Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 15479-15494 [06-2908]
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Federal Register / Vol. 71, No. 59 / Tuesday, March 28, 2006 / Notices
publication of a notice of proposed
action and an opportunity for hearing or
a notice of hearing is not warranted.
Notice is hereby given of the right of
interested persons to request a hearing
on whether the action should be
rescinded or modified. Also in
connection with this action, the
Commission performed an
Environmental Assessment and
determined that a Finding of No
Significant Impact was appropriate for
this action.
Further Information: The NRC has
prepared a Safety Evaluation Report
(SER) that documents the information
that was reviewed and NRC’s
conclusion. In accordance with 10 CFR
2.390 of NRC’s ‘‘Rules of Practice,’’ final
NRC records and documents regarding
this proposed action including the
amendment request dated May 23, 2005,
and the SER are publically available in
the records component of NRC’s
Agencywide Documents Access and
Management System (ADAMS). These
documents may be inspected at NRC’s
Public Electronic Reading Room on the
Internet at https://www.nrc.gov/readingrm/adams.html. These documents may
also be viewed electronically on the
public computers, located at the NRC
Public Document Room (PDR), O1F21,
One White Flint North, 11555 Rockville
Pike, Rockville, MD 20852.
The PDR reproduction contractor will
copy documents for a fee. Persons who
do not have access to ADAMS or who
encounter problems in accessing the
documents located in ADAMS, should
contact the NRC PDR Reference staff by
telephone at 1–800–397–4209 or (301)
415–4737, or by e-mail to pdr@nrc.gov.
Week of March 27, 2006
There are no meetings scheduled for
the Week of March 27, 2006.
Dated at Rockville, Maryland, this 17th day
of March 2006.
For the Nuclear Regulatory Commission.
Jill S. Caverly,
Project Manager, Licensing Section, Spent
Fuel Project Office, Office of Nuclear Material
Safety and Safeguards.
[FR Doc. E6–4445 Filed 3–27–06; 8:45 am]
Thursday, April 27, 2006
BILLING CODE 7590–01–P
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Sunshine Act; Notice of Meetings
AGENCY HOLDING THE MEETINGS: Nuclear
Regulatory Commission.
DATES: Weeks of March 27, April 3, 10,
17, 24, May 1, 2006.
PLACE: Commissioners’ Conference
Room, 11555 Rockville Pike, Rockville,
Maryland.
STATUS: Public and closed.
MATTERS TO BE CONSIDERED:
15:19 Mar 27, 2006
Monday, April 3, 2006
3:55 p.m.—Affirmation Session (Public
Meeting) (Tentative).
a. USEC, Inc. (American Centrifuge
Plant); Geoffrey Sea appeal of LBP–
05–28 (Tentative).
b. USEC, Inc. (American Centrifuge
Plan)—Appeal of LBP–05–28 by
Portsmouth/Piketon Residents for
Environmental Safety and Security
(PRESS) (Tentative).
c. Hydro Resources, Inc.—Petition for
Review of Partial Initial Decision on
Phase II Cultural Resource
Challengers (Tentative).
Week of April 10, 2006—Tentative
There are no meetings scheduled for
the Week of April 10, 2006.
Week of April 17, 2006—Tentative
There are no meetings scheduled for
the Week of April 17, 2006.
Week of April 24, 2006—Tentative
There are no meetings scheduled for
the Week of April 24, 2006.
Monday, April 24, 2006
2 p.m.—Meeting with Federal Energy
Regulatory Commission (FERC),
FERC Headquarters, 888 First St.,
NE., Washington, DC 20426, Room
2C (Public Meeting).
Wednesday, April 26, 2006
1 p.m.—Discussion of Management
Issues (closed—ex. 2).
1:30 p.m.—Meeting with Department of
Energy (DOE) on New Reactor
Issues (Public Meeting).
This meeting will be webcast live at
the Web address https://www.nrc.gov.
Week of May 1, 2006—Tentative
(Contact: Eileen McKenna, 301–
415–2189).
This meeting will be webcast live at
the Web address https://www.nrc.gov.
*
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*The schedule for Commission
meetings is subject to change on short
notice. To verify the status of meetings
call (recording)—(301) 415–1292.
Contact person for more information:
Michelle Schroll, (301) 415–1662.
*
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The NRC Commission Meeting
Schedule can be found on the Internet
at: https://www.nrc.gov/what-we-do/
policy-making/schedule.html.
*
*
*
*
*
The NRC provides reasonable
accommodation to individuals with
disabilities where appropriate. If you
need a reasonable accommodation to
participate in these public meetings, or
need this meeting notice or the
transcript or other information from the
public meetings in another format (e.g.,
braille, large print), please notify the
NRC’s Disability Program Coordinator,
Deborah Chan, at 301–415–7041, TDD:
301–415–2100, or by e-mail at
DLC@nrc.gov. Determinations on
requests for reasonable accommodation
will be made on a case-by-case basis.
*
*
*
*
*
This notice is distributed by mail to
several hundred subscribers; if you no
longer wish to receive it, or would like
to be added to the distribution, please
contact the Office of the Secretary,
Washington, DC 20555 (301–415–1969).
In addition, distribution of this meeting
notice over the Internet system is
available. If you are interested in
receiving this Commission meeting
schedule electronically, please send an
electronic message to dkw@nrc.gov.
Dated: March 23, 2006.
R. Michelle Schroll,
Office of the Secretary.
[FR Doc. 06–3031 Filed 3–24–06; 1:15 pm]
BILLING CODE 7590–01–M
Tuesday, May 2, 2006
NUCLEAR REGULATORY
COMMISSION
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9:30 a.m.—Briefing on Status of
Emergency Planning Activities—
Morning Session (Public Meeting)
(Contact: Eric Leeds, 301–415–
2334).
1 p.m.—Briefing on Status of Emergency
Planning Activities—Afternoon
Session (Public Meeting).
This meeting will be webcast live at
the Web address https://www.nrc.gov.
Wednesday, May 3, 2006
9 a.m.—Briefing on Status of RiskInformed, Performance-Based
Regulation (Public Meeting)
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NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a(2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
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Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from March 3,
2006 to March 16, 2006. The last
biweekly notice was published on
March 14, 2006 (71 FR 13169).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
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prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
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officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
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participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
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For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket
No. 50–461, Clinton Power Station, Unit
1, DeWitt County, Illinois
Date of amendment request:
December 1, 2006.
Description of amendment request:
The proposed amendment would revise
Technical Specification (TS) 3.6.4.1,
‘‘Secondary Containment.’’ Specifically,
the change would modify Surveillance
Requirements (SRs) 3.6.4.1.4 and
3.6.4.1.5 to clarify their intent with
respect to secondary containment
boundary integrity. The change is
submitted in accordance with the TS
Task Force Traveler 322–A, Revision 2,
‘‘Secondary Containment and Shield
Building Boundary Integrity SRs.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment
involve a significant increase in the
probability or consequences of an
accident previously evaluated?
Response: No. This change involves
an administrative clarification to reflect
the original intent of the Technical
Specifications. There is no impact on
the availability or capability of the
secondary containment or Standby Gas
Treatment (SGT) system as a result of
the proposed change. Both the
secondary containment and SGT system
are considered accident-mitigating
equipment and are not initiators of any
previously evaluated accidents.
Therefore, the proposed change does not
involve an increase in the probability of
an accident previously evaluated.
Additionally, the proposed change does
not alter the secondary containment or
SGT systems’ performance measures or
their ability to perform their accident
mitigation functions.
Therefore, the proposed change does
not involve a significant increase in the
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15481
consequences of an accident previously
evaluated.
2. Does the proposed amendment
create the possibility of a new or
different kind of accident from any
accident previously evaluated?
Response: No. The proposed changes
to the wording of TS SRs 3.6.4.1.4 and
3.6.4.1.5 clarify that only one SGT
subsystem is required to ensure the
requirements of TS 3.6.4.1 are met. The
proposed change does not alter the
parameters within which the plant is
operated. There are no new system
operating conditions or performance
measures introduced by this proposed
change that will affect the secondary
containment and SGT systems’
protective or mitigative functions. The
proposed changes will not alter the
methods in which equipment is
operated or tested. No new accident
scenarios or assumptions, failure
mechanisms, or limiting single failures
are introduced as a result of the
proposed change.
Therefore, the proposed change does
not create the possibility of a new or
different kind of accident from any
previously evaluated.
3. Does the proposed amendment
involve a significant reduction in a
margin of safety?
Response: No. Margins of safety are
established in the design of
components, the configuration of
components to meet certain
performance parameters, and in the
establishment of setpoints to initiate
alarms or actions. The proposed change
does not impact any of these margins of
safety parameters. This change involves
an administrative clarification to reflect
the original intent of the TS. There is no
adverse effect on the operability or
design requirements of the secondary
containment or SGT system. The
equipment will continue to be tested in
a manner and at a frequency necessary
to provide confidence that the
equipment can perform its intended
safety function. There is no impact on
the plant safety analyses.
Therefore, the proposed change does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. Bradley J.
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
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Calvert Cliffs Nuclear Power Plant, Inc.,
Docket Nos. 50–317 and 50–318, Calvert
Cliffs Nuclear Power Plant, Unit Nos. 1
and 2, Calvert County, Maryland
Date of amendments request:
February 27, 2006.
Description of amendments request:
The amendment would revise Technical
Specification 4.2.1, ‘‘Fuel Assemblies,’’
to allow fuel with advanced cladding
material to be installed in the core for
Cycle 19 only at Unit No. 1 or Cycle 17
only at Unit No. 2. Advanced cladding
material from Framatome-ANP may be
used in up to 2 lead test assemblies, and
advanced cladding material from
Westinghouse may be used in up to 2
lead test assemblies.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Would not involve a significant
increase in the probability or
consequences of an accident previously
evaluated.
Calvert Cliffs Technical Specification
4.2.1, Fuel Assemblies, states that fuel
rods are clad with either Zircaloy or
ZIRLOTM. Calvert Cliffs Nuclear Power
Plant, Inc. proposes to re-insert up to
four fuel assemblies into Calvert Cliffs
Unit 1 or Unit 2 that have some fuel
rods clad in zirconium alloys that do
not meet the definition of Zircaloy or
ZIRLOTM. A temporary exemption to the
regulations has also been requested to
allow these fuel assemblies to be reinserted into Unit 1 or Unit 2. The
proposed change to the Calvert Cliffs
Technical Specifications will allow the
use of cladding materials that are not
Zircaloy or ZIRLOTM for one fuel cycle
once the temporary exemption is
approved. The proposed change to the
Technical Specification is effective only
as long as the temporary exemption is
effective. The addition of what will be
an approved temporary exemption for
Unit 1 or Unit 2 to Technical
Specification 4.2.1 does not change the
probability or consequences of an
accident previously evaluated.
Therefore, the proposed change does
not involve a significant increase in the
probability or consequences of an
accident previously evaluated.
2. Would not create the possibility of
a new or different [kind] of accident
from any accident previously evaluated.
The proposed change does not add
any new equipment, modify any
interfaces with existing equipment,
change the equipment’s function, or
change the method of operating the
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equipment. The proposed change does
not affect normal plant operations or
configuration. Since the proposed
change does not change the design,
configuration, or operation, it could not
become an accident initiator.
Therefore, the proposed change does
not create the possibility of a new or
different [kind] of accident from any
previously evaluated.
3. Would not involve a significant
reduction in [a] margin of safety.
The proposed change will add an
approved temporary exemption to the
Calvert Cliffs Technical Specifications
allowing the installation of up to four
lead fuel assemblies. The assemblies use
advanced cladding materials that are not
specifically permitted by existing
regulations or Calvert Cliffs’ Technical
Specifications. A temporary exemption
to allow the installation of these
assemblies has been requested. The
addition of an approved temporary
exemption to Technical Specification
4.2.1 is an administrative change to
allow the installation of the lead fuel
assemblies under the provisions of the
temporary exemption. The license
amendment is effective only as long as
the exemption is effective. This
amendment does not change the margin
of safety since it only adds a reference
to an approved, temporary exemption to
the Technical Specifications.
Therefore, the proposed change does
not involve a significant reduction in [a]
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendments request involves no
significant hazards consideration.
Attorney for licensee: Carey Fleming,
Sr. Counsel—Nuclear Generation,
Constellation Generation Group, LLC,
750 East Pratt Street, 17th floor,
Baltimore, MD 21202.
NRC Branch Chief: Richard J. Laufer.
Duke Energy Corporation, Docket Nos.
50–269, 50–270, and 50–287, Oconee
Nuclear Station, Units 1, 2, and 3,
Oconee County, South Carolina
Date of amendment request: January
5, 2005, supplemented November 21,
2005.
Description of amendment request:
The proposed amendments would
revise the Technical Specification (TS)
5.5.19.b, TS 5.5.19.c, and TS
Surveillance Requirement (SR) 3.8.1.9.
TS 5.5.19.b currently requires
verification that a Lee Combustion
Turbine (LCT) can supply the
equivalent of one Unit’s maximum
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safeguard loads, plus two Units’ Mode
3 loads, when connected to the system
grid every 12 months. In the proposed
amendments, this requirement would be
more clearly specified as, ‘‘Verify an
LCT can supply equivalent of one Unit’s
Loss of Coolant Accident (LOCA) loads
plus two Unit’s Loss of Offsite Power
(LOOP) loads when connected to system
grid every 12 months.’’ TS 5.5.19.b and
SR 3.8.1.9 would be revised for
consistency.
This notice supersedes the notice
published in the Federal Register on
February 15, 2005 (70 FR 7764).
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
(1) Involve a significant increase in
the probability or consequences of an
accident previously evaluated:
Duke proposes to revise TS 5.5.19.b to
clarify the Lee Combustion Turbine
(LCT) testing requirements. Duke
proposes to revise TS 5.5.19.c and TS
3.8.1 Surveillance Requirement (SR)
3.8.1.19 to be consistent with the
proposed change to TS 5.5.19.b. The
proposed change makes the wording of
the test requirement consistent with the
UFSAR [Updated Final Safety Analysis
Report]. LCT testing has no impact on
the probability of an accident analyzed
in the UFSAR. The LCT can be credited
to mitigate the consequences of an
accident analyzed in the UFSAR.
However, this clarification of LCT
testing requirements has no impact on
its ability to mitigate the consequences
of an accident. As such, the proposed
LAR [license amendment request] does
not involve a significant increase in the
probability or consequences of an
accident previously evaluated.
(2) Create the possibility of a new or
different kind of accident from any kind
of accident previously evaluated:
Duke proposes to revise TS 5.5.19.b to
clarify the Lee Combustion Turbine
(LCT) testing requirements. Duke
proposes to revise TS 5.5.19.c and TS
3.8.1 SR 3.8.1.9 to be consistent with the
proposed change to TS 5.5.19.b. The
proposed change makes the wording of
the test requirement consistent with the
UFSAR. These changes do not alter the
nature of events postulated in the Safety
Analysis Report nor do they introduce
any unique precursor mechanisms.
Therefore, the proposed amendment
will not create the possibility of a new
or different kind of accident from any
accident previously evaluated.
(3) Involve a significant reduction in
a margin of safety:
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The proposed TS change does not
unfavorably affect any plant safety
limits, set points, or design parameters.
The changes also do not unfavorably
affect the fuel, fuel cladding, RCS
[reactor coolant system], or containment
integrity. Therefore, the proposed TS
change, which clarifies TS requirements
associated with the LCT testing
program, does not involve a significant
reduction in the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Ms. Lisa F.
Vaughn, Legal Department (PB05E),
Duke Energy Corporation, 422 South
Church Street, Charlotte, North Carolina
28201–1006.
NRC Branch Chief: Evangelos C.
Marinos.
Exelon Generation Company, LLC,
Docket Nos. 50–373 and 50–374, LaSalle
County Station, Units 1 and 2, LaSalle
County, Illinois
Date of amendment request: March
13, 2006.
Description of amendment request:
The proposed amendments would make
changes to the technical specifications
(TS) for LaSalle County Station (LSCS),
Units 1 and 2. Surveillance Requirement
(SR) 3.7.3.1 verifies the cooling water
temperature supplied to the plant from
the core standby cooling system (CSCS)
pond (i.e., the ultimate heat sink (UHS))
is ≤ 100 °F. Currently, if the temperature
of the cooling water supplied to the
plant from the CSCS pond is > 100 °F,
the UHS must be declared inoperable in
accordance with TS 3.7.3. TS 3.7.3,
Required Action B.1, requires that both
units be placed in Mode 3 within 12
hours and Required Action B.2 requires
that both units be placed in Mode 4
within 36 hours.
Prolonged hot weather in the area
during the summer months, in
conjunction with high humidity during
the daytime, minimal cooling at night
and little precipitation, has resulted in
sustained elevated cooling water
temperature supplied to the plant from
the CSCS pond. This license
amendment is being requested to
increase the temperature limit of the
cooling water supplied to the plant from
the CSCS pond to ≤ 101.5 °F by
reducing the temperature measurement
uncertainty by replacing the existing
thermocouples with higher precision
temperature measuring equipment.
Should the UHS indicated temperature
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exceed 101.5 °F, Required Action B.1
would be entered and both units would
be placed in Mode 3 within 12 hours
and Mode 4 within 36 hours.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed change does not
involve a significant increase in the
probability or consequences of an
accident previously evaluated? The
proposed change will allow the
indicated temperature of the cooling
water supplied to the plant from the
CSCS pond to be increased to ≤ 101.5
°F based on reducing the temperature
measurement uncertainty by replacing
the existing thermocouples with higher
precision temperature measuring
equipment.
Analyzed accidents are assumed to be
initiated by the failure of plant
structures, systems, or components. An
inoperable UHS is not considered as an
initiator of any analyzed events. As
such, there is not a significant increase
in the probability of a previously
evaluated accident. Allowing the UHS
to operate at a higher allowable
indicated temperature, but still within
the design limits of the equipment it
supplies, will not affect the failure
probability of that equipment. The
current heat analyses calculations of
record for LSCS, Units 1 and 2, assume
a UHS temperature of 100 °F and postaccident peak inlet temperature of 104
°F. The proposed temperature increase
is based solely on a reduction of the
existing instrument loop uncertainty
value. The current analysis bounds the
proposed change. This higher allowable
indicated temperature does not impact
the LOCA [loss-of-coolant accident]
Peak Clad Temperature Analysis, LOCA
Containment Analysis or the non-LOCA
analyses; therefore, continued operation
with a UHS temperature > 100 °F but ≤
101.5 °F will not increase the
consequences of an accident previously
evaluated in the UFSAR.
Based on the above information, the
increase in the allowable indicated
temperature of the cooling water
supplied to the plant from the UHS to
≤ 101.5 °F by reducing the existing
instrument loop uncertainty value has
no effect on the result of the design
basis event and will continue to allow
each required heat exchanger to perform
its safety function. The heat exchangers
will continue to provide sufficient
cooling for the heat loads during the
most severe 30-day period.
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Based on the above information,
increasing the allowable indicated
temperature of the cooling water
supplied to the plant from the CSCS
pond from ≤ 100 °F to ≤ 101.5 °F by
reducing the instrument uncertainty
value has no impact on any analyzed
accident; therefore, the proposed change
does not involve a significant increase
in the probability or consequences of an
accident previously evaluated.
2. The proposed change create the
possibility of a new or different kind of
accident from any previously evaluated?
The proposed change involves
replacing the presently installed
thermocouples with higher accuracy
temperature measurement equipment.
This proposed action will not alter the
manner in which equipment is
operated, nor will the functional
demands on credited equipment be
changed. No alteration in the
procedures that ensure the units remain
within analyzed limits is proposed, and
no change is being made to procedures
relied upon to respond to an off-normal
event. Raising the UHS temperature
limit does not introduce any new or
different modes of plant operation, nor
does it affect the operational
characteristics of any safety-related
equipment or systems; as such, no new
failure modes are being introduced. The
proposed action reduces the instrument
uncertainty value but does not alter
assumptions made in the safety
analysis.
Increasing the allowable indicated
temperature of the cooling water
supplied to the plant from the CSCS
pond from ≤ 100 °F to ≤ 101.5 °F has
no impact on safety related systems. The
plant is designed such that the RHR
[residual heat removal] pumps on the
unit undergoing the LOCA/LOOP [loss
of offsite power] conditions would start
upon the receipt of a signal, and would
load onto their respective Emergency
Diesel Generators emergency bus during
the LOOP event. The increase in the
allowable indicated temperature of the
cooling water supplied to the plant from
the CSCS pond will not require
operation of additional RHR pumps;
therefore, system operation is unaffected
by the proposed change in the UHS
temperature limit.
Based on the above information, the
proposed change does not create the
possibility of a new or different kind of
accident from any previously evaluated.
3. The proposed change does not
involve a significant reduction in a
margin of safety.
The proposed change allows an
increase in the allowable indicated
temperature of the cooling water
supplied to the plant from the CSCS
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pond to ≤ 101.5 °F. The margin of safety
is determined by the design and
qualification of the plant equipment, the
operation of the plant within analyzed
limits, and the point at which protective
or mitigative actions are initiated. The
proposed action does not impact these
factors as the analyzed peak inlet
temperature of the UHS is unaffected
based on the improved instrument
uncertainty of the new high precision
temperature measurement
instrumentation. No setpoints are
affected, and no other change is being
proposed in the plant operational limits
as a result of this change. All accident
analysis assumptions and conditions
will continue to be met. Adequate
design margin is available to ensure that
the required margin of safety is not
significantly reduced.
Therefore, the proposed change does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Bradley J.
Fewell, Assistant General Counsel,
Exelon Generation Company, LLC, 200
Exelon Way, Kennett Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–440,
Perry Nuclear Power Plant, Unit 1, Lake
County, Ohio
Date of amendment request: February
14, 2006.
Description of amendment request:
The proposed amendment would revise
the frequency of the Mode 5
Intermediate Range Monitoring (IRM)
Instrumentation CHANNEL
FUNCTIONAL TEST contained in
Technical Specification (TS) 3.3.1.1
from 7 days to 31 days. The
methodology used for the IRM drift
analysis is based upon guidance
contained in Generic Letter 91–04,
‘‘Changes in Technical Specification
Surveillance Intervals to Accommodate
a 24-month Fuel Cycle,’’ and Electric
Power Institute Report TI–103335,
‘‘Guidance for Instrument Calibration
Extension/Reduction Programs.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration which is presented below:
1. The proposed change does not
involve a significant increase in the
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probability or consequences of an
accident previously evaluated.
The proposed Technical
Specifications (TS) change involves an
increase in the Mode 5 CHANNEL
FUNCTIONAL TEST interval for RPS
[Reactor Protection System] IRM
channels from 7 days to 31 days. The
IRM system is used for event mitigation.
The failure of an IRM does not initiate
an accident or transient event. The
proposed TS change does not alter the
design or function of the IRM system for
no physical changes are being made to
the plant. Evaluation of the proposed
testing interval change demonstrated
that the availability of IRMs to mitigate
the consequences of a control rod
withdrawal event at low power levels
are not significantly affected based on
the effectiveness of other, required TS
surveillance testing that is performed,
the availability of redundant systems
and equipment, and the high reliability
of the IRM equipment.
Therefore, the proposed change does
not involve a significant increase in the
probability or consequences of an
accident previously evaluated.
2. The proposed change does not
create the possibility of a new or
different kind of accident from any
accident previously evaluated.
The proposed TS change involves an
increase in the Mode 5 IRM CHANNEL
FUNCTIONAL TEST interval from 7
clays [days] to 31 days. Existing TS
testing requirements ensure the
operability of the IRMs. The proposed
TS change does not introduce any
failure mechanisms of a different type
than those previously evaluated, since
no physical changes to the plant are
being made. No new or different
equipment is being installed, and no
installed equipment is being operated in
a different manner. As a result, no new
failure modes are introduced. In
addition, the manner in which
surveillance tests are performed remains
unchanged.
Therefore, the proposed TS change
does not create the possibility of a new
or different kind of accident from any
previously evaluated.
3. The proposed change does not
involve a significant reduction in a
margin of safety.
The proposed TS change involves an
increase in the Mode 5 CHANNEL
FUNCTIONAL TEST interval for RPS
IRM channels from 7 days to 31 days.
There is expected to be no impact on
system operability, based upon the
performance of the more frequent
Channel Checks, Control Room
monitoring when the IRMs are in use,
and the overall IRM reliability.
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Furthermore, a historical review of
surveillance test results and associated
maintenance records did not indicate
evidence of any failure that would
invalidate the above conclusions.
Therefore, the proposed change does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David W.
Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street,
Akron, OH 44308.
NRC Branch Chief: Mindy S. Landau,
Acting.
Nine Mile Point Nuclear Station, LLC,
Docket No. 50–220, Nine Mile Point
Nuclear Station Unit No. 1, Oswego
County, New York
Date of amendment request:
December 16, 2005.
Description of amendment request:
The proposed change to Technical
Specification (TS) Surveillance
Requirement (SR) 4.1.4d relocates the
SR for testing the core spray header
differential pressure (DP)
instrumentation to licensee-controlled
documents. TS SR 4.1.4d currently
requires that the core spray header DP
instrumentation be periodically tested
such that a check of each sensor is
performed at least once each day and
each channel is calibrated and tested at
least once every 3 months. The
proposed change will allow these SRs to
be placed in licensee-controlled
documents where future changes will be
made pursuant to Title 10 of the Code
of Federal Regulations (10 CFR), Section
50.59. The functional description of the
core spray header DP instrumentation
will also be relocated from the TS Bases
to licensee-controlled documents
consistent with the proposed TS change.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve
a significant increase in the probability
or consequences of an accident
previously evaluated?
Response: No.
The proposed changes are limited to
the relocation of selected
instrumentation requirements. The
proposed relocated requirements were
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determined not to meet the 10 CFR
50.36 screening criteria for retention in
the TSs and will be maintained in
licensee-controlled documents in
accordance with the provisions of 10
CFR 50.59. The proposed changes do
not introduce any new modes of plant
operation, make any physical changes to
the plant, or alter any operational
setpoints which could degrade the
performance of any safety system
assumed to function in the accident
analysis. Therefore, the proposed
changes do not involve a significant
increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create
the possibility of a new or different kind
of accident from any accident
previously evaluated?
Response: No. The proposed changes
do not introduce any new modes of
plant operation, make any physical
changes to the plant, or alter any
operational setpoints which could
create new accident initiators or failure
mechanisms. The proposed changes are
limited to the relocation of selected
instrumentation requirements, and will
have no impact on the accident
assumptions and initial conditions as
previously analyzed in the UFSAR
[Updated Final Safety Analysis Report].
Therefore, the proposed changes do not
create the possibility of a new or
different kind of accident from any
accident previously evaluated.
3. Does the proposed change involve
a significant reduction in a margin of
safety?
Response: No. The proposed changes
are consistent with the Improved
Standard TSs (NUREG–1433, Rev. 3)
and will have no impact on the
instrumentation setpoints, logic, or
functional requirements as described in
the TSs, TS Bases, and UFSAR. The
proposed relocated requirements were
determined to not meet the 10 CFR
50.36 screening criteria for retention in
the TSs. Thus, the relocated
requirements will be maintained in
accordance with 10 CFR 50.59 as
required. Accordingly, the proposed
relocated requirements will not degrade
the quality or performance of any safety
system assumed to mitigate an accident
or assure operation within the safety
limits. Therefore, the proposed changes
do not involve a significant reduction in
a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
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amendment request involves no
significant hazards consideration.
Attorney for licensee: Mark J.
Wetterhahn, Esquire, Winston & Strawn,
1700 K Street, NW., Washington, DC
20006.
NRC Branch Chief: Richard J. Laufer.
PPL Susquehanna, LLC, Docket Nos. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1
and 2), Luzerne County, Pennsylvania
Date of amendment request: February
28, 2006.
Description of amendment request:
The proposed amendments would
change the SSES 1 and 2 Technical
Specification (TS) Surveillance
Requirements (SRs) 3.8.4.7 and 3.8.4.8
to clarify that diesel generator ‘‘E’’ (DG
E) electrical power subsystem testing
does not require a mode restriction
when the DG E diesel is not required to
be OPERABLE.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve
a significant increase in the probability
or consequences of an accident
previously evaluated?
Response: No. Performance of TS
required SRs are not initiators to any
accident sequences analyzed in the
Final Safety Analysis Report (FSAR).
The changes do not involve any
physical change to structures, systems,
or components, (SSCs) and do not alter
the method of operation or control of
SSCs. The current assumptions in the
safety analysis regarding accident
initiators and mitigation of accidents are
unaffected by these changes. No
additional failure modes or mechanisms
are being introduced and the likelihood
of previously analyzed failures remains
unchanged.
Operation in accordance with the
proposed Technical Specification (TS)
ensures that the DC [direct current]
distribution system and supported
equipment functions remain capable of
performing the function as described in
the FSAR. Therefore, the mitigative
functions supported by the system will
continue to provide the protection
assumed by the analysis.
Therefore, this change does not
involve a significant increase in the
probability or consequences of an
accident previously evaluated.
2. Does the proposed change create
the possibility of a new or different kind
of accident from any accident
previously evaluated?
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Response: No. The proposed change
does not involve a physical alteration of
the plant. No new equipment is being
introduced, and installed equipment is
not being operated in a new or different
manner. There are no setpoints, at
which protective or mitigative actions
are initiated, affected by this change.
This change will not alter the manner in
which equipment operation is initiated,
nor will the function demands on
credited equipment be changed. No
alterations in the procedures that ensure
the plant remains within analyzed
limits are being proposed, and no
changes are being made to the
procedures relied upon to respond to an
off-normal event as described in the
FSAR. As such, no new failure modes
are being introduced. The change does
not alter assumptions made in the safety
analysis and licensing basis.
3. Does the proposed change involve
a significant reduction in a margin of
safety?
Response: No. The margin of safety is
established through equipment design,
operating parameters, and the setpoints
at which automatic actions are initiated.
The proposed change is acceptable
because performance of SRs on
equipment not require[d] to be
OPERABLE and isolated from the
OPERABLE plant equipment cannot
affect any margin of safety. Therefore,
the plant response to analyzed events
will continue to provide the margin of
safety assumed by the analysis.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Bryan A. Snapp,
Esquire, Assoc. General Counsel, PPL
Services Corporation, 2 North Ninth St.,
GENTW3, Allentown, PA 18101–1179.
NRC Branch Chief: Richard J. Laufer
Southern California Edison Company
(SCE), et al., Docket Nos. 50–361 and
50–362, San Onofre Nuclear Generating
Station, Units 2 and 3 (SONGS 2 and 3),
San Diego County, California
Date of amendment requests: March
10, 2006.
Description of amendment requests:
The licensee requests the Nuclear
Regulatory Commission consent to the
transfer of the City of Anaheim’s 3.16
percent undivided ownership interest in
SONGS 2 and 3 to Southern California
Edison, excluding Anaheim’s interest in
its spent fuel and the SONGS 2 and 3
independent spent fuel storage
installation.
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Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve
a significant increase in the probability
or consequences of an accident
previously evaluated?
Response: No. The amendments do
not involve any change in the design,
configuration, or operation of the
nuclear plant. All Limiting Conditions
for Operation, Limiting Safety System
Settings, and Safety Limits specified in
the Technical Specifications remain
unchanged. SCE will continue to be the
licensed operator of the units.
The technical qualifications of SCE to
carry out its exclusive responsibilities
under the operating licenses, as
amended, will remain unchanged.
Personnel engaged in operation,
maintenance, engineering, assessment,
training, and other related services are
not changed. The SCE officers and
executives currently responsible for the
overall safe operation of the nuclear
plants will continue in the same
capacity.
Therefore, the proposed change does
not involve a significant increase in the
probability or consequences of an
accident previously evaluated.
2. Does the proposed change create
the possibility of a new or different kind
of accident from any accident
previously evaluated?
Response: No. The amendments do
not involve any change in the design,
configuration, or operation of the
nuclear plant. The current plant design
and design bases will remain the same.
The current plant safety analyses,
therefore, remain complete and accurate
in addressing the design basis events
and in analyzing plant response and
consequences.
The Limiting Conditions for
Operation, Limiting Safety System
Settings, and Safety Limits specified in
the Technical Specifications are not
affected by the change. As such, the
plant conditions for which the design
basis accident analyses were performed
remain valid.
The amendments do not introduce a
new mode of plant operation or new
accident precursors, do not involve any
physical alterations to plant
configurations, or make changes to
system set points that could initiate a
new or different kind of accident.
Therefore, the proposed change does
not create the possibility of a new or
different kind of accident from any
previously evaluated.
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3. Does the proposed change involve
a significant reduction in a margin of
safety?
Response: No. The amendments do
not involve a change in the design,
configuration, or operation of the
nuclear plants. The change does not
affect either the way in which the plant
structures, systems, and components
perform their safety function, or their
design and licensing basis.
Plant safety margins are established
through Limiting Conditions for
Operation, Limiting Safety System
Settings, and Safety Limits specified in
the Technical Specifications. Because
there is no change to the physical design
of the plant, there is no change to any
of these margins.
Therefore, the proposed change does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Douglas K.
Porter, Esquire, Southern California
Edison Company, 2244 Walnut Grove
Avenue, Rosemead, California 91770.
NRC Branch Chief: David Terao.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–424 and 50–425,
Vogtle Electric Generating Plant, Units 1
and 2, Burke County, Georgia
Date of amendment request:
September 19, 2005.
Description of amendment request:
The proposed amendment would revise
Technical Specification (TS) Limiting
Conditions for Operation (LCO) 3.3.1,
‘‘Reactor Trip system (RTS)
Instrumentation’’ and TS Surveillance
Requirements (SR) 3.2.4.2, ‘‘Quadrant
Power Tilt Ration (QPTR)’’ to avoid
confusion as to when a flux map for
QPTR is required.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve
a significant increase in the probability
or consequences of an accident
previously evaluated?
No. The proposed changes do not
adversely affect accident initiators or
precursors nor alter the design
assumptions, conditions, or
configuration of the facility or the
manner in which the plant is operated
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and maintained. The proposed changes
do not alter or prevent the ability of
structures, systems, and components
(SSCs) from performing their intended
function to mitigate the consequences of
an initiating event within the assumed
acceptance limits. The proposed
changes do not affect the source term,
containment isolation, or radiological
release assumptions used in evaluating
the radiological consequences of an
accident previously evaluated. Further,
the proposed changes do not increase
the types or amounts of radioactive
effluent that may be release offsite, nor
significantly increase individual or
cumulative occupational/public
radiation exposures. The proposed
changes are consistent with safety
analysis assumptions and resultant
consequences.
Therefore, the proposed changes do
not increase the probability or
consequences of an accident previously
evaluated
2. Does the proposed change create
the possibility of a new or different kind
of accident from any previously
evaluated?
No. The proposed changes do not
result in a change in the manner in
which the RTS and ESFAS provide
plant protection. The RTS and ESFAS
will continue to have the same set
points after the proposed changes are
implemented. There are no design
changes associated with the license
amendment.
The changes do not involve a physical
alteration of the plant (i.e., no new or
different type of equipment will be
installed) or a change in the methods
governing normal plant operation. In
addition, the changes do not impose any
new or different requirements or
eliminate any existing requirements.
The changes do not alter assumptions
made in the safety analysis. The
proposed changes are consistent with
the safety analysis assumptions and
current plant operating practice.
Therefore, the proposed changes do
not create the possibility of a new or
different kind of accident from any
previously evaluated.
3. Does the proposed change involve
a significant reduction in a margin of
safety?
No. The proposed changes do not
alter the manner in which safety limits,
limiting safety system settings or
limiting conditions for operation are
determined. The safety analysis
acceptance criteria are not impacted by
these changes. Redundant RTS and
ESFAS trains are maintained, and
diversity with regard to the signals that
provide reactor trip and engineered
safety features actuation is also
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maintained. All signals credited as
primary or secondary, and all operator
actions credited in the accident analyses
will remain the same. The proposed
changes will not result in plant
operation in a configuration outside the
design basis.
Therefore, the proposed changes do
not involve a significant reduction in
the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. Arthur H.
Domby, Troutman Sanders,
NationsBank Plaza, Suite 5200, 600
Peachtree Street, NE., Atlanta, Georgia
30308–2216.
NRC Branch Chief: Evangelos C.
Marinos.
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Tennessee Valley Authority, Docket
Nos. 50–259, 50–260 and 50–296,
Browns Ferry Nuclear Plant, Units 1, 2
and 3, Limestone County, Alabama
Date of amendment request: January
10, 2006 (TS–453).
Description of amendment request:
The proposed amendment would
specify the methodology used for
determining, setting, and evaluating asfound setpoints for those drift
susceptible instruments, which are
either necessary to ensure compliance
with a Safety Limit or critical in
ensuring the fuel peak cladding
temperature acceptance criteria of 10
CFR 50.46 are met.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment
involve a significant increase in the
probability or consequences of an
accident previously evaluated?
Response: No. Including references to
TVA’s methodology for determining,
setting, and evaluating as-found
instrument setpoints in the TS is an
administrative change. There will be no
change to the manner in which Safety
Limits, Analytical Limits, or Allowable
Values are determined. No changes are
proposed in the manner in which the
Reactor Protection System (RPS),
Emergency Core Cooling System (ECCS),
Reactor Core Isolation Cooling (RCIC),
or Primary Containment Isolation
systems provide plant protection or
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which create new modes of plant
operation.
The proposed request will not affect
the probability of any event initiators.
There will be no degradation in the
performance of, or an increase in the
number of challenges imposed on,
safety-related equipment assumed to
function during an accident situation.
There will be no change to normal plant
operating parameters or accident
mitigation performance.
Therefore, the proposed amendment
does not involve a significant increase
in the probability or consequences of an
accident previously evaluated.
2. Does the proposed amendment
create the possibility of a new or
different kind of accident from any
accident previously evaluated?
Response: No. There are no hardware
changes nor are there any changes in the
method by which any plant system
performs a safety function. This request
does not affect the normal method of
plant operation. The proposed
amendment does not introduce new
equipment, which could create a new or
different kind of accident.
No new external threats, release
pathways, or equipment failure modes
are created. No new accident scenarios,
transient precursors, failure
mechanisms, or limiting single failures
are introduced as a result of this request.
Therefore, the implementation of the
proposed amendment will not create a
possibility for an accident of a new or
different type than those previously
evaluated.
3. Does the proposed amendment
involve a significant reduction in a
margin of safety?
Response: No. Including references to
TVA’s methodology for determining,
setting, and evaluating as-found
instrument setpoints in the TS is an
administrative change. No changes are
proposed in the manner in which the
RPS, ECCS, RCIC, or Primary
Containment Isolation systems satisfy
the Updated Final Safety Analysis
Report requirements for accident
mitigation or unit safe shutdown. There
will be no change to Safety Limits,
Analytical Limits, Allowable Values, or
post-Loss Of Coolant Accident peak clad
temperatures. For these reasons, the
proposed amendment does not involve
a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
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15487
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L.
Marshall, Jr.
Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton
County, Tennessee
Date of amendment request: February
6, 2006.
Description of amendment request:
The proposed amendment would
modify technical specification (TS)
requirements for inoperable snubbers by
adding Limiting Condition for
Operation 3.0.7. The changes are
consistent with Nuclear Regulatory
Commission approved Industry/
Technical Specification Task Force
(TSTF) standard TS change TSTF–373,
Revision 4. The availability of this TS
improvement was published in the
Federal Register on May 4, 2005 (70 FR
23252), as part of the consolidated line
item improvement process.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve
a significant increase in the probability
or consequences of an accident
previously evaluated?
Response: No. The proposed change
allows a delay time before declaring
supported TS systems inoperable when
the associated snubber(s) cannot
perform its required safety function.
Entrance into Actions or delaying
entrance into Actions is not an initiator
of any accident previously evaluated.
Consequently, the probability of an
accident previously evaluated is not
significantly increased. The
consequences of an accident while
relying on the delay time allowed before
declaring a TS supported system
inoperable and taking its Conditions
and Required Actions are no different
than the consequences of an accident
under the same plant conditions while
relying on the existing TS supported
system Conditions and Required
Actions. Therefore, the consequences of
an accident previously evaluated are not
significantly increased by this change.
Therefore, this change does not involve
a significant increase in the probability
or consequences of an accident
previously evaluated.
2. Does the proposed change create
the possibility of a new or different kind
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of accident from any accident
previously evaluated?
Response: No. The proposed change
allows a delay time before declaring
supported TS systems inoperable when
the associated snubber(s) cannot
perform its required safety function. The
proposed change does not involve a
physical alteration of the plant (no new
or different type of equipment will be
installed) or a change in the methods
governing normal plant operations.
Thus, this change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed change involve
a significant reduction in a margin of
safety?
Response: No. The proposed change
allows a delay time before declaring
supported TS systems inoperable when
the associated snubber(s) cannot
perform its required safety function. The
proposed change restores an allowance
in the pre-ISTS conversion TS that was
unintentionally eliminated by the
conversion. The pre-ISTS TS were
considered to provide an adequate
margin of safety for plant operation, as
does the post-ISTS conversion TS.
Therefore, this change does not involve
a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Section Chief: Michael L.
Marshall, Jr.
Generator Tube Inspection Report.’’ The
proposed changes are necessary in order
to implement the guidance for the
industry initiative on NEI 97–06,
‘‘Steam Generator Program Guidelines.’’
The amendment would also delete
License Condition 2.C.8 Item b. This
License Condition references the
licensee’s letters from 1997 that contain
commitments associated with NRC
Generic Letter 95–05, ‘‘Voltage-Based
Repair Criteria for Westinghouse Steam
Generator Tubes Affected by Outside
Diameter Stress Corrosion Cracking,’’
and the application of voltage-based
alternate repair criteria to the steam
generators. The licensee has concluded
that the provisions and requirements of
the proposed TS changes bound the
commitments identified in the existing
License Condition.
The NRC staff issued a notice of
opportunity for comment in the Federal
Register on March 2, 2005 (70 FR
10298), on possible amendments
adopting TSTF–449, including a model
safety evaluation and model no
significant hazards consideration
(NSHC) determination, using the
consolidated line item improvement
process. The NRC staff subsequently
issued a notice of availability of the
models for referencing in license
amendment applications in the Federal
Register on May 6, 2005 (70 FR 24126).
The licensee affirmed the applicability
of the following NSHC determination in
its application dated August 31, 2005.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
Criterion 1—The Proposed Change Does
Not Involve a Significant Increase in the
Probability or Consequences of an
Accident Previously Evaluated
Tennessee Valley Authority, Docket No.
The proposed change requires a SG
50–328, Sequoyah Nuclear Plant, Unit 2, Program that includes performance
Hamilton County, Tennessee
criteria that will provide reasonable
Date of amendment request: February assurance that the SG tubing will retain
integrity over the full range of operating
15, 2006.
Description of amendment request:
conditions (including startup, operation
The amendment would revise the
in the power range, hot standby,
Technical Specifications (TS) to adopt
cooldown and all anticipated transients
NRC-approved Revision 4 to Technical
included in the design specification).
Specification Task Force (TSTF)
The SG performance criteria are based
Standard Technical Specification
on tube structural integrity, accident
Change Traveler, TSTF–449, ‘‘Steam
induced leakage, and operational
Generator Tube Integrity.’’ The
LEAKAGE.
A steam generator tube rupture
proposed amendment includes changes
(SGTR) event is one of the design basis
to the TS definition of Leakage, TS
accidents that are analyzed as part of a
3.4.6.2, ‘‘Reactor Coolant System,
Operational Leakage,’’ TS 3.4.5, ‘‘Steam plant’s licensing basis. In the analysis of
a SGTR event, a bounding primary to
Generator (SG) Tube Integrity,’’ and
secondary LEAKAGE rate equal to the
adds TS 6.8.4.k, ‘‘Steam Generator (SG)
operational LEAKAGE rate limits in the
Program,’’ and TS 6.9.1.16, ‘‘Steam
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Frm 00117
Fmt 4703
Sfmt 4703
licensing basis plus the LEAKAGE rate
associated with a double-ended rupture
of a single tube is assumed.
For other design basis accidents such
as a main steamline break (MSLB), rod
ejection, and reactor coolant pump
locked rotor the tubes are assumed to
retain their structural integrity (i.e., they
are assumed not to rupture). These
analyses typically assume that primary
to secondary LEAKAGE for all SGs is 1
gallon per minute or increases to 1
gallon per minute as a result of accident
induced stresses. The accident induced
leakage criterion introduced by the
proposed changes accounts for tubes
that may leak during design basis
accidents. The accident induced leakage
criterion limits this leakage to no more
than the value assumed in the accident
analysis.
The SG performance criteria proposed
change to the TS identify the standards
against which tube integrity is to be
measured. Meeting the performance
criteria provides reasonable assurance
that the SG tubing will remain capable
of fulfilling its specific safety function
of maintaining reactor coolant pressure
boundary integrity throughout each
operating cycle and in the unlikely
event of a design basis accident. The
performance criteria are only a part of
the SG Program required by the
proposed change to the TS. The
program, defined by NEI 97–06, Steam
Generator Program Guidelines, includes
a framework that incorporates a balance
of prevention, inspection, evaluation,
repair, and leakage monitoring. The
proposed changes do not, therefore,
significantly increase the probability of
an accident previously evaluated.
The consequences of design basis
accidents are, in part, functions of the
DOSE EQUIVALENT I–131 in the
primary coolant and the primary to
secondary LEAKAGE rates resulting
from an accident. Therefore, limits are
included in the plant technical
specifications for operational leakage
and for DOSE EQUIVALENT I–131 in
primary coolant to ensure the plant is
operated within its analyzed condition.
The typical analysis of the limiting
design basis accident assumes that
primary to secondary leak rate after the
accident is 1 gallon per minute and that
the reactor coolant activity levels of
DOSE EQUIVALENT I–131 are at the TS
values before the accident.
The proposed change does not affect
the design of the SGs, their method of
operation, or primary coolant chemistry
controls. The proposed approach
updates the current TSs and enhances
the requirements for SG inspections.
The proposed change does not adversely
impact any other previously evaluated
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design basis accident and is an
improvement over the current TSs.
Therefore, the proposed change does
not affect the consequences of a SGTR
accident and the probability of such an
accident is reduced. In addition, the
proposed changes do not affect the
consequences of an MSLB, rod ejection,
or a reactor coolant pump locked rotor
event, or other previously evaluated
accident.
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Criterion 2—The Proposed Change Does
Not Create the Possibility of a New or
Different Kind of Accident From Any
Previously Evaluated
The proposed performance based
requirements are an improvement over
the requirements imposed by the
current technical specifications.
Implementation of the proposed SG
Program will not introduce any adverse
changes to the plant design basis or
postulated accidents resulting from
potential tube degradation. The result of
the implementation of the SG Program
will be an enhancement of SG tube
performance. Primary to secondary
LEAKAGE that may be experienced
during all plant conditions will be
monitored to ensure it remains within
current accident analysis assumptions.
The proposed change does not affect
the design of the SGs, their method of
operation, or primary or secondary
coolant chemistry controls. In addition,
the proposed change does not impact
any other plant system or component.
The change enhances SG inspection
requirements.
Therefore, the proposed change does
not create the possibility of a new or
different type of accident from any
accident previously evaluated.
Criterion 3—The Proposed Change Does
Not Involve a Significant Reduction in
the Margin of Safety
The SG tubes in pressurized water
reactors are an integral part of the
reactor coolant pressure boundary and,
as such, are relied upon to maintain the
primary system’s pressure and
inventory. As part of the reactor coolant
pressure boundary, the SG tubes are
unique in that they are also relied upon
as a heat transfer surface between the
primary and secondary systems such
that residual heat can be removed from
the primary system. In addition, the SG
tubes isolate the radioactive fission
products in the primary coolant from
the secondary system. In summary, the
safety function of an SG is maintained
by ensuring the integrity of its tubes.
Steam generator tube integrity is a
function of the design, environment,
and the physical condition of the tube.
The proposed change does not affect
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15:19 Mar 27, 2006
Jkt 208001
tube design or operating environment.
The proposed change is expected to
result in an improvement in the tube
integrity by implementing the SG
Program to manage SG tube inspection,
assessment, repair, and plugging. The
requirements established by the SG
Program are consistent with those in the
applicable design codes and standards
and are an improvement over the
requirements in the current TSs.
For the above reasons, the margin of
safety is not changed and overall plant
safety will be enhanced by the proposed
change to the TS.
The NRC staff proposes to determine
that the amendments request involves
no significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L.
Marshall, Jr.
Tennessee Valley Authority, Docket No.
50–390, Watts Bar Nuclear Plant, Unit 1,
Rhea County, Tennessee
Date of amendment request:
December 15, 2005.
Description of amendment request:
The amendment would revise the
Technical Specifications (TS) to adopt
NRC-approved Revision 4 to Technical
Specification Task Force (TSTF)
Standard Technical Specification
Change Traveler, TSTF–449, ‘‘Steam
Generator Tube Integrity.’’ The
proposed amendment includes:
—Revised TS definition of Leakage,
—Revised TS 3.4.13, ‘‘RCS [Reactor
Coolant System] Operational
Leakage,’’
—Added new TS 3.4.17, ‘‘Steam
Generator Tube Integrity,’’
—Revised TS 5.7.2.12, ‘‘Steam
Generator (SG) Tube Surveillance
Program,’’ and
—Revised TS 5.9.9, ‘‘SG Tube
Inspection Report.’’
The proposed changes are necessary in
order to implement the guidance for the
industry initiative on NEI 97–06,
‘‘Steam Generator Program Guidelines.’’
The NRC staff issued a notice of
opportunity for comment in the Federal
Register on March 2, 2005 (70 FR
10298), on possible amendments
adopting TSTF–449, including a model
safety evaluation and model no
significant hazards consideration
(NSHC) determination, using the
consolidated line item improvement
process. The NRC staff subsequently
issued a notice of availability of the
models for referencing in license
amendment applications in the Federal
Register on May 6, 2005 (70 FR 24126).
PO 00000
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Sfmt 4703
15489
The licensee affirmed the applicability
of the following NSHC determination in
its application dated December 15,
2005.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
Criterion 1—The Proposed Change Does
Not Involve a Significant Increase in the
Probability or Consequences of an
Accident Previously Evaluated
The proposed change requires a SG
Program that includes performance
criteria that will provide reasonable
assurance that the SG tubing will retain
integrity over the full range of operating
conditions (including startup, operation
in the power range, hot standby,
cooldown and all anticipated transients
included in the design specification).
The SG performance criteria are based
on tube structural integrity, accident
induced leakage, and operational
LEAKAGE.
A steam generator tube rupture
(SGTR) event is one of the design basis
accidents that are analyzed as part of a
plant’s licensing basis. In the analysis of
a SGTR event, a bounding primary to
secondary LEAKAGE rate equal to the
operational LEAKAGE rate limits in the
licensing basis plus the LEAKAGE rate
associated with a double-ended rupture
of a single tube is assumed.
For other design basis accidents such
as a main steamline break (MSLB), rod
ejection, and reactor coolant pump
locked rotor the tubes are assumed to
retain their structural integrity (i.e., they
are assumed not to rupture). These
analyses typically assume that primary
to secondary LEAKAGE for all SGs is 1
gallon per minute or increases to 1
gallon per minute as a result of accident
induced stresses. The accident induced
leakage criterion introduced by the
proposed changes accounts for tubes
that may leak during design basis
accidents. The accident induced leakage
criterion limits this leakage to no more
than the value assumed in the accident
analysis.
The SG performance criteria proposed
change to the TS identify the standards
against which tube integrity is to be
measured. Meeting the performance
criteria provides reasonable assurance
that the SG tubing will remain capable
of fulfilling its specific safety function
of maintaining reactor coolant pressure
boundary integrity throughout each
operating cycle and in the unlikely
event of a design basis accident. The
performance criteria are only a part of
the SG Program required by the
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cprice-sewell on PROD1PC66 with NOTICES
proposed change to the TS. The
program, defined by NEI 97–06, Steam
Generator Program Guidelines, includes
a framework that incorporates a balance
of prevention, inspection, evaluation,
repair, and leakage monitoring. The
proposed changes do not, therefore,
significantly increase the probability of
an accident previously evaluated.
The consequences of design basis
accidents are, in part, functions of the
DOSE EQUIVALENT I–131 in the
primary coolant and the primary to
secondary LEAKAGE rates resulting
from an accident. Therefore, limits are
included in the plant technical
specifications for operational leakage
and for DOSE EQUIVALENT I–131 in
primary coolant to ensure the plant is
operated within its analyzed condition.
The typical analysis of the limiting
design basis accident assumes that
primary to secondary leak rate after the
accident is 1 gallon per minute and that
the reactor coolant activity levels of
DOSE EQUIVALENT I–131 are at the TS
values before the accident.
The proposed change does not affect
the design of the SGs, their method of
operation, or primary coolant chemistry
controls. The proposed approach
updates the current TSs and enhances
the requirements for SG inspections.
The proposed change does not adversely
impact any other previously evaluated
design basis accident and is an
improvement over the current TSs.
Therefore, the proposed change does
not affect the consequences of a SGTR
accident and the probability of such an
accident is reduced. In addition, the
proposed changes do not affect the
consequences of an MSLB, rod ejection,
or a reactor coolant pump locked rotor
event, or other previously evaluated
accident.
Criterion 2—The Proposed Change Does
Not Create the Possibility of a New or
Different Kind of Accident From Any
Previously Evaluated
The proposed performance based
requirements are an improvement over
the requirements imposed by the
current technical specifications.
Implementation of the proposed SG
Program will not introduce any adverse
changes to the plant design basis or
postulated accidents resulting from
potential tube degradation. The result of
the implementation of the SG Program
will be an enhancement of SG tube
performance. Primary to secondary
LEAKAGE that may be experienced
during all plant conditions will be
monitored to ensure it remains within
current accident analysis assumptions.
The proposed change does not affect
the design of the SGs, their method of
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Jkt 208001
operation, or primary or secondary
coolant chemistry controls. In addition,
the proposed change does not impact
any other plant system or component.
The change enhances SG inspection
requirements.
Therefore, the proposed change does
not create the possibility of a new or
different type of accident from any
accident previously evaluated.
Criterion 3—The Proposed Change Does
Not Involve a Significant Reduction in
the Margin of Safety
The SG tubes in pressurized water
reactors are an integral part of the
reactor coolant pressure boundary and,
as such, are relied upon to maintain the
primary system’s pressure and
inventory. As part of the reactor coolant
pressure boundary, the SG tubes are
unique in that they are also relied upon
as a heat transfer surface between the
primary and secondary systems such
that residual heat can be removed from
the primary system. In addition, the SG
tubes isolate the radioactive fission
products in the primary coolant from
the secondary system. In summary, the
safety function of an SG is maintained
by ensuring the integrity of its tubes.
Steam generator tube integrity is a
function of the design, environment,
and the physical condition of the tube.
The proposed change does not affect
tube design or operating environment.
The proposed change is expected to
result in an improvement in the tube
integrity by implementing the SG
Program to manage SG tube inspection,
assessment, repair, and plugging. The
requirements established by the SG
Program are consistent with those in the
applicable design codes and standards
and are an improvement over the
requirements in the current TSs.
For the above reasons, the margin of
safety is not changed and overall plant
safety will be enhanced by the proposed
change to the TS.
The NRC staff proposes to determine
that the amendments request involves
no significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L.
Marshall, Jr.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Units 1 and
2, Somervell County, Texas
Date of amendment request:
December 12, 2005.
Brief description of amendments: The
amendments requested would revise
Technical Specification (TS) 3.3.1, ‘‘RTS
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Fmt 4703
Sfmt 4703
[Reactor Trip System] Instrumentation,’’
Surveillance Requirements (SRs) 3.3.1.2
and SR 3.3.1.3.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No. Overall protection
system performance will remain within
the bounds of the previously performed
accident analyses since there are no
hardware changes. The Reactor Trip
System (RTS) Instrumentation will be
unaffected. Protection systems will
continue to function in a manner
consistent with the plant design basis.
All design, material, and construction
standards that were applicable prior to
the request are maintained.
The probability and consequences of
accidents previously evaluated in the
Final Safety Analysis Report (FSAR) are
not adversely affected because the
change to the daily surveillance for the
normalization of the Nuclear
Instrumentation System (NIS) Power
Range and Nitrogen-16 (N–16) Power
Monitor indications assures the
conservative response of the channel
even at reduced power levels.
The proposed changes will not affect
the probability of any event initiators.
There will be no degradation in the
performance of, or an increase in the
number of challenges imposed on,
safety-related equipment assumed to
function during an accident situation.
There will be no change to normal plant
operating parameters or accident
mitigation performance.
The proposed changes will not alter
any assumptions or change any
mitigation actions in the radiological
consequence evaluations in the FSAR.
Therefore, the proposed changes do
not involve a significant increase in the
probability or consequences of an
accident previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No. There are no hardware
changes nor are there any changes in the
method by which any safety-related
plant system performs its safety
function. This amendment will not
affect the normal method of plant
operation or change any operating
parameters. No performance
requirements or response time limits
will be affected.
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No new accident scenarios, transient
precursors, failure mechanisms, or
limiting single failures are introduced as
a result of this amendment. There will
be no adverse effect or challenges
imposed on any safety-related system as
a result of this amendment.
Therefore, the proposed change does
not create the possibility of a new or
different kind of accident from any
previously evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of
safety?
Response: No. The proposed changes
require a revision to the criteria for
implementation of NIS Power Range
and N–16 Power Monitor indication
adjustments based on secondary power
calorimetric calculations; however, the
changes do not eliminate any RTS
surveillances or alter the frequency of
surveillances required by the TS. The
revision to the criteria for
implementation of the daily
surveillance will remove a requirement
for normalization of the NIS Power
Range and N–16 Power Monitor
indications at reduced power conditions
that could result in safety performance
outside the bounds of the safety
analyses. Therefore, the Nominal Trip
Setpoints and Allowable Values for the
Reactor Trip System functions, as
specified in the TS and related Bases, as
well as the safety analysis limits
assumed in the transient and accident
analyses, are unchanged. None of the
acceptance criteria for any accident
analysis is changed.
There will be no effect on the manner
in which safety limits or limiting safety
systems settings are determined nor will
there be any effect on those plant
systems necessary to assure the
accomplishment of protection functions.
There will be no impact on the
overpower limit, departure from
nucleate boiling ratio (DNBR) limits,
heat flux hot channel factor (FQ),
nuclear enthalpy rise hot channel factor
(FDH), loss of coolant accident peak
cladding temperature (LOCA PCT), peak
local power density, or any other margin
of safety. The radiological dose
consequences are unaffected by this
proposed change.
The imposition of appropriate
surveillance testing requirements will
not reduce any margin of safety since
the changes will assure that safety
analysis assumptions on equipment
operability are verified on a periodic
frequency.
Therefore the proposed change does
not involve a reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
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15:19 Mar 27, 2006
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review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: George L. Edgar,
Esq., Morgan, Lewis and Bockius, 1800
M Street, NW., Washington, DC 20036.
NRC Branch Chief: David Terao.
Previously Published Notices of
Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The following notices were previously
published as separate individual
notices. The notice content was the
same as above. They were published as
individual notices either because time
did not allow the Commission to wait
for this biweekly notice or because the
action involved exigent circumstances.
They are repeated here because the
biweekly notice lists all amendments
issued or proposed to be issued
involving no significant hazards
consideration.
For details, see the individual notice
in the Federal Register on the day and
page cited. This notice does not extend
the notice period of the original notice.
Florida Power and Light Company,
Docket No. 50–389, St. Lucie Plant, Unit
No. 2, St. Lucie County, Florida
Date of amendment request: February
14, 2006.
Description of amendment request:
Revise the Technical Specifications
regarding the Containment Ventilation
System to allow additional corrective
actions for inoperable containment
purge supply and exhaust valves.
Date of publication of individual
notice in the Federal Register: March
1, 2006 (71 FR 10566).
Expiration date of individual notice:
March 15, 2006.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
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15491
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
Carolina Power & Light Company, et al.,
Docket No. 50–400, Shearon Harris
Nuclear Power Plant, Unit 1, Wake and
Chatham Counties, North Carolina
Date of application for amendment:
June 20, 2005, as supplemented by letter
dated November 2, 2005.
Brief description of amendment: This
amendment revises the footnotes in
Tables 3.4–2 and 4.4–3 of Technical
Specification (TS) 3/4.4.7 by increasing
the temperature limit above which (1)
reactor coolant sampling and analysis
for dissolved oxygen is required, and (2)
when limit for dissolved oxygen,
specified in TS 4.4.7, applies. This
temperature limit will be increased from
180 °F to 250 °F.
Date of issuance: March 8, 2006.
Effective date: March 8, 2006.
Amendment No. 120.
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Facility Operating License No. NPF–
63: Amendment revises the Technical
Specifications.
Date of initial notice in Federal
Register: October 11, 2005 (70 FR
59084). The supplemental letter
provided clarifying information that was
within the scope of the initial notice
and did not change the initial proposed
no significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 8, 2006.
No significant hazards consideration
comments received: No.
cprice-sewell on PROD1PC66 with NOTICES
Carolina Power & Light Company, et al.,
Docket No. 50–400, Shearon Harris
Nuclear Power Plant, Unit 1, Wake and
Chatham Counties, North Carolina
Date of application for amendment:
September 1, 2005, as supplemented by
letters dated December 22, 2005, and
January 23, 2006.
Brief description of amendment: This
amendment revises the technical
specification (TS) requirements for
pressurized-water reactor Boraflex fuel
storage racks and adds TS requirements
for fuel storage pool boron
concentration. Specifically, the
amendment (1) adds a new TS 3/4.7.14,
‘‘Fuel Storage Pool Boron
Concentration,’’ with a Limiting
Condition for Operation that requires a
fuel pool boron concentration of at least
2000 ppm at all times, (2) revises and
reformats TS 5.6.1 to specify the design
features and fuel storage limitations in
accordance with the categorization of
spent fuel storage racks in various spent
fuel pools, and (3) revises TS 5.3.1 to
remove the cross-reference to TS 5.6.1.b.
Date of issuance: March 10, 2006.
Effective date: March 10, 2006.
Amendment No. 121.
Facility Operating License No. NPF–
63: Amendment revises the TS.
Date of initial notice in Federal
Register: November 8, 2005 (70 FR
67745). The supplemental letters
provided additional information that
was within the scope of the initial
notice and did not change the initial
proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 10, 2006.
No significant hazards consideration
comments received: No.
Dominion Nuclear Connecticut, Inc.,
Docket Nos. 50–336 and 50–423,
Millstone Power Station, Unit Nos. 2
and 3, New London County, Connecticut
Date of application for amendments:
February 25, 2005.
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15:19 Mar 27, 2006
Jkt 208001
Brief description of amendments: The
amendments made various
administrative changes to the Technical
Specifications (TSs).
Date of issuance: March 16, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 90 days from the date of
issuance.
Amendment Nos.: 291 and 229.
Facility Operating License Nos. DPR–
65 and NPF–49: The amendments
revised the TSs.
Date of initial notice in Federal
Register: March 29, 2005 (70 FR
15942).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 16, 2006.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket Nos. 50–373 and 50–374, LaSalle
County Station, Units 1 and 2, LaSalle
County, Illinois
Date of application for amendments:
December 17, 2004.
Brief description of amendments: The
amendments revised Appendix B,
Environmental Protection Plan (nonradiological), of the LaSalle County
Facility Operating Licenses.
Date of issuance: March 8, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment Nos.: 176/162.
Facility Operating License Nos. NPF–
11 and NPF–18: The amendments
revised the Environmental Protection
Plan.
Date of initial notice in Federal
Register: April 12, 2005 (70 FR 19115).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 8, 2006.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket Nos. 50–254 and 50–265, Quad
Cities Nuclear Power Station, Units 1
and 2, Rock Island County, Illinois
Date of application for amendments:
June 15, 2005.
Brief description of amendments: The
amendments revised Technical
Specification (TS) 3.3.2.2, ‘‘Feedwater
System and Main Turbine High Water
Level Trip Instrumentation,’’ to reflect a
design change in the instrumentation
logic that trips the three feedwater
pumps and main turbine.
Date of issuance: March 9, 2006.
Effective date: As of the date of
issuance and shall be implemented
prior to start-up from the spring 2006
refueling outage for Unit 2 and prior to
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start-up from the spring 2007 refueling
outage for Unit 1.
Amendment Nos.: 330/225.
Facility Operating License Nos. DPR–
29 and DPR–30: The amendments
revised the Technical Specifications and
Surveillance Requirements.
Date of initial notice in Federal
Register: August 30, 2005 (70 FR
51381).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 9, 2006.
No significant hazards consideration
comments received: No.
FirstEnergy Nuclear Operating
Company, et al. (FENOC), Docket No.
50–346, Davis-Besse Nuclear Power
Station, Unit 1, Ottawa County, Ohio
Date of application for amendment:
August, 20, 2004, as supplemented by
letters dated June 16 and December 6,
2005.
Brief description of amendment: The
amendment revised TS 3/4.8.1.1,‘‘A.C.
Sources—Operating,’’ by deleting
Surveillance Requirement (SR)
4.8.1.1.2.d.4, which requires verification
that the emergency diesel generator
auto-connected loads do not exceed the
2000-hour load limit. In addition, the
amendment revised TS 4/3.8.1.2, ‘‘A.C.
Sources—Shutdown,’’ to add exceptions
to SR 4.8.1.2 when performed in Modes
5 and 6. As a result of discussions held
on October 20, 2005, FENOC decided to
withdraw the portion of the amendment
request (LAR 01–0009) that requested
clarification of SR 4.8.1.1.b.
Date of issuance: March 2, 2006
Effective date: As of the date of
issuance and shall be implemented
within 120 days.
Amendment No.: 273.
Facility Operating License No. NPF–3:
Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: September 28, 2004 (69 FR
57989).
The June 16 and December 6, 2005,
supplements, contained clarifying
information and did not change the NRC
staff’s initial proposed finding of no
significant hazards consideration or
expand the scope of the original Federal
Register notice.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 2, 2006.
No significant hazards consideration
comments received: No.
FirstEnergy Nuclear Operating
Company, Docket No. 50–346, DavisBesse Nuclear Power Station, Unit 1,
Ottawa County, Ohio
Date of application for amendment:
May 2, 2005, as supplemented by letters
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dated August 28, September 15, 2005,
and January 12, 2006, and January 13,
February 9, and February 28, 2006.
Brief description of amendment: This
amendment revised the Technical
Specifications (TSs) Section 2.1.1,
‘‘Safety Limits—Reactor Core,’’ and TS
Section 2.2.1, ‘‘Limiting Safety
Settings—Reactor Protection System
Setpoints.’’ The amendment supports
the use of the Framatome Mark B–HTP
fuel design for Cycle 15, which is
scheduled to begin following the
refueling outage in March 2006.
Date of issuance: March 2, 2006
Effective date: As of the date of
issuance and shall be implemented
within 120 days.
Amendment No.: 274.
Facility Operating License No. NPF–3:
Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: May 24, 2005 (70 FR 29796).
The August 28, September 15, 2005,
and January 12, January 13, February 9,
and February 28, 2006, supplements,
contained clarifying information and
did not change the NRC staff’s initial
proposed finding of no significant
hazards consideration.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 2, 2006.
No significant hazards consideration
comments received: No.
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1, Washington County, Nebraska
Date of amendment request: August
11, 2005.
Brief description of amendment: The
amendment deleted the surveillance
requirement (SR) of TS 2.10.2(9)b(iii) to
verify shutdown margin every 8-hour
shift during low power physics testing.
This change made TS 2.10.2(9)b more
consistent with SR 3.1.7 of NUREG–
1432, ‘‘Standard Technical
Specifications Combustion Engineering
Plants, Revision 3.’’ In addition, the
Containment Structural Tests Report has
been deleted from TS 5.9.3c and several
administrative and editorial changes
were made.
Date of issuance: February 1, 2006.
Effective date: February 1, 2006 and
shall be implemented within 60 days
from the date of issuance.
Amendment No.: 237.
Renewed Facility Operating License
No. DPR–40: The amendment revised
the Technical Specifications.
Date of initial notice in Federal
Register: September 27, 2005 (70 FR
56503)
The Commission’s related evaluation
of the amendment is contained in a
safety evaluation dated February 1,
2006.
No significant hazards consideration
comments received: No.
cprice-sewell on PROD1PC66 with NOTICES
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
PPL Susquehanna, LLC, Docket Nos. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1
and 2), Luzerne County, Pennsylvania
Date of amendment request: August
25, 2005.
Brief description of amendment: The
amendment revised the definitions of
Channel Calibration, Channel Function
Test, and Logic System Functional Test
in accordance with the Technical
Specification Task Force Traveler
(TSTF)–205–A.
Date of issuance: March 10, 2006
Effective date: As of the date of
issuance and shall be implemented
within 30 days of issuance.
Amendment No.: 217.
Facility Operating License No. DPR–
46: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: October 11, 2005 (70 FR
59086).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 10, 2006
No significant hazards consideration
comments received: No.
Date of application for amendments:
June 27, 2005, as supplemented on
December 1, 2005, and February 28,
2006.
Brief description of amendments:
These amendments change the SSES 1
and 2 technical specifications for reactor
protection system and control rod block
instrumentation, oscillation power
range monitor instrumentation,
recirculation loops operating, shutdown
margin test—refueling, and the core
operating limits report. The
amendments modify the power range
neutron monitor system (PRNMS) by
installation of the General Electric
Nuclear Measurement Analysis and
Control PRNMS. The modification of
the PRNMS replaces analog technology
with a digital upgrade.
Date of issuance: March 3, 2006
Effective date: As of the date of
issuance and to be implemented prior to
startup following the Cycle 14 refueling
outage for Unit 1 and the Cycle 13
refueling outage for Unit 2.
Amendment Nos.: 230 and 207.
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15493
Facility Operating License Nos. NPF–
14 and NPF–22: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: September 13, 2005 (70 FR
54088).
The supplements dated December 1,
2005, and February 28, 2006, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 3, 2006.
No significant hazards consideration
comments received: No.
PPL Susquehanna, LLC, Docket No. 50–
388, Susquehanna Steam Electric
Station, Unit 2 (SSES 2), Luzerne
County, Pennsylvania
Date of application for amendment:
March 18, 2005, as supplemented on
February 28, 2006.
Brief description of amendment: The
amendment revises the SSES 2
Technical Specification 3.3.8.1, ‘‘Loss of
Power (LOP) Instrumentation,’’ to (1)
clarify that Condition A applies to the
LOP instrumentation associated with
both the Unit 1 and Unit 2 4.16 Kilovolt
(kV) Engineered Safeguards System
(ESS) buses since both the Unit 1 and
Unit 2 buses are required to support
Unit 2 operation, (2) add a new
Condition B to allow the LOP
instrumentation for two Unit 1 4.16kV
ESS buses in the same division to be
inoperable for up to 8 hours for the
performance of Surveillance
Requirement 3.8.1.19 on Unit 1. In
addition, the amendment revises the
SSES 2 TS 3.8.7, ‘‘Distribution
Systems—Operating,’’ to (1) eliminate
‘‘or more’’ and the plural to
‘‘subsystems’’ such that the condition
will read ‘‘one Unit 1 AC [alternating
current] electrical power distribution
subsystem inoperable,’’ and (2) add a
new Condition D for two Unit 1 AC
electrical power distribution subsystems
inoperable.
Date of issuance: March 16, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 208.
Facility Operating License No. NPF–
22: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: May 24, 2005 (70 FR 29800).
The supplement dated February 28,
2006, provided additional information
that clarified the application, did not
expand the scope of the application as
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originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 16, 2006.
No significant hazards consideration
comments received: No.
cprice-sewell on PROD1PC66 with NOTICES
PSEG Nuclear LLC, Docket No. 50–354,
Hope Creek Generating Station, Salem
County, New Jersey
Date of application for amendment:
February 4, 2005.
Brief description of amendment: The
amendment relocated the Transversing
In-Core Probe (TIP) system Technical
Specification (TS) to the Hope Creek
Generating Station Updated Final Safety
Analysis Report, as well as removed the
note on the TIP system from the Reactor
Protection System Instrumentation
Surveillance Requirements table.
Date of issuance: March 8, 2006.
Effective date: As of the date of
issuance, to be implemented within 60
days from date of issuance.
Amendment No.: 164.
Facility Operating License No. NPF–
57: This amendment revised the TSs.
Date of initial notice in Federal
Register: March 15, 2005 (70 FR
12750).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 8, 2006.
No significant hazards consideration
comments received: No.
R.E. Ginna Nuclear Power Plant, LLC,
Docket No. 50–244, R.E. Ginna Nuclear
Power Plant, Wayne County, New York
Date of application for amendment:
April 29, 2005, as supplemented on July
1 and November 21, 2005.
Brief description of amendment: The
amendment revised Technical
Specification 3.7.3, ‘‘Main Feedwater
Regulating Valves (MFRVs), Associated
Bypass Valves, and Main Feedwater
Pump Discharge Valves (MFPDVs),’’ to
allow the use of the main feedwater
isolation valves in lieu of the MFPDVs
to provide isolation capability to the
steam generators in the event of a steam
line break.
Date of issuance: March 16, 2006
Effective date: As of the date of
issuance to be implemented prior to
startup from the fall 2006 refueling
outage.
Amendment No.: 95.
Renewed Facility Operating License
No. DPR–18: Amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: June 7, 2005 (70 FR 33218).
The July 1 and November 21, 2005,
letters provided additional information
VerDate Aug<31>2005
15:19 Mar 27, 2006
Jkt 208001
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 16, 2006.
No significant hazards consideration
comments received: No.
No significant hazards consideration
comments received: No.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Unit Nos.
1 and 2, Somervell County, Texas
Date of amendment request: October
6, 2004, as supplemented by letters
dated September 16 and November 22,
2005.
Brief description of amendments: The
amendments revised the Technical
Tennessee Valley Authority, Docket No.
50–327, Sequoyah Nuclear Plant, Unit 1, Specification 3.8.1, ‘‘AC Sources—
Operating,’’ to remove mode restrictions
Hamilton County, Tennessee
on surveillance requirements.
Date of application for amendment:
Date of issuance: March 15, 2006.
August 31, 2005.
Effective date: As of the date of
Brief description of amendment: The
issuance and shall be implemented
amendment revises the Technical
within 120 days from the date of
Specifications associated with steam
issuance.
generator tube integrity consistent with
Amendment Nos.: 124.
Revision 4 to Technical Specification
Facility Operating License Nos. NPF–
Task Force (TSTF) Standard Technical
87 and NPF–89: The amendments
Specification Change Traveler, TSTF–
revised the Technical Specifications.
449, ‘‘Steam Generator Tube Integrity.’’
Date of initial notice in Federal
Date of issuance: February 23, 2006.
Register: March 15, 2005 (70 FR
Effective date: As of the date of
12751).
issuance and shall be implemented
The supplements dated September 16
within 45 days.
and November 22, 2005, provided
Amendment No.: 306.
additional information that clarified the
Facility Operating License No. DPR–
application, did not expand the scope of
77: Amendment revises the technical
the application as originally noticed,
specifications.
and did not change the staff’s original
Date of initial notice in Federal
proposed no significant hazards
Register: November 22, 2005 (70 FR
consideration determination as
70643).
published in the Federal Register.
The Commission’s related evaluation
The Commission’s related evaluation
of the amendment is contained in a
of the amendments is contained in a
Safety Evaluation dated February 23,
Safety Evaluation dated March 15, 2006.
2006.
No significant hazards consideration
No significant hazards consideration
comments received: No.
comments received: No.
TXU Generation Company LP, Docket
No. 50–446, Comanche Peak Steam
Electric Station, Unit No. 2, Somervell
County, Texas
Date of amendment request: April 27,
2005, as supplemented by letter dated
July 20, 2005.
Description of amendment: The
amendment revises the Technical
Specifications to add Topical Report
WCAP–13060–P–A to the list of NRC
approved methodologies to be used at
Comanche Peak Steam Electric Station,
Unit 2.
Date of issuance: March 15, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment No.: 123.
Facility Operating License No. NPF–
89: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: November 8, 2005 (70 FR
67753).
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Dated at Rockville, Maryland, this 20th day
of March 2006.
For the Nuclear Regulatory Commission.
Edwin M. Hackett,
Deputy Director, Division of Operating
Reactor Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. 06–2908 Filed 3–27–06; 8:45 am]
BILLING CODE 7590–01–P
OFFICE OF PERSONNEL
MANAGEMENT
Excepted Service
Office of Personnel
Management (OPM).
ACTION: Notice.
AGENCY:
SUMMARY: This gives notice of OPM
decisions granting authority to make
appointments under Schedules A, B,
and C in the excepted service as
required by 5 CFR 6.6 and 213.103.
FOR FURTHER INFORMATION CONTACT:
David Guilford, Center for Leadership
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Agencies
[Federal Register Volume 71, Number 59 (Tuesday, March 28, 2006)]
[Notices]
[Pages 15479-15494]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: 06-2908]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a(2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the
[[Page 15480]]
Commission publish notice of any amendments issued, or proposed to be
issued and grants the Commission the authority to issue and make
immediately effective any amendment to an operating license upon a
determination by the Commission that such amendment involves no
significant hazards consideration, notwithstanding the pendency before
the Commission of a request for a hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from March 3, 2006 to March 16, 2006. The last
biweekly notice was published on March 14, 2006 (71 FR 13169).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The
filing of requests for a hearing and petitions for leave to intervene
is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site,
https://www.nrc.gov/reading-rm/doc-collections/cfr/.
If a request
for a hearing or petition for leave to intervene is filed within
60 days, the Commission or a presiding officer designated by the
Commission or by the Chief Administrative Judge of the Atomic
Safety and Licensing Board Panel, will rule on the request
and/or petition; and the Secretary or the Chief Administrative
Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to
[[Page 15481]]
participate fully in the conduct of the hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site,
https://www.nrc.gov/reading-rm/adams.html.
If you do not have access
to ADAMS or if there are problems in accessing the documents
located in ADAMS, contact the PDR Reference staff at
1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket No. 50-461, Clinton Power Station,
Unit 1, DeWitt County, Illinois
Date of amendment request: December 1, 2006.
Description of amendment request: The proposed amendment would
revise Technical Specification (TS) 3.6.4.1, ``Secondary Containment.''
Specifically, the change would modify Surveillance Requirements (SRs)
3.6.4.1.4 and 3.6.4.1.5 to clarify their intent with respect to
secondary containment boundary integrity. The change is submitted in
accordance with the TS Task Force Traveler 322-A, Revision 2,
``Secondary Containment and Shield Building Boundary Integrity SRs.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No. This change involves an administrative clarification
to reflect the original intent of the Technical Specifications. There
is no impact on the availability or capability of the secondary
containment or Standby Gas Treatment (SGT) system as a result of the
proposed change. Both the secondary containment and SGT system are
considered accident-mitigating equipment and are not initiators of any
previously evaluated accidents. Therefore, the proposed change does not
involve an increase in the probability of an accident previously
evaluated. Additionally, the proposed change does not alter the
secondary containment or SGT systems' performance measures or their
ability to perform their accident mitigation functions.
Therefore, the proposed change does not involve a significant
increase in the consequences of an accident previously evaluated.
2. Does the proposed amendment create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No. The proposed changes to the wording of TS SRs
3.6.4.1.4 and 3.6.4.1.5 clarify that only one SGT subsystem is required
to ensure the requirements of TS 3.6.4.1 are met. The proposed change
does not alter the parameters within which the plant is operated. There
are no new system operating conditions or performance measures
introduced by this proposed change that will affect the secondary
containment and SGT systems' protective or mitigative functions. The
proposed changes will not alter the methods in which equipment is
operated or tested. No new accident scenarios or assumptions, failure
mechanisms, or limiting single failures are introduced as a result of
the proposed change.
Therefore, the proposed change does not create the possibility of a
new or different kind of accident from any previously evaluated.
3. Does the proposed amendment involve a significant reduction in a
margin of safety?
Response: No. Margins of safety are established in the design of
components, the configuration of components to meet certain performance
parameters, and in the establishment of setpoints to initiate alarms or
actions. The proposed change does not impact any of these margins of
safety parameters. This change involves an administrative clarification
to reflect the original intent of the TS. There is no adverse effect on
the operability or design requirements of the secondary containment or
SGT system. The equipment will continue to be tested in a manner and at
a frequency necessary to provide confidence that the equipment can
perform its intended safety function. There is no impact on the plant
safety analyses.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. Bradley J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Kennett
Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
[[Page 15482]]
Calvert Cliffs Nuclear Power Plant, Inc., Docket Nos. 50-317 and 50-
318, Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert
County, Maryland
Date of amendments request: February 27, 2006.
Description of amendments request: The amendment would revise
Technical Specification 4.2.1, ``Fuel Assemblies,'' to allow fuel with
advanced cladding material to be installed in the core for Cycle 19
only at Unit No. 1 or Cycle 17 only at Unit No. 2. Advanced cladding
material from Framatome-ANP may be used in up to 2 lead test
assemblies, and advanced cladding material from Westinghouse may be
used in up to 2 lead test assemblies.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Would not involve a significant increase in the probability or
consequences of an accident previously evaluated.
Calvert Cliffs Technical Specification 4.2.1, Fuel Assemblies,
states that fuel rods are clad with either Zircaloy or
ZIRLOTM. Calvert Cliffs Nuclear Power Plant, Inc. proposes
to re-insert up to four fuel assemblies into Calvert Cliffs Unit 1 or
Unit 2 that have some fuel rods clad in zirconium alloys that do not
meet the definition of Zircaloy or ZIRLOTM. A temporary
exemption to the regulations has also been requested to allow these
fuel assemblies to be re-inserted into Unit 1 or Unit 2. The proposed
change to the Calvert Cliffs Technical Specifications will allow the
use of cladding materials that are not Zircaloy or ZIRLOTM
for one fuel cycle once the temporary exemption is approved. The
proposed change to the Technical Specification is effective only as
long as the temporary exemption is effective. The addition of what will
be an approved temporary exemption for Unit 1 or Unit 2 to Technical
Specification 4.2.1 does not change the probability or consequences of
an accident previously evaluated.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident previously
evaluated.
2. Would not create the possibility of a new or different [kind] of
accident from any accident previously evaluated.
The proposed change does not add any new equipment, modify any
interfaces with existing equipment, change the equipment's function, or
change the method of operating the equipment. The proposed change does
not affect normal plant operations or configuration. Since the proposed
change does not change the design, configuration, or operation, it
could not become an accident initiator.
Therefore, the proposed change does not create the possibility of a
new or different [kind] of accident from any previously evaluated.
3. Would not involve a significant reduction in [a] margin of
safety.
The proposed change will add an approved temporary exemption to the
Calvert Cliffs Technical Specifications allowing the installation of up
to four lead fuel assemblies. The assemblies use advanced cladding
materials that are not specifically permitted by existing regulations
or Calvert Cliffs' Technical Specifications. A temporary exemption to
allow the installation of these assemblies has been requested. The
addition of an approved temporary exemption to Technical Specification
4.2.1 is an administrative change to allow the installation of the lead
fuel assemblies under the provisions of the temporary exemption. The
license amendment is effective only as long as the exemption is
effective. This amendment does not change the margin of safety since it
only adds a reference to an approved, temporary exemption to the
Technical Specifications.
Therefore, the proposed change does not involve a significant
reduction in [a] margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendments request involves no significant hazards consideration.
Attorney for licensee: Carey Fleming, Sr. Counsel--Nuclear
Generation, Constellation Generation Group, LLC, 750 East Pratt Street,
17th floor, Baltimore, MD 21202.
NRC Branch Chief: Richard J. Laufer.
Duke Energy Corporation, Docket Nos. 50-269, 50-270, and 50-287, Oconee
Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
Date of amendment request: January 5, 2005, supplemented November
21, 2005.
Description of amendment request: The proposed amendments would
revise the Technical Specification (TS) 5.5.19.b, TS 5.5.19.c, and TS
Surveillance Requirement (SR) 3.8.1.9. TS 5.5.19.b currently requires
verification that a Lee Combustion Turbine (LCT) can supply the
equivalent of one Unit's maximum safeguard loads, plus two Units' Mode
3 loads, when connected to the system grid every 12 months. In the
proposed amendments, this requirement would be more clearly specified
as, ``Verify an LCT can supply equivalent of one Unit's Loss of Coolant
Accident (LOCA) loads plus two Unit's Loss of Offsite Power (LOOP)
loads when connected to system grid every 12 months.'' TS 5.5.19.b and
SR 3.8.1.9 would be revised for consistency.
This notice supersedes the notice published in the Federal Register
on February 15, 2005 (70 FR 7764).
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
(1) Involve a significant increase in the probability or
consequences of an accident previously evaluated:
Duke proposes to revise TS 5.5.19.b to clarify the Lee Combustion
Turbine (LCT) testing requirements. Duke proposes to revise TS 5.5.19.c
and TS 3.8.1 Surveillance Requirement (SR) 3.8.1.19 to be consistent
with the proposed change to TS 5.5.19.b. The proposed change makes the
wording of the test requirement consistent with the UFSAR [Updated
Final Safety Analysis Report]. LCT testing has no impact on the
probability of an accident analyzed in the UFSAR. The LCT can be
credited to mitigate the consequences of an accident analyzed in the
UFSAR. However, this clarification of LCT testing requirements has no
impact on its ability to mitigate the consequences of an accident. As
such, the proposed LAR [license amendment request] does not involve a
significant increase in the probability or consequences of an accident
previously evaluated.
(2) Create the possibility of a new or different kind of accident
from any kind of accident previously evaluated:
Duke proposes to revise TS 5.5.19.b to clarify the Lee Combustion
Turbine (LCT) testing requirements. Duke proposes to revise TS 5.5.19.c
and TS 3.8.1 SR 3.8.1.9 to be consistent with the proposed change to TS
5.5.19.b. The proposed change makes the wording of the test requirement
consistent with the UFSAR. These changes do not alter the nature of
events postulated in the Safety Analysis Report nor do they introduce
any unique precursor mechanisms. Therefore, the proposed amendment will
not create the possibility of a new or different kind of accident from
any accident previously evaluated.
(3) Involve a significant reduction in a margin of safety:
[[Page 15483]]
The proposed TS change does not unfavorably affect any plant safety
limits, set points, or design parameters. The changes also do not
unfavorably affect the fuel, fuel cladding, RCS [reactor coolant
system], or containment integrity. Therefore, the proposed TS change,
which clarifies TS requirements associated with the LCT testing
program, does not involve a significant reduction in the margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Ms. Lisa F. Vaughn, Legal Department
(PB05E), Duke Energy Corporation, 422 South Church Street, Charlotte,
North Carolina 28201-1006.
NRC Branch Chief: Evangelos C. Marinos.
Exelon Generation Company, LLC, Docket Nos. 50-373 and 50-374, LaSalle
County Station, Units 1 and 2, LaSalle County, Illinois
Date of amendment request: March 13, 2006.
Description of amendment request: The proposed amendments would
make changes to the technical specifications (TS) for LaSalle County
Station (LSCS), Units 1 and 2. Surveillance Requirement (SR) 3.7.3.1
verifies the cooling water temperature supplied to the plant from the
core standby cooling system (CSCS) pond (i.e., the ultimate heat sink
(UHS)) is <= 100 [deg]F. Currently, if the temperature of the cooling
water supplied to the plant from the CSCS pond is > 100 [deg]F, the UHS
must be declared inoperable in accordance with TS 3.7.3. TS 3.7.3,
Required Action B.1, requires that both units be placed in Mode 3
within 12 hours and Required Action B.2 requires that both units be
placed in Mode 4 within 36 hours.
Prolonged hot weather in the area during the summer months, in
conjunction with high humidity during the daytime, minimal cooling at
night and little precipitation, has resulted in sustained elevated
cooling water temperature supplied to the plant from the CSCS pond.
This license amendment is being requested to increase the temperature
limit of the cooling water supplied to the plant from the CSCS pond to
<= 101.5 [deg]F by reducing the temperature measurement uncertainty by
replacing the existing thermocouples with higher precision temperature
measuring equipment. Should the UHS indicated temperature exceed 101.5
[deg]F, Required Action B.1 would be entered and both units would be
placed in Mode 3 within 12 hours and Mode 4 within 36 hours.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed change does not involve a significant increase in
the probability or consequences of an accident previously evaluated?
The proposed change will allow the indicated temperature of the cooling
water supplied to the plant from the CSCS pond to be increased to <=
101.5 [deg]F based on reducing the temperature measurement uncertainty
by replacing the existing thermocouples with higher precision
temperature measuring equipment.
Analyzed accidents are assumed to be initiated by the failure of
plant structures, systems, or components. An inoperable UHS is not
considered as an initiator of any analyzed events. As such, there is
not a significant increase in the probability of a previously evaluated
accident. Allowing the UHS to operate at a higher allowable indicated
temperature, but still within the design limits of the equipment it
supplies, will not affect the failure probability of that equipment.
The current heat analyses calculations of record for LSCS, Units 1 and
2, assume a UHS temperature of 100 [deg]F and post-accident peak inlet
temperature of 104 [deg]F. The proposed temperature increase is based
solely on a reduction of the existing instrument loop uncertainty
value. The current analysis bounds the proposed change. This higher
allowable indicated temperature does not impact the LOCA [loss-of-
coolant accident] Peak Clad Temperature Analysis, LOCA Containment
Analysis or the non-LOCA analyses; therefore, continued operation with
a UHS temperature > 100 [deg]F but <= 101.5 [deg]F will not increase
the consequences of an accident previously evaluated in the UFSAR.
Based on the above information, the increase in the allowable
indicated temperature of the cooling water supplied to the plant from
the UHS to <= 101.5 [deg]F by reducing the existing instrument loop
uncertainty value has no effect on the result of the design basis event
and will continue to allow each required heat exchanger to perform its
safety function. The heat exchangers will continue to provide
sufficient cooling for the heat loads during the most severe 30-day
period.
Based on the above information, increasing the allowable indicated
temperature of the cooling water supplied to the plant from the CSCS
pond from <= 100 [deg]F to <= 101.5 [deg]F by reducing the instrument
uncertainty value has no impact on any analyzed accident; therefore,
the proposed change does not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. The proposed change create the possibility of a new or different
kind of accident from any previously evaluated?
The proposed change involves replacing the presently installed
thermocouples with higher accuracy temperature measurement equipment.
This proposed action will not alter the manner in which equipment is
operated, nor will the functional demands on credited equipment be
changed. No alteration in the procedures that ensure the units remain
within analyzed limits is proposed, and no change is being made to
procedures relied upon to respond to an off-normal event. Raising the
UHS temperature limit does not introduce any new or different modes of
plant operation, nor does it affect the operational characteristics of
any safety-related equipment or systems; as such, no new failure modes
are being introduced. The proposed action reduces the instrument
uncertainty value but does not alter assumptions made in the safety
analysis.
Increasing the allowable indicated temperature of the cooling water
supplied to the plant from the CSCS pond from <= 100 [deg]F to <= 101.5
[deg]F has no impact on safety related systems. The plant is designed
such that the RHR [residual heat removal] pumps on the unit undergoing
the LOCA/LOOP [loss of offsite power] conditions would start upon the
receipt of a signal, and would load onto their respective Emergency
Diesel Generators emergency bus during the LOOP event. The increase in
the allowable indicated temperature of the cooling water supplied to
the plant from the CSCS pond will not require operation of additional
RHR pumps; therefore, system operation is unaffected by the proposed
change in the UHS temperature limit.
Based on the above information, the proposed change does not create
the possibility of a new or different kind of accident from any
previously evaluated.
3. The proposed change does not involve a significant reduction in
a margin of safety.
The proposed change allows an increase in the allowable indicated
temperature of the cooling water supplied to the plant from the CSCS
[[Page 15484]]
pond to <= 101.5 [deg]F. The margin of safety is determined by the
design and qualification of the plant equipment, the operation of the
plant within analyzed limits, and the point at which protective or
mitigative actions are initiated. The proposed action does not impact
these factors as the analyzed peak inlet temperature of the UHS is
unaffected based on the improved instrument uncertainty of the new high
precision temperature measurement instrumentation. No setpoints are
affected, and no other change is being proposed in the plant
operational limits as a result of this change. All accident analysis
assumptions and conditions will continue to be met. Adequate design
margin is available to ensure that the required margin of safety is not
significantly reduced.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Bradley J. Fewell, Assistant General
Counsel, Exelon Generation Company, LLC, 200 Exelon Way, Kennett
Square, PA 19348.
NRC Branch Chief: Daniel S. Collins.
FirstEnergy Nuclear Operating Company, et al., Docket No. 50-440, Perry
Nuclear Power Plant, Unit 1, Lake County, Ohio
Date of amendment request: February 14, 2006.
Description of amendment request: The proposed amendment would
revise the frequency of the Mode 5 Intermediate Range Monitoring (IRM)
Instrumentation CHANNEL FUNCTIONAL TEST contained in Technical
Specification (TS) 3.3.1.1 from 7 days to 31 days. The methodology used
for the IRM drift analysis is based upon guidance contained in Generic
Letter 91-04, ``Changes in Technical Specification Surveillance
Intervals to Accommodate a 24-month Fuel Cycle,'' and Electric Power
Institute Report TI-103335, ``Guidance for Instrument Calibration
Extension/Reduction Programs.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration which is presented below:
1. The proposed change does not involve a significant increase in
the probability or consequences of an accident previously evaluated.
The proposed Technical Specifications (TS) change involves an
increase in the Mode 5 CHANNEL FUNCTIONAL TEST interval for RPS
[Reactor Protection System] IRM channels from 7 days to 31 days. The
IRM system is used for event mitigation. The failure of an IRM does not
initiate an accident or transient event. The proposed TS change does
not alter the design or function of the IRM system for no physical
changes are being made to the plant. Evaluation of the proposed testing
interval change demonstrated that the availability of IRMs to mitigate
the consequences of a control rod withdrawal event at low power levels
are not significantly affected based on the effectiveness of other,
required TS surveillance testing that is performed, the availability of
redundant systems and equipment, and the high reliability of the IRM
equipment.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident previously
evaluated.
2. The proposed change does not create the possibility of a new or
different kind of accident from any accident previously evaluated.
The proposed TS change involves an increase in the Mode 5 IRM
CHANNEL FUNCTIONAL TEST interval from 7 clays [days] to 31 days.
Existing TS testing requirements ensure the operability of the IRMs.
The proposed TS change does not introduce any failure mechanisms of a
different type than those previously evaluated, since no physical
changes to the plant are being made. No new or different equipment is
being installed, and no installed equipment is being operated in a
different manner. As a result, no new failure modes are introduced. In
addition, the manner in which surveillance tests are performed remains
unchanged.
Therefore, the proposed TS change does not create the possibility
of a new or different kind of accident from any previously evaluated.
3. The proposed change does not involve a significant reduction in
a margin of safety.
The proposed TS change involves an increase in the Mode 5 CHANNEL
FUNCTIONAL TEST interval for RPS IRM channels from 7 days to 31 days.
There is expected to be no impact on system operability, based upon the
performance of the more frequent Channel Checks, Control Room
monitoring when the IRMs are in use, and the overall IRM reliability.
Furthermore, a historical review of surveillance test results and
associated maintenance records did not indicate evidence of any failure
that would invalidate the above conclusions.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David W. Jenkins, Attorney, FirstEnergy
Corporation, 76 South Main Street, Akron, OH 44308.
NRC Branch Chief: Mindy S. Landau, Acting.
Nine Mile Point Nuclear Station, LLC, Docket No. 50-220, Nine Mile
Point Nuclear Station Unit No. 1, Oswego County, New York
Date of amendment request: December 16, 2005.
Description of amendment request: The proposed change to Technical
Specification (TS) Surveillance Requirement (SR) 4.1.4d relocates the
SR for testing the core spray header differential pressure ([Delta]P)
instrumentation to licensee-controlled documents. TS SR 4.1.4d
currently requires that the core spray header [Delta]P instrumentation
be periodically tested such that a check of each sensor is performed at
least once each day and each channel is calibrated and tested at least
once every 3 months. The proposed change will allow these SRs to be
placed in licensee-controlled documents where future changes will be
made pursuant to Title 10 of the Code of Federal Regulations (10 CFR),
Section 50.59. The functional description of the core spray header
[Delta]P instrumentation will also be relocated from the TS Bases to
licensee-controlled documents consistent with the proposed TS change.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes are limited to the relocation of selected
instrumentation requirements. The proposed relocated requirements were
[[Page 15485]]
determined not to meet the 10 CFR 50.36 screening criteria for
retention in the TSs and will be maintained in licensee-controlled
documents in accordance with the provisions of 10 CFR 50.59. The
proposed changes do not introduce any new modes of plant operation,
make any physical changes to the plant, or alter any operational
setpoints which could degrade the performance of any safety system
assumed to function in the accident analysis. Therefore, the proposed
changes do not involve a significant increase in the probability or
consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No. The proposed changes do not introduce any new modes
of plant operation, make any physical changes to the plant, or alter
any operational setpoints which could create new accident initiators or
failure mechanisms. The proposed changes are limited to the relocation
of selected instrumentation requirements, and will have no impact on
the accident assumptions and initial conditions as previously analyzed
in the UFSAR [Updated Final Safety Analysis Report]. Therefore, the
proposed changes do not create the possibility of a new or different
kind of accident from any accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No. The proposed changes are consistent with the Improved
Standard TSs (NUREG-1433, Rev. 3) and will have no impact on the
instrumentation setpoints, logic, or functional requirements as
described in the TSs, TS Bases, and UFSAR. The proposed relocated
requirements were determined to not meet the 10 CFR 50.36 screening
criteria for retention in the TSs. Thus, the relocated requirements
will be maintained in accordance with 10 CFR 50.59 as required.
Accordingly, the proposed relocated requirements will not degrade the
quality or performance of any safety system assumed to mitigate an
accident or assure operation within the safety limits. Therefore, the
proposed changes do not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston &
Strawn, 1700 K Street, NW., Washington, DC 20006.
NRC Branch Chief: Richard J. Laufer.
PPL Susquehanna, LLC, Docket Nos. 50-387 and 50-388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1 and 2), Luzerne County,
Pennsylvania
Date of amendment request: February 28, 2006.
Description of amendment request: The proposed amendments would
change the SSES 1 and 2 Technical Specification (TS) Surveillance
Requirements (SRs) 3.8.4.7 and 3.8.4.8 to clarify that diesel generator
``E'' (DG E) electrical power subsystem testing does not require a mode
restriction when the DG E diesel is not required to be OPERABLE.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No. Performance of TS required SRs are not initiators to
any accident sequences analyzed in the Final Safety Analysis Report
(FSAR). The changes do not involve any physical change to structures,
systems, or components, (SSCs) and do not alter the method of operation
or control of SSCs. The current assumptions in the safety analysis
regarding accident initiators and mitigation of accidents are
unaffected by these changes. No additional failure modes or mechanisms
are being introduced and the likelihood of previously analyzed failures
remains unchanged.
Operation in accordance with the proposed Technical Specification
(TS) ensures that the DC [direct current] distribution system and
supported equipment functions remain capable of performing the function
as described in the FSAR. Therefore, the mitigative functions supported
by the system will continue to provide the protection assumed by the
analysis.
Therefore, this change does not involve a significant increase in
the probability or consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No. The proposed change does not involve a physical
alteration of the plant. No new equipment is being introduced, and
installed equipment is not being operated in a new or different manner.
There are no setpoints, at which protective or mitigative actions are
initiated, affected by this change. This change will not alter the
manner in which equipment operation is initiated, nor will the function
demands on credited equipment be changed. No alterations in the
procedures that ensure the plant remains within analyzed limits are
being proposed, and no changes are being made to the procedures relied
upon to respond to an off-normal event as described in the FSAR. As
such, no new failure modes are being introduced. The change does not
alter assumptions made in the safety analysis and licensing basis.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No. The margin of safety is established through equipment
design, operating parameters, and the setpoints at which automatic
actions are initiated. The proposed change is acceptable because
performance of SRs on equipment not require[d] to be OPERABLE and
isolated from the OPERABLE plant equipment cannot affect any margin of
safety. Therefore, the plant response to analyzed events will continue
to provide the margin of safety assumed by the analysis.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Bryan A. Snapp, Esquire, Assoc. General
Counsel, PPL Services Corporation, 2 North Ninth St., GENTW3,
Allentown, PA 18101-1179.
NRC Branch Chief: Richard J. Laufer
Southern California Edison Company (SCE), et al., Docket Nos. 50-361
and 50-362, San Onofre Nuclear Generating Station, Units 2 and 3 (SONGS
2 and 3), San Diego County, California
Date of amendment requests: March 10, 2006.
Description of amendment requests: The licensee requests the
Nuclear Regulatory Commission consent to the transfer of the City of
Anaheim's 3.16 percent undivided ownership interest in SONGS 2 and 3 to
Southern California Edison, excluding Anaheim's interest in its spent
fuel and the SONGS 2 and 3 independent spent fuel storage installation.
[[Page 15486]]
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No. The amendments do not involve any change in the
design, configuration, or operation of the nuclear plant. All Limiting
Conditions for Operation, Limiting Safety System Settings, and Safety
Limits specified in the Technical Specifications remain unchanged. SCE
will continue to be the licensed operator of the units.
The technical qualifications of SCE to carry out its exclusive
responsibilities under the operating licenses, as amended, will remain
unchanged. Personnel engaged in operation, maintenance, engineering,
assessment, training, and other related services are not changed. The
SCE officers and executives currently responsible for the overall safe
operation of the nuclear plants will continue in the same capacity.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident previously
evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No. The amendments do not involve any change in the
design, configuration, or operation of the nuclear plant. The current
plant design and design bases will remain the same. The current plant
safety analyses, therefore, remain complete and accurate in addressing
the design basis events and in analyzing plant response and
consequences.
The Limiting Conditions for Operation, Limiting Safety System
Settings, and Safety Limits specified in the Technical Specifications
are not affected by the change. As such, the plant conditions for which
the design basis accident analyses were performed remain valid.
The amendments do not introduce a new mode of plant operation or
new accident precursors, do not involve any physical alterations to
plant configurations, or make changes to system set points that could
initiate a new or different kind of accident.
Therefore, the proposed change does not create the possibility of a
new or different kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No. The amendments do not involve a change in the design,
configuration, or operation of the nuclear plants. The change does not
affect either the way in which the plant structures, systems, and
components perform their safety function, or their design and licensing
basis.
Plant safety margins are established through Limiting Conditions
for Operation, Limiting Safety System Settings, and Safety Limits
specified in the Technical Specifications. Because there is no change
to the physical design of the plant, there is no change to any of these
margins.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Attorney for licensee: Douglas K. Porter, Esquire, Southern
California Edison Company, 2244 Walnut Grove Avenue, Rosemead,
California 91770.
NRC Branch Chief: David Terao.
Southern Nuclear Operating Company, Inc., Docket Nos. 50-424 and 50-
425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County,
Georgia
Date of amendment request: September 19, 2005.
Description of amendment request: The proposed amendment would
revise Technical Specification (TS) Limiting Conditions for Operation
(LCO) 3.3.1, ``Reactor Trip system (RTS) Instrumentation'' and TS
Surveillance Requirements (SR) 3.2.4.2, ``Quadrant Power Tilt Ration
(QPTR)'' to avoid confusion as to when a flux map for QPTR is required.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in the
probability or consequences of an accident previously evaluated?
No. The proposed changes do not adversely affect accident
initiators or precursors nor alter the design assumptions, conditions,
or configuration of the facility or the manner in which the plant is
operated and maintained. The proposed changes do not alter or prevent
the ability of structures, systems, and components (SSCs) from
performing their intended function to mitigate the consequences of an
initiating event within the assumed acceptance limits. The proposed
changes do not affect the source term, containment isolation, or
radiological release assumptions used in evaluating the radiological
consequences of an accident previously evaluated. Further, the proposed
changes do not increase the types or amounts of radioactive effluent
that may be release offsite, nor significantly increase individual or
cumulative occupational/public radiation exposures. The proposed
changes are consistent with safety analysis assumptions and resultant
consequences.
Therefore, the proposed changes do not increase the probability or
consequences of an accident previously evaluated
2. Does the proposed change create the possibility of a new or
different kind of accident from any previously evaluated?
No. The proposed changes do not result in a change in the manner in
which the RTS and ESFAS provide plant protection. The RTS and ESFAS
will continue to have the same set points after the proposed changes
are implemented. There are no design changes associated with the
license amendment.
The changes do not involve a physical alteration of the plant
(i.e., no new or different type of equipment will be installed) or a
change in the methods governing normal plant operation. In addition,
the changes do not impose any new or different requirements or
eliminate any existing requirements. The changes do not alter
assumptions made in the safety analysis. The proposed changes are
consistent with the safety analysis assumptions and current plant
operating practice.
Therefore, the proposed changes do not create the possibility of a
new or different kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
No. The proposed changes do not alter the manner in which safety
limits, limiting safety system settings or limiting conditions for
operation are determined. The safety analysis acceptance criteria are
not impacted by these changes. Redundant RTS and ESFAS trains are
maintained, and diversity with regard to the signals that provide
reactor trip and engineered safety features actuation is also
[[Page 15487]]
maintained. All signals credited as primary or secondary, and all
operator actions credited in the accident analyses will remain the
same. The proposed changes will not result in plant operation in a
configuration outside the design basis.
Therefore, the proposed changes do not involve a significant
reduction in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders,
NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta,
Georgia 30308-2216.
NRC Branch Chief: Evangelos C. Marinos.
Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296,
Browns Ferry Nuclear Plant, Units 1, 2 and 3, Limestone County, Alabama
Date of amendment request: January 10, 2006 (TS-453).
Description of amendment request: The proposed amendment would
specify the methodology used for determining, setting, and evaluating
as-found setpoints for those drift susceptible instruments, which are
either necessary to ensure compliance with a Safety Limit or critical
in ensuring the fuel peak cladding temperature acceptance criteria of
10 CFR 50.46 are met.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No. Including references to TVA's methodology for
determining, setting, and evaluating as-found instrument setpoints in
the TS is an administrative change. There will be no change to the
manner in which Safety Limits, Analytical Limits, or Allowable Values
are determined. No changes are proposed in the manner in which the
Reactor Protection System (RPS), Emergency Core Cooling System (ECCS),
Reactor Core Isolation Cooling (RCIC), or Primary Containment Isolation
systems provide plant protection or which create new modes of plant
operation.
The proposed request will not affect the probability of any event
initiators. There will be no degradation in the performance of, or an
increase in the number of challenges imposed on, safety-related
equipment assumed to function during an accident situation. There will
be no change to normal plant operating parameters or accident
mitigation performance.
Therefore, the proposed amendment does not involve a significant
increase in the probability or consequences of an accident previously
evaluated.
2. Does the proposed amendment create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No. There are no hardware changes nor are there any
changes in the method by which any plant system performs a safety
function. This request does not affect the normal method of plant
operation. The proposed amendment does not introduce new equipment,
which could create a new or different kind of accident.
No new external threats, release pathways, or equipment failure
modes are created. No new accident scenarios, transient precursors,
failure mechanisms, or limiting single failures are introduced as a
result of this request. Therefore, the implementation of the proposed
amendment will not create a possibility for an accident of a new or
different type than those previously evaluated.
3. Does the proposed amendment involve a significant reduction in a
margin of safety?
Response: No. Including references to TVA's methodology for
determining, setting, and evaluating as-found instrument setpoints in
the TS is an administrative change. No changes are proposed in the
manner in which the RPS, ECCS, RCIC, or Primary Containment Isolation
systems satisfy the Updated Final Safety Analysis Report requirements
for accident mitigation or unit safe shutdown. There will be no change
to Safety Limits, Analytical Limits, Allowable Values, or post-Loss Of
Coolant Accident peak clad temperatures. For these reasons, the
proposed amendment does not involve a significant reduction in a margin
of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: General Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A, Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L. Marshall, Jr.
Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
Date of amendment request: February 6, 2006.
Description of amendment request: The proposed amendment would
modify technical specification (TS) requirements for inoperable
snubbers by adding Limiting Condition for Operation 3.0.7. The changes
are consistent with Nuclear Regulatory Commission approved Industry/
Technical Specification Task Force (TSTF) standard TS change TSTF-373,
Revision 4. The availability of this TS improvement was published in
the Federal Register on May 4, 2005 (70 FR 23252), as part of the
consolidated line item improvement process.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No. The proposed change allows a delay time before
declaring supported TS systems inoperable when the associated
snubber(s) cannot perform its required safety function. Entrance into
Actions or delaying entrance into Actions is not an initiator of any
accident previously evaluated. Consequently, the probability of an
accident previously evaluated is not significantly increased. The
consequences of an accident while relying on the delay time allowed
before declaring a TS supported system inoperable and taking its
Conditions and Required Actions are no different than the consequences
of an accident under the same plant conditions while relying on the
existing TS supported system Conditions and Required Actions.
Therefore, the consequences of an accident previously evaluated are not
significantly increased by this change. Therefore, this change does not
involve a significant increase in the probability or consequences of an
accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind
[[Page 15488]]
of accident from any accident previously evaluated?
Response: No. The proposed change allows a delay time before
declaring supported TS systems inoperable when the associated
snubber(s) cannot perform its required safety function. The proposed
change does not involve a physical alteration of the plant (no new or
different type of equipment will be installed) or a change in the
methods governing normal plant operations. Thus, this change does not
create the possibility of a new or different kind of accident from any
accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No. The proposed change allows a delay time before
declaring supported TS systems inoperable when the associated
snubber(s) cannot perform its required safety function. The proposed
change restores an allowance in the pre-ISTS conversion TS that was
unintentionally eliminated by the conversion. The pre-ISTS TS were
considered to provide an adequate margin of safety for plant operation,
as does the post-ISTS conversion TS. Therefore, this change does not
involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: General Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A, Knoxville, Tennessee 37902.
NRC Section Chief: Michael L. Marshall, Jr.
Tennessee Valley Authority, Docket No. 50-328, Sequoyah Nuclear Plant,
Unit 2, Hamilton County, Tennessee
Date of amendment request: February 15, 2006.
Description of amendment request: The amendment would revise the
Technical Specifications (TS) to adopt NRC-approved Revision 4 to
Technical Specification Task Force (TSTF) Standard Technical
Specification Change Traveler, TSTF-449, ``Steam Generator Tube
Integrity.'' The proposed amendment includes changes to the TS
definition of Leakage, TS 3.4.6.2, ``Reactor Coolant System,
Operational Leakage,'' TS 3.4.5, ``Steam Generator (SG) Tube
Integrity,'' and adds TS 6.8.4.k, ``Steam Generator (SG) Program,'' and
TS 6.9.1.16, ``Steam Generator Tube Inspection Report.'' The proposed
changes are necessary in order to implement the guidance for the
industry initiative on NEI 97-06, ``Steam Generator Program
Guidelines.''
The amendment would also delete License Condition 2.C.8 Item b.
This License Condition references the licensee's letters from 1997 that
contain commitments associated with NRC Generic Letter 95-05,
``Voltage-Based Repair Criteria for Westinghouse Steam Generator Tubes
Affected by Outside Diameter Stress Corrosion Cracking,'' and the
application of voltage-based alternate repair criteria to the steam
generators. The licensee has concluded that the provisions and
requirements of the proposed TS changes bound the commitments
identified in the existing License Condition.
The NRC staff issued a notice of opportunity for comment in the
Federal Register on March 2, 2005 (70 FR 10298), on possible amendments
adopting TSTF-449, including a model safety evaluation and model no
significant hazards consideration (NSHC) determination, using the
consolidated line item improvement process. The NRC staff subsequently
issued a notice of availability of the models for referencing in
license amendment applications in the Federal Register on May 6, 2005
(70 FR 24126). The licensee affirmed the applicability of the following
NSHC determination in its application dated August 31, 2005.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
Criterion 1--The Proposed Change Does Not Involve a Significant
Increase in the Probability or Consequences of an Accident Previously
Evaluated
The proposed change requires a SG Program that includes performance
criteria that will provide reasonable assurance that the SG tubing will
retain integrity over the full range of operating conditions (including
startup, operation in the power range, hot standby, cooldown and all
anticipated transients included in the design specification). The SG
performance criteria are based on tube structural integrity, accident
induced leakage, and operational LEAKAGE.
A steam generator tube rupture (SGTR) event is one of the design
basis accidents that are analyzed as part of a plant's licensing basis.
In the analysis of a SGTR event, a bounding primary to secondary
LEAKAGE rate equal to the operational LEAKAGE rate limits in the
licensing basis plus the LEAKAGE rate associated with a double-ended
rupture of a single tube is assumed.
For other design basis accidents such as a main steamline break
(MSLB), rod ejection, and reactor coolant pump locked rotor the tubes
are assumed to retain their structural integrity (i.e., they are
assumed not to rupture). These analyses typically assume that primary
to secondary LEAKAGE for all SGs is 1 gallon per minute or increases to
1 gallon per minute as a result of accident induced stresses. The
accident induced leakage criterion introduced by the proposed changes
accounts for tubes that may leak during design basis accidents. The
accident induced leakage criterion limits this leakage to no more than
the value assumed in the accident analysis.
The SG performance criteria proposed change to the TS identify the
standards against which tube integrity