Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 75489-75500 [05-24142]
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Federal Register / Vol. 70, No. 243 / Tuesday, December 20, 2005 / Notices
notice. To verify the status of meetings
call (recording)—(301) 415–1292.
Contact person for more information:
Michelle Schroll, (301) 415–1662.
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The NRC Commission Meeting
Schedule can be found on the Internet
at: https://www.nrc.gov/what-we-do/
policy-making/schedule.html.
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The NRC provides reasonable
accommodation to individuals with
disabilities where appropriate. If you
need a reasonable accommodation to
participate in these public meetings, or
need this meeting notice or the
transcript or other information from the
public meetings in another format (e.g.
braille, large print), please notify the
NRC’s Disability Program Coordinator,
August Spector, at 301–415–7080, TDD:
301–415–2100, or by e-mail at
aks@nrc.gov. Determinations on
requests for reasonable accommodation
will be made on a case-by-case basis.
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This notice is distributed by mail to
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longer wish to receive it, or would like
to be added to the distribution, please
contact the Office of the Secretary,
Washington, DC 20555 (301–415–1969).
In addition, distribution of this meeting
notice over the Internet system is
available. If you are interested in
receiving this Commission meeting
schedule electronically, please send an
electronic message to dkw@nrc.gov.
Dated: December 15, 2005.
R. Michelle Schroll,
Office of the Secretary.
[FR Doc. 05–24323 Filed 12–16–05; 2:18 pm]
BILLING CODE 7590–01–M
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
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hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from November
23, 2005 to December 8, 2005. The last
biweekly notice was published on
December 6, 2005 (70 FR 72667).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example,
in derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
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75489
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
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notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
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significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland 20852,
Attention: Rulemaking and
Adjudications Staff; (3) e-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
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Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
AmerGen Energy Company, LLC, et al.,
Docket No. 50–219, Oyster Creek
Nuclear Generating Station (OCNGS),
Ocean County, New Jersey
Date of amendment request: October
18, 2005.
Description of amendment request:
The licensee proposes to revise the
OCNGS Technical Specifications
Surveillance Requirement 4.4.B.1 to
provide an alternative means for testing
the electromatic relief valves located on
the main steam system. The proposed
change would allow demonstration of
the capability of the valves to perform
their function without requiring that the
valves be cycled with steam pressure
while installed.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration. The licensee’s analysis is
presented below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change modifies Technical
Specifications (TS) Surveillance Requirement
(SR) 4.4.B.1 to provide an alternative means
for testing the Electromatic Relief Valves
(EMRVs). Accidents are initiated by the
malfunction of plant equipment, or the
failure of plant structures, systems, or
components. The performance of EMRV
testing is not a precursor to any accident
previously evaluated and does not change the
manner in which the valves are operated.
The proposed testing requirements will not
contribute to the failure of the relief valves
nor any plant structure, system, or
component. AmerGen Energy Company, LLC
(AmerGen) has determined that the proposed
change in testing methodology provides an
equivalent level of assurance that the relief
valves are capable of performing their
intended safety functions. Thus, the
proposed change does not affect the
probability of an accident previously
evaluated.
The performance of EMRV testing provides
confidence that the EMRVs are capable of
depressurizing the reactor pressure vessel
(RPV). This will protect the reactor vessel
from overpressurization and allow the Core
Spray system to inject into the RPV as
designed. The proposed change involves the
manner in which the EMRVs are tested, and
has no effect on the types or amounts of
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radiation released or the predicted offsite
doses in the event of an accident. The
proposed testing requirements are sufficient
to provide confidence that the EMRVs are
capable of performing their intended safety
functions. In addition, a stuck open EMRV
accident is analyzed in the Updated Final
Safety Analysis Report (section 15.6.1). Since
the proposed testing requirements do not
alter the assumptions for the stuck open
EMRV accident, the consequences of any
accident previously evaluated are not
increased.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not affect the
assumed accident performance of the
EMRVs, nor any plant structure, system, or
component previously evaluated. The
proposed change does not involve the
installation of new equipment, and installed
equipment is not being operated in a new of
different manner. The change in test
methodology ensures that the EMRVs remain
capable of performing their safety functions.
No set points are being changed which would
alter the dynamic response of plant
equipment. Accordingly, no new failure
modes are introduced.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change will allow testing of
the EMRV actuation electrical circuitry,
including the solenoid, and mechanical
actuation components, without causing the
EMRV to open. Accordingly, in-situ EMRV
cycling is avoided, reducing the potential for
valve seat leakage. The valves will be tested
in accordance with the Inservice Test (IST)
Program that involves testing the valve at a
test facility using steam. The combination of
the IST and proposed actuator test provides
confidence that the EMRVs will perform their
design function.
The proposed change does not affect the
EMRV set points or the operational criteria
that directs the EMRVs to be manually
opened during plant transients. There are no
changes proposed which alter the set points
at which protective actions are initiated, and
there is no change to the operability
requirements for equipment assumed to
operate for accident mitigation.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the proposed
amendment involves no significant
hazards consideration.
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Attorney for licensee: Thomas S.
O’Neill, Associate General Counsel,
Exelon Generation Company, LCC, 4300
Winfield Road, Warrenville, IL 60555.
NRC Branch Chief: Darrell J. Roberts.
Entergy Operations Inc., Docket No. 50–
382, Waterford Steam Electric Station,
Unit 3, St. Charles Parish, Louisiana
Date of amendment request: October
27, 2005.
Description of amendment request:
This amendment proposes revisions to
the Technical Specification (TS)
Surveillance Requirements (SR) 4.5.2e
(Safety Injection), 4.6.2.1d (Containment
Spray), and 4.7.3b (Component Cooling
Water/Auxiliary Component Cooling
Water), by removing the words ‘‘during
shutdown.’’ Additionally, a revision to
delete TS SR 4.7.12.1c (Essential
Services Chilled Water) is requested.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Deletion of TS SR 4.7.12.1c is an
administrative change since there are no
valves in the essential services chilled water
system for which the TS SR 4.7.12.1c is
applicable. The deletion of the ‘‘during
shutdown’’ restriction from TS SRs 4.5.2e
(Safety Injection), 4.6.2.1d (Containment
Spray), and 4.7.3b (Component Cooling
Water/Auxiliary Component Cooling Water)
does not impact system operation nor does it
reduce TS SRs. Component actuations that
will be allowed to be performed online for
these TS SRs are either already actuated
online for other TS SRs or the components
to be actuated online are currently stroked
online in accordance with the Inservice
Testing Program. Therefore, the accident
mitigation features of the plant for previously
evaluated accidents are not affected by the
proposed amendment.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
Deletion of TS SR 4.7.12.1c is an
administrative change since there are no
valves in the essential services chilled water
system for which the TS SR 4.7.12.1c is
applicable. The deletion of the ‘‘during
shutdown’’ restriction from TS SRs 4.5.2e
(Safety Injection), 4.6.2.1d (Containment
Spray), and 4.7.3b (Component Cooling
Water/Auxiliary Component Cooling Water)
does not impact system operation nor does it
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reduce TS SR. Component actuations that
will be allowed to be performed online for
these TS SRs are either already actuated
online for other TS SRs or the components
to be actuated online are currently stroked
online in accordance with the Inservice
Testing Program. Therefore, the proposed
change introduces no new mode of plant
operation and no new possibility for an
accident is introduced.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
There are no automatic valves in the
essential services chilled water system that
actuate on an SIAS [safety injection actuation
signal]. Deletion of the ‘‘during shutdown’’
limitation does not change the TS test
requirements or surveillance frequency.
Therefore, existing TS surveillance
requirements are not reduced by the
proposed change, thus no margins of safety
are reduced.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: N.S. Reynolds,
Esquire, Winston & Strawn, 1700 K
Street NW., Washington, DC 20006–
3817
NRC Branch Chief: David Terao
FirstEnergy Nuclear Operating
Company, et al., Docket Nos. 50–334
and 50–412, Beaver Valley Power
Station, Unit Nos. 1 and 2 (BVPS–1 and
2), Beaver County, Pennsylvania
Date of amendment request:
November 7, 2005
Description of amendment request:
The amendment would revise the
Technical Specifications (TSs), to adopt
NRC-approved Revision 4 to Technical
Specification Task Force (TSTF)
Standard Technical Specification
Change Traveler, TSTF–449, ‘‘Steam
Generator Tube Integrity.’’ The
proposed amendment includes changes
to the TS definition of Leakage, TS 3/
4.4.6, ‘‘Reactor Coolant System
Leakage,’’ TS 3/4.4.5, ‘‘Steam
Generators,’’ and adds TS 6.19, ‘‘Steam
Generator (SG) Program,’’ and TS 6.9.7,
‘‘Steam Generator Tube Inspection
Report.’’ The proposed changes are
necessary in order to implement the
guidance for the industry initiative on
Nuclear Energy Institute (NEI) 97–06,
‘‘Steam Generator Program Guidelines.’’
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The NRC staff issued a notice of
opportunity for comment in the Federal
Register on March 2, 2005 (70 FR
10298), on possible amendments
adopting TSTF–449, including a model
safety evaluation and model no
significant hazards consideration
(NSHC) determination, using the
consolidated line item improvement
process. The NRC staff subsequently
issued a notice of availability of the
models for referencing in license
amendment applications in the Federal
Register on May 6, 2005 (70 FR 24126).
The licensee affirmed the applicability
of the following NSHC determination in
its application dated November 7, 2005.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
Criterion 1—The Proposed Change Does Not
Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated
The proposed change requires a SG
Program that includes performance criteria
that will provide reasonable assurance that
the SG tubing will retain integrity over the
full range of operating conditions (including
startup, operation in the power range, hot
standby, cooldown and all anticipated
transients included in the design
specification). The SG performance criteria
are based on tube structural integrity,
accident induced leakage, and operational
LEAKAGE.
A SGTR [steam generator tube rupture]
event is one of the design basis accidents that
are analyzed as part of a plant’s licensing
basis. In the analysis of a SGTR event, a
bounding primary to secondary LEAKAGE
rate equal to the operational LEAKAGE rate
limits in the licensing basis plus the
LEAKAGE rate associated with a doubleended rupture of a single tube is assumed.
For other design basis accidents such as a
MSLB [main steamline break], rod ejection,
and reactor coolant pump locked rotor the
tubes are assumed to retain their structural
integrity (i.e., they are assumed not to
rupture). These analyses typically assume
that primary to secondary LEAKAGE for all
SGs is 1 gallon per minute or increases to 1
gallon per minute as a result of accident
induced stresses. The accident induced
leakage criterion introduced by the proposed
changes accounts for tubes that may leak
during design basis accidents. The accident
induced leakage criterion limits this leakage
to no more than the value assumed in the
accident analysis.
The SG performance criteria proposed
change to the TS identify the standards
against which tube integrity is to be
measured. Meeting the performance criteria
provides reasonable assurance that the SG
tubing will remain capable of fulfilling its
specific safety function of maintaining
reactor coolant pressure boundary integrity
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throughout each operating cycle and in the
unlikely event of a design basis accident.
The performance criteria are only a part of
the SG Program required by the proposed
change to the TS. The program, defined by
NEI 97–06, Steam Generator Program
Guidelines, includes a framework that
incorporates a balance of prevention,
inspection, evaluation, repair, and leakage
monitoring. The proposed changes do not,
therefore, significantly increase the
probability of an accident previously
evaluated.
The consequences of design basis accidents
are, in part, functions of the DOSE
EQUIVALENT I–131 in the primary coolant
and the primary to secondary LEAKAGE
rates resulting from an accident. Therefore,
limits are included in the plant technical
specifications for operational leakage and for
DOSE EQUIVALENT I–131 in primary
coolant to ensure the plant is operated within
its analyzed condition. The typical analysis
of the limiting design basis accident assumes
that primary to secondary leak rate after the
accident is 1 gallon per minute with no more
than [500 gallons per day or 720 gallons per
day] in any one SG, and that the reactor
coolant activity levels of DOSE
EQUIVALENT I–131 are at the TS values
before the accident.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary coolant chemistry controls. The
proposed approach updates the current TSs
and enhances the requirements for SG
inspections. The proposed change does not
adversely impact any other previously
evaluated design basis accident and is an
improvement over the current TSs.
Therefore, the proposed change does not
affect the consequences of a SGTR accident
and the probability of such an accident is
reduced. In addition, the proposed changes
do not affect the consequences of an MSLB,
rod ejection, or a reactor coolant pump
locked rotor event, or other previously
evaluated accident.
The NRC staff proposes to determine
that the amendments request involves
no significant hazards consideration.
Attorney for licensee: Mary O’Reilly,
FirstEnergy Nuclear Operating
Company, FirstEnergy Corporation, 76
South Main Street, Akron, OH 44308.
NRC Branch Chief: Richard J. Laufer.
Criterion 2—The Proposed Change Does Not
Create the Possibility of a New or Different
Kind of Accident From Any Previously
Evaluated
The proposed performance based
requirements are an improvement over the
requirements imposed by the current
technical specifications. Implementation of
the proposed SG Program will not introduce
any adverse changes to the plant design basis
or postulated accidents resulting from
potential tube degradation. The result of the
implementation of the SG Program will be an
enhancement of SG tube performance.
Primary to secondary LEAKAGE that may be
experienced during all plant conditions will
be monitored to ensure it remains within
current accident analysis assumptions.
The proposed change does not affect the
design of the SGs, their method of operation,
or primary or secondary coolant chemistry
controls. In addition, the proposed change
does not impact any other plant system or
component. The change enhances SG
inspection requirements.
Therefore, the proposed change does not
create the possibility of a new or different
Florida Power and Light Company,
Docket No. 50–389, St. Lucie Plant, Unit
No. 2, St. Lucie County, Florida
Date of amendment request: October
21, 2005.
Description of amendment request:
The proposed amendment will revise
the Technical Specifications to allow
operation with a reduced reactor coolant
system (RCS) flow rate of 300,000 gpm
and a reduction in the maximum
thermal power to 89 percent of the rated
thermal power. The definition of rated
thermal power remains unchanged at
2700 MWt. The flow rate of 300,000
gpm is expected to conservatively
bound an analyzed steam generator tube
plugging level of 42 percent per steam
generator. The re-analysis performed to
support this reduction in RCS flow used
Westinghouse WCAP–9272–P–A
methodology, the same methodology
approved for St. Lucie Unit 2 in License
Amendment 138.
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[kind] of accident from any accident
previously evaluated.
Criterion 3—The Proposed Change Does Not
Involve a Significant Reduction in [a] Margin
of Safety
The SG tubes in pressurized water reactors
are an integral part of the reactor coolant
pressure boundary and, as such, are relied
upon to maintain the primary system’s
pressure and inventory. As part of the reactor
coolant pressure boundary, the SG tubes are
unique in that they are also relied upon as
a heat transfer surface between the primary
and secondary systems such that residual
heat can be removed from the primary
system. In addition, the SG tubes isolate the
radioactive fission products in the primary
coolant from the secondary system. In
summary, the safety function of [a] SG is
maintained by ensuring the integrity of its
tubes.
Steam generator tube integrity is a function
of the design, environment, and the physical
condition of the tube. The proposed change
does not affect tube design or operating
environment. The proposed change is
expected to result in an improvement in the
tube integrity by implementing the SG
Program to manage SG tube inspection,
assessment, repair, and plugging. The
requirements established by the SG Program
are consistent with those in the applicable
design codes and standards and are an
improvement over the requirements in the
current TSs.
For the above reasons, the margin of safety
is not changed and overall plant safety will
be enhanced by the proposed change to the
TS.
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Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
(1) Operation of the facility in accordance
with the proposed amendment would not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
None of the proposed changes to the
Technical Specifications results in operation
of the facility that adversely affects the
initiation of any accident previously
evaluated. There is no adverse impact on any
plant system. Plant systems will continue to
function as designed, and all performance
requirements for these systems remain
acceptable. The analysis, performed to
support the proposed changes, has included
evaluations and/or analyses of all the
analyzed accident analyses, including the
effects of changes on the SG tube sleeve
design. The analyses and evaluations have
verified that the accident analyses acceptance
criteria continue to be met. Dose
consequences acceptance criteria have been
verified to be met for analyzed events.
Therefore, the proposed changes do not
significantly increase the probability or
consequences of an accident previously
evaluated.
(2) Operation of the facility in accordance
with the proposed amendments would not
create the possibility of a new or different
kind of accident from any previously
evaluated.
No new accident scenarios, failure
mechanisms or limiting single failures are
introduced as a result of the proposed
changes to the Technical Specifications.
Although the allowable tube plugging level is
increased, the criteria for tube plugging/
sleeving and the tube integrity considerations
remain unchanged. The proposed changes
have no adverse effects on any safety-related
systems and do not challenge the
performance or integrity of any safety-related
system. The DNBR [Departure from Nucleate
Boiling Ratio] limits and trip setpoints
associated with the respective reactor
protection system functions have verified
that the accident analyses criteria continue to
be met. Therefore, this amendment will not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
(3) Operation of the facility in accordance
with the proposed amendments would not
involve a significant reduction in a margin of
safety.
The safety analyses of all analyzed design
basis accidents, supporting the proposed
changes to the Technical Specifications,
continue to meet the applicable acceptance
criteria with respect to the radiological
consequences, specified acceptable fuel
design limits (SAFDLs), primary and
secondary overpressurization, and 10 CFR
50.46 requirements. The DNBR and the
setpoint analyses are performed on a cyclespecific basis to verify that the reactor
protection system functions continue to
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provide adequate protection against fuel
design limits. Evaluation of the steam line
break and LOCA [Loss of Coolant Accident]
mass and energy releases determined that the
overall containment response remains
acceptable. The performance requirements
for all systems have been verified to be
acceptable from design basis accidents’
consideration. The proposed amendment,
therefore, will not involve a significant
reduction in the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 50.92(c) are satisfied.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Attorney for licensee: M.S. Ross,
Attorney, Florida Power & Light, P.O.
Box 14000, Juno Beach, Florida 33408–
0420.
NRC Branch Chief: Michael L.
Marshall, Jr.
Nuclear Management Company, LLC,
Docket No. 50–263, Monticello Nuclear
Generating Plant, Wright County,
Minnesota
Date of amendment request: July 25,
2005.
Description of amendment request:
The proposed amendment would add
new Technical Specifications
requirements to provide limiting
conditions for operation (LCOs) and
action statements and corresponding
surveillance requirements for the
Emergency Service Water (ESW) system.
In the absence of such new requirement,
the current requirement at Section
3.5.A.4 simply specifies that the unit be
shutdown within 24 hours.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The Emergency Service Water (ESW)
System is not an accident initiator. The
proposed change provides operability
requirements and surveillance requirements
to ensure the ESW System is operable as
required for accident mitigation. The
proposed operability requirements and
allowed outage time is consistent with the
requirements for the systems supported by
the ESW System. The [calculated
radiological] dose to the public and the
Control Room operators [due to a postulated
accident] are unaffected by the proposed
change. The proposed LCO provides
direction with respect to actions to be taken
when support systems are inoperable.
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75493
The proposed Technical Specifications
does not introduce new equipment operating
modes, nor does the proposed change alter
existing system relationships. The proposed
amendment does not introduce new failure
modes.
Therefore, the proposed amendment will
not significantly increase the probability or
the consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes do not introduce
new equipment operating modes, nor do they
alter existing system relationships. The
proposed changes do not introduce new
failure modes. They do not alter the
equipment required for accident mitigation
and they appropriately consider the effects
on supported systems when a support system
is inoperable. When support systems are
inoperable, actions are specified consistent
with safe plant operation.
Therefore, the proposed changes will not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in the margin of safety?
Response: No.
The proposed change provides
specifications for the ESW System that are
consistent with current Technical
Specification requirements for other
equipment. The proposed changes ensure
that the ESW and other support systems will
be available when required and provides
adequate alternative actions when the
support systems are not available. The
allowed outage times for the ESW subsystem
is consistent with that allowed for other
equipment required for accident mitigation.
Therefore, the proposed changes do not
involve a significant reduction in the margin
of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jonathan Rogoff,
Esquire, Vice President, Counsel &
Secretary, Nuclear Management
Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Branch Chief: L. Raghavan.
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1, Washington County, Nebraska
Date of amendment request: October
31, 2005.
Description of amendment request:
Omaha Public Power District (the
licensee) has proposed to revise the
Updated Safety Analysis Report (USAR)
Safety Analysis, General, Section 14.1,
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as well as the radiological consequences
analyses for the events of Seized Rotor
(SR), Section 14.6.2.8; Main Steam Line
Break (MSLB), Section 14.12.6; Control
Element Assembly Ejection (CEAE),
Section 14.13.4; and Steam Generator
Tube Rupture (SGTR), Section 14.14.3.
The USAR sections for radiological
consequences of events need to be
revised because of the planned
replacement of the steam generators and
pressurizer in the fall of 2006.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes to the USAR discuss
the changes to the Seized Rotor (SR), Control
Element Assembly Ejection (CEAE), Steam
Generator Tube Rupture (SGTR) and Main
Steam Line Break (MSLB) events resulting
from the installation of the replacement
steam generators (RSGs) and the replacement
pressurizer (RPZR). These changes do not
affect an accident initiator previously
evaluated in the USAR or the Technical
Specifications and will not prevent any
safety systems from performing their accident
mitigating function as discussed in the USAR
or the Technical Specifications.
In all events evaluated, with the exception
of the Control Room dose of the MSLB
concurrent iodine spike case, there is no
margin reduction. The Control Room dose of
the MSLB concurrent iodine spike case is
increased from 2.5 rem to 4.5 rem. The
calculated doses resulting from the proposed
changes to USAR Sections 14.1.6, 14.6.2.8,
14.12.6, 14.13.4 and 14.14.3 remain below
the regulatory limits set by 10 CFR 50.67.
Therefore, these changes do not involve a
significant increase in the probability or
consequences of any accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes are the result of
changes in the analysis of the radiological
consequences of the SR, CEAE, SGTR and
MSLB events of the replacement of the steam
generators (SGs) and the pressurizer. The
proposed changes do not modify or install
any safety related equipment. They do,
however, change the licensing basis by using
fuel gap fractions from Reference 7.6 in
accordance with previously accepted license
applications by other licensees and by
assuming shorter concurrent iodine spike
durations in accordance with Section 2.2 of
Appendix E of RG 1.183, since the activity
released during the eight-hour spike duration
exceeds the available release.
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Therefore, these changes do not create the
possibility of a new or different kind of
accident from any previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The calculated doses resulting from the
proposed changes to USAR Sections 14.1.6,
14.6.2.8, 14.12.6, 14.13.4 and 14.14.3 remain
below the regulatory limits set by 10 CFR
50.67. In all events evaluated, with the
exception of the Control Room dose of the
MSLB concurrent iodine spike case, there is
no margin reduction. The Control Room dose
of the MSLB concurrent iodine spike case is
increased from 2.5 rem to 4.5 rem. This
margin reduction is primarily due to the
significant delay in the reactor coolant
reaching 212 F with the RSGs and RPZR (i.e.,
at 159.2 hours versus the 10.94 hours
applicable to the original steam generators).
This analysis has conservatively used a spike
duration of 4 hours. If the updated analysis
took credit for the percentage of defective
fuels associated with Technical Specification
concentrations when developing the duration
of the concurrent iodine spike (i.e., used
0.28% defective fuel versus the
conservatively assumed 1% defective fuel
used in the analysis), the analysis would
have resulted in an estimated spike duration
of 2 hours instead of 4 hours and the control
room dose would be significantly reduced.
Therefore, the proposed changes do not
involve a significant reduction in the safety
margin.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: James R.
Curtiss, Esq., Winston & Strawn, 1400 L
Street, NW., Washington, DC 20005–
3502.
NRC Branch Chief: David Terao.
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1, Washington County, Nebraska
Date of amendment request:
November 8, 2005.
Description of amendment request:
The proposed amendment would revise
the Fort Calhoun Station (FCS)
Technical Specifications (TS) to add a
new Limiting Condition for Operation
2.8.3(6) and modify Table 3–4, Table 3–
5, and Design Features 4.3.1 to address
criticality control during spent fuel cask
loading operations in the spent fuel
pool. This request applies only to spent
fuel cask loading in the spent fuel pool
and does not affect the licensing basis
or invalidate our existing exemption
from the criticality monitoring
requirements of Title 10, Code of
Federal Regulations (CFR) 70.24 for new
and spent fuel storage.
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Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
These proposed changes affect only
operations in the spent fuel pool during
spent fuel cask loading operations. Plant
power operations and other spent fuel pool
operations are not affected. There are no
changes to the design or operation of the
power plant that could affect system,
component or accident functions resulting
from these changes.
Fuel loading into the spent fuel casks in
the spent fuel pool will not require any
significant changes to spent fuel pool
structures, systems, or components, nor will
their performance requirements be altered.
The potential to handle a spent fuel cask was
considered in the original design of the plant.
Therefore, the response of the plant to
previously analyzed Part 50 accidents and
related radiological releases will not be
adversely impacted, and will bound those
postulated during cask loading activities in
the cask loading area.
Accordingly, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
These proposed changes affect only
operations in the spent fuel pool during
spent fuel cask loading operations. Plant
power operations and other spent fuel pool
operations are not affected. No new accident
scenarios, failure mechanisms, or single
failures are introduced as a result of the
proposed changes. All systems, structures,
and components previously required for
mitigation of an event remain capable of
fulfilling their intended design function with
these changes to the TS.
Fuel handling procedures and associated
administrative controls for movement of
spent fuel in the spent fuel pool remain
applicable and are being appropriately
augmented to accommodate spent fuel cask
loading operations. Additionally, the soluble
boron concentration required to maintain keff
≤0.95 for postulated accidents associated
with cask loading operations was also
evaluated. The results of the analyses, using
a methodology previously approved by the
NRC, demonstrate that the amount of soluble
boron assumed to be in the pool water during
these postulated accidents (800 ppm [part per
million]) is much less than the value at
which the spent fuel pool is normally
maintained (approximately 1900 ppm).
Therefore, the possibility of a new or
different kind of accident from any accident
previously evaluated is not created.
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3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
An NRC-approved methodology was used
to perform the criticality analyses that
provide the basis to incorporate a boron
concentration and a new burnup versus
enrichment curve into the plant Technical
Specifications to ensure criticality safety
margins are maintained during spent fuel
cask loading. Spent fuel casks at FCS are
loaded in the spent fuel pool in an area
adjacent to the spent fuel racks. No physical
segregation such as a wall or gate exists
between the spent fuel racks and spent fuel
cask loading area. The cask loading area floor
is approximately two feet lower than the
floor on which the spent fuel racks are
located. Therefore, the spent fuel pool water
flows in and around the spent fuel racks and
spent fuel casks being loaded in a common
pool. Neutronic coupling between fuel in the
spent fuel racks and fuel in the spent fuel
cask has been appropriately considered in
the criticality analysis, including accident
events that postulate mis-loading of a fresh
fuel assembly into the cask and dropping a
fuel assembly between the spent fuel racks
and spent fuel cask during loading.
The normal condition criticality analysis
was performed assuming no soluble boron in
the spent fuel pool water and credit for fuel
burnup. The proposed new Technical
Specification requirement to permit only fuel
assemblies with the minimum required
burnup versus enrichment to be loaded into
the spent fuel cask preserves this analysis
basis. The accident condition criticality
analysis was performed assuming a
minimum of 800 ppm boron in the spent fuel
pool during cask loading operations. All
analyses account for uncertainties at a 95[-]
percent probability/95-percent confidence
level. The proposed new Technical
Specification requirement to maintain a
minimum boron concentration of 800 ppm in
the spent fuel pool during spent fuel cask
loading operations preserves this analysis
basis. For defense-in-depth, the spent fuel
pool boron concentration is typically
maintained at approximately 1900 ppm
during normal operations and would not be
expected to be reduced during spent fuel
cask loading operations.
Therefore, there is no significant reduction
in a margin of safety as a result of this
change.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: James R.
Curtiss, Esq., Winston & Strawn, 1400 L
Street, NW., Washington, DC 20005–
3502.
NRC Branch Chief: David Terao.
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Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of amendment requests: October
19, 2005.
Description of amendment requests:
The proposed change allows a delay
time for entering a supported system
Technical Specification (TS) when the
inoperability is due solely to an
inoperable snubber, if risk is assessed
and managed consistent with the
program in place for complying with the
requirements of 10 CFR 50.65(a)(4).
Limiting Condition for Operation (LCO)
3.0.8 is added to the TS to provide this
allowance and define the requirements
and limitations for its use.
This change was proposed by the
industry’s Technical Specification Task
Force (TSTF) and is designated TSTF–
372, Revision 4. The NRC staff issued a
notice of opportunity for comment in
the Federal Register on November 24,
2004 (69 FR 68412), on possible
amendments concerning TSTF–372,
including a model safety evaluation and
model no significant hazards
consideration (NSHC) determination,
using the consolidated line item
improvement process. The NRC staff
subsequently issued a notice of
availability of the models for referencing
in license amendment applications in
the Federal Register on May 4, 2005 (70
FR 23252). The licensee affirmed the
applicability of the following NSHC
determination in its application dated
October 19, 2005.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
Criterion 1—The Proposed Change Does Not
Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated
The proposed change allows a delay time
for entering a supported system TS when the
inoperability is due solely to an inoperable
snubber if risk is assessed and managed. The
postulated seismic event requiring snubbers
is a low-probability occurrence and the
overall TS system safety function would still
be available for the vast majority of
anticipated challenges. Therefore, the
probability of an accident previously
evaluated is not significantly increased, if at
all. The consequences of an accident while
relying on allowance provided by proposed
LCO 3.0.8 are no different than the
consequences of an accident while relying on
the TS required actions in effect without the
allowance provided by proposed LCO 3.0.8.
Therefore, the consequences of an accident
previously evaluated are not significantly
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75495
affected by this change. The addition of a
requirement to assess and manage the risk
introduced by this change will further
minimize possible concerns. Therefore, this
change does not involve a significant
increase in the probability or consequences
of an accident previously evaluated.
Criterion 2—The Proposed Change Does Not
Create the Possibility of a New or Different
Kind of Accident From Any Previously
Evaluated
The proposed change does not involve a
physical alteration of the plant (no new or
different type of equipment will be installed).
Allowing delay times for entering supported
system TS when inoperability is due solely
to inoperable snubbers, if risk is assessed and
managed, will not introduce new failure
modes or effects and will not, in the absence
of other unrelated failures, lead to an
accident whose consequences exceed the
consequences of accidents previously
evaluated. The addition of a requirement to
assess and manage the risk introduced by this
change will further minimize possible
concerns. Thus, this change does not create
the possibility of a new or different kind of
accident from an accident previously
evaluated.
Criterion 3—The Proposed Change Does Not
Involve a Significant Reduction in the Margin
of Safety
The proposed change allows a delay time
for entering a supported system TS when the
inoperability is due solely to an inoperable
snubber, if risk is assessed and managed. The
postulated seismic event requiring snubbers
is a low-probability occurrence and the
overall TS system safety function would still
be available for the vast majority of
anticipated challenges. The risk impact of the
proposed TS changes was assessed following
the three-tiered approach recommended in
Regulatory Guide 1.177. A bounding risk
assessment was performed to justify the
proposed TS changes. The proposed LCO
3.0.8 defines limitations on the use of the
provision and includes a requirement for the
licensee to assess and manage the risk
associated with operation with an inoperable
snubber. The net change to the margin of
safety is insignificant. Therefore, this change
does not involve a significant reduction in a
margin of safety.
The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorney for licensee: Richard F.
Locke, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of amendment requests: October
19, 2005.
Description of amendment requests:
The proposed amendments would
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update the Technical Specification (TS)
5.3, ‘‘Unit Staff Qualifications,’’ operator
minimum qualification requirements
contained in the March 28, 1980, NRC
letter to all licensees with the more
recent NRC-approved operator
qualification requirements contained in
American National Standards Institute/
American Nuclear Society (ANSI/ANS)
3.1–1993. In addition, the proposed
changes remove the TS 5.3.1 plant staff
retraining and replacement training
program requirements which have been
superseded by requirements contained
in section 50.120 of Title 10 of the Code
of Federal Regulations (10 CFR).
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change is an administrative
change to revise the Technical Specification
(TS) 5.3.1 licensed operator minimum
qualification requirements and remove the
plant staff retraining and replacement
training program requirements from the TS.
The proposed change does not directly
impact accidents previously evaluated. The
Diablo Canyon Power Plant (DCPP) licensed
operator training program is accredited by
the National Academy for Nuclear Training
(NANT) and is based on a systems approach
to training consistent with the requirements
of 10 CFR 55. Although licensed operator
qualifications and training may have an
indirect impact on accidents previously
evaluated, the NRC considered this impact
during the rulemaking process, and by
promulgation of the revised 10 CFR 55 rule,
concluded that this impact remains
acceptable as long as the licensed operator
training program is certified to be accredited
and is based on a systems approach to
training. The DCPP plant staff retraining and
replacement training program meets the
requirements of 10 CFR 50.120.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different accident
from any accident previously evaluated?
Response: No.
The proposed change is administrative in
nature and does not affect the plant design,
hardware, system operation, or operating
procedures. The DCPP licensed operator
training program is accredited by the NANT
and is based on a systems approach to
training consistent with the requirements of
10 CFR 55. Although licensed operator
qualifications and training may have an
indirect impact on accidents previously
evaluated, the NRC considered this impact
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during the rulemaking process, and by
promulgation of the revised 10 CFR 55 rule,
concluded that this impact remains
acceptable as long as the licensed operator
training program is certified to be accredited
and is based on a systems approach to
training. The DCPP plant staff retraining and
replacement training program meets the
requirements of 10 CFR 50.120.
Therefore, the proposed change does not
create the possibility of a new or different
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change is administrative in
nature and does not affect the plant design,
hardware, system operation, or operating
procedures. The change does not exceed or
alter a design basis or safety limit and thus
does not reduce the margin of safety.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Richard F.
Locke, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Branch Chief: David Terao.
PSEG Nuclear LLC, Docket Nos. 50–272
and 50–311, Salem Nuclear Generating
Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of amendment request: August
19, 2005.
Description of amendment request:
The amendment would relocate the
Technical Specification response time
testing tables to the Updated Final
Safety Analysis Report.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the change involve a significant
increase in the probability or consequences
of an accident previously evaluated?
Response: No.
The proposed amendment[s] relocate the
instrument response time limits for the
reactor trip system (RTS) and engineered
safety feature actuation system (ESFAS) from
the technical specifications to the Updated
Final Safety Analysis Report (UFSAR). The
proposed amendment[s] conform to the
guidance given in Enclosures 1 and 2 of
Generic Letter 93–08. Neither the response
time limits nor the surveillance requirements
for performing response time testing will be
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Fmt 4703
Sfmt 4703
altered by this submittal. The overall RTS
and ESFAS functional capabilities will not be
changed and assurance that action
requirements of the reactor trip and
engineered safety features systems are
completed within the time limits assumed in
the accident analyses is unaffected by the
proposed amendment[s].
Therefore, operation of the facility in
accordance with the proposed amendment[s]
will not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Create the possibility of a new or
different kind of accident from any accident
previously evaluated.
Response: No.
The proposed amendment[s] will not
change the physical plant or the modes of
plant operation defined in the operating
license[s]. The change does not involve the
addition or modification of equipment nor
does it alter the design or operation of plant
systems.
Therefore, operation of the facility in
accordance with the proposed amendment[s]
will not create the possibility of a new or
different kind of accident from any accident
previously evaluated.
3. Does the change involve a significant
reduction in a margin of safety?
Response: No.
The measurement of instrumentation
response times at the frequencies specified in
the technical specification provides
assurance that actions associated with the
reactor trip and engineered safety features
systems are accomplished within the time
limits assumed in the accident analyses. The
response time limits and the measurement
frequencies remain unchanged by the
proposed amendment[s].
There will be no effect on the manner in
which safety limits or limiting safety system
settings are determined nor will there be any
effect on those plant systems necessary to
assure the accomplishment of protection
functions.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jeffrie J. Keenan,
Esquire, Nuclear Business Unit—N21,
P.O. Box 236, Hancocks Bridge, NJ
08038.
NRC Branch Chief: Darrell J. Roberts.
South Carolina Electric & Gas Company,
South Carolina Public Service
Authority, Docket No. 50–395, Virgil C.
Summer Nuclear Station, Unit No. 1,
Fairfield County, South Carolina
Date of amendment request:
November 15, 2005.
Description of amendment request:
The amendment would revise the Virgil
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C. Summer Nuclear Station Technical
Specifications (TS) 3/4.3.1, ‘‘Reactor
Trip System Instrumentation,’’ and TS
3/4.3.2, ‘‘Engineered Safety Feature
Actuation System Instrumentation,’’ to
implement the allowed outage time and
bypass test time changes approved by
the Nuclear Regulatory Commission in
the Westinghouse topical report WCAP–
14333–P–A, Rev. 1, ‘‘Probabilistic Risk
Analysis of the Reactor Trip System and
Engineered Safety Features Actuation
System Test Times and Completion
Times,’’ dated October 1998.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Overall protection system performance will
remain within the bounds of the previously
performed accident analyses since no
hardware changes are proposed. The same
reactor trip system (RTS) and engineered
safety feature actuation system (ESFAS)
instrumentation will continue to be used.
The protection systems will continue to
function in a manner consistent with the
plant design basis. These changes to the
Technical Specifications do not result in a
condition where the design, material, and
construction standards that were applicable
prior to the changes are altered.
The proposed changes will not modify any
system interface. The proposed changes will
not affect the probability of any event
initiators. There will be no degradation in the
performance of, or an increase in the number
of challenges imposed on safety-related
equipment assumed to function during an
accident. There will be no changes to normal
plant operating parameters or accident
mitigation performance. The proposed
changes will not alter any assumptions or
change any mitigation actions in the
radiological consequence evaluations in the
FSAR [final safety analysis report]. The
determination that the results of the
proposed changes are acceptable was
established in the NRC SE [safety evaluation]
issued for WCAP [Westinghouse Commercial
Atomic Power report]-14333, dated July 15,
1998. Implementation of the proposed
changes will result in an insignificant risk
impact. The proposed changes to Action 16
of TS [Technical Specification] 3/4.3.2 are
also acceptable as demonstrated by meeting
the acceptance criteria contained in
Regulatory Guides 1.174 and 1.177.
The proposed changes to the AOTs
[allowable outage times] and bypass test
times, reduce the potential for inadvertent
reactor trips and spurious ESF [engineered
safety feature] actuations, and therefore do
not increase the probability of any accident
previously evaluated. The proposed changes
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Jkt 208001
do not change the response of the plant to
any accidents and have an insignificant
impact on the reliability of the RTS and
ESFAS signals. The RTS and ESFAS will
remain highly reliable and the proposed
changes will not result in a significant
increase in the risk of plant operation. This
is demonstrated by showing that the impact
on plant safety as measured by the increase
in CDF [core damage frequency] is less than
1.0E–06 per year and the increase in LERF
[large early release frequency] is less than
1.0E–07 per year. In addition, for the AOT
and bypass test time changes, the ICCDP
[incremental conditional core damage
probability] and ICLERP [incremental
conditional large early release probability]
values are less than 5.0E–07 and 5.0E–08,
respectively. The proposed changes meet the
acceptance criteria in Regulatory Guides
1.174 and 1.177. Therefore, since the RTS
and ESFAS will continue to perform their
functions with high reliability as originally
assumed, and the increase in risk as
measured by the ‘‘CDF, ‘‘LERF, ICCDP,
ICLERP risk metrics is within the acceptance
criteria of Regulatory Guides 1.174 and 1.177,
there will not be a significant increase in the
consequences of any accidents.
The proposed changes to the bypass test
times and AOTs do not adversely affect
accident initiators or precursors nor alter the
design assumptions, conditions, or
configuration of the facility or the manner in
which the plant is operated and maintained.
The proposed changes do not alter or prevent
the ability of structures, systems, and
components (SSCs) from performing their
intended function to mitigate the
consequences of an initiating event to within
the applicable acceptance criteria. The
proposed changes do not affect the source
term, containment isolation, or radiological
release assumptions used in evaluating the
radiological consequences of an accident
previously evaluated. The proposed changes
are consistent with safety analysis
assumptions and resultant consequences.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
There are no hardware changes or any
changes in the method by which any safetyrelated plant system performs its safety
function. The proposed changes will not
affect the normal method of plant operation.
No performance requirements will be
affected or eliminated. The proposed changes
will not result in a physical alteration to any
plant system or a change in the method by
which any safety-related plant system
performs its safety function. There will be no
setpoint changes or changes to accident
analysis assumptions.
No new accident scenarios, transient
precursors, failure mechanisms, or limiting
single failures are introduced as a result of
these changes. There will be no adverse effect
or challenges imposed on any safety-related
system as a result of these changes.
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Fmt 4703
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75497
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does this change involve a significant
reduction in a margin of safety?
Response: No.
The proposed changes do not affect the
acceptance criteria for any analyzed event
nor is there a change to any Safety Analysis
Limit (SAL). There will be no effect on the
manner in which safety limits, limiting safety
system settings, or limiting conditions for
operation are determined nor will there be
any effect on those plant systems necessary
to assure the accomplishment of protection
functions. There will be no impact on the
DNBR [departure from nucleate boiling ratio]
limits, FQ, FDH, LOCA [loss-of-coolant
accident] PCT [peak cladding temperature],
peak local power density, or any other
margin of safety. The radiological dose
consequence acceptance criteria continue to
be met.
Redundant RTS and ESFAS trains are
maintained, and diversity with regard to the
signals that provide reactor trip and
engineered safety features actuation is also
maintained. All signals credited as primary
or secondary, and all operator actions
credited in the accident analyses will remain
the same. The proposed changes will not
result in plant operation in a configuration
outside the design basis. The calculated
impact on risk is insignificant and meets the
acceptance criteria contained in Regulatory
Guides 1.174 and 1.177. Although there was
no attempt to quantify any positive human
factors benefit due to increased AOTs and
bypass test times, it is expected that there
would be a net benefit due to the reduced
potential for spurious reactor trips and
actuations associated with testing and
maintenance activities.
Implementation of the proposed changes is
expected to result in an overall improvement
in safety, as follows:
Improvements in the effectiveness of the
operating staff in monitoring and controlling
plant operation will be realized. This is due
to less frequent distraction of the operators
and shift supervisor to attend to RTS and
ESFAS instrumentation Actions with short
AOTs.
The increased AOTs will provide more
time for trouble shooting and repair
activities, therefore reducing the potential for
spurious trips and actuations.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
Pursuant to 10CFR50.91, the preceding
analyses provide a determination that the
proposed Technical Specification changes
pose no significant hazard as delineated by
10CFR50.92.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.929(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
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Federal Register / Vol. 70, No. 243 / Tuesday, December 20, 2005 / Notices
Attorney for licensee: Thomas G.
Eppink, South Carolina Electric & Gas
Company, Post Office Box 764,
Columbia, South Carolina 29218.
NRC Branch Chief: Evangelos C.
Marinos.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–348 and 50–364,
Joseph M. Farley Nuclear Plant, Units 1
and 2, Houston County, Alabama
Date of amendment request:
November 2, 2005.
Description of amendment request:
The proposed change allows entry into
a mode or other specified condition in
the applicability of a Technical
Specification (TS), while in a condition
statement and the associated required
actions of the TS, provided the licensee
performs a risk assessment and manages
risk consistent with the program in
place for complying with the
requirements of Title 10 of the Code of
Federal Regulations (10 CFR), Part 50,
Section 50.65(a)(4). Limiting Condition
for Operation (LCO) 3.0.4 exceptions in
individual TSs would be eliminated,
several notes or specific exceptions are
revised to reflect the related changes to
LCO 3.0.4, and Surveillance
Requirement 3.0.4 is revised to reflect
the LCO 3.0.4 allowance.
This change was proposed by the
industry’s Technical Specification Task
Force (TSTF) and is designated TSTF–
359. The NRC staff issued a notice of
opportunity for comment in the Federal
Register on August 2, 2002 (67 FR
50475), on possible amendments
concerning TSTF–359, including a
model safety evaluation and model no
significant hazards consideration
(NSHC) determination, using the
consolidated line item improvement
process. The NRC staff subsequently
issued a notice of availability of the
models for referencing in license
amendment applications in the Federal
Register on April 4, 2003 (68 FR 16579).
The licensee affirmed the applicability
of the following NSHC determination in
its application dated November 2, 2005.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
Criterion 1—The Proposed Change Does Not
Involve a Significant Increase in the
Probability or Consequences of an Accident
Previously Evaluated
The proposed change allows entry into a
mode or other specified condition in the
applicability of a TS, while in a TS condition
statement and the associated required actions
of the TS. Being in a TS condition and the
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Jkt 208001
associated required actions is not an initiator
of any accident previously evaluated.
Therefore, the probability of an accident
previously evaluated is not significantly
increased. The consequences of an accident
while relying on required actions as allowed
by proposed LCO 3.0.4, are no different than
the consequences of an accident while
entering and relying on the required actions
while starting in a condition of applicability
of the TS. Therefore, the consequences of an
accident previously evaluated are not
significantly affected by this change. The
addition of a requirement to assess and
manage the risk introduced by this change
will further minimize possible concerns.
Therefore, this change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
Criterion 2—The Proposed Change Does Not
Create the Possibility of a New or Different
Kind of Accident From Any Previously
Evaluated
The proposed change does not involve a
physical alteration of the plant (no new or
different type of equipment will be installed).
Entering into a mode or other specified
condition in the applicability of a TS, while
in a TS condition statement and the
associated required actions of the TS, will
not introduce new failure modes or effects
and will not, in the absence of other
unrelated failures, lead to an accident whose
consequences exceed the consequences of
accidents previously evaluated. The addition
of a requirement to assess and manage the
risk introduced by this change will further
minimize possible concerns. Thus, this
change does not create the possibility of a
new or different kind of accident from an
accident previously evaluated.
Criterion 3—The Proposed Change Does Not
Involve a Significant Reduction in a Margin
of Safety
The proposed change allows entry into a
mode or other specified condition in the
applicability of a TS, while in a TS condition
statement and the associated required actions
of the TS. The TS allow operation of the
plant without the full complement of
equipment through the conditions for not
meeting the TS LCO. The risk associated with
this allowance is managed by the imposition
of required actions that must be performed
within the prescribed completion times. The
net effect of being in a TS condition on the
margin of safety is not considered significant.
The proposed change does not alter the
required actions or completion times of the
TS. The proposed change allows TS
conditions to be entered, and the associated
required actions and completion times to be
used in new circumstances. This use is
predicated upon the licensee’s performance
of a risk assessment and the management of
plant risk. The change also eliminates current
allowances for utilizing required actions and
completion times in similar circumstances,
without assessing and managing risk. The net
change to the margin of safety is
insignificant. Therefore, this change does not
involve a significant reduction in a margin of
safety.
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The NRC staff proposes to determine
that the amendment request involves no
significant hazards consideration.
Attorney for licensee: M. Stanford
Blanton, Esq., Balch and Bingham, Post
Office Box 306, 1710 Sixth Avenue
North, Birmingham, Alabama 35201.
NRC Branch Chief: Evangelos C.
Marinos.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
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located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737, or by e-mail to
pdr@nrc.gov.
Calvert Cliffs Nuclear Power Plant, Inc.,
Docket Nos. 50–317 and 50–318, Calvert
Cliffs Nuclear Power Plant, Unit Nos. 1
and 2, Calvert County, Maryland
Date of application for amendments:
January 27, 2005, as supplemented on
November 2, 2005.
Brief description of amendments: The
amendments modify Technical
Specifications (TSs) requirements to
adopt the provisions of Industry/TS
Task Force (TSTF) change TSTF–359,
‘‘Increased Flexibility in Mode
Restraints.’’
Date of issuance: December 2, 2005
Effective date: As of the date of
issuance to be implemented within 60
days.
Amendment Nos.: 276 and 253
Renewed Facility Operating License
Nos. DPR–53 and DPR–69: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: May 10, 2005 (70 FR 24648)
The supplemental letter dated
November 2, 2005, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of these amendments is contained in a
Safety Evaluation dated December 2,
2005.
No significant hazards consideration
comments received: No
Duke Energy Corporation, et al., Docket
Nos. 50–413 and 50–414, Catawba
Nuclear Station, Units 1 and 2, York
County, South Carolina
Date of application for amendments:
November 16, 2004, as supplemented by
letters dated May 3, July 6, September
13, October 6, October 24 and November
15, 2005
Brief description of amendments: The
amendments revised the Technical
Specifications, on a one-time basis, to
allow the nuclear service water system
headers for each unit to be taken out of
service for up to 14 days each for system
upgrades.
Date of issuance: November 17, 2005
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of issuance
Amendment Nos.: 228/223 Renewed
Facility Operating License Nos. NPF–35
and NPF–52: Amendments revised the
Technical Specifications.
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Jkt 208001
Date of initial notice in Federal
Register: April 26, 2005 (70 FR 21454)
The supplements dated May 3, July 6,
September 13, October 6, October 24,
and November 15, 2005, provided
additional information that clarified the
application, did not expand the scope of
the November 16, 2004 application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated November 17,
2005.
No significant hazards consideration
comments received: No
Duke Energy Corporation, Docket Nos.
50–269 and 50–270, Oconee Nuclear
Station, Units 1 and 2, Oconee County,
South Carolina
Date of application of amendments:
August 18, 2005, as supplemented by
letter dated September 15, 2005
Brief description of amendments: The
amendments revised the Technical
Specifications 3.5.2.6 and 3.5.3.6 to
accommodate the replacement of the
reactor building emergency sump
suction inlet trash racks and screens
with strainers.
Date of Issuance: November 1, 2005
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 348/350
Renewed Facility Operating License
Nos. DPR–38 and DPR–47: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: August 31, 2005 (70 FR
51852)
The supplement dated September 15,
2005, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated November 1,
2005.
No significant hazards consideration
comments received: No
Entergy Gulf States, Inc., and Entergy
Operations, Inc., Docket No. 50–458,
River Bend Station, Unit 1, West
Feliciana Parish, Louisiana
Date of amendment request: March 8,
2005, as supplemented by letters dated
April 19, July 12, September 21,
November 14, and November 15, 2005
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75499
Brief description of amendment: The
amendment enables the licensee to
make changes to the Updated Safety
Analysis Report (USAR) to reflect the
use of the non-single-failure-proof Fuel
Building Cask Handling Crane for dry
spent fuel cask component lifting and
handling operations.
Date of issuance: December 1, 2005
Effective date: As of the date of
issuance, with the implementation to
begin immediately and be completed by
the next periodic update to the USAR,
in accordance with 10 CFR 50.71(e).
Amendment No.: 149
Facility Operating License No. NPF–
47: The amendment allows revision of
the USAR.
Date of initial notice in Federal
Register: April 26, 2005 (70 FR 21455).
The supplemental letters dated April 19,
July 12, September 21, November 14,
and November 15, 2005, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated December 1,
2005.
No significant hazards consideration
comments received: No
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request: May 25,
2005
Brief description of amendment: The
amendment deleted from the Cooper
Nuclear Station Technical
Specifications temporary footnotes that
have expired and are no longer in effect.
Date of issuance: December 5, 2005
Effective date: As of the date of
issuance and shall be implemented
within 30 days of issuance.
Amendment No.: 213
Facility Operating License No. DPR–
46: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: July 5, 2005 (70 FR 38721)
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated December 5,
2005.
No significant hazards consideration
comments received: No
PPL Susquehanna, LLC, Docket Nos. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2, Luzerne
County, Pennsylvania
Date of application for amendments:
January 28, 2005
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Federal Register / Vol. 70, No. 243 / Tuesday, December 20, 2005 / Notices
Brief description of amendments: The
amendments replace the reference to
American Society of Mechanical
Engineers Boiler and Pressure Vessel
Code (ASME Code) with a reference to
ASME Code for Operation and
Maintenance of Nuclear Power Plants in
Technical Specification 5.5.6.
Date of issuance: December 7, 2005
Effective date: As of the date of
issuance, and shall be implemented
within 30 days.
Amendment Nos.: 228 and 204
Facility Operating License Nos. NPF–
14 and NPF–22: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: May 24, 2005 (70 FR 29799)
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated December 7,
2005.
No significant hazards consideration
comments received: No
Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of application for amendment:
September 9, 2005, as supplemented by
letters dated October 24 and November
3, 2005
Brief description of amendment: The
amendment revises Surveillance
Requirements (SRs) 3.7.3.1 and 3.7.3.2
and adds SR 3.7.3.3 in TS 3.7.3, ‘‘Main
Feedwater Isolation Valves (MFIVs) and
Main Feedwater Regulating Valves
(MFRVs) and Main Feedwater
Regulating Valve Bypass Valves
(MFRVBVs).’’ The amendment also adds
Figure 3.7.3–1 to the TSs to specify the
acceptable MFIV stroke, or closure, time
with respect to steam generator
pressure.
Date of issuance: November 17, 2005
Effective date: Effective as of its date
of issuance, and shall be implemented
no later than entry into Mode 3 during
the startup from Refueling Outage 15,
which is scheduled for the spring of
2007. Completion of the baseline testing
of the main feedwater isolation valves,
which is described in the licensee’s
letters dated September 9 and October
24, 2005, and in Section 4.1.4 of the
Safety Evaluation for this amendment,
shall be completed as part of the
implementation of this amendment.
Amendment No.: 170
Facility Operating License No. NPF–
30: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: September 16, 2005 (70 FR
54776)The supplemental letters dated
October 24 and November 3, 2005,
provided additional information that
clarified the application, did not expand
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19:23 Dec 19, 2005
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the scope of the application as originally
noticed, and did not change the NRC
staff’s original proposed no significant
hazards consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated November 17,
2005.
No significant hazards consideration
comments received: No
Dated at Rockville, Maryland, this 12th day
of December 2005.
For the Nuclear Regulatory Commission.
Catherine Haney,
Director, Division of Operating Reactor
Licensing, Office of Nuclear Reactor
Regulation.
[FR Doc. 05–24142 Filed 12–19–05; 8:45 am]
BILLING CODE 7590–01–P
NUCLEAR REGULATORY
COMMISSION
Privacy Act of 1974, as Amended;
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Records
Nuclear Regulatory
Commission.
ACTION: Proposed revisions to an
existing system of records.
AGENCY:
SUMMARY: The Nuclear Regulatory
Commission (NRC) is issuing public
notice of its intent to modify an existing
system of records, NRC–20, ‘‘Official
Travel Records—NRC,’’ to incorporate
the collection and use of travel charge
card records, including credit data, to
comply with the Consolidated
Appropriations Act, 2005 (Pub. L. 108–
447).
DATES: The revised system of records
will become effective without further
notice on January 30, 2006 unless
comments received on or before that
date cause a contrary decision. If
changes are made based on NRC’s
review of comments received, a new
final notice will be published.
ADDRESSES: Comments may be provided
to the Chief, Rules and Directives
Branch, Division of Administrative
Services, Office of Administration, U.S.
Nuclear Regulatory Commission,
Washington, DC 20555–0001. Written
comments should also be transmitted to
the Chief of the Rules and Directives
Branch, either by means of facsimile
transmission to (301) 415–5144, or by email to nrcrep@nrc.gov.
FOR FURTHER INFORMATION CONTACT:
Sandra S. Northern, Privacy Program
Officer, FOIA/Privacy Act Team,
Records and FOIA/Privacy Services
Branch, Information and Records
Services Division, Office of Information
PO 00000
Frm 00056
Fmt 4703
Sfmt 4703
Services, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, telephone: 301–415–6879; e-mail:
ssn@nrc.gov.
SUPPLEMENTARY INFORMATION: NRC is
proposing to add new categories of
records in the system to include charge
card applications, terms and conditions
for use of charge cards, charge card
training documentation, monthly
reports regarding accounts, credit data,
and related documentation; update the
authority for the system by adding
Section 639 of the Consolidated
Appropriations Act, 2005 (Pub.L. 108–
447); and incorporate three new routine
uses which will allow disclosure of
information to the charge card issuing
bank, the Department of Interior,
National Business Center, to collect
severe travel card delinquencies by
employee salary offset, and to a
consumer reporting agency to obtain
credit reports.
A report on the proposed revisions is
being sent to OMB, the Committee on
Homeland Security and Governmental
Affairs of the U.S. Senate, and the
Committee on Government Reform of
the U.S. House of Representatives as
required by the Privacy Act and OMB
Circular No. A–130, Appendix I,
‘‘Federal Agency Responsibilities for
Maintaining Records About
Individuals.’’ NRC’s actions are also
consistent with OMB Circular A–123,
‘‘Management’s Responsibility for
Internal Control.’’
Accordingly, the NRC proposes to
amend NRC–20 to read as follows:
NRC–20
SYSTEM NAME:
Official Travel Records—NRC.
SYSTEM LOCATION:
Primary system—Division of
Financial Services, Office of the Chief
Financial Officer, NRC, Two White Flint
North, 11545 Rockville Pike, Rockville,
Maryland.
Duplicate system—Duplicate systems
may exist, in part, within the
organization where the employee
actually works for administrative
purposes, at the locations listed in
Addendum I, Parts 1 and 2, published
on September 24, 2004 (69 FR 57579).
CATEGORIES OF INDIVIDUALS COVERED BY THE
SYSTEM:
Current and former NRC employees,
prospective NRC employees,
consultants, and invitational travelers
for NRC programs.
CATEGORIES OF RECORDS IN THE SYSTEM:
These records contain requests and
authorizations for official travel, travel
E:\FR\FM\20DEN1.SGM
20DEN1
Agencies
[Federal Register Volume 70, Number 243 (Tuesday, December 20, 2005)]
[Notices]
[Pages 75489-75500]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: 05-24142]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from November 23, 2005 to December 8, 2005. The
last biweekly notice was published on December 6, 2005 (70 FR 72667).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example, in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The
filing of requests for a hearing and petitions for leave to intervene
is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a
[[Page 75490]]
notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland 20852, Attention: Rulemaking and
Adjudications Staff; (3) e-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
AmerGen Energy Company, LLC, et al., Docket No. 50-219, Oyster Creek
Nuclear Generating Station (OCNGS), Ocean County, New Jersey
Date of amendment request: October 18, 2005.
Description of amendment request: The licensee proposes to revise
the OCNGS Technical Specifications Surveillance Requirement 4.4.B.1 to
provide an alternative means for testing the electromatic relief valves
located on the main steam system. The proposed change would allow
demonstration of the capability of the valves to perform their function
without requiring that the valves be cycled with steam pressure while
installed.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration. The licensee's analysis is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change modifies Technical Specifications (TS)
Surveillance Requirement (SR) 4.4.B.1 to provide an alternative
means for testing the Electromatic Relief Valves (EMRVs). Accidents
are initiated by the malfunction of plant equipment, or the failure
of plant structures, systems, or components. The performance of EMRV
testing is not a precursor to any accident previously evaluated and
does not change the manner in which the valves are operated. The
proposed testing requirements will not contribute to the failure of
the relief valves nor any plant structure, system, or component.
AmerGen Energy Company, LLC (AmerGen) has determined that the
proposed change in testing methodology provides an equivalent level
of assurance that the relief valves are capable of performing their
intended safety functions. Thus, the proposed change does not affect
the probability of an accident previously evaluated.
The performance of EMRV testing provides confidence that the
EMRVs are capable of depressurizing the reactor pressure vessel
(RPV). This will protect the reactor vessel from overpressurization
and allow the Core Spray system to inject into the RPV as designed.
The proposed change involves the manner in which the EMRVs are
tested, and has no effect on the types or amounts of
[[Page 75491]]
radiation released or the predicted offsite doses in the event of an
accident. The proposed testing requirements are sufficient to
provide confidence that the EMRVs are capable of performing their
intended safety functions. In addition, a stuck open EMRV accident
is analyzed in the Updated Final Safety Analysis Report (section
15.6.1). Since the proposed testing requirements do not alter the
assumptions for the stuck open EMRV accident, the consequences of
any accident previously evaluated are not increased.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change does not affect the assumed accident
performance of the EMRVs, nor any plant structure, system, or
component previously evaluated. The proposed change does not involve
the installation of new equipment, and installed equipment is not
being operated in a new of different manner. The change in test
methodology ensures that the EMRVs remain capable of performing
their safety functions. No set points are being changed which would
alter the dynamic response of plant equipment. Accordingly, no new
failure modes are introduced.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change will allow testing of the EMRV actuation
electrical circuitry, including the solenoid, and mechanical
actuation components, without causing the EMRV to open. Accordingly,
in-situ EMRV cycling is avoided, reducing the potential for valve
seat leakage. The valves will be tested in accordance with the
Inservice Test (IST) Program that involves testing the valve at a
test facility using steam. The combination of the IST and proposed
actuator test provides confidence that the EMRVs will perform their
design function.
The proposed change does not affect the EMRV set points or the
operational criteria that directs the EMRVs to be manually opened
during plant transients. There are no changes proposed which alter
the set points at which protective actions are initiated, and there
is no change to the operability requirements for equipment assumed
to operate for accident mitigation.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
proposed amendment involves no significant hazards consideration.
Attorney for licensee: Thomas S. O'Neill, Associate General
Counsel, Exelon Generation Company, LCC, 4300 Winfield Road,
Warrenville, IL 60555.
NRC Branch Chief: Darrell J. Roberts.
Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric
Station, Unit 3, St. Charles Parish, Louisiana
Date of amendment request: October 27, 2005.
Description of amendment request: This amendment proposes revisions
to the Technical Specification (TS) Surveillance Requirements (SR)
4.5.2e (Safety Injection), 4.6.2.1d (Containment Spray), and 4.7.3b
(Component Cooling Water/Auxiliary Component Cooling Water), by
removing the words ``during shutdown.'' Additionally, a revision to
delete TS SR 4.7.12.1c (Essential Services Chilled Water) is requested.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
Deletion of TS SR 4.7.12.1c is an administrative change since
there are no valves in the essential services chilled water system
for which the TS SR 4.7.12.1c is applicable. The deletion of the
``during shutdown'' restriction from TS SRs 4.5.2e (Safety
Injection), 4.6.2.1d (Containment Spray), and 4.7.3b (Component
Cooling Water/Auxiliary Component Cooling Water) does not impact
system operation nor does it reduce TS SRs. Component actuations
that will be allowed to be performed online for these TS SRs are
either already actuated online for other TS SRs or the components to
be actuated online are currently stroked online in accordance with
the Inservice Testing Program. Therefore, the accident mitigation
features of the plant for previously evaluated accidents are not
affected by the proposed amendment.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
Deletion of TS SR 4.7.12.1c is an administrative change since
there are no valves in the essential services chilled water system
for which the TS SR 4.7.12.1c is applicable. The deletion of the
``during shutdown'' restriction from TS SRs 4.5.2e (Safety
Injection), 4.6.2.1d (Containment Spray), and 4.7.3b (Component
Cooling Water/Auxiliary Component Cooling Water) does not impact
system operation nor does it reduce TS SR. Component actuations that
will be allowed to be performed online for these TS SRs are either
already actuated online for other TS SRs or the components to be
actuated online are currently stroked online in accordance with the
Inservice Testing Program. Therefore, the proposed change introduces
no new mode of plant operation and no new possibility for an
accident is introduced.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
There are no automatic valves in the essential services chilled
water system that actuate on an SIAS [safety injection actuation
signal]. Deletion of the ``during shutdown'' limitation does not
change the TS test requirements or surveillance frequency.
Therefore, existing TS surveillance requirements are not reduced by
the proposed change, thus no margins of safety are reduced.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: N.S. Reynolds, Esquire, Winston & Strawn,
1700 K Street NW., Washington, DC 20006-3817
NRC Branch Chief: David Terao
FirstEnergy Nuclear Operating Company, et al., Docket Nos. 50-334 and
50-412, Beaver Valley Power Station, Unit Nos. 1 and 2 (BVPS-1 and 2),
Beaver County, Pennsylvania
Date of amendment request: November 7, 2005
Description of amendment request: The amendment would revise the
Technical Specifications (TSs), to adopt NRC-approved Revision 4 to
Technical Specification Task Force (TSTF) Standard Technical
Specification Change Traveler, TSTF-449, ``Steam Generator Tube
Integrity.'' The proposed amendment includes changes to the TS
definition of Leakage, TS 3/4.4.6, ``Reactor Coolant System Leakage,''
TS 3/4.4.5, ``Steam Generators,'' and adds TS 6.19, ``Steam Generator
(SG) Program,'' and TS 6.9.7, ``Steam Generator Tube Inspection
Report.'' The proposed changes are necessary in order to implement the
guidance for the industry initiative on Nuclear Energy Institute (NEI)
97-06, ``Steam Generator Program Guidelines.''
[[Page 75492]]
The NRC staff issued a notice of opportunity for comment in the
Federal Register on March 2, 2005 (70 FR 10298), on possible amendments
adopting TSTF-449, including a model safety evaluation and model no
significant hazards consideration (NSHC) determination, using the
consolidated line item improvement process. The NRC staff subsequently
issued a notice of availability of the models for referencing in
license amendment applications in the Federal Register on May 6, 2005
(70 FR 24126). The licensee affirmed the applicability of the following
NSHC determination in its application dated November 7, 2005.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
Criterion 1--The Proposed Change Does Not Involve a Significant
Increase in the Probability or Consequences of an Accident
Previously Evaluated
The proposed change requires a SG Program that includes
performance criteria that will provide reasonable assurance that the
SG tubing will retain integrity over the full range of operating
conditions (including startup, operation in the power range, hot
standby, cooldown and all anticipated transients included in the
design specification). The SG performance criteria are based on tube
structural integrity, accident induced leakage, and operational
LEAKAGE.
A SGTR [steam generator tube rupture] event is one of the design
basis accidents that are analyzed as part of a plant's licensing
basis. In the analysis of a SGTR event, a bounding primary to
secondary LEAKAGE rate equal to the operational LEAKAGE rate limits
in the licensing basis plus the LEAKAGE rate associated with a
double-ended rupture of a single tube is assumed.
For other design basis accidents such as a MSLB [main steamline
break], rod ejection, and reactor coolant pump locked rotor the
tubes are assumed to retain their structural integrity (i.e., they
are assumed not to rupture). These analyses typically assume that
primary to secondary LEAKAGE for all SGs is 1 gallon per minute or
increases to 1 gallon per minute as a result of accident induced
stresses. The accident induced leakage criterion introduced by the
proposed changes accounts for tubes that may leak during design
basis accidents. The accident induced leakage criterion limits this
leakage to no more than the value assumed in the accident analysis.
The SG performance criteria proposed change to the TS identify
the standards against which tube integrity is to be measured.
Meeting the performance criteria provides reasonable assurance that
the SG tubing will remain capable of fulfilling its specific safety
function of maintaining reactor coolant pressure boundary integrity
throughout each operating cycle and in the unlikely event of a
design basis accident.
The performance criteria are only a part of the SG Program
required by the proposed change to the TS. The program, defined by
NEI 97-06, Steam Generator Program Guidelines, includes a framework
that incorporates a balance of prevention, inspection, evaluation,
repair, and leakage monitoring. The proposed changes do not,
therefore, significantly increase the probability of an accident
previously evaluated.
The consequences of design basis accidents are, in part,
functions of the DOSE EQUIVALENT I-131 in the primary coolant and
the primary to secondary LEAKAGE rates resulting from an accident.
Therefore, limits are included in the plant technical specifications
for operational leakage and for DOSE EQUIVALENT I-131 in primary
coolant to ensure the plant is operated within its analyzed
condition. The typical analysis of the limiting design basis
accident assumes that primary to secondary leak rate after the
accident is 1 gallon per minute with no more than [500 gallons per
day or 720 gallons per day] in any one SG, and that the reactor
coolant activity levels of DOSE EQUIVALENT I-131 are at the TS
values before the accident.
The proposed change does not affect the design of the SGs, their
method of operation, or primary coolant chemistry controls. The
proposed approach updates the current TSs and enhances the
requirements for SG inspections. The proposed change does not
adversely impact any other previously evaluated design basis
accident and is an improvement over the current TSs.
Therefore, the proposed change does not affect the consequences
of a SGTR accident and the probability of such an accident is
reduced. In addition, the proposed changes do not affect the
consequences of an MSLB, rod ejection, or a reactor coolant pump
locked rotor event, or other previously evaluated accident.
Criterion 2--The Proposed Change Does Not Create the Possibility of
a New or Different Kind of Accident From Any Previously Evaluated
The proposed performance based requirements are an improvement
over the requirements imposed by the current technical
specifications. Implementation of the proposed SG Program will not
introduce any adverse changes to the plant design basis or
postulated accidents resulting from potential tube degradation. The
result of the implementation of the SG Program will be an
enhancement of SG tube performance. Primary to secondary LEAKAGE
that may be experienced during all plant conditions will be
monitored to ensure it remains within current accident analysis
assumptions.
The proposed change does not affect the design of the SGs, their
method of operation, or primary or secondary coolant chemistry
controls. In addition, the proposed change does not impact any other
plant system or component. The change enhances SG inspection
requirements.
Therefore, the proposed change does not create the possibility
of a new or different [kind] of accident from any accident
previously evaluated.
Criterion 3--The Proposed Change Does Not Involve a Significant
Reduction in [a] Margin of Safety
The SG tubes in pressurized water reactors are an integral part
of the reactor coolant pressure boundary and, as such, are relied
upon to maintain the primary system's pressure and inventory. As
part of the reactor coolant pressure boundary, the SG tubes are
unique in that they are also relied upon as a heat transfer surface
between the primary and secondary systems such that residual heat
can be removed from the primary system. In addition, the SG tubes
isolate the radioactive fission products in the primary coolant from
the secondary system. In summary, the safety function of [a] SG is
maintained by ensuring the integrity of its tubes.
Steam generator tube integrity is a function of the design,
environment, and the physical condition of the tube. The proposed
change does not affect tube design or operating environment. The
proposed change is expected to result in an improvement in the tube
integrity by implementing the SG Program to manage SG tube
inspection, assessment, repair, and plugging. The requirements
established by the SG Program are consistent with those in the
applicable design codes and standards and are an improvement over
the requirements in the current TSs.
For the above reasons, the margin of safety is not changed and
overall plant safety will be enhanced by the proposed change to the
TS.
The NRC staff proposes to determine that the amendments request
involves no significant hazards consideration.
Attorney for licensee: Mary O'Reilly, FirstEnergy Nuclear Operating
Company, FirstEnergy Corporation, 76 South Main Street, Akron, OH
44308.
NRC Branch Chief: Richard J. Laufer.
Florida Power and Light Company, Docket No. 50-389, St. Lucie Plant,
Unit No. 2, St. Lucie County, Florida
Date of amendment request: October 21, 2005.
Description of amendment request: The proposed amendment will
revise the Technical Specifications to allow operation with a reduced
reactor coolant system (RCS) flow rate of 300,000 gpm and a reduction
in the maximum thermal power to 89 percent of the rated thermal power.
The definition of rated thermal power remains unchanged at 2700 MWt.
The flow rate of 300,000 gpm is expected to conservatively bound an
analyzed steam generator tube plugging level of 42 percent per steam
generator. The re-analysis performed to support this reduction in RCS
flow used Westinghouse WCAP-9272-P-A methodology, the same methodology
approved for St. Lucie Unit 2 in License Amendment 138.
[[Page 75493]]
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
(1) Operation of the facility in accordance with the proposed
amendment would not involve a significant increase in the
probability or consequences of an accident previously evaluated.
None of the proposed changes to the Technical Specifications
results in operation of the facility that adversely affects the
initiation of any accident previously evaluated. There is no adverse
impact on any plant system. Plant systems will continue to function
as designed, and all performance requirements for these systems
remain acceptable. The analysis, performed to support the proposed
changes, has included evaluations and/or analyses of all the
analyzed accident analyses, including the effects of changes on the
SG tube sleeve design. The analyses and evaluations have verified
that the accident analyses acceptance criteria continue to be met.
Dose consequences acceptance criteria have been verified to be met
for analyzed events. Therefore, the proposed changes do not
significantly increase the probability or consequences of an
accident previously evaluated.
(2) Operation of the facility in accordance with the proposed
amendments would not create the possibility of a new or different
kind of accident from any previously evaluated.
No new accident scenarios, failure mechanisms or limiting single
failures are introduced as a result of the proposed changes to the
Technical Specifications. Although the allowable tube plugging level
is increased, the criteria for tube plugging/sleeving and the tube
integrity considerations remain unchanged. The proposed changes have
no adverse effects on any safety-related systems and do not
challenge the performance or integrity of any safety-related system.
The DNBR [Departure from Nucleate Boiling Ratio] limits and trip
setpoints associated with the respective reactor protection system
functions have verified that the accident analyses criteria continue
to be met. Therefore, this amendment will not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
(3) Operation of the facility in accordance with the proposed
amendments would not involve a significant reduction in a margin of
safety.
The safety analyses of all analyzed design basis accidents,
supporting the proposed changes to the Technical Specifications,
continue to meet the applicable acceptance criteria with respect to
the radiological consequences, specified acceptable fuel design
limits (SAFDLs), primary and secondary overpressurization, and 10
CFR 50.46 requirements. The DNBR and the setpoint analyses are
performed on a cycle-specific basis to verify that the reactor
protection system functions continue to provide adequate protection
against fuel design limits. Evaluation of the steam line break and
LOCA [Loss of Coolant Accident] mass and energy releases determined
that the overall containment response remains acceptable. The
performance requirements for all systems have been verified to be
acceptable from design basis accidents' consideration. The proposed
amendment, therefore, will not involve a significant reduction in
the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: M.S. Ross, Attorney, Florida Power & Light,
P.O. Box 14000, Juno Beach, Florida 33408-0420.
NRC Branch Chief: Michael L. Marshall, Jr.
Nuclear Management Company, LLC, Docket No. 50-263, Monticello Nuclear
Generating Plant, Wright County, Minnesota
Date of amendment request: July 25, 2005.
Description of amendment request: The proposed amendment would add
new Technical Specifications requirements to provide limiting
conditions for operation (LCOs) and action statements and corresponding
surveillance requirements for the Emergency Service Water (ESW) system.
In the absence of such new requirement, the current requirement at
Section 3.5.A.4 simply specifies that the unit be shutdown within 24
hours.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The Emergency Service Water (ESW) System is not an accident
initiator. The proposed change provides operability requirements and
surveillance requirements to ensure the ESW System is operable as
required for accident mitigation. The proposed operability
requirements and allowed outage time is consistent with the
requirements for the systems supported by the ESW System. The
[calculated radiological] dose to the public and the Control Room
operators [due to a postulated accident] are unaffected by the
proposed change. The proposed LCO provides direction with respect to
actions to be taken when support systems are inoperable.
The proposed Technical Specifications does not introduce new
equipment operating modes, nor does the proposed change alter
existing system relationships. The proposed amendment does not
introduce new failure modes.
Therefore, the proposed amendment will not significantly
increase the probability or the consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes do not introduce new equipment operating
modes, nor do they alter existing system relationships. The proposed
changes do not introduce new failure modes. They do not alter the
equipment required for accident mitigation and they appropriately
consider the effects on supported systems when a support system is
inoperable. When support systems are inoperable, actions are
specified consistent with safe plant operation.
Therefore, the proposed changes will not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in
the margin of safety?
Response: No.
The proposed change provides specifications for the ESW System
that are consistent with current Technical Specification
requirements for other equipment. The proposed changes ensure that
the ESW and other support systems will be available when required
and provides adequate alternative actions when the support systems
are not available. The allowed outage times for the ESW subsystem is
consistent with that allowed for other equipment required for
accident mitigation. Therefore, the proposed changes do not involve
a significant reduction in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Jonathan Rogoff, Esquire, Vice President,
Counsel & Secretary, Nuclear Management Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Branch Chief: L. Raghavan.
Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station,
Unit No. 1, Washington County, Nebraska
Date of amendment request: October 31, 2005.
Description of amendment request: Omaha Public Power District (the
licensee) has proposed to revise the Updated Safety Analysis Report
(USAR) Safety Analysis, General, Section 14.1,
[[Page 75494]]
as well as the radiological consequences analyses for the events of
Seized Rotor (SR), Section 14.6.2.8; Main Steam Line Break (MSLB),
Section 14.12.6; Control Element Assembly Ejection (CEAE), Section
14.13.4; and Steam Generator Tube Rupture (SGTR), Section 14.14.3. The
USAR sections for radiological consequences of events need to be
revised because of the planned replacement of the steam generators and
pressurizer in the fall of 2006.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes to the USAR discuss the changes to the
Seized Rotor (SR), Control Element Assembly Ejection (CEAE), Steam
Generator Tube Rupture (SGTR) and Main Steam Line Break (MSLB)
events resulting from the installation of the replacement steam
generators (RSGs) and the replacement pressurizer (RPZR). These
changes do not affect an accident initiator previously evaluated in
the USAR or the Technical Specifications and will not prevent any
safety systems from performing their accident mitigating function as
discussed in the USAR or the Technical Specifications.
In all events evaluated, with the exception of the Control Room
dose of the MSLB concurrent iodine spike case, there is no margin
reduction. The Control Room dose of the MSLB concurrent iodine spike
case is increased from 2.5 rem to 4.5 rem. The calculated doses
resulting from the proposed changes to USAR Sections 14.1.6,
14.6.2.8, 14.12.6, 14.13.4 and 14.14.3 remain below the regulatory
limits set by 10 CFR 50.67.
Therefore, these changes do not involve a significant increase
in the probability or consequences of any accident previously
evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes are the result of changes in the analysis
of the radiological consequences of the SR, CEAE, SGTR and MSLB
events of the replacement of the steam generators (SGs) and the
pressurizer. The proposed changes do not modify or install any
safety related equipment. They do, however, change the licensing
basis by using fuel gap fractions from Reference 7.6 in accordance
with previously accepted license applications by other licensees and
by assuming shorter concurrent iodine spike durations in accordance
with Section 2.2 of Appendix E of RG 1.183, since the activity
released during the eight-hour spike duration exceeds the available
release.
Therefore, these changes do not create the possibility of a new
or different kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The calculated doses resulting from the proposed changes to USAR
Sections 14.1.6, 14.6.2.8, 14.12.6, 14.13.4 and 14.14.3 remain below
the regulatory limits set by 10 CFR 50.67. In all events evaluated,
with the exception of the Control Room dose of the MSLB concurrent
iodine spike case, there is no margin reduction. The Control Room
dose of the MSLB concurrent iodine spike case is increased from 2.5
rem to 4.5 rem. This margin reduction is primarily due to the
significant delay in the reactor coolant reaching 212 F with the
RSGs and RPZR (i.e., at 159.2 hours versus the 10.94 hours
applicable to the original steam generators). This analysis has
conservatively used a spike duration of 4 hours. If the updated
analysis took credit for the percentage of defective fuels
associated with Technical Specification concentrations when
developing the duration of the concurrent iodine spike (i.e., used
0.28% defective fuel versus the conservatively assumed 1% defective
fuel used in the analysis), the analysis would have resulted in an
estimated spike duration of 2 hours instead of 4 hours and the
control room dose would be significantly reduced.
Therefore, the proposed changes do not involve a significant
reduction in the safety margin.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: James R. Curtiss, Esq., Winston & Strawn,
1400 L Street, NW., Washington, DC 20005-3502.
NRC Branch Chief: David Terao.
Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station,
Unit No. 1, Washington County, Nebraska
Date of amendment request: November 8, 2005.
Description of amendment request: The proposed amendment would
revise the Fort Calhoun Station (FCS) Technical Specifications (TS) to
add a new Limiting Condition for Operation 2.8.3(6) and modify Table 3-
4, Table 3-5, and Design Features 4.3.1 to address criticality control
during spent fuel cask loading operations in the spent fuel pool. This
request applies only to spent fuel cask loading in the spent fuel pool
and does not affect the licensing basis or invalidate our existing
exemption from the criticality monitoring requirements of Title 10,
Code of Federal Regulations (CFR) 70.24 for new and spent fuel storage.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
These proposed changes affect only operations in the spent fuel
pool during spent fuel cask loading operations. Plant power
operations and other spent fuel pool operations are not affected.
There are no changes to the design or operation of the power plant
that could affect system, component or accident functions resulting
from these changes.
Fuel loading into the spent fuel casks in the spent fuel pool
will not require any significant changes to spent fuel pool
structures, systems, or components, nor will their performance
requirements be altered. The potential to handle a spent fuel cask
was considered in the original design of the plant. Therefore, the
response of the plant to previously analyzed Part 50 accidents and
related radiological releases will not be adversely impacted, and
will bound those postulated during cask loading activities in the
cask loading area.
Accordingly, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
These proposed changes affect only operations in the spent fuel
pool during spent fuel cask loading operations. Plant power
operations and other spent fuel pool operations are not affected. No
new accident scenarios, failure mechanisms, or single failures are
introduced as a result of the proposed changes. All systems,
structures, and components previously required for mitigation of an
event remain capable of fulfilling their intended design function
with these changes to the TS.
Fuel handling procedures and associated administrative controls
for movement of spent fuel in the spent fuel pool remain applicable
and are being appropriately augmented to accommodate spent fuel cask
loading operations. Additionally, the soluble boron concentration
required to maintain keff <=0.95 for postulated accidents
associated with cask loading operations was also evaluated. The
results of the analyses, using a methodology previously approved by
the NRC, demonstrate that the amount of soluble boron assumed to be
in the pool water during these postulated accidents (800 ppm [part
per million]) is much less than the value at which the spent fuel
pool is normally maintained (approximately 1900 ppm).
Therefore, the possibility of a new or different kind of
accident from any accident previously evaluated is not created.
[[Page 75495]]
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
An NRC-approved methodology was used to perform the criticality
analyses that provide the basis to incorporate a boron concentration
and a new burnup versus enrichment curve into the plant Technical
Specifications to ensure criticality safety margins are maintained
during spent fuel cask loading. Spent fuel casks at FCS are loaded
in the spent fuel pool in an area adjacent to the spent fuel racks.
No physical segregation such as a wall or gate exists between the
spent fuel racks and spent fuel cask loading area. The cask loading
area floor is approximately two feet lower than the floor on which
the spent fuel racks are located. Therefore, the spent fuel pool
water flows in and around the spent fuel racks and spent fuel casks
being loaded in a common pool. Neutronic coupling between fuel in
the spent fuel racks and fuel in the spent fuel cask has been
appropriately considered in the criticality analysis, including
accident events that postulate mis-loading of a fresh fuel assembly
into the cask and dropping a fuel assembly between the spent fuel
racks and spent fuel cask during loading.
The normal condition criticality analysis was performed assuming
no soluble boron in the spent fuel pool water and credit for fuel
burnup. The proposed new Technical Specification requirement to
permit only fuel assemblies with the minimum required burnup versus
enrichment to be loaded into the spent fuel cask preserves this
analysis basis. The accident condition criticality analysis was
performed assuming a minimum of 800 ppm boron in the spent fuel pool
during cask loading operations. All analyses account for
uncertainties at a 95[-] percent probability/95-percent confidence
level. The proposed new Technical Specification requirement to
maintain a minimum boron concentration of 800 ppm in the spent fuel
pool during spent fuel cask loading operations preserves this
analysis basis. For defense-in-depth, the spent fuel pool boron
concentration is typically maintained at approximately 1900 ppm
during normal operations and would not be expected to be reduced
during spent fuel cask loading operations.
Therefore, there is no significant reduction in a margin of
safety as a result of this change.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: James R. Curtiss, Esq., Winston & Strawn,
1400 L Street, NW., Washington, DC 20005-3502.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo
Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County,
California
Date of amendment requests: October 19, 2005.
Description of amendment requests: The proposed change allows a
delay time for entering a supported system Technical Specification (TS)
when the inoperability is due solely to an inoperable snubber, if risk
is assessed and managed consistent with the program in place for
complying with the requirements of 10 CFR 50.65(a)(4). Limiting
Condition for Operation (LCO) 3.0.8 is added to the TS to provide this
allowance and define the requirements and limitations for its use.
This change was proposed by the industry's Technical Specification
Task Force (TSTF) and is designated TSTF-372, Revision 4. The NRC staff
issued a notice of opportunity for comment in the Federal Register on
November 24, 2004 (69 FR 68412), on possible amendments concerning
TSTF-372, including a model safety evaluation and model no significant
hazards consideration (NSHC) determination, using the consolidated line
item improvement process. The NRC staff subsequently issued a notice of
availability of the models for referencing in license amendment
applications in the Federal Register on May 4, 2005 (70 FR 23252). The
licensee affirmed the applicability of the following NSHC determination
in its application dated October 19, 2005.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
Criterion 1--The Proposed Change Does Not Involve a Significant
Increase in the Probability or Consequences of an Accident
Previously Evaluated
The proposed change allows a delay time for entering a supported
system TS when the inoperability is due solely to an inoperable
snubber if risk is assessed and managed. The postulated seismic
event requiring snubbers is a low-probability occurrence and the
overall TS system safety function would still be available for the
vast majority of anticipated challenges. Therefore, the probability
of an accident previously evaluated is not significantly increased,
if at all. The consequences of an accident while relying on
allowance provided by proposed LCO 3.0.8 are no different than the
consequences of an accident while relying on the TS required actions
in effect without the allowance provided by proposed LCO 3.0.8.
Therefore, the consequences of an accident previously evaluated are
not significantly affected by this change. The addition of a
requirement to assess and manage the risk introduced by this change
will further minimize possible concerns. Therefore, this change does
not involve a significant increase in the probability or
consequences of an accident previously evaluated.
Criterion 2--The Proposed Change Does Not Create the Possibility of
a New or Different Kind of Accident From Any Previously Evaluated
The proposed change does not involve a physical alteration of
the plant (no new or different type of equipment will be installed).
Allowing delay times for entering supported system TS when
inoperability is due solely to inoperable snubbers, if risk is
assessed and managed, will not introduce new failure modes or
effects and will not, in the absence of other unrelated failures,
lead to an accident whose consequences exceed the consequences of
accidents previously evaluated. The addition of a requirement to
assess and manage the risk introduced by this change will further
minimize possible concerns. Thus, this change does not create the
possibility of a new or different kind of accident from an accident
previously evaluated.
Criterion 3--The Proposed Change Does Not Involve a Significant
Reduction in the Margin of Safety
The proposed change allows a delay time for entering a supported
system TS when the inoperability is due solely to an inoperable
snubber, if risk is assessed and managed. The postulated seismic
event requiring snubbers is a low-probability occurrence and the
overall TS system safety function would still be available for the
vast majority of anticipated challenges. The risk impact of the
proposed TS changes was assessed following the three-tiered approach
recommended in Regulatory Guide 1.177. A bounding risk assessment
was performed to justify the proposed TS changes. The proposed LCO
3.0.8 defines limitations on the use of the provision and includes a
requirement for the licensee to assess and manage the risk
associated with operation with an inoperable snubber. The net change
to the margin of safety is insignificant. Therefore, this change
does not involve a significant reduction in a margin of safety.
The NRC staff proposes to determine that the amendment request
involves no significant hazards consideration.
Attorney for licensee: Richard F. Locke, Esq., Pacific Gas and
Electric Company, P.O. Box 7442, San Francisco, California 94120.
NRC Branch Chief: David Terao.
Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo
Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County,
California
Date of amendment requests: October 19, 2005.
Description of amendment requests: The proposed amendments would
[[Page 75496]]
update the Technical Specification (TS) 5.3, ``Unit Staff
Qualifications,'' operator minimum qualification requirements contained
in the March 28, 1980, NRC letter to all licensees with the more recent
NRC-approved operator qualification requirements contained in American
National Standards Institute/American Nuclear Society (ANSI/ANS) 3.1-
1993. In addition, the proposed changes remove the TS 5.3.1 plant staff
retraining and replacement training program requirements which have
been superseded by requirements contained in section 50.120 of Title 10
of the Code of Federal Regulations (10 CFR).
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change is an administrative change to revise the
Technical Specification (TS) 5.3.1 licensed operator minimum
qualification requirements and remove the plant staff retraining and
replacement training program requirements from the TS. The proposed
change does not directly impact accidents previously evaluated. The
Diablo Canyon Power Plant (DCPP) licensed operator training program
is accredited by the National Academy for Nuclear Training (NANT)
and is based on a systems approach to training consistent with the
requirements of 10 CFR 55. Although licensed operator qualifications
and training may have an indirect impact on accidents previously
evaluated, the NRC considered this impact during the rulemaking
process, and by promulgation of the revised 10 CFR 55 rule,
concluded that this impact remains acceptable as long as the
licensed operator training program is certified to be accredited and
is based on a systems approach to training. The DCPP plant staff
retraining and replacement training program meets the requirements
of 10 CFR 50.120.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different accident from any accident previously evaluated?
Response: No.
The proposed change is administrative in nature and does not
affect the plant design, hardware, system operation, or operating
procedures. The DCPP licensed operator training program is
accredited by the NANT and is based on a systems approach to
training consistent with the requirements of 10 CFR 55. Although
licensed operator qualifications and training may have an indirect
impact on accidents previously evaluated, the NRC considered this
impact during the rulemaking process, and by promulgation of the
revised 10 CFR 55 rule, concluded that this impact remains
acceptable as long as the licensed operator training program is
certified to be accredited and is based on a systems approach to
training. The DCPP plant staff retraining and replacement training
program meets the requirements of 10 CFR 50.120.
Therefore, the proposed change does not create the possibility
of a new or different accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change is administrative in nature and does not
affect the plant design, hardware, system operation, or operating
procedures. The change does not exceed or alter a design basis or
safety limit and thus does not reduce the margin of safety.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Attorney for licensee: Richard F. Locke, Esq., Pacific Gas and
Electric Company, P.O. Box 7442, San Francisco, California 94120.
NRC Branch Chief: David Terao.
PSEG Nuclear LLC, Docket Nos. 50-272 and 50-311, Salem Nuclear
Generating Station, Unit Nos. 1 and 2, Salem County, New Jersey
Date of amendment request: August 19, 2005.
Description of amendment request: The amendment would relocate the
Technical Specification response time testing tables to the Updated
Final Safety Analysis Report.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
The proposed amendment[s] relocate the instrument response time
limits for the reactor trip system (RTS) and engineered safety
feature actuation system (ESFAS) from the technical specifications
to the Updated Final Safety Analysis Report (UFSAR). The proposed
amendment[s] conform to the guidance given in Enclosures 1 and 2 of
Generic Letter 93-08. Neither the response time limits nor the
surveillance requirements for performing response time testing will
be altered by this submittal. The overall RTS and ESFAS functional
capabilities will not be changed and assurance that action
requirements of the reactor trip and engineered safety features
systems are completed within the time limits assumed in the accident
analyses is unaffected by the proposed amendment[s].
Therefore, operation of the facility in accordance with the
proposed amendment[s] will not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. Create the possibility of a new or different kind of accident
from any accident previously evaluated.
Response: No.
The proposed amendment[s] will not change the physical plant or
the modes of plant operation defined in the operating license[s].
The change does not involve the addition or modification of
equipment nor does it alter the design or operation of plant
systems.
Therefore, operation of the facility in accordance with the
proposed amendment[s] will not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3. Does the change involve a significant reduction in a margin
of safety?
Response: No.
The measurement of instrumentation response times at the
frequencies specified in the technical specification provides
assurance that actions associated with the reactor trip and
engineered safety features systems are accomplished within the time
limits assumed in the accident analyses. The response time limits
and the measurement frequencies remain unchanged by the proposed
amendment[s].
There will be no effect on the manner in which safety limits or
limiting safety system settings are determined nor will there be any
effect on those plant systems necessary to assure the accomplishment
of protection functions.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Jeffrie J. Keenan, Esquire, Nuclear Business
Unit--N21, P.O. Box 236, Hancocks Bridge, NJ 08038.
NRC Branch Chief: Darrell J. Roberts.
South Carolina Electric & Gas Company, South Carolina Public Service
Authority, Docket No. 50-395, Virgil C. Summer Nuclear Station, Unit
No. 1, Fairfield County, South Carolina
Date of amendment request: November 15, 2005.
Description of amendment request: The amendment would revise the
Virgil
[[Page 75497]]
C. Summer Nuclear Station Technical Specifications (TS) 3/4.3.1,
``Reactor Trip System Instrumentation,'' and TS 3/4.3.2, ``Engineered
Safety Feature Actuation System Instrumentation,'' to implement the
allowed outage time and bypass test time changes approved by the
Nuclear Regulatory Commission in the Westinghouse topical report WCAP-
14333-P-A, Rev. 1, ``Probabilistic Risk Analysis of the Reactor Trip
System and Engineered Safety Features Actuation System Test Times and
Completion Times,'' dated October 1998.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
Overall protection system performance will remain within the
bounds of the previously performed accident analyses since no
hardware changes are proposed. The same reactor trip system (RTS)
and engineered safety feature actuation system (ESFAS)
instrumentation will continue to be used. The protection systems
will continue to function in a manner consistent with the plant
design basis. These changes to the Technical Specifications do not
result in a condition where the design, material, and construction
standards that were applicable prior to the changes are altered.
The proposed changes will not modify any system interface. The
proposed changes will not affect the probability of any event