Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 10071-10084 [06-1737]
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Federal Register / Vol. 71, No. 39 / Tuesday, February 28, 2006 / Notices
information: Michelle Schroll, 301–415–
1662.
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The NRC Commission Meeting
Schedule can be found on the Internet
at: https://nrc.gov/what-we-do/policymaking/schedule.html.
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need a reasonable accommodation to
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DLC@nrc.gov. Determinations on
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receiving this Commission meeting
schedule electronically, please send an
electronic message to dkw@nrc.gov.
Dated: February 23, 2006.
R. Michelle Schroll,
Office of the Secretary.
[FR Doc. 06–1908 Filed 2–24–06; 11:55 am]
BILLING CODE 7590–01–M
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
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I. Background
Pursuant to section 189a(2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
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the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from February 3,
2006, to February 15, 2006. The last
biweekly notice was published on
February 14, 2006 (71 FR 7804).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
Involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
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10071
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
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As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
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when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemaking and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by
email to OGCMailCenter@nrc.gov. A
copy of the request for hearing and
petition for leave to intervene should
also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
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at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
Carolina Power & Light Company,
Docket No. 50–261, H. B. Robinson
Steam Electric Plant, Unit No. 2,
Darlington County, South Carolina
Date of amendment request:
November 30, 2005.
Description of amendment request:
The proposed amendment would revise
the frequency of the diesel generator
automatic trips bypass surveillance
requirement (SR) 3.8.1.11 from 18
months to 24 months.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
No. The proposed change does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated. The proposed change decreases
the frequency of SR 3.8.1.11, verification of
the DG [diesel generator] automatic trips
bypass, from 18 months to 24 months. The
DG automatic trips bypass circuitry is
required for DG operability and reliability
during emergency operation of the DG. The
proposed test frequency will continue to
assure that the DG will perform as required.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated, because the factors that
are used to determine the probability and
consequences of accidents are not being
affected.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any previously evaluated?
No. The proposed change does not create
the possibility of a new or different kind of
accident from any previously evaluated.
There are no new or different accident
initiators or sequences being created by the
proposed Technical Specifications change.
The required surveillance performed at the
proposed frequency will continue to provide
assurance that the trips bypass function is
operable and is properly supporting
operation of the associated DG. Therefore, the
proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Do the proposed changes involve a
significant reduction in the margin of safety?
No. The proposed change does not involve
a significant reduction in the margin of
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safety. The proposed change will continue to
ensure that the DG trips bypass function
operates as designed. The functionality and
operability of emergency power system is not
being changed. Therefore, the proposed
change does not involve a significant
reduction in the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Branch Chief: Michael L.
Marshall, Jr.
Dominion Nuclear Connecticut, Inc.,
Docket No. 50–336, Millstone Power
Station, Unit No. 2, New London
County, Connecticut
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Date of amendment request: January
4, 2006.
Description of amendment request:
The proposed amendment would
change the Millstone Power Station,
Unit No. 2 Technical Specification (TS)
3/4.3.3.8, ‘‘Instrumentation, Accident
Monitoring,’’ to modify the description
of the pressurizer power operated relief
valves (PORVs) and pressurizer safety
valves position indicators.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed amendment removes the
wording ‘‘Acoustic Monitor,’’ which provides
specific details related to system design, from
items 4 and 6 of TS 3/4.3.3.8, Tables 3.3–11
and 4.3–7. The PORVs and Pressurizer Safety
Valves position indicators (and the
associated ‘‘Acoustic Monitor’’) provide only
indications of valve position. They do not
constitute a design feature that is an initial
condition for a design basis accident or
transient analysis. Furthermore, they do not
affect the function of the system, equipment
in the system or actuate to mitigate a design
basis accident or transient. Therefore, the
proposed changes do not increase the
probability or consequences of an accident
previously evaluated.
Additionally, the TS retains the
requirement for the total and minimum
channels required to be OPERABLE and to
verify channel OPERABILITY at the
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designated frequencies. The PORVs and
Pressurizer Safety Valves are equipped with
positive position indication that meets the
requirements of RG [Regulatory Guide] 1.97.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes do not impact the
capability of existing equipment to perform
its intended functions. No system setpoints
are being modified and no changes are being
made to the method in which plant
operations are conducted. No new failure
modes that would impact accident analyses
are introduced by the proposed changes. The
proposed amendment does not introduce
accident initiators or malfunctions that
would cause a new or different kind of
accident. Therefore, the proposed
amendment does not create the possibility of
a new or different kind of accident from any
accident previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
The proposed amendment removes the
wording ‘‘Acoustic Monitor’’ from items 4
and 6 of TS 3/4.3.3.8, Table[s] 3.3–11 and
4.3–7. The proposed changes do not affect
any of the assumptions used in the accident
analysis, nor does it affect any operability
requirements for equipment important to
plant safety. Therefore, the margin of safety
is not impacted by the proposed amendment.
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Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request:
December 30, 2005.
Description of amendment request:
The proposed amendment establishes a
combined leakage rate limit for the sum
of the four Main Steam line leakage
rates that is equal to four times the
current individual Main Steam Isolation
Valve (MSIV) leakage rate limit.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed amendment does not involve
a change to structures, systems, or
components that would affect the probability
of an accident previously evaluated in the
Cooper Nuclear Station (CNS) Updated
Safety Analysis Report (USAR). The
proposed amendment results in no change in
the radiological consequences of the design
basis Loss-of-Coolant Accident (LOCA) as
currently analyzed for CNS. That analysis
was calculated for a combined Main Steam
Isolation Valve (MSIV) leakage for
determining acceptance to the regulatory
limits for the offsite and Control Room
radiation doses, as contained in 10 CFR 100
[Part 100 of Title 10 of the Code of Federal
Regulations] and 10 CFR 50[,] Appendix A,
General Design Criterion (GDC) 19. The
aggregate Main Steam line leakage rate limit
has no adverse effect on the environmental
qualification of equipment important to
safety, as provided for in 10 CFR 50.49.
Based on the above conclusions, this
proposed amendment does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not modify the
MSIVs or any other plant system or structure
associated with this amendment and
therefore, will not affect their capability to
perform their design function. The combined
total Main Steam line leakage rate is included
in the current radiological analyses for the
assessment of radiation exposure following
an accident. This License Amendment
Request revises the allowable leakage rate
from a per valve limit to a total combined
leakage rate limit for all four Main Steam
lines but does not change the cumulative
limit.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
analyzed.
3. Do the proposed changes involve a
significant reduction in the margin of safety?
Response: No.
The leakage rate limit specified for the
MSIVs is used to quantify the maximum
amount of Secondary Containment bypass
leakage assumed in the LOCA radiological
analysis. Results of the analysis are evaluated
against the dose limits contained in 10 CFR
50[,] Appendix A[,] GDC 19 and 10 CFR 100.
The margin of safety in this context is
considered to be the difference between the
calculated dose exposures and the limits
provided by GDC 19 and 10 CFR 100.
Therefore, since the proposed combined
Main Steam line leakage rate limit is
unchanged from the assumed maximum
leakage rate for MSIVs, for the purpose of
calculating [a] potential radiation dose, the
margin of safety is not affected because the
postulated radiation doses remain the same.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Lillian M.
Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc.,
Rope Ferry Road, Waterford, CT 06385.
NRC Branch Chief: Darrell J. Roberts.
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standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John C.
McClure, Nebraska Public Power
District, Post Office Box 499, Columbus,
NE 68602–0499.
NRC Branch Chief: David Terao.
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Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request: January
30, 2006.
Description of amendment request:
The proposed change allows a delay
time for entering a supported system
Technical Specification (TS) when the
inoperability is due solely to an
inoperable snubber, if risk is assessed
and managed consistent with the
program in place for complying with the
requirements of 10 CFR 50.65(a)(4).
Limiting Condition for Operation (LCO)
3.0.8 is added to the TS to provide this
allowance and define the requirements
and limitations for its use.
This change was proposed by the
industry’s Technical Specification Task
Force (TSTF) and is designated TSTF–
372, Revision 4. The NRC staff issued a
notice of opportunity for comment in
the Federal Register on November 24,
2004 (69 FR 68412), on possible
amendments concerning TSTF–372,
including a model safety evaluation and
model no significant hazards
consideration (NSHC) determination,
using the consolidated line item
improvement process. The NRC staff
subsequently issued a notice of
availability of the models for referencing
in license amendment applications in
the Federal Register on May 4, 2005 (70
FR 23252). The licensee affirmed the
applicability of the following NSHC
determination in its application dated
January 30, 2006.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
Criterion 1—The Proposed Change Does
Not Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated.
The proposed change allows a delay time
for entering a supported system TS when the
inoperability is due solely to an inoperable
snubber if risk is assessed and managed. The
postulated seismic event requiring snubbers
is a low-probability occurrence and the
overall TS system safety function would still
be available for the vast majority of
anticipated challenges. Therefore, the
probability of an accident previously
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evaluated is not significantly increased, if at
all. The consequences of an accident while
relying on allowance provided by proposed
LCO 3.0.8 are no different than the
consequences of an accident while relying on
the TS required actions in effect without the
allowance provided by proposed LCO 3.0.8.
Therefore, the consequences of an accident
previously evaluated are not significantly
affected by this change. The addition of a
requirement to assess and manage the risk
introduced by this change will further
minimize possible concerns. Therefore, this
change does not involve a significant
increase in the probability or consequences
of an accident previously evaluated.
Criterion 2—The Proposed Change Does
Not Create the Possibility of a New or
Different Kind of Accident from any
Previously Evaluated.
The proposed change does not involve a
physical alteration of the plant (no new or
different type of equipment will be installed).
Allowing delay times for entering supported
system TS when inoperability is due solely
to inoperable snubbers, if risk is assessed and
managed, will not introduce new failure
modes or effects and will not, in the absence
of other unrelated failures, lead to an
accident whose consequences exceed the
consequences of accidents previously
evaluated. The addition of a requirement to
assess and manage the risk introduced by this
change will further minimize possible
concerns. Thus, this change does not create
the possibility of a new or different kind of
accident from an accident previously
evaluated.
Criterion 3—The Proposed Change Does
Not Involve a Significant Reduction in a
Margin of Safety.
The proposed change allows a delay time
for entering a supported system TS when the
inoperability is due solely to an inoperable
snubber, if risk is assessed and managed. The
postulated seismic event requiring snubbers
is a low-probability occurrence and the
overall TS system safety function would still
be available for the vast majority of
anticipated challenges. The risk impact of the
proposed TS changes was assessed following
the three-tiered approach recommended in
Regulatory Guide 1.177. A bounding risk
assessment was performed to justify the
proposed TS changes. The proposed LCO
3.0.8 defines limitations on the use of the
provision and includes a requirement for the
licensee to assess and manage the risk
associated with operation with an inoperable
snubber. The net change to the margin of
safety is insignificant. Therefore, this change
does not involve a significant reduction in a
margin of safety.
The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John C.
McClure, Nebraska Public Power
District, Post Office Box 499, Columbus,
NE 68602–0499.
NRC Branch Chief: David Terao.
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Nuclear Management Company, LLC,
Docket Nos. 50–282 and 50–306, Prairie
Island Nuclear Generating Plant, Units
1 and 2, Goodhue County, Minnesota
Date of amendment request:
November 11, 2005.
Description of amendment request:
The proposed amendments would
revise Technical Specification (TS)
3.6.5, ‘‘Containment Spray and Cooling
Systems’’; an existing Condition, two
Surveillance Requirements, and add a
new Condition which will allow
continued plant operation with TS
limitations when two Containment
Cooling System fan coil units (FCUs),
one in each train, are inoperable.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
This license amendment proposes to revise
the Technical Specifications to allow plant
operation to continue for a limited time
period under Technical Specification
controls with two fan coil units, one fan coil
unit from each containment cooling train,
providing the required cooling function.
Analyses demonstrate that any two fan coil
units, whether they are in the same train or
from opposite trains, are sufficient to supply
the required containment cooling following a
design basis accident when the plant in the
proper configuration as required by the
proposed Technical Specifications.
The containment cooling system is
required for accident mitigation and is not an
accident initiator, thus revising the
equipment required to provide the safety
function does not involve a significant
increase in the probability of an accident
previously evaluated.
Since the proposed change continues to
provide the post-accident containment
cooling function under Technical
Specification controls, this change does not
involve an increase in the consequences of an
accident. Thus this change does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
This license amendment proposes to revise
the Technical Specifications to allow plant
operation to continue for a limited time
period under Technical Specification
controls with two fan coil units, one fan coil
unit from each containment cooling train,
providing the required cooling function.
Analyses demonstrate that any two fan coil
units, whether they are in the same train or
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from opposite trains, are sufficient to supply
the required containment cooling following a
design basis accident when the plant in the
proper configuration as required by the
proposed Technical Specifications.
The proposed licensing basis changes do
not involve a change in the function or use
of the containment cooling system. It does
assure that the containment cooling function
is provided during plant operations for postaccident mitigation. There are no new failure
modes or mechanisms created through
allowing different combinations of fan coil
units to provide the cooling function as
proposed by this Technical Specification
change. There are no new accident
precursors generated by providing the
required cooling function with an operable
fan coil unit from each train.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
This license amendment proposes to revise
the Technical Specifications to allow plant
operation to continue for a limited time
period under Technical Specification
controls with two fan coil units, one fan coil
unit from each containment cooling train,
providing the required cooling function.
Analyses demonstrate that any two fan coil
units, whether they are in the same train or
from opposite trains, are sufficient to supply
the required containment cooling following a
design basis accident when the plant in the
proper configuration as required by the
proposed Technical Specifications.
Current plant Technical Specifications
allow plant operation to continue for 7 days
with the containment cooling function
provided by the two operable fan coil units
of a single operable containment cooling
train. This is acceptable because engineering
analyses demonstrate that the two fan coil
units of a single train can provide the
required post-accident containment cooling.
Likewise, engineering analyses
demonstrate that any two fan coil units from
opposite containment cooling trains can also
provide the required post-accident
containment cooling if the cooling water flow
to the other fan coil unit in each train is
isolated. This license amendment request
proposes Technical Specifications which will
allow plant operation to continue for 7 days
with the containment cooling function
provided by two fan coils from opposite
trains provided the cooling water flow to the
other fan coil unit in each train is isolated.
Thus, from a cooling capacity perspective,
this proposed Technical Specification change
does not involve a reduction in a margin of
safety.
When inoperable plant systems are under
Technical Specification controls that limit
the time for inoperability, a single failure in
addition to the inoperable equipment is not
postulated. Therefore, whether two
inoperable fan coil units are in the same train
or opposite trains does not change the
availability of the two remaining operable fan
coil units. Thus from a Technical
Specification perspective, this proposed
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Technical Specification change does not
involve a reduction in a margin of safety.
Therefore, based on the considerations
given above, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Jonathan Rogoff,
Esquire, Vice President, Counsel &
Secretary, Nuclear Management
Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Acting Branch Chief: Timothy J.
Kobetz.
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1, Washington County, Nebraska
Date of amendment request:
December 19, 2005.
Description of amendment request:
The proposed change will revise Fort
Calhoun Station, (FCS) Technical
Specification 2.4, ‘‘Containment
Cooling,’’ (and associated Bases) to
reduce the required number of operable
Containment Spray (CS) pumps from
three to two in order to enhance net
positive suction head (NPSH) margins.
This change will be accomplished by
disabling the containment spray
actuation signal (CSAS) automatic start
feature of CS pump SI–3C. This change
will reduce the head loss across the
containment sump strainers during the
recirculation phase of a design-basis
accident (DBA) by reducing flow rates,
and will improve NPSH available
(NPSHA).
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The Containment Spray (CS) system is not
an initiator of any accident previously
evaluated at the Fort Calhoun Station (FCS);
the CS system is an accident mitigation
system. The CS system’s licensing basis
functions are to limit the containment
pressure rise and reduce the leakage of
airborne radioactivity from the containment
by providing a means for cooling the
containment following a loss-of-coolant
accident (LOCA) or main steam line break
(MSLB) inside containment. The proposed
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change disables the CSAS automatic start
feature of one of the three CS pumps.
The only FCS safety analysis that currently
assumes three CS pumps operating to
mitigate an accident is the Containment
Pressure Analysis for a[n] MSLB inside
containment. Even though this analysis
assumes operation of all three CS pumps, it
also shows that peak containment pressure
occurs prior to the CS system starting,
therefore, the CS system does not mitigate the
peak pressure for a[n] MSLB. The reviews
evaluated both existing AORs [analyses of
record] and those analyses developed for the
Steam Generator Replacement (RSG) project.
The analysis developed for the RSG project
that evaluates the Containment Pressure
Analysis for MSLB inside containment was
reviewed for the impact of reducing the
number of operating CS pumps from three to
two. This review determined that the RSG
MSLB analysis will be acceptable and will
continue to be bounded by the analysis
currently documented in USAR. AOR peak
pressure is unaffected by implementation of
this proposed change. Therefore, the
combination of the RSG project and this
containment spray modification will not
result in an increase in the currently
documented peak containment pressure for
an MSLB. Therefore, the evaluation for the
MSLB event has determined that the
containment pressure response is acceptable
with less than three CS pumps operating.
The LOCA analysis source term is based on
operation of minimum safeguards due to a
worst-case single failure. The minimum
safeguards configuration is unchanged by
this modification. Following implementation
of the proposed change at least one CS pump
will be available to mitigate a LOCA as
currently assumed in the analysis, therefore,
the proposed change will have no adverse
effect on the radiological consequences
following a LOCA. The analyses that
establish the radiological consequences for
the site are based on a Large Break LOCA
with a single CS pump in operation,
therefore, single CS pump operation during
a[n] MSLB inside containment is bounded by
the LOCA analysis.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change will reduce the
number of operable CS pumps from three to
two; however, previous accident analyses
will remain valid. No credible new failure
mechanisms, malfunctions, or accident
initiators not considered in the design and
licensing basis have been created and none
of the initial condition assumptions of any
accident evaluated in the safety analysis are
impacted.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
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Response: No.
The containment building and associated
penetrations are designed to withstand an
internal pressure of 60 psig at 305 °F,
including all thermal loads resulting from the
temperature associated with this pressure,
with a leakage rate of 0.1 percent by weight
or less of the contained volume per 24 hours.
The CS System and the Containment Fan
Coolers are credited for maintaining
containment pressure and temperatures
within design limitations, and assure that the
release of fission products to the
environment following a design[-]basis
accident will not exceed regulatory
guidelines. The FCS licensing basis credits
only one of the three CS pumps to limit the
containment pressure to below the design
value for a LOCA. Currently, the FCS
licensing basis credits three CS pumps for
a[n] MSLB, however, the CS system is not
credited for limiting peak containment
pressure for a[n] MSLB.
The EEQ [electrical equipment
qualification] profile developed for the
current plant configuration bounds those
associated with the upcoming RSG
modification. Both the proposed CS system
changes and the RSG projects are scheduled
for the same refueling outage. The thermal
lag analysis of equipment performed using
the current plant configuration demonstrated
a large margin between the equipment
evaluated during the accident versus the
conditions under which it was tested. The
RSG modification will further increase this
margin. As part of the RSG effort the EEQ
analysis will be revised to address RSG
issues and will include the changes to
containment spray. When the margins
associated with the current analysis as well
as increases in margin when the new analysis
is implemented it is expected that the
changes to the containment spray system will
not produce an adverse result. All equipment
will remain qualified to operate in the
accident environment.
Additionally, the CFCs [containment fan
coolers] operate independently of the CS
system to remove heat from the containment
atmosphere. The CFCs consist of two
redundant trains; each train with one air
cooling and filtering unit and one air cooling
unit, for a total of four cooling units.
Operation of the CFCs is credited in the
MSLB containment pressure analysis. The
CFCs are not impacted by this proposed
change. During the MSLB containment spray
takes place after the peak containment
pressure occurs. Therefore, the licensing
basis capabilities of the Containment Cooling
System, which consists of the CS and CFCs,
is not adversely affected by the proposed
change; the ability to maintain containment
peak pressure and temperature and long[]term containment pressure and temperature
will be maintained.
Particulate fission products that are
released into the containment following a
DBA are removed by the CS system for those
events that result in CS actuation. The water
spray strips radioactive particles from the
atmosphere where they fall to the floor and
are washed into the containment sump. The
radiological consequences analysis credits CS
system operation for removal of particulates
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from the containment atmosphere during a
LOCA. The LOCA analysis source term is
based on operation of minimum safeguards
due to a worst-case single failure, and a
presumption of core damage. Minimum
safeguards corresponds to one CS pump and
one CS header operation and take into
account pump degradation, and instrument
uncertainties. The analyses that establish the
radiological consequences for the site are not
impacted by the proposed modification.
These analyses are based on a Large Break
LOCA with a single CS pump in operation.
Therefore, single CS pump operation bounds
the plant configuration following the
proposed modification.
The Large Break LOCA assumes that there
will be three CS pumps operating when
evaluating the effects of containment
pressure on ECCS [emergency core cooling
system] performance. The analysis assumes
three CS pumps, which minimizes
containment pressure, to conservatively
evaluate ECCS performance in response to a
LOCA. The use of two CS pumps versus three
improves ECCS performance and thus
increases margin to 10 CFR 50.46 limits on
peak clad temperature.
In summary, following implementation of
the proposed change:
• Peak containment pressure for analyzed
DBAs will not be increased;
• The assumptions used in the
environmental qualification of equipment
exposed to the containment atmosphere
following a DBA remaining bounding; and
• The radiological consequences for the
bounding DBA remains unchanged.
• The currently calculated peak clad
temperature following a LOCA remains
bounded by existing analysis.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: James R.
Curtiss, Esq., Winston & Strawn, 1400 L
Street, NW., Washington, DC 20005–
3502.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Company,
Docket No. 50–323, Diablo Canyon
Nuclear Power Plant, Unit No. 2, San
Luis Obispo County, California
Date of amendment requests: January
13, 2006.
Description of amendment requests:
The proposed amendment would revise
Technical Specification 5.6.5, ‘‘Core
Operating Limits Report (COLR),’’ by
adding WCAP–16009–P–A, ‘‘Realistic
Large-Break LOCA [Loss-of-Coolant
Accident] Evaluation Methodology
Using the Automated Statistical
Treatment of Uncertainty Method
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(ASTRUM),’’ dated January 2005, as an
approved analytical method for
determining core operating limits for
Unit 2.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change to allow the use of
the best estimate loss-of-coolant accident
(LOCA) analysis methodology using the
automated statistical treatment of uncertainty
methodology (ASTRUM) does not involve a
physical alteration of any plant equipment or
change operating practice at Unit 2 of Diablo
Canyon Power Plant (DCPP). Therefore, there
will be no increase in the probability of a
LOCA. The consequences of a LOCA are not
being increased.
The plant conditions assumed in the
analysis are bounded by the design
conditions for all equipment in Unit 2. That
is, it is shown that the emergency core
cooling system is designed so that its
calculated cooling performance conforms to
the criteria contained in 10 CFR [Title 10 of
the Code of Federal Regulations, Section]
50.46, paragraph b. No other accident is
potentially affected by this change.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different accident
from any accident previously evaluated?
Response: No.
The proposed change would not result in
any physical alteration to any Unit 2 system,
and there would not be a change in the
method by which any safety [-]related system
performs its function. Analyses of transient
events have confirmed that no transient event
results in a new sequence of events that
could lead to a new accident scenario. The
parameters assumed in the analysis are
within the design limits of existing plant
equipment.
In addition, employing the ASTRUM
methodology does not create any new failure
modes that could lead to a different kind of
accident. The design of all systems remains
unchanged and no changes are being made to
any reactor protection system or engineered
safeguard features actuation setpoints.
Based on this review, it is concluded that
no new accident scenarios, failure
mechanisms or limiting single failures are
introduced as a result of the proposed
changes.
Therefore, the proposed change does not
create the possibility of a new or different
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
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It has been shown that the analytic
technique used in the analysis realistically
describes the expected behavior of the DCPP
Unit 2 reactor system during a postulated
LOCA. Uncertainties have been accounted for
as required by 10 CFR 50.46. A sufficient
number of LOCAs with different break sizes,
different locations, and other variations in
properties have been analyzed to provide
assurance that the most severe postulated
LOCAs were analyzed. The analysis has
demonstrated that all acceptance criteria
contained in 10 CFR 50.46[,] paragraph b
continue to be satisfied.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Richard F.
Locke, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Co., Docket No.
50–133, Humboldt Bay Power Plant
(HBPP), Unit 3 Humboldt County,
California
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Date of amendment request: January
19, 2006.
Description of amendment request:
The licensee has proposed to revise the
Technical Specifications (TS) to correct
an editorial error in TS 3.1.2, ‘‘Spent
Fuel Pool Load Restrictions,’’ and to
change TS 5.2.2, ‘‘Facility Staff,’’ to
allow the Unit 3 control room to be
temporarily unmanned during
emergency conditions that require
personnel to evacuate buildings for their
safety.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the change involve a significant
increase in the probability or consequences
of an accident previously evaluated?
Response: No.
The proposed editorial change has no
impact on probability or consequences of
accidents. The following discussion applies
to the proposed change related to control
room evacuation.
Allowing plant personnel to not
continuously man the control room has no
impact on the probability of an accident from
occurring, especially acts of nature such as
earthquakes and tsunamis.
The HBPP DSAR, Appendix A, and NRC
SER, Section 10, dated April 29, 1987,
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evaluate various accidents at HBPP. Because
all fuel has been removed from the reactor
vessel and stored in the spent fuel pool, the
majority of accidents analyzed pertain to
events that could only affect spent fuel or the
spent fuel pool. All accidents affecting spent
fuel or the spent fuel pool do not require
operator action to protect the public health
and safety or to maintain offsite radiological
doses well within regulatory limits. In
addition, NRC SER, Section 10.7, ‘‘Impact of
Tsunami Flooding,’’ analyzes the impact of
tsunami flooding. That analysis identifies a
likely impact of the tsunami to be a release
of the radwaste tank radionuclide contents to
the bay and some damage to the reactor
building. For both situations, no operator
action is required to maintain offsite
radiological doses well within regulatory
limits.
Allowing the control room to be
temporarily unmanned under emergency
conditions does not create problems that
could increase the consequences of an
accident. The primary function of manning
the control room is for an operator to observe
and acknowledge alarms. Recovery actions to
respond to damage to spent fuel, the spent
fuel pool, or radwaste tanks are taken by
personnel outside the control room. No
recovery actions are required to be taken by
the control room operator to respond to
damage to spent fuel, the spent fuel pool, or
radwaste tanks.
Evacuating occupied buildings, including
the control room, during a tsunami, allows
the control room operator to return to the
control room after the tsunami and assess
damage by observing indicators and alarms.
Upon returning to the control room, the
operator would be able to direct and monitor
recovery efforts from the control room that
may be necessary to bring plant parameters
within required specifications.
If an operator remains in the control room
during a tsunami and becomes injured, that
operator would be unable to direct and
monitor recovery efforts. Under this scenario,
other plant personnel who evacuated to
higher ground onsite within the OCA would
eventually return to the plant, including the
control room, and perform any required
recovery functions. Therefore, consequences
of a tsunami are not increased by not
continually manning the control room during
the event.
2. Does the change create the possibility of
a new or different kind of accident from any
accident evaluated?
Response: No.
The proposed editorial change has no
impact on accidents. The following
discussion applies to the proposed change
related to control room evacuation.
As discussed in the response to question 1
above, none of the analyzed accidents require
operator action to keep offsite radiological
doses well within regulatory limits. In
addition, allowing plant personnel to not
continuously man the control room after an
emergency situation has occurred, has no
impact on the possibility of a new or
different kind of accident from occurring. If
the plant is evacuated, no work activities will
be performed in the plant. With the plant in
SAFSTOR and no work being performed,
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there are no actions required to be taken by
personnel manning the control room.
3. Does the change involve a significant
reduction in a margin of safety?
Response: The proposed editorial change
has no impact on margin of safety. The
following discussion applies to the proposed
change related to control room evacuation.
NRC SER Section 10.8, ‘‘Accident Analysis
Conclusions,’’ summarizes the consequences
from accidents in terms of offsite radiological
doses. SER Section 10.8 includes the
statement, ‘‘The (NRC) staff has determined
that offsite radiological consequences due to
a tsunami are within acceptable dose
guideline values.’’ As discussed in the
response to question 1 above, none of the
analyzed accidents require operator action to
keep offsite radiological doses well within
regulatory limits. Therefore, temporarily not
manning the control room during an
emergency will have no impact on the
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based upon the
staff’s review of the licensee’s analyses
as well as the staff’s own evaluation, the
staff concludes that the three standards
of 10 CFR 50.92(c) are satisfied.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Attorney for licensee: Richard F.
Locke, Esquire, Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Section Chief: Claudia Craig.
STP Nuclear Operating Company,
Docket Nos. 50–498 and 50–499, South
Texas Project, Units 1 and 2, Matagorda
County, Texas
Date of amendment request: January
31, 2006.
Description of amendment request:
The amendments would revise
Technical Specification (TS) 3.8.3.1,
‘‘Onsite Power Distribution-Operating,’’
to extend the allowed outage time
(AOT) for an inoperable Class 1E vital
120-volt alternating current inverter.
The TS currently provides an AOT of 24
hours to restore an inoperable inverter.
Based on risk-informed assessment, the
amendments would extend the AOT to
7 days.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed formatting changes to TS
3.8.3.1 Action b and the change to the AOT
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for an inoperable inverter to be extended
from 24 hours to 7 days do not alter any plant
equipment or operating practices in such a
manner that the probability of an accident is
increased. The proposed changes will not
alter assumptions relative to the mitigation of
an accident or transient event.
An evaluation was performed to determine
the risk significance of the proposed change
to the AOT. The risk evaluation concludes
that the DCDF [core damage frequency] and
DLERF [large early release frequency]
associated with the proposed changes are
1.88E–07 and 2.05E–09, respectively, which
are characterized as ‘‘very small changes’’ by
RG [Regulatory Guide] 1.174. The ICCDP
[incremental conditional core damage
probability] and ICLERP [incremental
conditional large early release probability]
associated with the proposed change are
3.63E–07 and 1.08E–08, respectively, which
are within the acceptance criteria in RG
1.177. Therefore, the proposed changes do
not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes do not involve a
physical alteration of the plant (no new or
different type of equipment will be installed)
or a change in the methods governing normal
plant operation. Therefore, the proposed
changes do not create the possibility of a new
or different kind of accident from any
accident previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
Margin of safety is associated with
confidence in the ability of the fission
product barriers (i.e., fuel and fuel cladding,
reactor coolant pressure boundary, and
containment structure) to limit the level of
radiation dose to the public. The proposed
change to TS 3.8.3.1 to allow the AOT for an
inoperable inverter to be extended from 24
hours to 7 days has been evaluated for its
effect on plant safety. The risk-informed
evaluation concludes that the DCDF and
DLERF associated with the proposed change
are 1.88E–07 and 2.05E–09, respectively,
which are characterized as ‘‘very small
changes’’ by RG 1.174. The ICCDP and
ICLERP associated with the proposed change
are 3.63E–07 and 1.08E–08, respectively,
which are within the acceptance criteria in
RG 1.177. The proposed changes to the
formatting of TS 3.8.3.1 Action b are
administrative only and have no impact on
margin of safety. Therefore, the proposed
changes do not involve a significant
reduction in the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the standards of
10 CFR 50.92(c) are satisfied. Therefore,
the NRC staff proposes to determine that
the request for amendments involves no
significant hazards consideration.
Attorney for licensee: A. H.
Gutterman, Esq., Morgan, Lewis &
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17:06 Feb 27, 2006
Jkt 208001
Bockius, 1111 Pennsylvania Avenue,
NW., Washington, DC 20004.
NRC Branch Chief: David Terao.
Tennessee Valley Authority (TVA),
Docket No. 50–390, Watts Bar Nuclear
Plant, Unit 1 (WBN) Rhea County,
Tennessee
Date of amendment request:
December 14, 2005 (TS–05–07).
Description of amendment request:
The proposed amendment would revise
Technical Specification Section
5.7.2.19, ‘‘Containment Leakage Rate
Testing Program,’’ to allow a one time,
5-year extension to the current 10-year
test interval for the performance-based
leakage rate test program for 10 CFR Part
50, Appendix J, Type A tests.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change for extending Type A
test frequency does not significantly increase
the probability of an accident previously
evaluated since the change is not a
modification to plant systems, nor a change
to plant operation that could initiate an
accident.
TVA performed an evaluation of the risk
significance for the proposed increase to the
WBN Unit 1 Type A test frequency. The
results of the TVA risk evaluation indicates
that the increase in Large Early Release
Frequency (LERF) remains below the level of
risk significance defined in the NRC
Regulatory Guide 1.174, ‘‘An Approach for
Using Probabilistic Risk Assessment In RiskInformed Decisions On Plant-Specific
Changes to the Licensing Basis.’’ TVA’s
evaluation indicates that the calculated
increase in frequency for all releases (small,
large, early and late) and the increase in
radiation dose to the population are also nonrisk significant.
The proposed test interval extension does
not involve a significant increase in the
consequences of an accident. Research
documented in NUREG–1493, ‘‘PerformanceBased Containment Leakage-Test Program,’’
determined that generically, very few
potential containment leakage paths fail to be
identified by Type A tests. An analysis of 144
Type A test results, including 23 failures,
found that no failures were due to
containment liner breach. The NUREG
concluded that reducing the Type A test
frequency to once per 20 years would lead to
an imperceptible increase in risk.
Furthermore, the NUREG concluded that
Type B and C testing provides assurance that
containment leakage from penetration leak
paths (i.e., valves, flanges, containment airlocks) identify any leakage that would
otherwise be detected by the Type A tests.
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In addition to the NUREG conclusions,
TVA’s American Society of Mechanical
Engineers (ASME) IWE program performs
containment inspections in order to detect
evidence of degradation that may either affect
the containment structural integrity or leak
tightness.
Therefore, the proposed extension of the
Type A test interval does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change to extend the Type
A test interval does not create the possibility
of a new or different type of accident because
there are no physical changes made to the
plant or plant equipment governing normal
plant operation. There are no changes to the
operation of the plant that would introduce
a new failure mode creating the possibility of
a new or different kind of accident.
Therefore, the proposed extension does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change to extend the Type
A test interval will not significantly reduce
the margin of safety. A generic study
documented in NUREG–1493 indicates that
extending the Type A leak test interval to 20
years would result in an imperceptible
increase in risk to the public. The NUREG
also found that, generically, the containment
leakage rate contributes a very small amount
to the individual risk and that the decrease
in the Type A test frequency would have a
minimal effect on risk because most potential
leakage paths are detected by Type C testing.
Previous Type A leakage tests conducted
on WBN Unit 1 indicate that leakage from
containment have been less than the 10 CFR
50, Appendix J leakage limit of 1.0 La. A
review of the previous Type A test results
indicate a stable trend with an increase of
less than 15 percent of La, well below the 1.0
La leakage limit.
Therefore, these test results, in conjunction
with the research findings from NUREG–
1493, provide assurance that the proposed
extension to the Type A test interval does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L.
Marshall, Jr.
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Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of application request: August
26, 2005, as supplemented by letter
dated December 16, 2005.
Description of amendment request:
The amendment would authorize
changes to the Final Safety Analysis
Report (FSAR) for the Callaway Plant,
Unit 1, that would revise the
methodology for the reactor coolant
system (RCS) leak detection
instrumentation. This revision would
clarify the requirements of the
containment atmosphere gaseous
radioactivity monitor with regard to the
RCS leak detection capability and
would justify that the monitor can be
considered operable in compliance with
Limiting Condition for Operation 3.4.15,
in Technical Specification (TS) 3.4.15,
‘‘RCS Leakage Detection
Instrumentation,’’ during all applicable
reactor modes. There are no proposed
changes to the TS.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed change does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated.
The proposed change has been evaluated
and determined to not increase the
probability or consequences of an accident
previously evaluated. The proposed change
does not make hardware changes and does
not alter the configuration of any plant
system, structure, or component (SSC). The
proposed change only clarifies the design
and OPERABILITY requirements for the
containment atmosphere gaseous
radioactivity monitor[s] and identifies the
capabilities of the containment atmosphere
gaseous radioactivity monitors at low RCS
[radio]activity levels. The containment
radiation monitors are not initiators of any
accident; therefore, the probability of
occurrence of an accident is not increased.
The FSAR and TS will continue to require
diverse means of [RCS] leakage detection
equipment, thus ensuring that leakage due to
cracks [in the RCS] would continue to be
identified prior to propagating to the point of
a [RCS] pipe break. Therefore, the
consequences of an accident [previously
evaluated] are not increased.
2. The proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
The proposed change does not involve the
use or installation of new equipment and the
currently installed equipment will not be
operated in a new or different manner. No
new or different system interactions are
created and no new processes are introduced.
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17:06 Feb 27, 2006
Jkt 208001
The proposed changes will not introduce any
new failure mechanisms, malfunctions, or
accident initiators not already considered in
the design and licensing bas[i]s [for the
Callaway Plant]. The proposed change does
not affect any SSC associated with an
accident initiator. Based on this evaluation,
the proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. The proposed change does not involve
a significant reduction in a margin of safety.
The proposed change does not alter any
RCS leakage detection components. The
proposed change only clarifies the design
and OPERABILITY requirements for the
containment atmosphere gaseous
radioactivity monitor[s] and identifies the
capabilities of the containment atmosphere
gaseous radioactivity monitors at low RCS
[radio]activity levels. This change is required
since the level of radioactivity in the
Callaway Plant reactor coolant has become
much lower than what was assumed in the
FSAR [when the plant was licensed] and the
gaseous channel [(monitor)] can no longer
promptly detect a small RCS leak under all
operating conditions. The proposed
amendment continues to require diverse
means of [RCS] leakage detection equipment
with [the] capability to promptly detect RCS
leakage. Although not required by TS,
additional diverse means of leakage detection
capability are available as described in the
FSAR Section 5.2.5. Early detection of [RCS]
leakage, as the potential indicator of a
crack(s) in the RCS pressure boundary, will
thus continue to be in place so that such a
condition is known and appropriate actions
taken well before any such crack would
propagate to a more severe condition. Based
on this evaluation, the proposed change does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: John O’Neill,
Esq., Shaw, Pittman, Potts &
Trowbridge, 2300 N Street, NW.,
Washington, DC 20037.
NRC Branch Chief: David Terao.
Wolf Creek Nuclear Operating
Corporation, Docket No. 50–482, Wolf
Creek Generating Station, Coffey
County, Kansas
Date of amendment request: February
1, 2006.
Description of amendment request:
The amendment would revise the
Inservice Testing Program in Section
5.5.8 of the Administrative Controls,
Programs and Manuals, section of the
Technical Specifications (TSs). The
licensee is adopting NRC-approved
Technical Specification Task Force
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10079
(TSTF) 479, Revision 0, ‘‘Changes to
Reflect Revision of 10 CFR 50.55a.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
(1) Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change revises TS 5.5.8,
‘‘Inservice Testing Program,’’ for consistency
with the requirements of 10 CFR 50.55a(f)
regarding the inservice testing of pumps and
valves. The proposed change incorporates
revisions to the ASME [American Society of
Mechanical Engineers] Code [for Operation
and Maintenance of Nuclear Power Plants]
that result in a net improvement in the
measures for testing pumps and valves.
The proposed change does not impact any
accident initiators or analyzed events or
assumed mitigation of accident or transient
events. They do not involve the addition or
removal of any equipment, or any design
changes to the facility. Therefore, the
proposed change does not represent a
significant increase in the probability or
consequences of an accident previously
evaluated.
(2) Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change revises TS 5.5.8,
‘‘Inservice Testing Program,’’ for consistency
with the requirements of 10 CFR 50.55a(f)
regarding the inservice testing of pumps and
valves. The proposed change incorporates
revisions to the ASME Code that result in a
net improvement in the measures for testing
pumps and valves.
The proposed change does not involve a
modification to the physical configuration of
the plant (i.e., no new equipment will be
installed) or change in the methods
governing normal plant operation. The
proposed change will not impose any new or
different requirements or introduce a new
accident initiator, accident precursor, or
malfunction mechanism. Additionally, there
is no change in the types or increases in the
amounts of any effluent that may be released
off-site and there is no increase in individual
or cumulative occupational exposure.
Therefore, this proposed change does not
create the possibility of an accident of a
different kind than previously evaluated.
(3) Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change revises TS 5.5.8,
‘‘Inservice Testing Program,’’ for consistency
with the requirements of 10 CFR 50.55a(f)
regarding the inservice testing of pumps and
valves. The proposed change incorporates
revisions to the ASME Code that result in a
net improvement in the measures for testing
pumps and valves. The safety function of the
affected pumps and valves will be
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Federal Register / Vol. 71, No. 39 / Tuesday, February 28, 2006 / Notices
maintained. Therefore, this proposed change
does not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jay Silberg, Esq.,
Shaw, Pittman, Potts and Trowbridge,
2300 N Street, NW., Washington, DC
20037.
NRC Branch Chief: David Terao.
Wolf Creek Nuclear Operating
Corporation, Docket No. 50–482, Wolf
Creek Generating Station, Coffey
County, Kansas
wwhite on PROD1PC65 with NOTICES
Date of amendment request: February
7, 2006.
Description of amendment request:
The amendment would add
Surveillance Requirement (SR) 3.3.1.16,
to verify the reactor trip system
response time, to Function 3.a, power
range neutron flux—high positive rate
trip function, in Table 3.3.1–1, ‘‘Reactor
Trip System Instrumentation,’’ of the
Technical Specifications (TSs).
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
(1) Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Overall protection system performance will
remain within the bounds of the accident
analysis since there are no hardware changes.
The design of the Reactor Trip System (RTS)
instrumentation, specifically the positive
[neutron] flux rate trip (PFRT) function, will
be unaffected. The reactor protection system
will continue to function in a manner
consistent with the plant design basis. All
design, material, and construction standards
that were applicable prior to the request [(i.e.,
this amendment application)] are
maintained.
The proposed change imposes additional
surveillance requirements to assure safety
related structures, systems, and components
are verified to be consistent with the [plant]
safety analysis and licensing basis. In this
specific case, a response time verification
requirement will be added to the PFRT
Function [in TS Table 3.3.1–1].
The proposed [change] will not modify any
system interface. The proposed [change] will
not affect the probability of any event
initiators. There will be no degradation in the
performance of or an increase in the number
of challenges imposed on safety-related
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17:06 Feb 27, 2006
Jkt 208001
equipment assumed to function during an
accident situation. There will be no change
to normal plant operating parameters or
accident mitigation performance. The
proposed [change] will not alter any
assumptions or change any mitigation actions
in the radiological consequence evaluations
in the Updated Safety Analysis Report
(USAR) [for Wolf Creek Generating Station].
The proposed [change does] not adversely
affect accident initiators or precursors nor
alter the design assumptions, conditions, or
configuration of the facility or the manner in
which the plant is operated or maintained.
The proposed [change does] not alter or
prevent the ability of structures, systems, and
components (SSCs) from performing their
intended function to mitigate the
consequences of an initiating event within
the assumed acceptance limits. The proposed
[change does] not affect the source term,
containment isolation, or radiological release
assumptions used in evaluating the
radiological consequences of an accident
previously evaluated. The proposed [change
is] consistent with the safety analysis
assumptions and resultant consequences.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
(2) Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
There are no hardware changes nor are
there any changes in the method by which
any safety related plant system performs its
safety function. This change will not affect
the normal method of plant operation or
change any operating parameters. No
performance requirements will be affected;
however, the proposed change does impose
additional surveillance requirements. The
additional requirements are consistent with
assumptions made in the safety analysis and
licensing basis.
No new accident scenarios, transient
precursors, failure mechanisms, or limiting
single failures are introduced as a result of
[the change]. There will be no adverse effect
or challenges imposed on any safety-related
system as a result of [the change].
Therefore, the proposed change does not
create the possibility of a new or different
[kind of] accident from any accident
previously evaluated.
(3) Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed [change does] not affect the
acceptance criteria for any analyzed event
nor is there a change to any Safety Analysis
Limit (SAL). There will be no effect on the
manner in which safety limits, limiting safety
system settings, or limiting conditions for
operation are determined nor will there be
any effect on those plant systems necessary
to assure the accomplishment of protection
functions. There will be no impact on the
overpower limit, DNBR [departure from
nucleate boiling ratio] limit, FQ [heat flux hot
channel factor], F>H [nuclear enthalpy rise
hot channel factor], LOCA PCT [loss-ofcoolant accident peak cladding temperature],
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Fmt 4703
Sfmt 4703
peak local power density, or any other
margin of safety. The radiological dose
consequence acceptance criteria listed in the
[NRC] Standard Review Plan [NUREG–0800]
will continue to be met.
The safety analysis limits assumed in the
transient and accident analyses are
unchanged. None of the acceptance criteria
for any accident analysis is changed. The
imposition of additional surveillance
requirements increases the margin of safety
by assuring that the affected safety analysis
assumptions on equipment response time are
verified on a periodic frequency. Therefore,
the proposed change does not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jay Silberg, Esq.,
Shaw, Pittman, Potts and Trowbridge,
2300 N Street, NW., Washington, DC
20037.
NRC Branch Chief: David Terao.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
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Federal Register / Vol. 71, No. 39 / Tuesday, February 28, 2006 / Notices
For further details with respect to the
action see (1) The applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
wwhite on PROD1PC65 with NOTICES
Carolina Power & Light Company,
Docket Nos. 50–325 and 50–324,
Brunswick Steam Electric Plant, Units 1
and 2, Brunswick County, North
Carolina
Date of application for amendments:
August 11, 2005.
Brief Description of amendments: The
amendments revise Technical
Specification (TS) 5.5.12, ‘‘Primary
Containment Leakage Rate Testing
Program,’’ by removing an exception
that allows for compensation of flow
meter instrument inaccuracies in
accordance with ANSI/ANS–56.8–1987
rather than ANSI/ANS–56.8–1994.
Date of issuance: February 8, 2006.
Effective date: Date of issuance to be
implemented within 60 days.
Amendment Nos.: 238 and 266.
Facility Operating License Nos. DPR–
71 and DPR–62: Amendments change
the TS.
Date of initial notice in Federal
Register: September 13, 2005 (70 FR
54087).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated February 8,
2006.
No significant hazards consideration
comments received: No.
Entergy Nuclear Operations, Inc.,
Docket Nos. 50–247 and 50–286, Indian
Point Nuclear Generating Unit Nos. 2
and 3, Westchester County, New York
Date of application for amendment:
June 8, 2005.
Brief description of amendment: The
proposed changes would add Limiting
Condition for Operation 3.0.8 to address
conditions where one or more snubbers
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17:06 Feb 27, 2006
Jkt 208001
are unable to perform their associated
support function.
Date of issuance: February 13, 2006.
Effective date: As of the date of
issuance, and shall be implemented
within 60 days.
Amendment Nos.: 245 and 229.
Facility Operating License Nos. DPR–
26 and DPR–64: The amendment
revised the Technical Specifications.
Date of initial notice in Federal
Register: August 16, 2005 (70 FR
48203).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated February 13,
2006.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket Nos. 50–373 and 50–374, LaSalle
County Station, Units 1 and 2, LaSalle
County, Illinois
Date of application for amendments:
March 7, 2005, as supplemented by
letter dated December 5, 2005.
Brief description of amendments: The
amendments will add two Nuclear
Regulatory Commission (NRC) approved
topical report references to the list of
analytical methods in Technical
Specification 5.6.5, ‘‘Core Operating
Limits Report,’’ that can be used to
determine core operating limits.
Date of issuance: February 1, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 90 days.
Amendment Nos.: 174 and 160.
Facility Operating License Nos. NPF–
11 and NPF–18: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: August 16, 2005 (70 FR
48205).
The supplemental letter contained
clarifying information and did not
change the initial no significant hazards
consideration determination and did not
expand the scope of the original Federal
Register notice.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated February 1,
2006.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket Nos. 50–254 and 50–265, Quad
Cities Nuclear Power Station, Units 1
and 2, Rock Island County, Illinois
Date of application for amendments:
December 17, 2004.
Brief description of amendments: The
amendments revised the Appendix B,
Environmental Protection Plan (nonradiological), of the Quad Cities Station
Renewed Facility Operating Licenses.
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10081
Date of issuance: February 2, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment Nos.: 229 and 224.
Facility Operating License Nos. DPR–
29 and DPR–30: The amendments
revised the Environmental Protection
Plan.
Date of initial notice in Federal
Register: April 12, 2005 (70 FR 19115).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated February 2,
2006.
No significant hazards consideration
comments received: No.
FirstEnergy Nuclear Operating
Company, et al., Docket No. 50–334,
Beaver Valley Power Station, Unit No. 1
(BVPS–1), Beaver County, Pennsylvania
Date of application for amendment:
April 13, 2005, as supplemented by
letters dated August 26, October 28 and
31, November 18, and December 6 and
16, 2005.
Brief description of amendment: The
amendment revised the Technical
Specifications (TSs) to allow
replacement of the BVPS–1 steam
generators (SGs). These changes include
revising the fuel assembly-specific
departure from nucleate boiling ratios
and correlations, modifying the
Overtemperature DT and Overpower DT
equations, revising the SG water level
low-low and high-high setpoints,
revising the SG secondary side level in
Modes 4 and 5, revising the SG TSs to
reflect the replacement SGs and remove
TS requirements that are no longer
applicable to the new SGs, revising the
required charging pump discharge
pressure for reactor coolant pump seal
injection flow, raising the accumulator
pressure, and adding WCAP–14565–P–
A (VIPRE) and WCAP–15025–P–A
(WRB–2M) Topical Reports to the list of
NRC-approved methodologies listed in
TS 6.9.5. The amendment also approves
an expanded selective alternate source
term methodology implementation in
accordance with Regulatory Guide
1.183, ‘‘Alternate Radiological Source
Terms for Evaluating Design Basis
Accidents at Nuclear Power Reactors,’’
and approves use of the 1979 ANS
Decay Heat + 2s model for mass and
energy releases for a main steam line
break outside containment.
Date of issuance: February 9, 2005.
Effective date: As of its date of
issuance and shall be implemented
prior to entry into Mode 4 upon startup
from refueling outage 1R17 which
begins on or about February 10, 2006.
Amendment No: 273.
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Facility Operating License No. DPR–
66: The Amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: June 21, 2005 (70 FR 35737).
The supplements dated August 26,
October 28 and 31, November 18, and
December 6 and 16, 2005, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated February 9,
2006.
No significant hazards consideration
comments received: No.
wwhite on PROD1PC65 with NOTICES
FirstEnergy Nuclear Operating
Company, et al., Docket Nos. 50–334
and 50–412, Beaver Valley Power
Station, Unit Nos. 1 and 2 (BVPS–1 and
2), Beaver County, Pennsylvania
Date of application for amendments:
October 4, 2004, as supplemented July
8, and November 14, 2005.
Brief description of amendments:
These amendments approved
application of the Westinghouse bestestimate loss-of-coolant accident
(LOCA) analysis methodology to BVPS–
1 and 2 for large-break LOCA analysis.
Date of issuance: February 6, 2006.
Effective date: These license
amendments are effective as of the date
of issuance and shall be implemented
for BVPS–1, prior to Mode 4 entry
during startup from refueling outage
1R17 which begins on or about February
10, 2006, and for BVPS–2, prior to Mode
4 entry during startup from refueling
outage 2R12 which begins October 2006.
Amendment Nos.: 272 and 154.
Facility Operating License Nos. DPR–
66 and NPF–73: Amendments revised
the Technical Specifications.
Date of initial notice in Federal
Register: December 7, 2004 (69 FR
70718). The supplements dated July 8,
and November 14, 2005, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the Nuclear
Regulatory Commission staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated February 6,
2006.
No significant hazards consideration
comments received: No.
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Indiana Michigan Power Company,
Docket Nos. 50–315 and 50–316, Donald
C. Cook Nuclear Plant, Units 1 and 2,
Berrien County, Michigan
Date of application for amendment:
August 10, 2005.
Brief description of amendment: The
amendments deleted the power range
neutron flux high negative rate trip
function from Table 3.3.1–1, ‘‘Reactor
Trip System Instrumentation.’’
Date of issuance: February 10, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 30 days.
Amendment No.: 293, 275.
Facility Operating License No. DPR–
58: Amendment revises the Technical
Specifications.
Date of initial notice in Federal
Register: December 6, 2005 (70 FR
72674). The Commission’s related
evaluation of the amendment is
contained in a Safety Evaluation dated
February 10, 2006.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket No. 50–354,
Hope Creek Generating Station, Salem
County, New Jersey
Date of application for amendment:
June 7, 2004, as supplemented by letters
dated February 18, May 20, June 16, July
8, August 3, September 23, and
November 16, 2005, and February 6,
2006.
Brief description of amendment: The
amendment revised the Technical
Specifications (TSs) to reflect an
expanded operating domain resulting
from the implementation of the Average
Power Range Monitor, Rod Block
Monitor TSs/Maximum Extended Load
Line Limit Analysis (ARTS/MELLLA).
Date of issuance: February 8, 2006.
Effective date: As of the date of
issuance, to be implemented within 120
days.
Amendment No.: 163.
Facility Operating License No. NPF–
57: This amendment revised the TSs.
Date of initial notice in Federal
Register: September 14, 2004 (69 FR
55471). The supplements dated
February 18, May 20, June 16, July 8,
August 3, September 23, and November
16, 2005, and February 6, 2006,
provided clarifying information that did
not change the initial proposed no
significant hazards consideration
determination or expand the application
beyond the scope of the original Federal
Register notice.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated February 8,
2006.
PO 00000
Frm 00083
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No significant hazards consideration
comments received: No.
Nuclear Management Company, LLC,
Docket Nos. 50–282 and 50–306, Prairie
Island Nuclear Generating Plant, Units
1 and 2, Goodhue County, Minnesota
Date of application for amendments:
February 1, 2005, supplemented by
letters dated February 22, September 16,
December 2, 2005, and January 5, 2006.
Brief description of amendments: The
amendments revise the spent fuel pool
(SFP) criticality analysis methodology
and technical specifications governing
the storage of irradiated fuel in the SFP.
The licensee’s amendment request
stated that subcritical conditions would
be maintained in the SFP under the
revised technical specification storage
requirements.
Date of issuance: February 5, 2006.
Effective date: As of the date of
issuance and shall be implemented
within 90 days.
Amendment Nos.: 172, 162.
Facility Operating License Nos. DPR–
42 and DPR–60: Amendments revised
the Technical Specifications.
Date of initial notice in Federal
Register: March 15, 2005, (70 FR
12748). The supplemental letters
contained clarifying information and
did not change the initial no significant
hazards consideration determination
and did not expand the scope of the
original Federal Register notice. The
Commission’s related evaluation of the
amendments is contained in a Safety
Evaluation dated February 5, 2006.
No significant hazards consideration
comments received: No.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–348 and 50–364,
Joseph M. Farley Nuclear Plant, Units 1
and 2, Houston County, Alabama
Date of amendments request: January
19, 2005, as supplemented on June 9
(two letters) and November 18, 2005.
Brief Description of amendments: The
amendment authorizes revision of the
Updated Final Safety Analysis Report
(UFSAR) to reflect the utilization of firerated electrical Mineral Insulated cables
in lieu of Appendix R, Section III.G.2 1hour rated fire barriers.
Date of issuance: February 13, 2006.
Effective date: As of the date of
issuance, to be incorporated into the
UFSAR at the time of its next update.
Amendment No.: 162.
Renewed Facility Operating License
Nos. NPF–2 and NPF–8: Amendment
authorizes revision to the UFSAR.
Date of initial notice in Federal
Register: April 26, 2005 (70 FR 21464).
The supplemental letters provided
clarifying information that was within
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the scope of the initial notice and did
not change the initial proposed no
significant hazards consideration
determination. The Commission’s
related evaluation of the amendments is
contained in a Safety Evaluation dated
February 13, 2006.
No significant hazards consideration
comments received: No.
Notice of Issuance of Amendments to
Facility Operating Licenses and Final
Determination of No Significant
Hazards Consideration and
Opportunity for a Hearing (Exigent
Public Announcement or Emergency
Circumstances)
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application for the
amendment complies with the
standards and requirements of the
Atomic Energy Act of 1954, as amended
(the Act), and the Commission’s rules
and regulations. The Commission has
made appropriate findings as required
by the Act and the Commission’s rules
and regulations in 10 CFR Chapter I,
which are set forth in the license
amendment.
Because of exigent or emergency
circumstances associated with the date
the amendment was needed, there was
not time for the Commission to publish,
for public comment before issuance, its
usual Notice of Consideration of
Issuance of Amendment, Proposed No
Significant Hazards Consideration
Determination, and Opportunity for a
Hearing.
For exigent circumstances, the
Commission has either issued a Federal
Register notice providing opportunity
for public comment or has used local
media to provide notice to the public in
the area surrounding a licensee’s facility
of the licensee’s application and of the
Commission’s proposed determination
of no significant hazards consideration.
The Commission has provided a
reasonable opportunity for the public to
comment, using its best efforts to make
available to the public means of
communication for the public to
respond quickly, and in the case of
telephone comments, the comments
have been recorded or transcribed as
appropriate and the licensee has been
informed of the public comments.
In circumstances where failure to act
in a timely way would have resulted, for
example, in derating or shutdown of a
nuclear power plant or in prevention of
either resumption of operation or of
increase in power output up to the
plant’s licensed power level, the
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Commission may not have had an
opportunity to provide for public
comment on its no significant hazards
consideration determination. In such
case, the license amendment has been
issued without opportunity for
comment. If there has been some time
for public comment but less than 30
days, the Commission may provide an
opportunity for public comment. If
comments have been requested, it is so
stated. In either event, the State has
been consulted by telephone whenever
possible.
Under its regulations, the Commission
may issue and make an amendment
immediately effective, notwithstanding
the pendency before it of a request for
a hearing from any person, in advance
of the holding and completion of any
required hearing, where it has
determined that no significant hazards
consideration is involved.
The Commission has applied the
standards of 10 CFR 50.92 and has made
a final determination that the
amendment involves no significant
hazards consideration. The basis for this
determination is contained in the
documents related to this action.
Accordingly, the amendments have
been issued and made effective as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) The application for
amendment, (2) the amendment to
Facility Operating License, and (3) the
Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment, as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
PO 00000
Frm 00084
Fmt 4703
Sfmt 4703
10083
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
The Commission is also offering an
opportunity for a hearing with respect to
the issuance of the amendment. Within
60 days after the date of publication of
this notice, the licensee may file a
request for a hearing with respect to
issuance of the amendment to the
subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland,
and electronically on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If there
are problems in accessing the document,
contact the PDR Reference staff at 1
(800) 397–4209, (301) 415–4737, or by email to pdr@nrc.gov. If a request for a
hearing or petition for leave to intervene
is filed by the above date, the
Commission or a presiding officer
designated by the Commission or by the
Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also identify the specific
contentions which the petitioner/
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requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner intends to
rely in proving the contention at the
hearing. The petitioner must also
provide references to those specific
sources and documents of which the
petitioner is aware and on which the
petitioner intends to rely to establish
those facts or expert opinion. The
petition must include sufficient
information to show that a genuine
dispute exists with the applicant on a
material issue of law or fact.1
Contentions shall be limited to matters
within the scope of the amendment
under consideration. The contention
must be one which, if proven, would
entitle the petitioner to relief. A
petitioner/requestor who fails to satisfy
these requirements with respect to at
least one contention will not be
permitted to participate as a party.
Each contention shall be given a
separate numeric or alpha designation
within one of the following groups:
1. Technical—primarily concerns/
issues relating to technical and/or
health and safety matters discussed or
referenced in the applications.
2. Environmental—primarily
concerns/issues relating to matters
discussed or referenced in the
environmental analysis for the
applications.
3. Miscellaneous—does not fall into
one of the categories outlined above.
As specified in 10 CFR 2.309, if two
or more petitioners/requestors seek to
co-sponsor a contention, the petitioners/
requestors shall jointly designate a
representative who shall have the
authority to act for the petitioners/
requestors with respect to that
contention. If a petitioner/requestor
seeks to adopt the contention of another
sponsoring petitioner/requestor, the
petitioner/requestor who seeks to adopt
the contention must either agree that the
sponsoring petitioner/requestor shall act
as the representative with respect to that
contention, or jointly designate with the
sponsoring petitioner/requestor a
representative who shall have the
1 To the extent that the applications contain
attachments and supporting documents that are not
publicly available because they are asserted to
contain safeguards or proprietary information,
petitioners desiring access to this information
should contact the applicant or applicant’s counsel
and discuss the need for a protective order.
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17:06 Feb 27, 2006
Jkt 208001
authority to act for the petitioners/
requestors with respect to that
contention.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing. Since the Commission has
made a final determination that the
amendment involves no significant
hazards consideration, if a hearing is
requested, it will not stay the
effectiveness of the amendment. Any
hearing held would take place while the
amendment is in effect.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer or
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
Detroit Edison Company, Docket No.
50–341, Fermi 2, Monroe County,
Michigan
Date of amendment request: February
5, 2006, as supplemented February 5,
2006.
Description of amendment request:
The amendment revised Technical
PO 00000
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Specification 3.8.1, ‘‘AC Sources—
Operating,’’ to extend the allowed
outage time for Emergency Diesel
Generator 12 from seven days to 14 days
for one specific incident.
Date of issuance: February 6, 2006.
Effective date: As of the date of
issuance and shall be implemented
immediately.
Amendment No.: 171.
Facility Operating License No. 50–
341: Amendment revised the Technical
Specifications.
Public comments requested as to
proposed no significant hazards
consideration (NSHC): No. The
Commission’s related evaluation of the
amendment, finding of emergency
circumstances, state consultation, and
final NSHC determination are contained
in a safety evaluation dated February 6,
2006.
Attorney for licensee: David G.
Pettinari, Legal Department, 688 WCB,
Detroit Edison Company, 2000 2nd
Avenue, Detroit, Michigan 48226–1279.
NRC Branch Chief: Timothy J. Kobetz,
Acting.
Dated at Rockville, Maryland, this 16th day
of February, 2006.
For the Nuclear Regulatory Commission.
Catherine Haney,
Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. 06–1737 Filed 2–27–06; 8:45 am]
BILLING CODE 7590–01–P
POSTAL RATE COMMISSION
Briefings on International Mail and FY
2005 Cost and Revenue Analysis
Postal Rate Commission.
Notice of briefings.
AGENCY:
ACTION:
SUMMARY: The Commission will host
two briefings on March 1, 2006. One
will address a study of postal volume
growth in developing countries. The
other will address the effect of certain
data collection design changes on a
major Postal Service annual financial
report. These briefings will provide an
open forum for the presentation of
information of interest to the postal
community and the general public.
SUPPLEMENTARY INFORMATION: The first
briefing will be presented by an
economist in the Universal Postal
Union’s International Bureau, who will
address the preliminary results of a
study of factors that contribute to postal
volume growth in developing countries.
This briefing will also address the
reasons why factors that affect postal
volume growth in industrialized
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Agencies
[Federal Register Volume 71, Number 39 (Tuesday, February 28, 2006)]
[Notices]
[Pages 10071-10084]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: 06-1737]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a(2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from February 3, 2006, to February 15, 2006. The
last biweekly notice was published on February 14, 2006 (71 FR 7804).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
Involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The
filing of requests for a hearing and petitions for leave to intervene
is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
[[Page 10072]]
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland, 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemaking and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by email to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam
Electric Plant, Unit No. 2, Darlington County, South Carolina
Date of amendment request: November 30, 2005.
Description of amendment request: The proposed amendment would
revise the frequency of the diesel generator automatic trips bypass
surveillance requirement (SR) 3.8.1.11 from 18 months to 24 months.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
No. The proposed change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated. The proposed change decreases the frequency of SR
3.8.1.11, verification of the DG [diesel generator] automatic trips
bypass, from 18 months to 24 months. The DG automatic trips bypass
circuitry is required for DG operability and reliability during
emergency operation of the DG. The proposed test frequency will
continue to assure that the DG will perform as required. Therefore,
the proposed change does not involve a significant increase in the
probability or consequences of an accident previously evaluated,
because the factors that are used to determine the probability and
consequences of accidents are not being affected.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any previously evaluated?
No. The proposed change does not create the possibility of a new
or different kind of accident from any previously evaluated. There
are no new or different accident initiators or sequences being
created by the proposed Technical Specifications change. The
required surveillance performed at the proposed frequency will
continue to provide assurance that the trips bypass function is
operable and is properly supporting operation of the associated DG.
Therefore, the proposed change does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
3. Do the proposed changes involve a significant reduction in
the margin of safety?
No. The proposed change does not involve a significant reduction
in the margin of
[[Page 10073]]
safety. The proposed change will continue to ensure that the DG
trips bypass function operates as designed. The functionality and
operability of emergency power system is not being changed.
Therefore, the proposed change does not involve a significant
reduction in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Branch Chief: Michael L. Marshall, Jr.
Dominion Nuclear Connecticut, Inc., Docket No. 50-336, Millstone Power
Station, Unit No. 2, New London County, Connecticut
Date of amendment request: January 4, 2006.
Description of amendment request: The proposed amendment would
change the Millstone Power Station, Unit No. 2 Technical Specification
(TS) 3/4.3.3.8, ``Instrumentation, Accident Monitoring,'' to modify the
description of the pressurizer power operated relief valves (PORVs) and
pressurizer safety valves position indicators.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed amendment removes the wording ``Acoustic Monitor,''
which provides specific details related to system design, from items
4 and 6 of TS 3/4.3.3.8, Tables 3.3-11 and 4.3-7. The PORVs and
Pressurizer Safety Valves position indicators (and the associated
``Acoustic Monitor'') provide only indications of valve position.
They do not constitute a design feature that is an initial condition
for a design basis accident or transient analysis. Furthermore, they
do not affect the function of the system, equipment in the system or
actuate to mitigate a design basis accident or transient. Therefore,
the proposed changes do not increase the probability or consequences
of an accident previously evaluated.
Additionally, the TS retains the requirement for the total and
minimum channels required to be OPERABLE and to verify channel
OPERABILITY at the designated frequencies. The PORVs and Pressurizer
Safety Valves are equipped with positive position indication that
meets the requirements of RG [Regulatory Guide] 1.97.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed changes do not impact the capability of existing
equipment to perform its intended functions. No system setpoints are
being modified and no changes are being made to the method in which
plant operations are conducted. No new failure modes that would
impact accident analyses are introduced by the proposed changes. The
proposed amendment does not introduce accident initiators or
malfunctions that would cause a new or different kind of accident.
Therefore, the proposed amendment does not create the possibility of
a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
The proposed amendment removes the wording ``Acoustic Monitor''
from items 4 and 6 of TS 3/4.3.3.8, Table[s] 3.3-11 and 4.3-7. The
proposed changes do not affect any of the assumptions used in the
accident analysis, nor does it affect any operability requirements
for equipment important to plant safety. Therefore, the margin of
safety is not impacted by the proposed amendment.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Lillian M. Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc., Rope Ferry Road, Waterford, CT
06385.
NRC Branch Chief: Darrell J. Roberts.
Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear
Station, Nemaha County, Nebraska
Date of amendment request: December 30, 2005.
Description of amendment request: The proposed amendment
establishes a combined leakage rate limit for the sum of the four Main
Steam line leakage rates that is equal to four times the current
individual Main Steam Isolation Valve (MSIV) leakage rate limit.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
The proposed amendment does not involve a change to structures,
systems, or components that would affect the probability of an
accident previously evaluated in the Cooper Nuclear Station (CNS)
Updated Safety Analysis Report (USAR). The proposed amendment
results in no change in the radiological consequences of the design
basis Loss-of-Coolant Accident (LOCA) as currently analyzed for CNS.
That analysis was calculated for a combined Main Steam Isolation
Valve (MSIV) leakage for determining acceptance to the regulatory
limits for the offsite and Control Room radiation doses, as
contained in 10 CFR 100 [Part 100 of Title 10 of the Code of Federal
Regulations] and 10 CFR 50[,] Appendix A, General Design Criterion
(GDC) 19. The aggregate Main Steam line leakage rate limit has no
adverse effect on the environmental qualification of equipment
important to safety, as provided for in 10 CFR 50.49.
Based on the above conclusions, this proposed amendment does not
involve a significant increase in the probability or consequences of
an accident previously evaluated.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change does not modify the MSIVs or any other plant
system or structure associated with this amendment and therefore,
will not affect their capability to perform their design function.
The combined total Main Steam line leakage rate is included in the
current radiological analyses for the assessment of radiation
exposure following an accident. This License Amendment Request
revises the allowable leakage rate from a per valve limit to a total
combined leakage rate limit for all four Main Steam lines but does
not change the cumulative limit.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously analyzed.
3. Do the proposed changes involve a significant reduction in
the margin of safety?
Response: No.
The leakage rate limit specified for the MSIVs is used to
quantify the maximum amount of Secondary Containment bypass leakage
assumed in the LOCA radiological analysis. Results of the analysis
are evaluated against the dose limits contained in 10 CFR 50[,]
Appendix A[,] GDC 19 and 10 CFR 100. The margin of safety in this
context is considered to be the difference between the calculated
dose exposures and the limits provided by GDC 19 and 10 CFR 100.
Therefore, since the proposed combined Main Steam line leakage
rate limit is unchanged from the assumed maximum leakage rate for
MSIVs, for the purpose of calculating [a] potential radiation dose,
the margin of safety is not affected because the postulated
radiation doses remain the same.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three
[[Page 10074]]
standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff
proposes to determine that the amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John C. McClure, Nebraska Public Power
District, Post Office Box 499, Columbus, NE 68602-0499.
NRC Branch Chief: David Terao.
Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear
Station, Nemaha County, Nebraska
Date of amendment request: January 30, 2006.
Description of amendment request: The proposed change allows a
delay time for entering a supported system Technical Specification (TS)
when the inoperability is due solely to an inoperable snubber, if risk
is assessed and managed consistent with the program in place for
complying with the requirements of 10 CFR 50.65(a)(4). Limiting
Condition for Operation (LCO) 3.0.8 is added to the TS to provide this
allowance and define the requirements and limitations for its use.
This change was proposed by the industry's Technical Specification
Task Force (TSTF) and is designated TSTF-372, Revision 4. The NRC staff
issued a notice of opportunity for comment in the Federal Register on
November 24, 2004 (69 FR 68412), on possible amendments concerning
TSTF-372, including a model safety evaluation and model no significant
hazards consideration (NSHC) determination, using the consolidated line
item improvement process. The NRC staff subsequently issued a notice of
availability of the models for referencing in license amendment
applications in the Federal Register on May 4, 2005 (70 FR 23252). The
licensee affirmed the applicability of the following NSHC determination
in its application dated January 30, 2006.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
Criterion 1--The Proposed Change Does Not Involve a Significant
Increase in the Probability or Consequences of an Accident
Previously Evaluated.
The proposed change allows a delay time for entering a supported
system TS when the inoperability is due solely to an inoperable
snubber if risk is assessed and managed. The postulated seismic
event requiring snubbers is a low-probability occurrence and the
overall TS system safety function would still be available for the
vast majority of anticipated challenges. Therefore, the probability
of an accident previously evaluated is not significantly increased,
if at all. The consequences of an accident while relying on
allowance provided by proposed LCO 3.0.8 are no different than the
consequences of an accident while relying on the TS required actions
in effect without the allowance provided by proposed LCO 3.0.8.
Therefore, the consequences of an accident previously evaluated are
not significantly affected by this change. The addition of a
requirement to assess and manage the risk introduced by this change
will further minimize possible concerns. Therefore, this change does
not involve a significant increase in the probability or
consequences of an accident previously evaluated.
Criterion 2--The Proposed Change Does Not Create the Possibility
of a New or Different Kind of Accident from any Previously
Evaluated.
The proposed change does not involve a physical alteration of
the plant (no new or different type of equipment will be installed).
Allowing delay times for entering supported system TS when
inoperability is due solely to inoperable snubbers, if risk is
assessed and managed, will not introduce new failure modes or
effects and will not, in the absence of other unrelated failures,
lead to an accident whose consequences exceed the consequences of
accidents previously evaluated. The addition of a requirement to
assess and manage the risk introduced by this change will further
minimize possible concerns. Thus, this change does not create the
possibility of a new or different kind of accident from an accident
previously evaluated.
Criterion 3--The Proposed Change Does Not Involve a Significant
Reduction in a Margin of Safety.
The proposed change allows a delay time for entering a supported
system TS when the inoperability is due solely to an inoperable
snubber, if risk is assessed and managed. The postulated seismic
event requiring snubbers is a low-probability occurrence and the
overall TS system safety function would still be available for the
vast majority of anticipated challenges. The risk impact of the
proposed TS changes was assessed following the three-tiered approach
recommended in Regulatory Guide 1.177. A bounding risk assessment
was performed to justify the proposed TS changes. The proposed LCO
3.0.8 defines limitations on the use of the provision and includes a
requirement for the licensee to assess and manage the risk
associated with operation with an inoperable snubber. The net change
to the margin of safety is insignificant. Therefore, this change
does not involve a significant reduction in a margin of safety.
The NRC staff proposes to determine that the amendment request
involves no significant hazards consideration.
Attorney for licensee: Mr. John C. McClure, Nebraska Public Power
District, Post Office Box 499, Columbus, NE 68602-0499.
NRC Branch Chief: David Terao.
Nuclear Management Company, LLC, Docket Nos. 50-282 and 50-306, Prairie
Island Nuclear Generating Plant, Units 1 and 2, Goodhue County,
Minnesota
Date of amendment request: November 11, 2005.
Description of amendment request: The proposed amendments would
revise Technical Specification (TS) 3.6.5, ``Containment Spray and
Cooling Systems''; an existing Condition, two Surveillance
Requirements, and add a new Condition which will allow continued plant
operation with TS limitations when two Containment Cooling System fan
coil units (FCUs), one in each train, are inoperable.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
This license amendment proposes to revise the Technical
Specifications to allow plant operation to continue for a limited
time period under Technical Specification controls with two fan coil
units, one fan coil unit from each containment cooling train,
providing the required cooling function. Analyses demonstrate that
any two fan coil units, whether they are in the same train or from
opposite trains, are sufficient to supply the required containment
cooling following a design basis accident when the plant in the
proper configuration as required by the proposed Technical
Specifications.
The containment cooling system is required for accident
mitigation and is not an accident initiator, thus revising the
equipment required to provide the safety function does not involve a
significant increase in the probability of an accident previously
evaluated.
Since the proposed change continues to provide the post-accident
containment cooling function under Technical Specification controls,
this change does not involve an increase in the consequences of an
accident. Thus this change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
This license amendment proposes to revise the Technical
Specifications to allow plant operation to continue for a limited
time period under Technical Specification controls with two fan coil
units, one fan coil unit from each containment cooling train,
providing the required cooling function. Analyses demonstrate that
any two fan coil units, whether they are in the same train or
[[Page 10075]]
from opposite trains, are sufficient to supply the required
containment cooling following a design basis accident when the plant
in the proper configuration as required by the proposed Technical
Specifications.
The proposed licensing basis changes do not involve a change in
the function or use of the containment cooling system. It does
assure that the containment cooling function is provided during
plant operations for post-accident mitigation. There are no new
failure modes or mechanisms created through allowing different
combinations of fan coil units to provide the cooling function as
proposed by this Technical Specification change. There are no new
accident precursors generated by providing the required cooling
function with an operable fan coil unit from each train.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
Response: No.
This license amendment proposes to revise the Technical
Specifications to allow plant operation to continue for a limited
time period under Technical Specification controls with two fan coil
units, one fan coil unit from each containment cooling train,
providing the required cooling function. Analyses demonstrate that
any two fan coil units, whether they are in the same train or from
opposite trains, are sufficient to supply the required containment
cooling following a design basis accident when the plant in the
proper configuration as required by the proposed Technical
Specifications.
Current plant Technical Specifications allow plant operation to
continue for 7 days with the containment cooling function provided
by the two operable fan coil units of a single operable containment
cooling train. This is acceptable because engineering analyses
demonstrate that the two fan coil units of a single train can
provide the required post-accident containment cooling.
Likewise, engineering analyses demonstrate that any two fan coil
units from opposite containment cooling trains can also provide the
required post-accident containment cooling if the cooling water flow
to the other fan coil unit in each train is isolated. This license
amendment request proposes Technical Specifications which will allow
plant operation to continue for 7 days with the containment cooling
function provided by two fan coils from opposite trains provided the
cooling water flow to the other fan coil unit in each train is
isolated. Thus, from a cooling capacity perspective, this proposed
Technical Specification change does not involve a reduction in a
margin of safety.
When inoperable plant systems are under Technical Specification
controls that limit the time for inoperability, a single failure in
addition to the inoperable equipment is not postulated. Therefore,
whether two inoperable fan coil units are in the same train or
opposite trains does not change the availability of the two
remaining operable fan coil units. Thus from a Technical
Specification perspective, this proposed Technical Specification
change does not involve a reduction in a margin of safety.
Therefore, based on the considerations given above, the proposed
changes do not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Attorney for licensee: Jonathan Rogoff, Esquire, Vice President,
Counsel & Secretary, Nuclear Management Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Acting Branch Chief: Timothy J. Kobetz.
Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station,
Unit No. 1, Washington County, Nebraska
Date of amendment request: December 19, 2005.
Description of amendment request: The proposed change will revise
Fort Calhoun Station, (FCS) Technical Specification 2.4, ``Containment
Cooling,'' (and associated Bases) to reduce the required number of
operable Containment Spray (CS) pumps from three to two in order to
enhance net positive suction head (NPSH) margins. This change will be
accomplished by disabling the containment spray actuation signal (CSAS)
automatic start feature of CS pump SI-3C. This change will reduce the
head loss across the containment sump strainers during the
recirculation phase of a design-basis accident (DBA) by reducing flow
rates, and will improve NPSH available (NPSHA).
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The Containment Spray (CS) system is not an initiator of any
accident previously evaluated at the Fort Calhoun Station (FCS); the
CS system is an accident mitigation system. The CS system's
licensing basis functions are to limit the containment pressure rise
and reduce the leakage of airborne radioactivity from the
containment by providing a means for cooling the containment
following a loss-of-coolant accident (LOCA) or main steam line break
(MSLB) inside containment. The proposed change disables the CSAS
automatic start feature of one of the three CS pumps.
The only FCS safety analysis that currently assumes three CS
pumps operating to mitigate an accident is the Containment Pressure
Analysis for a[n] MSLB inside containment. Even though this analysis
assumes operation of all three CS pumps, it also shows that peak
containment pressure occurs prior to the CS system starting,
therefore, the CS system does not mitigate the peak pressure for
a[n] MSLB. The reviews evaluated both existing AORs [analyses of
record] and those analyses developed for the Steam Generator
Replacement (RSG) project. The analysis developed for the RSG
project that evaluates the Containment Pressure Analysis for MSLB
inside containment was reviewed for the impact of reducing the
number of operating CS pumps from three to two. This review
determined that the RSG MSLB analysis will be acceptable and will
continue to be bounded by the analysis currently documented in USAR.
AOR peak pressure is unaffected by implementation of this proposed
change. Therefore, the combination of the RSG project and this
containment spray modification will not result in an increase in the
currently documented peak containment pressure for an MSLB.
Therefore, the evaluation for the MSLB event has determined that the
containment pressure response is acceptable with less than three CS
pumps operating.
The LOCA analysis source term is based on operation of minimum
safeguards due to a worst-case single failure. The minimum
safeguards configuration is unchanged by this modification.
Following implementation of the proposed change at least one CS pump
will be available to mitigate a LOCA as currently assumed in the
analysis, therefore, the proposed change will have no adverse effect
on the radiological consequences following a LOCA. The analyses that
establish the radiological consequences for the site are based on a
Large Break LOCA with a single CS pump in operation, therefore,
single CS pump operation during a[n] MSLB inside containment is
bounded by the LOCA analysis.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed change will reduce the number of operable CS pumps
from three to two; however, previous accident analyses will remain
valid. No credible new failure mechanisms, malfunctions, or accident
initiators not considered in the design and licensing basis have
been created and none of the initial condition assumptions of any
accident evaluated in the safety analysis are impacted.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
[[Page 10076]]
Response: No.
The containment building and associated penetrations are
designed to withstand an internal pressure of 60 psig at 305 [deg]F,
including all thermal loads resulting from the temperature
associated with this pressure, with a leakage rate of 0.1 percent by
weight or less of the contained volume per 24 hours. The CS System
and the Containment Fan Coolers are credited for maintaining
containment pressure and temperatures within design limitations, and
assure that the release of fission products to the environment
following a design[-]basis accident will not exceed regulatory
guidelines. The FCS licensing basis credits only one of the three CS
pumps to limit the containment pressure to below the design value
for a LOCA. Currently, the FCS licensing basis credits three CS
pumps for a[n] MSLB, however, the CS system is not credited for
limiting peak containment pressure for a[n] MSLB.
The EEQ [electrical equipment qualification] profile developed
for the current plant configuration bounds those associated with the
upcoming RSG modification. Both the proposed CS system changes and
the RSG projects are scheduled for the same refueling outage. The
thermal lag analysis of equipment performed using the current plant
configuration demonstrated a large margin between the equipment
evaluated during the accident versus the conditions under which it
was tested. The RSG modification will further increase this margin.
As part of the RSG effort the EEQ analysis will be revised to
address RSG issues and will include the changes to containment
spray. When the margins associated with the current analysis as well
as increases in margin when the new analysis is implemented it is
expected that the changes to the containment spray system will not
produce an adverse result. All equipment will remain qualified to
operate in the accident environment.
Additionally, the CFCs [containment fan coolers] operate
independently of the CS system to remove heat from the containment
atmosphere. The CFCs consist of two redundant trains; each train
with one air cooling and filtering unit and one air cooling unit,
for a total of four cooling units. Operation of the CFCs is credited
in the MSLB containment pressure analysis. The CFCs are not impacted
by this proposed change. During the MSLB containment spray takes
place after the peak containment pressure occurs. Therefore, the
licensing basis capabilities of the Containment Cooling System,
which consists of the CS and CFCs, is not adversely affected by the
proposed change; the ability to maintain containment peak pressure
and temperature and long[-]term containment pressure and temperature
will be maintained.
Particulate fission products that are released into the
containment following a DBA are removed by the CS system for those
events that result in CS actuation. The water spray strips
radioactive particles from the atmosphere where they fall to the
floor and are washed into the containment sump. The radiological
consequences analysis credits CS system operation for removal of
particulates from the containment atmosphere during a LOCA. The LOCA
analysis source term is based on operation of minimum safeguards due
to a worst-case single failure, and a presumption of core damage.
Minimum safeguards corresponds to one CS pump and one CS header
operation and take into account pump degradation, and instrument
uncertainties. The analyses that establish the radiological
consequences for the site are not impacted by the proposed
modification. These analyses are based on a Large Break LOCA with a
single CS pump in operation. Therefore, single CS pump operation
bounds the plant configuration following the proposed modification.
The Large Break LOCA assumes that there will be three CS pumps
operating when evaluating the effects of containment pressure on
ECCS [emergency core cooling system] performance. The analysis
assumes three CS pumps, which minimizes containment pressure, to
conservatively evaluate ECCS performance in response to a LOCA. The
use of two CS pumps versus three improves ECCS performance and thus
increases margin to 10 CFR 50.46 limits on peak clad temperature.
In summary, following implementation of the proposed change:
Peak containment pressure for analyzed DBAs will not be
increased;
The assumptions used in the environmental qualification
of equipment exposed to the containment atmosphere following a DBA
remaining bounding; and
The radiological consequences for the bounding DBA
remains unchanged.
The currently calculated peak clad temperature
following a LOCA remains bounded by existing analysis.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: James R. Curtiss, Esq., Winston & Strawn,
1400 L Street, NW., Washington, DC 20005-3502.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Company, Docket No. 50-323, Diablo Canyon
Nuclear Power Plant, Unit No. 2, San Luis Obispo County, California
Date of amendment requests: January 13, 2006.
Description of amendment requests: The proposed amendment would
revise Technical Specification 5.6.5, ``Core Operating Limits Report
(COLR),'' by adding WCAP-16009-P-A, ``Realistic Large-Break LOCA [Loss-
of-Coolant Accident] Evaluation Methodology Using the Automated
Statistical Treatment of Uncertainty Method (ASTRUM),'' dated January
2005, as an approved analytical method for determining core operating
limits for Unit 2.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change to allow the use of the best estimate loss-
of-coolant accident (LOCA) analysis methodology using the automated
statistical treatment of uncertainty methodology (ASTRUM) does not
involve a physical alteration of any plant equipment or change
operating practice at Unit 2 of Diablo Canyon Power Plant (DCPP).
Therefore, there will be no increase in the probability of a LOCA.
The consequences of a LOCA are not being increased.
The plant conditions assumed in the analysis are bounded by the
design conditions for all equipment in Unit 2. That is, it is shown
that the emergency core cooling system is designed so that its
calculated cooling performance conforms to the criteria contained in
10 CFR [Title 10 of the Code of Federal Regulations, Section] 50.46,
paragraph b. No other accident is potentially affected by this
change.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different accident from any accident previously evaluated?
Response: No.
The proposed change would not result in any physical alteration
to any Unit 2 system, and there would not be a change in the method
by which any safety [-]related system performs its function.
Analyses of transient events have confirmed that no transient event
results in a new sequence of events that could lead to a new
accident scenario. The parameters assumed in the analysis are within
the design limits of existing plant equipment.
In addition, employing the ASTRUM methodology does not create
any new failure modes that could lead to a different kind of
accident. The design of all systems remains unchanged and no changes
are being made to any reactor protection system or engineered
safeguard features actuation setpoints.
Based on this review, it is concluded that no new accident
scenarios, failure mechanisms or limiting single failures are
introduced as a result of the proposed changes.
Therefore, the proposed change does not create the possibility
of a new or different accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
[[Page 10077]]
It has been shown that the analytic technique used in the
analysis realistically describes the expected behavior of the DCPP
Unit 2 reactor system during a postulated LOCA. Uncertainties have
been accounted for as required by 10 CFR 50.46. A sufficient number
of LOCAs with different break sizes, different locations, and other
variations in properties have been analyzed to provide assurance
that the most severe postulated LOCAs were analyzed. The analysis
has demonstrated that all acceptance criteria contained in 10 CFR
50.46[,] paragraph b continue to be satisfied.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Attorney for licensee: Richard F. Locke, Esq., Pacific Gas and
Electric Company, P.O. Box 7442, San Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Co., Docket No. 50-133, Humboldt Bay Power
Plant (HBPP), Unit 3 Humboldt County, California
Date of amendment request: January 19, 2006.
Description of amendment request: The licensee has proposed to
revise the Technical Specifications (TS) to correct an editorial error
in TS 3.1.2, ``Spent Fuel Pool Load Restrictions,'' and to change TS
5.2.2, ``Facility Staff,'' to allow the Unit 3 control room to be
temporarily unmanned during emergency conditions that require personnel
to evacuate buildings for their safety.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
The proposed editorial change has no impact on probability or
consequences of accidents. The following discussion applies to the
proposed change related to control room evacuation.
Allowing plant personnel to not continuously man the control
room has no impact on the probability of an accident from occurring,
especially acts of nature such as earthquakes and tsunamis.
The HBPP DSAR, Appendix A, and NRC SER, Section 10, dated April
29, 1987, evaluate various accidents at HBPP. Because all fuel has
been removed from the reactor vessel and stored in the spent fuel
pool, the majority of accidents analyzed pertain to events that
could only affect spent fuel or the spent fuel pool. All accidents
affecting spent fuel or the spent fuel pool do not require operator
action to protect the public health and safety or to maintain
offsite radiological doses well within regulatory limits. In
addition, NRC SER, Section 10.7, ``Impact of Tsunami Flooding,''
analyzes the impact of tsunami flooding. That analysis identifies a
likely impact of the tsunami to be a release of the radwaste tank
radionuclide contents to the bay and some damage to the reactor
building. For both situations, no operator action is required to
maintain offsite radiological doses well within regulatory limits.
Allowing the control room to be temporarily unmanned under
emergency conditions does not create problems that could increase
the consequences of an accident. The primary function of manning the
control room is for an operator to observe and acknowledge alarms.
Recovery actions to respond to damage to spent fuel, the spent fuel
pool, or radwaste tanks are taken by personnel outside the control
room. No recovery actions are required to be taken by the control
room operator to respond to damage to spent fuel, the spent fuel
pool, or radwaste tanks.
Evacuating occupied buildings, including the control room,
during a tsunami, allows the control room operator to return to the
control room after the tsunami and assess damage by observing
indicators and alarms. Upon returning to the control room, the
operator would be able to direct and monitor recovery efforts from
the control room that may be necessary to bring plant parameters
within required specifications.
If an operator remains in the control room during a tsunami and
becomes injured, that operator would be unable to direct and monitor
recovery efforts. Under this scenario, other plant personnel who
evacuated to higher ground onsite within the OCA would eventually
return to the plant, including the control room, and perform any
required recovery functions. Therefore, consequences of a tsunami
are not increased by not continually manning the control room during
the event.
2. Does the change create the possibility of a new or different
kind of accident from any accident evaluated?
Response: No.
The proposed editorial change has no impact on accidents. The
following discussion applies to the proposed change related to
control room evacuation.
As discussed in the response to question 1 above, none of the
analyzed accidents require operator action to keep offsite
radiological doses well within regulatory limits. In addition,
allowing plant personnel to not continuously man the control room
after an emergency situation has occurred, has no impact on the
possibility of a new or different kind of accident from occurring.
If the plant is evacuated, no work activities will be performed in
the plant. With the plant in SAFSTOR and no work being performed,
there are no actions required to be taken by personnel manning the
control room.
3. Does the change involve a significant reduction in a margin
of safety?
Response: The proposed editorial change has no impact on margin
of safety. The following discussion applies to the proposed change
related to control room evacuation.
NRC SER Section 10.8, ``Accident Analysis Conclusions,''
summarizes the consequences from accidents in terms of offsite
radiological doses. SER Section 10.8 includes the statement, ``The
(NRC) staff has determined that offsite radiological consequences
due to a tsunami are within acceptable dose guideline values.'' As
discussed in the response to question 1 above, none of the analyzed
accidents require operator action to keep offsite radiological doses
well within regulatory limits. Therefore, temporarily not manning
the control room during an emergency will have no impact on the
margin of safety.
The NRC staff has reviewed the licensee's analysis and, based upon
the staff's review of the licensee's analyses as well as the staff's
own evaluation, the staff concludes that the three standards of 10 CFR
50.92(c) are satisfied. Therefore, the NRC staff proposes to determine
that the amendment request involves no significant hazards
consideration.
Attorney for licensee: Richard F. Locke, Esquire, Pacific Gas and
Electric Company, P.O. Box 7442, San Francisco, California 94120.
NRC Section Chief: Claudia Craig.
STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South
Texas Project, Units 1 and 2, Matagorda County, Texas
Date of amendment request: January 31, 2006.
Description of amendment request: The amendments would revise
Technical Specification (TS) 3.8.3.1, ``Onsite Power Distribution-
Operating,'' to extend the allowed outage time (AOT) for an inoperable
Class 1E vital 120-volt alternating current inverter. The TS currently
provides an AOT of 24 hours to restore an inoperable inverter. Based on
risk-informed assessment, the amendments would extend the AOT to 7
days.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed formatting changes to TS 3.8.3.1 Action b and the
change to the AOT
[[Page 10078]]
for an inoperable inverter to be extended from 24 hours to 7 days do
not alter any plant equipment or operating practices in such a
manner that the probability of an accident is increased. The
proposed changes will not alter assumptions relative to the
mitigation of an accident or transient event.
An evaluation was performed to determine the risk significance
of the proposed change to the AOT. The risk evaluation concludes
that the [Delta]CDF [core damage frequency] and [Delta]LERF [large
early release frequency] associated with the proposed changes are
1.88E-07 and 2.05E-09, respectively, which are characterized as
``very small changes'' by RG [Regulatory Guide] 1.174. The ICCDP
[incremental conditional core damage probability] and ICLERP
[incremental conditional large early release probability] associated
with the proposed change are 3.63E-07 and 1.08E-08, respectively,
which are within the acceptance criteria in RG 1.177. Therefore, the
proposed changes do not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes do not involve a physical alteration of the
plant (no new or different type of equipment will be installed) or a
change in the methods governing normal plant operation. Therefore,
the proposed changes do not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
Margin of safety is associated with confidence in the ability of
the fission product barriers (i.e., fuel and fuel cladding, reactor
coolant pressure boundary, and containment structure) to limit the
level of radiation dose to the public. The proposed change to TS
3.8.3.1 to allow the AOT for an inoperable inverter to be extended
from 24 hours to 7 days has been evaluated for its effect on plant
safety. The risk-informed evaluation concludes that the [Delta]CDF
and [Delta]LERF associated with the proposed change are 1.88E-07 and
2.05E-09, respectively, which are characterized as ``very small
changes'' by RG 1.174. The ICCDP and ICLERP associated with the
proposed change are 3.63E-07 and 1.08E-08, respectively, which are
within the acceptance criteria in RG 1.177. The proposed changes to
the formatting of TS 3.8.3.1 Action b are administrative only and
have no impact on margin of safety. Therefore, the proposed changes
do not involve a significant reduction in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
request for amendments involves no significant hazards consideration.
Attorney for licensee: A. H. Gutterman, Esq., Morgan, Lewis &
Bockius, 1111 Pennsylvania Avenue, NW., Washington, DC 20004.
NRC Branch Chief: David Terao.
Tennessee Valley Authority (TVA), Docket No. 50-390, Watts Bar Nuclear
Plant, Unit 1 (WBN) Rhea County, Tennessee
Date of amendment request: December 14, 2005 (TS-05-07).
Description of amendment request: The proposed amendment would
revise Technical Specification Section 5.7.2.19, ``Containment Leakage
Rate Testing Program,'' to allow a one time, 5-year extension to the
current 10-year test interval for the performance-based leakage rate
test program for 10 CFR Part 50, Appendix J, Type A tests.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change for extending Type A test frequency does not
significantly increase the probability of an accident previously
evaluated since the change is not a modification to plant systems,
nor a change to plant operation that could initiate an accident.
TVA performed an evaluation of the risk significance for the
proposed increase to the WBN Unit 1 Type A test frequency. The
results of the TVA risk evaluation indicates that the increase in
Large Early Release Frequency (LERF) remains below the level of risk
significance defined in the NRC Regulatory Guide 1.174, ``An
Approach for Using Probabilistic Risk Assessment In Risk-Informed
Decisions On Plant-Specific Changes to the Licensing Basis.'' TVA's
evaluation indicates that the calculated increase in frequency for
all releases (small, large, early and late) and the increase in
radiation dose to the population are also non-risk significant.
The proposed test interval extension does not involve a
significant increase in the consequences of an accident. Research
documented in NUREG-1493, ``Performance-Based Containment Leakage-
Test Program,'' determined that generically, very few potential
containment leakage paths fail to be identified by Type A tests. An
analysis of 144 Type A test results, including 23 failures, found
that no failures were due to containment liner breach. The NUREG
concluded that reducing the Type A test frequency to once per 20
years would lead to an imperceptible increase in risk. Furthermore,
the NUREG concluded that Type B and C testing provides assurance
that containment leakage from penetration leak paths (i.e., valves,
flanges, containment air-locks) identify any leakage that would
otherwise be detected by the Type A tests.
In addition to the NUREG conclusions, TVA's American Society of
Mechanical Engineers (ASME) IWE program performs containment
inspections in order to detect evidence of degradation that may
either affect the containment structural integrity or leak
tightness.
Therefore, the proposed extension of the Type A test interval
does not involve a significant increase in the probability or
consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change to extend the Type A test interval does not
create the possibility of a new or different type of accident
because there are no physical changes made to the plant or plant
equipment governing normal plant operation. There are no changes to
the operation of the plant that would introduce a new failure mode
creating the possibility of a new or different kind of accident.
Therefore, the proposed extension does not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change to extend the Type A test interval will not
significantly reduce the margin of safety. A generic study
documented in NUREG-1493 indicates that extending the Type A leak
test interval to 20 years would result in an imperceptible increase
in risk to the public. The NUREG also found that, generically, the
containment leakage rate contributes a very small amount to the
individual risk and that the decrease in the Type A test frequency
would have a minimal effect on risk because most potential leakage
paths are detected by Type C testing.
Previous Type A leakage tests conducted on WBN Unit 1 indicate
that leakage from containment have been less than the 10 CFR 50,
Appendix J leakage limit of 1.0 La. A review of the
previous Type A test results indicate a stable trend with an
increase of less than 15 percent of La, well below the
1.0 La leakage limit.
Therefore, these test results, in conjunction with the research
findings from NUREG-1493, provide assurance that the proposed
extension to the Type A test interval does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: General Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A, Knoxville, Tennessee 37902.
NRC Branch Chief: Michael L. Marshall, Jr.
[[Page 10079]]
Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of application request: August 26, 2005, as supplemented by
letter dated December 16, 2005.
Description of amendment request: The amendment would authorize
changes to the Final Safety Analysis Report (FSAR) for the Callaway
Plant, Unit 1, that would revise the methodology for the reactor
coolant system (RCS) leak detection instrumentation. This revision
would clarify the requirements of the containment atmosphere gaseous
radioactivity monitor with regard to the RCS leak detection capability