will
make the CNS Primary Containment Leakage Rate Testing Program more
closely aligned with the assumptions used in associated accident
consequence analyses. Therefore, the proposed change does not
involve a significant increase in the probability or consequences of
an accident previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
This proposed change to TS 5.5.12.a does not modify existing
SSC's of the plant, and it does not introduce new SSC's. Thus, it
does not affect the design function or operation of SSC's involved,
and it does not introduce a new accident initiator. Therefore, the
proposed change does not create the possibility of a new or
different kind of accident from any previously evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
Since MSIV leakage bypasses the containment and its filtration
system (Standby Gas Treatment System) during a Loss-of-Coolant
Accident (LOCA), the effects on release to the environment [are]
analyzed and specifically accounted for in the CNS dose analysis
methodology approved by Amendments 196 and 206. This proposed change
to exclude MSIV leakage from Type A and Type B and C test results
does not change dose analysis values, and thus, does not affect
actual margin in the dose analysis. Therefore, the proposed change
does not involve a significant reduction in an actual margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. John C. McClure, Nebraska Public Power
District, Post Office Box 499, Columbus, NE 68602-0499.
NRC Branch Chief: David Terao.
Nine Mile Point Nuclear Station, LLC, Docket No. 50-410, Nine Mile
Point Nuclear Station, Unit 2, Oswego County, New York
Date of amendment request: December 29, 2005.
Description of amendment request: The proposed change would delete
Section 2.F of the Nine Mile Point, Unit 2 Facility Operating License
(FOL), NPF-69, which requires the licensee report violations of the
requirements contained in Section 2.C of this license. The NRC staff
issued a notice of opportunity for comment in the Federal Register on
August 29, 2005 (70 FR 51098), on possible amendments to delete this
reporting requirement, including a model safety evaluation and model no
significant hazards consideration (NSHC) determination, using the
consolidated line item improvement process. The NRC staff subsequently
issued a notice of availability of the models for referencing in
license amendment applications in the Federal Register on November 4,
2005 (70 FR 67202). The licensee affirmed the applicability of the
following NSHC determination in its application dated December 29,
2005.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change involves the deletion of a reporting
requirement. The change does not affect any plant equipment or
operating practices and therefore does not significantly increase
the probability or consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change is administrative in that it deletes a
reporting requirement. The change does not add new plant equipment,
change existing plant equipment, or affect the operating practices
of the facility. Therefore, the change will not create the
possibility of a new or different kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change deletes a reporting requirement. The change
does not affect plant equipment or operating practices and therefore
does not involve a significant reduction in a margin of safety.
Based on the above, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston &
Strawn, 1700 K Street, NW., Washington, DC 20006.
NRC Branch Chief: Richard J. Laufer.
Nuclear Management Company, LLC, Docket Nos. 50-266 and 50-301, Point
Beach Nuclear Plant, Units 1 and 2, Town of Two Creeks, Manitowoc
County, Wisconsin
Date of amendment request: March 23, 2006.
Description of amendment request: The proposed amendment would
revise Technical Specification (TS) 3.3.4, ``Loss of Power (LOP) Diesel
Generator (DG) Start and Load Sequence Instrumentation''. The revision
modifies the section title and corrects a nonconservatism in the
degraded voltage time delay values in TS Surveillance Requirement (SR)
3.3.4.3.b.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. Operation of the Point Beach Nuclear Plant in accordance with
the proposed amendments does not result in a significant increase in
the probability or consequences of any accident previously
evaluated.
The diesel generators (DGs) provide emergency electrical power
to the safeguard
[[Page 23959]]
buses in support of equipment required to mitigate the consequences
of design basis accidents and anticipated operational occurrences,
including an assumed loss of all offsite power. SR 3.3.4.3 verifies
that the loss of power (LOP) DG start instrumentation channels
respond to measured parameters within the necessary range and
accuracy. The proposed amendment revises the section title and
corrects nonconservative values in the allowed time delays for the
degraded voltage protection function. The revised values are more
restrictive than the previously allowed values.
Reducing the time delays for the degraded voltage function as
proposed does not significantly increase the probability of a loss
of offsite power event. The degraded voltage analysis established
both maximum time delay limits for a degraded voltage condition and
minimum time delays to prevent premature disconnection from offsite
power. The analyzed time delay limits considered prevention of
premature disconnection from offsite power such that the probability
of an unnecessary loss of offsite power is not significantly
increased.
The proposed change does not involve any hardware changes, nor
does it affect the probability of any event initiators. There will
be no change to normal plant operating parameters, accident
mitigation capabilities, or accident analysis assumptions or inputs.
Therefore, the probability or consequences of any accident
previously evaluated will not be significantly increased as a result
of the proposed change.
2. Operation of the Point Beach Nuclear Plant in accordance with
the proposed amendments does not result in a new or different kind
of accident from any accident previously evaluated.
No new accident scenarios, transient precursors, failure
mechanisms, or limiting single failures are introduced as a result
of the proposed change. The revised surveillance requirements are
more restrictive and will continue to assure equipment reliability
such that plant safety is maintained or will be enhanced.
Equipment important to safety will continue to operate as
designed. The changes do not result in any event previously deemed
incredible being made credible. The changes do not result in adverse
conditions or result in any increase in the challenges to safety
systems. Therefore, operation of the Point Beach Nuclear Plant in
accordance with the proposed amendment will not create the
possibility of a new or different type of accident from any accident
previously evaluated.
3. Operation of the Point Beach Nuclear Plant in accordance with
the proposed amendments does not result in a significant reduction
in a margin of safety.
The diesel generators (DGs) provide emergency electrical power
to the safeguard buses in support of equipment required to mitigate
the consequences of design basis accidents and anticipated
operational occurrences, including an assumed loss of all offsite
power. SR 3.3.4.3 verifies that the loss of power (LOP) DG start
instrumentation channels respond to measured parameters within the
necessary range and accuracy. The proposed amendment corrects
nonconservative values in the allowed time delays for the degraded
voltage protection function. The revised values are more restrictive
than the previously allowed values. The proposed change to this SR
assures that design requirements of the emergency electrical power
system continue to be met.
There are no new or significant changes to the initial
conditions contributing to accident severity or consequences. The
proposed amendment will not otherwise affect the plant protective
boundaries, will not cause a release of fission products to the
public, nor will it degrade the performance of any other structures,
systems or components (SSCs) important to safety. Therefore, the
requested change will not result in a significant reduction in the
margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Jonathan Rogoff, Esquire, Vice President,
Counsel & Secretary, Nuclear Management Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Branch Chief: L. Raghavan.
PPL Susquehanna, LLC, Docket Nos. 50-387 and 50-388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1 and 2), Luzerne County,
Pennsylvania
Date of amendment request: February 1, 2006.
Description of amendment request: The proposed amendment would
modify Technical Specification (TS) requirements for inoperable
snubbers by adding Limiting Condition for Operation (LCO) 3.0.8 for
SSES 1 and 2. This change is based on the TS Task Force (TSTF) change
traveler TSTF-372, Revision 4. A notice of availability for this TS
improvement using the consolidated line item improvement process was
published in the Federal Register on November 24, 2004, and May 4,
2005.
The Nuclear Regulatory Commission (NRC) staff issued a notice of
availability of a model no significant hazards consideration (NSHC)
determination for referencing license amendment applications in the
Federal Register on November 24, 2004 (69 FR 68412), and May 4, 2005
(70 FR 23252). The licensee affirmed the applicability of the model
NSHC determination in its application dated February 1, 2006.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Criterion 1--The Proposed Change Does Not Involve a
Significant Increase in the Probability or Consequences of an
Accident Previously Evaluated.
The proposed change allows a delay time for entering a supported
system technical specification (TS) when the inoperability is due
solely to an inoperable snubber if risk is assessed and managed. The
postulated seismic event requiring snubbers is a low-probability
occurrence and the overall TS system safety function would still be
available for the vast majority of anticipated challenges.
Therefore, the probability of an accident previously evaluated is
not significantly increased, if at all. The consequences of an
accident while relying on allowance provided by proposed LCO 3.0.8
are no different than the consequences of an accident while relying
on the TS required actions in effect without the allowance provided
by proposed LCO 3.0.8. Therefore the consequences of an accident
previously evaluated are not significantly affected by this change.
The addition of a requirement to assess and manage the risk
introduced by this change will further minimize possible concerns.
Therefore, this change does not involve a significant increase in
the probability or consequences of an accident previously evaluated.
2. Criterion 2--The Proposed Change Does Not Create the
Possibility of a New or Different Kind of Accident From Any
Previously Evaluated.
The proposed change does not involve a physical alteration of
the plant (no new or different type of equipment will be installed).
Allowing delay times for entering supported system TS when
inoperability is due solely to inoperable snubbers, if risk is
assessed and managed, will not introduce new failure modes or
effects and will not, in the absence of other unrelated failures,
lead to an accident whose consequences exceed the consequences of
accidents previously evaluated. The addition of a requirement to
assess and manage the risk introduced by this change will further
minimize possible concerns.
Thus, this change does not create the possibility of a new or
different kind of accident from an accident previously evaluated.
3. Criterion 3--The Proposed Change Does Not Involve a
Significant Reduction in the Margin of Safety.
The proposed change allows a delay time for entering a supported
system TS when the inoperability is due solely to an inoperable
snubber, if risk is assessed and managed. The postulated seismic
event requiring snubbers is a low-probability occurrence and the
overall TS system safety function would still be available for the
vast majority of anticipated challenges. The risk impact of the
proposed TS changes was assessed following the three-tiered approach
recommended in RG 1.177. A bounding risk assessment was performed to
justify the proposed TS changes. This application of LCO 3.0.8 is
predicated upon the licensee's performance
[[Page 23960]]
of a risk assessment and the management of plant risk. The net
change to the margin of safety is insignificant. Therefore, this
change does not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Bryan A. Snapp, Esquire, Assoc. General
Counsel, PPL Services Corporation, 2 North Ninth St., GENTW3,
Allentown, PA 18101-1179.
NRC Branch Chief: Richard J. Laufer.
R.E. Ginna Nuclear Power Plant, LLC, Docket No. 50-244, R.E. Ginna
Nuclear Power Plant, Wayne County, New York
Date of amendment request: March 28, 2006.
Description of amendment request: The proposed amendment would
revise Technical Specification Surveillance Requirement 3.5.1.4 by
changing the method and sample frequency for boron concentration
verification for the emergency core cooling system (ECCS) accumulators.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The ECCS Accumulators are used only to respond to an accident
and are not an accident initiator. Therefore, the probability of an
accident has not increased.
Boron concentration is controlled in the ECCS Accumulators to
prevent either excessive boron concentrations or insufficient boron
concentrations. Post-loss-of-coolant accident (LOCA) emergency
procedures directing the operator to establish simultaneous hot and
cold leg injection are based on the worst case minimum boron
precipitation time. Maintaining the maximum ECCS Accumulator boron
concentration within the upper limit ensures that the ECCS
Accumulators do not invalidate these steps. The minimum boron
requirements of 2100 (2550 after EPU [extended power uprate]) ppm
[parts per million] ppm are based on beginning-of-life reactivity
values and are selected to ensure that the reactor will remain
subcritical during the reflood stage of a large break LOCA. During a
large break LOCA, all control element assemblies are assumed not to
insert into the core, and the initial reactor shutdown is
accomplished by void formation during blowdown. Sufficient boron
concentration must be maintained in the ECCS Accumulators to prevent
a return to criticality during reflood. Level and pressure
instrumentation is provided to monitor the availability of the ECCS
Accumulators during plant operation.
The Technical Specification Surveillance Requirement (SR
3.5.1.4) verifies that the boron concentration remains within the
required range by sampling. Currently, the boron concentration in
each ECCS Accumulator is required to be verified by taking a sample
of the water in the ECCS Accumulator every 31 days on a staggered
test basis. A containment entry is required to take a sample from
each of the two ECCS Accumulators. In addition, the makeup water
source for the ECCS Accumulators is from the RWST [refueling water
storage tank], which is maintained between 2300 ppm and 2600 ppm
(2750 and 3050 after EPU) by SR 3.5.4.2, ensuring the ECCS
Accumulators are not diluted during makeup/fill evolutions. However,
the Reactor Coolant System boron concentration is lower during power
operation than the boron concentration in the ECCS Accumulators. Two
check valves in series prevent leakage from the Reactor Coolant
System into the ECCS Accumulators.
This proposed amendment would require inleakage monitoring to be
done every twelve hours in addition to taking samples from each ECCS
Accumulator every six months. Samples would continue to be taken to
verify the inleakage observations remain conservative.
The engineering analysis and risk insights combine to
demonstrate that the method of ECCS Accumulator boron concentration
verification can be changed from sampling every 31 days on a
staggered test basis to monitoring inleakage every twelve hours and
sampling each ECCS Accumulator every six months. The inleakage
monitoring is based on a calculational method that has sufficient
conservatism to predict the boron concentration of the ECCS
Accumulator as shown by sample. Therefore, the ECCS Accumulator
would remain capable of responding to an accident as described above
and the consequences of an accident previously evaluated are not
increased.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change does not alter the function of any
equipment, nor cause it to operate differently than it was designed
to operate. All equipment required to mitigate the consequences of
an accident would continue to operate as before. The proposed change
alters the method of verification of the ECCS Accumulator boron
concentration, but not the boron concentration requirements
themselves.
Therefore, this change does not create the possibility of a new
or different [kind] of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The inleakage monitoring done to verify the concentration of
boron in the ECCS Accumulators, is sufficiently conservative to
ensure that a decrease in boron concentration would be detected,
leading to attempts to increase the boron concentration or a need to
sample the affected ECCS Accumulator. Sampling of the ECCS
Accumulators every six months will continue to be done to ensure
that the inleakage monitoring remains conservative and
representative. If the boron concentration is maintained in the ECCS
Accumulators, the system operates as assumed in the Updated Final
Safety Analysis Report Chapter 15 analyses and the analyses
continues to meet the dose consequences acceptance criteria given in
the Updated Final Safety Analysis Report.
Therefore, this proposed change does not involve a significant
reduction in [a] margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the t