Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 67744-67757 [05-22002]
Download as PDF
67744
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
Environment Assessment (Closed—
Ex. 1)
* The schedule for Commission
meetings is subject to change on short
notice. To verify the status of meetings
call (recording)—(301) 415–1292.
Contact person for more information:
Michelle Schroll, (301) 415–1662.
*
*
*
*
*
The NRC Commission Meeting
Schedule Can Be Found on the Internet
At: https://www.nrc.gov/what-we-do/
policy-making/schedule.html.
*
*
*
*
*
The NRC provides reasonable
accommodation to individuals with
disabilities where appropriate. If you
need a reasonable accommodation to
participate in these public meetings, or
need this meeting notice or the
transcript or other information from the
public meetings in another format (e.g.
braille, large print), please notify the
NRC’s Disability Program Coordinator,
August Spector, at 301–415–7080, TDD:
301–415–2100, or by e-mail at
aks@nrc.gov. Determinations on
requests for reasonable accommodation
will be made on a case-by-case basis.
*
*
*
*
*
This notice is distributed by mail to
several hundred subscribers; if you no
longer wish to receive it, or would like
to be added to the distribution, please
contact the Office of the Secretary,
Washington, DC 20555 (301–415–1969).
In addition, distribution of this meeting
notice over the Internet system is
available. If you are interested in
receiving this Commission meeting
schedule electronically, please send an
electronic message to dkw@nrc.gov.
Dated: November 3, 2005.
R. Michelle Schroll,
Office of the Secretary.
[FR Doc. 05–22316 Filed 11–4–05; 11:02 am]
BILLING CODE 7590–01–M
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from October 14,
2005 to October 27, 2005. The last
biweekly notice was published on
October 25, 2005 (70 FR 61655).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
PO 00000
Frm 00087
Fmt 4703
Sfmt 4703
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
E:\FR\FM\08NON1.SGM
08NON1
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
PO 00000
Frm 00088
Fmt 4703
Sfmt 4703
67745
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
Carolina Power & Light Company, et al.,
Docket No. 50–400, Shearon Harris
Nuclear Power Plant, Unit 1 (HNP),
Wake and Chatham Counties, North
Carolina
Date of amendment request: August
18, 2005.
Description of amendment request:
The amendment will allow the use of
fire-resistive electrical cable, which has
been demonstrated to provide an
equivalent level of protection as would
be provided by 3-hour and 1-hour rated
electrical cable raceway fire barriers, for
the protection of safe shutdown
electrical cable.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Operation of HNP in accordance with the
proposed amendment does not increase the
probability or consequences of accidents
previously evaluated. The Final Safety
Analysis Report (FSAR) documents the
analyses of design basis accidents (DBA) at
HNP. Any scenario or previously analyzed
accidents that result in offsite dose were
evaluated as part of this analysis. The
proposed amendment does not adversely
affect accident initiators nor alter design
assumptions, conditions, or configurations of
the facility. The proposed amendment does
not adversely affect the ability of structures,
systems, or components (SSCs) to perform
their design function. SSCs required to safely
shut down the reactor and to maintain it in
a safe shutdown condition remain capable of
performing their design functions.
The purpose of this amendment is to
assure that redundant trains of safe shutdown
(SSD) control circuits remain protected from
damage in the event of a postulated fire. The
proposed amendment revises the Final Safety
Analysis Report (FSAR) to use three-hour
fire-resistive electrical cable, which has been
demonstrated to provide an equivalent level
of protection as would be provided by threehour and one-hour rated electrical cable
raceway fire barriers, for the protection of
E:\FR\FM\08NON1.SGM
08NON1
67746
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
SSD electrical cables. Based on the above,
SSD control circuit protection is maintained
by this amendment.
Therefore, this amendment does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
Operation of HNP in accordance with the
proposed amendment does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated. The FSAR documents the analyses
of design basis accidents (DBA) at HNP. Any
scenario or previously analyzed accidents
that result in offsite dose were evaluated as
part of this analysis. The proposed
amendment does not change or affect any
accident previously evaluated in the FSAR,
and no new or different scenarios are created
by the proposed amendment. The proposed
amendment does not adversely affect
accident initiators nor alter design
assumptions, conditions, or configurations of
the facility. The proposed amendment does
not adversely affect the ability of SSCs to
perform their design function. SSCs required
to safely shut down the reactor and to
maintain it in a safe shutdown condition
remain capable of performing their design
functions.
The purpose of this amendment is to
assure that redundant trains of Safe
Shutdown (SSD) control circuits remain
protected from damage in the event of a
postulated fire. The proposed amendment
revises the Final Safety Analysis Report
(FSAR) to use three-hour fire-resistive
electrical cable, which has been
demonstrated to provide an equivalent level
of protection as would be provided by threehour and one-hour rated electrical cable
raceway fire barriers, for the protection of
SSD electrical cables. Based on the above,
SSD control circuit protection is maintained
by this amendment.
Therefore, this amendment does not create
the possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
Operation of HNP in accordance with the
proposed amendment does not involve a
significant reduction in a margin of safety.
The proposed amendment does not alter the
manner in which safety limits, limiting safety
system settings or limiting conditions for
operation are determined. The safety analysis
acceptance criteria are not affected by this
change. The proposed amendment does not
adversely affect existing plant safety margins
or the reliability of equipment assumed to
mitigate accidents in the FSAR. The
proposed amendment does not adversely
affect the ability of SSCs to perform their
design function. SSCs required to safely shut
down the reactor and to maintain it in a safe
shutdown condition remain capable of
performing their design functions.
The purpose of this amendment is to
assure that redundant trains of Safe
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
Shutdown (SSD) control circuits remain
protected from damage in the event of a
postulated fire. The proposed amendment
revises the Final Safety Analysis Report
(FSAR) to use three-hour fire-resistive
electrical cable, which has been
demonstrated to provide an equivalent level
of protection as would be provided by threehour and one-hour rated electrical cable
raceway fire barriers, for the protection of
SSD electrical cables. Based on the above,
SSD control circuit protection is maintained
by this amendment.
Therefore, this amendment does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Section Chief: Michael L.
Marshall, Jr.
Carolina Power & Light Company, et al.,
Docket No. 50–400, Shearon Harris
Nuclear Power Plant, Unit 1, Wake and
Chatham Counties, North Carolina
Date of amendment request:
September 1, 2005.
Description of amendment request:
The amendment will add Technical
Specification (TS) 3.7.14, ‘‘Fuel Storage
Pool Boron Concentration’’ and revise
TS 5.6, ‘‘Fuel Storage.’’ The proposed
changes are related to requirements for
ensuring adequate subcriticality margin
in the spent fuel storage pools. TS 5.6.1
is being revised to include the design
requirements for dry storage of new fuel.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes do not modify the
facility. The accident previously analyzed for
the spent fuel pool is a fuel handling
accident. The proposed change applies
administrative controls for maintaining the
required boron concentration in the spent
fuel storage pools, revises acceptance criteria
and storage arrangements for fuel storage in
PWR [pressurized-water reactor] ‘‘flux trap’’
style racks and adds acceptance criteria for
dry storage of new fuel to the Technical
PO 00000
Frm 00089
Fmt 4703
Sfmt 4703
Specifications. The controls on spent fuel
pool boron and dry storage of new fuel have
previously been implemented but are being
added to the Technical Specifications as
requirements. The proposed change applies
new acceptance criteria for criticality safety
of fuel storage in PWR ‘‘flux trap’’ style racks
in Pools ‘‘A’’ and ‘‘B.’’ The new acceptance
criteria require new administrative controls
on the placement of fuel in Pools ‘‘A’’ and
‘‘B.’’ Similar administrative controls have
previously been placed on fuel stored in
Pools C and D. These changes will eliminate
the dependence on Boraflex in the PWR ‘‘flux
trap’’ style storage racks. These changes do
not impact the probability of having a fuel
handling accident and do not impact the
consequences of a fuel handling accident.
Therefore, this amendment does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
No change is being made to the acceptance
criteria of the dry storage of new fuel. These
criteria are being added to Technical
Specification Section 5.6.1. Detailed analyses
have been performed to ensure a criticality
accident in Pools ‘‘A’’ and ‘‘B’’ is not a
credible event. The events that could lead to
a criticality accident are not new. These
events include a fuel mis-positioning event,
a fuel drop event, and a boron dilution event.
The proposed changes do not impact the
probability of any of these events. The
detailed criticality analyses performed
demonstrate that criticality would not occur
following any of these events. For the more
likely event, such as a fuel mis-positioning
event, the acceptance criteria for keff remains
less than or equal to 0.95. For the unlikely
event that the spent fuel storage pool boron
concentration was reduced to zero, keff
remains less than 1.0.
Therefore, a criticality accident remains
‘‘not credible,’’ and this amendment does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
Incorporation of acceptance criteria for dry
storage of new fuel into TS 5.6.1 does not
involve a reduction in the margin of safety.
The new fuel storage condition continues to
meet keff ≤ 0.95 during normal conditions and
keff ≤ 0.98 under optimal moderation
conditions.
The proposed changes for storage of new
and irradiated fuel in Pools ‘‘A’’ and ‘‘B’’
continue to provide the controls necessary to
ensure a criticality event could not occur in
the spent fuel storage spool. The acceptance
criteria are consistent with the acceptance
criteria specified in 10 CFR 50.68, which
provide an acceptable margin of safety with
regard to the potential for a criticality event.
Therefore, this amendment does not
involve a significant reduction in a margin of
safety.
E:\FR\FM\08NON1.SGM
08NON1
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Section Chief: Michael L.
Marshall, Jr.
Entergy Nuclear Operations, Inc.,
Docket No. 50–247, Indian Point
Nuclear Generating Unit No. 2,
Westchester County, New York
Date of amendment request:
September 26, 2005.
Description of amendment request:
The proposed amendment will revise
the analysis method used for the largebreak loss-of-coolant accident
(LBLOCA) by incorporating the use of a
new approach (ASTRUM) for the
treatment of parameter uncertainties.
The new approach is described in
Westinghouse Topical Report WCAP–
16009–P–A, approved by the NRC on
November 5, 2004.
Changes to the Technical
Specifications to reflect the proposed
use of ASTRUM in LBLOCA analysis
consist of revisions to the list of
references provided in Technical
Specification Section 5.6.5, Core
Operating Limits Report.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change modifies the analysis
methodology used to account for the
variation in parameters that are used for the
safety analysis of the LBLOCA. This
proposed change has no effect on the design
or operation of plant equipment. Use of the
new methodology will revise the results of
the current analysis, but there will be no
change in initiating events for this accident
scenario or the ability of the plant equipment
or plant operators to respond.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
Response: No.
The proposed change does not involve
modifications to existing plant equipment or
the installation of any new equipment. The
proposed change only affects the analysis
methodology that is used to evaluate the
response of existing plant equipment to the
LBLOCA scenario. Plant operating and
emergency procedures that are in place for
the LBLOCA scenario are also not being
changed by this proposed amendment. This
proposed change does not create new failure
modes or malfunctions of plant equipment
nor is there a new credible failure
mechanism.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed license amendment revises
the analysis methodology which is used to
assess the impact of the LBLOCA scenario
with respect to established acceptance
criteria. Margins of safety for LBLOCA
include quantitative limits for fuel
performance established in 10 CFR 50.46.
These acceptance criteria and the associated
margins of safety are not being changed. The
evaluation of the LBLOCA scenario, using the
proposed new methodology must still meet
the existing established acceptance criteria.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John Fulton,
Assistant General Counsel, Entergy
Nuclear Operations, Inc., 440 Hamilton
Avenue, White Plains, NY 10601.
NRC Section Chief: Richard J. Laufer.
Exelon Generation Company, LLC,
Docket Nos. 50–237 and 50–249,
Dresden Nuclear Power Station, Units 2
and 3, Grundy County, Illinois
Date of amendment request: April 4,
2005.
Description of amendment request:
The proposed amendments would
revise the maximum and minimum
allowable values for the degraded
voltage function of the 4160 volt
essential service system (ESS) bus
under-voltage instrumentation.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
PO 00000
Frm 00090
Fmt 4703
Sfmt 4703
67747
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes revise the Technical
Specifications (TS) maximum and minimum
allowable values for the degraded voltage
protection function and implement the use of
automatic load tap changers (LTCs) on
transformers that provide power to safetyrelated equipment. The only accident
previously evaluated for which the
probability is potentially affected by these
changes is the loss of offsite power (LOOP).
An allowable value for the degraded voltage
protection function that is too high could
cause the emergency buses to transfer to the
emergency diesel generators (EDG) and thus
increase the probability of a LOOP. The
allowable value for the degraded voltage
protection function has been revised in
accordance with an NRC-approved setpoint
methodology and will continue to ensure that
the degraded voltage protection function
actuates when required, but does not actuate
prematurely to cause a LOOP.
A failure of an LTC while in automatic
operation mode that results in decreased
voltage to the ESS buses could also cause a
LOOP. This could occur in two ways. A
failure of the LTC controller that results in
rapidly decreasing the voltage to the
emergency buses is the most severe failure
mode. However, a backup controller is
provided with the LTC that makes this failure
highly unlikely. A failure of the LTC
controller to respond to decreasing grid
voltage is less severe, since grid voltage
changes occur slowly. In both of the above
potential failure modes, operators will take
manual control of the LTC to mitigate the
effects of the failure. Thus, the probability of
a LOOP is not significantly increased.
The proposed changes will have no effect
on the consequences of a LOOP, since the
EDGs provide power to safety related
equipment following a LOOP. The EDGs are
not affected by the proposed changes.
The probability of other accidents
previously evaluated is not affected, since the
proposed changes do not affect the way plant
equipment is operated and thus do not
contribute to the initiation of any of the
previously evaluated accidents. The only
way in which the consequences of other
previously evaluated accidents could be
affected is if a failure of the LTC while in
automatic operation mode caused a sustained
high voltage which resulted in damage to
safety related equipment that is used to
mitigate an accident. Damage due to overvoltage is time-dependent. Since the LTC is
equipped with a backup controller, and since
operator action is available to prevent a
sustained high voltage condition from
occurring, damage to safety related
equipment is extremely unlikely, and thus
the consequences of these accidents are not
significantly increased.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
E:\FR\FM\08NON1.SGM
08NON1
67748
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
accident from any accident previously
evaluated?
Response: No.
The proposed changes involve functions
that provide offsite power to safety related
equipment for accident mitigation. Thus, the
proposed changes potentially affect the
consequences of previously evaluated
accidents (as addressed in Question 1), but
do not result in any new mechanisms that
could initiate damage to the reactor and its
principal safety barriers (i.e., fuel cladding,
reactor coolant system, or primary
containment).
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes do not affect the
inputs or assumptions of any of the analyses
that demonstrate the integrity of the fuel
cladding, reactor coolant system, or
containment during accident conditions. The
allowable values for the degraded voltage
protection function have been revised in
accordance with an NRC-approved setpoint
methodology and will continue to ensure that
the degraded voltage protection function
actuates when required, but does not actuate
prematurely to cause a LOOP. Automatic
operation of the LTC increases margin by
reducing the potential for transferring to the
EDGs during an event.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Thomas S.
O’Neill, Associate General Counsel,
Exelon Generation Company, LLC, 4300
Winfield Road, Warrenville, IL 60555.
NRC Section Chief: Gene Y. Suh.
FPL Energy Seabrook, LLC, Docket No.
50–443, Seabrook Station, Unit No. 1,
Rockingham County, New Hampshire
Date of amendment request:
September 22, 2005.
Description of amendment request:
The proposed amendment would revise
the Seabrook Station, Unit No. 1
operating license and Technical
Specifications to increase the licensed
rated power level by 1.7 percent from
3587 megawatts thermal (MWt) to 3648
MWt. Basis for proposed no significant
hazards consideration determination: As
required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
1. The proposed change will not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
Seabrook Station performed evaluations of
the Nuclear Steam Supply System (NSSS)
and balance of plant systems, components,
and analyses that could be affected by the
proposed change. A power uncertainty
calculation was performed, and the effect of
increase core thermal power by 1.7 percent
to 3648 MWt on the Seabrook Station design
and licensing basis was evaluated. The result
of the evaluations determined that all
systems and components continue to be
capable of performing their design function
at the MUR [measurement uncertainty
recapture] core power level of 3648 MWt. An
evaluation of the accident analyses
demonstrates that the applicable analyses
acceptance criteria continue to be met. No
accident initiators are affected by the MUR
power uprate and no challenges to any plant
safety barriers are created by the proposed
change.
The proposed change does not affect the
release paths, the frequency of release, or the
analyzed source term for any accidents
previously evaluated in the Seabrook Station
Updated Final Safety Analysis Report
(UFSAR). Systems, structures, and
components required to mitigate transients
continue to be capable of performing their
design functions, and thus were found
acceptable. The reduced uncertainty in the
feedwater flow input to the power
calorimetric measurement ensures that
applicable accident analyses acceptance
criteria continue to be met, to support
operation at the MUR core power level of
3648 MWt. Analyses performed to assess the
effects of mass and energy remain valid. The
source term used to assess radiological
consequences [has] been reviewed and
determined to bound operation at the MUR
core power level.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. The proposed change will not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
No new accident scenarios, failure
mechanisms, or single failures are introduced
as a result of the proposed change. The
installation of the Caldon LEFM CheckPlusTM
System has been analyzed, and failures of the
system will have no adverse effect on any
safety-related system or any systems,
structures, and components required for
transient mitigation. Systems, structures, and
components previously required for the
mitigation of a transient continue to be
capable of fulfilling their intended design
functions. The proposed change has no
adverse affect on any safety-related system or
component and does not change the
performance or integrity of any safety-related
system.
The proposed change does not adversely
affect any current system interfaces or create
any new interfaces that could result in an
accident or malfunction of a different kind
than previously evaluated. Operating at a
PO 00000
Frm 00091
Fmt 4703
Sfmt 4703
core power level of 3648 MWt does not create
any new accident initiators or precursors.
The reduced uncertainty in the feedwater
flow input to the power calorimetric
measurement ensures that applicable
accident analyses acceptance criteria
continue to be met, to support operation at
the MUR core power level of 3648 MWt.
Credible malfunctions continue to be
bounded by the current accident analyses of
record or evaluations that demonstrate that
applicable criteria continue to be met.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. The proposed change will not involve a
significant reduction in a margin [of] safety.
The margins of safety associated with the
MUR are those pertaining to core thermal
power. These include those associated with
the fuel cladding, Reactor Coolant System
pressure boundary, and containment barriers.
An engineering evaluation of the 1.7 percent
increase in core thermal power from 3587
MWt to 3648 MWt was performed. The
current licensing bases analyzed core power
is 3659 MWt. The analyzed core power level
of 3659 MWt bounds the NSSS thermal and
hydraulic parameters at the MUR core power
level of 3648 MWt. The NSSS systems and
components were evaluated at the MUR core
power level and it was determined that the
NSSS systems and components continue to
operate satisfactorily at the MUR power level.
The NSSS accident analyses were evaluated
at the MUR core power level of 3648 MWt.
In all cases, the accident analyses at the MUR
core power level of 3648 MWt were bounded
by the current licensing bases analyzed core
power level of 3659 MWt. As such, the
margins of safety continue to be bounded by
the current analyses of record for this change.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M. S. Ross,
Florida Power & Light Company, P.O.
Box 14000, Juno Beach, FL 33408–0420.
NRC Section Chief: Darrell J. Roberts.
FPL Energy Seabrook, LLC, Docket No.
50–443, Seabrook Station, Unit No. 1,
Rockingham County, New Hampshire
Date of amendment request:
September 29, 2005.
Description of amendment request:
The proposed amendment would revise
the Seabrook Station, Unit No. 1,
Technical Specifications (TSs) to permit
a one-time, six-month extension to the
currently approved 15-year test interval
for the containment integrated leak rate
test.
Basis for proposed no significant
hazards consideration determination:
E:\FR\FM\08NON1.SGM
08NON1
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed change [does] not involve
a significant increase in the probability or
consequences of an accident previously
evaluated.
The probability or consequences of
accidents previously evaluated in the UFSAR
[updated final safety analysis report] are
unaffected by this proposed change. There is
no change to any equipment response or
accident mitigation scenario, and this change
results in no additional challenges to fission
product barrier integrity. The proposed
change does not alter the design,
configuration, operation, or function of any
plant system, structure, or component. As a
result, the outcomes of previously evaluated
accidents are unaffected. The proposed
extension to the containment integrated leak
rate test (ILRT) interval does not involve a
significant increase in consequences because,
as discussed in NUREG 1493, Performance
Based Containment Leak Rate Test Program,
Type B and C tests identify the vast majority
(greater than 95 percent) of all potential
leakage paths. Further, ILRTs identify only a
few potential leakage paths that cannot be
identified through Type B and C testing, and
leaks found by Type A testing have been only
marginally greater than existing
requirements. In addition, periodic
inspections ensure that any significant
containment degradation will not go
undetected. Therefore, the proposed change
does not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. The proposed change [does] not create
the possibility of a new or different kind of
accident from any [accident] previously
evaluated.
No new accident scenarios, failure
mechanisms, or limiting single failures are
introduced as a result of the proposed
change. The proposed change does not
challenge the performance or integrity of any
safety-related system. The proposed change
neither installs or removes any plant
equipment, nor alters the design, physical
configuration, or mode of operation of any
plant structure, system, or component. No
physical changes are being made to the plant,
so no new accident causal mechanisms are
being introduced. The proposed change only
changes the frequency of performing the
ILRT; however, the test implementation and
acceptance criteria are unchanged. Therefore,
the proposed change does not create the
possibility of a new or different kind of
accident from any previously evaluated.
3. The proposed change [does] not involve
a significant reduction in a margin of safety.
The margin of safety associated with the
acceptance criteria of any accident is
unchanged. The proposed change will have
no affect on the availability, operability, or
performance of the safety-related systems and
components. The proposed change does not
alter the design, configuration, operation, or
function of any plant system, structure, or
component. The ability of any operable
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
structure, system, or component to perform
its designated safety function is unaffected by
this change. NUREG 1493 concluded that
reducing the frequency of ILRTs to 20 years
resulted in an imperceptible increase in risk.
Also, inspections of containment, required by
the ASME code [American Society of
Mechanical Engineers Boiler and Pressure
Vessel Code] and the maintenance rule,
ensure that containment will not degrade in
a manner that is only detectable by Type A
(ILRT) testing. Therefore, the margin of safety
as defined in the TS is not reduced and the
proposed change does not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M. S. Ross,
Florida Power & Light Company, P.O.
Box 14000, Juno Beach, FL 33408–0420.
NRC Section Chief: Darrell J. Roberts.
FPL Energy Seabrook, LLC, Docket No.
50–443, Seabrook Station, Unit No. 1,
Rockingham County, New Hampshire
Date of amendment request:
September 29, 2005.
Description of amendment request:
The proposed amendment would revise
the Seabrook Station, Unit No. 1
Technical Specifications to permit a
change in the steam generator tube
inspection requirements to include a
sampling of the bulges and overexpansions for portions of the steam
generator tubes within the hot leg
tubesheet region.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed changes do not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
The previously analyzed accidents are
initiated by the failure of plant structures,
systems, or components. The proposed
changes that alter the steam generator
inspection criteria do not have a detrimental
impact on the integrity of any plant structure,
system, or component that initiates an
analyzed event. The proposed changes will
not alter the operation of, or otherwise
increase the failure probability of any plant
equipment that initiates an analyzed
accident.
Of the applicable accidents previously
evaluated, the limiting transients with
consideration to the proposed changes to the
steam generator tube inspection criteria, are
the steam generator tube rupture (SGTR)
PO 00000
Frm 00092
Fmt 4703
Sfmt 4703
67749
event and the steam line break (SLB)
accident.
During the SGTR event, the required
structural integrity margins of the steam
generator tubes will be maintained by the
presence of the steam generator tubesheet
area. Tube rupture in tubes with cracks in the
tubesheet is precluded by the constraint
provided by the tubesheet. This constraint
results from the hydraulic expansion process,
thermal expansion mismatch between the
tube and tubesheet and from the differential
pressure between the primary and secondary
side. Based on this design, the structural
margins against burst, as discussed in
Regulatory Guide (RG) 1.121, ‘‘Bases for
Plugging Degraded PWR [pressurized-water
reactor] Steam Generator Tubes,’’ are
maintained for both normal and postulated
accident conditions.
At normal operating pressures, leakage
from primary water stress corrosion cracking
(PWSCC) below the proposed limited
inspection depth is limited by both the tubeto-tubesheet crevice and the limited crack
opening permitted by the tubesheet
constraint. Consequently, negligible normal
operating leakage is expected from cracks
within the tubesheet region. The
consequences of an SGTR event are affected
by the primary-to-secondary leakage flow
during the event. Primary-to-secondary
leakage flow through a postulated ruptured
tube is not affected by the proposed changes
since the tubesheet enhances the tube
integrity in the region of the hydraulic
expansion by precluding tube deformation
beyond its initial hydraulically-expanded
outside diameter.
Furthermore, the proposed changes do not
affect other systems, structures, components
or operational features. Therefore, the
proposed changes result in no significant
increase in the probability of the occurrence
of a SGTR accident.
The probability of a[n] SLB accident is
unaffected by the potential failure of a steam
generator tube as this failure is not an
initiator for a[n] SLB accident.
The consequences of a[n] SLB accident are
also not significantly affected by the
proposed changes. During a[n] SLB accident,
the reduction in pressure above the tubesheet
on the shell side of the steam generator
creates an axially uniformly distributed load
on the tubesheet due to the reactor coolant
system pressure on the underside of the
tubesheet. The resulting bending action
constrains the tubes in the tubesheet thereby
restricting primary-to-secondary leakage
below the midplane.
Primary-to-secondary leakage from tube
degradation in the tubesheet area during the
limiting accident (i.e., a[n] SLB) is limited by
flow restrictions resulting from the crack and
tube-to-tubesheet contact pressures that
provide a restricted leakage path above the
indications and also limit the degree of
potential crack face opening as compared to
free span indications. The primary-tosecondary leak rate during postulated SLB
accident conditions would be expected to be
less than that during normal operation for
indications near the bottom of the tubesheet
(i.e., including indications in the tube end
welds). This conclusion is based on the
E:\FR\FM\08NON1.SGM
08NON1
67750
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
observation that while the driving pressure
causing leakage increases by approximately a
factor of (two) 2, the flow resistance
associated with an increase in tube-totubesheet contact pressure, during a[n] SLB
accident, increases by approximately a factor
of 2.5. While such a leakage decrease is
logically expected, the postulated accident
leak rate could be conservatively bounded by
twice the normal operating leak rate even if
the increase in contact pressure is ignored.
Since normal operating leakage (spiking) is
limited to less that 0.104 gpm (150 gpd) for
continued power operation per station
operating procedure OS 1227.02, ‘‘Steam
Generator Tube Leak,’’ the associated
accident condition leak rate, assuming all
leakage to be from lower tube sheet
indications, would be bound by 0.208 gpm
(twice normal operating leak rate). This value
is well within the assumed accident leakage
rate of 0.347 gpm discussed in the Seabrook
Station Updated Safety Analysis Report,
Section 15.1.5 ‘‘Steam System Piping
Failure.’’ Hence it is reasonable to omit any
consideration of inspection of the tube, tube
end weld, bulges / overexpansions or other
anomalies below 17 inches from the top of
the hot leg tubesheet. Therefore, the
consequences of a[n] SLB accident remain
unaffected.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. The proposed changes do not create the
possibility of a new or different kind of
accident from any [accident] previously
evaluated.
The proposed changes do not introduce
any new equipment, create new failure
modes for existing equipment, or create any
new limiting single failures. Plant operation
will not be altered, and all safety functions
will continue to perform as previously
assumed in accident analyses. Therefore, the
proposed changes do not create the
possibility of a new or different kind of
accident from any previously evaluated.
3. The proposed changes do not involve a
significant reduction in the margin of safety.
The proposed changes maintain the
required structural margins of the steam
generator tubes for both normal and accident
conditions. Nuclear Energy Institute (NEI)
97–06, ‘‘Steam Generator Program
Guidelines,’’ and NRC Regulatory Guide (RG)
1.121, ‘‘Bases for Plugging Degraded PWR
Steam Generator Tubes,’’ are used as the
bases in the development of the limited hot
leg tubesheet inspection depth methodology
for determining that steam generator tube
integrity considerations are maintained
within acceptable limits. RG 1.121 describes
a method acceptable to the NRC for meeting
General Design Criteria (GDC) 14, ‘‘Reactor
Coolant Pressure Boundary,’’ GDC 15,
‘‘Reactor Coolant System Design,’’ GDC 31,
‘‘Fracture Prevention of Reactor Coolant
Pressure Boundary,’’ and GDC 32,
‘‘Inspection of Reactor Coolant Pressure
Boundary,’’ by reducing the probability and
consequences of a SGTR. RG 1.121 concludes
that by determining the limiting safe
conditions for tube wall degradation the
probability and consequences of a SGTR are
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
reduced. RG 1.121 uses safety factors on
loads for tube burst that are consistent with
the requirements of Section III of the
American Society of Mechanical Engineers
(ASME) Code.
For axially oriented cracking located
within the tubesheet, tube burst is precluded
due to the presence of the tubesheet. For
circumferentially oriented cracking,
Westinghouse evaluation LTR-CDME–05–
170, ‘‘Limited Inspection of the Steam
Generator Tube Portion Within the Tubesheet
at Seabrook Generating Station,’’ defines a
length of degradation-free expanded tubing
that provides the necessary resistance to tube
pullout due to the pressure induced forces,
with applicable safety factors applied.
Application of the limited hot leg tubesheet
inspection criteria will preclude
unacceptable primary-to-secondary leakage
during all plant conditions. The methodology
for determining leakage provides for large
margins between calculated and actual
leakage values in the proposed limited hot
leg tubesheet inspection depth criteria.
Therefore, the proposed changes do not
involve a significant reduction in any margin
of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M. S. Ross,
Florida Power & Light Company, P.O.
Box 14000, Juno Beach, FL 33408–0420.
NRC Section Chief: Darrell J. Roberts.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–348 and 50–364,
Joseph M. Farley Nuclear Plant, Units 1
and 2, Houston County, Alabama
Date of amendment request:
September 27, 2005.
Description of amendment request:
The amendments proposed by Southern
Nuclear Operating Company would
revise the Technical Specifications (TS)
to eliminate the Power Range Neutron
Flux-High Negative Rate Reactor Trip
function, based on the approved
methodology contained in
Westinghouse Topical Report WCAP–
11394–P–A, ‘‘Methodology for the
Analysis of the Dropped Rod Event.’’
The changes will allow the elimination
of a trip circuitry that is not credited in
the Farley Nuclear Plant safety analysis,
and which can result in an unnecessary
reactor trip. These changes will be
implemented sequentially, concurrent
with each unit’s refueling outage during
which the design change is
implemented. Additionally, this
amendment request deletes TS Bases
text associated with an unconservative
local Departure from Nucleate Boiling
Ratio.
PO 00000
Frm 00093
Fmt 4703
Sfmt 4703
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
No. The proposed changes do not
significantly increase the probability or
consequences of an accident previously
evaluated in the Updated Final Safety
Analysis Report (UFSAR). All of the safety
analyses have been evaluated for impact due
to this change. The elimination of the Power
Range Neutron Flux-High Negative Rate
Reactor Trip function and the elimination of
text in the TS [Technical Specifications]
Bases for LC0 3.3.1, page B 3.3.1–1 1,
associated with an unconservative local
DNBR [departure from nucleate boiling ratio],
does not affect the dropped RCCA [Rod
Cluster Control Assembly] analyses nor any
other analyses, since it is not credited in any
of the safety analyses; therefore, the
probability of an accident has not been
increased. All dose consequences have been
evaluated with respect to the proposed
changes, there is no impact due to the
proposed change, and all acceptance criteria
continue to be met. Therefore, these changes
do not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any previously evaluated?
No. The proposed changes do not create
the possibility of a new or different kind of
accident from any accident already evaluated
in the UFSAR. No new accident scenarios,
failure mechanisms or limiting single failures
are introduced as result of the proposed
changes. The changes have no adverse effects
on any safety-related system. Therefore, all
accident analyses criteria continue to be met
and these changes do not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
No. The proposed changes do not involve
a significant reduction in a margin of safety.
The dropped RCCA(s) event does not credit
the Power Range Neutron Flux-High Negative
Rate Reactor Trip function. The conclusion
presented in the UFSAR Section 15.2.3.3 that
the DNBR design basis is met for a dropped
RCCA(s) event remains valid for the
proposed changes, which are based on the
NRC approved methodology contained in
CAP–11394–PA. Additionally, WCAP–
11394–P–A indicates that the analysis for a
dropped rod event envelops a multiple rod
drop accident at high power levels, and that
such an accident will not result in an
unconservative local DNBR. All applicable
acceptance criteria continue to be met.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
E:\FR\FM\08NON1.SGM
08NON1
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M. Stanford
Blanton, Esq., Balch and Bingham, Post
Office Box 306, 1710 Sixth Avenue
North, Birmingham, Alabama 35201.
NRC Section Chief: Evangelos C.
Marinos.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–348 and 50–364,
Joseph M. Farley Nuclear Plant, Units
1 and 2, Houston County, Alabama
Date of amendment request: October
6, 2005.
Description of amendment request:
The amendments proposed by Southern
Nuclear Operating Company (SNC)
would revise the Technical
Specifications (TS) to support a revision
to the Best Estimate Loss of Coolant
Accident (BELOCA) for Farley Nuclear
Plant (FNP). The NRC recently approved
a new Westinghouse BELOCA
methodology, Automated Statistical
Treatment of Uncertainty Method
(ASTRUM). ASTRUM was submitted in
WCAP–16009–P. The NRC issued a
Safety Evaluation Report in a letter
dated November 5, 2004. Westinghouse
issued WCAP–16009–P–A in January
2005. SNC has completed the analysis
for FNP and the enclosed proposed
amendment is to incorporate a reference
to WCAP–16009–P–A in TS section
5.6.5 Core Operating Limits Report
(COLR).
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
No physical plant changes are being made
as a result of using the Westinghouse Best
Estimate Large Break LOCA [Loss of Coolant
Accident] (BELOCA) analysis methodology.
The proposed TS changes simply involve
updating the references in TS 5.6.5.b, Core
Operating Limits Report (COLR), to reference
the Westinghouse BELOCA analysis
methodology. The plant conditions assumed
in the analysis are bounded by the design
conditions for all equipment in the plant;
therefore, there will be no increase in the
probability of a LOCA. The consequences of
a LOCA are not being increased, since the
analysis has shown that the Emergency Core
Cooling System (ECCS) is designed such that
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
its calculated cooling performance conforms
to the criteria contained in 10 CFR 50.46,
‘‘Acceptance criteria for emergency core
cooling systems for light-water nuclear power
reactors.’’ No other accident consequence is
potentially affected by this change.
All systems will continue to be operated in
accordance with current design requirements
under the new analysis, therefore no new
components or system interactions have been
identified that could lead to an increase in
the probability of any accident previously
evaluated in the Updated Final Safety
Analysis Report (UFSAR). No changes were
required to the Reactor Protection System
(RPS) or Engineering Safety Features (ESF)
setpoints because of the new analysis
methodology.
Therefore, it is concluded that this change
does not significantly increase the probability
or consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
There are no physical changes being made
to the plant as a result of using the
Westinghouse Best Estimate Large Break
LOCA analysis methodology. No new modes
of plant operation are being introduced. The
configuration, operation and accident
response of the structures or components are
unchanged by utilization of the new analysis
methodology. Analyses of transient events
have confirmed that no transient event
results in a new sequence of events that
could lead to a new accident scenario. The
parameters assumed in the analysis are
within the design limits of existing plant
equipment.
In addition, employing the Westinghouse
Best Estimate Large Break LOCA analysis
methodology does not create any new failure
modes that could lead to a different kind of
accident. The design of all systems remains
unchanged and no new equipment or
systems have been installed which could
potentially introduce new failure modes or
accident sequences. No changes have been
made to any RPS or ESF actuation setpoints.
Based on this review, it is concluded that
no new accident scenarios, failure
mechanisms or limiting single failures are
introduced as a result of the proposed
changes.
Therefore, the proposed TS changes do not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
It has been shown that the analytic
technique used in the Westinghouse Best
Estimate Large Break LOCA analysis
methodology realistically describes the
expected behavior of the reactor system
during a postulated LOCA. Uncertainties
have been accounted for as required by 10
CFR 50.46. A sufficient number of LOCAs
with different break sizes, different locations,
and other variations in properties have been
considered to provide assurance that the
most severe postulated LOCAs have been
evaluated. The analysis has demonstrated
that all acceptance criteria contained in 10
PO 00000
Frm 00094
Fmt 4703
Sfmt 4703
67751
CFR 50.46 paragraph b continue to be
satisfied.
Therefore, it is concluded that this change
does not involve a significant reduction in
the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M. Stanford
Blanton, Esq., Balch and Bingham, Post
Office Box 306, 1710 Sixth Avenue
North, Birmingham, Alabama 35201.
NRC Section Chief: Evangelos C.
Marino.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–424 and 50–425,
Vogtle Electric Generating Plant, Units 1
and 2, Burke County, Georgia
Date of amendment request: January
27, 2005.
Description of amendment request:
The proposed amendments would
revise Technical Specifications Limiting
Conditions for Operations 3.3.1, 3.3.2,
3.3.6, and 3.3.8, by extending the
Surveillance Test Intervals for the
Reactor Protection System.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the Proposed Change Involve a
Significant Increase in the Probability or
Consequences of an Accident Previously
Evaluated?
The proposed changes to the Completion
Time, bypass test time, and Surveillance
Frequencies reduce the potential for
inadvertent reactor trips and spurious
actuations and, therefore, do not increase the
probability of any accident previously
evaluated. The proposed changes to the
allowed Completion Time, bypass test time,
and Surveillance Frequencies do not change
the response of the plant to any accidents
and have an insignificant impact on the
reliability of the reactor trip system and
engineered safety feature actuation system
(RTS and ESFAS) signals. The RTS and
ESFAS will remain highly reliable, and the
proposed changes will not result in a
significant increase in the risk of plant
operation. This is demonstrated by showing
that the impact on plant safety as measured
by core damage frequency (CDF) is less than
1.01E–06 per year and the impact on large
early release frequency (LERF) is less than
1.0E–07 per year. In addition, for the
Completion Time change, the incremental
conditional core damage probabilities
(ICCDP) and incremental conditional large
early release probabilities (ICLERP) are less
than 5.0E–08. These changes meet the
E:\FR\FM\08NON1.SGM
08NON1
67752
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
acceptance criteria in Regulatory Guides
1.174 and 1.177. Therefore, since the RTS
and ESFAS will continue to perform their
functions with high reliability as originally
assumed, and the increase in risk as
measured by CDF, LERF, ICCDP, and ICLERP
is within the acceptance criteria of existing
regulatory guidance, there will not be a
significant increase in the consequences of
any accidents. The proposed changes do not
adversely affect accident initiators or
precursors nor alter the design assumptions,
conditions, or configuration of the facility or
the manner in which the plant is operated
and maintained. The proposed changes do
not alter or prevent the ability of structures,
systems, and components (SSCs) from
performing their intended function to
mitigate the consequences of an initiating
event within the assumed acceptance limits.
The proposed changes do not affect the
source term, containment isolation, or
radiological release assumptions used in
evaluating the radiological consequences of
an accident previously evaluated. Further,
the proposed changes do not increase the
types or amounts of radioactive effluent that
may be released offsite, nor significantly
increase individual or cumulative
occupational/public radiation exposures. The
proposed changes are consistent with the
safety analysis assumptions and resultant
consequences. Therefore, it is concluded that
this change does not increase the probability
of occurrence of a malfunction of equipment
important to safety.
2. Does the Proposed Change Create the
Possibility of a New or Different Kind of
Accident from any Previously Evaluated?
The proposed changes do not result in a
change in the manner in which the RTS and
ESFAS provide plant protection. The RTS
and ESFAS will continue to have the same
setpoints after the proposed changes are
implemented. There are no design changes
associated with the license amendment. The
changes to Completion Time, bypass test
time, and Surveillance Frequency do not
change any existing accident scenarios, nor
create any new or different accident
scenarios. The changes do not involve a
physical alteration of the plant (i.e., no new
or different type of equipment will be
installed) or a change in the methods
governing normal plant operation. In
addition, the changes do not impose any new
or different requirements or eliminate any
existing requirements. The changes do not
alter assumptions made in the safety
analysis. The proposed changes are
consistent with the safety analysis
assumptions and current plant operating
practice. Therefore, the possibility of a new
or different malfunction of safety related
equipment is not created.
3. Does the Proposed Change Involve a
Significant Reduction in the Margin of
Safety?
The proposed changes do not alter the
manner in which safety limits, limiting safety
system settings, or limiting conditions for
operation are determined. The safety analysis
acceptance criteria are not impacted by these
changes. Redundant RTS and ESFAS trains
are maintained, and diversity with regard to
the signals that provide reactor trip and
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
engineered safety features actuation is also
maintained. All signals credited as primary
or secondary and all operator actions
credited in the accident analyses will remain
the same. The proposed changes will not
result in plant operation in a configuration
outside the design basis. The calculated
impact on risk is insignificant and meets the
acceptance criteria contained in Regulatory
Guides 1.174 and 1.177. Although there was
no attempt to quantify any positive human
factors benefit due to increased Completion
Time, bypass test time, and Surveillance
Frequencies, it is expected there would be a
net benefit due to a reduced potential for
spurious reactor trips and actuations
associated with testing. Therefore, it is
concluded that this change does not involve
a significant reduction in the margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. Arthur H.
Domby, Troutman Sanders,
NationsBank Plaza, Suite 5200, 600
Peachtree Street, NE., Atlanta, Georgia
30308–2216.
NRC Section Chief: Evangelos C.
Marinos.
Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant (SQN), Units 1 and 2,
Hamilton County, Tennessee
Date of amendment request:
September 30, 2005 (TS–05–02).
Description of amendment request:
The proposed amendment would revise
the SQN Technical Specification (TS)
Section 5.0, ‘‘Design Features,’’ to more
conform with NUREG–1431 Revision 3,
‘‘Standard Technical Specifications for
Westinghouse Plants.’’ The proposed
change included the elimination of
exclusion area, low population zone,
and effluent subsections and associated
figures referred to in Section 5.1, ‘‘Site’’;
elimination of Section 5.2,
‘‘Containment’’; elimination of Section
5.4, ‘‘Reactor Coolant System,’’ as well
as Section 5.5, ‘‘Meteorological Tower
Location,’’ and its figure. Lastly, a
proposed change to the TS
‘‘Administrative Control’’ section to
acquire the component cyclic or
transient limits currently located in the
‘‘Design Features’’ section.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
PO 00000
Frm 00095
Fmt 4703
Sfmt 4703
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The removal of information and figures
featuring the locations of the site exclusion
area, gaseous and liquid effluent boundaries,
low population zone, and the meteorological
tower is administrative in nature. Most, if
not, all of this information is located in other
licensee control documents, such as the Final
Safety Analysis Report (FSAR). Congruently,
the addition of a site location description
only adds geographical information to the
TSs. The relocation and revision of the
component cyclic or transient limits
requirement does not alter the requirement to
track and maintain these limits and thus
considered administrative. This proposed
amendment involves no technical changes to
the existing TSs and does not impact
initiators of analyzed events. The changes
also do not impact the assumed mitigation of
accidents or transient events. Therefore, the
proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not involve a
change to plant systems, components, or
operating practices that could result in a
change in accident generation potential. The
proposed changes do not impose any new or
different requirements or eliminate any
existing requirements. The proposed changes
do not alter assumptions made in the safety
analyses and licensing basis. Therefore, the
proposed change does not create the
possibility of a new or different kind of
accident from any previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The deletion of information and figures
featuring the locations of the site exclusion
area, gaseous and liquid effluent boundaries,
low population zone, and the meteorological
tower does not affect operational limits or
functional capabilities of plant systems,
structures and components. The addition of
a site location description adds geographical
information to the TSs. The relocation and
revision of the component cyclic or transient
limits requirements also does not affect
operational limits or functional capabilities
of plant systems, structures and components.
These changes pose no effect on margin of
safety. The TS identified maximum steel
containment temperature value is not the
current limiting design value, which is found
in the FSAR. Its elimination is considered
administrative in nature and does not result
in a change of margin of safety to the
containment design. Therefore, the proposed
change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
E:\FR\FM\08NON1.SGM
08NON1
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Section Chief: Michael L.
Marshall, Jr.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Unit 2,
Somervell County, Texas
Date of amendment request: April 27,
2005, as supplemented by letter dated
July 20, 2005.
Brief description of amendments: The
amendment revises Technical
Specification (TS) 5.6.5, ‘‘Core
Operating Limits Report,’’ by adding
topical report WCAP–13060–P–A,
‘‘Westinghouse Fuel Assembly
Reconstitution Evaluation
Methodology,’’ to the list of approved
methodologies to be used at Comanche
Peak Steam Electric Station (CPSES),
Unit 2.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change is administrative in
nature and as such does not impact the
condition or performance of any plant
structure, system or component. The core
operating limits are established to support
Technical Specifications 3.1, 3.2, 3.3, 3.4,
and 3.9. The core operating limits ensure that
fuel design limits are not exceeded during
any conditions of normal operation or in the
event of any Anticipated Operational
Occurrence (AOO). The methods used to
determine the core operating limits for each
operating cycle are based on methods
previously found acceptable by the NRC and
listed in TS section 5.6.5.b. Application of
these approved methods will continue to
ensure that acceptable operating limits are
established to protect the fuel cladding
integrity during normal operation and AOOs.
The requested Technical Specification
change does not involve any plant
modifications or operational changes that
could affect system reliability, performance,
or possibility of operator error. The requested
change does not affect any postulated
accident precursors, does not affect any
accident mitigation systems, and does not
introduce any new accident initiation
mechanisms.
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
As a result, the proposed change to the
CPSES Technical Specifications does not
involve any increase in the probability or the
consequences of any accident or malfunction
of equipment important to safety previously
evaluated since neither accident probabilities
nor consequences are being affected by this
proposed administrative change.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change is administrative in
nature, and therefore does not involve any
change in station operation or physical
modifications to the plant. In addition, no
changes are being made in the methods used
to respond to plant transients that have been
previously analyzed. No changes are being
made to plant parameters within which the
plant is normally operated or in the
setpoints, which initiate protective or
mitigative actions, and no new failure modes
are being introduced.
Therefore, the proposed administrative
change to the CPSES Technical
Specifications does not create the possibility
of a new or different kind of accident or
malfunction of equipment important to safety
from any accident previously evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The proposed change is administrative in
nature and does not impact station operation
or any plant structure, system or component
that is relied upon for accident mitigation.
Furthermore, the margin of safety assumed in
the plant safety analysis is not affected in any
way by the proposed administrative change.
Therefore, the proposed change to the
CPSES Technical Specifications does not
involve any reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: George L. Edgar,
Esq., Morgan, Lewis and Bockius, 1800
M Street, NW., Washington, DC 20036.
NRC Section Chief: David Terao.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Units 1 and
2, Somervell County, Texas
Date of amendment request: January
24, 2005.
Brief description of amendments: The
amendments will revise the surveillance
requirements (SRs) for Technical
Specification 3.7.5, ‘‘Auxilary Feed
Water (AFW) System.’’ Specifically, a
note will be added to SRs 3.7.5.1,
3.7.5.3, and 3.7.5.4 that states, ‘‘AFW
train(s) may be considered OPERABLE
during alignment and operation for
steam generator level control, if it is
PO 00000
Frm 00096
Fmt 4703
Sfmt 4703
67753
capable of being manually realigned to
the AFW mode of operation.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change has no impact on the
probability of any accident previously
evaluated. The consequences of the limiting
transients and accidents (full power
operation) are unaffected by the proposed
change. At low power sufficient time is
available to establish auxiliary feedwater
injection if needed.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
No new accident scenarios, transient
precursors, failure mechanisms, or limiting
single failures are introduced as a result of
these changes. There will be no adverse effect
or challenges imposed on any safety-related
system as a result of these changes. There are
no changes in the method by which any
safety-related plant system performs its safety
function. Overall protection system
performance will remain within the bounds
of the previously performed accident
analyses and the protection systems will
continue to function in a manner consistent
with the plant design basis. The proposed
changes do not affect the probability of any
event initiators. The proposed changes do not
alter any assumptions or change any
mitigation actions in the radiological
consequence evaluations in the Final Safety
Analysis Report (FSAR).
Therefore, the proposed change[s] do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes do not affect the
acceptance criteria for any analyzed event
nor is there a change to any Safety Analysis
Limit (SAL). There will be no effect on the
manner in which safety limits, limiting safety
system settings, or limiting conditions for
operation are determined nor will there be
any effect on those plant systems necessary
to assure the accomplishment of protection
functions. There will be no impact on the
overpower limit, the Departure from Nucleate
Boiling Ratio (DNBR) limits, the Heat Flux
Hot Channel Factor (FQ), the Nuclear
Enthalpy Rise Hot Channel Factor (F’H), the
Loss of Coolant Accident Peak Centerline
Temperature (LOCA PCT), peak local power
density, or any other margin of safety. The
E:\FR\FM\08NON1.SGM
08NON1
67754
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
radiological dose consequence acceptance
criteria listed in the Standard Review Plan
will continue to be met. Since the limiting
transients and accidents are unaffected, the
proposed change[s] do not involve a
reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: George L. Edgar,
Esq., Morgan, Lewis and Bockius, 1800
M Street, NW., Washington, DC 20036.
NRC Section Chief: David Terao.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Units 1 and
2, Somervell County, Texas
Date of amendment request: August
10, 2005.
Brief description of amendments: The
amendments would revise the Technical
Specification (TS) 5.5.13, ‘‘Diesel Fuel
Oil Testing Program,’’ to relocate the
specific American Society for Testing
and Materials (ASTM) Standard
reference from the Administrative
Controls Section of TS to a licenseecontrolled document.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes relocate the specific
American Society for Testing and Materials
(ASTM) Standard references from the
Administrative Controls of TS to a licenseecontrolled document. Since any change to
the licensee-controlled document will be
evaluated pursuant to the requirements of 10
CFR 50.59, ‘‘Changes, tests and
experiments,’’ no increase in the probability
or consequences of an accident previously
evaluated is involved.
The proposed changes do not adversely
affect accident initiators or precursors nor
alter the design assumptions, conditions, or
configuration of the facility or the manner in
which the plant is operated and maintained.
The proposed changes do not alter or prevent
the ability of structures, systems, and
components (SSCs) from performing their
intended function to mitigate the
consequences of an initiating event within
the assumed acceptance limits. The proposed
changes do not affect the source term,
containment isolation, or radiological release
assumptions used in evaluating the
radiological consequences of an accident
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
previously evaluated. Further, the proposed
changes do not increase individual or
cumulative occupational or public radiation
exposure.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes do not involve a
physical alteration of the plant (i.e., no new
or different type of equipment will be
installed) or change in the methods
governing normal plant operation. In
addition, the changes do not alter the
assumptions made in the analysis and
licensing basis.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The level of safety of facility operation is
unaffected by the proposed changes since
there is no change in the intent of the TS
requirements of assuring fuel oil is of the
appropriate quality for emergency DG [diesel
generator] use. The proposed changes
provide the flexibility needed to utilize stateof-the-art technology in fuel oil sampling and
analysis methods.
Therefore the proposed changes do not
involve a reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: George L. Edgar,
Esq., Morgan, Lewis and Bockius, 1800
M Street, NW., Washington, DC 20036.
NRC Section Chief: David Terao.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Units 1 and
2, Somervell County, Texas
Date of amendment request: August
22, 2005.
Brief description of amendments: The
amendments revise Technical
Specification (TS) 3.7.10, ‘‘Control
Room Emergency Filtration/
Pressurization System (CREFS) and
Control Room Envelope (CRE),’’ and
adds new TS 5.5.20, ‘‘Control Room
Integrity Program,’’ and TS 5.6.11,
‘‘Control Room Report.’’ In addition the
amendments update the Final Safety
Analysis Report to include new
methods and assumptions as described
in Regulatory Guide 1.195 for evaluation
of radiological consequences.
PO 00000
Frm 00097
Fmt 4703
Sfmt 4703
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change addresses the Control
Room Envelope (CRE), including updated
surveillances for the Control Room
Emergency Filtration/Pressurization System
(CREFS) trains and the CRE, a new TS 5.5.20,
‘‘Control Room Integrity Program,’’ and a
new TS 5.6.11, ‘‘Control Room Report.’’
These changes are consistent with the
guidance in Regulatory Guides 1.196 and
1.197. New methods and assumptions for
evaluating radiological consequences for
design basis accidents are adopted consistent
with NRC Regulatory Guide 1.195. The
acceptance limits for the Control Room
Integrity Program are based on these revised
radiological dose consequences calculations.
The proposed changes do not adversely affect
accident initiators or precursors nor alter the
configuration of the facility. The proposed
changes do not alter or prevent the ability of
structures, systems, and components (SSCs)
from performing their intended function to
mitigate the consequences of an initiating
event to within the Regulatory Guide 1.195
acceptance limits. This activity is a revision
to the Technical Specifications and the
supporting radiological dose consequences
analyses for the control room ventilation
system which is a mitigating system designed
to minimize in-leakage into the control room
and to filter the control room atmosphere to
protect the control room operators following
accidents previously analyzed. An important
part of the system is the control room
envelope (CRE). The CRE integrity is not an
initiator or precursor to any accident
previously evaluated. Therefore the
probability of occurrence of any accident
previously evaluated is not increased.
Performing tests and implementing programs
that verify the integrity of the CRE and
control room habitability ensure mitigation
features are capable of performing the
assumed function.
The revised radiological consequences
analyses, performed using the assumptions
and methodologies presented in Regulatory
Guidance 1.195, do not result in significant
increases in the radiological dose
consequences to the general public nor to the
control room operators. All calculated dose
consequences are within acceptance limits of
Regulatory Guide 1.195.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes will not alter the
requirements of the control room ventilation
E:\FR\FM\08NON1.SGM
08NON1
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
system or its function during accident
conditions. No new or different accidents
result from performing the new revised
actions and surveillances or programs
required. The changes do not involve a
physical alteration of the plant (i.e., no new
or different type of equipment will be
installed) or a change in the methods
governing normal plant operation which
could create the possibility of a new or
different kind of accident. The proposed
changes are consistent with the safety
analysis assumptions and current plant
operating practices. Therefore, the proposed
changes do not create the possibility of a new
or different kind of accident from any
previously evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes do not alter the
manner in which safety limits, limiting safety
system settings or limiting conditions for
operation are determined. The safety analysis
acceptance criteria are not affected by these
changes. The proposed changes will not
result in plant operation in a configuration
outside the design basis for an unacceptable
period of time without mitigating actions.
The proposed changes do not affect systems
that are required to respond to safely shut
down the plant and to maintain the plant in
a safe shutdown condition.
Therefore the proposed change does not
involve a reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: George L. Edgar,
Esq., Morgan, Lewis and Bockius, 1800
M Street, NW., Washington, DC 20036.
NRC Section Chief: David Terao.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing in
connection with these actions was
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
Detroit Edison Company, Docket No.
50–341, Fermi 2, Monroe County,
Michigan
Date of application for amendment:
May 27, 2005.
Brief description of amendment: The
amendment revised the technical
specification (TS) testing frequency for
the surveillance requirement (SR) in TS
3.1.4, ‘‘Control Rod Scram Times.’’
Specifically, the change revised the
frequency for SR 3.1.4.2, ‘‘Control Rod
Scram Time Testing,’’ from ‘‘120 days
cumulative operation in MODE 1’’ to
‘‘200 days cumulative operation in
MODE 1.’’
Date of issuance: October 25, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days.
Amendment No.: 167.
Facility Operating License No. NPF–
43: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: July 19, 2005 (70 FR 41443).
The Commission’s related evaluation
of the amendment is contained in a
PO 00000
Frm 00098
Fmt 4703
Sfmt 4703
67755
Safety Evaluation dated October 25,
2005.
No significant hazards consideration
comments received: No.
Entergy Nuclear Operations, Inc.,
Docket No. 50–333, James A. FitzPatrick
Nuclear Power Plant, Oswego County,
New York
Date of application for amendment:
May 31, 2005.
Brief description of amendment: The
amendment modifies Technical
Specification (TS) requirements to adopt
the provisions of Industry/TS Task
Force (TSTF) change TSTF–359,
‘‘Increased Flexibility in Mode
Restraints.’’
Date of issuance: October 20, 2005.
Effective date: As of the date of
issuance, and shall be implemented
within 60 days.
Amendment No.: 284.
Facility Operating License No. DPR–
59: The amendment revised the TSs.
Date of initial notice in Federal
Register: August 16, 2005 (70 FR
48204).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 20,
2005.
No significant hazards consideration
comments received: No.
Exelon Generating Company, LLC,
Docket Nos. STN 50–454 and STN 50–
455, Byron Station, Unit Nos. 1 and 2,
Ogle County, Illinois
Date of application for amendment:
December 17, 2004, as supplemented by
letter dated September 28, 2005.
Brief description of amendment: The
amendments revised Appendix B,
Environmental Protection Plan (nonradiological), of the Byron Station
Facility Operating Licenses.
Date of issuance: October 18, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 145.
Facility Operating License Nos. NPF–
37 and NPF–66: The amendments
revised the Environmental Protection
Plan.
Date of initial notice in Federal
Register: April 12, 2005 (70 FR 19115).
The supplement dated September 28,
2005, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
E:\FR\FM\08NON1.SGM
08NON1
67756
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
Safety Evaluation dated October 18,
2005.
No significant hazards consideration
comments received: No.
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request: October
25, 2004, as supplement by letter dated
August 1, 2005.
Brief description of amendment: The
amendment revises the required
channels per trip system for several
instrument functions contained in
Technical Specification Tables 3.3.6.1–
1, ‘‘Primary Containment Isolation
Instrumentation,’’ 3.3.6.2–1, ‘‘Secondary
Containment Isolation
Instrumentation,’’ and 3.3.7.1–1
‘‘Control Room Emergency Filter System
Instrumentation.’’
Date of issuance: October 27, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days of issuance.
Amendment No.: 212.
Facility Operating License No. DPR–
46: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: January 4, 2005 (70 FR 402).
The supplement dated August 1,
2005, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 27,
2005.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket No. 50–272,
Salem Nuclear Generating Station Unit
No. 1, Salem County, New Jersey
Date of application for amendment:
February 23, 2005, as supplemented by
letters dated August 2, 2005, and
September 21, 2005.
Brief description of amendment: The
amendments revised Technical
Specifications (TSs) to implement a new
steam generator tube surveillance
program that is consistent with the
program proposed by the TS Task Force
(TSTF) in TSTF–449.
Date of issuance: October 14, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 268.
Facility Operating License No. DPR–
70: The amendments revised the TSs.
VerDate Aug<31>2005
16:11 Nov 07, 2005
Jkt 208001
Date of initial notice in Federal
Register: May 10, 2005 (70 FR 24655).
Supplements dated August 2, 2005, and
September 21, 2005, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 14,
2005.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket Nos. 50–272
and 50–311, Salem Nuclear Generating
Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of application for amendments:
March 4, 2005, as supplemented August
2, 2005.
Brief description of amendments:
These amendments extend the
completion time from 1 hour to 24
hours for Actions ‘‘a’’ and ‘‘b’’ of Salem
Nuclear Generating Station, Unit Nos. 1
and 2 Technical Specification (TS)
3.5.1, ‘‘Accumulators,’’ which requires
restoration of an accumulator when it
has been declared inoperable for reasons
other than boron concentration in the
accumulator not being within the
required range.
Date of issuance: October 14, 2005.
Effective date: As of the date of
issuance and to be implemented within
60 days.
Amendment Nos.: 267 and 249.
Facility Operating License Nos. DPR–
70 and DPR–75: The amendments
revised the TSs.
Date of initial notice in Federal
Register: May 24, 2005 (70 FR 29800).
The August 2, 2005, supplement
provided clarifying information only
and did not change the scope of the
proposed amendment, and did not
change the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 14,
2005.
No significant hazards consideration
comments received: No.
Sacramento Municipal Utility District,
Docket No. 50–312, Rancho Seco
Nuclear Generating Station, Sacramento
County, California
Date of application for amendment:
January 24, 2005.
Brief description of amendment: The
amendment removes unnecessary and
PO 00000
Frm 00099
Fmt 4703
Sfmt 4703
obsolete information from the facility
operating license.
Date of issuance: September 21, 2005.
Effective date: September 21, 2005.
Amendment No.: 132.
Facility Operating License No. DPR–
54: The amendment revised the License.
Date of initial notice in Federal
Register: March 29, 2005 (70 FR
15947).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 22,
2005.
No significant hazards consideration
comments received: No.
Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton
County, Tennessee
Date of application for amendments:
August 12, 2004.
Brief description of amendments: The
amendments revised Surveillance
Requirement (SR) 4.7.8.d.3 of the
Auxiliary Building Gas Treatment
System (ABGTS) by deleting vacuum
relief flow requirements. The change
removes criteria from the SR that is not
necessary to verify the operability of the
ABGTS and eliminates confusion
regarding the basis for the vacuum relief
flow requirement.
Date of issuance: August 18, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 45 days.
Amendment Nos.: 303 and 293.
Facility Operating License Nos. DPR–
77 and DPR–79: Amendments revised
the technical specifications.
Date of initial notice in Federal
Register: October 12, 2004 (69 FR
60687).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated August 18,
2005.
No significant hazards consideration
comments received: No.
Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of application for amendment:
October 27, 2004, as supplemented by
letter dated June 17, 2005.
Brief description of amendment: The
amendment (1) deleted Conditions
2.C.(3), 2.C.(4), 2.C.(6) through 2.C.(14),
Section 2.F, and Attachments 1 and 2,
and (2) revised Conditions 2.C.(1) and
2.C.(5), to the facility operating license,
to reflect completed requirements. In
addition, the list of attachments and
appendices to the operating license was
revised to reflect the deletion of
Attachments 1 and 2. The proposed
E:\FR\FM\08NON1.SGM
08NON1
Federal Register / Vol. 70, No. 215 / Tuesday, November 8, 2005 / Notices
changes to Technical Specifications
Table 5.5.9–2, ‘‘Steam Generator Tube
Inspection,’’ and Table 5.5.9–3, ‘‘Steam
Generator Repaired Tube Inspection,’’
were also submitted in the licensee’s
application dated September 17, 2004
(ULNRC–05056), for the replacement
steam generator project and were
approved in Amendment No. 168,
which was issued in the NRC letter
dated September 29, 2005.
Date of issuance: October 25, 2005.
Effective date: October 25, 2005, and
shall be implemented within 90 days of
the date of issuance.
Amendment No.: 169.
Facility Operating License No. NPF–
30: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: December 7, 2004 (69 FR
70723). The June 17, 2005,
supplemental letter provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
no significant hazards consideration
determination. The Commission’s
related evaluation of the amendment is
contained in a Safety Evaluation dated
October 25, 2005.
No significant hazards consideration
comments received: No.
Dated at Rockville, Maryland, this 31st day
of October, 2005.
For the Nuclear Regulatory Commission.
Ledyard B. Marsh,
Director, Division of Licensing Project
Management, Office of Nuclear Reactor
Regulation.
[FR Doc. 05–22002 Filed 11–7–05; 8:45 am]
BILLING CODE 7590–01–P
NUCLEAR REGULATORY
COMMISSION
Notice of Availability of Interim Staff
Guidance Documents for Fuel Cycle
Facilities
FOR FURTHER INFORMATION CONTACT:
James Smith, Project manager,
Technical Support Group, Division of
Fuel Cycle Safety and Safeguards, Office
of Nuclear Material Safety and
Safeguards, U.S. Nuclear Regulatory
Commission, Washington, DC 20005–
0001. Telephone: (301) 415–6459; fax
number: (301) 415–5370; e-mail:
jas4@nrc.gov.
16:11 Nov 07, 2005
Jkt 208001
III. Further Information
The document related to this action is
available electronically at the NRC’s
Electronic Reading Room at https://
www.nrc.gov/reading-rm/adams.html.
From this site, you can access the NRC’s
Agencywide Documents Access and
Management System (ADAMS), which
provides text and image files of NRC’s
public documents. The ADAMS
ascension number for the document
related to this notice is provided in the
following table. If you do not have
access to ADAMS or if there are
problems in accessing the document
located in ADAMS, contact the NRC
Public Document Room (PDR) Reference
staff at 1–800–397–4209, 301–415–4737,
or by e-mail to pdr@nrc.gov.
ADAMS
Accession No.
FCSS Interim Staff Guidance-08, Revision 0.
Nuclear Regulatory
Commission.
ACTION: Notice of availability.
VerDate Aug<31>2005
II. Summary
The purpose of this notice is to
provide notice to the public of the
issuance of FCSS–ISG–08, Revision 0,
which provides guidance to NRC staff to
address accident sequences that may
result from natural phenomena hazards
relative to license application or
amendment request under 10 CFR Part
70, Subpart H. FCSS–ISG–08, Revision
0, has been approved and issued after a
general revision based on NRC staff and
public comments on the initial draft.
Interim staff guidance
AGENCY:
SUPPLEMENTARY INFORMATION:
I. Introduction
The Nuclear Regulatory Commission
(NRC) continues to prepare and issue
Interim Staff Guidance (ISG) documents
for fuel cycle facilities. These ISG
documents provide clarifying guidance
to the NRC staff when reviewing
licensee integrated safety analysis,
license applications or amendment
requests or other related licensing
activities for fuel cycle facilities under
subpart H of 10 CFR part 70. FCSS–ISG–
08 has been issued and is provided for
information.
ML052650305
This document may also be viewed
electronically on the public computers
located at the NRC’s PDR, O 1 F21, One
White Flint North, 11555 Rockville
Pike, Rockville, MD 20852. The PDR
reproduction contractor will copy
documents for a fee. Comments on these
documents may be forwarded to James
Smith, Project Manager, Technical
Support Group, Division of Fuel Cycle
Safety and Safeguards, Office of Nuclear
Material Safety and Safeguards, U.S.
Nuclear Regulatory Commission,
Washington, DC 20005–0001.
PO 00000
Frm 00100
Fmt 4703
Sfmt 4703
67757
Comments can also be submitted by
telephone, fax, or e-mail which are as
follows: Telephone: (301) 415–6459; fax
number: (301) 415–5370; e-mail:
jas4@nrc.gov.
Dated at Rockville, Maryland this 27th day
of October 2005.
For the Nuclear Regulatory Commission.
Melanie A. Galloway,
Chief, Technical Support Group, Division of
Fuel Cycle Safety and Safeguards, Office of
Nuclear Material Safety and Safeguards.
Attachment—FCSS Interim Staff
Guidance-08, Revision 0, Natural
Phenomena Hazards
Prepared by Division of Fuel Cycle
Safety and Safeguards, Office of
Nuclear Material Safety and Safeguards
Issue
Additional guidance is required to
address accident sequences that may
result from natural phenomena hazards
in the context of a license application or
an amendment request under Title 10
Code of Federal Regulations (10 CFR)
part 70, subpart H.
Introduction
This Interim Staff Guidance (ISG)
provides additional guidance for
reviewing the applicant’s (or licensee’s)
evaluation of natural phenomena
hazards up to and including ‘‘highly
unlikely’’ events for both new and
existing facilities.
Discussion
The performance requirements of 10
CFR 70.61 for facilities processing
special nuclear materials require that
individual accident sequences resulting
in high consequences to workers and
the public be ‘‘highly unlikely’’ and that
sequences resulting in intermediate
consequences to these receptors be
‘‘unlikely.’’ Although the threshold
levels that differentiate high
consequence events from intermediate
consequence events are established in
the regulations, the definitions of
‘‘highly unlikely’’ and ‘‘unlikely’’ are
not. Definitions of these terms must be
described in the integrated safety
analysis (ISA) summary submitted by
applicants and licensees according to 10
CFR 70.65(b)(9) and subjected to staff
approval. Further description of the
acceptance criteria for the definitions of
these terms can be found in Chapter 3
of NUREG–1520, ‘‘Standard Review
Plan for the Review of a License
Application for a Fuel Cycle Facility.’’
The implementation of these
requirements may vary somewhat due to
different definitions of likelihood
proposed by different applicants (or
E:\FR\FM\08NON1.SGM
08NON1
Agencies
[Federal Register Volume 70, Number 215 (Tuesday, November 8, 2005)]
[Notices]
[Pages 67744-67757]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: 05-22002]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from October 14, 2005 to October 27, 2005. The
last biweekly notice was published on October 25, 2005 (70 FR 61655).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The
filing of requests for a hearing and petitions for leave to intervene
is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board
[[Page 67745]]
Panel, will rule on the request and/or petition; and the Secretary or
the Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland, 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
Carolina Power & Light Company, et al., Docket No. 50-400, Shearon
Harris Nuclear Power Plant, Unit 1 (HNP), Wake and Chatham Counties,
North Carolina
Date of amendment request: August 18, 2005.
Description of amendment request: The amendment will allow the use
of fire-resistive electrical cable, which has been demonstrated to
provide an equivalent level of protection as would be provided by 3-
hour and 1-hour rated electrical cable raceway fire barriers, for the
protection of safe shutdown electrical cable.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
Operation of HNP in accordance with the proposed amendment does
not increase the probability or consequences of accidents previously
evaluated. The Final Safety Analysis Report (FSAR) documents the
analyses of design basis accidents (DBA) at HNP. Any scenario or
previously analyzed accidents that result in offsite dose were
evaluated as part of this analysis. The proposed amendment does not
adversely affect accident initiators nor alter design assumptions,
conditions, or configurations of the facility. The proposed
amendment does not adversely affect the ability of structures,
systems, or components (SSCs) to perform their design function. SSCs
required to safely shut down the reactor and to maintain it in a
safe shutdown condition remain capable of performing their design
functions.
The purpose of this amendment is to assure that redundant trains
of safe shutdown (SSD) control circuits remain protected from damage
in the event of a postulated fire. The proposed amendment revises
the Final Safety Analysis Report (FSAR) to use three-hour fire-
resistive electrical cable, which has been demonstrated to provide
an equivalent level of protection as would be provided by three-hour
and one-hour rated electrical cable raceway fire barriers, for the
protection of
[[Page 67746]]
SSD electrical cables. Based on the above, SSD control circuit
protection is maintained by this amendment.
Therefore, this amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
Operation of HNP in accordance with the proposed amendment does
not create the possibility of a new or different kind of accident
from any accident previously evaluated. The FSAR documents the
analyses of design basis accidents (DBA) at HNP. Any scenario or
previously analyzed accidents that result in offsite dose were
evaluated as part of this analysis. The proposed amendment does not
change or affect any accident previously evaluated in the FSAR, and
no new or different scenarios are created by the proposed amendment.
The proposed amendment does not adversely affect accident initiators
nor alter design assumptions, conditions, or configurations of the
facility. The proposed amendment does not adversely affect the
ability of SSCs to perform their design function. SSCs required to
safely shut down the reactor and to maintain it in a safe shutdown
condition remain capable of performing their design functions.
The purpose of this amendment is to assure that redundant trains
of Safe Shutdown (SSD) control circuits remain protected from damage
in the event of a postulated fire. The proposed amendment revises
the Final Safety Analysis Report (FSAR) to use three-hour fire-
resistive electrical cable, which has been demonstrated to provide
an equivalent level of protection as would be provided by three-hour
and one-hour rated electrical cable raceway fire barriers, for the
protection of SSD electrical cables. Based on the above, SSD control
circuit protection is maintained by this amendment.
Therefore, this amendment does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
Operation of HNP in accordance with the proposed amendment does
not involve a significant reduction in a margin of safety. The
proposed amendment does not alter the manner in which safety limits,
limiting safety system settings or limiting conditions for operation
are determined. The safety analysis acceptance criteria are not
affected by this change. The proposed amendment does not adversely
affect existing plant safety margins or the reliability of equipment
assumed to mitigate accidents in the FSAR. The proposed amendment
does not adversely affect the ability of SSCs to perform their
design function. SSCs required to safely shut down the reactor and
to maintain it in a safe shutdown condition remain capable of
performing their design functions.
The purpose of this amendment is to assure that redundant trains
of Safe Shutdown (SSD) control circuits remain protected from damage
in the event of a postulated fire. The proposed amendment revises
the Final Safety Analysis Report (FSAR) to use three-hour fire-
resistive electrical cable, which has been demonstrated to provide
an equivalent level of protection as would be provided by three-hour
and one-hour rated electrical cable raceway fire barriers, for the
protection of SSD electrical cables. Based on the above, SSD control
circuit protection is maintained by this amendment.
Therefore, this amendment does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Section Chief: Michael L. Marshall, Jr.
Carolina Power & Light Company, et al., Docket No. 50-400, Shearon
Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North
Carolina
Date of amendment request: September 1, 2005.
Description of amendment request: The amendment will add Technical
Specification (TS) 3.7.14, ``Fuel Storage Pool Boron Concentration''
and revise TS 5.6, ``Fuel Storage.'' The proposed changes are related
to requirements for ensuring adequate subcriticality margin in the
spent fuel storage pools. TS 5.6.1 is being revised to include the
design requirements for dry storage of new fuel.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes do not modify the facility. The accident
previously analyzed for the spent fuel pool is a fuel handling
accident. The proposed change applies administrative controls for
maintaining the required boron concentration in the spent fuel
storage pools, revises acceptance criteria and storage arrangements
for fuel storage in PWR [pressurized-water reactor] ``flux trap''
style racks and adds acceptance criteria for dry storage of new fuel
to the Technical Specifications. The controls on spent fuel pool
boron and dry storage of new fuel have previously been implemented
but are being added to the Technical Specifications as requirements.
The proposed change applies new acceptance criteria for criticality
safety of fuel storage in PWR ``flux trap'' style racks in Pools
``A'' and ``B.'' The new acceptance criteria require new
administrative controls on the placement of fuel in Pools ``A'' and
``B.'' Similar administrative controls have previously been placed
on fuel stored in Pools C and D. These changes will eliminate the
dependence on Boraflex in the PWR ``flux trap'' style storage racks.
These changes do not impact the probability of having a fuel
handling accident and do not impact the consequences of a fuel
handling accident.
Therefore, this amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
No change is being made to the acceptance criteria of the dry
storage of new fuel. These criteria are being added to Technical
Specification Section 5.6.1. Detailed analyses have been performed
to ensure a criticality accident in Pools ``A'' and ``B'' is not a
credible event. The events that could lead to a criticality accident
are not new. These events include a fuel mis-positioning event, a
fuel drop event, and a boron dilution event. The proposed changes do
not impact the probability of any of these events. The detailed
criticality analyses performed demonstrate that criticality would
not occur following any of these events. For the more likely event,
such as a fuel mis-positioning event, the acceptance criteria for
keff remains less than or equal to 0.95. For the unlikely
event that the spent fuel storage pool boron concentration was
reduced to zero, keff remains less than 1.0.
Therefore, a criticality accident remains ``not credible,'' and
this amendment does not create the possibility of a new or different
kind of accident from any accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
Incorporation of acceptance criteria for dry storage of new fuel
into TS 5.6.1 does not involve a reduction in the margin of safety.
The new fuel storage condition continues to meet keff <=
0.95 during normal conditions and keff <= 0.98 under
optimal moderation conditions.
The proposed changes for storage of new and irradiated fuel in
Pools ``A'' and ``B'' continue to provide the controls necessary to
ensure a criticality event could not occur in the spent fuel storage
spool. The acceptance criteria are consistent with the acceptance
criteria specified in 10 CFR 50.68, which provide an acceptable
margin of safety with regard to the potential for a criticality
event.
Therefore, this amendment does not involve a significant
reduction in a margin of safety.
[[Page 67747]]
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Section Chief: Michael L. Marshall, Jr.
Entergy Nuclear Operations, Inc., Docket No. 50-247, Indian Point
Nuclear Generating Unit No. 2, Westchester County, New York
Date of amendment request: September 26, 2005.
Description of amendment request: The proposed amendment will
revise the analysis method used for the large-break loss-of-coolant
accident (LBLOCA) by incorporating the use of a new approach (ASTRUM)
for the treatment of parameter uncertainties. The new approach is
described in Westinghouse Topical Report WCAP-16009-P-A, approved by
the NRC on November 5, 2004.
Changes to the Technical Specifications to reflect the proposed use
of ASTRUM in LBLOCA analysis consist of revisions to the list of
references provided in Technical Specification Section 5.6.5, Core
Operating Limits Report.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change modifies the analysis methodology used to
account for the variation in parameters that are used for the safety
analysis of the LBLOCA. This proposed change has no effect on the
design or operation of plant equipment. Use of the new methodology
will revise the results of the current analysis, but there will be
no change in initiating events for this accident scenario or the
ability of the plant equipment or plant operators to respond.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change does not involve modifications to existing
plant equipment or the installation of any new equipment. The
proposed change only affects the analysis methodology that is used
to evaluate the response of existing plant equipment to the LBLOCA
scenario. Plant operating and emergency procedures that are in place
for the LBLOCA scenario are also not being changed by this proposed
amendment. This proposed change does not create new failure modes or
malfunctions of plant equipment nor is there a new credible failure
mechanism.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed license amendment revises the analysis methodology
which is used to assess the impact of the LBLOCA scenario with
respect to established acceptance criteria. Margins of safety for
LBLOCA include quantitative limits for fuel performance established
in 10 CFR 50.46. These acceptance criteria and the associated
margins of safety are not being changed. The evaluation of the
LBLOCA scenario, using the proposed new methodology must still meet
the existing established acceptance criteria.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. John Fulton, Assistant General Counsel,
Entergy Nuclear Operations, Inc., 440 Hamilton Avenue, White Plains, NY
10601.
NRC Section Chief: Richard J. Laufer.
Exelon Generation Company, LLC, Docket Nos. 50-237 and 50-249, Dresden
Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
Date of amendment request: April 4, 2005.
Description of amendment request: The proposed amendments would
revise the maximum and minimum allowable values for the degraded
voltage function of the 4160 volt essential service system (ESS) bus
under-voltage instrumentation.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes revise the Technical Specifications (TS)
maximum and minimum allowable values for the degraded voltage
protection function and implement the use of automatic load tap
changers (LTCs) on transformers that provide power to safety-related
equipment. The only accident previously evaluated for which the
probability is potentially affected by these changes is the loss of
offsite power (LOOP). An allowable value for the degraded voltage
protection function that is too high could cause the emergency buses
to transfer to the emergency diesel generators (EDG) and thus
increase the probability of a LOOP. The allowable value for the
degraded voltage protection function has been revised in accordance
with an NRC-approved setpoint methodology and will continue to
ensure that the degraded voltage protection function actuates when
required, but does not actuate prematurely to cause a LOOP.
A failure of an LTC while in automatic operation mode that
results in decreased voltage to the ESS buses could also cause a
LOOP. This could occur in two ways. A failure of the LTC controller
that results in rapidly decreasing the voltage to the emergency
buses is the most severe failure mode. However, a backup controller
is provided with the LTC that makes this failure highly unlikely. A
failure of the LTC controller to respond to decreasing grid voltage
is less severe, since grid voltage changes occur slowly. In both of
the above potential failure modes, operators will take manual
control of the LTC to mitigate the effects of the failure. Thus, the
probability of a LOOP is not significantly increased.
The proposed changes will have no effect on the consequences of
a LOOP, since the EDGs provide power to safety related equipment
following a LOOP. The EDGs are not affected by the proposed changes.
The probability of other accidents previously evaluated is not
affected, since the proposed changes do not affect the way plant
equipment is operated and thus do not contribute to the initiation
of any of the previously evaluated accidents. The only way in which
the consequences of other previously evaluated accidents could be
affected is if a failure of the LTC while in automatic operation
mode caused a sustained high voltage which resulted in damage to
safety related equipment that is used to mitigate an accident.
Damage due to over-voltage is time-dependent. Since the LTC is
equipped with a backup controller, and since operator action is
available to prevent a sustained high voltage condition from
occurring, damage to safety related equipment is extremely unlikely,
and thus the consequences of these accidents are not significantly
increased.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of
[[Page 67748]]
accident from any accident previously evaluated?
Response: No.
The proposed changes involve functions that provide offsite
power to safety related equipment for accident mitigation. Thus, the
proposed changes potentially affect the consequences of previously
evaluated accidents (as addressed in Question 1), but do not result
in any new mechanisms that could initiate damage to the reactor and
its principal safety barriers (i.e., fuel cladding, reactor coolant
system, or primary containment).
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed changes do not affect the inputs or assumptions of
any of the analyses that demonstrate the integrity of the fuel
cladding, reactor coolant system, or containment during accident
conditions. The allowable values for the degraded voltage protection
function have been revised in accordance with an NRC-approved
setpoint methodology and will continue to ensure that the degraded
voltage protection function actuates when required, but does not
actuate prematurely to cause a LOOP. Automatic operation of the LTC
increases margin by reducing the potential for transferring to the
EDGs during an event.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Thomas S. O'Neill, Associate General
Counsel, Exelon Generation Company, LLC, 4300 Winfield Road,
Warrenville, IL 60555.
NRC Section Chief: Gene Y. Suh.
FPL Energy Seabrook, LLC, Docket No. 50-443, Seabrook Station, Unit No.
1, Rockingham County, New Hampshire
Date of amendment request: September 22, 2005.
Description of amendment request: The proposed amendment would
revise the Seabrook Station, Unit No. 1 operating license and Technical
Specifications to increase the licensed rated power level by 1.7
percent from 3587 megawatts thermal (MWt) to 3648 MWt. Basis for
proposed no significant hazards consideration determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
1. The proposed change will not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
Seabrook Station performed evaluations of the Nuclear Steam
Supply System (NSSS) and balance of plant systems, components, and
analyses that could be affected by the proposed change. A power
uncertainty calculation was performed, and the effect of increase
core thermal power by 1.7 percent to 3648 MWt on the Seabrook
Station design and licensing basis was evaluated. The result of the
evaluations determined that all systems and components continue to
be capable of performing their design function at the MUR
[measurement uncertainty recapture] core power level of 3648 MWt. An
evaluation of the accident analyses demonstrates that the applicable
analyses acceptance criteria continue to be met. No accident
initiators are affected by the MUR power uprate and no challenges to
any plant safety barriers are created by the proposed change.
The proposed change does not affect the release paths, the
frequency of release, or the analyzed source term for any accidents
previously evaluated in the Seabrook Station Updated Final Safety
Analysis Report (UFSAR). Systems, structures, and components
required to mitigate transients continue to be capable of performing
their design functions, and thus were found acceptable. The reduced
uncertainty in the feedwater flow input to the power calorimetric
measurement ensures that applicable accident analyses acceptance
criteria continue to be met, to support operation at the MUR core
power level of 3648 MWt. Analyses performed to assess the effects of
mass and energy remain valid. The source term used to assess
radiological consequences [has] been reviewed and determined to
bound operation at the MUR core power level.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. The proposed change will not create the possibility of a new
or different kind of accident from any accident previously
evaluated.
No new accident scenarios, failure mechanisms, or single
failures are introduced as a result of the proposed change. The
installation of the Caldon LEFM CheckPlusTM System has
been analyzed, and failures of the system will have no adverse
effect on any safety-related system or any systems, structures, and
components required for transient mitigation. Systems, structures,
and components previously required for the mitigation of a transient
continue to be capable of fulfilling their intended design
functions. The proposed change has no adverse affect on any safety-
related system or component and does not change the performance or
integrity of any safety-related system.
The proposed change does not adversely affect any current system
interfaces or create any new interfaces that could result in an
accident or malfunction of a different kind than previously
evaluated. Operating at a core power level of 3648 MWt does not
create any new accident initiators or precursors. The reduced
uncertainty in the feedwater flow input to the power calorimetric
measurement ensures that applicable accident analyses acceptance
criteria continue to be met, to support operation at the MUR core
power level of 3648 MWt. Credible malfunctions continue to be
bounded by the current accident analyses of record or evaluations
that demonstrate that applicable criteria continue to be met.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. The proposed change will not involve a significant reduction
in a margin [of] safety.
The margins of safety associated with the MUR are those
pertaining to core thermal power. These include those associated
with the fuel cladding, Reactor Coolant System pressure boundary,
and containment barriers. An engineering evaluation of the 1.7
percent increase in core thermal power from 3587 MWt to 3648 MWt was
performed. The current licensing bases analyzed core power is 3659
MWt. The analyzed core power level of 3659 MWt bounds the NSSS
thermal and hydraulic parameters at the MUR core power level of 3648
MWt. The NSSS systems and components were evaluated at the MUR core
power level and it was determined that the NSSS systems and
components continue to operate satisfactorily at the MUR power
level. The NSSS accident analyses were evaluated at the MUR core
power level of 3648 MWt. In all cases, the accident analyses at the
MUR core power level of 3648 MWt were bounded by the current
licensing bases analyzed core power level of 3659 MWt. As such, the
margins of safety continue to be bounded by the current analyses of
record for this change.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: M. S. Ross, Florida Power & Light Company,
P.O. Box 14000, Juno Beach, FL 33408-0420.
NRC Section Chief: Darrell J. Roberts.
FPL Energy Seabrook, LLC, Docket No. 50-443, Seabrook Station, Unit No.
1, Rockingham County, New Hampshire
Date of amendment request: September 29, 2005.
Description of amendment request: The proposed amendment would
revise the Seabrook Station, Unit No. 1, Technical Specifications (TSs)
to permit a one-time, six-month extension to the currently approved 15-
year test interval for the containment integrated leak rate test.
Basis for proposed no significant hazards consideration
determination:
[[Page 67749]]
As required by 10 CFR 50.91(a), the licensee has provided its analysis
of the issue of no significant hazards consideration, which is
presented below:
1. The proposed change [does] not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
The probability or consequences of accidents previously
evaluated in the UFSAR [updated final safety analysis report] are
unaffected by this proposed change. There is no change to any
equipment response or accident mitigation scenario, and this change
results in no additional challenges to fission product barrier
integrity. The proposed change does not alter the design,
configuration, operation, or function of any plant system,
structure, or component. As a result, the outcomes of previously
evaluated accidents are unaffected. The proposed extension to the
containment integrated leak rate test (ILRT) interval does not
involve a significant increase in consequences because, as discussed
in NUREG 1493, Performance Based Containment Leak Rate Test Program,
Type B and C tests identify the vast majority (greater than 95
percent) of all potential leakage paths. Further, ILRTs identify
only a few potential leakage paths that cannot be identified through
Type B and C testing, and leaks found by Type A testing have been
only marginally greater than existing requirements. In addition,
periodic inspections ensure that any significant containment
degradation will not go undetected. Therefore, the proposed change
does not involve a significant increase in the probability or
consequences of an accident previously evaluated.
2. The proposed change [does] not create the possibility of a
new or different kind of accident from any [accident] previously
evaluated.
No new accident scenarios, failure mechanisms, or limiting
single failures are introduced as a result of the proposed change.
The proposed change does not challenge the performance or integrity
of any safety-related system. The proposed change neither installs
or removes any plant equipment, nor alters the design, physical
configuration, or mode of operation of any plant structure, system,
or component. No physical changes are being made to the plant, so no
new accident causal mechanisms are being introduced. The proposed
change only changes the frequency of performing the ILRT; however,
the test implementation and acceptance criteria are unchanged.
Therefore, the proposed change does not create the possibility of a
new or different kind of accident from any previously evaluated.
3. The proposed change [does] not involve a significant
reduction in a margin of safety.
The margin of safety associated with the acceptance criteria of
any accident is unchanged. The proposed change will have no affect
on the availability, operability, or performance of the safety-
related systems and components. The proposed change does not alter
the design, configuration, operation, or function of any plant
system, structure, or component. The ability of any operable
structure, system, or component to perform its designated safety
function is unaffected by this change. NUREG 1493 concluded that
reducing the frequency of ILRTs to 20 years resulted in an
imperceptible increase in risk. Also, inspections of containment,
required by the ASME code [American Society of Mechanical Engineers
Boiler and Pressure Vessel Code] and the maintenance rule, ensure
that containment will not degrade in a manner that is only
detectable by Type A (ILRT) testing. Therefore, the margin of safety
as defined in the TS is not reduced and the proposed change does not
involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: M. S. Ross, Florida Power & Light Company,
P.O. Box 14000, Juno Beach, FL 33408-0420.
NRC Section Chief: Darrell J. Roberts.
FPL Energy Seabrook, LLC, Docket No. 50-443, Seabrook Station, Unit No.
1, Rockingham County, New Hampshire
Date of amendment request: September 29, 2005.
Description of amendment request: The proposed amendment would
revise the Seabrook Station, Unit No. 1 Technical Specifications to
permit a change in the steam generator tube inspection requirements to
include a sampling of the bulges and over-expansions for portions of
the steam generator tubes within the hot leg tubesheet region.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed changes do not involve a significant increase in
the probability or consequences of an accident previously evaluated.
The previously analyzed accidents are initiated by the failure
of plant structures, systems, or components. The proposed changes
that alter the steam generator inspection criteria do not have a
detrimental impact on the integrity of any plant structure, system,
or component that initiates an analyzed event. The proposed changes
will not alter the operation of, or otherwise increase the failure
probability of any plant equipment that initiates an analyzed
accident.
Of the applicable accidents previously evaluated, the limiting
transients with consideration to the proposed changes to the steam
generator tube inspection criteria, are the steam generator tube
rupture (SGTR) event and the steam line break (SLB) accident.
During the SGTR event, the required structural integrity margins
of the steam generator tubes will be maintained by the presence of
the steam generator tubesheet area. Tube rupture in tubes with
cracks in the tubesheet is precluded by the constraint provided by
the tubesheet. This constraint results from the hydraulic expansion
process, thermal expansion mismatch between the tube and tubesheet
and from the differential pressure between the primary and secondary
side. Based on this design, the structural margins against burst, as
discussed in Regulatory Guide (RG) 1.121, ``Bases for Plugging
Degraded PWR [pressurized-water reactor] Steam Generator Tubes,''
are maintained for both normal and postulated accident conditions.
At normal operating pressures, leakage from primary water stress
corrosion cracking (PWSCC) below the proposed limited inspection
depth is limited by both the tube-to-tubesheet crevice and the
limited crack opening permitted by the tubesheet constraint.
Consequently, negligible normal operating leakage is expected from
cracks within the tubesheet region. The consequences of an SGTR
event are affected by the primary-to-secondary leakage flow during
the event. Primary-to-secondary leakage flow through a postulated
ruptured tube is not affected by the proposed changes since the
tubesheet enhances the tube integrity in the region of the hydraulic
expansion by precluding tube deformation beyond its initial
hydraulically-expanded outside diameter.
Furthermore, the proposed changes do not affect other systems,
structures, components or operational features. Therefore, the
proposed changes result in no significant increase in the
probability of the occurrence of a SGTR accident.
The probability of a[n] SLB accident is unaffected by the
potential failure of a steam generator tube as this failure is not
an initiator for a[n] SLB accident.
The consequences of a[n] SLB accident are also not significantly
affected by the proposed changes. During a[n] SLB accident, the
reduction in pressure above the tubesheet on the shell side of the
steam generator creates an axially uniformly distributed load on the
tubesheet due to the reactor coolant system pressure on the
underside of the tubesheet. The resulting bending action constrains
the tubes in the tubesheet thereby restricting primary-to-secondary
leakage below the midplane.
Primary-to-secondary leakage from tube degradation in the
tubesheet area during the limiting accident (i.e., a[n] SLB) is
limited by flow restrictions resulting from the crack and tube-to-
tubesheet contact pressures that provide a restricted leakage path
above the indications and also limit the degree of potential crack
face opening as compared to free span indications. The primary-to-
secondary leak rate during postulated SLB accident conditions would
be expected to be less than that during normal operation for
indications near the bottom of the tubesheet (i.e., including
indications in the tube end welds). This conclusion is based on the
[[Page 67750]]
observation that while the driving pressure causing leakage
increases by approximately a factor of (two) 2, the flow resistance
associated with an increase in tube-to-tubesheet contact pressure,
during a[n] SLB accident, increases by approximately a factor of
2.5. While such a leakage decrease is logically expected, the
postulated accident leak rate could be conservatively bounded by
twice the normal operating leak rate even if the increase in contact
pressure is ignored. Since normal operating leakage (spiking) is
limited to less that 0.104 gpm (150 gpd) for continued power
operation per station operating procedure OS 1227.02, ``Steam
Generator Tube Leak,'' the associated accident condition leak rate,
assuming all leakage to be from lower tube sheet indications, would
be bound by 0.208 gpm (twice normal operating leak rate). This value
is well within the assumed accident leakage rate of 0.347 gpm
discussed in the Seabrook Station Updated Safety Analysis Report,
Section 15.1.5 ``Steam System Piping Failure.'' Hence it is
reasonable to omit any consideration of inspection of the tube, tube
end weld, bulges / overexpansions or other anomalies below 17 inches
from the top of the hot leg tubesheet. Therefore, the consequences
of a[n] SLB accident remain unaffected.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. The proposed changes do not create the possibility of a new
or different kind of accident from any [accident] previously
evaluated.
The proposed changes do not introduce any new equipment, create
new failure modes for existing equipment, or create any new limiting
single failures. Plant operation will not be altered, and all safety
functions will continue to perform as previously assumed in accident
analyses. Therefore, the proposed changes do not create the
possibility of a new or different kind of accident from any
previously evaluated.
3. The proposed changes do not involve a significant reduction
in the margin of safety.
The proposed changes maintain the required structural margins of
the steam generator tubes for both normal and accident conditions.
Nuclear Energy Institute (NEI) 97-06, ``Steam Generator Program
Guidelines,'' and NRC Regulatory Guide (RG) 1.121, ``Bases for
Plugging Degraded PWR Steam Generator Tubes,'' are used as the bases
in the development of the limited hot leg tubesheet inspection depth
methodology for determining that steam generator tube integrity
considerations are maintained within acceptable limits. RG 1.121
describes a method acceptable to the NRC for meeting General Design
Criteria (GDC) 14, ``Reactor Coolant Pressure Boundary,'' GDC 15,
``Reactor Coolant System Design,'' GDC 31, ``Fracture Prevention of
Reactor Coolant Pressure Boundary,'' and GDC 32, ``Inspection of
Reactor Coolant Pressure Boundary,'' by reducing the probability and
consequences of a SGTR. RG 1.121 concludes that by determining the
limiting safe conditions for tube wall degradation the probability
and consequences of a SGTR are reduced. RG 1.121 uses safety factors
on loads for tube burst that are consistent with the requirements of
Section III of the American Society of Mechanical Engineers (ASME)
Code.
For axially oriented cracking located within the tubesheet, tube
burst is precluded due to the presence of the tubesheet. For
circumferentially oriented cracking, Westinghouse evaluation LTR-
CDME-05-170, ``Limited Inspection of the Steam Generator Tube
Portion Within the Tubesheet at Seabrook Generating Station,''
defines a length of degradation-free expanded tubing that provides
the necessary resistance to tube pullout due to the pressure induced
forces, with applicable safety factors applied. Application of the
limited hot leg tubesheet inspection criteria will preclude
unacceptable primary-to-secondary leakage during all plant
conditions. The methodology for determining leakage provides for
large margins between calculated and actual leakage values in the
proposed limited hot leg tubesheet inspection depth criteria.
Therefore, the proposed changes do not involve a significant
reduction in any margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: M. S. Ross, Florida Power & Light Company,
P.O. Box 14000, Juno Beach, FL 33408-0420.
NRC Section Chief: Darrell J. Roberts.
Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 50-
364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County,
Alabama
Date of amendment request: September 27, 2005.
Description of amendment request: The amendments proposed by
Southern Nuclear Operating Company would revise the Technical
Specifications (TS) to eliminate the Power Range Neutron Flux-High
Negative Rate Reactor Trip function, based on the approved methodology
contained in Westinghouse Topical Report WCAP-11394-P-A, ``Methodology
for the Analysis of the Dropped Rod Event.'' The changes will allow the
elimination of a trip circuitry that is not credited in the Farley
Nuclear Plant safety analysis, and which can result in an unnecessary
reactor trip. These changes will be implemented sequentially,
concurrent with each unit's refueling outage during which the design
change is implemented. Additionally, this amendment request deletes TS
Bases text associated with an unconservative local Departure from
Nucleate Boiling Ratio.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
No. The proposed changes do not significantly increase the
probability or consequences of an accident previously evaluated in
the Updated Final Safety Analysis Report (UFSAR). All of the safety
analyses have been evaluated for impact due to this change. The
elimination of the Power Range Neutron Flux-High Negative Rate
Reactor Trip function and the elimination of text in the TS
[Technical Specifications] Bases for LC0 3.3.1, page B 3.3.1-1 1,
associated with an unconservative local DNBR [departure from
nucleate boiling ratio], does not affect the dropped RCCA [Rod
Cluster Control Assembly] analyses nor any other analyses, since it
is not credited in any of the safety analyses; therefore, the
probability of an accident has not been increased. All dose
consequences have been evaluated with respect to the proposed
changes, there is no impact due to the proposed change, and all
acceptance criteria continue to be met. Therefore, these changes do
not involve a significant increase in the probability or
consequences of an accident previously evaluated.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any previously evaluated?
No. The proposed changes do not create the possibility of a new
or different kind of accident from any accident already evaluated in
the UFSAR. No new accident scenarios, failure mechanisms or limiting
single failures are introduced as result of the proposed changes.
The changes have no adverse effects on any safety-related system.
Therefore, all accident analyses criteria continue to be met and
these changes do not create the possibility of a new or different
kind of accident from any accident previously evaluated.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
No. The proposed changes do not involve a significant reduction
in a margin of safety. The dropped RCCA(s) event does not credit the
Power Range Neutron Flux-High Negative Rate Reactor Trip function.
The conclusion presented in the UFSAR Section 15.2.3.3 that the DNBR
design basis is met for a dropped RCCA(s) event remains valid for
the proposed changes, which are based on the NRC approved
methodology contained in CAP-11394-PA. Additionally, WCAP-11394-P-A
indicates that the analysis for a dropped rod event envelops a
multiple rod drop accident at high power levels, and that such an
accident will not result in an unconservative local DNBR. All
applicable acceptance criteria continue to be met. Therefore, the
proposed changes do not involve a significant reduction in a margin
of safety.
[[Page 67751]]
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: M. Stanford Blanton, Esq., Balch and
Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham,
Alabama 35201.
NRC Section Chief: Evangelos C. Marinos.
Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 50-
364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County,
Alabama
Date of amendment request: October 6, 2005.
Description of amendment request: The amendments proposed by
Southern Nuclear Operating Company (SNC) would revise the Technical
Specifications (TS) to support a revision to the Best Estimate Loss of
Coolant Accident (BELOCA) for Farley Nuclear Plant (FNP). The NRC
recently approved a new Westinghouse BELOCA methodology, Automated
Statistical Treatment of Uncertainty Method (ASTRUM). ASTRUM was
submitted in WCAP-16009-P. The NRC issued a Safety Evaluation Report in
a letter dated November 5, 2004. Westinghouse issued WCAP-16009-P-A in
January 2005. SNC has completed the analysis for FNP and the enclosed
proposed amendment is to incorporate a reference to WCAP-16009-P-A in
TS section 5.6.5 Core Operating Limits Report (COLR).
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
No physical plant changes are being made as a result of using
the Westinghouse Best Estimate Large Break LOCA [Loss of Coolant
Accident] (BELOCA) analysis methodology. The proposed TS changes
simply involve updating the references in TS 5.6.5.b, Core Operating
Limits Report (COLR), to reference the Westinghouse BELOCA analysis
methodology. The plant conditions assumed in the analysis are
bounded by the design conditions for all equipment in the plant;
therefore, there will be no increase in the probability of a LOCA.
The consequences of a LOCA are not being increased, since the
analysis has shown that the Emergency Core Cooling System (ECCS) is
designed such that its calculated cooling performance conforms to
the criteria contained in 10 CFR 50.46, ``Acceptance criteria for
emergency core cooling systems for light-water nuclear power
reactors.'' No other accident consequence is potentially affected by
this change.
All systems will continue to be operated in accordance with
current design requirements under the new analysis, therefore no new
components or system interactions have been identified that could
lead to an increase in the probability of any accident previously
evaluated in the Updated Final Safety Analysis Report (UFSAR). No
changes were required to the Reactor Protection System (RPS) or
Engineering Safety Features (ESF) setpoints because of the new
analysis methodology.
Therefore, it is concluded that this change does not
significantly increase the probability or consequences of an
accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
There are no physical changes being made to the plant as a
result of using the Westinghouse Best Estimate Large Break LOCA
analysis methodology. No new modes of plant operation are being
introduced. The configuration, operation and accident response of
the structures or components are unchanged by utilization of the new
analysis methodology. Analyses of transient events have confirmed
that no transient event results in a new sequence of events that
could lead to a new accident scenario. The parameters assumed in the
analysis are within the design limits of existing plant equipment.
In addition, employing the Westinghouse Best Estimate Large
Break LOCA analysis methodology does not create any new failure
modes that could lead to a different kind of accident. The design of
all systems remains unchanged and no new equipment or systems have
been installed which could potentially introduce new failure modes
or accident sequences. No changes have been made to any RPS or ESF
actuation setpoints.
Based on this review, it is concluded that no new accident
scenarios, failure mechanisms or limiting single failures are
introduced as a result of the proposed changes.
Therefore, the proposed TS changes do not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
It has been shown that the analytic technique used in the
Westinghouse Best Estimate Large Break LOCA analysis methodology
realistically describes the expected behavior of the reactor system
during a postulated LOCA. Uncertainties have been accounted for as
required by 10 CFR 50.46. A sufficient number of LOCAs with
different break sizes, different locations, and other variations in
properties have been considered to provide assurance that the most
severe postulated LOCAs have been evaluated. The analysis has
demonstrated that all acceptance criteria contained in 10 CFR 50.46
paragraph b continue to be satisfied.
Therefore, it is concluded that this change does not involve a
significant reduction in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: M. Stanford Blanton, Esq., Balch and
Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham,
Alabama 35201.
NRC Section Chief: Evangelos C. Marino.
Southern Nuclear Operating Company, Inc., Docket Nos. 50-424 and 50-
425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County,
Georgia
Date of amendment request: January 27, 2005.
Description of amendment request: The proposed amendments would
revise Technical Specifications Limiting Conditions for Operations
3.3.1, 3.3.2, 3.3.6, and 3.3.8, by extending the Surveillance Test
Intervals for the Reactor Protection System.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the Proposed Change Involve a Significant Increase in
the Probability or Consequences of an Accident Previously Evaluated?
The proposed changes to the Completion Time, bypass test time,
and Surveillance Frequencies reduce the potential for inadvertent
reactor trips and spurious actuations and, therefore, do not
increase the probability of any accident previously evaluated. The
proposed changes to the allowed Completion Time, bypass test time,
and Surveillance Frequencies do not change the response of the plant
to any accidents and have an insignificant impact on the reliability
of the reactor trip system and engineered safety feature actuation
system (RTS and ESFAS) signals. The RTS and ESFAS will remain highly
reliable, and the proposed changes will not result in a significant
increase in the risk of plant operation. This is demonstrated by
showing that the impact on plant safety as measured by core damage
frequency (CDF) is less than 1.01E-06 per year and the impact on
large early release frequency (LERF) is less than 1.0E-07 per year.
In addition, for the Completion Time change, the incremental
conditional core damage probabilities (ICCDP) and incremental
conditional large early release probabilities (ICLERP) are less than
5.0E-08. These changes meet the
[[Page 67752]]
acceptance criteria in Regulatory Guides 1.174 and 1.177. Therefore,
since the RTS and ESFAS will continue to perform their functions
with high reliability as originally assumed, and the increase in
risk a