Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 59082-59096 [05-20168]
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59082
Federal Register / Vol. 70, No. 195 / Tuesday, October 11, 2005 / Notices
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meetings where this material is being
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agreements are effective and related to
the material being discussed.
The DFO should be informed of such
an agreement at least five working days
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made regarding the applicability of the
agreement to the material that will be
discussed during the meeting. The
minimum information provided should
include information regarding the date
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executed agreement should be provided
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meeting for admittance to the closed
session.
Dated: October 5, 2005.
Annette L. Vietti-Cook,
Secretary of the Commission.
[FR Doc. 05–20317 Filed 10–7–05; 8:45 am]
BILLING CODE 7590–01–P
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from September
6, 2005, to September 29, 2005. The last
biweekly notice was published on
September 27, 2005 (70 FR 56499).
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Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
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Federal Register / Vol. 70, No. 195 / Tuesday, October 11, 2005 / Notices
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
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with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
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the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
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59084
Federal Register / Vol. 70, No. 195 / Tuesday, October 11, 2005 / Notices
Carolina Power & Light Company, et al.,
Docket No. 50–400, Shearon Harris
Nuclear Power Plant, Unit 1, Wake and
Chatham Counties, North Carolina
Date of amendment request: April 6,
2005, as supplemented by letter dated
August 8, 2005.
Description of amendment request:
The proposed amendment will modify
Technical Specification (TS) 6.8.4.k,
‘‘Containment Leakage Rate Testing
Program,’’ and TS Surveillance
Requirement (SR) 4.6.1.6.1,
‘‘Containment Vessel Surfaces.’’ The
proposed amendment would modify the
TS to allow for a one-time extension of
the containment Type A test interval
from once in 10 years to once in 15
years.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
This change does not involve a
significant hazards consideration for the
following reasons:
1. The proposed amendment does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The proposed change to HNP [Harris
Nuclear Plant] TS 6.8.4.k and TS SR 4.6.1.6.1
provide a one-time extension of the
containment Type A test interval from 10
years to 15 years and specifies that additional
visual inspections are done in accordance
with Subsections IWE and IWL of the ASME
[American Society of Mechanical Engineers]
Section XI Code. The existing 10-year test
interval is based on past test performance.
The proposed TS change does not involve a
physical change to the plant or a change in
the manner in which the plant is operated or
controlled. The containment vessel is
designed to provide a leak-tight barrier
against the uncontrolled release of
radioactivity to the environment in the
unlikely event of postulated accidents. As
such, the containment vessel is not
considered as the initiator of an accident.
Therefore, the proposed TS change does not
involve a significant increase in the
probability of an accident previously
evaluated.
The proposed change involves only a onetime change to the interval between
containment Type A tests. Type B and C
leakage testing will continue to be performed
at the intervals specified in 10 CFR Part 50,
Appendix J, Option A, as required by the
HNP TS. As documented in NUREG–1493,
‘‘Performance-Based Containment LeakageTest Program,’’ industry experience has
shown that Type B and C containment leak
rate tests have identified a very large
percentage of containment leak paths, and
that the percentage of containment leak paths
that are detected only by Type A testing is
very small. In fact, an analysis of 144
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integrated leak rate tests, including 23
failures, found that none of the failures
involved a containment liner breach.
NUREG–1493 also concluded, in part, that
reducing the frequency of containment Type
A testing to once per 20 years results in an
imperceptible increase in risk. The HNP test
history and risk-based evaluation of the
proposed extension to the Type A test
interval supports this conclusion. The design
and construction requirements of the
containment vessel, combined with the
containment inspections performed in
accordance with the American Society of
Mechanical Engineers (ASME) Code, Section
XI, and the Maintenance Rule (10 CFR 50.65)
provide a high degree of assurance that the
containment vessel will not degrade in a
manner that is detectable only by Type A
testing. Therefore, the proposed TS change
does not involve a significant increase in the
consequences of an accident previously
evaluated.
Therefore, this change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. The proposed amendment does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
The proposed change to HNP TS 6.8.4.k
and TS SR 4.6.1.6.1 provide a one-time
extension of the containment Type A test
interval to 15 years and specifies that
additional visual inspections are done in
accordance with Subsections IWE and IWL of
the ASME Section XI Code. The existing 10year test interval is based on past test
performance. The proposed change to the
Type A test interval does not result in any
physical changes to HNP. In addition, the
proposed test interval extension does not
change the operation of HNP such that a
failure mode involving the possibility of a
new or different kind of accident from any
accident previously evaluated is created.
Thus, this change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. The proposed amendment does not
involve a significant reduction in a margin of
safety.
The proposed change to HNP TS 6.8.4.k
and TS SR 4.6.1.6.1 provide a one-time
extension of the containment Type A test
interval from 10 years to 15 years and
specifies that additional visual inspections
are done in accordance with Subsections IWE
and IWL of the ASME Section XI Code. The
existing 10-year test interval is based on past
test performance. The NUREG–1493 study of
the effects of extending containment leak rate
testing found that a 20 year extension for
Type A testing resulted in an imperceptible
increase in risk to the public. NUREG–1493
found that, generically, the design
containment leak rate contributes a very
small amount to the individual risk and that
the decrease in Type A testing frequency
would have a minimal affect on this risk
since most potential leak paths are detected
by Type B and C testing. The proposed
change involves only a one-time extension of
the interval for containment Type A testing;
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the overall containment leak rate specified by
the HNP TS is being maintained. Type B and
C testing will continue to be performed at the
frequency required by the HNP TS. The
regular containment inspections being
performed in accordance with the ASME
Code, Section XI, and the Maintenance Rule
(10 CFR 50.65) provide a high degree of
assurance that the containment will not
degrade in a manner that is only detectable
by Type A testing. In addition, a plantspecific risk evaluation has demonstrated
that the one-time extension of the Type A test
interval from 10 years to 15 years results in
a very small increase in risk for those
accident sequences influenced by Type A
testing.
Therefore, this change does not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Section Chief: Michael L.
Marshall, Jr.
Carolina Power & Light Company, et al.,
Docket No. 50–400, Shearon Harris
Nuclear Power Plant (HNP), Unit 1,
Wake and Chatham Counties, North
Carolina
Date of amendment request: June 20,
2005.
Description of amendment request:
The amendment would revise Technical
Specifications (TS) 3/4.4.7, ‘‘Reactor
Coolant System Chemistry.’’
Specifically, the proposed amendment
would revise the footnotes in Tables
3.4–2 and 4.4–3 of the TS to increase the
temperature limit from 180 °F to 250 °F
above which reactor coolant sampling
and analysis for dissolved oxygen is
required and dissolved oxygen limits
apply.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
This amendment does not involve a
significant hazards consideration for the
following reasons:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Operation of HNP in accordance with the
proposed amendment does not increase the
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Federal Register / Vol. 70, No. 195 / Tuesday, October 11, 2005 / Notices
probability or consequences of accidents
previously evaluated. The Final Safety
Analysis Report (FSAR) documents the
analyses of design basis accidents (DBA) at
HNP. Any scenario or previously analyzed
accident that results in offsite dose were
evaluated as part of this analysis. The
proposed amendment does not change or
affect any accident previously evaluated in
the FSAR. The proposed amendment does
not modify any plant equipment. In addition,
the proposed amendment does not result in
a change to a structure, system, or component
(SSC), or adversely affect its design function.
The purpose of the temperature limit for
RCS [Reactor Coolant System] oxygen control
is to minimize corrosion at high temperatures
on RCS components. Increasing the
temperature at which oxygen levels are
required to be maintained within specified
limits from 180 °F to 250 °F is supported by
industry and vendor data which indicates
that the influence of dissolved oxygen at or
below 250 °F is not significant with regard
to stress corrosion cracking and general
corrosion of RCS components. The proposed
amendment is consistent with the Electric
Power Research Institute’s (EPRI’s)
guidelines for Pressurized Water Reactor
(PWR) Primary Water Chemistry. This
amendment places HNP in line with standard
industry specifications for reactors of similar
size and vintage. HNP’s proposed
amendment to increase the temperature limit
for applicability to 250 °F would decrease the
time needed to achieve compliance with the
dissolved oxygen limit and decrease the
overall time to restart the plant from cold
shutdown. Removing oxygen in a more
expeditious fashion enhances RCS chemistry.
Based on the above, RCS integrity is
maintained by this amendment.
Therefore, this amendment does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
Operation of HNP in accordance with the
proposed amendment does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated. The FSAR documents the analyses
of design basis accidents (DBA) at HNP. Any
scenario or previously analyzed accident that
results in offsite dose were evaluated as part
of this analysis. The proposed amendment
does not change or affect any accident
previously evaluated in the FSAR, and no
new or different scenarios are created by the
proposed amendment to the TS. The
proposed amendment does not modify any
plant equipment. In addition, the proposed
amendment does not result in a change to an
SSC [structure, system, or component] or
adversely affect its design function.
The purpose of the temperature limit for
RCS oxygen control is to minimize corrosion
at high temperatures on RCS components.
Increasing the temperature at which oxygen
levels are required to be maintained within
specified limits from 180 °F to 250 °F is
supported by industry and vendor data
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which indicates that the influence of
dissolved oxygen at or below 250 °F is not
significant with regard to stress corrosion
cracking and general corrosion of RCS
components. The proposed amendment is
consistent with EPRI’s guidelines for PWR
Primary Water Chemistry. This amendment
places HNP in line with standard industry
specifications for reactors of similar size and
vintage. HNP’s proposed amendment to
increase the temperature limit for
applicability to 250 °F would decrease the
time needed to achieve compliance with the
dissolved oxygen limit and decrease the
overall time to restart the plant from cold
shutdown. Removing oxygen in a more
expeditious fashion enhances RCS chemistry.
Based on the above, RCS integrity is
maintained by this amendment.
Therefore, this amendment does not create
the possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
Operation of HNP in accordance with the
proposed amendment does not involve a
significant reduction in a margin of safety.
Existing TS operability and surveillance
requirements are not reduced by the
proposed amendment. The proposed
amendment does not modify any plant
equipment. In addition, the proposed
amendment does not result in a change to a
structure, system, or component (SSC), or its
design function. The proposed amendment
does not adversely affect existing plant safety
margins or the reliability of equipment
assumed to mitigate accidents in the FSAR.
The purpose of the temperature limit for
RCS oxygen control is to minimize corrosion
at high temperatures on RCS components.
Increasing the temperature at which oxygen
levels are required to be maintained within
specified limits from 180 °F to 250 °F is
supported by industry and vendor data
which indicates that the influence of
dissolved oxygen at or below 250 °F is not
significant with regard to stress corrosion
cracking and general corrosion of RCS
components. The proposed amendment is
consistent with EPRI’s guidelines for PWR
Primary Water Chemistry. This amendment
places HNP in line with standard industry
specifications for reactors of similar size and
vintage. HNP’s proposed amendment to
increase the temperature limit for
applicability to 250 °F would decrease the
time needed to achieve compliance with the
dissolved oxygen limit and decrease the
overall time to restart the plant from cold
shutdown. Removing oxygen in a more
expeditious fashion enhances RCS chemistry.
Based on the above, RCS integrity is
maintained by this amendment.
Therefore, this amendment does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
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59085
amendment request involves no
significant hazards consideration.
Attorney for licensee: David T.
Conley, Associate General Counsel II—
Legal Department, Progress Energy
Service Company, LLC, Post Office Box
1551, Raleigh, North Carolina 27602.
NRC Section Chief: Michael L.
Marshall, Jr.
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request: June 20,
2005.
Description of amendment request:
The proposed amendment would revise
Cooper Nuclear Station (CNS) Technical
Specification (TS) 5.3, ‘‘Unit Staff
Qualifications,’’ to upgrade the
qualification standard for the Shift
Manager, Senior Operator, Licensed
Operator, and Shift Technical Engineer
from Regulatory Guide (RG) 1.8,
Revision 2 ‘‘Qualification and Training
of Personnel for Nuclear Power Plants,’’
to RG 1.8, Revision 3. It also clarifies
qualification requirements applicable to
the Operations Manager position.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
These changes are administrative in nature
and do not require any physical
modifications, affect any plant components,
or result in any changes in plant operation.
They provide clarity and consistency to the
CNS licensing basis.
Upgrading the unit staff qualifications for
the Shift Manager, Senior Operator, Licensed
Operator, and Shift Technical Engineer from
Regulatory Guide 1.8, Revision 2, to
Regulatory Guide 1.8, Revision 3, is an
administrative change that will clarify the
current requirements for qualification and
training of operations personnel. The changes
are consistent with the application of a
systems approach to training in an accredited
training program. By promulgation of the 10
CFR Part 55 rule change, the NRC determined
that an accredited licensed operator training
program based on a systems approach to
training provides an acceptable means of
qualifying licensed operating personnel.
The addition of qualification requirements
for the Operations Manager position clarifies
SRO [Senior Reactor Operator] license
requirements for Operations management
personnel by specifying that the Operations
Supervisor is the member of Operations
management required to have a current SRO
license at CNS. The Operations Manager is
required to hold or have previously held a
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SRO license. This will ensure an acceptable
level of operations knowledge to perform in
a managerial oversight role. This approach is
consistent with current guidance in ANSI/
ANS [American Nuclear Standards Institute/
American Nuclear Society] 3.1–1993. This
change is administrative in nature and has no
impact on previously evaluated accidents.
Therefore, these changes do not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
These changes are administrative in nature
and do not involve a physical alteration of
the plant or a change to plant operations. No
new failure mechanisms, malfunctions, or
accident initiators are introduced. The
proposed changes provide clarity and
consistency to the CNS licensing basis in
regard to training and qualification of
operations personnel and SRO license
requirements for Operations management
personnel.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
evaluated.
Response: No.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
These changes are administrative in nature
and do not affect any Technical Specification
safety limit or limiting condition for
operation. No safety margins are affected by
these changes. The proposed changes do not
involve a change in plant design or operation
for the mitigation of postulated accidents.
The proposed changes provide clarity and
consistency to the CNS licensing basis in
regard to training and qualification of
operations personnel and SRO license
requirements for Operations management
personnel.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John C.
McClure, Nebraska Public Power
District, Post Office Box 499, Columbus,
NE 68602–0499.
NRC Section Chief: David Terao.
Nebraska Public Power District, Docket
No. 50–298, Cooper Nuclear Station,
Nemaha County, Nebraska
Date of amendment request: August
25, 2005.
Description of amendment request:
The proposed amendment would revise
the definitions of Channel Calibration,
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Channel Function Test, and Logic
System Functional Test in accordance
with the Technical Specification Task
Force Traveler 205–A.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
done. Revising these definitions as proposed
will not result in a change to the design or
operation of any plant SSC used to shutdown
the plant, initiate the Emergency Core
Cooling Systems, or isolate primary or
secondary containment. As a result the
ability of the plant to respond to and mitigate
accidents is unchanged by the revised
definitions.
Based on the above, NPPD concludes that
the proposed changes do not involve a
significant reduction in a margin of safety.
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The definitions of Channel Calibration,
Channel Functional Test, and Logic System
Functional Test specified in Technical
Specifications (TS) provide basic information
regarding what the test involves, the
components involved in the test, and general
information regarding how the test is to be
performed. These definitions and their
specific wording are not precursors to any
accident. As a result these revised definitions
result in no increase in the probability of an
accident previously evaluated.
The proposed revisions of these definitions
involve no changes to plant design,
equipment, or operation related to mitigation
of accidents. The proposed revisions of these
definitions do not change their meaning or
intent. The proposed revisions clarify the
definitions and do not result in a reduction
of required testing of instrumentation used to
mitigate accidents.
Based on the above NPPD [Nebraska Public
Power District] concludes that the proposed
changes do not involve a significant increase
in the probability or consequences of an
accident previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed revisions of the definitions
do not involve a change to the design or
operation of any plant structure, system, or
component (SSC). As a result the plant will
continue to be operated in the same manner.
The proposed revisions will not result in a
change to how the instrumentation used to
monitor plant operation and to mitigate
accidents is tested. Operating the plant and
testing the plant’s instrumentation in the
same manner as is currently done will not
create the possibility of a new or different
kind of accident.
Based on the above NPPD concludes that
the proposed changes do not create the
possibility of a new or different kind of
accident from any previously evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The affected definitions involve testing of
instrumentation used in the mitigation of
accidents to ensure that the instrumentation
will perform as assumed in safety analyses.
The proposed revisions of these definitions
will not change their meaning or intent. As
a result, the instrumentation will continue to
be tested in the same manner as is currently
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mr. John C.
McClure, Nebraska Public Power
District, Post Office Box 499, Columbus,
NE 68602–0499.
NRC Section Chief: David Terao.
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Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of amendment requests: July 29,
2005.
Description of amendment requests:
The proposed amendments would
revise Technical Specification 3.7.5,
‘‘Auxiliary Feedwater (AFW) System,’’
to change the frequency of Surveillance
Requirement 3.7.5.6 from 92 days to 24
months.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change to increase [the]
frequency interval for Surveillance
Requirement (SR) 3.7.5.6 from 92 days to 24
months has no impact on the probability of
accidents previously evaluated. The valves
controlled by SR 3.7.5.6 are used to provide
an alternate supply of water to the auxiliary
feedwater (AFW) system from the fire water
storage tank (FWST) and are only operated
after an accident has occurred. They are not
accident initiators.
Misoperation, or failure of a[n] FWST
supply to be correctly positioned following
an accident, could result in an inadequate
supply of water to the AFW system. Failure
to provide adequate core cooling could
increase the radiological consequences of an
accident. However, operating and
maintenance histories of the FWST supply
valves show that these valves have been
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capable of full stroke cycling each time they
have been tested. There is no evidence of any
time-related degradation mechanism that
would prevent the valves from performing
their design function. Thus[,] the proposed
change has no impact on the consequences
of an accident.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different [kind of]
accident from any accident previously
evaluated?
Response: No.
The proposed change to increase frequency
interval for SR 3.7.5.6 from 92 days to 24
months has no impact on the probability of
accidents of the type evaluated in the Final
Safety Analysis Report, as updated. The
valves are used to provide an alternate
supply of water to the AFW system from the
FWST, and are only operated after an
accident has occurred. They are not accident
initiators. Review of the operating and
maintenance histories of the FWST supply
valves show that they are highly reliable in
maintaining their capability to perform their
design function.
Therefore, the proposed change does not
create the possibility of a new or different
[kind of] accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change to SR 3.7.5.6
involves only an increase in the frequency
interval. No physical changes are required to
the facility or to the plant operating or
emergency procedures as a result of the
change. Based on review of the operating and
maintenance histories of the FWST supply
valves, they have been capable of full stroke
cycling each time they have been tested.
There is no evidence of any time-related
degradation mechanism that would prevent
the valves from performing their design
function. This evidence supports the
conclusion that there will be no impact in the
operation of these valves following an
accident.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee’s
analysis and, based on this review, it appears
that the three standards of 10 CFR 50.92(c)
are satisfied. Therefore, the NRC staff
proposes to determine that the amendment
requests involve no significant hazards
consideration.
Attorney for licensee: Richard F.
Locke, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Section Chief: Daniel S. Collins
(Acting).
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Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of amendment requests: August
23, 2005.
Description of amendment requests:
The proposed amendments would
revise the expiration dates of the Units
1 and 2 facility-operating licenses to
recapture low-power testing time, and to
reflect a 40-year term measured from the
date of issuance of each unit’s fullpower operating license.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed additional operating license
periods do not affect the probability or
consequences of an accident previously
evaluated since they require no physical
change in the plant equipment or operating
procedures and the Final Safety Analysis
Report (FSAR) Update safety analyses are
based on [a] 40-year full[-]power operation.
Surveillance and maintenance practices, as
well as other programs such as
environmental qualification of equipment,
ensure timely identification and correction of
any degradation of safety-related plant
equipment. The long-term integrity of the
reactor vessels has been evaluated using
currently acceptable NRC calculational
methods and best available Diablo Canyon
Power Plant (DCPP) specific data. The
evaluation results demonstrate that both
reactor vessels are safe for normal operations
in excess of 40 years.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different [kind of]
accident from any accident previously
evaluated?
Response: No.
The possibility of a new or different kind
of accident is not created by the proposed
additional operating periods since at least 40
years of full[-]power operation was assumed
in the design and construction of DCPP Units
1 and 2. The plant maintenance programs are
also designed to both maintain and
determine the need to replace safety-related
components. These programs will continue
to be applied as they are presently to assure
safe operation.
Therefore, the proposed change does not
create the possibility of a new or different
[kind of] accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
PO 00000
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59087
Response: No.
The proposed additional operating periods
do not involve a significant reduction in a
margin of safety since, as is the case with
present operation, degradation of safetyrelated equipment will be identified and
corrected by ongoing surveillance and
maintenance practices. Existing programs,
routine maintenance, and compliance with
Technical Specifications assure that an
adequate margin of safety is maintained.
These activities will remain in effect for the
duration of the proposed additional operating
periods.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Richard F.
Locke, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Section Chief: Daniel S. Collins
(Acting).
South Carolina Electric & Gas Company,
South Carolina Public Service
Authority, Docket No. 50–395, Virgil C.
Summer Nuclear Station, Unit No. 1,
Fairfield County, South Carolina
Date of amendment request: June 30,
2005.
Description of amendment request:
The proposed changes would revise the
Administrative Control section of the
Technical Specifications (TSs) to permit
the Westinghouse best estimate
methodology for loss-of-coolantaccident (LOCA) analysis methodology
to be utilized for analyses as required by
Title 10 of the Code of Federal
Regulations, Part 50, Section 46,
‘‘Acceptance criteria for emergency core
cooling systems [ECCS] for light water
nuclear power reactors’ (10 CFR 50.46).
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
Implementation of the best-estimate large
break LOCA methodology and associated TS
changes is proposed to increase margin to the
peak clad temperature limits defined in 10
CFR 50.46. There are no physical plant
changes or changes in manner in which the
plant will be operated as a result of this
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change. Since the plant conditions and ECCS
performance assumed in the analysis are
consistent with the plant’s current design,
the proposed change in methodology will
thus have no impact on the probability of a
LOCA. When applied, the best estimate
methodology shows that the ECCS is more
effective than previously evaluated in
mitigating the consequences of a LOCA, as
lower peak clad temperatures are predicted
relative to current 10 CFR 50.46 Appendix K
results. Since the proposed best-estimate
methodology is only applicable to a large
break LOCA and since the application of the
proposed methodology shows there is a high
probability that all of the acceptance criteria
contained in 10 CFR 50.46, Paragraph b are
met, the proposed change does not increase
the consequences of an accident previously
evaluated.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
There are no physical changes being made
to the plant. No new modes of plant
operation are being introduced. The
parameters assumed in the analysis remain
within the design limits of the existing plant
equipment. All plant systems will perform as
designed during the response to a potential
accident.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any previously
analyzed.
3. Does this change involve a significant
reduction in a margin of safety?
Response: No.
It has been shown that the methodology
used in the analysis would more realistically
describe the expected behavior of V. C.
Summer Nuclear Station systems during a
postulated loss of coolant accident.
Uncertainties have been accounted for as
required by 10 CFR 50.46. A sufficient
number of loss of coolant accidents with
different break sizes, different locations and
other variations in properties are analyzed to
provide assurance that the most severe
postulated loss of coolant accidents are
calculated. It has been shown by analysis that
there is a high level of probability that all
criteria contained in 10 CFR 50.46, Paragraph
b are met.
Pursuant to 10 CFR 50.91, the preceding
analyses provide a determination that the
proposed Technical Specifications change
poses no significant hazard as delineated by
10 CFR 50.92.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92 (c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Thomas G.
Eppink, South Carolina Electric & Gas
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Company, Post Office Box 764,
Columbia, South Carolina 29218.
NRC Section Chief: Evangelos C.
Marinos.
STP Nuclear Operating Company,
Docket Nos. 50–498 and 50–499, South
Texas Project, Units 1 and 2, Matagorda
County, Texas.
Date of amendment request: August
30, 2005.
Description of amendment request:
The proposed amendment would
change the Technical Specifications
(TSs) to reflect the use of the
Westinghouse Best Estimate Analyzer
for Core Operations—Nuclear
(BEACON) to augment the functional
capability of the flux mapping system
for the purpose of power distribution
surveillances. In addition, editorial
changes to the TSs are proposed.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The PDMS [power distribution monitoring
system] performs continuous core power
distribution monitoring. This system utilizes
the NRC-approved Westinghouse proprietary
computer code BEACON to provide data
reduction for incore flux maps, core
parameter analysis, load follow operation
simulation, and core prediction. It in no way
provides any protection or control system
function. Fission product barriers are not
impacted by these proposed changes. The
proposed changes occurring with PDMS will
not result in any additional challenges to
plant equipment that could increase the
probability of any previously evaluated
accident. The changes associated with the
PDMS do not affect plant systems such that
their function in the control of radiological
consequences is adversely affected. These
proposed changes will therefore not affect the
mitigation of the radiological consequences
of any accident described in the Updated
Final Safety Analysis Report Update
(UFSAR).
Continuous on-line monitoring through the
use of PDMS provides significantly more
information about the power distributions
present in the core than is currently
available. This results in more time (i.e.,
earlier determination of an adverse condition
developing) for operator action prior to
having an adverse condition develop that
could lead to an accident condition or to
unfavorable initial conditions for an
accident.
Each accident analysis addressed in the
UFSAR is examined with respect to changes
in cycle-dependent parameters, which are
obtained from application of the NRC-
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Frm 00061
Fmt 4703
Sfmt 4703
approved reload design methodologies, to
ensure that the transient evaluations of
reload cores are bounded by previously
accepted analyses. This examination, which
is performed in accordance with the
requirements set forth in 10 CFR [Title 10 of
the Code of Federal Regulations] 50.59,
ensures that future reloads will not involve
a significant increase in the probability or
consequences of any accident previously
evaluated.
The three editorial changes only correct
typographical errors made in previously
approved TS changes. They do not affect
plant operation or structures, systems, and
components important to safety.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequence of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The implementation of the PDMS has no
influence or impact on plant operations or
safety, nor does it contribute in any way to
the probability or consequences of an
accident. No safety-related equipment, safety
function, or plant operation will be altered as
a result of this proposed change. The
possibility for a new or different type of
accident from any accident previously
evaluated is not created since the changes
associated with implementation of the PDMS
do not result in a change to the design basis
of any plant component or system. The
evaluation of the effects of using the PDMS
to monitor core power distribution
parameters shows that all design standards
and applicable safety criteria limits are met.
The proposed changes do not result in any
event previously deemed incredible being
made credible. Implementation of the PDMS
will not result in more adverse conditions
and will not result in any increase in the
challenges to safety systems. The cyclespecific variables required by the PDMS are
calculated using NRC-approved methods.
The TS will continue to require operation
within the required core operating limits and
appropriate actions will be taken if limits are
exceeded.
The three editorial changes only correct
typographical errors made in previously
approved TS changes. They do not affect
plant operation or structures, systems, and
components important to safety.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The margin of safety is not affected by
implementation of the PDMS. The margin of
safety provided by current TS is unchanged.
The proposed changes continue to require
operation within the core limits that are
based on NRC-approved reload design
methodologies. Appropriate measures exist
to control the values of these cycle-specific
limits. The proposed changes continue to
ensure that appropriate actions will be taken
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if limits are violated. These actions remain
unchanged.
The three editorial changes only correct
typographical errors made in previously
approved TS changes. They do not affect
plant operation or structures, systems, and
components important to safety.
Therefore, the proposed changes do
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the standards of
10 CFR 50.92(c) are satisfied. Therefore,
the NRC staff proposes to determine that
the request for amendments involves no
significant hazards consideration.
Attorney for licensee: A. H.
Gutterman, Esq., Morgan, Lewis &
Bockius, 1111 Pennsylvania Avenue,
NW., Washington, DC 20004.
NRC Section Chief: David Terao.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for A Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
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16:40 Oct 07, 2005
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at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket
No. 50–461, Clinton Power Station, Unit
1, DeWitt County, Illinois
Date of application for amendment:
April 3, 2003, as supplemented
December 23, 2003, December 9 and 17,
2004, and March 30 and August 19,
2005.
Brief description of amendment: The
amendment revised the Technical
Specifications (TSs) to support the
application of an alternative source term
methodology in accordance with Title
10 of the Code of Federal Regulations,
Section 50.67, ‘‘Accident Source Term,’’
with the exception that Technical
Information Document 14844,
‘‘Calculation of Distance Factors for
Power and Test Reactor Sites,’’ was used
as the radiation dose basis for
equipment qualification.
Date of issuance: September 19, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 167.
Facility Operating License No. NPF–
62: The amendment revised the TSs.
Date of initial notice in Federal
Register: September 2, 2003 (68 FR
52234).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 19,
2005.
The supplements dated December 23,
2003, December 9 and 17, 2004, and
March 30 and August 19, 2005 provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination.
No significant hazards consideration
comments received: No.
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59089
AmerGen Energy Company, LLC, Docket
No. 50–461, Clinton Power Station, Unit
1, DeWitt County, Illinois
Date of application for amendment:
November 11, 2003, as supplemented
April 16 and September 10, 2004, and
March 30 and September 21, 2005.
Brief description of amendment: The
amendment revised the instrument
channel trip setpoint allowable values
for thirteen Technical Specification (TS)
functions at Clinton Power Station, Unit
1.
Date of issuance: September 27, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 168.
Facility Operating License No. NPF–
62: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: March 16, 2004 (69 FR
12363).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 21,
2005. The supplements dated April 16
and September 10, 2004, and March 30
and September 21, 2005, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination. No
significant hazards consideration
comments received: No.
Calvert Cliffs Nuclear Power Plant, Inc.,
Docket Nos. 50–317 and 50–318, Calvert
Cliffs Nuclear Power Plant, Unit Nos. 1
and 2, Calvert County, Maryland
Date of application for amendments:
August 3, 2004, as supplemented on
July 8 and August 26, 2005.
Brief description of amendments: The
amendments extend the surveillance
frequency interval from monthly to
quarterly for Technical Specification
surveillance requirement (SR) 3.3.3.1,
which involves a channel functional test
of each reactor trip circuit breaker
(RTCB). SRs 3.3.3.1 and 3.3.3.2 will be
scheduled such that the RTCBs testing
is performed every 6 weeks, which
meets the vendor-recommended interval
for cycling each RTCB.
Date of issuance: September 26, 2005.
Effective date: As of the date of
issuance to be implemented within 60
days.
Amendment Nos.: 275 and 252.
Renewed Facility Operating License
Nos. DPR–53 and DPR–69: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: January 4, 2005 (70 FR 400).
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The July 8 and August 26, 2005,
supplemental letters provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of these amendments is contained in a
Safety Evaluation dated September 26,
2005.
No significant hazards consideration
comments received: No.
Dominion Nuclear Connecticut, Inc.,
Docket No. 50–245, Millstone Power
Station Unit No. 1, New London County,
Connecticut
Date of application for amendment:
September 8, 2004, as supplemented by
letters dated May 5 and July 27, 2005.
Brief description of amendment: The
amendment revised the Millstone Power
Station, Unit No. 1 Technical
Specifications (TSs) to support the
implementation of the proposed
Dominion Nuclear Facility Quality
Assurance Program (Topical Report
DOM–QA–1). Implementation of this
Topical Report would create a common
quality assurance program for all sites
owned by Dominion Nuclear
Connecticut, Inc. Review of this
proposed amendment was requested in
concert with the review of the Topical
Report.
Date of issuance: September 15, 2005.
Effective date: As of the date of
issuance, and shall be implemented by
February 28, 2006.
Amendment No.: 115.
Facility Operating License No. DPR–
21: The amendment revised the TSs.
Date of initial notice in Federal
Register: January 18, 2005 (70 FR 2888).
The additional information provided
in the supplemental letters dated May 5
and July 27, 2005, did not expand the
scope of the application as noticed and
did not change the NRC staff’s original
proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 15,
2005.
No significant hazards consideration
comments received: No.
Dominion Nuclear Connecticut, Inc.,
Docket No. 50–336, Millstone Power
Station, Unit No. 2, New London
County, Connecticut
Date of application for amendment:
July 15, 2004, as supplemented by letter
dated August 23, 2004.
Brief description of amendment: The
amendment revised the Facility
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Operating License DPR–65 to address
the resolution of a non-conservative
Technical Specifications (TSs)
associated with control room isolation
radiation monitoring instrumentation.
Specifically, the amendment would
revise the TSs to require two operable
channels of control room isolation
radiation monitoring instrumentation.
Date of issuance: September 23, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment No.: 289.
Facility Operating License No. DPR–
65: The amendment revised the TSs.
Date of initial notice in Federal
Register: January 18, 2005 (70 FR 2887).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 23,
2005.
No significant hazards consideration
comments received: No.
Dominion Nuclear Connecticut, Inc., et
al., Docket No. 50–423, Millstone Power
Station, Unit No. 3, New London
County, Connecticut
Date of application for amendment:
April 15, 2004, as supplemented on
June 23, 2005.
Brief description of amendment: The
amendment approves modifications to
the Fire Protection Program.
Specifically, the modifications involve
converting the existing automatic
carbon dioxide fire suppression systems
installed in the cable spreading room to
manual actuation.
Date of issuance: September 22, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 90 days from the date of
issuance.
Amendment No.: 227.
Facility Operating License No. NPF–
49: The amendment allows for
conversion from an automatic to a
manual carbon dioxide suppression
system in the cable spreading area.
Date of initial notice in Federal
Register: July 6, 2004 (69 FR 40672).
The supplement dated June 23, 2005,
provided clarifying information and did
not change the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 22,
2005.
No significant hazards consideration
comments received: No.
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Dominion Nuclear Connecticut, Inc.,
Docket Nos. 50–336 and 50–423,
Millstone Power Station, Unit Nos. 2
and 3, New London County, Connecticut
Date of application for amendments:
September 8, 2004, as supplemented by
letters dated May 5 and July 27, 2005.
Brief description of amendments: The
amendments revised the Millstone
Power Station, Unit Nos. 2 and 3
Technical Specifications (TSs) to
support the implementation of the
proposed Dominion Nuclear Facility
Quality Assurance Program (Topical
Report DOM–QA–1). Implementation of
this Topical Report would create a
common quality assurance program for
all sites owned by Dominion Nuclear
Connecticut, Inc. Review of these
proposed amendments was requested to
be done in concert with the review of
the Topical Report.
Date of issuance: September 15, 2005.
Effective date: As of the date of
issuance, and shall be implemented by
February 28, 2006.
Amendment Nos.: 288 and 226.
Facility Operating License Nos. DPR–
65 and NPF–49: The amendments
revised the TSs.
Date of initial notice in Federal
Register: January 18, 2005 (70 FR
2888). The additional information
provided in the supplemental letters
dated May 5, and July 27, 2005, did not
expand the scope of the application as
noticed and did not change the NRC
staff’s original proposed no significant
hazards consideration determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 15,
2005.
No significant hazards consideration
comments received: No.
Entergy Nuclear Vermont Yankee, LLC
and Entergy Nuclear Operations, Inc.,
Docket No. 50–271, Vermont Yankee
Nuclear Power Station, Vernon,
Vermont
Date of application for amendment:
October 6, 2004, as supplemented on
February 16, and August 9, 2005.
Brief description of amendment: The
amendment revised Technical
Specification (TS) surveillance
requirement 4.5.B.1 related to air testing
of the drywell spray headers and
nozzles. Specifically, the amendment
changes the test frequency from once
every five years to following
maintenance that could result in nozzle
blockage.
Date of Issuance: September 20, 2005.
Effective date: As of the date of
issuance, and shall be implemented
within 60 days.
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Amendment No.: 228.
Facility Operating License No. DPR–
28: The amendment revised the TSs.
Date of initial notice in Federal
Register: December 21, 2004 (69 FR
76492). The supplements contained
clarifying information only, and did not
change the initial no significant hazards
consideration determination or expand
the scope of the initial Federal Register
notice.
The Commission’s related evaluation
of this amendment is contained in a
Safety Evaluation dated September 20,
2005.
No significant hazards consideration
comments received: No.
Date of issuance: September 19, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 138.
Facility Operating License Nos. NPF–
72 and NPF–77: The amendments
revised the Environmental Protection
Plan.
Date of initial notice in Federal
Register: April 12, 2005 (70 FR 19115).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 19,
2005.
No significant hazards consideration
comments received: No.
Entergy Operations, Inc., Docket No. 50–
313, Arkansas Nuclear One, Unit No. 1,
Pope County, Arkansas
Exelon Generation Company, LLC,
Docket No. STN 50–455, Byron Station,
Unit No. 2, Ogle County, Illinois
Date of amendment request:
September 30, 2004, as supplemented
by letter dated May 20, 2005.
Brief description of amendment: The
amendment revises the Technical
Specifications to allow the use of M5
fuel cladding and of Mark-B-high
thermal performance fuel in Arkansas
Nuclear One, Unit 1, during its fuel
Cycle 20 and beyond.
Date of issuance: September 12, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment No.: 226.
Renewed Facility Operating License
No. DPR–51: Amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: November 9, 2004 (69 FR
64988). The supplement dated May 20,
2005, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 12,
2005.
No significant hazards consideration
comments received: No.
Date of application for amendment:
May 24, 2005.
Brief description of amendment: The
amendment modifies the inspection
requirements for portions of the steam
generator (SG) tubes within the hot leg
tubesheet region of the SGs.
Date of issuance: September 19, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days.
Amendment No.: 144.
Facility Operating License No. NPF–
66: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: July 5, 2005 (70 FR 38718).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 19,
2005.
No significant hazards consideration
comments received: No.
Exelon Generating Company, LLC,
Docket Nos. STN 50–456 and STN 50–
457, Braidwood Station, Units 1 and 2,
Will County, Illinois
Date of application for amendment:
December 17, 2004.
Brief description of amendment: The
amendments revised Appendix B,
Environmental Protection Plan (nonradiological), of the Braidwood Station
Facility Operating Licenses.
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Exelon Generation Company, LLC,
Docket Nos. 50–237 and 50–249,
Dresden Nuclear Power Station, Units 2
and 3, Grundy County, Illinois
Docket Nos. 50–254 and 50–265, Quad
Cities Nuclear Power Station, Units 1
and 2, Rock Island County, Illinois
Date of application for amendments:
February 27, 2004, as supplemented by
letters dated October 11, 2004, January
3, 2005, August 11, 2005, and
September 12, 2005.
Brief description of amendments: The
amendments add the Oscillation Power
Range Monitor (OPRM) instrumentation
to the Technical Specifications.
Date of issuance: September 22, 2005.
Effective date: As of the date of
issuance and shall be implemented by
December 31, 2005.
Amendment Nos.: 227, 222.
Facility Operating License Nos. DPR–
19, DPR–25, DPR–29 and DPR–30. The
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59091
amendments revised the Technical
Specifications.
Date of initial notice in Federal
Register: December 7, 2004 (69 FR
70718). The October 11, 2004, and
January 3, 2005, August 11, 2005, and
September 12, 2005, submittals
provided clarifying information that did
not change the initial proposed no
significant hazards consideration.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated: September 22,
2005.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket Nos. 50–352 and 50–353,
Limerick Generating Station, Units 1
and 2, Montgomery County,
Pennsylvania
Date of application for amendments:
July 22, 2004, as supplemented
December 3, 2004, and September 20,
2005. The September 20, 2005,
supplement withdrew a portion of the
original application from consideration.
Brief description of amendments: The
amendments modified the operability
and surveillance requirements in
Technical Specification (TS) 3/4.1.3,
‘‘Control Rods.’’ Specifically, the
changes (1) exclude a fully-inserted
immovable control rod from the
shutdown action statement, and (2)
limit the 24-hour exercise test of other
control rods to a one-time occasion
following detection of an immovable
control rod.
Date of issuance: September 27, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment Nos.: 178 and 140.
Facility Operating License Nos. NPF–
39 and NPF–85. The amendments
revised the TSs.
Date of initial notice in Federal
Register: May 24, 2005 (70 FR 29794).
The September 20, 2005, supplement
withdrew a portion of the original
application from consideration and did
not change the proposed no significant
hazards consideration.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 27,
2005.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket Nos. 50–352 and 50–353,
Limerick Generating Station, Units 1
and 2, Montgomery County,
Pennsylvania
Date of application for amendments:
June 1, 2004.
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Brief description of amendments: The
amendments relocate the operability
and surveillance requirements for the
reactor coolant system safety/relief
valve position instrumentation from the
Limerick Generating Station (LGS)
Technical Specifications (TSs) to the
LGS Technical Requirements Manual
(TRM) and plant procedures.
Specifically, the amendments relocate
TSs 3.4.2.c, 4.4.2.1, and the associated
footnotes to the TRM. Additionally, the
‘‘Safety/Relief Valve Position
Indicators’’ instrumentation is relocated
from Tables 3.3.7.5–1 and 4.3.7.5–1 of
TSs 3.3.7.5 and 4.3.7.5, respectively, to
the TRM.
Date of issuance: September 27, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment Nos.: 179 and 141.
Facility Operating License Nos. NPF–
39 and NPF–85. The amendments
revised the TSs.
Date of initial notice in Federal
Register: October 26, 2004 (69 FR
62475).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 27,
2005.
No significant hazards consideration
comments received: No.
FirstEnergy Nuclear Operating
Company, et al., Docket Nos. 50–334
and 50–412, Beaver Valley Power
Station, Unit Nos. 1 and 2 (BVPS–1 and
2), Beaver County, Pennsylvania
Date of application for amendments:
June 2, 2004, as supplemented February
23 and August 19, 2005.
Brief description of amendments: The
amendments revised the BVPS–1 and 2,
Technical Specifications (TSs) 3/4 3.1,
‘‘Reactor Trip System (RTS)
Instrument,’’ and 3/4 3.2, ‘‘Engineered
Safety Features Actuation System
(ESFAS) Instrument,’’ to increase the
surveillance interval from monthly to
quarterly for certain RTS and ESFAS
instrument channel functional tests.
Date of issuance: September 19, 2005.
Effective date: September 19, 2005.
Amendment Nos.: 267 and 149.
Facility Operating License Nos. DPR–
66 and NPF–73: Amendments revised
the TSs.
Date of initial notice in Federal
Register: July 6, 2004 (69 FR 40674).
The supplements dated February 23
and August 19, 2005, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the Nuclear
Regulatory Commission (NRC) staff’s
original proposed no significant hazards
consideration determination.
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The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 19,
2005.
No significant hazards consideration
comments received: No.
FirstEnergy Nuclear Operating
Company, et al., Docket Nos. 50–334
and 50–412, Beaver Valley Power
Station, Unit Nos. 1 and 2 (BVPS–1 and
2), Beaver County, Pennsylvania
Date of application for amendments:
May 26, 2004, as supplemented by
letters dated October 29 and December
3, 2004, and January 18, June 15, and
August 15, 2005.
Brief description of amendments: The
amendments extended the allowable
outage time for the BVPS–1 and 2
emergency diesel generators (EDGs)
from 72 hours to 14 days. The
amendments also deleted surveillance
requirement (SR) 4.8.1.1.2.b.1
concerning periodic EDG inspections.
Requirements for periodic EDG
inspections will be specified in a
licensee-controlled EDG maintenance
program referenced in the Updated
Final Safety Analysis Report. The
amendments also revised footnote (1) of
TS 3.8.1.1 to clarify the wording to
allow actions to be delayed for up to 7
days to allow time to restore fuel oil
back to its specified limits when an EDG
is inoperable solely due to failure to
meet fuel oil property limits of SR
4.8.1.1.2.d.2 or SR 4.8.1.1.2.e.
Date of issuance: September 29, 2005.
Effective date: Upon issuance to be
implemented within 60 days. The
implementation shall include the
commitments as described in the
licensee’s submittals dated May 26 and
December 3, 2004, and January 18 and
June 15, 2005, and as described in the
NRC staff’s safety evaluation related to
this amendment.
Amendment Nos.: 268 and 150.
Facility Operating License Nos. DPR–
66 and NPF–73: Amendments revised
the Technical Specifications.
Date of initial notice in Federal
Register: July 6, 2004 (69 FR 40673).
The supplements dated October 29
and December 3, 2004, and January 18,
June 15, and August 15, 2005, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 29,
2005.
No significant hazards consideration
comments received: No.
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Florida Power and Light Company,
Docket No. 50–335, St. Lucie Plant, Unit
No. 1, St. Lucie County, Florida
Date of application for amendment:
December 20, 2004.
Brief description of amendment: This
amendment revises Technical
Specifications Figures 3.1–1b, 3.4–2a,
3.4–2b and 3.4–3 to reflect an extension
in the effectiveness of the pressure/
temperature (P/T) limit curves from 23.6
to 35 effective full power years (EFPY).
The low temperature overpressure
protection requirements, which are
based on the P/T limits, are also
extended to 35 EFPY.
Date of Issuance: September 21, 2005.
Effective Date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment No.: 196.
Renewed Facility Operating License
No. DPR–67: Amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: March 1, 2005 (70 FR 9993).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 21,
2005.
No significant hazards consideration
comments received: No.
Florida Power and Light Company, et
al., Docket Nos. 50–335 and 50–389, St.
Lucie Plant, Unit Nos. 1 and 2, St. Lucie
County, Florida
Date of application for amendments:
September 18, 2003, as supplemented
on August 25 and September 15, 2005.
Brief description of amendments: The
amendments revise Technical
Specifications (TSs) for the control room
ventilation systems to model the
Combustion Engineering Standard
Technical Specifications, NUREG–1432.
In addition, Table 3.3–6, Radiation
Monitoring Instrumentation, in each
unit’s TSs is revised to resolve minor
inconsistencies that resulted from
changes associated with previously
issued Amendments 184 (Unit 1) and
127 (Unit 2). The amendments also
correct some minor typographical
errors.
Date of Issuance: September 27, 2005.
Effective Date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment Nos.: 197 and 139.
Renewed Facility Operating License
Nos. DPR–67 and NPF–16: Amendments
revised the TSs.
Date of initial notice in Federal
Register: October 28, 2003 (68 FR
61478). The August 25 and September
15, 2005, supplements did not affect the
original proposed no significant hazards
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determination, or expand the scope of
the request as noticed in the Federal
Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 27,
2005.
No significant hazards consideration
comments received: No.
Florida Power Corporation, et al.,
Docket No. 50–302, Crystal River Unit
No. 3 Nuclear Generating Plant, Citrus
County, Florida
Date of application for amendment:
January 13, 2005, as supplemented by
letters dated February 11, May 6, and
June 9, 2005.
Brief description of amendment: The
amendment allows a one-time extended
allowed outage time (AOT) change to
Improved Technical Specifications (ITS)
3.5.2, Emergency Core Cooling Systems
(ECCS)—Operating; 3.6.6, Reactor
Building Spray and Containment
Cooling Systems; 3.7.8, Decay Heat
Closed Cycle Cooling Water System
(DC); and 3.7.10, Decay Heat Seawater
System to allow the refurbishment of
Decay Heat Seawater System Pump
RWP–3B online.
Date of issuance: September 15, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment No.: 221.
Facility Operating License No.
DPR–72: Amendment revises the
Technical Specifications.
Date of initial notice in Federal
Register: February 1, 2005 (70 FR
5246). The February 11, May 6, and June
9, 2005, supplements contained
clarifying information only and did not
change the initial no significant hazards
consideration determination or expand
the scope of the initial application.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 15,
2005.
No significant hazards consideration
comments received: No.
Nuclear Management Company, LLC,
Docket Nos. 50–266 and 50–1, Point
Beach Nuclear Plant, Units 1 and 2,
Town of Two Creeks, Manitowoc
County, Wisconsin
Date of application for amendments:
July 24, 2005.
Brief description of amendments: The
amendments incorporated a Point Beach
Nuclear Plant (PBNP), Unit 1 reactor
vessel head (RVH) drop accident
analysis into the PBNP Final Safety
Analysis Report and revised the PBNP,
Unit 2 RVH drop accident analysis.
Date of issuance: September 23, 2005.
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16:40 Oct 07, 2005
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Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment Nos.: 220, 226.
Facility Operating License Nos. DPR–
24 and DPR–27: Amendments revised
the License.
Date of initial notice in Federal
Register: August 16, 2005 (70 FR
48198).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 23,
2005.
No significant hazards consideration
comments received: No.
Nuclear Management Company, LLC,
Docket Nos. 50–266 and 50–301, Point
Beach Nuclear Plant, Units 1 and 2,
Town of Two Creeks, Manitowoc
County, Wisconsin
Date of amendment request: April 8,
2004, as supplemented by letters dated
November 15, 2004, July 15 and August
8, 2005.
Description of amendment request:
The amendments revised technical
specification surveillance requirements
(SR) 3.8.4.6 and SR 3.8.4.7, ‘‘DC
Sources—Operating.’’ Specifically, the
amendments revised battery charger
current values, added a new allowance
for verifying battery charger capacity,
and removed a restriction on the
conduct of a modified performance
discharge test.
Date of issuance: September 27, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 45 days.
Amendment Nos.: 221, 227.
Facility Operating License Nos. DPR–
24 and DPR–27: Amendments revised
the Technical Specifications.
Date of initial notice in Federal
Register: August 19, 2004 (69 FR
51489). The November 15, 2004, July 15
and August 8, 2005, supplemental
letters provided additional information
that clarified the application, did not
expand the scope of the application
originally noticed, and did not change
the NRC staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 27,
2005.
No significant hazards consideration
comments received: No.
R.E. Ginna Nuclear Power Plant, LLC,
Docket No. 50–244, R.E. Ginna Nuclear
Power Plant, Wayne County, New York
Date of application for amendment:
September 30, 2004, and May 28, 2005.
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59093
Brief description of amendment: The
amendment revises information in the
Updated Final Safety Analysis Report
(UFSAR) regarding the application of
‘‘leak-before-break’’ methodology for the
emergency core cooling system
accumulator lines A and B and the
pressurizer surge line. The amendment
permits the exclusion of these lines
from the evaluation of the dynamic
effects associated with postulated highenergy line breaks in the analyzed
segments of the accumulator lines
piping system and the pressurizer surge
line piping system.
Date of issuance: September 22, 2005.
Effective date: As of the date of
issuance and shall be implemented with
the next update of the UFSAR in
accordance with 10 CFR 50.71(e).
Amendment No.: 92.
Renewed Facility Operating License
No. DPR–18: Amendment revised the
UFSAR.
Date of initial notice in Federal
Register: July 5, 2005 (70 FR 38721).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 22,
2005.
No significant hazards consideration
comments received: No.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–424 and 50–425,
Vogtle Electric Generating Plant, Units 1
and 2, Burke County, Georgia
Date of application for amendments:
August 12, 2005, as supplemented by
letter dated August 24, 2005.
Brief description of amendments: The
amendments revised the Technical
Specifications to incorporate changes in
the steam generator (SG) inspection
scope for Vogtle, Unit 2 during
Refueling Outage 11 and the subsequent
operating cycle. The proposed changes
modify the inspection requirements for
portions of SG tubes within the hot leg
tubesheet region of the SGs. The license
for Vogtle, Unit 1 is affected only due
to the fact that Unit 1 and Unit 2 use
common Technical Specifications.
Date of issuance: September 21, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 138/117.
Facility Operating License Nos.
NPF–68 and NPF–81: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: August 22, 2005 (70 FR
48985).
The supplement dated August 24,
2005, provided clarifying information
that did not change the scope of the
August 12, 2005, application nor the
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initial proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 21,
2005.
No significant hazards consideration
comments received: No.
Southern Nuclear Operating Company,
Inc., Docket Nos. 50–424 and 50–425,
Vogtle Electric Generating Plant, Units 1
and 2, Burke County, Georgia
Date of application for amendments:
August 13, 2004, as supplemented by
letters dated May 3 and July 7, 2005.
Brief description of amendments: The
amendments revised the Technical
Specifications (TSs) to reflect updated
spent fuel rack criticality analyses for
Units 1 and 2. The amendments also
corrected a typographical error on Page
vi of the TSs Table of Contents
associated with the issuance of
Amendments 130 and 109, for Units 1
and 2 TSs, respectively.
Date of issuance: September 22, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment Nos.: 139/118.
Facility Operating License Nos.
NPF–68 and NPF–81: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: November 9, 2004 (69 FR
64990).
The supplements dated May 3 and
July 7, 2005, provided clarifying
information that did not change the
scope of the August 13, 2004,
application nor the initial proposed no
significant hazards consideration
determination.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 22,
2005.
No significant hazards consideration
comments received: No.
Tennessee Valley Authority, Docket No.
50–390, Watts Bar Nuclear Plant, Unit 1,
Rhea County, Tennessee
Date of application for amendment:
November 21, 2003, as supplemented by
letters dated May 5 and August 19,
2004, and July 11, 2005.
Brief description of amendment: The
amendment allows the position of the
control and shutdown rods to be
monitored by a means other than the
movable incore detectors.
Date of issuance: September 20, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days.
Amendment No.: 58.
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16:40 Oct 07, 2005
Jkt 208001
Facility Operating License No. NPF–
90: Amendment revises the Technical
Specifications.
Date of initial notice in Federal
Register: December 23, 2003 (68 FR
74267). The supplemental letters
provided clarifying information that was
within the scope of the initial notice
and did not change the initial proposed
no significant hazards consideration
determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated September 20,
2005.
No significant hazards consideration
comments received: No.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Unit Nos.
1 and 2, Somervell County, Texas
Date of amendment request: March
24, 2005.
Brief description of amendments: The
amendments revise Technical
Specification (TS) 3.3.1 entitled
‘‘Reactor Trip System (RTS)
Instrumentation’’ and TS 3.3.2 entitled
‘‘Engineered Safety Feature Actuation
System (ESFAS) Instrumentation’’, and
Required Action Notes in the TSs to
reflect wording in the Commissions
Standard TSs incorporating the channel
bypass capabilities as discussed in TS
Task Force Traveler 418, Revision 2.
Date of issuance: September 29, 2005.
Effective date: Effective as of the date
of issuance and shall be implemented in
90 days from the date of issuance.
Amendment Nos.: 121 and 121.
Facility Operating License Nos. NPF–
87 and NPF–89: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: April 26, 2005 (70 FR 21464).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 29,
2005.
No significant hazards consideration
comments received: No.
Virginia Electric and Power Company,
Docket Nos. 50–338 and 50–339, North
Anna Power Station, Units 1 and 2,
Louisa County, Virginia
Date of application for amendment:
September 15, 2004, as supplemented
by letter dated May 5, 2005.
Brief description of amendment:
These amendments revise the Technical
Specifications for North Anna Power
Station, Units 1 and 2 to support the
implementation of the proposed Topical
Report DOM–QA–1, ‘‘Dominion Nuclear
Facility Quality Assurance Program
Description.’’ The implementation of
this topical report would create a
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Sfmt 4703
common quality assurance program for
North Anna, Surry, and Millstone Power
Stations. The review of these proposed
amendments was requested to be done
in concert with the review of the
Topical Report. The Topical Report was
submitted to the NRC staff for review on
August 24, 2004, and supplemented by
letter dated May 5, 2005. By letter dated
September 9, 2005, the NRC staff
approved of Topical Report DOM–QA–
1.
Date of issuance: September 15, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 6 months from the date of
issuance.
Amendment Nos.: 243 and 224.
Renewed Facility Operating License
Nos. NPF–4 and NPF–7: Amendments
change the Technical Specifications.
Date of initial notice in Federal
Register: November 23, 2004 (69 FR
68187). The supplement dated May 5,
2005, contained clarifying information
only and did not change the initial no
significant hazards consideration
determination or expand the scope of
the initial application.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 15,
2005.
No significant hazards consideration
comments received: No.
Virginia Electric and Power Company, et
al., Docket Nos. 50–280 and 50–281,
Surry Power Station, Units 1 and 2,
Surry County, Virginia
Date of application for amendments:
September 15, 2004, as supplemented
by letter dated May 5, 2005.
Brief description of amendments:
These amendments revise the Technical
Specifications for Surry Power Station,
Units 1 and 2 to support the
implementation of the proposed Topical
Report DOM–QA–1, ‘‘Dominion Nuclear
Facility Quality Assurance Program
Description.’’ The implementation of
this topical report would create a
common quality assurance program for
North Anna, Surry, and Millstone Power
Stations. The review of these proposed
amendments was requested to be done
in concert with the review of the
Topical Report. The Topical Report was
submitted to the NRC staff for review on
August 24, 2004, and supplemented by
letter dated May 5, 2005. Subsequently,
the NRC staff approved this Topical
Report on September 9, 2005.
Date of issuance: As of the date of
issuance and shall be implemented
within 6 months from the date of
issuance.
Effective date: September 15, 2005.
Amendment Nos.: 244/243.
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Federal Register / Vol. 70, No. 195 / Tuesday, October 11, 2005 / Notices
Renewed Facility Operating License
Nos. DPR–32 and DPR–37: Amendments
change the Technical Specifications.
Date of initial notice in Federal
Register: December 7, 2004 (69 FR
70723). The supplement dated May 5,
2005, contained clarifying information
only and did not change the initial no
significant hazards consideration
determination or expand the scope of
the initial application.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated September 15,
2005.
No significant hazards consideration
comments received: No.
Notice of Issuance of Amendments to
Facility Operating Licenses and Final
Determination of No Significant
Hazards Consideration and
Opportunity for a Hearing (Exigent
Public Announcement or Emergency
Circumstances)
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application for the
amendment complies with the
standards and requirements of the
Atomic Energy Act of 1954, as amended
(the Act), and the Commission’s rules
and regulations. The Commission has
made appropriate findings as required
by the Act and the Commission’s rules
and regulations in 10 CFR Chapter I,
which are set forth in the license
amendment.
Because of exigent or emergency
circumstances associated with the date
the amendment was needed, there was
not time for the Commission to publish,
for public comment before issuance, its
usual Notice of Consideration of
Issuance of Amendment, Proposed No
Significant Hazards Consideration
Determination, and Opportunity for a
Hearing.
For exigent circumstances, the
Commission has either issued a Federal
Register notice providing opportunity
for public comment or has used local
media to provide notice to the public in
the area surrounding a licensee’s facility
of the licensee’s application and of the
Commission’s proposed determination
of no significant hazards consideration.
The Commission has provided a
reasonable opportunity for the public to
comment, using its best efforts to make
available to the public means of
communication for the public to
respond quickly, and in the case of
telephone comments, the comments
have been recorded or transcribed as
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16:40 Oct 07, 2005
Jkt 208001
appropriate and the licensee has been
informed of the public comments.
In circumstances where failure to act
in a timely way would have resulted, for
example, in derating or shutdown of a
nuclear power plant or in prevention of
either resumption of operation or of
increase in power output up to the
plant’s licensed power level, the
Commission may not have had an
opportunity to provide for public
comment on its no significant hazards
consideration determination. In such
case, the license amendment has been
issued without opportunity for
comment. If there has been some time
for public comment but less than 30
days, the Commission may provide an
opportunity for public comment. If
comments have been requested, it is so
stated. In either event, the State has
been consulted by telephone whenever
possible.
Under its regulations, the Commission
may issue and make an amendment
immediately effective, notwithstanding
the pendency before it of a request for
a hearing from any person, in advance
of the holding and completion of any
required hearing, where it has
determined that no significant hazards
consideration is involved.
The Commission has applied the
standards of 10 CFR 50.92 and has made
a final determination that the
amendment involves no significant
hazards consideration. The basis for this
determination is contained in the
documents related to this action.
Accordingly, the amendments have
been issued and made effective as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the application for
amendment, (2) the amendment to
Facility Operating License, and (3) the
Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment, as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
PO 00000
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Fmt 4703
Sfmt 4703
59095
will be accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
The Commission is also offering an
opportunity for a hearing with respect to
the issuance of the amendment. Within
60 days after the date of publication of
this notice, the licensee may file a
request for a hearing with respect to
issuance of the amendment to the
subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland,
and electronically on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If there
are problems in accessing the document,
contact the PDR Reference staff at 1
(800) 397–4209, (301) 415–4737, or by email to pdr@nrc.gov. If a request for a
hearing or petition for leave to intervene
is filed by the above date, the
Commission or a presiding officer
designated by the Commission or by the
Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
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Federal Register / Vol. 70, No. 195 / Tuesday, October 11, 2005 / Notices
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also identify the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner intends to
rely in proving the contention at the
hearing. The petitioner must also
provide references to those specific
sources and documents of which the
petitioner is aware and on which the
petitioner intends to rely to establish
those facts or expert opinion. The
petition must include sufficient
information to show that a genuine
dispute exists with the applicant on a
material issue of law or fact.1
Contentions shall be limited to matters
within the scope of the amendment
under consideration. The contention
must be one which, if proven, would
entitle the petitioner to relief. A
petitioner/requestor who fails to satisfy
these requirements with respect to at
least one contention will not be
permitted to participate as a party.
Each contention shall be given a
separate numeric or alpha designation
within one of the following groups:
1. Technical—primarily concerns/
issues relating to technical and/or
health and safety matters discussed or
referenced in the applications.
2. Environmental—primarily
concerns/issues relating to matters
discussed or referenced in the
environmental analysis for the
applications.
3. Miscellaneous—does not fall into
one of the categories outlined above.
As specified in 10 CFR 2.309, if two
or more petitioners/requestors seek to
co-sponsor a contention, the petitioners/
requestors shall jointly designate a
representative who shall have the
authority to act for the petitioners/
requestors with respect to that
contention. If a petitioner/requestor
1 To the extent that the applications contain
attachments and supporting documents that are not
publicly available because they are asserted to
contain safeguards or proprietary information,
petitioners desiring access to this information
should contact the applicant or applicant’s counsel
and discuss the need for a protective order.
VerDate Aug<31>2005
16:40 Oct 07, 2005
Jkt 208001
seeks to adopt the contention of another
sponsoring petitioner/requestor, the
petitioner/requestor who seeks to adopt
the contention must either agree that the
sponsoring petitioner/requestor shall act
as the representative with respect to that
contention, or jointly designate with the
sponsoring petitioner/requestor a
representative who shall have the
authority to act for the petitioners/
requestors with respect to that
contention.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing. Since the Commission has
made a final determination that the
amendment involves no significant
hazards consideration, if a hearing is
requested, it will not stay the
effectiveness of the amendment. Any
hearing held would take place while the
amendment is in effect.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer or
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(I)–(viii).
PO 00000
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Indiana Michigan Power Company,
Docket Nos. 50–315 and 50–316, Donald
C. Cook Nuclear Plant, Units 1 and 2,
Berrien County, Michigan
Date of amendment request:
September 12, 2005.
Description of amendment request:
The amendments replace the paragraph
of Improved Technical Specification
(ITS) Surveillance Requirement (SR)
3.8.1.18 with the wording of previous
TS SR 4.8.1.1.2.e.11.
Date of issuance: September 23, 2005.
Effective date: Immediately.
Amendment Nos.: 290, 272.
Facility Operating License Nos. (DPR–
58 and DPR–74): Amendment revises
the technical specifications.
Public comments requested as to
proposed no significant hazards
consideration (NSHC): Yes. HeraldPalladium on September 18, 2005. The
notice provided an opportunity to
submit comments on the Commission’s
proposed NSHC determination. No
comments have been received.
The Commission’s related evaluation
of the amendment, finding of exigent
circumstances, state consultation, and
final NSHC determination are contained
in a safety evaluation dated September
23, 2005.
Attorney for licensee: James M. Petro,
Jr., Esquire, One Cook Place, Bridgman,
MI 49106.
NRC Section Chief: L. Raghavan.
Dated at Rockville, Maryland, this 3rd day
of October 2005.
For the Nuclear Regulatory Commission.
Ledyard B. Marsh,
Director, Division of Licensing Project
Management, Office of Nuclear Reactor
Regulation.
[FR Doc. 05–20168 Filed 10–7–05; 8:45 am]
BILLING CODE 7590–01–P
SECURITIES AND EXCHANGE
COMMISSION
[File No. 1–31514]
Issuer Delisting; Notice of Application
of Meredith Enterprises, Inc. to
Withdraw Its Common Stock, $.01 Par
Value, From Listing and Registration
on the American Stock Exchange LLC
October 4, 2005.
On September 15, 2005, Meredith
Enterprises, Inc., a Delaware corporation
(‘‘Issuer’’), filed an application with the
Securities and Exchange Commission
(‘‘Commission’’), pursuant to Section
12(d) of the Securities Exchange Act of
1934 (‘‘Act’’) 1 and Rule 12d2–2(d)
1 15
E:\FR\FM\11OCN1.SGM
U.S.C. 78l(d).
11OCN1
Agencies
[Federal Register Volume 70, Number 195 (Tuesday, October 11, 2005)]
[Notices]
[Pages 59082-59096]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: 05-20168]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a.(2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from September 6, 2005, to September 29, 2005.
The last biweekly notice was published on September 27, 2005 (70 FR
56499).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
[[Page 59083]]
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File Area
O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland. The
filing of requests for a hearing and petitions for leave to intervene
is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland, 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
[[Page 59084]]
Carolina Power & Light Company, et al., Docket No. 50-400, Shearon
Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North
Carolina
Date of amendment request: April 6, 2005, as supplemented by letter
dated August 8, 2005.
Description of amendment request: The proposed amendment will
modify Technical Specification (TS) 6.8.4.k, ``Containment Leakage Rate
Testing Program,'' and TS Surveillance Requirement (SR) 4.6.1.6.1,
``Containment Vessel Surfaces.'' The proposed amendment would modify
the TS to allow for a one-time extension of the containment Type A test
interval from once in 10 years to once in 15 years.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
This change does not involve a significant hazards consideration
for the following reasons:
1. The proposed amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
The proposed change to HNP [Harris Nuclear Plant] TS 6.8.4.k and
TS SR 4.6.1.6.1 provide a one-time extension of the containment Type
A test interval from 10 years to 15 years and specifies that
additional visual inspections are done in accordance with
Subsections IWE and IWL of the ASME [American Society of Mechanical
Engineers] Section XI Code. The existing 10-year test interval is
based on past test performance. The proposed TS change does not
involve a physical change to the plant or a change in the manner in
which the plant is operated or controlled. The containment vessel is
designed to provide a leak-tight barrier against the uncontrolled
release of radioactivity to the environment in the unlikely event of
postulated accidents. As such, the containment vessel is not
considered as the initiator of an accident. Therefore, the proposed
TS change does not involve a significant increase in the probability
of an accident previously evaluated.
The proposed change involves only a one-time change to the
interval between containment Type A tests. Type B and C leakage
testing will continue to be performed at the intervals specified in
10 CFR Part 50, Appendix J, Option A, as required by the HNP TS. As
documented in NUREG-1493, ``Performance-Based Containment Leakage-
Test Program,'' industry experience has shown that Type B and C
containment leak rate tests have identified a very large percentage
of containment leak paths, and that the percentage of containment
leak paths that are detected only by Type A testing is very small.
In fact, an analysis of 144 integrated leak rate tests, including 23
failures, found that none of the failures involved a containment
liner breach. NUREG-1493 also concluded, in part, that reducing the
frequency of containment Type A testing to once per 20 years results
in an imperceptible increase in risk. The HNP test history and risk-
based evaluation of the proposed extension to the Type A test
interval supports this conclusion. The design and construction
requirements of the containment vessel, combined with the
containment inspections performed in accordance with the American
Society of Mechanical Engineers (ASME) Code, Section XI, and the
Maintenance Rule (10 CFR 50.65) provide a high degree of assurance
that the containment vessel will not degrade in a manner that is
detectable only by Type A testing. Therefore, the proposed TS change
does not involve a significant increase in the consequences of an
accident previously evaluated.
Therefore, this change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
2. The proposed amendment does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
The proposed change to HNP TS 6.8.4.k and TS SR 4.6.1.6.1
provide a one-time extension of the containment Type A test interval
to 15 years and specifies that additional visual inspections are
done in accordance with Subsections IWE and IWL of the ASME Section
XI Code. The existing 10-year test interval is based on past test
performance. The proposed change to the Type A test interval does
not result in any physical changes to HNP. In addition, the proposed
test interval extension does not change the operation of HNP such
that a failure mode involving the possibility of a new or different
kind of accident from any accident previously evaluated is created.
Thus, this change does not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3. The proposed amendment does not involve a significant
reduction in a margin of safety.
The proposed change to HNP TS 6.8.4.k and TS SR 4.6.1.6.1
provide a one-time extension of the containment Type A test interval
from 10 years to 15 years and specifies that additional visual
inspections are done in accordance with Subsections IWE and IWL of
the ASME Section XI Code. The existing 10-year test interval is
based on past test performance. The NUREG-1493 study of the effects
of extending containment leak rate testing found that a 20 year
extension for Type A testing resulted in an imperceptible increase
in risk to the public. NUREG-1493 found that, generically, the
design containment leak rate contributes a very small amount to the
individual risk and that the decrease in Type A testing frequency
would have a minimal affect on this risk since most potential leak
paths are detected by Type B and C testing. The proposed change
involves only a one-time extension of the interval for containment
Type A testing; the overall containment leak rate specified by the
HNP TS is being maintained. Type B and C testing will continue to be
performed at the frequency required by the HNP TS. The regular
containment inspections being performed in accordance with the ASME
Code, Section XI, and the Maintenance Rule (10 CFR 50.65) provide a
high degree of assurance that the containment will not degrade in a
manner that is only detectable by Type A testing. In addition, a
plant-specific risk evaluation has demonstrated that the one-time
extension of the Type A test interval from 10 years to 15 years
results in a very small increase in risk for those accident
sequences influenced by Type A testing.
Therefore, this change does not involve a significant reduction
in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Section Chief: Michael L. Marshall, Jr.
Carolina Power & Light Company, et al., Docket No. 50-400, Shearon
Harris Nuclear Power Plant (HNP), Unit 1, Wake and Chatham Counties,
North Carolina
Date of amendment request: June 20, 2005.
Description of amendment request: The amendment would revise
Technical Specifications (TS) 3/4.4.7, ``Reactor Coolant System
Chemistry.'' Specifically, the proposed amendment would revise the
footnotes in Tables 3.4-2 and 4.4-3 of the TS to increase the
temperature limit from 180 [deg]F to 250 [deg]F above which reactor
coolant sampling and analysis for dissolved oxygen is required and
dissolved oxygen limits apply.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
This amendment does not involve a significant hazards consideration
for the following reasons:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
Operation of HNP in accordance with the proposed amendment does
not increase the
[[Page 59085]]
probability or consequences of accidents previously evaluated. The
Final Safety Analysis Report (FSAR) documents the analyses of design
basis accidents (DBA) at HNP. Any scenario or previously analyzed
accident that results in offsite dose were evaluated as part of this
analysis. The proposed amendment does not change or affect any
accident previously evaluated in the FSAR. The proposed amendment
does not modify any plant equipment. In addition, the proposed
amendment does not result in a change to a structure, system, or
component (SSC), or adversely affect its design function.
The purpose of the temperature limit for RCS [Reactor Coolant
System] oxygen control is to minimize corrosion at high temperatures
on RCS components. Increasing the temperature at which oxygen levels
are required to be maintained within specified limits from 180
[deg]F to 250 [deg]F is supported by industry and vendor data which
indicates that the influence of dissolved oxygen at or below 250
[deg]F is not significant with regard to stress corrosion cracking
and general corrosion of RCS components. The proposed amendment is
consistent with the Electric Power Research Institute's (EPRI's)
guidelines for Pressurized Water Reactor (PWR) Primary Water
Chemistry. This amendment places HNP in line with standard industry
specifications for reactors of similar size and vintage. HNP's
proposed amendment to increase the temperature limit for
applicability to 250 [deg]F would decrease the time needed to
achieve compliance with the dissolved oxygen limit and decrease the
overall time to restart the plant from cold shutdown. Removing
oxygen in a more expeditious fashion enhances RCS chemistry. Based
on the above, RCS integrity is maintained by this amendment.
Therefore, this amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
Operation of HNP in accordance with the proposed amendment does
not create the possibility of a new or different kind of accident
from any accident previously evaluated. The FSAR documents the
analyses of design basis accidents (DBA) at HNP. Any scenario or
previously analyzed accident that results in offsite dose were
evaluated as part of this analysis. The proposed amendment does not
change or affect any accident previously evaluated in the FSAR, and
no new or different scenarios are created by the proposed amendment
to the TS. The proposed amendment does not modify any plant
equipment. In addition, the proposed amendment does not result in a
change to an SSC [structure, system, or component] or adversely
affect its design function.
The purpose of the temperature limit for RCS oxygen control is
to minimize corrosion at high temperatures on RCS components.
Increasing the temperature at which oxygen levels are required to be
maintained within specified limits from 180 [deg]F to 250 [deg]F is
supported by industry and vendor data which indicates that the
influence of dissolved oxygen at or below 250 [deg]F is not
significant with regard to stress corrosion cracking and general
corrosion of RCS components. The proposed amendment is consistent
with EPRI's guidelines for PWR Primary Water Chemistry. This
amendment places HNP in line with standard industry specifications
for reactors of similar size and vintage. HNP's proposed amendment
to increase the temperature limit for applicability to 250 [deg]F
would decrease the time needed to achieve compliance with the
dissolved oxygen limit and decrease the overall time to restart the
plant from cold shutdown. Removing oxygen in a more expeditious
fashion enhances RCS chemistry. Based on the above, RCS integrity is
maintained by this amendment.
Therefore, this amendment does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
Operation of HNP in accordance with the proposed amendment does
not involve a significant reduction in a margin of safety. Existing
TS operability and surveillance requirements are not reduced by the
proposed amendment. The proposed amendment does not modify any plant
equipment. In addition, the proposed amendment does not result in a
change to a structure, system, or component (SSC), or its design
function. The proposed amendment does not adversely affect existing
plant safety margins or the reliability of equipment assumed to
mitigate accidents in the FSAR.
The purpose of the temperature limit for RCS oxygen control is
to minimize corrosion at high temperatures on RCS components.
Increasing the temperature at which oxygen levels are required to be
maintained within specified limits from 180 [deg]F to 250 [deg]F is
supported by industry and vendor data which indicates that the
influence of dissolved oxygen at or below 250 [deg]F is not
significant with regard to stress corrosion cracking and general
corrosion of RCS components. The proposed amendment is consistent
with EPRI's guidelines for PWR Primary Water Chemistry. This
amendment places HNP in line with standard industry specifications
for reactors of similar size and vintage. HNP's proposed amendment
to increase the temperature limit for applicability to 250 [deg]F
would decrease the time needed to achieve compliance with the
dissolved oxygen limit and decrease the overall time to restart the
plant from cold shutdown. Removing oxygen in a more expeditious
fashion enhances RCS chemistry. Based on the above, RCS integrity is
maintained by this amendment.
Therefore, this amendment does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David T. Conley, Associate General Counsel
II--Legal Department, Progress Energy Service Company, LLC, Post Office
Box 1551, Raleigh, North Carolina 27602.
NRC Section Chief: Michael L. Marshall, Jr.
Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear
Station, Nemaha County, Nebraska
Date of amendment request: June 20, 2005.
Description of amendment request: The proposed amendment would
revise Cooper Nuclear Station (CNS) Technical Specification (TS) 5.3,
``Unit Staff Qualifications,'' to upgrade the qualification standard
for the Shift Manager, Senior Operator, Licensed Operator, and Shift
Technical Engineer from Regulatory Guide (RG) 1.8, Revision 2
``Qualification and Training of Personnel for Nuclear Power Plants,''
to RG 1.8, Revision 3. It also clarifies qualification requirements
applicable to the Operations Manager position.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
These changes are administrative in nature and do not require
any physical modifications, affect any plant components, or result
in any changes in plant operation. They provide clarity and
consistency to the CNS licensing basis.
Upgrading the unit staff qualifications for the Shift Manager,
Senior Operator, Licensed Operator, and Shift Technical Engineer
from Regulatory Guide 1.8, Revision 2, to Regulatory Guide 1.8,
Revision 3, is an administrative change that will clarify the
current requirements for qualification and training of operations
personnel. The changes are consistent with the application of a
systems approach to training in an accredited training program. By
promulgation of the 10 CFR Part 55 rule change, the NRC determined
that an accredited licensed operator training program based on a
systems approach to training provides an acceptable means of
qualifying licensed operating personnel.
The addition of qualification requirements for the Operations
Manager position clarifies SRO [Senior Reactor Operator] license
requirements for Operations management personnel by specifying that
the Operations Supervisor is the member of Operations management
required to have a current SRO license at CNS. The Operations
Manager is required to hold or have previously held a
[[Page 59086]]
SRO license. This will ensure an acceptable level of operations
knowledge to perform in a managerial oversight role. This approach
is consistent with current guidance in ANSI/ANS [American Nuclear
Standards Institute/American Nuclear Society] 3.1-1993. This change
is administrative in nature and has no impact on previously
evaluated accidents.
Therefore, these changes do not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
These changes are administrative in nature and do not involve a
physical alteration of the plant or a change to plant operations. No
new failure mechanisms, malfunctions, or accident initiators are
introduced. The proposed changes provide clarity and consistency to
the CNS licensing basis in regard to training and qualification of
operations personnel and SRO license requirements for Operations
management personnel.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously
evaluated.
Response: No.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
These changes are administrative in nature and do not affect any
Technical Specification safety limit or limiting condition for
operation. No safety margins are affected by these changes. The
proposed changes do not involve a change in plant design or
operation for the mitigation of postulated accidents. The proposed
changes provide clarity and consistency to the CNS licensing basis
in regard to training and qualification of operations personnel and
SRO license requirements for Operations management personnel.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. John C. McClure, Nebraska Public Power
District, Post Office Box 499, Columbus, NE 68602-0499.
NRC Section Chief: David Terao.
Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear
Station, Nemaha County, Nebraska
Date of amendment request: August 25, 2005.
Description of amendment request: The proposed amendment would
revise the definitions of Channel Calibration, Channel Function Test,
and Logic System Functional Test in accordance with the Technical
Specification Task Force Traveler 205-A.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
Response: No.
The definitions of Channel Calibration, Channel Functional Test,
and Logic System Functional Test specified in Technical
Specifications (TS) provide basic information regarding what the
test involves, the components involved in the test, and general
information regarding how the test is to be performed. These
definitions and their specific wording are not precursors to any
accident. As a result these revised definitions result in no
increase in the probability of an accident previously evaluated.
The proposed revisions of these definitions involve no changes
to plant design, equipment, or operation related to mitigation of
accidents. The proposed revisions of these definitions do not change
their meaning or intent. The proposed revisions clarify the
definitions and do not result in a reduction of required testing of
instrumentation used to mitigate accidents.
Based on the above NPPD [Nebraska Public Power District]
concludes that the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed revisions of the definitions do not involve a
change to the design or operation of any plant structure, system, or
component (SSC). As a result the plant will continue to be operated
in the same manner. The proposed revisions will not result in a
change to how the instrumentation used to monitor plant operation
and to mitigate accidents is tested. Operating the plant and testing
the plant's instrumentation in the same manner as is currently done
will not create the possibility of a new or different kind of
accident.
Based on the above NPPD concludes that the proposed changes do
not create the possibility of a new or different kind of accident
from any previously evaluated.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
Response: No.
The affected definitions involve testing of instrumentation used
in the mitigation of accidents to ensure that the instrumentation
will perform as assumed in safety analyses. The proposed revisions
of these definitions will not change their meaning or intent. As a
result, the instrumentation will continue to be tested in the same
manner as is currently done. Revising these definitions as proposed
will not result in a change to the design or operation of any plant
SSC used to shutdown the plant, initiate the Emergency Core Cooling
Systems, or isolate primary or secondary containment. As a result
the ability of the plant to respond to and mitigate accidents is
unchanged by the revised definitions.
Based on the above, NPPD concludes that the proposed changes do
not involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mr. John C. McClure, Nebraska Public Power
District, Post Office Box 499, Columbus, NE 68602-0499.
NRC Section Chief: David Terao.
Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo
Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County,
California
Date of amendment requests: July 29, 2005.
Description of amendment requests: The proposed amendments would
revise Technical Specification 3.7.5, ``Auxiliary Feedwater (AFW)
System,'' to change the frequency of Surveillance Requirement 3.7.5.6
from 92 days to 24 months.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change to increase [the] frequency interval for
Surveillance Requirement (SR) 3.7.5.6 from 92 days to 24 months has
no impact on the probability of accidents previously evaluated. The
valves controlled by SR 3.7.5.6 are used to provide an alternate
supply of water to the auxiliary feedwater (AFW) system from the
fire water storage tank (FWST) and are only operated after an
accident has occurred. They are not accident initiators.
Misoperation, or failure of a[n] FWST supply to be correctly
positioned following an accident, could result in an inadequate
supply of water to the AFW system. Failure to provide adequate core
cooling could increase the radiological consequences of an accident.
However, operating and maintenance histories of the FWST supply
valves show that these valves have been
[[Page 59087]]
capable of full stroke cycling each time they have been tested.
There is no evidence of any time-related degradation mechanism that
would prevent the valves from performing their design function.
Thus[,] the proposed change has no impact on the consequences of an
accident.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different [kind of] accident from any accident previously evaluated?
Response: No.
The proposed change to increase frequency interval for SR
3.7.5.6 from 92 days to 24 months has no impact on the probability
of accidents of the type evaluated in the Final Safety Analysis
Report, as updated. The valves are used to provide an alternate
supply of water to the AFW system from the FWST, and are only
operated after an accident has occurred. They are not accident
initiators. Review of the operating and maintenance histories of the
FWST supply valves show that they are highly reliable in maintaining
their capability to perform their design function.
Therefore, the proposed change does not create the possibility
of a new or different [kind of] accident from any accident
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change to SR 3.7.5.6 involves only an increase in
the frequency interval. No physical changes are required to the
facility or to the plant operating or emergency procedures as a
result of the change. Based on review of the operating and
maintenance histories of the FWST supply valves, they have been
capable of full stroke cycling each time they have been tested.
There is no evidence of any time-related degradation mechanism that
would prevent the valves from performing their design function. This
evidence supports the conclusion that there will be no impact in the
operation of these valves following an accident.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c)
are satisfied. Therefore, the NRC staff proposes to determine that
the amendment requests involve no significant hazards consideration.
Attorney for licensee: Richard F. Locke, Esq., Pacific Gas and
Electric Company, P.O. Box 7442, San Francisco, California 94120.
NRC Section Chief: Daniel S. Collins (Acting).
Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo
Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County,
California
Date of amendment requests: August 23, 2005.
Description of amendment requests: The proposed amendments would
revise the expiration dates of the Units 1 and 2 facility-operating
licenses to recapture low-power testing time, and to reflect a 40-year
term measured from the date of issuance of each unit's full-power
operating license.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed additional operating license periods do not affect
the probability or consequences of an accident previously evaluated
since they require no physical change in the plant equipment or
operating procedures and the Final Safety Analysis Report (FSAR)
Update safety analyses are based on [a] 40-year full[-]power
operation. Surveillance and maintenance practices, as well as other
programs such as environmental qualification of equipment, ensure
timely identification and correction of any degradation of safety-
related plant equipment. The long-term integrity of the reactor
vessels has been evaluated using currently acceptable NRC
calculational methods and best available Diablo Canyon Power Plant
(DCPP) specific data. The evaluation results demonstrate that both
reactor vessels are safe for normal operations in excess of 40
years.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different [kind of] accident from any accident previously evaluated?
Response: No.
The possibility of a new or different kind of accident is not
created by the proposed additional operating periods since at least
40 years of full[-]power operation was assumed in the design and
construction of DCPP Units 1 and 2. The plant maintenance programs
are also designed to both maintain and determine the need to replace
safety-related components. These programs will continue to be
applied as they are presently to assure safe operation.
Therefore, the proposed change does not create the possibility
of a new or different [kind of] accident from any accident
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed additional operating periods do not involve a
significant reduction in a margin of safety since, as is the case
with present operation, degradation of safety-related equipment will
be identified and corrected by ongoing surveillance and maintenance
practices. Existing programs, routine maintenance, and compliance
with Technical Specifications assure that an adequate margin of
safety is maintained. These activities will remain in effect for the
duration of the proposed additional operating periods.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Attorney for licensee: Richard F. Locke, Esq., Pacific Gas and
Electric Company, P.O. Box 7442, San Francisco, California 94120.
NRC Section Chief: Daniel S. Collins (Acting).
South Carolina Electric & Gas Company, South Carolina Public Service
Authority, Docket No. 50-395, Virgil C. Summer Nuclear Station, Unit
No. 1, Fairfield County, South Carolina
Date of amendment request: June 30, 2005.
Description of amendment request: The proposed changes would revise
the Administrative Control section of the Technical Specifications
(TSs) to permit the Westinghouse best estimate methodology for loss-of-
coolant-accident (LOCA) analysis methodology to be utilized for
analyses as required by Title 10 of the Code of Federal Regulations,
Part 50, Section 46, ``Acceptance criteria for emergency core cooling
systems [ECCS] for light water nuclear power reactors' (10 CFR 50.46).
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
Implementation of the best-estimate large break LOCA methodology
and associated TS changes is proposed to increase margin to the peak
clad temperature limits defined in 10 CFR 50.46. There are no
physical plant changes or changes in manner in which the plant will
be operated as a result of this
[[Page 59088]]
change. Since the plant conditions and ECCS performance assumed in
the analysis are consistent with the plant's current design, the
proposed change in methodology will thus have no impact on the
probability of a LOCA. When applied, the best estimate methodology
shows that the ECCS is more effective than previously evaluated in
mitigating the consequences of a LOCA, as lower peak clad
temperatures are predicted relative to current 10 CFR 50.46 Appendix
K results. Since the proposed best-estimate methodology is only
applicable to a large break LOCA and since the application of the
proposed methodology shows there is a high probability that all of
the acceptance criteria contained in 10 CFR 50.46, Paragraph b are
met, the proposed change does not increase the consequences of an
accident previously evaluated.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
There are no physical changes being made to the plant. No new
modes of plant operation are being introduced. The parameters
assumed in the analysis remain within the design limits of the
existing plant equipment. All plant systems will perform as designed
during the response to a potential accident.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any previously analyzed.
3. Does this change involve a significant reduction in a margin
of safety?
Response: No.
It has been shown that the methodology used in the analysis
would more realistically describe the expected behavior of V. C.
Summer Nuclear Station systems during a postulated loss of coolant
accident. Uncertainties have been accounted for as required by 10
CFR 50.46. A sufficient number of loss of coolant accidents with
different break sizes, different locations and other variations in
properties are analyzed to provide assurance that the most severe
postulated loss of coolant accidents are calculated. It has been
shown by analysis that there is a high level of probability that all
criteria contained in 10 CFR 50.46, Paragraph b are met.
Pursuant to 10 CFR 50.91, the preceding analyses provide a
determination that the proposed Technical Specifications change
poses no significant hazard as delineated by 10 CFR 50.92.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92 (c)
are satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Thomas G. Eppink, South Carolina Electric &
Gas Company, Post Office Box 764, Columbia, South Carolina 29218.
NRC Section Chief: Evangelos C. Marinos.
STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South
Texas Project, Units 1 and 2, Matagorda County, Texas.
Date of amendment request: August 30, 2005.
Description of amendment request: The proposed amendment would
change the Technical Specifications (TSs) to reflect the use of the
Westinghouse Best Estimate Analyzer for Core Operations--Nuclear
(BEACON) to augment the functional capability of the flux mapping
system for the purpose of power distribution surveillances. In
addition, editorial changes to the TSs are proposed.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The PDMS [power distribution monitoring system] performs
continuous core power distribution monitoring. This system utilizes
the NRC-approved Westinghouse proprietary computer code BEACON to
provide data reduction for incore flux maps, core parameter
analysis, load follow operation simulation, and core prediction. It
in no way provides any protection or control system function.
Fission product barriers are not impacted by these proposed changes.
The proposed changes occurring with PDMS will not result in any
additional challenges to plant equipment that could increase the
probability of any previously evaluated accident. The changes
associated with the PDMS do not affect plant systems such that their
function in the control of radiological consequences is adversely
affected. These proposed changes will therefore not affect the
mitigation of the radiological consequences of any accident
described in the Updated Final Safety Analysis Report Update
(UFSAR).
Continuous on-line monitoring through the use of PDMS provides
significantly more information about the power distributions present
in the core than is currently available. This results in more time
(i.e., earlier determination of an adverse condition developing) for
operator action prior to having an adverse condition develop that
could lead to an accident condition or to unfavorable initial
conditions for an accident.
Each accident analysis addressed in the UFSAR is examined with
respect to changes in cycle-dependent parameters, which are obtained
from application of the NRC-approved reload design methodologies, to
ensure that the transient evaluations of reload cores are bounded by
previously accepted analyses. This examination, which is performed
in accordance with the requirements set forth in 10 CFR [Title 10 of
the Code of Federal Regulations] 50.59, ensures that future reloads
will not involve a significant increase in the probability or
consequences of any accident previously evaluated.
The three editorial changes only correct typographical errors
made in previously approved TS changes. They do not affect plant
operation or structures, systems, and components important to
safety.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequence of an accident previously
evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The implementation of the PDMS has no influence or impact on
plant operations or safety, nor does it contribute in any way to the
probability or consequences of an accident. No safety-related
equipment, safety function, or plant operation will be altered as a
result of this proposed change. The possibility for a new or
different type of accident from any accident previously evaluated is
not created since the changes associated with implementation of the
PDMS do not result in a change to the design basis of any plant
component or system. The evaluation of the effects of using the PDMS
to monitor core power distribution parameters shows that all design
standards and applicable safety criteria limits are met.
The proposed changes do not result in any event previously
deemed incredible being made credible. Implementation of the PDMS
will not result in more adverse conditions and will not result in
any increase in the challenges to safety systems. The cycle-specific
variables required by the PDMS are calculated using NRC-approved
methods. The TS will continue to require operation within the
required core operating limits and appropriate actions will be taken
if limits are exceeded.
The three editorial changes only correct typographical errors
made in previously approved TS changes. They do not affect plant
operation or structures, systems, and components important to
safety.
Therefore, the proposed changes do not create the possibility of
a new or different kind of accident from any previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The margin of safety is not affected by implementation of the
PDMS. The margin of safety provided by current TS is unchanged. The
proposed changes continue to require operation within the core
limits that are based on NRC-approved reload design methodologies.
Appropriate measures exist to control the values of these cycle-
specific limits. The proposed changes continue to ensure that
appropriate actions will be taken
[[Page 59089]]
if limits are violated. These actions remain unchanged.
The three editorial changes only correct typographical errors
made in previously approved TS changes. They do not affect plant
operation or structures, systems, and components important to
safety.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
request for amendments involves no significant hazards consideration.
Attorney for licensee: A. H. Gutterman, Esq., Morgan, Lewis &
Bockius, 1111 Pennsylvania Avenue, NW., Washington, DC 20004.
NRC Section Chief: David Terao.
Notice of Issuance of Amendments to Facility Operating Licenses
During the period since publication of the last biweekly notice,
the Commission has issued the following amendments. The Commission has
determined for each of these amendments that the application complies
with the standards and requirements of the Atomic Energy Act of 1954,
as amended (the Act), and the Commission's rules and regulations. The
Commission has made appropriate findings as required by the Act and the
Commission's rules and regulations in 10 CFR Chapter I, which are set
forth in the license amendment.
Notice of Consideration of Issuance of Amendment to Facility
Operating License, Proposed No Significant Hazards Consideration
Determination, and Opportunity for A Hearing in connection with these
actions was published in the Federal Register as indicated.
Unless otherwise indicated, the Commission has determined that
these amendments satisfy the criteria for categorical exclusion in
accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b),
no environmental impact statement or environmental assessment need be
prepared for these amendments. If the Commission has prepared an
environmental assessment under the special circumstances provision in
10 CFR 51.12(b) and has made a determination based on that assessment,
it is so indicated.
For further details with respect to the action see (1) the
applications for amendment, (2) the amendment, and (3) the Commission's
related letter, Safety Evaluation and/or Environmental Assessment as
indicated. All of these items are available for public inspection at
the Commission's Public Document Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555 Rockville Pike (first floor),
Rockville, Maryland. Publicly available records will be accessible from
the Agencywide Documents Access and Management Systems (ADAMS) Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket No. 50-461, Clinton Power Station,
Unit 1, DeWitt County, Illinois
Date of application for amendment: April 3, 2003, as supplemented
December 23, 2003, December 9 and 17, 2004, and March 30 and August 19,
2005.
Brief description of amendment: The amendment revised the Technical
Specifications (TSs) to support the application of an alternative
source term methodology in accordance with Title 10 of the Code of
Federal Regulations, Section 50.67, ``Accident Source Term,'' with the
exception that Technical Information Document 14844, ``Calculation of
Distance Factors for Power and Test Reactor Sites,'' was used as the
radiation dose basis for equipment qualification.
Date of issuance: September 19, 2005.
Effective date: As of the date of issuance and shall be implemented
within 60 days.
Amendment No.: 167.
Facility Operating License No. NPF-62: The amendment revised the
TSs.
Date of initial notice in Federal Register: September 2, 2003 (68
FR 52234).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated September 19, 2005.
The supplements dated December 23, 2003, December 9 and 17, 2004,
and March 30 and August 19, 2005 provided additional information that
clarified the application, did not expand the scope of the application
as originally noticed, and did not change the staff's original proposed
no significant hazards consideration determination.
No significant hazards consideration comments received: No.
AmerGen Energy Company, LLC, Docket No. 50-461, Clinton Power Station,
Unit 1, DeWitt County, Illinois
Date of application for amendment: November 11, 2003, as
supplemented April 16 and September 10, 2004, and March 30 and
September 21, 2005.
Brief description of amendment: The amendment revised the
instrument channel trip setpoint allowable values for thirteen
Technical Specification (TS) functions at Clinton Power Station, Unit
1.
Date of issuance: September 27, 2005.
Effective date: As of the date of issuance and shall be implemented
within 60 days.
Amendment No.: 168.
Facility Operating License No. NPF-62: The amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: March 16, 2004 (69 FR
12363).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated September 21, 2005. The supplements dated
April 16 and September 10, 2004, and March 30 and September 21, 2005,
provided additional information that clarified the application, did not
expand the scope of the application as originally noticed, and did not
change the staff's original proposed no significant hazards
consideration determination. No significant hazards consideration
comments received: No.
Calvert Cliffs Nuclear Power Plant, Inc., Docket Nos. 50-317 and 50-
318, Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert
County, Maryland
Date of application for amendments: August 3, 2004, as supplemented
on July 8 and August 26, 2005.
Brief description of amendments: The amendments extend the
surveillance frequency interval from monthly to quarterly for Technical
Specification surveillance requirement (SR) 3.3.3.1, which involves a
channel functional test of each reactor trip circuit breaker (RTCB).
SRs 3.3.3.1 and 3.3.3.2 will be scheduled such that the RTCBs testing
is performed every 6 weeks, which meets the vendor-recommended interval
for cycling each RTCB.
Date of issuance: September 26, 2005.
Effective date: As of the date of issuance to be implemented within
60 days.
Amendment Nos.: 275 and 252.
Renewed Facility Operating License Nos. DPR-53 and DPR-69:
Amendments revised the Technical Specifications.
Date of initial notice in Federal Register: January 4, 2005 (70 FR
400).
[[Page 59090]]
The July 8 and August 26, 2005, supplemental letters provided
additional information that clarified the application, did not expand
the scope of the application as originally noticed, and did not change
the staff's original proposed no significant hazards consideration
determination.
The Commission's related evaluation of these amendments is
contained in a Safety Evaluation dated September 26, 2005.
No significant hazards consideration comments received: No.
Dominion Nuclear Connecticut, Inc., Docket No. 50-245, Millstone Power
Station Unit No. 1, New London County, Connecticut
Date of application for amendment: September 8, 2004, as
supplemented by letters dated May 5 and July 27, 2005.
Brief description of amendment: The amendment revised the Millstone
Power Station, Unit No. 1 Technical Specifications (TSs) to support the
implementation of the proposed Dominion Nuclear Facility Quality
Assurance Program (Topical Report DOM-QA-1). Implementation of this
Topical Report would create a common quality assurance program for all
sites owned by Dominion Nuclear Connecticut, Inc. Review of this
proposed amendment was requested in concert with the review of the
Topical Report.
Date of issuance: September 15, 2005.
Effective date: As of the date of issuance, and shall be
implemented by February 28, 2006.
Amendment No.: 115.
Facility Operating License No. DPR-21: The amendment revised the
TSs.
Date of initial notice in Federal Register: January 18, 2005 (70 FR
2888).
The additional information provided in the supplemental letters
dated May 5 and July 27, 2005, did not expand the scope of the
application as noticed and did not change the NRC staff's original
proposed no significant hazards consideration determination.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated September 15, 2005.
No significant hazards consideration comments received: No.
Dominion Nuclear Connecticut, Inc., Docket No. 50-336, Millstone Power
Station, Unit No. 2, New London County, Connecticut
Date of application for amendment: July 15, 2004, as supplemented
by letter dated August 23, 2004.
Brief description of amendment: The amendment revised the Facility
Operating License DPR-65 to address the resolution of a non-
conservative Technical Specifications (TSs) associated with control
room isolation radiation monitoring instrumentation. Specifically, the
amendment would revise the TSs to require two operable channels of
control room isolation radiation monitoring instrumentation.
Date of issuance: September 23, 2005.
Effective date: As of the date of issuance and shall be implemented
within 30 days from the date of issuance.
Amendment No.: 289.
Facility Operating License No. DPR-65: The amendment revised the
TSs.
Date of initial notice in Federal Register: January 18, 2005 (70 FR
2887).
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated September 23, 2005.
No significant hazards consideration comments received: No.
Dominion Nuclear Connecticut, Inc., et al., Docket No. 50-423,
Millstone Power Station, Unit No. 3, New London County, Connecticut
Date of application for amendment: April 15, 2004, as supplemented
on June 23, 2005.
Brief description of amendment: The amendment approves
modifications to the Fire Protection Program. Specifically, the
modifications involve converting the existing automatic carbon dioxide
fire suppression systems installed in the cable spreading room to
manual actuation.
Date of issuance: September 22, 2005.
Effective date: As of the date of issuance and shall be implemented
within 90 days from the date of issuance.
Amendment No.: 227.
Facility Operating License No. NPF-49: The amendment allows for
conversion from an automatic to a manual carbon dioxide suppression
system in the cable spreading area.
Date of initial notice in Federal Register: July 6, 2004 (69 FR
40672). The supplement dated June 23, 2005, provided clarifying
information and did not change the initial proposed no significant
hazards consideration determination.
The Commission's related evaluation of the amendment is contained
in a Safety Evaluation dated September 22, 2005.
No significant hazards consideration comments received: No.
Dominion Nuclear Connecticut, Inc., Docket Nos. 50-336 and 50-423,
Millstone Power Station, Unit Nos. 2 and 3, New London County,
Connecticut
Date of application for amendments: September 8, 2004, as
supplemented by letters dated May 5 and July 27, 2005.
Brief description of amendments: The amendments revised the
Millstone Power Station, Unit N