Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 61655-61669 [05-21180]
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Federal Register / Vol. 70, No. 205 / Tuesday, October 25, 2005 / Notices
This notice is distributed by mail to
several hundred subscribers; if you no
longer wish to receive it, or would like
to be added to the distribution, please
contact the Office of the Secretary,
Washington, DC 20555 (301) 415–1969.
In addition, distribution of this meeting
notice over the Internet system is
available. If you are interested in
receiving this Commission meeting
schedule electronically, please send an
electronic message to dkw@nrc.gov.
Dated: October 20, 2005.
R. Michelle Schroll,
Office of the Secretary.
[FR Doc. 05–21337 Filed 10–21–05; 9:54 am]
BILLING CODE 7590–01–M
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from September
30 to October 13, 2005. The last
biweekly notice was published on
October 11, 2005 (70 FR 59082).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
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create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
PO 00000
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61655
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
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Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
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Pike, Rockville, Maryland 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(I)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
Dominion Nuclear Connecticut Inc., et
al., Docket No. 50–423, Millstone Power
Station, Unit No. 3, New London
County, Connecticut
Date of amendment request:
September 13, 2005.
Description of amendment request:
The amendment would reduce the
temperature at which shutdown and
control rod cluster control assemblies
(RCCA) drop testing is done from greater
than or equal to 551 °Fahrenheit (F) to
greater than or equal to 500 °F.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
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issue of no significant hazards
consideration, which is presented
below:
Criterion 1: Does the proposed
amendment involve a significant
increase in the probability or
consequences of an accident previously
evaluated?
Response: No. DNC [Dominion
Nuclear Connecticut, Inc.] is proposing
to change the temperature at which the
shutdown and control RCCA drop tests
are performed from ‘‘greater than or
equal to 551 °F,’’ to ‘‘greater than or
equal to 500 °F.’’ The proposed change
does not modify any plant equipment
and does not impact any failure modes
that could lead to an accident.
Additionally, the proposed change has
no effect on the consequence of any
analyzed accident since the change does
not affect the function of any equipment
credited for accident mitigation. Based
on this discussion, the proposed
amendment does not increase the
probability or consequences of an
accident previously evaluated.
Criterion 2: Does the proposed
amendment create the possibility of a
new or different kind of accident from
any accident previously evaluated?
Response: No. The proposed change
does not modify any plant equipment
and there is no impact on the capability
of existing equipment to perform its
intended functions. No system setpoints
are being modified and no changes are
being made to the method in which
plant operations are conducted. No new
failure modes are introduced by the
proposed change. The proposed
amendment does not introduce accident
initiators or malfunctions that would
cause a new or different kind of
accident.
As noted above, the proposed change
does not affect the revisions to plant
procedures, which were made to
address Westinghouse Nuclear Safety
Advisory Letter, NSAL–00–016 (Rod
Withdrawal from Subcritical Protection
in Lower Modes, issued in 2000).
Therefore, the proposed amendment
does not create the possibility of a new
or different kind of accident from any
accident previously evaluated.
Criterion 3: Does the proposed
amendment involve a significant
reduction in a margin of safety?
Response: No. The TS [technical
specification] change does not involve a
significant reduction in margin because
the acceptance criterion for the RCCA
drop time will not change. The
proposed change will reduce the
minimum RCCA drop test temperature
from greater than or equal to 551 °F to
greater than or equal to 500 °F. This will
slightly increase the measured test
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RCCA drop time. However, the
measured test RCCA drop time is
required to remain within the current
TS limit of 2.7 seconds and the 2.19
seconds for surveillance testing
acceptance criteria (plant specific
seismic allowance of 0.51 seconds). The
proposed change does not affect any of
the assumptions used in the accident
analysis, nor does it affect any
operability requirements for equipment
important to plant safety. Therefore, the
margin of safety is not impacted by the
proposed amendment.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Lillian M.
Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc.,
Waterford, CT 06141–5127.
NRC Section Chief: Darrell J. Roberts.
Dominion Nuclear Connecticut Inc., et
al., Docket No. 50–423, Millstone Power
Station, Unit No. 3, New London
County, Connecticut
Date of amendment request:
September 13, 2005.
Description of amendment request:
The changes revise surveillance
requirements for the recirculation spray
system (RSS) to verify proper initiation
of recirculation spray through actuation
by the refueling water storage tank
(RWST) low-low level signal instead of
actuation by a timer.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
Criterion 1: Does the proposed
amendment involve a significant
increase in the probability or
consequences of an accident previously
evaluated?
Response: No. The RSS is only an
accident mitigation system. As such,
changes in the operation of RSS cannot
have an impact on the probability of an
accident. The delay in the start of the
RSS pump is to assure there is sufficient
water in the containment sump for
adequate RSS pump NPSH [net positive
suction head] and margin to suction
pipe flashing in light of the debris
analysis conducted in response to GL
[Generic Letter] 2004–02. Containment
analyses have been performed to
demonstrate that there is no impact on
the peak containment pressure and
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temperature following a LOCA [loss-ofcoolant accident]. While there are some
changes in the predicted post-LOCA
environmental conditions, evaluations
have been performed to show that there
is no significant impact on the
environmental qualification for
equipment inside containment. The
impact to piping and supports has been
demonstrated to be acceptable without
modification. Delay in RSS spray start
will result in a reduction in diesel
generator loading since the RSS pumps
and the RHS pumps will no longer be
running concurrently. The reduction in
iodine removal efficiency during the
delay period is more than offset by
elimination of over-conservatisms in
assumptions for long term iodine
removal by the RSS system. The net
impact is a reduction in the predicted
offsite doses and control room doses
following a design basis LOCA. Based
on this discussion, the proposed
amendment does not increase the
probability or consequence of an
accident previously evaluated.
Criterion 2: Does the proposed
amendment create the possibility of a
new or different kind of accident from
any accident previously evaluated?
Response: No. The proposed
modification alters the RSS pump
circuitry by initiating the start sequence
with an existing RWST low-low level
signal instead of a timer. The timer is
now used to sequence pump starts. The
pump function is not changed in any
way. The proposed amendment does not
introduce failure modes, accident
initiators, or malfunctions that would
cause a new or different kind of
accident. Therefore, the proposed
amendment does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
Criterion 3: Does the proposed
amendment involve a significant
reduction in a margin of safety?
Response: No. The proposed change
ensures that adequate margin to suction
line flashing and NPSH margin exists
for proper operation of the RSS pumps
once the effects of debris are considered
as required per GL 2004–02. Function of
the pumps is not affected. Analyses
have been performed that show the
containment design basis limits are
satisfied and the post-LOCA offsite and
control room doses meet the required
criteria. Therefore, based on the above,
the proposed amendment does not
involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
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satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Lillian M.
Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc.,
Waterford, CT 06141–5127.
NRC Section Chief: Darrell J. Roberts.
Duke Energy Corporation, et al., Docket
Nos. 50–369 and 50–370, McGuire
Nuclear Station, Units 1 and 2,
Mecklenburg County, North Carolina
and Docket Nos. 50–413 and 50–414,
Catawba Nuclear Station, Units 1 and 2,
York County, South Carolina
Date of amendment request: June 29,
2005.
Description of amendment request:
The amendment would revise Technical
Specification Bases Section 3.6.11, ‘‘Air
Return System (ARS),’’ and the Updated
Final Safety Analysis Reports (UFSAR),
Section 6.2, ‘‘Containment Systems,’’ for
McGuire Nuclear Station, Units 1 and 2
and Catawba Nuclear Station, Units 1
and 2. The licensee proposes to
implement an additional manual
operator action to respond to NRC
Bulletin 2003–01, ‘‘Potential Impact of
Debris Blockage on Emergency Sump
Recirculation at Pressurized-Water
Reactors.’’ This amendment would
allow plant operators to manually start
one air return fan at a containment
pressure of 1 psig prior to the automatic
9 minutes (+ 1 minute) delayed start
described in the UFSAR.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
First Standard
Does the change involve a significant
increase in the probability or
consequences of an accident previously
evaluated?
No. The manual start of an Air Return
System (ARS) fan will not result in a
significant increase in the probability of
an accident previously evaluated. The
starting of an ARS fan is not considered
to be an initiator of any accident or
transient. This action is not taken
during normal plant operation, but in
response to an accident. The ARS fans
do not operate to provide any normal
ventilation requirement. The
Containment Pressure Control System
(CPCS) is provided to prevent excessive
depressurization of the containment
through inadvertent or excessive
operation of certain engineered safety
features. The CPCS prevents the
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inadvertent actuation of an ARS fan
during normal operation.
This change is being requested in
order to mitigate the consequences of a
small break loss of coolant accident
(SBLOCA) and help prevent or delay
reaching the initiation pressure setpoint
for containment spray, thereby reducing
associated problems with possible sump
debris buildup. SBLOCA events are
bounded by the consequences of a
design basis large break [loss of coolant
accident] LOCA as addressed in Section
15 of the McGuire and Catawba
[Updated Final Safety Analysis Report]
UFSARs. Accordingly, this amendment
will not involve a significant increase in
the consequences of an accident
previously evaluated.
Second Standard
Does the change create the possibility
of a new or different kind of accident
from any accident previously evaluated?
No. The change proposed in this
[license amendment request] LAR does
not involve a physical alteration to the
plant (i.e., no new or different type of
equipment will be installed) or a change
in the methods governing any normal
plant operation. It does allow for the
early start of one ARS fan during a
SBLOCA event with containment
pressure greater than 1 psig and less
than 3 psig. This change will not affect
or degrade the ability of the ARS to
perform its specified safety functions.
Accidents of a different type are
credible accidents that the proposed
amendment could create that are not
bounded by UFSAR evaluated
accidents. This amendment allows for
the manual start of an ARS fan
following a SBLOCA within the
containment. No new failure modes are
introduced due to the manual start of an
ARS fan. The circuit used to manually
start an ARS fan does not interfere with
the automatic signal to start an ARS fan.
This change does not require any
modifications to the control circuitry for
the ARS. The starting of an ARS fan is
not considered to be an initiator of any
accident or transient. This action
(starting of an ARS fan) is not taken
during normal operation, but in
response to an accident. Previous
accidents considered incredible are not
made more likely by this change. A
human performance error, such as
starting the ARS fan too early, too late,
or not at all, would not result in a
substantial difference in the calculated
differential pressure across the divider
deck. Since no new malfunctions of
equipment with a different result are
introduced, all effects of any
malfunctions are bounded by those
already evaluated in the UFSAR. Thus
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it is concluded that the change
contained in this LAR will not create
the possibility of a new or different kind
of accident from any accident
previously evaluated.
Third Standard
Does the proposed change involve a
significant reduction in a margin of
safety?
No. The early manual start of an ARS
fan for SBLOCA events will not reduce
the ability of this system to perform its
design functions to assure the rapid
return of air from the upper to the lower
containment compartment after the
initial blowdown following a Design
Basis Accident (DBA). The return of this
air to the lower compartment and
subsequent recirculation back up
through the ice condenser assists in
cooling the containment atmosphere
and limiting post accident pressure and
temperature in containment to less than
design values. Limiting pressure and
temperature also reduces the release of
fission product radioactivity from
containment to the environment in the
event of a DBA. Therefore, there are no
adverse dose effects from the early start
of the ARS fan or from the delay of
containment spray based on the current
licensing basis.
Analyses have shown that there will
be no fan or damper malfunction due to
the early manual start of a fan. The other
functions of the system are not affected
by the change proposed in this LAR.
The manual start of the ARS during a
SBLOCA will help maintain the margin
of safety by forcing air and steam
through the ice condenser with a
subsequent reduction in the rate of
pressure increase in the containment,
and a delay in reaching the actuation
setpoint for the containment spray
system. The containment spray system
will continue to be initiated at the
normal setpoint pressure of the system
(-3 psig). Therefore, the proposed
changes listed above do not involve a
significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Ms. Lisa F.
Vaughn, Legal Department (PB05E),
Duke Energy Corporation, 422 South
Church Street, Charlotte, North Carolina
28201–1006.
NRC Section Chief: Evangelos C.
Marinos.
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Entergy Operations, Inc., System Energy
Resources, Inc., South Mississippi
Electric Power Association, and Entergy
Mississippi, Inc., Docket No. 50–416,
Grand Gulf Nuclear Station, Unit 1,
Claiborne County, Mississippi
Date of amendment request: August
17, 2005.
Description of amendment request:
The proposed changes will revise the
Operating License Condition 2.C.(41),
Fire Protection Program, to add a
reference to the Nuclear Regulatory
Commission (NRC) safety evaluation
that allows the application of National
Fire Protection Agency risk-informed,
performance based fire protection
methods and tools that have been
approved by the NRC.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve
a significant increase in the probability
or consequences of an accident
previously evaluated?
Response: No. The proposed activity
involves the use of a risk-informed,
performance-based method to identify
those circuits where a single fire could
damage more than one safe shutdown
train. These circuits would then be
provided with one hour rated fire wrap.
With the exception of the fire wrap
itself, the proposed activity does not
result in any physical changes to safetyrelated structures, systems, or
components (SSCs), or the manner in
which safety-related SSCs are operated,
maintained, modified, tested, or
inspected. The proposed activity does
not degrade the performance or increase
the challenges of any safety-related
SSCs assumed to function in the
accident analysis. As a result, the
proposed activity does not introduce
any new accident initiators. In addition,
fires are not an accident that is
previously evaluated in Chapter 15.
Regardless, the proposed activity does
not change the probability of a fire
occurring since fire ignition frequency is
independent of the presence of the fire
wrap. The consequences of the
proposed activity are bounded by the
fire safe shutdown analysis, which
assumes one train is free of fire damage.
Therefore, providing one hour rated
fire wrap for those circuits where a
single fire could damage more than one
safe shutdown train does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
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2. Does the proposed change create
the possibility of a new or different kind
of accident from any accident
previously evaluated?
Response: No. The proposed activity
involves the use of a risk-informed,
performance-based method to identify
those circuits where a single fire could
damage more than one safe shutdown
train. These circuits would then be
provided with one hour rated fire wrap.
With the exception of the fire wrap
itself, the proposed activity does not
result in any physical changes to safetyrelated structures, systems, or
components (SSCs), or the manner in
which safety-related SSCs are operated,
maintained, modified, tested, or
inspected. The proposed activity does
not degrade the performance or increase
the challenges of any safety-related
SSCs assumed to function in the
accident analysis. As a result, the
proposed activity does not introduce
nor increase the number of failure
mechanisms of a new or different type
than those previously evaluated. The
fire safe shutdown analysis assumes one
train is maintained free of fire damage.
Therefore, providing one hour rated
fire wrap for those circuits where a
single fire could damage more than one
safe shutdown train does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed change involve
a significant reduction in a margin of
safety?
Response: No. The proposed activity
involves the use of a risk-informed,
performance-based method to identify
those circuits where a single fire could
damage more than one safe shutdown
train. These circuits would then be
provided with one hour rated fire wrap.
With the exception of the fire wrap
itself, the proposed activity does not
result in any physical changes to safetyrelated structures, systems, or
components (SSCs), or the manner in
which safety-related SSCs are operated,
maintained, modified, tested, or
inspected. The proposed activity does
not degrade the performance or increase
the challenges of any safety-related
SSCs assumed to function in the
accident analysis.
The proposed activity does not impact
plant safety since the conclusions of the
fire safe shutdown analysis remain
unchanged.
Therefore, providing one hour rated
fire wrap for those circuits where a
single fire could damage more than one
safe shutdown train does not involve a
significant reduction in a margin of
safety.
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The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Nicholas S.
Reynolds, Esquire, Winston and Strawn,
1700 K Street, NW., Washington, DC
20006–3817.
NRC Section Chief: David Terao.
Entergy Operations Inc., Docket No. 50–
382, Waterford Steam Electric Station,
Unit 3, St. Charles Parish, Louisiana
Date of amendment request: July 21,
2005.
Description of amendment request:
The amendment proposes to replace the
existing steam generator tube
surveillance program with that being
proposed by the Technical Specification
Task Force (TSTF) in TSTF 449,
Revision 4.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve
a significant increase in the probability
or consequences of an accident
previously evaluated?
Response: No. The proposed change
requires a Steam Generator Program that
includes performance criteria that will
provide reasonable assurance that the
steam generator (SG) tubing will retain
integrity over the full range of operating
conditions (including startup, operation
in the power range, hot standby,
cooldown and all anticipated transients
included in the design specification).
The SG performance criteria are based
on tube structural integrity, accident
induced leakage, and operational
leakage.
The structural integrity performance
criterion is:
Structural integrity performance
criterion: All in-service steam generator
tubes shall retain structural integrity
over the full range of normal operating
conditions (including startup, operation
in the power range, hot standby, and
cool down and all anticipated transients
included in the design specification)
and design basis accidents. This
includes retaining a safety factor of 3.0
against burst under normal steady state
full power operation primary to
secondary pressure differential and a
safety factor of 1.4 against burst applied
to the design basis accident primary to
secondary pressure differentials. Apart
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61659
from the above requirements, additional
loading conditions associated with the
design basis accidents, or combination
of accidents in accordance with the
design and licensing basis, shall also be
evaluated to determine if the associated
loads contribute significantly to burst or
collapse. In the assessment of tube
integrity, those loads that do
significantly affect burst or collapse
shall be determined and assessed in
combination with the loads due to
pressure with a safety factor of 1.2 on
the combined primary loads and 1.0 on
axial secondary loads.
The accident induced leakage
performance criterion is: The primary to
secondary accident induced leakage rate
for any design basis accidents, other
than a SG tube rupture, shall not exceed
the leakage rate assumed in the accident
analysis in terms of total leakage rate for
all SGs and leakage rate for an
individual SG. Leakage is not to exceed
540 gallons per day through any one SG,
except for specific types of degradation
at specific locations as described in
paragraph c of the Steam Generator
Program.
The operational leakage performance
criterion is: The RCS operational
primary to secondary leakage through
any one SG shall be limited to ≤ 75
gallons per day per SG.
A steam generator tube rupture
(SGTR) event is one of the design basis
accidents that is analyzed as part of a
plant’s licensing basis. In the analysis of
a SGTR event, a bounding primary to
secondary leakage rate equal to the
leakage rate associated with a doubleended rupture of a single tube is
assumed.
For other design basis accidents such
as main steam line break (MSLB),
control element assembly (CEA)
ejection, and reactor coolant pump
seized rotor/sheared shaft, the tubes are
assumed to retain their structural
integrity (i.e., they are assumed not to
rupture). The accident induced leakage
criterion introduced by the proposed
changes account for tubes that may leak
during design basis accidents. The
accident induced leakage criterion
limits this leakage to no more than the
value assumed in the accident analysis.
The SG performance criteria proposed
change identify the standards against
which tube integrity is to be measured.
Meeting the performance criteria
provides reasonable assurance that the
SG tubing will remain capable of
fulfilling its specific safety function of
maintaining reactor coolant pressure
boundary integrity throughout each
operating cycle and in the unlikely
event of a design basis accident. The
performance criteria are only a part of
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the Steam Generator Program required
by the proposed change. The program,
defined by NEI [Nuclear Energy
Institute] 97–06, Steam Generator
Program Guidelines, includes a
framework that incorporates a balance
of prevention, inspection, evaluation,
repair, and leakage monitoring.
The consequences of design basis
accidents are, in part, functions of the
Specific Activity in the primary coolant
and the primary to secondary leakage
rates resulting from an accident.
Therefore, limits are included in the
plant technical specifications for
operational leakage and for Specific
Activity in primary coolant to ensure
the plant is operated within its analyzed
condition. For those analyzed events
that do not result in faulted steam
generators, greater than or equal to 75
gpd [gallons per day] primary to
secondary leakage per steam generator is
assumed in the analysis. For those
analyzed events that result in a faulted
steam generator (e.g., MSLB), 540 gpd
primary to secondary leakage is
assumed though the faulted steam
generator while greater than or equal to
75 gpd primary to secondary leakage is
assumed though the intact steam
generator.
The proposed change does not affect
the design of the SGs, their method of
operation, or primary coolant chemistry
controls. The proposed approach
updates the current technical
specifications and enhances the
requirements for SG inspections. The
proposed change does not adversely
impact any other previously evaluated
design basis accident and is an
improvement over the current Technical
Specifications.
Therefore, the proposed change does
not affect the consequences of a SGTR
accident and the probability of such an
accident is reduced. In addition, the
proposed changes do not affect the
consequences of other design basis
events.
2. Does the proposed change create
the possibility of a new or different kind
of accident from any previously
evaluated?
Response: No. The proposed
performance based requirements are an
improvement over the requirements
imposed by the current technical
specifications.
Implementation of the proposed
Steam Generator Program will not
introduce any adverse changes to the
plant design basis or postulated
accidents resulting from potential tube
degradation. The result of the
implementation of the Steam Generator
Program will be an enhancement of SG
tube performance. Primary to secondary
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15:53 Oct 24, 2005
Jkt 208001
leakage that may be experienced during
all plant conditions will be monitored to
ensure it remains within current
accident analysis assumptions.
The proposed change does not affect
the design of the SGs, their method of
operation, or primary or secondary
coolant chemistry controls. In addition,
the proposed change does not impact
any other plant system or component.
The change enhances SG inspection
requirements. Therefore, the proposed
change does not create the possibility of
a new or different type of accident from
any accident previously evaluated.
3. Does the proposed change involve
a significant reduction in a margin of
safety?
Response: No. The SG tubes in
pressurized water reactors are an
integral part of the reactor coolant
pressure boundary and, as such, are
relied upon to maintain the primary
system’s pressure and inventory. As part
of the reactor coolant pressure
boundary, the SG tubes are unique in
that they are also relied upon as a heat
transfer surface between the primary
and secondary systems such that
residual heat can be removed from the
primary system. In addition, the SG
tubes isolate the radioactive fission
products in the primary coolant from
the secondary system. In summary, the
safety function of a SG is maintained by
ensuring the integrity of its tubes.
Steam generator tube integrity is a
function of the design, environment,
and the physical condition of the tube.
The proposed change does not affect
tube design or operating environment.
The proposed change is expected to
result in an improvement in the tube
integrity by implementing the Steam
Generator Program to manage SG tube
inspection, assessment, repair, and
plugging. The requirements established
by the Steam Generator Program are
consistent with those in the applicable
design codes and standards and are an
improvement over the requirements in
the current technical specifications.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: N.S. Reynolds,
Esquire, Winston & Strawn 1700 K
Street, NW., Washington, DC 20006–
3817.
NRC Section Chief: David Terao.
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Florida Power and Light Company,
Docket Nos. 50–250 and 50–251, Turkey
Point Plant, Units 3 and 4, Miami-Dade
County, Florida
Date of amendment request: July 21,
2005.
Description of amendment request:
The requested change will delete
Technical Specification (TS) 6.9.1.2
related to Occupational Radiation
Exposure Reports and TS 6.9.1.5,
‘‘Monthly Operating Reports.’’
Basis for proposed no significant
hazards consideration determination:
The NRC staff issued a notice of
availability of a model no significant
hazards consideration (NSHC)
determination for referencing in license
amendment applications in the Federal
Register on June 23, 2004 (69 FR 35067).
The licensee affirmed the applicability
of the model NSHC determination in its
application dated July 21, 2005.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
1. Does the proposed change involve
a significant increase in the probability
or consequences of an accident
previously evaluated?
Response: No. The proposed change
eliminates the Technical Specifications
(TSs) reporting requirements to provide
a monthly operating letter report of
shutdown experience and operating
statistics if the equivalent data is
submitted using an industry electronic
database. It also eliminates the TS
reporting requirement for an annual
occupational radiation exposure report,
which provides information beyond that
specified in NRC regulations. The
proposed change involves no changes to
plant systems or accident analyses. As
such, the change is administrative in
nature and does not affect initiators of
analyzed events or assumed mitigation
of accidents or transients. Therefore, the
proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create
the possibility of a new or different kind
of accident from any accident
previously evaluated?
Response: No. The proposed change
does not involve a physical alteration of
the plant, add any new equipment, or
require any existing equipment to be
operated in a manner different from the
present design. Therefore, the proposed
change does not create the possibility of
a new or different kind of accident from
any accident previously evaluated.
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3. Does the proposed change involve
a significant reduction in a margin of
safety?
Response: No. This is an
administrative change to reporting
requirements of plant operating
information and occupational radiation
exposure data, and has no effect on
plant equipment, operating practices or
safety analyses assumptions. For these
reasons, the proposed change does not
involve a significant reduction in the
margin of safety.
Based upon the reasoning presented
above, the requested change does not
involve significance hazards
consideration.
Attorney for licensee: M.S. Ross,
Attorney, Florida Power & Light, P.O.
Box 14000, Juno Beach, Florida 33408–
0420.
NRC Section Chief: Michael L.
Marshall, Jr.
Florida Power and Light Company, et
al., Docket Nos. 50–335 and 50–389, St.
Lucie Plant, Unit Nos. 1 and 2, St. Lucie
County, Florida
Date of amendment request:
September 1, 2005.
Description of amendment request:
The requested change will delete
Technical Specification (TS) 6.9.1.2
related to Occupational Radiation
Exposure Reports and TS 6.9.1.6,
‘‘Monthly Operating Reports.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve
a significant increase in the probability
or consequences of an accident
previously evaluated?
No. The proposed change eliminates
the Technical Specifications (TSs)
reporting requirements to provide a
monthly operating report of shutdown
experience and operating statistics if the
equivalent data is submitted using an
industry electronic database. It also
eliminates the TS reporting requirement
for an annual occupational radiation
exposure report, which provides
information beyond that specified in
NRC regulations. The proposed change
involves no changes to plant systems or
accident analyses. As such, the change
is administrative in nature and does not
affect initiators of analyzed events or
assumed mitigation of accidents or
transients. Therefore, the proposed
change does not involve a significant
increase in the probability or
consequences of an accident previously
evaluated.
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15:53 Oct 24, 2005
Jkt 208001
2. Does the proposed change create
the possibility of a new or different kind
of accident from any accident
previously evaluated?
No. The proposed change does not
involve a physical alteration of the
plant, add any new equipment, or
require any existing equipment to be
operated in a manner different from the
present design. Therefore, the proposed
change does not create the possibility of
a new or different kind of accident from
any accident previously evaluated.
3. Does the proposed change involve
a significant reduction in a margin of
safety?
No. This is an administrative change
to reporting requirements of plant
operating information and occupational
radiation exposure data, and has no
effect on plant equipment, operating
practices or safety analyses
assumptions. For these reasons, the
proposed change does not involve a
significant reduction in the margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 50.92(c) are satisfied.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Attorney for licensee: M.S. Ross,
Attorney, Florida Power & Light, P.O.
Box 14000, Juno Beach, Florida 33408–
0420.
NRC Section Chief: Michael L.
Marshall, Jr.
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request: July 21,
2005.
Description of amendment request:
The proposed amendment would revise
Technical Specification (TS) testing
frequency for the surveillance
requirement (SR) in TS 3.1.4, ‘‘Control
Rod Scram Times.’’ Specifically, the
proposed change would revise the
frequency for SR 3.1.4.2, control rod
scram time testing, from ‘‘120 days
cumulative operation in MODE 1’’ to
‘‘200 days cumulative operation in
MODE 1.’’
The NRC staff issued a notice of
availability of a model no significant
hazards consideration (NSHC)
determination for referencing in
licensing amendment applications in
the Federal Register on August 23, 2004
(69 FR 51864). The licensee affirmed the
applicability of the model NSHC
determination in its application dated
July 21, 2005.
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61661
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), an
analysis of the issue of no significant
hazards consideration is presented
below:
1. Does the change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No. The proposed change
extends the frequency for testing control
rod scram time testing from every 120
days of cumulative Mode 1 operation to
200 days of cumulative Mode 1
operation. The frequency of surveillance
testing is not an initiator of any accident
previously evaluated. The frequency of
surveillance testing does not affect the
ability to mitigate any accident
previously evaluated, as the tested
component is still required to be
operable. Therefore, the proposed
change does not involve a significant
increase in the probability or
consequences of an accident previously
evaluated.
2. Does the change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No. The proposed change
extends the frequency for testing control
rod scram time testing from every 120
days of cumulative Mode 1 operation to
200 days of cumulative Mode 1
operation. The proposed change does
not result in any new or different modes
of plant operation. Therefore, the
proposed change does not create the
possibility of a new or different kind of
accident from any previously evaluated.
3. Does the proposed change involve
a significant reduction in a margin of
safety?
Response: No. The proposed change
extends the frequency for testing control
rod scram time testing from every 120
days of cumulative Mode 1 operation to
200 days of cumulative Mode 1
operation. The proposed change
continues to test the control rod scram
time to ensure the assumptions in the
safety analysis are protected. Therefore,
the proposed change does not involve a
significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John R.
McClure, Nebraska Public Power
District, Post Office Box 499, Columbus,
NE 68602–0499.
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NRC Section Chief: David Terao.
Southern Nuclear Operating Company,
Inc., Georgia Power Company,
Oglethorpe Power Corporation,
Municipal Electric Authority of Georgia,
City of Dalton, Georgia, Docket Nos. 50–
321 and 50–366, Edwin I. Hatch Nuclear
Plant, Units 1 and 2, Appling County,
Georgia
Date of amendment request:
November 12, 2004, as supplemented by
letters dated September 2 and
September 16, 2005.
Description of amendment request:
The proposed amendments would
revise Technical Specifications 3.1.7,
‘‘Standby Liquid Control (SLC) System,’’
for Hatch, Units 1 and 2. The proposed
amendments would update Figures
3.1.7–1 and 3.1.7–2 for Units 1 and 2 TS
to reflect the increased concentration of
Boron-10 in the solution. Conforming
revisions to Bases B 3.1.7, ‘‘Standby
Liquid Control (SLC) System’’ are also
included.
The proposed amendment was
previously noticed on February 1, 2005
(70 FR 5249).
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve
a significant increase in the probability
or consequences of an accident
previously evaluated?
This is a proposed change to Figures
3.1.7–1 and 3.1.7–2 of the Units 1 and
2 TS [Technical Specifications]. Figure
3.1.7–1 is a plot of the weight percent
of Sodium Pentaborate solution in the
Standby Liquid Control (SLC) Tank, as
a function of the gross volume of
solution in the tank. Figure 3.1.7–2 is a
plot of the Sodium Pentaborate
temperature versus concentration
requirements.
Figure 3.1.7–1 is proposed to be
changed in order to accommodate an
injection of Sodium Pentaborate
solution into the reactor, following an
ATWS [anticipated transient without
scram] event, such that the
concentration of Boron-10 atoms in the
reactor will be 800 ppm natural Boron
equivalent. This is necessary to
accommodate increased cycle energy
requirements for the Hatch Units 1 and
2 cores. Both Figures 3.1.7–1 and 3.1.7–
2 are changed to reflect that the
boundary between Region A and B is
changing from 6.9% to 7.0%. The
proposed change to the Figures will not
increase the probability of an ATWS
event because the curves have nothing
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15:53 Oct 24, 2005
Jkt 208001
to do with the prevention of an ATWS
event. The new requirements will insure
that, in the future, the core will have
adequate shutdown margin to mitigate
the consequences of an ATWS event.
The minimum concentration of
Sodium Pentaborate which also
represents the boundary between Region
A and Region B, is changing from 6.9%
to 7.0%. This increase in the
concentration ensures a conservative
margin to the ATWS equivalency
determination required by 10 CFR
50.62.
Also, no systems or components
designed to ensure the safe shutdown of
the reactor are being physically changed
as a result of this proposed TS change.
In fact, no safety related systems or
components designed for the prevention
of previously evaluated events are being
altered by the amendment.
2. The proposed change does not
create the possibility of a new or
different kind of accident from any
previously evaluated.
This proposed TS revision results in
a change to SLC TS Figures 3.1.7–1 and
3.1.7–2 requirements. However, these
changes do not result in physical
changes to the SLC system. SLC pump
operation, maintenance and testing
remain the same. Accordingly, no
changes to the operation, maintenance
or surveillance procedures will result
from this TS revision request. Therefore,
no new modes of operation are
introduced by this TS change.
Since no new modes of operation are
introduced, the proposed change does
not create the possibility of a new or
different type event from any previously
evaluated.
3. The proposed change does not
involve a significant reduction in the
margin of safety.
This proposed TS change is being
made to increase the boron
concentration requirements of the
sodium pentaborate solution injected
into the reactor vessel following an
Anticipated Transient Without Scram
(ATWS) event. The change is necessary
due to new fuel designs and higher
energy requirements for fuel cycles.
Therefore, the change is being made to
insure that shutdown requirements can
be met for the ATWS event. This will
insure the margin of safety with respect
to ATWS will continue to be met.
The increase in the minimum
concentration from 6.9% to 7.0%
ensures a conservative margin with
respect to the ATWS equivalency
determination. Consequently, this
proposed TS change will not result in a
decrease in the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
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review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Ernest L. Blake,
Jr., Esquire, Shaw, Pittman, Potts and
Trowbridge, 2300 N Street, NW.,
Washington, DC 20037.
NRC Section Chief: Evangelos C.
Marinos.
Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton
County, Tennessee
Date of amendment request:
September 1, 2005 (TS–05–04).
Description of amendment request:
The proposed amendment would revise
the reactor protection system turbine
trip allowable value for low trip system
pressure from greater than or equal to 43
pounds per square inch gauge (psig) to
39.5 psig. This change would allow the
instrumentation that performs this trip
function to be tested and verified to be
operable within the capabilities of the
pressure switches.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve
a significant increase in the probability
or consequences of an accident
previously evaluated?
Response: No. The proposed change
revises the allowable value for reactor
trip as a result of a turbine trip on low
trip system pressure. This change will
not alter any plant components,
systems, or processes and will only
provide a more appropriate value to
assess operability of the associated
pressure switches. Since the plant
features and operating practices are not
altered, the possibility of an accident is
not affected. This reactor trip is not
directly credited in SQN’s accident
analysis and is maintained as an
anticipatory trip to enhance the overall
reliability of the reactor trip system. As
such, there is not a specific safety limit
associated with this function and the
generation of a reactor trip based on low
trip system pressure is above the
required actuations to ensure acceptable
mitigation of accidents. As the proposed
change will continue to provide an
acceptable anticipatory trip signal, the
offsite dose potential is not affected by
this change. Therefore, the proposed
change does not involve a significant
increase in the probability or
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consequences of an accident previously
evaluated.
2. Does the proposed change create
the possibility of a new or different kind
of accident from any accident
previously evaluated?
Response: No. As described above,
this change will not alter any plant
equipment or operating practices that
have the ability to create a new potential
for accident generation. The proposed
change revises the operability limits for
a function that generates a trip signal
when appropriate conditions exist to
require accident mitigation response.
This type of function does not have the
ability to create an accident as its
purpose and function is to mitigate
events. Therefore, the proposed change
does not create the possibility of a new
or different kind of accident from any
previously evaluated.
3. Does the proposed change involve
a significant reduction in a margin of
safety?
Response: No. The proposed change
will revise an allowable value for a
reactor trip initiator that results from a
turbine trip condition. This change will
not alter the setpoint, and the
calibration of the associated pressure
switches will continue to be set at the
current values. The allowable value
change is in response to accuracy
aspects of the instrumentation and does
not alter the ability of this trip function
to operate when and as needed to
mitigate accident conditions.
Therefore, the proposed change does
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: General
Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A,
Knoxville, Tennessee 37902.
NRC Section Chief: Michael L.
Marshall, Jr.
Wolf Creek Nuclear Operating
Corporation, Docket No. 50–482, Wolf
Creek Generating Station, Coffey
County, Kansas
Date of amendment request: August
26, 2005.
Description of amendment request:
The amendment would authorize
changes to the Updated Safety Analysis
Report (USAR) for Wolf Creek
Generating Station (WCGS) that would
revise the methodology for the reactor
coolant system (RCS) leak detection
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instrumentation. This revision would
clarify the requirements of the
containment atmosphere gaseous
radioactivity monitor with regard to the
RCS leak detection capability and
would justify that the monitor can be
considered operable in compliance with
Limiting Condition for Operation 3.4.15,
in Technical Specification (TS) 3.4.15,
‘‘RCS Leakage Detection
Instrumentation,’’ during all applicable
Modes. There are no proposed changes
to the WCGS TSs.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed change does not
involve a significant increase in the
probability or consequences of an
accident previously evaluated.
The proposed change has been
evaluated and determined to not
increase the probability or consequences
of an accident previously evaluated. The
proposed change does not make
hardware changes and does not alter the
configuration of any plant system,
structure, or component (SSC). The
proposed change only clarifies the
design and OPERABILITY requirements
for the containment atmosphere gaseous
radioactivity monitors and identifies the
capabilities of the monitors at low RCS
[radio]activity levels. The containment
atmosphere gaseous radioactivity
monitors are not initiators of any
accident; therefore, the probability of
occurrence of an accident is not
increased. The USAR and TSs will
continue to require diverse means of
[RCS] leakage detection equipment, thus
ensuring that leakage due to cracks [in
the RCS] would continue to be
identified prior to propagating to the
point of a[n] [RCS] pipe break.
Therefore, the consequences of an
accident [previously evaluated] are not
increased.
2. The proposed change does not
create the possibility of a new or
different kind of accident from any
accident previously evaluated.
The proposed change does involve the
use or installation of new equipment
and the currently installed equipment
will not be operated in a new or
different manner. No new or different
system interactions are created and no
new processes are introduced. The
proposed changes will not introduce
any new failure mechanisms,
malfunctions, or accident initiators not
already considered in the design and
licensing basis [for WCGS]. The
proposed change does not affect any
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61663
SSC associated with an accident
initiator. Based on this evaluation, the
proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. The proposed change does not
involve a significant reduction in a
margin of safety.
The proposed change does not alter
any RCS leakage detection components.
The proposed change only clarifies the
design and operability requirements for
the containment atmosphere gaseous
radioactivity monitor and identifies the
capabilities of the containment
atmosphere gaseous radioactivity
monitors at low RCS [radio]activity
levels. This change is required since the
level of radioactivity in the WCGS
reactor coolant has become much lower
than what was assumed in the USAR
and the gaseous channel [(monitor)] can
no longer promptly detect a small RCS
leak under all operating conditions. The
proposed amendment continues to
require diverse means of [RCS] leakage
detection equipment with [the]
capability to promptly detect RCS
leakage. Although not required by [the]
TS[s], additional diverse means of
leakage detection capability are
available as described in the USAR
Section 5.2.5. Early detection of [RCS]
leakage, as the potential indicator of a
crack(s) in the RCS pressure boundary,
will thus continue to be in place so that
such a condition is known and
appropriate actions [are] taken well
before any such crack would propagate
to a more severe condition. Based on
this evaluation, the proposed change
does not involve a significant reduction
in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Jay Silberg, Esq.,
Shaw, Pittman, Potts and Trowbridge,
2300 N Street, NW., Washington, DC
20037.
NRC Section Chief: Daniel S. Collins,
Acting.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
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of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket
No. 50–289, Three Mile Island Nuclear
Station, Unit 1 (TMI–1), Dauphin
County, Pennsylvania
Date of application for amendment:
October 20, 2004, as supplemented by
letters dated June 30, July 29, August 17,
and September 19, 2005.
Brief description of amendment: The
amendment revised the Technical
Specifications to (1) eliminate the
existing requirement in Section 3.8.6
regarding maintaining the containment
equipment hatch cover in place with a
minimum of four bolts during fuel
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loading and refueling operations, and
(2) revise or introduce commitments to
the Technical Specifications Bases in
support of the change in Section 3.8.6.
Date of issuance: October 13, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days.
Amendment No.: 257.
Facility Operating License No. DPR–
50. Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: December 7, 2004 (69 FR
70714) The supplements dated June 30,
July 29, August 17, and September 19,
2005, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the NRC staff’s original proposed no
significant hazards consideration
determination. The Commission’s
related evaluation of the amendment is
contained in a Safety Evaluation dated
October 13, 2005.
No significant hazards consideration
comments received: No.
Arizona Public Service Company, et al.,
Docket Nos. STN 50–528, STN 50–529,
and STN 50–530, Palo Verde Nuclear
Generating Station, Units Nos. 1, 2, and
3, Maricopa County, Arizona
Date of application for amendments:
May 28, 2003, as supplemented by
letters dated January 22 and June 23,
2004, and February 2 and September 27,
2005.
Brief description of amendments: The
amendments revise several surveillance
requirements (SRs) in Technical
Specification (TS) 3.8.1 on alternating
current power sources and SR 3.8.4.6 for
direct current power sources for plant
operation. The revised SRs have notes
deleted or modified to adopt in part the
staff-approved TS Task Force 283,
Revision 3, to allow these SRs to be
performed, or partially performed, in
reactor modes that previously were not
allowed by the TSs.
Date of issuance: September 29, 2005.
Effective date: September 29, 2005,
and shall be implemented within 90
days of the date of issuance including
the incorporation of the changes to the
TS Bases for TS 3.8.1 and SR 3.8.4.6 as
described in the licensee’s letters dated
May 28, 2003, January 22 and June 23,
2004, and February 2 and September 27,
2005.
Amendment Nos.: Unit 1—156, Unit
2—156, Unit 3—156.
Facility Operating License Nos. NPF–
41, NPF–51, and NPF–74: The
amendments revised the Technical
Specifications.
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Date of initial notice in Federal
Register: July 8, 2003 (68 FR 40709).
The supplemental letters dated
January 22, June 23, 2004, and February
2 and September 27, 2005, do not
expand the scope of the application as
originally noticed and do not change the
NRC staff’s original proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 29,
2005.
No significant hazards consideration
comments received: No.
Dominion Energy Kewaunee, Inc. Docket
No. 50–305, Kewaunee Power Station,
Kewaunee County, Wisconsin
Date of application for amendment:
February 3, 2005.
Brief description of amendment: The
amendment modified Technical
Specification (TS) 6.16.b.1, ‘‘Radioactive
Effluent Controls Program,’’ and TS
6.18, ‘‘Off-site Dose Calculation Manual
(ODCM),’’ to be consistent with Title 10
of the Code of Federal Regulations (10
CFR) part 20 and NUREG–1431,
‘‘Standard Technical Specifications
Westinghouse Plants.’’
Date of issuance: October 4, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 186.
Facility Operating License No. DPR–
43: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: March 29, 2005 (70 FR
15944).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 4, 2005.
No significant hazards consideration
comments received: No.
Duke Energy Corporation, et al., Docket
Nos. 50–413 and 50–414, Catawba
Nuclear Station, Units 1 and 2, York
County, South Carolina
Date of application for amendments:
November 25, 2002, as supplemented by
letters dated November 13 and
December 16, 2003, September 22, 2004,
April 6, June 14, July 8, August 17, and
September 8 and September 19, 2005.
Brief description of amendments: The
amendments include a full-scope
implementation of an alternative source
term for evaluating the consequences of
design basis accidents at Catawba
Nuclear Station. The amendments also
revised the Technical Specifications for
the Ventilation Filter Testing Program,
Annulus Ventilation System, Auxiliary
Building Filtered Ventilation Exhaust
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System, Fuel Handling Ventilation
Exhaust System, and Control Room Area
Ventilation System, and containment
penetrations.
Date of issuance: September 30, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 227 and 222.
Renewed Facility Operating License
Nos. NPF–35 and NPF–52: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: April 15, 2003 (68 FR 18272).
This application was renoticed on May
24, 2005 (70 FR 29789).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 30,
2005.
No significant hazards consideration
comments received: No.
Energy Northwest, Docket No. 50–397,
Columbia Generating Station, Benton
County, Washington
Date of application for amendment:
April 19, 2005.
Brief description of amendment: The
amendment revised technical
specifications (TSs) testing frequency
for the surveillance requirement (SR) in
TS 3.1.4, ‘‘Control Rod Scram Times.’’
Specifically, the change revised the
frequency for SR 3.1.4.2, ‘‘Control Rod
Scram Time Testing,’’ from ‘‘120 days
cumulative operation in MODE 1’’ to
‘‘200 days cumulative operation in
MODE 1.’’
Date of issuance: September 29, 2005.
Effective date: September 29, 2005,
and shall be implemented within 60
days from the date of issuance.
Amendment No.: 194.
Facility Operating License No. NPF–
21: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: June 7, 2005 (70 FR 33212).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 29,
2005.
No significant hazards consideration
comments received: No.
Entergy Gulf States, Inc., and Entergy
Operations, Inc., Docket No. 50–458,
River Bend Station, Unit 1, West
Feliciana Parish, Louisiana
Date of amendment request:
December 17, 2004, as supplemented by
letters dated June 29, and August 12,
2005.
Brief description of amendment: The
amendment revises the Technical
Specification (TS) requirements for
direct current (DC) sources. The current
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15:53 Oct 24, 2005
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TS only includes ACTION Statements
for an inoperable DC Power subsystems.
The change adds a new ACTION
Statement to TS 3.8.4, ‘‘DC Sources—
Operating,’’ to specifically address an
inoperable battery charger.
Date of issuance: October 7, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment No.: 148.
Facility Operating License No. NPF–
47: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: January 4, 2005 (70 FR 401).
The supplements dated June 29, and
August 12, 2005, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated October 7, 2005.
No significant hazards consideration
comments received: No.
Entergy Operations, Inc., Docket No. 50–
368, Arkansas Nuclear One, Unit No. 2,
Pope County, Arkansas
Date of application for amendment:
December 20, 2004, as supplemented by
letter dated April 26, 2005.
Brief description of amendment: The
amendment changed the existing
containment structures and tendon
inservice inspection requirements to be
consistent with NUREG–1432, Revision
3, and the American Society of
Mechanical Engineers Boiler and
Pressure Vessel Code, Section XI.
Specifically, the amendment modified
the Surveillance Requirement of
Technical Specification (TS) 3.6.1.5,
added a new Surveillance Program to
TS 6.5.6 and a report to TS 6.5.7, and
made two administrative changes to the
TSs.
Date of issuance: September 29, 2005.
Effective date: As of the date of
issuance to be implemented within 90
days from the date of issuance.
Amendment No.: 262.
Renewed Facility Operating License
No. NPF–6: Amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: March 29, 2005 (70 FR
15943).
The supplement dated April 26, 2005,
provided additional information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the staff’s
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original proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 29,
2005.
No significant hazards consideration
comments received: No.
Indiana Michigan Power Company,
Docket Nos. 50–315 and 50–316, Donald
C. Cook Nuclear Plant, Units 1 and 2,
Berrien County, Michigan
Date of application for amendments:
September 21, 2004, as supplemented
by letters dated March 18, April 7, May
6, August 10, and September 19, 2005.
Brief description of amendments: The
amendments extended the outage times
from 72 hours to 14 days for an
inoperable emergency diesel generator.
It also changed formats of the affected
technical specification pages to improve
their appearance but not alter any
requirements.
Date of issuance: September 30, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 120 days.
Amendment Nos.: 291, 273.
Facility Operating License Nos. DPR–
58 and DPR–74: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: October 26, 2004 (69 FR
62476). The supplements provided
clarifying information that did not
change the scope of the proposed
amendment as described in the original
notice of proposed action published in
the Federal Register, and did not
change the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 30,
2005.
No significant hazards consideration
comments received: No.
Nuclear Management Company, LLC,
Docket No. 50–263, Monticello Nuclear
Generating Plant, Wright County,
Minnesota
Date of application for amendment:
June 30, 2004, as supplemented by
letters dated September 16, 2004,
November 5, 2004, March 3, 2005, July
1, 2005, and September 27, 2005.
Brief description of amendment: The
amendment changed the TSs to support
an increase in the length of the fuel
cycle from 18 to 24 months at
Monticello. In addition, the proposed
amendment requested changes in
calibration times of various instruments.
These changes will be evaluated in a
separate license amendment.
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Date of issuance: September 30, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 143.
Facility Operating License No. DPR–
22: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: January 18, 2005 (70 FR
2892). The supplements dated
September 16, 2004, November 5, 2004,
March 3, 2005, July 1, 2005, and
September 27, 2005, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register on
January 18, 2005 (70 FR 2892).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 30,
2005.
No significant hazards consideration
comments received: No.
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1, Washington County, Nebraska
Date of amendment request:
November 23, 2004, as supplemented by
letter dated July 8, 2005.
Brief description of amendment: The
amendment (1) revised the descriptive
wording of Technical Specifications
(TSs) Table 1–1, ‘‘RPS [reactor
protection system] Limiting Safety
System Settings,’’ for the reactor trip
setpoint for low steam generator water
level to relocate unnecessary detail, and
(2) converted TSs Section 4.0, ‘‘Design
Features,’’ to the format and content of
NUREG–1432, Revision 3, ‘‘Standard
Technical Specifications for
Combustion Engineering Plants.’’
Date of issuance: October 3, 2005.
Effective date: October 3, 2005, and
shall be implemented within 60 days
from the date of issuance.
Amendment No.: 236.
Renewed Facility Operating License
No. DPR–40: The amendment revised
the Technical Specifications.
Date of initial notice in Federal
Register: May 24, 2005 (70 FR 29798).
The July 8, 2005, supplemental letter
provided additional information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the staff’s
original no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
safety evaluation dated October 3, 2005.
No significant hazards consideration
comments received: No.
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PPL Susquehanna, LLC, Docket Nos. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1
and 2), Luzerne County, Pennsylvania
Date of application for amendments:
September 8, 2004, as supplemented by
letters dated July 8 and September 28,
2005.
Brief description of amendments: The
amendments changed SSES 1 and 2
Technical Specifications 3.6.4.1,
‘‘Secondary Containment,’’ and 3.6.4.3,
‘‘Standby Gas Treatment System
(SGTS),’’ to extend, on a one-time basis,
the allowable completion time for
required actions for secondary
containment inoperable and two SGTS
subsystems inoperable, in mode 1, 2, or
3, from 4 hours to 48 hours.
Date of issuance: October 6, 2005.
Effective date: October 6, 2005.
Amendment Nos.: 226 and 203.
Facility Operating License Nos. NPF–
14 and NPF–22: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: March 1, 2005 (70 FR 9994).
The supplements dated July 8 and
September 28, 2005, contained
clarifying information and did not
change the initial no significant hazards
consideration determination or expand
the scope of the initial Federal Register
notice.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 6, 2005.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket Nos. 50–272
and 50–311, Salem Nuclear Generating
Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of application for amendments:
April 15, 2004, as supplemented by
letters dated August 11, 2004, and
August 11, 2005. The August 11, 2005,
supplement withdrew a portion of the
original application from consideration.
Brief description of amendments: The
amendments revised Technical
Specification (TS) 3.6.2.3 Action B, for
both units, to correct a non-conservative
action statement.
Date of issuance: September 30, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days.
Amendment Nos.: 266 and 248.
Facility Operating License Nos. DPR–
70 and DPR–75: The amendments
revised the TSs.
Date of initial notice in Federal
Register: October 12, 2004 (69 FR
60684). The licensee’s supplement
dated August 11, 2005, withdrew a
portion of the original application from
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consideration and did not increase the
scope of the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 30,
2005.
No significant hazards consideration
comments received: No.
Southern California Edison Company, et
al., Docket Nos. 50–361 and 50–362,
San Onofre Nuclear Generating Station,
Units 2 and 3, San Diego County,
California
Date of application for amendments:
March 24, 2005.
Brief description of amendments: The
proposed changes revised various
Technical Specifications (TSs) related to
cycle-specific values and the shutdown
margin, and are consistent with the
following Nuclear Regulatory
Commission approved Technical
Specification Task Force (TSTF)
Standard TS Change Travelers: TSTF–
9–A, Revision 1, ‘‘Relocate Value for
Shutdown Margin to COLR;’’ TSTF–67–
A, Revision 0, ‘‘Correction of Shutdown
Margin Definition;’’ TSTF–142–A,
Revision 0, ‘‘Increase the Completion
Time When the Core Reactivity Balance
is Not Within Limit;’’ and TSTF–150–A,
Revision 0, ‘‘Replace DNBR Power
Decrease Number with Reference to the
COLR.’’
Date of issuance: October 3, 2005.
Effective date: As of the date of
issuance, and shall be implemented
within 60 days from the date of
issuance.
Amendment Nos.: 200/191.
Facility Operating License Nos. NPF–
10 and NPF–15: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: May 10, 2005 (70 FR 24656).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 3, 2005.
No significant hazards consideration
comments received: No.
STP Nuclear Operating Company,
Docket Nos. 50–498 and 50–499, South
Texas Project, Units 1 and 2, Matagorda
County, Texas
Date of amendment request: July 4,
2005.
Brief description of amendments: The
amendments change Technical
Specification 4.0.5 to add a reference to
the NRC-approved exemption of
selected pumps, valves, and other
components from special treatment
requirements. As an editorial change,
references to Title 10, Code of Federal
Regulations (10 CFR) part 50, section
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50.55a(f) and 10 CFR part 50, section
50.55a(f)(6)(I) is added to the paragraph
for inservice testing, similar to the
existing references for inservice
inspection. In addition, ‘‘inservice
testing’’ and ‘‘inservice inspection’’ are
reordered for consistency with the
sequence of the regulations in 10 CFR
50.55a.
Date of issuance: October 4, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 90 days of issuance.
Amendment Nos.: Unit 1—173; Unit
2—161.
Facility Operating License Nos. NPF–
76 and NPF–80: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: August 2, 2005 (70 FR 44403).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated October 4, 2005.
No significant hazards consideration
comments received: No.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Unit Nos.
1 and 2, Somervell County, Texas
Date of amendment request:
September 9, 2004.
Brief description of amendments: The
Amendments revised the Technical
Specification 3.6.6.8 to change the
current interval for surveillance from
every 10 years to verification that the
nozzles are unobstructed following a
maintenance that could have resulted in
nozzle blockage.
Date of issuance: September 23, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment Nos.: 120 and 120.
Facility Operating License Nos. NPF–
87 and NPF–89: The Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: October 26, 2004 (69 FR
62478).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 23,
2005.
No significant hazards consideration
comments received: No.
Union Electric Company, Docket No.
50–483, Callaway Plant, Unit 1,
Callaway County, Missouri
Date of application for amendment:
September 17, 2004, as supplemented
by letters dated February 11, May 26,
June 17 (two letters), July 15, July 29,
August 16, and September 6, 2005.
Brief description of amendment: The
amendment supports the installation of
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replacement steam generators (SGs) at
Callaway during the refueling outage in
the fall of 2005. The amendment affects
the following affected TSs: the reactor
core safety limits (TS 2.1.1), reactor trip
system and engineered safety feature
actuation system instrumentation (TSs
3.3.1 and 3.3.2), reactor coolant system
(RCS) limits (TS 3.4.1), RCS loops (TSs
3.4.5, 3.4.6, and 3.4.7), RCS operational
leakage (TS 3.4.13), SG tube integrity
(the new TS 3.4.17), main steam safety
valves (TS 3.7.1), SG tube surveillance
program (TS 5.5.9), containment
integrated leakage rate testing program
(TS 5.5.16), and SG tube inspection
report (TS 5.6.10).
Date of issuance: September 29, 2005.
Effective date: Effective on the date of
issuance, and shall be implemented
before entry into Mode 5 during the
restart from the fall 2005 refueling
outage when the replacement steam
generators are installed including (1)
revising the pressure temperature limits
report to change the cold overpressure
mitigation system setpoints to reflect no
reactor coolant pump operation
restrictions and (2) incorporating the TS
Bases changes identified in the
licensee’s letter of September 6, 2005,
into the TS Bases.
Amendment No.: 168.
Facility Operating License No. NPF–
30: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: November 23, 2004 (69 FR
68185). The supplemental letters dated
February 11, May 26, June 17 (two
letters), July 15, July 29, August 16, and
September 6, 2005, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed and
did not change the NRC staff’s original
proposed no significant hazards
consideration determination published
in the Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 29,
2005.
No significant hazards consideration
comments received: No.
Notice of Issuance of Amendments to
Facility Operating Licenses and Final
Determination of No Significant
Hazards Consideration and
Opportunity for a Hearing (Exigent
Public Announcement or Emergency
Circumstances)
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application for the
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61667
amendment complies with the
standards and requirements of the
Atomic Energy Act of 1954, as amended
(the Act), and the Commission’s rules
and regulations. The Commission has
made appropriate findings as required
by the Act and the Commission’s rules
and regulations in 10 CFR Chapter I,
which are set forth in the license
amendment.
Because of exigent or emergency
circumstances associated with the date
the amendment was needed, there was
not time for the Commission to publish,
for public comment before issuance, its
usual Notice of Consideration of
Issuance of Amendment, Proposed No
Significant Hazards Consideration
Determination, and Opportunity for a
Hearing.
For exigent circumstances, the
Commission has either issued a Federal
Register notice providing opportunity
for public comment or has used local
media to provide notice to the public in
the area surrounding a licensee’s facility
of the licensee’s application and of the
Commission’s proposed determination
of no significant hazards consideration.
The Commission has provided a
reasonable opportunity for the public to
comment, using its best efforts to make
available to the public means of
communication for the public to
respond quickly, and in the case of
telephone comments, the comments
have been recorded or transcribed as
appropriate and the licensee has been
informed of the public comments.
In circumstances where failure to act
in a timely way would have resulted, for
example, in derating or shutdown of a
nuclear power plant or in prevention of
either resumption of operation or of
increase in power output up to the
plant’s licensed power level, the
Commission may not have had an
opportunity to provide for public
comment on its no significant hazards
consideration determination. In such
case, the license amendment has been
issued without opportunity for
comment. If there has been some time
for public comment but less than 30
days, the Commission may provide an
opportunity for public comment. If
comments have been requested, it is so
stated. In either event, the State has
been consulted by telephone whenever
possible.
Under its regulations, the Commission
may issue and make an amendment
immediately effective, notwithstanding
the pendency before it of a request for
a hearing from any person, in advance
of the holding and completion of any
required hearing, where it has
determined that no significant hazards
consideration is involved.
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Federal Register / Vol. 70, No. 205 / Tuesday, October 25, 2005 / Notices
The Commission has applied the
standards of 10 CFR 50.92 and has made
a final determination that the
amendment involves no significant
hazards consideration. The basis for this
determination is contained in the
documents related to this action.
Accordingly, the amendments have
been issued and made effective as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the application for
amendment, (2) the amendment to
Facility Operating License, and (3) the
Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment, as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
The Commission is also offering an
opportunity for a hearing with respect to
the issuance of the amendment. Within
60 days after the date of publication of
this notice, the licensee may file a
request for a hearing with respect to
issuance of the amendment to the
subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
VerDate Aug<31>2005
15:53 Oct 24, 2005
Jkt 208001
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland,
and electronically on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If there
are problems in accessing the document,
contact the PDR Reference staff at 1
(800) 397–4209, (301) 415–4737, or by email to pdr@nrc.gov. If a request for a
hearing or petition for leave to intervene
is filed by the above date, the
Commission or a presiding officer
designated by the Commission or by the
Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also identify the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner intends to
rely in proving the contention at the
hearing. The petitioner must also
provide references to those specific
sources and documents of which the
petitioner is aware and on which the
petitioner intends to rely to establish
those facts or expert opinion. The
petition must include sufficient
information to show that a genuine
dispute exists with the applicant on a
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Fmt 4703
Sfmt 4703
material issue of law or fact.1
Contentions shall be limited to matters
within the scope of the amendment
under consideration. The contention
must be one which, if proven, would
entitle the petitioner to relief. A
petitioner/requestor who fails to satisfy
these requirements with respect to at
least one contention will not be
permitted to participate as a party.
Each contention shall be given a
separate numeric or alpha designation
within one of the following groups:
1. Technical: primarily concerns/
issues relating to technical and/or
health and safety matters discussed or
referenced in the applications.
2. Environmental: primarily concerns/
issues relating to matters discussed or
referenced in the environmental
analysis for the applications.
3. Miscellaneous: does not fall into
one of the categories outlined above.
As specified in 10 CFR 2.309, if two
or more petitioners/requestors seek to
co-sponsor a contention, the petitioners/
requestors shall jointly designate a
representative who shall have the
authority to act for the petitioners/
requestors with respect to that
contention. If a petitioner/requestor
seeks to adopt the contention of another
sponsoring petitioner/requestor, the
petitioner/requestor who seeks to adopt
the contention must either agree that the
sponsoring petitioner/requestor shall act
as the representative with respect to that
contention, or jointly designate with the
sponsoring petitioner/requestor a
representative who shall have the
authority to act for the petitioners/
requestors with respect to that
contention.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing. Since the Commission has
made a final determination that the
amendment involves no significant
hazards consideration, if a hearing is
requested, it will not stay the
effectiveness of the amendment. Any
hearing held would take place while the
amendment is in effect.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
1 To the extent that the applications contain
attachments and supporting documents that are not
publicly available because they are asserted to
contain safeguards or proprietary information,
petitioners desiring access to this information
should contact the applicant or applicant’s counsel
and discuss the need for a protective order.
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Federal Register / Vol. 70, No. 205 / Tuesday, October 25, 2005 / Notices
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer or
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(I)–(viii).
Entergy Gulf States, Inc., and Entergy
Operations, Inc., Docket No. 50–458,
River Bend Station, Unit 1, West
Feliciana Parish, Louisiana
Date of amendment request: August
31, 2005, as supplemented by letter
dated September 13, 2005.
Brief description of amendment: The
amendment permitted a one-time
change to Technical Specification Table
3.3.8.1–1 to provide a one-time
relaxation of the Loss of Power
instrumentation requirements.
Date of issuance: September 15, 2005.
Effective date: As of the date of
issuance to be implemented
immediately.
Amendment No.: 147.
Facility Operating License No. NPF–
47: Amendment revised the Technical
Specifications.
Public comments requested as to
proposed no significant hazards
consideration: Yes.
The NRC published a public notice of
the proposed amendment, issued a
proposed finding of no significant
hazards consideration, and requested
that any comments on the proposed no
significant hazards consideration be
VerDate Aug<31>2005
15:53 Oct 24, 2005
Jkt 208001
provided to the NRC staff by the close
of business on September 9, 2005. The
notice was published in The St.
Francisville Democrat (in St.
Francisville) on September 8, 2005, and
The Advocate (in Baton Rouge) on
September 7, 2005. No public comments
were received.
The Commission’s related evaluation
of the amendment, finding of exigent
circumstances, consultation with the
State of Louisiana, and final no
significant hazards consideration
determination are contained in a Safety
Evaluation dated September 15, 2005.
XU Generation Company LP, Docket No.
50–445, Comanche Peak Steam Electric
Station, Unit No. 1, Somervell County,
Texas
Date of amendment request: April 27,
2005 as supplemented by letter dated
July 20, 2005.
Description of amendment: The
amendments revise the Technical
Specifications to add the topical report
WCAP–13060–P–A to the list of NRC
approved methodologies to be used at
Comanche Peak Steam Electric Station,
Unit 1.
Date of issuance: October 11, 2005.
Effective date: As of the date of
issuance and shall be implemented
immediately.
Amendment No.: 123.
Facility Operating License No. NPF–
87: Amendment revised the Technical
Specifications.
Public comments requested as to
proposed no significant hazards
consideration (NSHC): Yes.
The notice published on September
26, 2005 (70 FR 56191) provided an
opportunity to submit comments on the
Commission’s proposed NSHC
determination. No comments have been
received. The notice also provided an
opportunity to request a hearing within
60 days from the date of publication, but
indicated that if the Commission makes
a final NSHC determination, any such
hearing would take place after issuance
of the amendment.
The Commission’s related evaluation
of the amendment, finding of exigent
circumstances, state consultation, and
final NSHC determination are contained
in a safety evaluation dated October 11,
2005.
Attorney for licensee: George L. Edgar,
Esq., Morgan, Lewis and Bockius, 1800
M Street, NW., Washington, DC 20036.
NRC Section Chief: David Terao.
Dated at Rockville, Maryland, this 17th day
of October, 2005.
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61669
For the Nuclear Regulatory Commission.
Ledyard B. Marsh,
Director, Division of Licensing Project
Management, Office of Nuclear Reactor
Regulation.
[FR Doc. 05–21180 Filed 10–24–05; 8:45 am]
BILLING CODE 7590–01–P
SECURITIES AND EXCHANGE
COMMISSION
Sunshine Act Meeting
Notice is hereby given, pursuant to
the provisions of the Government in the
Sunshine Act, Public Law 94–409, that
the Securities and Exchange
Commission will hold the following
meeting during the week of October 24,
2005:
A Closed Meeting will be held on
Thursday, October 27, 2005 at 2 p.m.
Commissioners, Counsel to the
Commissioners, the Secretary to the
Commission, and recording secretaries
will attend the Closed Meeting. Certain
staff members who have an interest in
the matters may also be present.
The General Counsel of the
Commission, or his designee, has
certified that, in his opinion, one or
more of the exemptions set forth in 5
U.S.C. 552b(c)(5), (7), (9)(B), and (10)
and 17 CFR 200.402(a)(5), (7), 9(ii) and
(10) permit consideration of the
scheduled matters at the Closed
Meeting.
Commissioner Atkins, as duty officer,
voted to consider the items listed for the
closed meeting in closed session and
that no earlier notice thereof was
possible.
The subject matters of the Closed
Meeting scheduled for Thursday,
October 27, 2005 will be:
Formal orders of private investigations;
Institution and settlement of injunctive
actions;
Institution and settlement of
administrative proceedings of an
enforcement nature; and
Opinions.
At times, changes in Commission
priorities require alterations in the
scheduling of meeting items.
For further information and to
ascertain what, if any, matters have been
added, deleted or postponed, please
contact:
The Office of the Secretary at (202)
551–5400.
Dated: October 20, 2005.
Jonathan G. Katz,
Secretary.
[FR Doc. 05–21355 Filed 10–21–05; 11:26
am]
BILLING CODE 8010–01–P
E:\FR\FM\25OCN1.SGM
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Agencies
[Federal Register Volume 70, Number 205 (Tuesday, October 25, 2005)]
[Notices]
[Pages 61655-61669]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: 05-21180]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from September 30 to October 13, 2005. The last
biweekly notice was published on October 11, 2005 (70 FR 59082).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The
filing of requests for a hearing and petitions for leave to intervene
is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
[[Page 61656]]
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(I)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
Dominion Nuclear Connecticut Inc., et al., Docket No. 50-423, Millstone
Power Station, Unit No. 3, New London County, Connecticut
Date of amendment request: September 13, 2005.
Description of amendment request: The amendment would reduce the
temperature at which shutdown and control rod cluster control
assemblies (RCCA) drop testing is done from greater than or equal to
551 [deg]Fahrenheit (F) to greater than or equal to 500 [deg]F.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
Criterion 1: Does the proposed amendment involve a significant
increase in the probability or consequences of an accident previously
evaluated?
Response: No. DNC [Dominion Nuclear Connecticut, Inc.] is proposing
to change the temperature at which the shutdown and control RCCA drop
tests are performed from ``greater than or equal to 551 [deg]F,'' to
``greater than or equal to 500 [deg]F.'' The proposed change does not
modify any plant equipment and does not impact any failure modes that
could lead to an accident. Additionally, the proposed change has no
effect on the consequence of any analyzed accident since the change
does not affect the function of any equipment credited for accident
mitigation. Based on this discussion, the proposed amendment does not
increase the probability or consequences of an accident previously
evaluated.
Criterion 2: Does the proposed amendment create the possibility of
a new or different kind of accident from any accident previously
evaluated?
Response: No. The proposed change does not modify any plant
equipment and there is no impact on the capability of existing
equipment to perform its intended functions. No system setpoints are
being modified and no changes are being made to the method in which
plant operations are conducted. No new failure modes are introduced by
the proposed change. The proposed amendment does not introduce accident
initiators or malfunctions that would cause a new or different kind of
accident.
As noted above, the proposed change does not affect the revisions
to plant procedures, which were made to address Westinghouse Nuclear
Safety Advisory Letter, NSAL-00-016 (Rod Withdrawal from Subcritical
Protection in Lower Modes, issued in 2000).
Therefore, the proposed amendment does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
Criterion 3: Does the proposed amendment involve a significant
reduction in a margin of safety?
Response: No. The TS [technical specification] change does not
involve a significant reduction in margin because the acceptance
criterion for the RCCA drop time will not change. The proposed change
will reduce the minimum RCCA drop test temperature from greater than or
equal to 551 [deg]F to greater than or equal to 500 [deg]F. This will
slightly increase the measured test
[[Page 61657]]
RCCA drop time. However, the measured test RCCA drop time is required
to remain within the current TS limit of 2.7 seconds and the 2.19
seconds for surveillance testing acceptance criteria (plant specific
seismic allowance of 0.51 seconds). The proposed change does not affect
any of the assumptions used in the accident analysis, nor does it
affect any operability requirements for equipment important to plant
safety. Therefore, the margin of safety is not impacted by the proposed
amendment.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Lillian M. Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc., Waterford, CT 06141-5127.
NRC Section Chief: Darrell J. Roberts.
Dominion Nuclear Connecticut Inc., et al., Docket No. 50-423, Millstone
Power Station, Unit No. 3, New London County, Connecticut
Date of amendment request: September 13, 2005.
Description of amendment request: The changes revise surveillance
requirements for the recirculation spray system (RSS) to verify proper
initiation of recirculation spray through actuation by the refueling
water storage tank (RWST) low-low level signal instead of actuation by
a timer.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
Criterion 1: Does the proposed amendment involve a significant
increase in the probability or consequences of an accident previously
evaluated?
Response: No. The RSS is only an accident mitigation system. As
such, changes in the operation of RSS cannot have an impact on the
probability of an accident. The delay in the start of the RSS pump is
to assure there is sufficient water in the containment sump for
adequate RSS pump NPSH [net positive suction head] and margin to
suction pipe flashing in light of the debris analysis conducted in
response to GL [Generic Letter] 2004-02. Containment analyses have been
performed to demonstrate that there is no impact on the peak
containment pressure and temperature following a LOCA [loss-of-coolant
accident]. While there are some changes in the predicted post-LOCA
environmental conditions, evaluations have been performed to show that
there is no significant impact on the environmental qualification for
equipment inside containment. The impact to piping and supports has
been demonstrated to be acceptable without modification. Delay in RSS
spray start will result in a reduction in diesel generator loading
since the RSS pumps and the RHS pumps will no longer be running
concurrently. The reduction in iodine removal efficiency during the
delay period is more than offset by elimination of over-conservatisms
in assumptions for long term iodine removal by the RSS system. The net
impact is a reduction in the predicted offsite doses and control room
doses following a design basis LOCA. Based on this discussion, the
proposed amendment does not increase the probability or consequence of
an accident previously evaluated.
Criterion 2: Does the proposed amendment create the possibility of
a new or different kind of accident from any accident previously
evaluated?
Response: No. The proposed modification alters the RSS pump
circuitry by initiating the start sequence with an existing RWST low-
low level signal instead of a timer. The timer is now used to sequence
pump starts. The pump function is not changed in any way. The proposed
amendment does not introduce failure modes, accident initiators, or
malfunctions that would cause a new or different kind of accident.
Therefore, the proposed amendment does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
Criterion 3: Does the proposed amendment involve a significant
reduction in a margin of safety?
Response: No. The proposed change ensures that adequate margin to
suction line flashing and NPSH margin exists for proper operation of
the RSS pumps once the effects of debris are considered as required per
GL 2004-02. Function of the pumps is not affected. Analyses have been
performed that show the containment design basis limits are satisfied
and the post-LOCA offsite and control room doses meet the required
criteria. Therefore, based on the above, the proposed amendment does
not involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Lillian M. Cuoco, Senior Nuclear Counsel,
Dominion Nuclear Connecticut, Inc., Waterford, CT 06141-5127.
NRC Section Chief: Darrell J. Roberts.
Duke Energy Corporation, et al., Docket Nos. 50-369 and 50-370, McGuire
Nuclear Station, Units 1 and 2, Mecklenburg County, North Carolina and
Docket Nos. 50-413 and 50-414, Catawba Nuclear Station, Units 1 and 2,
York County, South Carolina
Date of amendment request: June 29, 2005.
Description of amendment request: The amendment would revise
Technical Specification Bases Section 3.6.11, ``Air Return System
(ARS),'' and the Updated Final Safety Analysis Reports (UFSAR), Section
6.2, ``Containment Systems,'' for McGuire Nuclear Station, Units 1 and
2 and Catawba Nuclear Station, Units 1 and 2. The licensee proposes to
implement an additional manual operator action to respond to NRC
Bulletin 2003-01, ``Potential Impact of Debris Blockage on Emergency
Sump Recirculation at Pressurized-Water Reactors.'' This amendment
would allow plant operators to manually start one air return fan at a
containment pressure of 1 psig prior to the automatic 9 minutes (+ 1
minute) delayed start described in the UFSAR.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
First Standard
Does the change involve a significant increase in the probability
or consequences of an accident previously evaluated?
No. The manual start of an Air Return System (ARS) fan will not
result in a significant increase in the probability of an accident
previously evaluated. The starting of an ARS fan is not considered to
be an initiator of any accident or transient. This action is not taken
during normal plant operation, but in response to an accident. The ARS
fans do not operate to provide any normal ventilation requirement. The
Containment Pressure Control System (CPCS) is provided to prevent
excessive depressurization of the containment through inadvertent or
excessive operation of certain engineered safety features. The CPCS
prevents the
[[Page 61658]]
inadvertent actuation of an ARS fan during normal operation.
This change is being requested in order to mitigate the
consequences of a small break loss of coolant accident (SBLOCA) and
help prevent or delay reaching the initiation pressure setpoint for
containment spray, thereby reducing associated problems with possible
sump debris buildup. SBLOCA events are bounded by the consequences of a
design basis large break [loss of coolant accident] LOCA as addressed
in Section 15 of the McGuire and Catawba [Updated Final Safety Analysis
Report] UFSARs. Accordingly, this amendment will not involve a
significant increase in the consequences of an accident previously
evaluated.
Second Standard
Does the change create the possibility of a new or different kind
of accident from any accident previously evaluated?
No. The change proposed in this [license amendment request] LAR
does not involve a physical alteration to the plant (i.e., no new or
different type of equipment will be installed) or a change in the
methods governing any normal plant operation. It does allow for the
early start of one ARS fan during a SBLOCA event with containment
pressure greater than 1 psig and less than 3 psig. This change will not
affect or degrade the ability of the ARS to perform its specified
safety functions.
Accidents of a different type are credible accidents that the
proposed amendment could create that are not bounded by UFSAR evaluated
accidents. This amendment allows for the manual start of an ARS fan
following a SBLOCA within the containment. No new failure modes are
introduced due to the manual start of an ARS fan. The circuit used to
manually start an ARS fan does not interfere with the automatic signal
to start an ARS fan. This change does not require any modifications to
the control circuitry for the ARS. The starting of an ARS fan is not
considered to be an initiator of any accident or transient. This action
(starting of an ARS fan) is not taken during normal operation, but in
response to an accident. Previous accidents considered incredible are
not made more likely by this change. A human performance error, such as
starting the ARS fan too early, too late, or not at all, would not
result in a substantial difference in the calculated differential
pressure across the divider deck. Since no new malfunctions of
equipment with a different result are introduced, all effects of any
malfunctions are bounded by those already evaluated in the UFSAR. Thus
it is concluded that the change contained in this LAR will not create
the possibility of a new or different kind of accident from any
accident previously evaluated.
Third Standard
Does the proposed change involve a significant reduction in a
margin of safety?
No. The early manual start of an ARS fan for SBLOCA events will not
reduce the ability of this system to perform its design functions to
assure the rapid return of air from the upper to the lower containment
compartment after the initial blowdown following a Design Basis
Accident (DBA). The return of this air to the lower compartment and
subsequent recirculation back up through the ice condenser assists in
cooling the containment atmosphere and limiting post accident pressure
and temperature in containment to less than design values. Limiting
pressure and temperature also reduces the release of fission product
radioactivity from containment to the environment in the event of a
DBA. Therefore, there are no adverse dose effects from the early start
of the ARS fan or from the delay of containment spray based on the
current licensing basis.
Analyses have shown that there will be no fan or damper malfunction
due to the early manual start of a fan. The other functions of the
system are not affected by the change proposed in this LAR. The manual
start of the ARS during a SBLOCA will help maintain the margin of
safety by forcing air and steam through the ice condenser with a
subsequent reduction in the rate of pressure increase in the
containment, and a delay in reaching the actuation setpoint for the
containment spray system. The containment spray system will continue to
be initiated at the normal setpoint pressure of the system (-3 psig).
Therefore, the proposed changes listed above do not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Ms. Lisa F. Vaughn, Legal Department
(PB05E), Duke Energy Corporation, 422 South Church Street, Charlotte,
North Carolina 28201-1006.
NRC Section Chief: Evangelos C. Marinos.
Entergy Operations, Inc., System Energy Resources, Inc., South
Mississippi Electric Power Association, and Entergy Mississippi, Inc.,
Docket No. 50-416, Grand Gulf Nuclear Station, Unit 1, Claiborne
County, Mississippi
Date of amendment request: August 17, 2005.
Description of amendment request: The proposed changes will revise
the Operating License Condition 2.C.(41), Fire Protection Program, to
add a reference to the Nuclear Regulatory Commission (NRC) safety
evaluation that allows the application of National Fire Protection
Agency risk-informed, performance based fire protection methods and
tools that have been approved by the NRC.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No. The proposed activity involves the use of a risk-
informed, performance-based method to identify those circuits where a
single fire could damage more than one safe shutdown train. These
circuits would then be provided with one hour rated fire wrap. With the
exception of the fire wrap itself, the proposed activity does not
result in any physical changes to safety-related structures, systems,
or components (SSCs), or the manner in which safety-related SSCs are
operated, maintained, modified, tested, or inspected. The proposed
activity does not degrade the performance or increase the challenges of
any safety-related SSCs assumed to function in the accident analysis.
As a result, the proposed activity does not introduce any new accident
initiators. In addition, fires are not an accident that is previously
evaluated in Chapter 15. Regardless, the proposed activity does not
change the probability of a fire occurring since fire ignition
frequency is independent of the presence of the fire wrap. The
consequences of the proposed activity are bounded by the fire safe
shutdown analysis, which assumes one train is free of fire damage.
Therefore, providing one hour rated fire wrap for those circuits
where a single fire could damage more than one safe shutdown train does
not involve a significant increase in the probability or consequences
of an accident previously evaluated.
[[Page 61659]]
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No. The proposed activity involves the use of a risk-
informed, performance-based method to identify those circuits where a
single fire could damage more than one safe shutdown train. These
circuits would then be provided with one hour rated fire wrap. With the
exception of the fire wrap itself, the proposed activity does not
result in any physical changes to safety-related structures, systems,
or components (SSCs), or the manner in which safety-related SSCs are
operated, maintained, modified, tested, or inspected. The proposed
activity does not degrade the performance or increase the challenges of
any safety-related SSCs assumed to function in the accident analysis.
As a result, the proposed activity does not introduce nor increase the
number of failure mechanisms of a new or different type than those
previously evaluated. The fire safe shutdown analysis assumes one train
is maintained free of fire damage.
Therefore, providing one hour rated fire wrap for those circuits
where a single fire could damage more than one safe shutdown train does
not create the possibility of a new or different kind of accident from
any accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No. The proposed activity involves the use of a risk-
informed, performance-based method to identify those circuits where a
single fire could damage more than one safe shutdown train. These
circuits would then be provided with one hour rated fire wrap. With the
exception of the fire wrap itself, the proposed activity does not
result in any physical changes to safety-related structures, systems,
or components (SSCs), or the manner in which safety-related SSCs are
operated, maintained, modified, tested, or inspected. The proposed
activity does not degrade the performance or increase the challenges of
any safety-related SSCs assumed to function in the accident analysis.
The proposed activity does not impact plant safety since the
conclusions of the fire safe shutdown analysis remain unchanged.
Therefore, providing one hour rated fire wrap for those circuits
where a single fire could damage more than one safe shutdown train does
not involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and
Strawn, 1700 K Street, NW., Washington, DC 20006-3817.
NRC Section Chief: David Terao.
Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric
Station, Unit 3, St. Charles Parish, Louisiana
Date of amendment request: July 21, 2005.
Description of amendment request: The amendment proposes to replace
the existing steam generator tube surveillance program with that being
proposed by the Technical Specification Task Force (TSTF) in TSTF 449,
Revision 4.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No. The proposed change requires a Steam Generator
Program that includes performance criteria that will provide reasonable
assurance that the steam generator (SG) tubing will retain integrity
over the full range of operating conditions (including startup,
operation in the power range, hot standby, cooldown and all anticipated
transients included in the design specification). The SG performance
criteria are based on tube structural integrity, accident induced
leakage, and operational leakage.
The structural integrity performance criterion is:
Structural integrity performance criterion: All in-service steam
generator tubes shall retain structural integrity over the full range
of normal operating conditions (including startup, operation in the
power range, hot standby, and cool down and all anticipated transients
included in the design specification) and design basis accidents. This
includes retaining a safety factor of 3.0 against burst under normal
steady state full power operation primary to secondary pressure
differential and a safety factor of 1.4 against burst applied to the
design basis accident primary to secondary pressure differentials.
Apart from the above requirements, additional loading conditions
associated with the design basis accidents, or combination of accidents
in accordance with the design and licensing basis, shall also be
evaluated to determine if the associated loads contribute significantly
to burst or collapse. In the assessment of tube integrity, those loads
that do significantly affect burst or collapse shall be determined and
assessed in combination with the loads due to pressure with a safety
factor of 1.2 on the combined primary loads and 1.0 on axial secondary
loads.
The accident induced leakage performance criterion is: The primary
to secondary accident induced leakage rate for any design basis
accidents, other than a SG tube rupture, shall not exceed the leakage
rate assumed in the accident analysis in terms of total leakage rate
for all SGs and leakage rate for an individual SG. Leakage is not to
exceed 540 gallons per day through any one SG, except for specific
types of degradation at specific locations as described in paragraph c
of the Steam Generator Program.
The operational leakage performance criterion is: The RCS
operational primary to secondary leakage through any one SG shall be
limited to <= 75 gallons per day per SG.
A steam generator tube rupture (SGTR) event is one of the design
basis accidents that is analyzed as part of a plant's licensing basis.
In the analysis of a SGTR event, a bounding primary to secondary
leakage rate equal to the leakage rate associated with a double-ended
rupture of a single tube is assumed.
For other design basis accidents such as main steam line break
(MSLB), control element assembly (CEA) ejection, and reactor coolant
pump seized rotor/sheared shaft, the tubes are assumed to retain their
structural integrity (i.e., they are assumed not to rupture). The
accident induced leakage criterion introduced by the proposed changes
account for tubes that may leak during design basis accidents. The
accident induced leakage criterion limits this leakage to no more than
the value assumed in the accident analysis.
The SG performance criteria proposed change identify the standards
against which tube integrity is to be measured. Meeting the performance
criteria provides reasonable assurance that the SG tubing will remain
capable of fulfilling its specific safety function of maintaining
reactor coolant pressure boundary integrity throughout each operating
cycle and in the unlikely event of a design basis accident. The
performance criteria are only a part of
[[Page 61660]]
the Steam Generator Program required by the proposed change. The
program, defined by NEI [Nuclear Energy Institute] 97-06, Steam
Generator Program Guidelines, includes a framework that incorporates a
balance of prevention, inspection, evaluation, repair, and leakage
monitoring.
The consequences of design basis accidents are, in part, functions
of the Specific Activity in the primary coolant and the primary to
secondary leakage rates resulting from an accident. Therefore, limits
are included in the plant technical specifications for operational
leakage and for Specific Activity in primary coolant to ensure the
plant is operated within its analyzed condition. For those analyzed
events that do not result in faulted steam generators, greater than or
equal to 75 gpd [gallons per day] primary to secondary leakage per
steam generator is assumed in the analysis. For those analyzed events
that result in a faulted steam generator (e.g., MSLB), 540 gpd primary
to secondary leakage is assumed though the faulted steam generator
while greater than or equal to 75 gpd primary to secondary leakage is
assumed though the intact steam generator.
The proposed change does not affect the design of the SGs, their
method of operation, or primary coolant chemistry controls. The
proposed approach updates the current technical specifications and
enhances the requirements for SG inspections. The proposed change does
not adversely impact any other previously evaluated design basis
accident and is an improvement over the current Technical
Specifications.
Therefore, the proposed change does not affect the consequences of
a SGTR accident and the probability of such an accident is reduced. In
addition, the proposed changes do not affect the consequences of other
design basis events.
2. Does the proposed change create the possibility of a new or
different kind of accident from any previously evaluated?
Response: No. The proposed performance based requirements are an
improvement over the requirements imposed by the current technical
specifications.
Implementation of the proposed Steam Generator Program will not
introduce any adverse changes to the plant design basis or postulated
accidents resulting from potential tube degradation. The result of the
implementation of the Steam Generator Program will be an enhancement of
SG tube performance. Primary to secondary leakage that may be
experienced during all plant conditions will be monitored to ensure it
remains within current accident analysis assumptions.
The proposed change does not affect the design of the SGs, their
method of operation, or primary or secondary coolant chemistry
controls. In addition, the proposed change does not impact any other
plant system or component.
The change enhances SG inspection requirements. Therefore, the
proposed change does not create the possibility of a new or different
type of accident from any accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No. The SG tubes in pressurized water reactors are an
integral part of the reactor coolant pressure boundary and, as such,
are relied upon to maintain the primary system's pressure and
inventory. As part of the reactor coolant pressure boundary, the SG
tubes are unique in that they are also relied upon as a heat transfer
surface between the primary and secondary systems such that residual
heat can be removed from the primary system. In addition, the SG tubes
isolate the radioactive fission products in the primary coolant from
the secondary system. In summary, the safety function of a SG is
maintained by ensuring the integrity of its tubes.
Steam generator tube integrity is a function of the design,
environment, and the physical condition of the tube. The proposed
change does not affect tube design or operating environment. The
proposed change is expected to result in an improvement in the tube
integrity by implementing the Steam Generator Program to manage SG tube
inspection, assessment, repair, and plugging. The requirements
established by the Steam Generator Program are consistent with those in
the applicable design codes and standards and are an improvement over
the requirements in the current technical specifications.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: N.S. Reynolds, Esquire, Winston & Strawn
1700 K Street, NW., Washington, DC 20006-3817.
NRC Section Chief: David Terao.
Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey
Point Plant, Units 3 and 4, Miami-Dade County, Florida
Date of amendment request: July 21, 2005.
Description of amendment request: The requested change will delete
Technical Specification (TS) 6.9.1.2 related to Occupational Radiation
Exposure Reports and TS 6.9.1.5, ``Monthly Operating Reports.''
Basis for proposed no significant hazards consideration
determination: The NRC staff issued a notice of availability of a model
no significant hazards consideration (NSHC) determination for
referencing in license amendment applications in the Federal Register
on June 23, 2004 (69 FR 35067). The licensee affirmed the applicability
of the model NSHC determination in its application dated July 21, 2005.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
1. Does the proposed change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No. The proposed change eliminates the Technical
Specifications (TSs) reporting requirements to provide a monthly
operating letter report of shutdown experience and operating statistics
if the equivalent data is submitted using an industry electronic
database. It also eliminates the TS reporting requirement for an annual
occupational radiation exposure report, which provides information
beyond that specified in NRC regulations. The proposed change involves
no changes to plant systems or accident analyses. As such, the change
is administrative in nature and does not affect initiators of analyzed
events or assumed mitigation of accidents or transients. Therefore, the
proposed change does not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No. The proposed change does not involve a physical
alteration of the plant, add any new equipment, or require any existing
equipment to be operated in a manner different from the present design.
Therefore, the proposed change does not create the possibility of a new
or different kind of accident from any accident previously evaluated.
[[Page 61661]]
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No. This is an administrative change to reporting
requirements of plant operating information and occupational radiation
exposure data, and has no effect on plant equipment, operating
practices or safety analyses assumptions. For these reasons, the
proposed change does not involve a significant reduction in the margin
of safety.
Based upon the reasoning presented above, the requested change does
not involve significance hazards consideration.
Attorney for licensee: M.S. Ross, Attorney, Florida Power & Light,
P.O. Box 14000, Juno Beach, Florida 33408-0420.
NRC Section Chief: Michael L. Marshall, Jr.
Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-389,
St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
Date of amendment request: September 1, 2005.
Description of amendment request: The requested change will delete
Technical Specification (TS) 6.9.1.2 related to Occupational Radiation
Exposure Reports and TS 6.9.1.6, ``Monthly Operating Reports.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in the
probability or consequences of an accident previously evaluated?
No. The proposed change eliminates the Technical Specifications
(TSs) reporting requirements to provide a monthly operating report of
shutdown experience and operating statistics if the equivalent data is
submitted using an industry electronic database. It also eliminates the
TS reporting requirement for an annual occupational radiation exposure
report, which provides information beyond that specified in NRC
regulations. The proposed change involves no changes to plant systems
or accident analyses. As such, the change is administrative in nature
and does not affect initiators of analyzed events or assumed mitigation
of accidents or transients. Therefore, the proposed change does not
involve a significant increase in the probability or consequences of an
accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
No. The proposed change does not involve a physical alteration of
the plant, add any new equipment, or require any existing equipment to
be operated in a manner different from the present design. Therefore,
the proposed change does not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
No. This is an administrative change to reporting requirements of
plant operating information and occupational radiation exposure data,
and has no effect on plant equipment, operating practices or safety
analyses assumptions. For these reasons, the proposed change does not
involve a significant reduction in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: M.S. Ross, Attorney, Florida Power & Light,
P.O. Box 14000, Juno Beach, Florida 33408-0420.
NRC Section Chief: Michael L. Marshall, Jr.
Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear
Station, Nemaha County, Nebraska
Date of amendment request: July 21, 2005.
Description of amendment request: The proposed amendment would
revise Technical Specification (TS) testing frequency for the
surveillance requirement (SR) in TS 3.1.4, ``Control Rod Scram Times.''
Specifically, the proposed change would revise the frequency for SR
3.1.4.2, control rod scram time testing, from ``120 days cumulative
operation in MODE 1'' to ``200 days cumulative operation in MODE 1.''
The NRC staff issued a notice of availability of a model no
significant hazards consideration (NSHC) determination for referencing
in licensing amendment applications in the Federal Register on August
23, 2004 (69 FR 51864). The licensee affirmed the applicability of the
model NSHC determination in its application dated July 21, 2005.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), an analysis of the issue
of no significant hazards consideration is presented below:
1. Does the change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No. The proposed change extends the frequency for testing
control rod scram time testing from every 120 days of cumulative Mode 1
operation to 200 days of cumulative Mode 1 operation. The frequency of
surveillance testing is not an initiator of any accident previously
evaluated. The frequency of surveillance testing does not affect the
ability to mitigate any accident previously evaluated, as the tested
component is still required to be operable. Therefore, the proposed
change does not involve a significant increase in the probability or
consequences of an accident previously evaluated.
2. Does the change create the possibility of a new or different
kind of accident from any accident previously evaluated?
Response: No. The proposed change extends the frequency for testing
control rod scram time testing from every 120 days of cumulative Mode 1
operation to 200 days of cumulative Mode 1 operation. The proposed
change does not result in any new or different modes of plant
operation. Therefore, the proposed change does not create the
possibility of a new or different kind of accident from any previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No. The proposed change extends the frequency for testing
control rod scram time testing from every 120 days of cumulative Mode 1
operation to 200 days of cumulative Mode 1 operation. The proposed
change continues to test the control rod scram time to ensure the
assumptions in the safety analysis are protected. Therefore, the
proposed change does not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. John R. McClure, Nebraska Public Power
District, Post Office Box 499, Columbus, NE 68602-0499.
[[Page 61662]]
NRC Section Chief: David Terao.
Southern Nuclear Operating Company, Inc., Georgia Power Company,
Oglethorpe Power Corporation, Municipal Electric Authority of Georgia,
City of Dalton, Georgia, Docket Nos. 50-321 and 50-366, Edwin I. Hatch
Nuclear Plant, Units 1 and 2, Appling County, Georgia
Date of amendment request: November 12, 2004, as supplemented by
letters dated September 2 and September 16, 2005.
Description of amendment request: The proposed amendments would
revise Technical Specifications 3.1.7, ``Standby Liquid Control (SLC)
System,'' for Hatch, Units 1 and 2. The proposed amendments would
update Figures 3.1.7-1 and 3.1.7-2 for Units 1 and 2 TS to reflect the
increased concentration of Boron-10 in the solution. Conforming
revisions to Bases B 3.1.7, ``Standby Liquid Control (SLC) System'' are
also included.
The proposed amendment was previously noticed on February 1, 2005
(70 FR 5249).
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in the
probability or consequences of an accident previously evaluated?
This is a proposed change to Figures 3.1.7-1 and 3.1.7-2 of the
Units 1 and 2 TS [Technical Specifications]. Figure 3.1.7-1 is a plot
of the weight percent of Sodium Pentaborate solution in the Standby
Liquid Control (SLC) Tank, as a function of the gross volume of
solution in the tank. Figure 3.1.7-2 is a plot of the Sodium
Pentaborate temperature versus concentration requirements.
Figure 3.1.7-1 is proposed to be changed in order to accommodate an
injection of Sodium Pentaborate solution into the reactor, following an
ATWS [anticipated transient without scram] event, such that the
concentration of Boron-10 atoms in the reactor will be 800 ppm natural
Boron equivalent. This is necessary to accommodate increased cycle
energy requirements for the Hatch Units 1 and 2 cores. Both Figures
3.1.7-1 and 3.1.7-2 are changed to reflect that the boundary between
Region A and B is changing from 6.9% to 7.0%. The proposed change to
the Figures will not increase the probability of an ATWS event because
the curves have nothing to do with the prevention of an ATWS event. The
new requirements will insure that, in the future, the core will have
adequate shutdown margin to mitigate the consequences of an ATWS event.
The minimum concentration of Sodium Pentaborate which also
represents the boundary between Region A and Region B, is changing from
6.9% to 7.0%. This increase in the concentration ensures a conservative
margin to the ATWS equivalency determination required by 10 CFR 50.62.
Also, no systems or components designed to ensure the safe shutdown
of the reactor are being physically changed as a result of this
proposed TS change. In fact, no safety related systems or components
designed for the prevention of previously evaluated events are being
altered by the amendment.
2. The proposed change does not create the possibility of a new or
different kind of accident from any previously evaluated.
This proposed TS revision results in a change to SLC TS Figures
3.1.7-1 and 3.1.7-2 requirements. However, these changes do not result
in physical changes to the SLC system. SLC pump operation, maintenance
and testing remain the same. Accordingly, no changes to the operation,
maintenance or surveillance procedures will result from this TS
revision request. Therefore, no new modes of operation are introduced
by this TS change.
Since no new modes of operation are introduced, the proposed change
does not create the possibility of a new or different type event from
any previously evaluated.
3. The proposed change does not involve a significant reduction in
the margin of safety.
This proposed TS change is being made to increase the boron
concentration requirements of the sodium pentaborate solution injected
into the reactor vessel following an Anticipated Transient Without
Scram (ATWS) event. The change is necessary due to new fuel designs and
higher energy requirements for fuel cycles. Therefore, the change is
being made to insure that shutdown requirements can be met for the ATWS
event. This will insure the margin of safety with respect to ATWS will
continue to be met.
The increase in the minimum concentration from 6.9% to 7.0% ensures
a conservative margin with respect to the ATWS equivalency
determination. Consequently, this proposed TS change will not result in
a decrease in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw,
Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC
20037.
NRC Section Chief: Evangelos C. Marinos.
Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
Date of amendment request: September 1, 2005 (TS-05-04).
Description of amendment request: The proposed amendment would
revise the reactor protection system turbine trip allowable value for
low trip system pressure from greater than or equal to 43 pounds per
square inch gauge (psig) to 39.5 psig. This change would allow the
instrumentation that performs this trip function to be tested and
verified to be operable within the capabilities of the pressure
switches.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No. The proposed change revises the allowable value for
reactor trip as a result of a turbine trip on low trip system pressure.
This change will not alter any plant components, systems, or processes
and will only provide a more appropriate value to assess operability of
the associated pressure switches. Since the plant features and
operating practices are not altered, the possibility of an accident is
not affected. This reactor trip is not directly credited in SQN's
accident analysis and is maintained as an anticipatory trip to enhance
the overall reliability of the reactor trip system. As such, there is
not a specific safety limit associated with this function and the
generation of a reactor trip based on low trip system pressure is above
the required actuations to ensure acceptable mitigation of accidents.
As the proposed change will continue to provide an acceptable
anticipatory trip signal, the offsite dose potential is not affected by
this change. Therefore, the proposed change does not involve a
significant increase in the probability or
[[Page 61663]]
consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No. As described above, this change will not alter any
plant equipment or operating practices that have the ability to create
a new potential for accident generation. The proposed change revises
the operability limits for a function that generates a trip signal when
appropriate conditions exist to require accident mitigation response.
This type of function does not have the ability to create an accident
as its purpose and function is to mitigate events. Therefore, the
proposed change does not create the possibility of a new or different
kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No. The proposed change will revise an allowable value
for a reactor trip initiator that results from a turbine trip
condition. This change will not alter the setpoint, and the calibration
of the associated pressure switches will continue to be set at the
current values. The allowable value change is in response to accuracy
aspects of the instrumentation and does not alter the ability of this
trip function to operate when and as needed to mitigate accident
conditions.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: General Counsel, Tennessee Valley Authority,
400 West Summit Hill Drive, ET 11A, Knoxville, Tennessee 37902.
NRC Section Chief: Michael L. Marshall, Jr.
Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek
Generating Station, Coffey County, Kansas
Date of amendment request: August 26, 2005.
Description of amendment request: The amendment would authorize
changes to the Updated Safety Analysis Report (USAR) for Wolf Creek
Generating Station (WCGS) that would revise the methodology for the
reactor coolant system (RCS) leak detection instrumentation. This
revision would clarify the requirements of the containment atmosphere
gaseous radioactivity monitor with regard to the RCS leak detection
capability and would justify that the monitor can be considered
operable in compliance with Limiting Condition for Operation 3.4.15, in
Technical Specification (TS) 3.4.15, ``RCS Leakage Detection
Instrumentation,'' during all applicable Modes. There are no proposed
changes to the WCGS TSs.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed change does not involve a significant increase in
the probability or consequences of an accident previously evaluated.
The proposed change has been evaluated and determined to not
increase the probability or consequences of an accident previously
evaluated. The proposed change does not make hardware changes and does
not alter the configuration of any plant system, structure, or
component (SSC). The proposed change only clarifies the design and
OPERABILITY requirements for the containment atmosphere gaseous
radioactivity monitors and identifies the capabilities of the monitors
at low RCS [radio]activity levels. The containment atmosphere gaseous
radioactivity monitors are not initiators of any accident; therefore,
the probability of occurrence of an accident is not increased. The USAR
and TSs will continue to require diverse means of [RCS] leakage
detection equipment, thus ensuring that leakage due to cracks [in the
RCS] would continue to be identified prior to propagating to the point
of a[n] [RCS] pipe break. Therefore, the consequences of an accident
[previously evaluated] are not increased.
2. The proposed change does not create the possibility of a new or
different kind of accident from any accident previously evaluated.
The proposed change does involve the use or installation of new
equipment and the currently installed equipment will not be operated in
a new or different manner. No new or different system interactions are
created and no new processes are introduced. The proposed changes will
not introduce any new failure mechanisms, malfunctions, or accident
initiators not already considered in the design and licensing basis
[for WCGS]. The proposed change does not affect any SSC associated with
an accident initiator. Based on this evaluation, the proposed change
does not create the possibility of a new or different kind of accident
from any accident previously evaluated.
3. The proposed change does not involve a significant reduction in
a margin of safety.
The proposed change does not alter any RCS leakage detection
components. The proposed change only clarifies the design and
operability requirements for the containment atmosphere gaseous
radioactivity monitor and identifies the capabilities of the
containment atmosphere gaseous radioactivity monitors at low RCS
[radio]activity levels. This change is required since the level of
radioactivity in the WCGS reactor coolant has become much lower than
what was assumed in the USAR and the gaseous channel [(monitor)] can no
longer promptly detect a small RCS leak under all operating conditions.
The proposed amendment continues to require diverse means of [RCS]
leakage detection equipment with [the] capability to promptly detect
RCS leakage. Although not required by [the] TS[s], additional diverse
means of leakage detection capability are available as described in the
USAR Section 5.2.5. Early detection of [RCS] leakage, as the potential
indicator of a crack(s) in the RCS pressure boundary, will thus
continue to be in place so that such a condition is known and
appropriate actions [are] taken well before any such crack would
propagate to a more severe condition. Based on this evaluation, the
proposed change does not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and
Trowbridge, 2300 N Street, NW., Washington, DC 20037.
NRC Section Chief: Daniel S. Collins, Acting.
Notice of Issuance of Amendments to Facility Operating Licenses
During the period since publication of the last biweekly notice,
the Commission has issued the following amendments. The Commission has
determined for each of these amendments that the applicati