Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations, 21449-21470 [05-8166]
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Federal Register / Vol. 70, No. 79 / Tuesday, April 26, 2005 / Notices
[Docket No. 50–368]
Entergy Operations, Inc., Arkansas
Nuclear One, Unit 2; Notice of
Availability of the Final Supplement 19
to the Generic Environmental Impact
Statement for the License Renewal of
Arkansas Nuclear One, Unit 2
Notice is hereby given that the U.S.
Nuclear Regulatory Commission
(Commission) has published a final
plant-specific supplement to the
Generic Environmental Impact
Statement (GEIS), NUREG–1437,
regarding the renewal of operating
license NPF–6 for an additional 20 years
of operation at Arkansas Nuclear One,
Unit 2 (ANO–2). ANO–2 is located in
Pope County, Arkansas, approximately
6 miles west-northwest of Russellville,
Arkansas. Possible alternatives to the
proposed action (license renewal)
include no action and reasonable
alternative energy sources.
In Section 9.3 of the final Supplement
19 to the GEIS, the staff concludes that
based on: (1) The analysis and findings
in the GEIS; (2) the environmental
report submitted by Entergy; (3)
consultation with Federal, State, and
local agencies; (4) the staff’s own
independent review; and (5) the staff’s
consideration of public comments
received during the environmental
review, the staff recommends that the
Commission determine that the adverse
environmental impacts of license
renewal for ANO–2, are not so great that
preserving the option of license renewal
for energy-planning decisionmakers
would be unreasonable.
The final Supplement 19 to the GEIS
is available for public inspection in the
NRC Public Document Room (PDR)
located at One White Flint North, 11555
Rockville Pike, Rockville, Maryland, or
from the Publicly Available Records
(PARS) component of NRC’s
Agencywide Documents Access and
Management System (ADAMS). ADAMS
is accessible from the NRC Web site at
https://www.nrc.gov/reading-rm/
adams.html (the Public Electronic
Reading Room). Persons who do not
have access to ADAMS, or who
encounter problems in accessing the
documents located in ADAMS, should
contact the PDR reference staff at 1–
800–397–4209, 301–415–4737, or by email to pdr@nrc.gov. In addition, the
Ross Pendergraft Library at Arkansas
Tech University, 305 West Q Street,
Russellville, Arkansas 72801, has agreed
to make the final plant-specific
supplement to the GEIS available for
public inspection.
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Mr.
Thomas Kenyon, License Renewal and
Environmental Impacts Program,
Division of Regulatory Improvement
Programs, U.S. Nuclear Regulatory
Commission, Washington, DC 20555.
Mr. Kenyon may be contacted at 301–
415–1120 or TJK@nrc.gov.
FOR FURTHER INFORMATION CONTACT:
NUCLEAR REGULATORY
COMMISSION
Jkt 205001
Dated in Rockville, Maryland, this 7th day
of April, 2005.
For the Nuclear Regulatory Commission.
Pao-Tsin Kuo,
Program Director, License Renewal and
Environmental Impacts Program, Division of
Regulatory Improvement Programs, Office of
Nuclear Reactor Regulation.
[FR Doc. E5–1967 Filed 4–25–05; 8:45 am]
BILLING CODE 7590–01–P
NUCLEAR REGULATORY
COMMISSION
Biweekly Notice; Applications and
Amendments to Facility Operating
Licenses Involving No Significant
Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the
Atomic Energy Act of 1954, as amended
(the Act), the U.S. Nuclear Regulatory
Commission (the Commission or NRC
staff) is publishing this regular biweekly
notice. The Act requires the
Commission publish notice of any
amendments issued, or proposed to be
issued and grants the Commission the
authority to issue and make
immediately effective any amendment
to an operating license upon a
determination by the Commission that
such amendment involves no significant
hazards consideration, notwithstanding
the pendency before the Commission of
a request for a hearing from any person.
This biweekly notice includes all
notices of amendments issued, or
proposed to be issued from April 1,
2005, through April 14, 2005. The last
biweekly notice was published on April
12, 2005 (70 FR 19110).
Notice of Consideration of Issuance of
Amendments to Facility Operating
Licenses, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a
proposed determination that the
following amendment requests involve
no significant hazards consideration.
Under the Commission’s regulations in
10 CFR 50.92, this means that operation
of the facility in accordance with the
proposed amendment would not (1)
involve a significant increase in the
probability or consequences of an
accident previously evaluated; or (2)
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21449
create the possibility of a new or
different kind of accident from any
accident previously evaluated; or (3)
involve a significant reduction in a
margin of safety. The basis for this
proposed determination for each
amendment request is shown below.
The Commission is seeking public
comments on this proposed
determination. Any comments received
within 30 days after the date of
publication of this notice will be
considered in making any final
determination. Within 60 days after the
date of publication of this notice, the
licensee may file a request for a hearing
with respect to issuance of the
amendment to the subject facility
operating license and any person whose
interest may be affected by this
proceeding and who wishes to
participate as a party in the proceeding
must file a written request for a hearing
and a petition for leave to intervene.
Normally, the Commission will not
issue the amendment until the
expiration of 60 days after the date of
publication of this notice. The
Commission may issue the license
amendment before expiration of the 60day period provided that its final
determination is that the amendment
involves no significant hazards
consideration. In addition, the
Commission may issue the amendment
prior to the expiration of the 30-day
comment period should circumstances
change during the 30-day comment
period such that failure to act in a
timely way would result, for example in
derating or shutdown of the facility.
Should the Commission take action
prior to the expiration of either the
comment period or the notice period, it
will publish in the Federal Register a
notice of issuance. Should the
Commission make a final No Significant
Hazards Consideration Determination,
any hearing will take place after
issuance. The Commission expects that
the need to take this action will occur
very infrequently.
Written comments may be submitted
by mail to the Chief, Rules and
Directives Branch, Division of
Administrative Services, Office of
Administration, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and should cite the publication
date and page number of this Federal
Register notice. Written comments may
also be delivered to Room 6D22, Two
White Flint North, 11545 Rockville
Pike, Rockville, Maryland, from 7:30
a.m. to 4:15 p.m. Federal workdays.
Copies of written comments received
may be examined at the Commission’s
Public Document Room (PDR), located
at One White Flint North, Public File
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Area O1F21, 11555 Rockville Pike (first
floor), Rockville, Maryland. The filing of
requests for a hearing and petitions for
leave to intervene is discussed below.
Within 60 days after the date of
publication of this notice, the licensee
may file a request for a hearing with
respect to issuance of the amendment to
the subject facility operating license and
any person whose interest may be
affected by this proceeding and who
wishes to participate as a party in the
proceeding must file a written request
for a hearing and a petition for leave to
intervene. Requests for a hearing and a
petition for leave to intervene shall be
filed in accordance with the
Commission’s ‘‘Rules of Practice for
Domestic Licensing Proceedings’’ in 10
CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309,
which is available at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the Agencywide
Documents Access and Management
System’s (ADAMS) Public Electronic
Reading Room on the Internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a
request for a hearing or petition for
leave to intervene is filed within 60
days, the Commission or a presiding
officer designated by the Commission or
by the Chief Administrative Judge of the
Atomic Safety and Licensing Board
Panel, will rule on the request and/or
petition; and the Secretary or the Chief
Administrative Judge of the Atomic
Safety and Licensing Board will issue a
notice of a hearing or an appropriate
order.
As required by 10 CFR 2.309, a
petition for leave to intervene shall set
forth with particularity the interest of
the petitioner in the proceeding, and
how that interest may be affected by the
results of the proceeding. The petition
should specifically explain the reasons
why intervention should be permitted
with particular reference to the
following general requirements: (1) The
name, address, and telephone number of
the requestor or petitioner; (2) the
nature of the requestor’s/petitioner’s
right under the Act to be made a party
to the proceeding; (3) the nature and
extent of the requestor’s/petitioner’s
property, financial, or other interest in
the proceeding; and (4) the possible
effect of any decision or order which
may be entered in the proceeding on the
requestor’s/petitioner’s interest. The
petition must also set forth the specific
contentions which the petitioner/
requestor seeks to have litigated at the
proceeding.
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Each contention must consist of a
specific statement of the issue of law or
fact to be raised or controverted. In
addition, the petitioner/requestor shall
provide a brief explanation of the bases
for the contention and a concise
statement of the alleged facts or expert
opinion which support the contention
and on which the petitioner/requestor
intends to rely in proving the contention
at the hearing. The petitioner/requestor
must also provide references to those
specific sources and documents of
which the petitioner is aware and on
which the petitioner/requestor intends
to rely to establish those facts or expert
opinion. The petition must include
sufficient information to show that a
genuine dispute exists with the
applicant on a material issue of law or
fact. Contentions shall be limited to
matters within the scope of the
amendment under consideration. The
contention must be one which, if
proven, would entitle the petitioner/
requestor to relief. A petitioner/
requestor who fails to satisfy these
requirements with respect to at least one
contention will not be permitted to
participate as a party.
Those permitted to intervene become
parties to the proceeding, subject to any
limitations in the order granting leave to
intervene, and have the opportunity to
participate fully in the conduct of the
hearing.
If a hearing is requested, and the
Commission has not made a final
determination on the issue of no
significant hazards consideration, the
Commission will make a final
determination on the issue of no
significant hazards consideration. The
final determination will serve to decide
when the hearing is held. If the final
determination is that the amendment
request involves no significant hazards
consideration, the Commission may
issue the amendment and make it
immediately effective, notwithstanding
the request for a hearing. Any hearing
held would take place after issuance of
the amendment. If the final
determination is that the amendment
request involves a significant hazards
consideration, any hearing held would
take place before the issuance of any
amendment.
A request for a hearing or a petition
for leave to intervene must be filed by:
(1) First class mail addressed to the
Office of the Secretary of the
Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, Attention: Rulemaking and
Adjudications Staff; (2) courier, express
mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor,
One White Flint North, 11555 Rockville
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Pike, Rockville, Maryland, 20852,
Attention: Rulemaking and
Adjudications Staff; (3) E-mail
addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission,
HearingDocket@nrc.gov; or (4) facsimile
transmission addressed to the Office of
the Secretary, U.S. Nuclear Regulatory
Commission, Washington, DC,
Attention: Rulemakings and
Adjudications Staff at (301) 415–1101,
verification number is (301) 415–1966.
A copy of the request for hearing and
petition for leave to intervene should
also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory
Commission, Washington, DC 20555–
0001, and it is requested that copies be
transmitted either by means of facsimile
transmission to (301) 415–3725 or by email to OGCMailCenter@nrc.gov. A copy
of the request for hearing and petition
for leave to intervene should also be
sent to the attorney for the licensee.
Nontimely requests and/or petitions
and contentions will not be entertained
absent a determination by the
Commission or the presiding officer of
the Atomic Safety and Licensing Board
that the petition, request and/or the
contentions should be granted based on
a balancing of the factors specified in 10
CFR 2.309(a)(1)(i)–(viii).
For further details with respect to this
action, see the application for
amendment which is available for
public inspection at the Commission’s
PDR, located at One White Flint North,
Public File Area 01F21, 11555 Rockville
Pike (first floor), Rockville, Maryland.
Publicly available records will be
accessible from the ADAMS Public
Electronic Reading Room on the Internet
at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If
you do not have access to ADAMS or if
there are problems in accessing the
documents located in ADAMS, contact
the PDR Reference staff at 1 (800) 397–
4209, (301) 415–4737 or by e-mail to
pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket
No. 50–461, Clinton Power Station, Unit
1, DeWitt County, Illinois
Date of amendment request: February
25, 2005.
Description of amendment request:
The proposed change would delete
Section 2.G of the Clinton’s Facility
Operating License (FOL), NPF–62,
which requires AmerGen Energy
Company, LLC, to report violations of
the requirements contained in Section
2.C of this license. The proposed change
will reduce unnecessary regulatory
burden and will allow AmerGen to take
full advantage of the revisions to Title
10, Code of Federal Regulations (10
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CFR), Section 50.72, ‘‘Immediate
notification requirements for operating
nuclear power reactors,’’ and 10 CFR
50.73, ‘‘Licensee event report system.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
The proposed change involves an
administrative change only. The proposed
change does not involve the modification of
any plant equipment or affect plant
operation. The proposed change will have no
impact on any safety related structures,
systems or components. The reporting
requirement section of the FOL is not
required because the requirements are either
adequately addressed by 10 CFR 50.72 and
10 CFR 50.73, or other regulatory
requirements, or are not required based on
the nature of the Condition.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
The proposed change has no impact on the
design, function or operation of any plant
structure, system or component. The
proposed change is administrative in nature
and does not affect plant equipment or
accident analyses. The reporting requirement
section of the FOL is not required because
the requirements are either adequately
addressed by 10 CFR 50.72 and 10 CFR
50.73, or other regulatory requirements, or
are not required based on the nature of the
Condition.
Therefore, the proposed change will not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
The proposed change is administrative in
nature, does not negate any existing
requirement, and does not adversely affect
existing plant safety margins or the reliability
of the equipment assumed to operate in the
safety analysis. As such, there is no change
being made to safety analysis assumptions,
safety limits or safety system settings that
would adversely affect plant safety as a result
of the proposed change. Margins of safety are
unaffected by deletion of the reporting
requirement that is adequately addressed
elsewhere.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
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satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendment involves no
significant hazards consideration.
Attorney for licensee: Mr. Thomas S.
O’Neill, Associate General Counsel,
Exelon Generation Company, LLC, 4300
Winfield Road, Warrenville, IL 60555.
NRC Section Chief: Gene Y. Suh.
AmerGen Energy Company, LLC, Docket
No. 50–461, Clinton Power Station, Unit
1, DeWitt County, Illinois
Date of amendment request: March
25, 2005.
Description of amendment request:
The proposed change would revise
Technical Specification Surveillance
Requirement (SR) 3.6.1.3.8 to add a note
excluding leakage through primary
containment penetrations 1MC–101 and
1MC–102 from the secondary
containment bypass leakage total
specified in the SR.
Implementation of this proposed
change will provide operational
flexibility by allowing Clinton Power
Station (CPS) to utilize the additional
margin in the regulatory dose limit
analysis that supports the
implementation of the alternative source
term.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed amendment adds a note
excluding the leakage through the primary
containment purge lines from the secondary
containment bypass leakage based on
separate analysis of these paths using the
assumptions in the alternative source term
(AST) revision to the loss of coolant accident
(LOCA) analysis.
The proposed change does not require
modification to the facility. The proposed
change in secondary containment bypass
leakage does not affect the operation of any
facility equipment, the interface between
facility systems, or the reliability of any
equipment. In addition, secondary
containment bypass leakage does not
constitute an initiator of any previously
evaluated accidents. Therefore, the proposed
amendment does not involve a significant
increase in the probability of an accident
previously evaluated.
The radiological consequences of the
LOCA analysis using the primary
containment purge line leakage as separate
from the secondary containment bypass
leakage, has been evaluated as part of the
application of AST assumptions. The results
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conclude that the radiological consequences
remain within applicable regulatory limits.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create
the possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change does not affect the
design, functional performance or operation
of the facility. No new equipment is being
introduced and installed equipment is not
being operated in a new or different manner.
Similarly, the proposed change does not
affect the design or operation of any
structures, systems or components involved
in the mitigation of any accidents, nor does
it affect the design or operation of any
component in the facility such that new
equipment failure modes are created. There
are no set points at which protective or
mitigative actions are initiated that are
affected by this proposed action. No change
is being made to procedures relied upon to
respond to an off-normal event.
As such the proposed amendment will not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed amendment involve
a significant reduction in a margin of safety?
Response: No.
Margins of safety are established in the
design of components, the configuration of
components to meet certain performance
parameters, and in the establishment of set
points to initiate alarms or actions. The
proposed change adds a note excluding the
leakage through the primary containment
purge lines from the secondary containment
bypass leakage based on separate analysis of
these paths using the assumptions in the AST
revision to the LOCA analysis. There is no
change in the design of the affected systems,
no alteration of the set points at which
alarms or actions are initiated, and no change
in plant configuration from original design.
The margin of safety is considered to be
that provided by meeting the applicable
regulatory limits. The AST analysis indicates
that the doses following a LOCA remain
within the regulatory limits, and therefore,
there is not a significant reduction in a
margin of safety. The AST analysis confirms
the change continues to ensure that the doses
at the exclusion area and low population
zone boundaries, as well as the control room,
are within the corresponding regulatory
limits.
Therefore, operation of CPS in accordance
with the proposed change will not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendment involves no
significant hazards consideration.
Attorney for licensee: Mr. Thomas S.
O’Neill, Associate General Counsel,
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Exelon Generation Company, LLC, 4300
Winfield Road, Warrenville, IL 60555.
NRC Section Chief: Gene Y. Suh.
AmerGen Energy Company, LLC, Docket
No. 50–461, Clinton Power Station, Unit
1, DeWitt County, Illinois
Date of amendment request: April 1,
2005.
Description of amendment request:
The proposed changes would
incorporate into the Technical
Specifications (TSs) the Oscillation
Power Range Monitor (OPRM)
instrumentation that will be declared
operable within 30 days after
completion of the February 2006
refueling outage. The proposed changes
would add TS Section 3.3.1.3,
‘‘Oscillation Power Range Monitor
(OPRM) Instrumentation,’’ and would
revise TS Sections 3.4.1, ‘‘Recirculation
Loops Operating,’’ and 5.6.5, ‘‘Core
Operating Limits Report (COLR).’’ In
addition, the changes would insert a
new TS section for the OPRM
instrumentation, delete the current
thermal-hydraulic instability
administrative requirements, and add
the appropriate references for the OPRM
trip set points and methodology. Clinton
Power Station (CPS) will activate the
automatic reactor protection system
(i.e., scram) outputs of the OPRM
instrumentation upon implementation
of these proposed TS changes.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed changes specify limiting
conditions for operation, required actions
and surveillance requirements for the OPRM
system, and allows operation in regions of
the power to flow map currently restricted by
the requirements of the Interim Corrective
Actions (ICAs) and certain limiting
conditions of operation of TS Section 3.4.1,
‘‘Recirculation Loops Operating.’’ The
restrictions of the ICAs and TS Section 3.4.1
were imposed to ensure adequate capability
to detect and suppress conditions consistent
with the onset of thermal-hydraulic
oscillations that may develop into a thermalhydraulic instability event. A thermalhydraulic instability event has the potential
to challenge the Minimum Critical Power
Ratio (MCPR) safety limit. The OPRM system
can automatically detect and suppress
conditions necessary for thermal-hydraulic
instability. With the activation of the OPRM
system, the restrictions of the ICAs and TS
Section 3.4.1 will no longer be required.
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This proposed change has no impact on
any of the existing neutron monitoring
functions. When the OPRM is operable with
operating limits as specified in the Core
Operating Limits Report (COLR), the OPRM
can automatically detect the imminent onset
of local power oscillations and generate a trip
signal. Actuation of a Reactor Protection
System (RPS) trip (i.e., scram) will suppress
conditions necessary for thermal-hydraulic
instability and decrease the probability of a
thermal-hydraulic instability event. In the
event the trip capability of the OPRM is not
maintained, the proposed changes limit the
period of time before an alternate method to
detect and suppress thermal-hydraulic
oscillations is required. CPS intends to
utilize the ICAs as the alternative method for
ensuring thermal-hydraulic oscillations do
not occur. Since the duration of this period
of time is limited, the increase in the
probability of a thermal-hydraulic instability
event is not significant.
Activation of the OPRM scram function
will replace the current methods that require
operators to insert an immediate manual
reactor scram in certain reactor operating
regions where thermal hydraulic instabilities
could potentially occur. While these regions
will continue to be avoided during normal
operation, certain transients, such as a
reduction in reactor recirculation flow, could
place the reactor in these regions. During
these transient conditions, with the OPRM
instrumentation scram function activated; an
immediate manual scram will no longer be
required. This may potentially cause a
marginal increase in the probability of
occurrence of an instability event. This
potential increase in probability is acceptable
because the OPRM function will
automatically detect the instability condition
and initiate a reactor scram before the
Minimum Critical Power Ratio (MCPR)
Safety Limit is reached. Consequences of the
potential instability event are reduced
because of the more reliable automatic
detection and suppression of an instability
event, and the elimination of dependence on
the manual operator actions. Operators
monitor for indications of thermal hydraulic
instability when the reactor is operating in
regions of potential instability as a backup to
the OPRM instrumentation.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed changes replace procedural
actions that were established to avoid
operating conditions where reactor
instabilities might occur with an NRC
approved automatic detect and suppress
function (i.e., OPRM).
Potential failures in the OPRM trip
function could result in either failure to take
the required mitigating action or an
unintended reactor scram. These are the
same potential effects of failure of the
operator to take the correct appropriate
action under the current procedural actions.
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The effects of failure of the OPRM equipment
are limited to reduced or failed mitigation,
but such failure cannot cause an instability
event or other type of accident.
The OPRM system uses input signals
shared with the Average Power Range
Monitor (APRM) system and rod block
functions to monitor core conditions and
generate a Reactor Protection System (RPS)
trip when required. Quality requirements for
software design, testing, implementation and
module self-testing of the OPRM system
provide assurance that no new equipment
malfunctions due to software errors are
created. The design of the OPRM system also
ensures that neither operation nor
malfunction of the OPRM system will
adversely impact the operation of the other
systems and no accident or equipment
malfunction of these other systems could
cause the OPRM system to malfunction or
cause a different kind of accident. No new
failure modes of either the new OPRM
equipment or of the existing APRM
equipment have been introduced.
Operation in regions currently restricted by
the ICAs and TS Section 3.4.1 is within the
nominal operating domain and ranges of
plant systems and components for which
postulated equipment and accidents have
been evaluated. Therefore, operation within
these regions does not create the possibility
of a new or different kind of accident from
any previously evaluated.
These proposed changes which specify
limiting conditions for operations, required
actions and surveillance requirements of the
OPRM system and allow operation in certain
regions of the power-to-flow map do not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The OPRM system monitors small groups
of Local Power Range Monitor (LPRM)
signals for indication of local variations of
core power consistent with thermalhydraulic oscillations and generates an RPS
trip when conditions consistent with the
onset of oscillations are detected. An
unmitigated thermal-hydraulic instability
event has the potential to result in a
challenge to the MCPR safety limit. The
OPRM system provides the capability to
automatically detect and suppress conditions
that might result in a thermal-hydraulic
instability event and thereby maintains the
margin of safety by providing automatic
protection for the MCPR safety limit while
reducing the burden on the control room
operators significantly. The OPRM trip
provides a trip output of the same type as
currently used for the APRM. Its failure
modes and types are similar to those for the
present APRM output. Since the MCPR
Safety Limit will not be exceeded as a result
of an instability event following
implementation of the OPRM trip function, it
is concluded that the proposed change does
not reduce the margin of safety.
Operation in regions currently restricted by
the requirements of the ICAs and TS Section
3.4.1 is within the nominal operating domain
assumed for identifying the range of initial
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conditions considered in the analysis of
anticipated operational occurrences and
postulated accidents. Therefore, operation in
these regions does not involve a significant
reduction in the margin of safety.
The proposed changes, which specify
limiting conditions for operations, required
actions and surveillance requirements of the
OPRIVI system and allow operation in
certain regions of the power to flow map, do
not involve a significant reduction in a
margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendment involves no
significant hazards consideration.
Attorney for licensee: Mr. Thomas S.
O’Neill, Associate General Counsel,
Exelon Generation Company, LLC, 4300
Winfield Road, Warrenville, IL 60555.
NRC Section Chief: Gene Y. Suh.
AmerGen Energy Company, LLC, Docket
No. 50–219, Oyster Creek Nuclear
Generating Station, Ocean County, New
Jersey
Date of amendment request: February
25, 2005.
Description of amendment request:
The proposed change would delete
Section 2.E of the Oyster Creek’s
Facility Operating License (FOL), DPR–
16, which requires AmerGen Energy
Company, LLC, to report violations of
the requirements contained in Section
2.C of this license. The proposed change
will reduce unnecessary regulatory
burden and will allow AmerGen to take
full advantage of the revisions to Title
10, Code of Federal Regulations (10
CFR), Section 50.72, ‘‘Immediate
notification requirements for operating
nuclear power reactors,’’ and 10 CFR
50.73, ‘‘Licensee event report system.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change involves an
administrative change only. The proposed
change does not involve the modification of
any plant equipment or affect plant
operation. The proposed change will have no
impact on any safety related structures,
systems or components. The reporting
requirement section of the FOL is not
required because the requirements are either
adequately addressed by 10 CFR 50.72 and
10 CFR 50.73, or other regulatory
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requirements, or are not required based on
the nature of the Condition.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change has no impact on the
design, function or operation of any plant
structure, system or component. The
proposed change is administrative in nature
and does not affect plant equipment or
accident analyses. The reporting requirement
section of the FOL is not required because
the requirements are either adequately
addressed by 10 CFR 50.72 and 10 CFR
50.73, or other regulatory requirements, or
are not required based on the nature of the
Condition.
Therefore, the proposed change will not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change is administrative in
nature, does not negate any existing
requirement, and does not adversely affect
existing plant safety margins or the reliability
of the equipment assumed to operate in the
safety analysis. As such, there is no change
being made to safety analysis assumptions,
safety limits or safety system settings that
would adversely affect plant safety as a result
of the proposed change. Margins of safety are
unaffected by deletion of the reporting
requirement that is adequately addressed
elsewhere.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendment involves no
significant hazards consideration.
Attorney for licensee: Mr. Thomas S.
O’Neill, Associate General Counsel,
Exelon Generation Company, LLC, 4300
Winfield Road, Warrenville, IL 60555.
NRC Section Chief: Richard J. Laufer.
Detroit Edison Company, Docket No.
50–341, Fermi 2, Monroe County,
Michigan
Date of amendment request: March
17, 2005.
Description of amendment request:
The proposed amendment would revise
Technical Specification 3.4.10, ‘‘Reactor
Coolant System (RCS) Pressure and
Temperature (P/T) Limits,’’ to replace
the combination figure with separate P/
T limit figures for each one of the three
categories of operation: hydrostatic
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pressure test [Curve A], non-nuclear
heatup and cooldown [Curve B], and
nuclear (core critical) operation [Curve
C]. The new curves also provide
composite limits for all reactor pressure
vessel (RPV) regions including core
beltline region. RPV bottom head
individual limit curves are
superimposed on Curves A and B. In
addition, two sets of curves are
calculated; one for 32 effective full
power years (EFPY) which represents
the end of the current 40-year plant
license and the other one is for 24 EFPY
which has been selected as an
intermediate point between the current
EFPY and 32 EFPY.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed change does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated.
The revised P/T curves are based on the
1998 Edition of the American Society of
Mechanical Engineers (ASME) Boiler and
Pressure Vessel (B&PV) Code, Section XI,
including the 2000 Addenda. This edition of
the Code has been approved for use in both
10 CFR 50.55a and Regulatory Guide (RG)
1.147. The revised curves are also based on
updated fluence calculations performed
utilizing NRC-approved methodology
consistent with RG 1.190 for calculating
Reactor Pressure Vessel (RPV) neutron
fluence. Revised fluence calculations are
applicable for 24 and for 32 Effective Full
Power Years (EFPY). The 32 EFPY represents
a conservative exposure level at the end of
the current 40-year plant operating license.
The proposed change incorporates
adjustment of the reference temperature for
all beltline material to account for irradiation
effects and provide a comparable level of
protection as previously evaluated and
approved. The adjusted reference
temperature calculations were performed in
accordance with the requirements of 10 CFR
50 Appendix G using the guidance contained
in RG 1.99, Revision 2, to provide operating
limits for up to 32 EFPY.
There are no changes being made to the
RCS pressure boundary or to RCS material,
design or construction standards. The
proposed P/T curves define limits that
continue to ensure the prevention of
nonductile failure of the RCS pressure
boundary. The revision of the P/T curves
does not alter any assumptions previously
made in the radiological consequence
evaluations since the integrity of the RCS
pressure boundary is unaffected. Therefore,
the proposed changes will not significantly
increase the probability or consequences of
an accident previously evaluated.
2. The proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
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The revised P/T curves are based on a later
edition and addenda of the ASME Code that
incorporates current industry standards for
the curves. The revised curves are also based
on an RPV fluence that has been recalculated
in accordance with the methodology of RG
1.190. The proposed change does not involve
a modification to plant structures, systems or
components. There is no effect on the
function of any plant system, and no newly
introduced system interactions. The
proposed change does not create new failure
modes or cause any systems, structures or
components to be operated beyond their
design bases. Therefore, the proposed change
does not create the possibility of a new or
different kind of accident from any
previously evaluated.
3. The proposed change does not involve
a significant reduction in the margin of
safety.
The proposed P/T curves define the limits
of operation to prevent nonductile failure of
the RPV upper vessel, bottom head and
beltline region. The new curves conform to
the guidance contained in RG 1. 190,
‘‘Calculational and Dosimetry Methods for
Determining Pressure Vessel Neutron
Fluence,’’ and RG 1.99, Revision 2,
‘‘Radiation Embrittlement of Reactor Vessel
Materials,’’ and maintain the safety margins
specified in 10 CFR 50 Appendix G.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David G.
Pettinari, Legal Department, 688 WCB,
Detroit Edison Company, 2000 2nd
Avenue, Detroit, Michigan 48226–1279
NRC Section Chief: L. Raghavan.
Detroit Edison Company, Docket No.
50–341, Fermi 2, Monroe County,
Michigan
Date of amendment request: March
17, 2005. This amendment request
supercedes, in its entirety, a previous
application dated March 19, 2004,
published in the Federal Register on
June 22, 2004 (69 FR 34698).
Description of amendment request:
The proposed amendment would revise
Technical Specification (TS) 3.3.6.1,
‘‘Primary Containment Isolation
Instrumentation,’’ to correct a formatting
error introduced during conversion to
Improved Technical Specifications (ITS)
by replacing ‘‘1 per room’’ with ‘‘2’’ for
the required channels per trip system
for the reactor water cleanup (RWCU)
area ventilation differential
temperature—high primary containment
isolation instrumentation.
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Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed amendment involve
a significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change restores the number
of Required Channels Per Trip System of the
RWCU Area Ventilation Differential
Temperature—High isolation, Function 5.c of
Table 3.3.6.1–1 of TS 3.3.6.1, Primary
Containment Isolation Instrumentation, to its
pre-ITS value and adds a note to Table
3.3.6.1–1 of TS 3.3.6.1, Primary Containment
Isolation Instrumentation, that ensures,
during surveillance testing and normal
operation, there will always be at least one
instrument monitoring for a small leak in all
RWCU locations. No changes in operating
practices or physical plant equipment are
created as a result of this change. Therefore,
the proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different type of
accident from any accident previously
evaluated?
Response: No.
The proposed change restores the number
of Required Channels Per Trip System of the
RWCU Area Ventilation Differential
Temperature—High isolation, Function 5.c of
Table 3.3.6.1–1 of TS 3.3.6.1, Primary
Containment Isolation Instrumentation, to its
pre-ITS value and adds a note to Table
3.3.6.1–1 of TS 3.3.6.1, Primary Containment
Isolation Instrumentation, that ensures,
during surveillance testing and normal
operation, there will always be at least one
instrument monitoring for a small leak in all
RWCU locations. No physical change in plant
equipment will result from this proposed
change. Therefore, the proposed change does
not create the possibility of a new or different
type of accident from any previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change restores the number
of Required Channels Per Trip System of the
RWCU Area Ventilation Differential
Temperature—High isolation, Function 5.c of
Table 3.3.6.1–1 of TS 3.3.6.1, Primary
Containment Isolation Instrumentation, to its
pre-ITS value and adds a note to Table
3.3.6.1–1 of TS 3.3.6.1, Primary Containment
Isolation Instrumentation, that ensures,
during surveillance testing and normal
operation, there will always be at least one
instrument monitoring for a small leak in all
RWCU locations. Therefore, the proposed
change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
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review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: David G.
Pettinari, Legal Department, 688 WCB,
Detroit Edison Company, 2000 2nd
Avenue, Detroit, Michigan 48226–1279
NRC Section Chief: L. Raghavan.
Duke Energy Corporation, et al., Docket
Nos. 50–413 and 50–414, Catawba
Nuclear Station, Units 1 and 2, York
County, South Carolina
Date of amendment request:
November 16, 2004.
Description of amendment request:
The amendments would revise
Technical Specifications (TS) 3.5.2,
‘‘Emergency Core Cooling System,’’ TS
3.6.6, ‘‘Containment Spray System,’’ TS
3.6.17, ‘‘Containment Valve Injection
Water System,’’ TS 3.7.5, ‘‘Auxiliary
Feedwater System,’’ TS 3.7.7,
‘‘Component Cooling Water System,’’
TS 3.7.8, ‘‘Nuclear Service Water
System (NSWS),’’ TS 3.7.10, ‘‘Control
Room Area Ventilation System’’ TS
3.7.12, ‘‘Auxiliary Building Filtered
Ventilation Exhaust System,’’ and TS
3.8.1, ‘‘AC Sources-Operating’’ for
Catawba, Units 1 and 2. The revisions
would allow for the ‘‘A’’ and ‘‘B’’ NSWS
headers to be take out of service for up
to 14 days each for system upgrades.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does operation of the facility in
accordance with the proposed amendment
involve a significant increase in the
probability or consequences of an accident
previously evaluated?
Response: No.
The pipe repair project for the [nuclear
service water system] NSWS and proposed
[technical specifications] TS changes have
been evaluated to assess their impact on
normal operation of the systems affected and
to ensure that the design basis safety
functions are preserved. During the pipe
repair the other NSWS train will be operable
and no major maintenance or testing will be
done on the operable train. The operable
train will be protected to help ensure it
would be available if called upon.
This pipe repair project will enhance the
long term structural integrity in the NSWS
system. This will ensure that the NSWS
headers maintain their integrity to ensure its
ability to comply with design basis
requirements and increase the overall
reliability for many years.
The increased NSWS train unavailability
as a result of the implementation of this
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amendment does involve a one time increase
in the probability or consequences of an
accident previously evaluated during the
time frame the NSWS headers are out of
service for pipe repair. Considering this small
time frame for the NSWS train outages with
the increased reliability and the decrease in
unavailability of the NSWS system in the
future because of this project, the overall
probability or consequences of an accident
previously evaluated will decrease.
Therefore, because this is a temporary and
not a permanent change, the time averaged
risk increase is acceptable. The increase in
the overall reliability of the NSWS along with
the decreased unavailability in the future
because of the pipe repair project will result
in an overall increase in the safety of both
Catawba units. Therefore, the consequences
of an accident previously evaluated remains
unaffected and there will be minimal impact
on any accident consequences.
2. Does operation of the facility in
accordance with the proposed amendment
create the possibility of a new or different
kind of accident from any accident
previously evaluated?
Response: No.
Implementation of this amendment would
not create the possibility of a new or different
kind of accident from any accident
previously evaluated. The proposed
temporary TS changes do not affect the basic
operation of the [emergency core cooling
system] ECCS, [containment spray system]
CSS, [containment valve injection water
system] CVIWS, NSWS, [auxiliary feedwater]
AFW, [component cooling water] CCW,
[control room area ventilation system] [sic]
CRAVS, [auxiliary building filtered
ventilation exhaust system] ABFVES, or
[emergency diesel generator] EDG systems.
The only change is increasing the required
action time frame from 72 hours (ECCS, CSS,
NSWS, AFW, CCW, and EDG) or 168 hours
(CVIWS, CRAVS and ABFVES) to 336 hours.
The train not undergoing maintenance will
be operable and capable of meeting its design
requirements. Therefore, only the
redundancy of the above systems is affected
by the extension of the required action to 336
hours. During the project, contingency
measures will be in place to provide
additional assurance that the affected
systems will be able to complete their design
functions.
No new accident causal mechanisms are
created as a result of NRC approval of this
amendment request. No changes are being
made to the plant, which will introduce any
new accident causal mechanisms.
3. Does operation of the facility in
accordance with the proposed amendment
involve a significant reduction in the margin
of safety?
Response: No.
Implementation of this amendment would
not involve a significant reduction in a
margin of safety. Margin of safety is related
to the confidence in the ability of the fission
product barriers to perform their design
functions during and following an accident
situation. These barriers include the fuel
cladding, the reactor coolant system, and the
containment system. The performance of
these fission product barriers will not be
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impacted by implementation of this proposed
temporary TS amendment. During the NSWS
train outages, the affected systems will still
be capable of performing their required
functions and contingency measures will be
in place to provide additional assurance that
the affected systems will be maintained in a
condition to be able to complete their design
functions. No safety margins will be
impacted.
The probabilistic risk analysis conducted
for this proposed amendment demonstrated
that the [core damage probability] CDP
associated with the outage extension is
judged to be acceptable for a one-time or rare
evolution. Therefore, there is not a significant
reduction in the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Ms. Lisa F.
Vaughn, Legal Department (PB05E),
Duke Energy Corporation, 422 South
Church Street, Charlotte, North Carolina
28201–1006.
NRC Section Chief: John A. Nakoski.
Entergy Gulf States, Inc., and Entergy
Operations, Inc., Docket No. 50–458,
River Bend Station, Unit 1, West
Feliciana Parish, Louisiana
Date of amendment request: March 8,
2005.
Description of amendment request:
The proposed amendment would enable
the licensee to make changes to the
Updated Safety Analysis Report (USAR)
to reflect the use of the non-singlefailure-proof Fuel Building Cask
Handling Crane (FBCHC) for dry spent
fuel cask component lifting and
handling operations.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Will operation of the facility in
accordance with this proposed amendment
involve a significant increase in the
probability or consequences of an accident
previously evaluated?
Response: No.
The proposed amendment introduces no
new mode of plant operations and does not
affect Structures, Systems, and Components
(SSCs) associated with power production,
accident mitigation, or safe plant shutdown.
The SSCs affected by this proposed
amendment are the Fuel Building Cask
Handling Crane (FBCHC), the spent fuel
storage canister, the spent fuel transfer cask,
and the spent fuel inside the storage canister.
A hypothetical 30 ft. drop of a loaded spent
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fuel shipping cask from the FBCHC is part of
the River Bend Station (RBS) current
licensing basis. With the proposed spent fuel
transfer cask design and procedural changes
implemented, the FCHC will be used to lift
and handle a fuel-loaded spent fuel transfer
cask of the same maximum weight and
approximately the same dimensions as
previously evaluated in the RBS USAR. The
proposed amendment involves the use of
redundant crane rigging during most lateral
moves with a loaded spent fuel transfer cask,
which provides temporary single-failure
proof design features to provide protection
against an uncontrolled lowering of the load
or load drop. In those cases where the spent
fuel transfer cask is not supported with
redundant rigging, certain hypothetical, nonmechanistic load drops have been postulated
and evaluated, with due consideration of the
use of impact limiters in some locations.
With this amendment, the probability of a
loaded spent fuel transfer cask drop is
actually less likely than previously evaluated
because the capacity of the spent fuel multipurpose canister [MPC] (68 fuel assemblies)
is larger than the capacity of the shipping
cask described in the current licensing basis
(18 fuel assemblies), which means that fewer
casks will be required to be loaded, lifted,
and handled for a given population of spent
fuel assemblies. The consequences of the
hypothetical spent fuel transfer cask load
drops on plant SSCs are bounded by those
previously evaluated for a shipping cask.
That is, there is no significant damage to the
Fuel Building structure or any SSCs used for
safe plant shutdown. New analyses of
hypothetical drops of a loaded transfer cask
or canister confirm that there is no release of
radioactive material from the storage canister
and no unacceptable damage to the fuel,
MPC, or transfer cask.
The hypothetical drop of a spent fuel
canister lid into an open, fuel-filled canister
in the spent fuel pool during fuel loading has
also been evaluated. Again, this hypothetical
accident is no more likely to occur than
previously considered due to the higher
capacity of the spent fuel transfer cask over
the spent fuel shipping cask (i.e., fewer casks
will need to be loaded for a given number of
fuel assemblies). The radiological
consequences of this event due to the
potential damage of spent fuel assemblies in
the canister onto which the lid could be
dropped have been evaluated. While more
total fuel assemblies could potentially be
damaged from a spent fuel canister lid drop
compared to that assumed for the fuel
handling accident described in the RBS
current licensing basis, the significantly
longer decay time of the spent fuel
assemblies in the canister results in a much
smaller source term, such that the existing
fuel handling accident described in USAR
Section 15.7.4 provides a bounding
evaluation for the radiological consequences
MPC lid drop. There is no rearrangement of
the fuel or deformation of the fuel basket in
the canister such that a critical geometry is
created as a result of an MPC lid drop.
The likelihood of a spent fuel canister lid
drop due to the failure of a crane component
due to overload is very unlikely because the
rated load of the crane (250,000 lbs) is
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approximately 16 times the weight of
components lifted to install the canister lid.
2. Will operation of the facility in
accordance with this proposed amendment
create the possibility of a new or different
kind of accident from any accident
previously evaluated?
Response: No.
The proposed amendment introduces no
new mode of plant operations and does not
affect SSCs associated with power
production, accident mitigation, or safe plant
shutdown. The SSCs affected by this
proposed amendment are the non-singlefailure-proof FBCHC, the spent fuel canister,
the spent fuel transfer cask, and the spent
fuel inside the canister. The design function
of the FBCHC is not changed. The proposed
amendment does not create the possibility of
a new or different kind of accident due to
credible new failure mechanisms,
malfunctions, or accident initiators. The
proposed amendment creates a new initiator
of two accidents previously evaluated and
caused by the non-mechanistic single failure
of a component in the FBCHC load path.
The current licensing basis accidents for
which new initiators are created by this
amendment are the spent fuel shipping cask
drop and the fuel handling accident. The
RBS current licensing basis includes
evaluations of the consequences of a spent
fuel shipping cask drop and the
consequences of the drop of a spent fuel
assembly into the reactor core shortly after
shutdown and reactor head removal. The
new initiators include the drop of a spent
fuel transfer cask of the same maximum
weight and approximately the same
dimensions as the shipping cask, and the
drop of a spent fuel canister lid into an open,
fuel filled canister in the spent fuel pool.
Both of these new initiators create
hypothetical accidents that are comparable in
consequences to those previously evaluated.
For the drop of a spent fuel transfer cask, the
consequences are bounded by the current
licensing basis analysis of the spent fuel
shipping cask drop. That is, there is no
significant damage to the Fuel Building
structure or any SSCs used for safe plant
shutdown, and there is no release of
radioactive material. New analyses of the
drop of a loaded transfer cask confirm that
there is no release of radioactive material
from the storage canister and no
unacceptable damage to the fuel, MPC, or
transfer cask.
For the drop of the spent fuel canister lid,
the significantly longer decay time of the
spent fuel assemblies in the canister
compared to a spent fuel assembly in a
recently shutdown reactor results in doses to
the public that are less than the previously
analyzed fuel handling accident. There is no
rearrangement of the fuel in the canister such
that a critical geometry is created as a result
of an MPC lid drop.
3. Will operation of the facility in
accordance with this proposed amendment
involve a significant reduction in a margin of
safety?
Response: No.
The proposed amendment introduces no
new mode of plant operations and does not
affect SSCs associated with power
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production, accident mitigation, or safe plant
shutdown. The SSCs affected by this
proposed amendment are the non-singlefailure-proof FBCHC, the spent fuel storage
canister, the spent fuel transfer cask, and the
spent fuel inside the canister. Therefore, this
amendment does not affect the reactor or fuel
during power operations, the reactor coolant
pressure boundary, or primary or secondary
containment. All activities associated with
this amendment occur in the Fuel Building
or in the adjacent outdoor truck bay area. The
design function of the FBCHC is not changed.
The proposed changes to plant operating
procedures needed to implement dry spent
fuel storage at RBS do not exceed or alter a
design basis or safety limit associated with
plant operation, accident mitigation, or safe
shutdown. The FBCHC is used to lift and
handle the spent fuel canister lid over spent
fuel in the canister while in the spent fuel
pool, and to lift and handle the spent fuel
transfer cask, both when it is empty and after
it is loaded with spent fuel in the spent fuel
pool.
This proposed amendment results in a net
safety benefit because a larger capacity cask
is being used to move spent fuel out of the
spent fuel pool that was previously evaluated
(68 fuel assemblies versus 18 fuel
assemblies), while maintaining the same
maximum analyzed cask weight described in
the USAR. This yields fewer casks to be
loaded, fewer heavy load lifts, and, as a
result, fewer opportunities for events such as
load drops. Because the maximum weight of
the loaded spent fuel transfer cask is the
same as that assumed for the shipping cask
and for which the FBCHC was designed, all
design safety margins for use of the FBCHC
remain unchanged. The rated capacity of the
FBCHC is approximately 16 times that of
components lifted to place the spent fuel
canister lid, yielding significant safety
margins for that particular lift.
Based on the above review, it is concluded
that: (1) the proposed amendment does not
constitute a significant hazards consideration
as defined by 10 CFR 50.92; and (2) there is
reasonable assurance that the health and
safety of the public will not be endangered
by the proposed amendment; and (3) this
action will not result in a condition which
significantly alters the impact of the station
on the environment as described in the NRC
Final Environmental Impact Statement.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mark
Wetterhahn, Esq., Winston & Strawn,
1400 L Street, NW., Washington, DC
20005.
NRC Section Chief: Allen G. Howe.
PO 00000
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Exelon Generation Company, LLC,
Docket Nos. STN 50–456 and STN 50–
457, Braidwood Station, Unit Nos. 1 and
2, Will County, Illinois
Docket Nos. STN 50–454 and STN 50–
455, Byron Station, Unit Nos. 1 and 2,
Ogle County, Illinois
Docket No. 50–237, Dresden Nuclear
Power Station, Unit 2, Grundy County,
Illinois
Docket Nos. 50–373 and 50–374,
LaSalle County Station, Units 1 and 2,
LaSalle County, Illinois
Date of amendment request: February
25, 2005.
Description of amendment request:
The proposed change would delete the
applicable sections of the Facility
Operating Licenses (FOLs); NPF–72,
NPF–77, NPF–37, NPF–66, DPR–19,
NPF–11, and NPF–18, respectively;
which require Exelon Generation
Company, LLC, to report violations of
the requirements contained in Section
2.C of the Braidwood Station, Units 1
and 2, and Byron Station, Units 1 and
2 FOLs; Section 2.C of the Dresden
Nuclear Power Station, Unit 2, renewed
FOL; and Sections 2.C and 2.E of the
LaSalle County Station, Units 1 and 2,
FOLs. The proposed change will reduce
unnecessary regulatory burden and will
allow Exelon to take full advantage of
the revisions to Title 10, Code of Federal
Regulations (10 CFR), Section 50.72,
‘‘Immediate notification requirements
for operating nuclear power reactors,’’
and 10 CFR 50.73, ‘‘Licensee event
report system.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change involves an
administrative change only. The proposed
change does not involve the modification of
any plant equipment or affect plant
operation. The proposed change will have no
impact on any safety related structures,
systems or components. The reporting
requirement section of the FOL is not
required because the requirements are either
adequately addressed by 10 CFR 50.72 and
10 CFR 50.73, or other regulatory
requirements, or are not required based on
the nature of the Condition.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
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accident from any accident previously
evaluated?
Response: No.
The proposed change has no impact on the
design, function or operation of any plant
structure, system or component. The
proposed change is administrative in nature
and does not affect plant equipment or
accident analyses. The reporting requirement
section of the FOL is not required because
the requirements are either adequately
addressed by 10 CFR 50.72 and 10 CFR
50.73, or other regulatory requirements, or
are not required based on the nature of the
Condition.
Therefore, the proposed change will not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change is administrative in
nature, does not negate any existing
requirement, and does not adversely affect
existing plant safety margins or the reliability
of the equipment assumed to operate in the
safety analysis. As such, there is no change
being made to safety analysis assumptions,
safety limits or safety system settings that
would adversely affect plant safety as a result
of the proposed change. Margins of safety are
unaffected by deletion of the reporting
requirement that is adequately addressed
elsewhere.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendments involve no
significant hazards consideration.
Attorney for licensee: Mr. Thomas S.
O’Neill, Associate General Counsel,
Exelon Generation Company, LLC, 4300
Winfield Road, Warrenville, IL 60555.
NRC Section Chief: Gene Y. Suh.
Exelon Generation Company, LLC,
Docket Nos. 50–352 and 50–353,
Limerick Generating Station, Unit Nos.
1 and 2, Montgomery County,
Pennsylvania
Date of amendment request: February
25, 2005.
Description of amendment request:
The proposed change would delete the
applicable sections of the Limerick
Generating Station, Units 1 and 2,
Facility Operating Licenses (FOLs),
NPF–39 and NPF–85, which require
Exelon Generation Company, LLC,
(Exelon), to report violations of the
requirements contained in Section 2.C
of these licenses. The proposed change
will reduce unnecessary regulatory
burden and will allow AmerGen to take
full advantage of the revisions to Title
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11:52 Apr 25, 2005
Jkt 205001
10, Code of Federal Regulations (10
CFR), Section 50.72, ‘‘Immediate
notification requirements for operating
nuclear power reactors,’’ and 10 CFR
50.73, ‘‘Licensee event report system.’’
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed change involves an
administrative change only. The proposed
change does not involve the modification of
any plant equipment or affect plant
operation. The proposed change will have no
impact on any safety related structures,
systems or components. The reporting
requirement section of the FOL is not
required because the requirements are either
adequately addressed by 10 CFR 50.72 and
10 CFR 50.73, or other regulatory
requirements, or are not required based on
the nature of the Condition.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed change has no impact on the
design, function or operation of any plant
structure, system or component. The
proposed change is administrative in nature
and does not affect plant equipment or
accident analyses. The reporting requirement
section of the FOL is not required because
the requirements are either adequately
addressed by 10 CFR 50.72 and 10 CFR
50.73, or other regulatory requirements, or
are not required based on the nature of the
Condition.
Therefore, the proposed change will not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed change is administrative in
nature, does not negate any existing
requirement, and does not adversely affect
existing plant safety margins or the reliability
of the equipment assumed to operate in the
safety analysis. As such, there is no change
being made to safety analysis assumptions,
safety limits or safety system settings that
would adversely affect plant safety as a result
of the proposed change. Margins of safety are
unaffected by deletion of the reporting
requirement that is adequately addressed
elsewhere.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
PO 00000
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21457
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
requested amendment involves no
significant hazards consideration.
Attorney for licensee: Mr. Thomas S.
O’Neill, Associate General Counsel,
Exelon Generation Company, LLC, 4300
Winfield Road, Warrenville, IL 60555.
NRC Section Chief: Darrell J. Roberts.
FirstEnergy Nuclear Operating
Company, et al., Docket Nos. 50–334
and 50–412, Beaver Valley Power
Station, Unit Nos. 1 and 2 (BVPS–1 and
2), Beaver County, Pennsylvania
Date of amendment request: February
11, 2005.
Description of amendment request:
The proposed changes would modify
the BVPS–1 and 2 Technical
Specifications (TSs) to implement the
relaxed axial offset control (RAOC) and
FQ surveillance methodologies. These
methodologies are used to reduce
operator action required to maintain
conformance with power distribution
control TSs, and increase the ability to
return to power after a plant trip while
still maintaining margin to safety limits
under all operating conditions.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No. The proposed changes will
not involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The proposed changes do not initiate an
accident. Evaluations and analyses of
accidents, which are potentially affected by
the parameters and assumptions, associated
with the RAOC and FQ(Z) methodologies
have shown that all design standards and
applicable safety criteria will continue to be
met. The consideration of these changes does
not result in a situation where the design,
material, or construction standards that were
applicable prior to the change are altered.
Therefore, the proposed changes will not
result in any additional challenges to plant
equipment that could increase the probability
of any previously evaluated accident.
The proposed changes associated with the
RAOC and FQ(Z) methodologies do not affect
plant systems such that their function in the
control of radiological consequences is
adversely affected. The actual plant
configuration, performance of systems, or
initiating event mechanisms are not being
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changed as a result of the proposed changes.
The design standards and applicable safety
criteria limits will continue to be met,
therefore, fission barrier integrity is not
challenged. The proposed changes associated
with the RAOC and FQ(Z) methodologies
have been shown not to adversely affect the
plant response to postulated accident
scenarios. The proposed changes will
therefore not affect the mitigation of the
radiological consequences of any accident
described in the Updated Final Safety
Analysis Report (UFSAR).
Therefore the proposed changes do not
involve a significant increase in the
probability or consequences of any accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No. The proposed changes will
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
No new accident scenarios, failure
mechanisms, or limiting single failures are
introduced as a result of the proposed
change. The proposed changes do not
challenge the performance or integrity of any
safety-related system. The possibility for a
new or different type of accident from any
accident previously evaluated is not created
since the proposed change does not result in
a change to the design basis of any plant
structure, system or component. Evaluation
of the effects of the proposed changes has
shown that all design standards and
applicable safety criteria continue to be met.
Equipment important to safety will
continue to operate as designed and
component integrity will not be challenged.
The proposed changes do not result in any
event previously deemed incredible being
made credible. The proposed changes will
not result in conditions that are more adverse
and will not result in any increase in the
challenges to safety systems.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
analyzed.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No. The proposed changes will
not involve a significant reduction in a
margin of safety. The proposed changes will
assure continued compliance within the
acceptance limits previously reviewed and
approved by the NRC for RAOC and FQ(Z)
methodologies. All of the appropriate
acceptance criteria for the various analyses
and evaluations will continue to be met.
The impact associated with the
implementation of RAOC on peak cladding
temperature (PCT) has been evaluated for the
planned extended power uprate. This
evaluation has determined that
implementation of RAOC at the extended
power uprate power level will not result in
a significant reduction in a margin of safety
for either unit.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
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Jkt 205001
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mary O’Reilly,
FirstEnergy Nuclear Operating
Company, FirstEnergy Corporation, 76
South Main Street, Akron, OH 44308.
NRC Section Chief: Richard J. Laufer.
FirstEnergy Nuclear Operating
Company, et al., Docket Nos. 50–334
and 50–412, Beaver Valley Power
Station, Unit Nos. 1 and 2 (BVPS–1 and
2), Beaver County, Pennsylvania
Date of amendment request: February
17, 2005.
Description of amendment request:
The proposed amendments would
revise Technical Specification (TS)
3.7.7.1, ‘‘Control Room Emergency
Habitability Systems’’ (BVPS–1), and TS
3.7.7, ‘‘Control Room Emergency Air
Cleanup and Pressurization System’’
(BVPS–2), by dividing each
specification into two specifications,
addressing control room emergency
ventilation and control room air cooling
functions separately. Other minor
changes are proposed to improve
consistency with the Standard TSs and
consistency between BVPS–1 and 2.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
No.
The proposed changes do not adversely
affect accident initiators or precursors or alter
the design assumptions, conditions or
configuration of the facility. The proposed
changes do not alter or prevent the ability of
structures, systems, or components to
perform their intended function to mitigate
the consequences of an initiating event
within the assumed acceptance limits. The
proposed change revises the TSs for the
control room ventilation systems which are
mitigating systems designed to minimize
inleakage, to filter the control room
atmosphere and to provide heat removal for
the control room envelope. These functions
maintain the control room temperature
within design limits and protect the control
room personnel following accidents
previously analyzed. The proposed changes
do not alter or reduce the capability of the
affected systems to maintain the control room
temperature and protect the control room
personnel consistent with the assumptions of
PO 00000
Frm 00070
Fmt 4703
Sfmt 4703
the applicable safety analyses. Therefore, the
probability of any accident previously
evaluated is not significantly increased. The
proposed change continues to assure [that]
adequate system and component testing is
performed to verify the operability of the
control room habitability systems to ensure
mitigation features are capable of performing
the assumed functions. Therefore, the
consequences of any accident previously
evaluated are not significantly increased.
Therefore, it is concluded that the
proposed change does not involve a
significant increase in the probability or
consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
No.
The proposed changes will not adversely
impact the accident analysis. The changes
will not alter the requirements of the control
room ventilation systems or their functions
during accident conditions. No new or
different accidents result from the
application of the revised TS requirements.
The changes do not involve a physical
alteration of the plant (i.e., no new or
different type of equipment will be installed)
or a significant change in the methods
governing normal plant operation. The
changes do not alter assumptions made in the
safety analyses. The proposed changes are
consistent with the safety analyses
assumptions and current plant operating
practices.
Therefore, the proposed change does not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
No.
The proposed changes do not alter the
manner in which safety limits, limiting safety
system settings or limiting conditions for
operation are determined. The safety analysis
acceptance criteria are not affected by these
changes. The proposed changes will not
result in plant operation in a configuration
outside the design basis for an unacceptable
period of time without compensatory
measures. The proposed changes do not
adversely affect systems that respond to
safely shut down the plant and to maintain
the plant in a safe shutdown condition.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Mary O’Reilly,
FirstEnergy Nuclear Operating
Company, FirstEnergy Corporation, 76
South Main Street, Akron, OH 44308.
NRC Section Chief: Richard J. Laufer.
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Nuclear Management Company, LLC,
Docket Nos. 50–282 and 50–306, Prairie
Island Nuclear Generating Plant, Units
1 and 2, Goodhue County, Minnesota
Date of amendment request: February
28, 2005.
Description of amendment request:
The proposed amendments would allow
the use of the Small Break Loss of
Coolant Accident (SBLOCA)
methodology described in Westinghouse
WCAP 10054–P–A Addendum 2
Revision 1, ‘‘Addendum to the
Westinghouse Small Break emergency
core cooling system (ECCS) Evaluation
Model Using the NOTRUMP Code:
Safety Injection into the Broken Loop
and COSI Condensation Model’’ dated
July 1997. This revised methodology
determines the core response following
a SBLOCA event and will be used to
assure compliance with the post Loss of
Coolant Accident (LOCA) acceptance
criteria specified in 10 CFR 50.46.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
The proposed amendment will change the
Prairie Island Nuclear Generating Plant
licensing basis by allowing the use of the
approved NOTRUMP SBLOCA Evaluation
Model described in Westinghouse WCAP
10054–P–A Addendum 2 Revision 1,
‘‘Addendum to the Westinghouse Small
Break ECCS Evaluation Model Using the
NOTRUMP Code: Safety Injection into the
Broken Loop and COSI Condensation
Model’’.
The methodology used to perform small
break loss of coolant accident (SBLOCA)
analyses is not an accident initiator, thus
changing the methodology does not increase
the probability of an accident.
The fuel heat-up results generated by the
proposed methodology will be utilized to
demonstrate that the loss of coolant accident
(LOCA) criteria for design basis for fission
product barriers as described in 10 CFR Part
50.46 are not exceeded. The proposed
methodology does not alter the nuclear
reactor core, reactor coolant system, or
equipment used directly in mitigation of a
Small Break LOCA, thus radioactive releases
due to a SBLOCA accident are not affected
by the proposed change in analysis
methodology. Therefore, this change does not
increase the consequences of an accident
previously evaluated.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
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11:52 Apr 25, 2005
Jkt 205001
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
The proposed amendment will change the
Prairie Island Nuclear Generating Plant
licensing basis by allowing the use of the
approved NOTRUMP SBLOCA Evaluation
Model described in Westinghouse WCAP
10054–P–A Addendum 2 Revision 1,
‘‘Addendum to the Westinghouse Small
Break ECCS Evaluation Model Using the
NOTRUMP Code: Safety Injection into the
Broken Loop and COSI Condensation
Model’’.
The analysis of a SBLOCA accident using
the proposed methodology does not alter the
nuclear reactor core, reactor coolant system,
or equipment used directly in mitigation of
a Small Break LOCA.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The proposed amendment will change the
Prairie Island Nuclear Generating Plant
licensing basis by allowing the use of the
approved NOTRUMP SBLOCA Evaluation
Model described in Westinghouse WCAP
10054–P–A Addendum 2 Revision 1,
‘‘Addendum to the Westinghouse Small
Break ECCS Evaluation Model Using the
NOTRUMP Code: Safety Injection into the
Broken Loop and COSI Condensation
Model’’.
The methodology in the proposed licensing
basis change has previously been reviewed
and approved by the Nuclear Regulatory
Commission as a conservative methodology.
The Prairie Island configuration is
representative of the modeling used in the
methodology. Therefore, the proposed
licensing basis change will result in a
conservative calculation of fuel conditions
following a SBLOCA event. This will ensure
that there is no reduction in the margin of
safety for Prairie Island SBLOCA analyses
that utilize this methodology.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Jonathan Rogoff,
Esquire, Vice President, Counsel &
Secretary, Nuclear Management
Company, LLC, 700 First Street,
Hudson, WI 54016.
NRC Section Chief: L. Raghavan.
PO 00000
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21459
Omaha Public Power District, Docket
No. 50–285, Fort Calhoun Station, Unit
No. 1, Washington County, Nebraska
Date of amendment request: March
31, 2005.
Description of amendment request:
The proposed amendment will increase
the licensed power level to 1522
megawatts thermal (MWt) or 1.50
percent greater than the current power
level of 1500 MWt. The requested
increase in licensed rated power is the
result of a measurement uncertainty
recapture (MUR) power uprate. The
information provided in support of this
request is based on the NRC’s
Regulatory Issue Summary 2002–03,
‘‘Guidance on the Content of
Measurement Uncertainty Recapture
Power Uprate Applications,’’ dated
January 31, 2002.
On July 18, 2003, the licensee
submitted, and the NRC subsequently
approved, an MUR power uprate
amendment to increase the licensed
power level to 1524 MWt or 1.6 percent
greater than the current level of 1500
MWt. Problems during implementation
resulted in the submission of an exigent
license amendment request (LAR),
which returned the licensed power to its
original level (1500 MWt). The current
LAR references the analysis from the
July 18, 2003 submittal.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed change does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated.
Response: No.
There are no changes as a result of the
MUR power uprate to the design or operation
of the plant that could affect system,
component, or accident functions. All
systems and components function as
designed and the performance requirements
have been evaluated and found to be
acceptable.
The reduction in power measurement
uncertainty allows for safety analyses to
continue to be used without modification.
This is because those safety analyses were
performed or evaluated at 102% of 1500 MWt
(1530 MWt) or higher. Analyses at these
power levels support a core power level of
1522 MWt with a measurement uncertainty
of 0.5%. Radiological consequences of USAR
[Updated Safety Analysis Report] Chapter 14
accidents were assessed previously using the
alternate source term methodology
(Reference 10.2 [Agencywide Documents
Access Management System accession
number ML013410095]). These analyses were
performed at 102% of 1500 MWt (1530 MWt)
and continue to be bounding. Updated Safety
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Analysis Report (USAR) Chapter 14 analyses
and accident analyses continue to
demonstrate compliance with the relevant
accident analyses’ acceptance criteria.
Therefore, there is no significant increase in
the consequences of any accident previously
evaluated.
The primary loop components (reactor
vessel, reactor internals, control element
drive mechanisms, loop piping and supports,
reactor coolant pumps, steam generators, and
pressurizer) were evaluated at an uprated
core power level of 1524 MWt and continue
to comply with their applicable structural
limits. These analyses also demonstrate the
components will continue to perform their
intended design functions. Changing the
heatup and cooldown curves is based on
uprated fluence values. This does not have a
significant effect on the reactor vessel
integrity. Thus, there is no significant
increase in the probability of a structural
failure of the primary loop components. The
LBB [leak before break] analysis conclusions
remain valid and the breaks previously
exempted from structural consideration
remain unchanged.
All of the NSSS [nuclear steam system
supplier] systems will continue to perform
their intended design functions during
normal and accident conditions. The
auxiliary systems and components continue
to comply with the applicable structural
limits and will continue to perform their
intended functions. The NSSS/BOP [nuclear
steam system supplier/balance of plant]
interface systems were evaluated at 1522
MWt and will continue to perform their
intended design functions. Plant electrical
equipment was also evaluated and will
continue to perform their intended functions.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. The proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
Response: No.
No new accident scenarios, failure
mechanisms, or single failures are introduced
as a result of the proposed change. All
systems, structures, and components
previously required for the mitigation of an
event remain capable of fulfilling their
intended design function at the uprated
power level. The proposed change has no
adverse effects on any safety related systems
or component and does not challenge the
performance or integrity of any safety related
system. Therefore, the proposed change does
not create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. The proposed change does not involve
a significant reduction in a margin of safety.
Response: No.
Operation at 1522 MWt core power does
not involve a significant reduction in the
margin of safety. The current accident
analyses have been previously performed
with a 2% power measurement uncertainty
or at uprated core powers that exceed the
MUR uprated core power. System and
component analyses have been completed at
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the MUR uprated core power conditions.
Analyses of the primary fission product
barriers at uprated core powers have
concluded that all relevant design basis
criteria remain satisfied in regard to integrity
and compliance with the regulatory
acceptance criteria. As appropriate, all
evaluations have been both reviewed and
approved by the NRC, or are currently under
review (the proposed Pressure-Temperature
Limits Report). Therefore, the proposed
change does not involve a significant
reduction in margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: James R.
Curtiss, Esq., Winston & Strawn, 1400 L
Street, NW., Washington, DC 20005–
3502.
NRC Section Chief: Robert A. Gramm.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of amendment requests:
December 28, 2004.
Description of amendment requests:
The proposed amendments would
relocate reactor coolant system related
cycle-specific parameters from the
Technical Specifications to the Core
Operating Limits Report.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed change does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated.
The proposed changes are programmatic
and administrative in nature, which do not
physically alter safety related systems, nor
affect the way in which safety related
systems perform their functions. More
specific requirements regarding the safety
limits (i.e., departure from nucleate boiling
ratio limit and peak fuel centerline
temperature limit) are being imposed in
Technical Specification (TS) 2.1.1, ‘‘Reactor
Core SLs [Safety Limits],’’ which replace the
reactor core safety limits figure and are
consistent with the values stated in the Final
Safety Analysis Report Update (FSARU). The
proposed changes remove cycle-specific
parameters from TS 3.4.1 and relocate them
to the Core Operating Limits Report (COLR),
which do not change the plant design or
affect system operating parameters. In
addition, the minimum limit for reactor
coolant system (RCS) total flow rate is being
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Sfmt 4703
retained in TS 3.4.1 to assure that a lower
flow rate than reviewed by the NRC will not
be used. The proposed changes do not, by
themselves, alter any of the parameters. The
removal of the cycle-specific parameters from
the TS does not eliminate existing
requirements to comply with the parameters.
The proposed changes to TS 5.6.5b to
reference only the topical report number and
title for three of the topical reports do not
alter the use of the analytical methods used
to determine core operating limits that have
been reviewed and approved by the NRC.
This method of referencing topical reports
would allow the use of current topical
reports to support limits in the COLR without
having to submit a request for an amendment
to the operating license. Implementation of
revisions to these topical reports would still
be reviewed in accordance with 10 CFR 50.59
and, where required, receive NRC review and
approval.
Although the relocation of the cyclespecific parameters to the COLR would allow
revision of the affected parameters without
prior NRC approval, there is no significant
effect on the probability or consequences of
an accident previously evaluated. Future
changes to the COLR parameters could result
in event consequences which are either
slightly less or slightly more severe than the
consequences for the same event using the
present parameters. The differences would
not be significant and would be bounded by
the existing requirement of TS 5.6.5c to meet
the applicable limits of the safety analyses.
The cycle-specific parameters being
transferred from the TS to the COLR will
continue to be controlled under existing
programs and procedures. The FSARU
accident analyses will continue to be
examined with respect to changes in the
cycle-dependent parameters obtained using
NRC reviewed and approved reload design
methodologies, ensuring that the transient
evaluation of new reload designs are
bounded by previously accepted analyses.
This examination will continue to be
performed pursuant to 10 CFR 50.59
requirements, ensuring that future reload
designs will not involve a significant increase
in the probability or consequences of an
accident previously evaluated. Additionally,
the proposed changes do not allow for an
increase in plant power levels, do not
increase the production, nor alter the flow
path or method of disposal of radioactive
waste or byproducts. Therefore, the proposed
changes do not change the type or increase
the amount of any effluents released offsite.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. The proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
The proposed changes that retain the
minimum limit for RCS total flow rate in the
TS, and that relocate certain cycle-specific
parameters from the TS to the COLR, thus
removing the requirement for prior NRC
approval of revisions to those parameters, do
not involve a physical change to the plant.
No new equipment is being introduced, and
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installed equipment is not being operated in
a new or different manner. There are no
changes being made to the parameters within
which the plant is operated, other than their
relocation to the COLR. There are no set
points affected by the proposed changes at
which protective or mitigative actions are
initiated. The proposed changes will not alter
the manner in which equipment operation is
initiated, nor will the function demands on
credited equipment be changed. No alteration
in the procedures which ensure the plant
remains within analyzed limits is being
proposed, and no change is being made to the
procedures relied upon to respond to an offnormal event. As such, no new failure modes
are being introduced.
The proposed changes to reference only the
topical report number and title do not alter
the use of the analytical methods used to
determine core operating limits that have
been reviewed and approved by the NRC.
This method of referencing topical reports
would allow the use of current topical
reports to support limits in the COLR without
having to submit a request for an amendment
to the operating license. Implementation of
revisions to topical reports would still be
reviewed in accordance with 10 CFR 50.59
and, where required, receive NRC review and
approval.
Relocation of cycle-specific parameters has
no influence or impact on, nor does it
contribute in any way to the possibility of a
new or different kind of accident. The
relocated cycle-specific parameters will
continue to be calculated using the NRC
reviewed and approved methodology. The
proposed changes do not alter assumptions
made in the safety analysis, and operation
within the core operating limits will
continue.
Therefore, the proposed changes do not
create a new or different kind of accident
from any accident previously evaluated.
3. The proposed change does not involve
a significant reduction in a margin of safety.
The margin of safety is established through
equipment design, operating parameters, and
the set points at which automatic actions are
initiated. The proposed changes do not
physically alter safety-related systems, nor do
they affect the way in which safety-related
systems perform their functions. The set
points at which protective actions are
initiated are not altered by the proposed
changes. Therefore, sufficient equipment
remains available to actuate upon demand for
the purpose of mitigating an analyzed event.
As the proposed changes to relocate cyclespecific parameters to the COLR will not
affect plant design or system operating
parameters, there is no detrimental impact on
any equipment design parameter, and the
plant will continue to operate within
prescribed limits.
The development of cycle-specific
parameters for future reload designs will
continue to conform to NRC reviewed and
approved methodologies, and will be
performed pursuant to 10 CFR 50.59 to
assure that the plant operates within cyclespecific parameters.
The proposed changes to reference only the
topical report number and title do not alter
the use of the analytical methods used to
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determine core operating limits that have
been reviewed and approved by the NRC.
This method of referencing topical reports
would allow the use of current NRCapproved topical reports to support limits in
the COLR without having to submit a request
for an amendment to the operating license.
Implementation of revisions to topical
reports would still be reviewed in accordance
with 10 CFR 50.59 and, where required,
receive NRC review and approval.
Therefore, the proposed changes do not
involve a significant reduction in the margin
of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Richard F.
Locke, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Section Chief: Robert A. Gramm.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of amendment requests:
December 31, 2004.
Description of amendment requests:
The proposed amendments would
revise Technical Specification 3.4.10,
‘‘Pressurizer Safety Valves’’ to add a
separate Action and associated
Completion Times for one or more
inoperable pressurizer safety valves for
the condition where the valves are
inoperable solely due to loop seal
temperatures being outside of design
limits.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The proposed change does not involve
a significant increase in the probability or
consequences of an accident previously
evaluated.
This proposed change revises Technical
Specification (TS) 3.4.10, ‘‘Pressurizer Safety
Valves,’’ to add a separate Action and
associated Completion Times (CTs) for one or
more inoperable pressurizer safety valves
(PSV) for the condition where the valves are
inoperable solely due to loop seal
temperatures being outside of design limits.
Currently, when a PSV is in such a condition,
it is conservatively declared inoperable and
TS 3.4.10 Condition A is entered which has
a CT of 15 minutes. A CT of 15 minutes
normally provides insufficient time for
restoring a PSV loop seal temperature to
within limits. The new Action will provide
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21461
CTs of 12 hours for exceeding the high
temperature limit and 24 hours (MODES 1
and 2) or 72 hours (MODES 3 and 4) for
exceeding the low temperature limit. In
addition, two new PSV loop seal temperature
surveillance requirements are proposed to
assist in assuring PSV operability.
Loop seals are provided in the PSV inlet
piping to maintain PSV body temperature
within vendor recommended limits. This
prevents PSV seat leakage that can result
from spring relaxation with increased
temperature. However, the water in the loop
seals must be maintained at or above a
minimum temperature to allow it to flash to
steam when a PSV lifts. Because of the low
density and low mass flow rate, PSV steam
relief imposes minimal loading on the
discharge piping ensuring acceptable pipe
stresses. However, if cooler water is
maintained in the loop seals, it may not flash
completely, and a water and steam mixture
could be discharged when a PSV lifts.
Because of the higher density and higher
mass flow rate, PSV relief of water and steam
could impose increased loading and could
result in unacceptably high pipe stresses on
the discharge piping which could render the
PSVs inoperable and/or damage the
discharge piping.
The concern with the PSV opening during
liquid relief conditions or with the loop seal
temperature outside design limits, is the
ability to ensure the valve reseats properly
and no leakage occurs after the valve closes.
However, even under liquid relief conditions,
PSVs are still capable of providing their
required relief capacity.
Failure of the PSV to reseat following
discharge would result in an unisolable
reactor coolant system leak. The
consequences of such a leak are bounded by
existing Final Safety Analysis Report Update
(FSARU) accident analyses. Probabilistic risk
assessment methods and a deterministic
analysis have been utilized to determine
there is no significant increase in core
damage frequency or large early release
frequency.
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. The proposed change does not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
Failure of one or more PSVs to reseat
following discharge would result in an
unisolable reactor coolant system leak. The
consequences of such a leak are bounded by
existing FSARU accident analyses and no
new failure modes are introduced.
Therefore, the proposed change does not
create the possibility of a new or different
accident from any accident previously
evaluated.
3. The proposed change does not involve
a significant reduction in a margin of safety.
The proposed change is based upon both
a deterministic evaluation and a riskinformed assessment.
The deterministic evaluation concluded
that even with the loop seal temperature
outside of design limits, causing one or more
PSVs to be declared inoperable, the PSVs
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would still lift on demand to perform their
safety function. Failure of one or more PSVs
to reseat following discharge, resulting in an
unisolable reactor coolant system leak, is an
event bounded by existing FSARU accident
analyses.
The risk assessment performed to support
this license amendment request concluded
that the increase in plant risk is small and
consistent with the NRC’s Safety Goal Policy
Statement, ‘‘Use of Probabilistic Risk
Assessment Methods in Nuclear Activities:
Final Policy Statement,’’ Federal Register,
Volume 60, p. 42622, August 16, 1995 and
guidance contained in of Regulatory Guides
(RG) 1.174, ‘‘An Approach for Using
Probabilistic Risk Assessment in RiskInformed Decisions on Plant-Specific
Changes to the Licensing Basis,’’ dated July
1998 and RG 1.177, ‘‘An Approach for PlantSpecific, Risk-Informed Decisionmaking:
Technical Specifications,’’ dated August
1998.
Together, the deterministic evaluation and
the risk-informed assessment provide high
assurance that the PSVs will meet their
design requirements.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Richard F.
Locke, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Section Chief: Robert A. Gramm.
Pacific Gas and Electric Company,
Docket Nos. 50–275 and 50–323, Diablo
Canyon Nuclear Power Plant, Unit Nos.
1 and 2, San Luis Obispo County,
California
Date of amendment requests: March
11, 2005.
Description of amendment requests:
The proposed amendment would
modify Technical Specification (TS)
5.5.9, ‘‘Steam Generator (SG) Tube
Surveillance Program,’’ and 5.6.10,
‘‘Steam Generator (SG) Tube Inspection
Report,’’ to allow the use of the SG tube
W star (W*) alternate repair criteria
(ARC) on a permanent basis. The W*
ARC allows axial primary water stress
corrosion cracking indications in the
Westinghouse explosive tube expansion
(WEXTEX) region to remain in service if
the indication is located below the
bottom of the WEXTEX transition. In
addition, TS 5.6.10.d for NRC
notification requirements of the voltagebased ARC would be revised.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
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Jkt 205001
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability-or
consequences of an accident previously
evaluated?
Response: No.
Of the various accidents previously
evaluated, the permanent use of the steam
generator (SG) tube W star (W*) alternate
repair criteria (ARC) only affects the steam
generator tube rupture (SGTR) accident
evaluation and the postulated main steam
line break (MSLB) accident evaluation. Lossof-coolant accident (LOCA) conditions cause
a compressive axial load to act on the tube.
Therefore, since the LOCA tends to force the
tube into the tubesheet rather than pull it out,
it is not a factor in this evaluation.
For the SGTR accident, the required
structural margins of the SG tubes will be
maintained by the presence of the tubesheet.
Tube rupture is precluded for cracks in the
Westinghouse explosive tube expansion
(WEXTEX) region due to the constraint
provided by the tubesheet. Therefore,
Regulatory Guide (RG) 1.121, ‘‘Bases for
Plugging Degraded PWR Steam Generator
Tubes,’’ margins against burst are maintained
for both normal and postulated accident
conditions.
WCAP–14797–P, Revision 2, defines a
length, W*, of degradation-free expanded
tubing that provides the necessary resistance
to tube pullout due to the pressure-induced
forces (with applicable safety factors
applied). The W* length supplies the
necessary resistive force to preclude pullout
loads under both normal operating and
accident conditions. The contact pressure
results from the WEXTEX expansion process,
thermal expansion mismatch between the
tube and tubesheet and from the differential
pressure between the primary and secondary
side as offset at higher tubesheet elevations
by bow of the tubesheet. The proposed
changes do not affect other systems,
structures, components, or operational
features. Therefore, the proposed change
results in no significant increase in the
probability of the occurrence of an SGTR or
MSLB accident.
The consequences of an SGTR accident are
affected by the primary-to-secondary leakage
flow during the accident. Primary-tosecondary leakage flow through a postulated
broken tube is not affected by the proposed
changes since the tubesheet enhances the
tube integrity in the region of the WEXTEX
expansion by precluding tube deformation
beyond its initial expanded outside diameter.
The resistance to both tube rupture and
collapse is strengthened by the tubesheet in
that region. At normal operating pressures,
leakage from primary water stress corrosion
cracking in the W* length is limited by both
the tube-to-tubesheet crevice and the limited
crack opening permitted by the tubesheet
constraint. No leakage has been observed in
any in situ test of W* indications to date.
Consequently, negligible normal operating
leakage is expected from cracks within the
tubesheet region.
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MSLB leakage is limited by leakage flow
restrictions resulting from the crack and
tubesheet that provide a restricted leakage
path and also limit the degree of crack face
opening compared to free span indications.
The total leakage, that is, the combined
leakage for all such tubes, plus the combined
leakage developed by any other ARC and
non-ARC degradation, is limited to less than
the maximum allowable MSLB accident dose
analysis leak rate limit, such that offsite dose
is maintained less than the guideline value
in Title 10 to the Code of Federal Regulations
(10 CFR) Part 100 and control room dose is
maintained less than the value in General
Design Criterion (GDC) 19 of Appendix A to
10 CFR Part 50. In addition, the editorial
changes made to Technical Specifications
5.5.9 and 5.6.10 have no impact on the MSLB
leakage [and the SGTR].
Therefore, the proposed change does not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different accident
from any accident previously evaluated?
Response: No.
The proposed changes do not introduce
any changes or mechanisms that create the
possibility of a new or different kind of
accident. Tube bundle integrity is expected
to be maintained for all plant conditions
upon continued implementation of the W*
ARC.
Axial indications left in service shall have
the upper crack tip below the top of the
tubesheet (TTS) by at least the value of the
nondestructive examination (NDE)
uncertainty and crack growth allowance,
such that at the end of the subsequent
operating cycle the entire crack remains
below the tubesheet secondary face, thereby
minimizing the potential for free span
cracking and demonstrating that an
acceptable level of risk is maintained for
tubes returned to service under W* ARC.
This repair criterion is in addition to
ensuring that the upper crack tip is located
below the bottom of the WEXTEX transition
by at least the NDE measurement uncertainty.
Condition monitoring will verify that all tube
cracks returned to service under W* ARC
remain below the TTS, including an
allowance for NDE uncertainty.
These changes do not introduce any new
equipment or any change to existing
equipment. No new effects on existing
equipment are created nor are any new
malfunctions introduced.
Therefore, the proposed change does not
create the possibility of a new or different
accident from any accident previously
evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes maintain the
required structural margins of the SG tubes
for both normal and accident conditions. RG
1.121 is used as the basis in the development
of the W* ARC for determining that SG tube
integrity considerations are maintained
within acceptable limits. RG 1.121 describes
a method acceptable to the NRC staff for
meeting General Design Criteria 14, 15, 31,
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and 32 by reducing the probability and
consequences of an SGTR. RG 1.121
concludes that by determining the limiting
safe conditions of tube wall degradation
beyond which tubes with unacceptable
cracking, as established by inservice
inspection, should be removed from service
or repaired, the probability and consequences
of a SGTR are reduced. This RG uses safety
factors on loads for tube-burst that are
consistent with the requirements of Section
III of the ASME Code.
For primarily axially oriented cracking
located within the tubesheet, tubeburst is
precluded due to the presence of the
tubesheet. WCAP–14797–P, Revision 2,
defines a length, W*, of degradation free
expanded tubing that provides the necessary
resistance to tube pullout due to the pressure
induced forces (with applicable safety factors
applied). Application of the W* ARC will
preclude unacceptable primary-to-secondary
leakage during all plant conditions. The
methodology for determining MSLB leakage
due to indications within the tubesheet
region provides for large margins between
calculated and actual leakage values. In
addition, the total leakage, including leakage
due to use of other ARC, is maintained below
the maximum allowable MSLB accident dose
analysis leak rate limit, such that offsite dose
is maintained less than the guideline value
in 10 CFR Part 100 and control room dose is
maintained less than the value in GDC 19. In
addition, the editorial changes made to
Technical Specifications 5.5.9 and 5.6.10
have no impact on the determination of
MSLB leakage [and the SGTR].
Plugging of the SG tubes reduces the
reactor coolant flow margin for core cooling.
Continued implementation of W* ARC will
result in maintaining the margin of flow that
may have otherwise been reduced by tube
plugging.
Therefore, the proposed change does not
involve a significant reduction in a margin of
safety.
Based on the above evaluation, PG&E
[Pacific Gas and Electric Company]
concludes that the proposed change presents
no significant hazards consideration under
the standards set forth in 10 CFR 50.92(c),
and accordingly, a finding of ‘‘no significant
hazards consideration’’ is justified.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment requests involve no
significant hazards consideration.
Attorney for licensee: Richard F.
Locke, Esq., Pacific Gas and Electric
Company, P.O. Box 7442, San
Francisco, California 94120.
NRC Section Chief: Robert Gramm.
PPL Susquehanna, LLC, Docket Nos. 50–
387 and 50–388, Susquehanna Steam
Electric Station, Units 1 and 2 (SSES 1
and 2), Luzerne County, Pennsylvania
Date of amendment request:
November 9, 2004.
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Jkt 205001
Description of amendment request:
The proposed amendments would
change the SSES 1 and 2 Technical
Specifications (TSs) 3.8.4, ‘‘DC Sources–
Operating,’’ 3.8.5, ‘‘DC Sources–
Shutdown,’’ 3.8.6, ‘‘Battery Cell
Parameters,’’ and add a new TS Section,
5.5.13, ‘‘Battery Monitoring and
Maintenance Program.’’ These changes
are consistent with Technical
Specifications Change Traveler (TSTF)
360, Revision 1 to request new actions
with increased completion times for an
inoperable battery chargers and
alternate battery charger testing criteria
for limiting condition for operation
(LCO) 3.8.4 and LCO 3.8.5.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
No. The proposed changes restructure the
Technical Specifications (TSs) for the DC
Electrical Power Systems. The proposed
changes add actions to specifically address
battery charger inoperability. This change
will rely upon the capability of providing the
battery charger function by an alternate
means (e.g., a 125 volts direct current (VDC)
portable battery charger or a 250 VDC
portable battery charger) to justify the
proposed Completion Times. The DC
electrical power systems, including
associated battery chargers, are not initiators
to any accident sequence analyzed in the
Final Safety Analysis Report (FSAR).
Operation in accordance with the proposed
TS ensures that the DC electrical power
systems are capable of performing functions
as described in the FSAR. Therefore the
mitigative functions supported by the DC
Power Systems will continue to provide the
protection assumed by the analysis.
The relocation of preventive maintenance
surveillance, and certain operating limits and
actions to a newly-created, licenseecontrolled TS 5.5.13, ‘‘Battery Monitoring
and Maintenance Program,’’ will not
challenge the ability of the DC electrical
power systems to perform their design
functions. The maintenance and monitoring
required by current TS, which are based on
industry standards, will continue to be
performed. In addition, the DC Power
Systems are within the scope of 10 CFR
50.65, ‘‘Requirements for Monitoring the
Effectiveness of Maintenance at Nuclear
Power Plants,’’ which will ensure the control
of maintenance activities associated with the
DC electrical power systems. The integrity of
fission product barriers, plant configuration,
and operating procedures as described in the
FSAR will not be affected by the proposed
changes.
Therefore, the proposed changes do not
involve a significant increase in the
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21463
probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
No. The proposed changes involve
restructuring the TS for the DC electrical
power systems. These changes will rely upon
the capability of providing the battery
charger function by an alternate means to
justify the proposed completion times when
a normal battery charger is inoperable. The
DC electrical power systems, which include
the associated battery chargers, are not
initiators to any accident sequence analyzed
in the FSAR. Rather, the DC electrical power
systems are used to supply equipment used
to mitigate an accident. These mitigative
functions, supported by the DC electrical
power systems are not affected by these
changes and they will continue to provide
the protection assumed by the safety analysis
described in the FSAR. There are no new
types of failures or new or different kinds of
accidents or transients that could be created
by these changes.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any accident
previously evaluated.
3. Does the proposed change involve a
significant reduction in a margin of safety?
No. The margin of safety is established
through equipment design, operating
parameters, and the set points at which
automatic actions are initiated. The proposed
changes will not adversely affect operation of
plant equipment. These changes will not
result in a change to the set points at which
protective actions are initiated. Sufficient DC
electrical system capacity is ensured to
support operation of mitigation equipment.
The changes associated with the new Battery
Maintenance and Monitoring Program will
ensure that the station batteries are
maintained in a highly reliable state. The use
of spare battery chargers will increase the
reliability of the DC electrical systems during
periods of normal battery charger
inoperability. The equipment fed by the DC
electrical sources will continue to provide
adequate power to safety related loads in
accordance with analysis assumptions.
Therefore, the proposed changes do not
involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Bryan A. Snapp,
Esquire, Assoc. General Counsel, PPL
Services Corporation, 2 North Ninth St.,
GENTW3, Allentown, PA 18101–1179.
NRC Section Chief: Richard J. Laufer.
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Southern Nuclear Operating Company,
Inc., Docket No. 50–364, Joseph M.
Farley Nuclear Plant, Unit 2, Houston
County, Alabama
Date of amendment request: January
19, 2005.
Description of amendment request:
The proposed amendments would
revise the Updated Final Safety
Analysis Report to allow the use of fire
rated electrical cable for fire areas 2–013
and 2–042 in lieu of a one hour rated
electrical cable raceway fire barrier
enclosure as described by Title 10 of the
Code of Federal Regulations (10 CFR)
Part 50, Appendix R, Section III.G.2 for
protection of safe shutdown circuits.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Does the proposed change involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
The proposed change does not adversely
affect accident initiators or precursors nor
alter the design assumptions, conditions, or
configuration of the facility. The proposed
change does not alter or prevent the ability
of structures, systems, and components
(SSCs) from performing their intended
function to mitigate the consequences of an
initiating event within the assumed
acceptance limits. This is a revision to the
FSAR to use [mineral insulated] MI cable in
fire areas 2–013 and 2–042. The MI cable has
been tested to applicable requirements and
the implementation design reflects the test
results. Therefore, the probability of any
accident previously evaluated is not
increased. Equipment required to mitigate an
accident remain capable of performing the
assumed function. Therefore, the
consequences of any accident previously
evaluated are not increased.
Therefore, it is concluded that this change
does not significantly increase the probability
or consequences of an accident previously
evaluated.
2. Does the proposed change create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
The proposed change will not alter the
requirements or function for systems
required during accident conditions. No new
or different accidents result from
implementing MI cable for fire areas 2–013
and 2–042. The MI cable has been tested to
applicable requirements, and the
implementation design reflects the test
results. The use of MI cable is not a
significant change in the methods governing
normal plant operation. The proposed change
is consistent with the safety analysis
assumptions and current plant operating
practice.
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Therefore, the possibility of a new or
different kind of accident from any accident
previously evaluated is not created.
3. Does the proposed change involve a
significant reduction in a margin of safety?
The proposed change does not alter the
manner in which safety limits, limiting safety
system settings or limiting conditions for
operation are determined. The safety analysis
acceptance criteria are not affected by this
change. The proposed change will not result
in plant operation in a configuration outside
the design basis for an unacceptable period
of time without mitigating actions. The
proposed change does not affect systems that
respond to safely shutdown the plant and to
maintain the plant in a safe shutdown
condition.
Therefore, it is concluded that this change
does not involve a significant reduction in
the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: M. Stanford
Blanton, Esq., Balch and Bingham, Post
Office Box 306, 1710 Sixth Avenue
North, Birmingham, Alabama 35201.
NRC Section Chief: John A. Nakoski.
TXU Generation Company LP, Docket
Nos. 50–445 and 50–446, Comanche
Peak Steam Electric Station, Units 1 and
2, Somervell County, Texas
Date of amendment request: March
24, 2005.
Brief description of amendments:
These proposed changes would revise
Technical Specification (TS) 3.3.1
entitled ‘‘Reactor Trip System
Instrumentation’’ (RTS) and TS 3.3.2
entitled ‘‘Engineered Safety Feature
Actuation System Instrumentation’’
(ESFAS) Required Action Notes to
reflect the wording in Standard
Technical Specifications (STS) for
plants with bypass capability per TS
Task Force Traveler 418, Revision 2.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do the proposed changes involve a
significant increase in the probability or
consequences of an accident previously
evaluated?
Response: No.
[Westinghouse Topical Report] WCAP–
14333 provided the technical justification for
relaxing various RTS and ESFAS
Instrumentation bypass test times,
Completion Times, and Surveillance
Frequencies located in TS 3.3.1 and 3.3.2. As
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such, the proposed changes do not represent
a significant hazards consideration or present
a reduction in the margin of safety.
The protection system performance will
remain within the bounds of the previously
performed accident analyses since no
hardware changes are proposed. The same
Reactor Trip System (RTS) Instrumentation
and Engineered Safety Feature Actuation
(ESFAS) Instrumentation will continue to be
used and remain unchanged. The protection
systems will continue to function in a
manner consistent with the plant design
basis. These changes to the TS do not result
in a condition where the design, material,
and construction standards, which were
applicable prior to these changes, are altered.
The proposed changes will not modify any
system interface. The proposed changes will
not affect the probability of any event
initiators. There will be no degradation in the
performance of or an increase in the number
of challenges imposed on safety-related
equipment assumed to function during an
accident situation. There will be no change
to normal plant operating parameters or
accident mitigation performance. The
proposed changes will not alter any
assumptions or change any mitigation actions
in the radiological consequence evaluations
in the FSAR [final safety analysis report].
The proposed changes do not adversely
affect accident initiators or precursors nor
alter the design assumptions, conditions, or
configurations of the facility or change the
manner in which the plant is operated and
maintained. The proposed changes do not
alter or prevent the ability of structures,
systems, and components (SSCs) from
performing their intended function to
mitigate the consequences of an initiating
event within the assumed acceptance limits.
The proposed changes will not affect the
source term, containment isolation, or
radiological release assumptions used in
evaluating the radiological consequences of
an accident previously evaluated. The
proposed changes are consistent with safety
analysis assumptions and resultant
consequences.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do the proposed changes create the
possibility of a new or different kind of
accident from any accident previously
evaluated?
Response: No.
There are no hardware changes nor is there
any change in the method by which any
safety-related plant system performs its safety
function. The proposed changes will not
affect the normal method of plant operation.
No performance requirements will be
affected or eliminated. The proposed changes
will not result in physical alteration to any
plant system nor will there be any change in
the method by which any safety-related plant
system performs its safety function.
There will be no setpoint changes or
changes to accident analysis assumptions. No
new accident scenarios, transient precursors,
failure mechanisms, or limiting single
failures are introduced as a result of these
changes. There will be no adverse effect or
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challenges imposed on any safety-related
system as a result of these changes.
Therefore, the proposed changes do not
create the possibility of a new or different
kind of accident from any previously
evaluated.
3. Do the proposed changes involve a
significant reduction in a margin of safety?
Response: No.
The proposed changes do not affect the
acceptance criteria for any analyzed event
nor is there a change to any Safety Analysis
Limit (SAL). There will be no effect on the
manner in which safety limits, limiting safety
system settings, or limiting conditions for
operation are determined nor will there be
any effect on those plant systems necessary
to assure the accomplishment of protection
functions. The radiological dose consequence
acceptance criteria listed in the Standard
Review Plan will continue to be met.
Redundant RTS and ESFAS trains are
maintained and diversity, with regard to the
signals that provide reactor trip and
engineered safety features actuation, is also
maintained. All signals are credited as
primary or secondary and all operator actions
credited in the accident analyses will remain
the same. The proposed changes will not
result in plant operation in a configuration
outside the design basis.
Therefore, the proposed changes do not
involve a reduction in the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: George L. Edgar,
Esq., Morgan, Lewis and Bockius, 1800
M Street, NW., Washington, DC 20036.
NRC Section Chief: Allen G. Howe.
Virginia Electric and Power Company,
Docket Nos. 50–338 and 50–339, North
Anna Power Station, Units No. 1 and
No. 2, Louisa County, Virginia
Date of amendment request: March 1,
2005.
Description of amendment request:
The proposed changes to the Technical
Specifications (TS) would revise the
frequency for the Trip Actuating Device
Operational Test of the P–4 Interlock
Function and add Mode 4 to the
Applicability for TS 3.3.2.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. Do changes involve a significant increase
in the probability or consequences of an
accident previously evaluated?
The proposed changes do not significantly
increase the probability or consequences of
an accident previously evaluated in the
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11:52 Apr 25, 2005
Jkt 205001
UFSAR [Updated Final Safety Analysis
Report]. These interlocks and the associated
testing do not directly initiate an accident.
The consequences of accidents previously
evaluated in the UFSAR are not adversely
affected by these proposed changes because
the changes are made to accurately reflect the
design of the ESFAS [Engineered Safety
Features Actuation System] system.
Therefore, the proposed changes do not
involve a significant increase in the
probability or consequences of an accident
previously evaluated.
2. Do changes create the possibility of a
new or different kind of accident from any
accident previously evaluated?
The proposed changes do not create the
possibility of a new or different kind of
accident from any accident already evaluated
in the UFSAR. No new accident scenarios,
failure mechanisms, or limiting single
failures are introduced as a result of the
proposed changes. The proposed changes do
not challenge the performance or integrity of
any safety-related systems. Therefore, the
proposed changes do not create the
possibility of a new or different kind of
accident from any accident previously
evaluated.
3. Do changes involve a significant
reduction in the margin of safety?
The proposed changes do not involve a
significant reduction in a margin of safety.
The proposed changes are made to accurately
reflect the design of the ESFAS system. The
nominal actuation set points specified by the
Technical Specifications and the safety
analysis limits assumed in the transient and
accident analysis are unchanged. Therefore,
the proposed changes will not significantly
reduce the margin of safety as defined in the
Technical Specifications.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 50.92(c) are satisfied.
Therefore, the NRC staff proposes to
determine that the amendment request
involves no significant hazards
consideration.
Attorney for licensee: Ms. Lillian M.
Cuoco, Esq., Senior Counsel, Dominion
Resources Services, Inc., Millstone
Power Station, Building 475, 5th Floor,
Rope Ferry Road, Rt. 156, Waterford,
Connecticut 06385.
NRC Section Chief: John A. Nakoski.
Virginia Electric and Power Company,
Docket Nos. 50–280 and 50–281, Surry
Power Station, Unit Nos. 1 and 2, Surry
County, Virginia
Date of amendment request: March 8,
2005.
Description of amendment request:
The proposed changes would revise the
auxiliary feedwater (AFW) operability
requirements and add an AFW allowed
outage time and required actions.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
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21465
issue of no significant hazards
consideration, which is presented
below:
1. Involve a significant increase in the
probability or consequences of an accident
previously evaluated.
The proposed revision to the AFW pump
and flowpath requirements, as well as the
revision of AFW surveillances, does not
increase the probability of accidents
previously evaluated since the AFW System
is not required to operate until after the
occurrence of the previously evaluated
accidents. The change does not impact any
of the initiators of the accidents. The
proposed change does not involve a
significant increase in the consequences of an
accident previously evaluated because the
AFW System will continue to perform its
intended safety function for these accidents.
The operation of the AFW System with the
revised required action statements and added
surveillances continues to meet the
applicable design criteria.
2. Create the possibility of a new or
different type of accident from any accident
previously identified.
The safety function of the AFW System
continues to be the same and is met using the
same equipment. The change does not
involve any plant modifications and does not
revise the design of the plant or the AFW
System. Operation of the AFW System with
the revised required action statements and
revised surveillances continues to meet the
applicable design criteria and is consistent
with the Surry accident analyses. Therefore,
the proposed change does not introduce any
new failures that could create the possibility
of a new or different kind of accident from
any accident previously identified.
3. Involve a significant reduction in a
margin of safety.
The revised requirements for the AFW
pumps and flowpaths, as well as the revision
of AFW surveillances, continue to assure that
the margins of safety assumed in the
accidents and transients that rely upon
operation of the AFW System are maintained.
The proposed required action statements
appropriately place the plant in a safe
condition for the circumstances being
addressed. Therefore, this proposed revision
does not affect the margin of safety.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Ms. Lillian M.
Cuoco, Esq., Senior Counsel, Dominion
Resources Services, Inc., Millstone
Power Station, Building 475, 5th Floor,
Rope Ferry Road, Rt. 156, Waterford,
Connecticut 06385.
NRC Section Chief: John A. Nakoski.
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Virginia Electric and Power Company,
Docket Nos. 50–280 and 50–281, Surry
Power Station, Unit Nos. 1 and 2, Surry
County, Virginia
Date of amendment request: March
17, 2005.
Description of amendment request:
The proposed change would incorporate
a license condition that would permit
irradiation of the fuel assemblies to a
lead rod average burnup of 62,000
MWD/MTU.
Basis for proposed no significant
hazards consideration determination:
As required by 10 CFR 50.91(a), the
licensee has provided its analysis of the
issue of no significant hazards
consideration, which is presented
below:
1. The probability of occurrence or the
consequences of an accident previously
evaluated is not significantly increased.
For most of the accidents analyzed in the
UFSAR [Updated Final Safety Analysis
Report] (e.g., LOCA [loss-of-coolant
accident], Steam Line Break, etc.) the fuel
design has no impact on the likelihood of
initiation of an accident. Fuel performance is
evaluated as a consequence of the accident.
The only accident where the fuel design may
have an impact on the likelihood of a Chapter
14 accident is the Fuel Handling Accident
discussed in Chapter 14.4.1 of the Surry
UFSAR. The activity being evaluated is a
slight increase in the lead rod average burnup
limit for the fuel assemblies. No change in
fuel design or fuel enrichment will be
required to increase the lead rod average
burnup. The fuel rods at the extended lead
rod average burnup will continue to meet the
design limits with respect to fuel rod growth,
clad fatigue, rod internal pressure and
corrosion. Thus, there will be no impact on
the capability to engage the fuel assemblies
with the handling tools. Therefore, it is
concluded that the change will not result in
more than a minimal increase in the
frequency of occurrence of any accident
previously evaluated in the UFSAR. The
impact of extending the lead rod average
burnup to 62,000 MWD/MTU from 60,000
MWD/MTU on the Core Kinetics Parameter,
Core Thermal-Hydraulics/DNBR [Departure
from Nucleate Boiling Ratio], Specific
Accident Considerations, and Radiological
Consequences was considered. Based on the
evaluation of these considerations, it is
concluded that increasing the lead rod
average burnup limit to 62,000 MWD/MTU
will not result in a significant increase in the
consequences of the accidents previously
evaluated in the Surry UFSAR.
2. The possibility for a new or different
type of accident from any accident
previously evaluated is not created.
The fuel is the only component affected by
the change in the burnup limit. The change
does not affect the thermal hydraulic
response to any transient or accident. The
fuel rod design criteria [will] continue to be
met at the higher burnup limit. Thus, the
change does not create the possibility of an
accident of a different type.
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3. The margin of safety as defined in the
Bases to the Surry Technical Specifications is
not significantly reduced.
The operation of the Surry cores with a
limited number of fuel assemblies with some
fuel rods irradiated to a lead rod average
burnup of 62,000 MWD/MTU will not change
the performance requirements of any system
or component such that any design criteria
will be exceeded. The normal limits on core
operation defined in the Surry Technical
Specifications will remain applicable for the
irradiation of the fuel to a lead rod average
burnup of 62,000 MWD/MTU. Therefore, the
margin of safety as defined in Bases to the
Surry Technical Specifications is not
significantly reduced.
The NRC staff has reviewed the
licensee’s analysis and, based on this
review, it appears that the three
standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff
proposes to determine that the
amendment request involves no
significant hazards consideration.
Attorney for licensee: Ms. Lillian M.
Cuoco, Esq., Senior Counsel, Dominion
Resources Services, Inc., Millstone
Power Station, Building 475, 5th Floor,
Rope Ferry Road, Rt. 156, Waterford,
Connecticut 06385.
NRC Section Chief: John A. Nakoski.
Notice of Issuance of Amendments to
Facility Operating Licenses
During the period since publication of
the last biweekly notice, the
Commission has issued the following
amendments. The Commission has
determined for each of these
amendments that the application
complies with the standards and
requirements of the Atomic Energy Act
of 1954, as amended (the Act), and the
Commission’s rules and regulations.
The Commission has made appropriate
findings as required by the Act and the
Commission’s rules and regulations in
10 CFR Chapter I, which are set forth in
the license amendment.
Notice of Consideration of Issuance of
Amendment to Facility Operating
License, Proposed No Significant
Hazards Consideration Determination,
and Opportunity for a Hearing in
connection with these actions was
published in the Federal Register as
indicated.
Unless otherwise indicated, the
Commission has determined that these
amendments satisfy the criteria for
categorical exclusion in accordance
with 10 CFR 51.22. Therefore, pursuant
to 10 CFR 51.22(b), no environmental
impact statement or environmental
assessment need be prepared for these
amendments. If the Commission has
prepared an environmental assessment
under the special circumstances
provision in 10 CFR 51.12(b) and has
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made a determination based on that
assessment, it is so indicated.
For further details with respect to the
action see (1) the applications for
amendment, (2) the amendment, and (3)
the Commission’s related letter, Safety
Evaluation and/or Environmental
Assessment as indicated. All of these
items are available for public inspection
at the Commission’s Public Document
Room (PDR), located at One White Flint
North, Public File Area 01F21, 11555
Rockville Pike (first floor), Rockville,
Maryland. Publicly available records
will be accessible from the Agencywide
Documents Access and Management
Systems (ADAMS) Public Electronic
Reading Room on the internet at the
NRC Web site, https://www.nrc.gov/
reading-rm/adams.html. If you do not
have access to ADAMS or if there are
problems in accessing the documents
located in ADAMS, contact the PDR
Reference staff at 1 (800) 397–4209,
(301) 415–4737 or by e-mail to
pdr@nrc.gov.
Dominion Nuclear Connecticut, Inc.,
Docket No. 50–336, Millstone Power
Station, Unit No. 2, New London
County, Connecticut
Date of application for amendment:
July 6, 2004, as supplemented by letters
dated September 21, and December 23,
2004.
Brief description of amendment: The
amendment revised the Technical
Specifications (TSs) to allow a one-time
change in the Appendix J, Type A,
Containment Integrated Leak Rate Test
from the required 10 years to 15 years.
Date of issuance: April 6, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment No.: 285.
Facility Operating License No. DPR–
65: The amendment revised the TSs.
Date of initial notice in Federal
Register: February 1, 2005 (70 FR
5237). The September 21 and December
23, 2004, letters provided clarifying
information that did not change the
initial proposed no significant hazards
consideration determination or expand
the application beyond the scope of the
original Federal Register notice.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 6, 2005.
No significant hazards consideration
comments received: No.
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21467
Duke Energy Corporation, et al., Docket
Nos. 50–413 and 50–414, Catawba
Nuclear Station, Units 1 and 2, York
County, South Carolina
Duke Energy Corporation, Docket Nos.
50–369 and 50–370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg
County, North Carolina
Duke Energy Corporation, Docket Nos.
50–369 and 50–370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg
County, North Carolina
Date of application for amendments:
April 6, 2004, as supplemented by letter
dated August 5, 2004.
Brief description of amendments: The
amendments revised the Technical
Specifications to allow a diesel
generator battery to remain operable
with no more than one cell less than
1.36 Volts DC on float charge.
Date of issuance: March 29, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment Nos.: 221 and 216.
Renewed Facility Operating License
Nos. NPF–35 and NPF–52: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: September 14, 2004 (69 FR
55469). The supplement dated August 5,
2004 provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the staff’s original proposed no
significant hazards consideration
determination as published in the
Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 29, 2005.
No significant hazards consideration
comments received: No.
Date of application for amendments:
June 3, 2003, as supplemented by letters
dated July 29 and December 7, 2004,
and January 18, 2005.
Brief description of amendments: The
amendments revise TS 3.6.14 to allow a
pressurizer enclosure hatch between the
upper and lower containment volumes
to be open for up to 6 hours to facilitate
inspections of components such as the
power operated relief valve block
valves.
Date of issuance: April 5, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 228/210.
Renewed Facility Operating License
Nos. NPF–9 and NPF–17: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: July 22, 2003 (68 FR 43383).
The supplemental letters dated July 29
and December 7, 2004, and January 18,
2005, provided clarifying information
that did not change the initial proposed
no significant hazards consideration
determinations.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 5, 2005.
No significant hazards consideration
comments received: No.
Date of application for amendments:
September 28, 2004.
Brief description of amendments: The
amendments eliminate the technical
specification requirements to submit
monthly operating reports and annual
occupational radiation exposure reports.
Date of issuance: March 31, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 226 and 208.
Renewed Facility Operating License
Nos. NPF–9 and NPF–17: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: November 23, 2004 (69 FR
68182).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 31, 2005.
No significant hazards consideration
comments received: No.
Duke Energy Corporation, et al., Docket
Nos. 50–413 and 50–414, Catawba
Nuclear Station, Units 1 and 2, York
County, South Carolina
Date of application for amendments:
September 28, 2004.
Brief description of amendments: The
amendments eliminate the technical
specification requirements to submit
monthly operating reports and annual
occupational radiation exposure reports.
Date of issuance: March 31, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 222 and 217.
Renewed Facility Operating License
Nos. NPF–35 and NPF–52: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: November 23, 2004 (69 FR
68182).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 31, 2005.
No significant hazards consideration
comments received: No.
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Duke Energy Corporation, Docket Nos.
50–369 and 50–370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg
County, North Carolina
Date of application for amendments:
September 20, 2004.
Brief description of amendments: The
amendments deleted the Technical
Specifications associated with hydrogen
recombiners and hydrogen monitors.
Date of issuance: April 4, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment Nos.: 227 and 209.
Renewed Facility Operating License
Nos. NPF–9 and NPF–17: Amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: February 1, 2005 (70 FR 5239)
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 4, 2005.
No significant hazards consideration
comments received: No.
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Duke Energy Corporation, Docket Nos.
50–269, 50–270, and 50–287, Oconee
Nuclear Station, Units 1, 2, and 3,
Oconee County, South Carolina
Date of application of amendments:
October 16, 2003, as supplemented by
letters dated May 11, 2004, and January
10, 2005.
Brief description of amendments: The
amendments revised the Technical
Specification (TS) 3.4.9 and the
associated Bases to change the
minimum pressurizer heater capacity
from 126 kW to 400 kW to correct a nonconservative TS associated with a
pressurizer design-basis deficiency.
Date of Issuance: March 28, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 90 days from the date of
issuance.
Amendment Nos.: 343, 345, & 344.
Renewed Facility Operating License
Nos. DPR–38, DPR–47, and DPR–55:
Amendments revised the Technical
Specifications.
Date of initial notice in Federal
Register: January 20, 2004 (69 FR
2740).
The supplements dated May 11, 2004,
and January 10, 2005, provided
additional information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register on
January 20, 2004 (69 FR 2740).
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The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 28, 2005.
No significant hazards consideration
comments received: No.
Duke Energy Corporation, Docket Nos.
50–269, 50–270, and 50–287, Oconee
Nuclear Station, Units 1, 2, and 3,
Oconee County, South Carolina
Date of application of amendments:
September 20, 2004.
Brief description of amendments: The
amendments delete the Technical
Specifications associated with hydrogen
monitors.
Date of Issuance: April 4, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days after completion of the
Spring 2005 refueling outage for Unit 1.
Amendment Nos.: 344, 346 & 345.
Renewed Facility Operating License
Nos. DPR–38, DPR–47, and DPR–55:
Amendments revised the Technical
Specifications.
Date of initial notice in Federal
Register: February 1, 2005 (70 FR
5239).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 4, 2005.
No significant hazards consideration
comments received: No.
Energy Northwest, Docket No. 50–397,
Columbia Generating Station, Benton
County, Washington
Date of application for amendment:
August 5, 2004.
Brief description of amendment: This
amendment revises Technical
Specification Section 5.5.12, ‘‘Primary
Containment Integrity,’’ to allow a onetime extension of its Appendix J, Type
A, Containment Integrated Leak Rate
Test interval from the current 10-year
interval to a proposed 15-year interval.
Date of issuance: April 12, 2005.
Effective date: April 12, 2005, and
shall be implemented within 30 days.
Amendment No.: 191.
Facility Operating License No. NPF–
21: The amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: August 31, 2004 (69 FR
53102).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 12, 2005.
No significant hazards consideration
comments received: No.
Entergy Nuclear Operations, Inc.,
Docket No. 50–286, Indian Point
Nuclear Generating Unit No. 3,
Westchester County, New York
Date of application for amendment:
June 24, 2004.
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Brief description of amendment: The
amendment modifies Technical
Specification (TS) requirements to adopt
the provisions of Industry/TS Task
Force (TSTF) change TSTF–359,
‘‘Increased Flexibility in Mode
Restraints.’’
Date of issuance: April 6, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 226.
Facility Operating License No. DPR–
64: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: October 26, 2004 (69 FR
62474).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 6, 2005.
No significant hazards consideration
comments received: No.
Entergy Nuclear Operations, Inc.,
Docket No. 50–333, James A. FitzPatrick
Nuclear Power Plant, Oswego County,
New York
Date of application for amendment:
December 30, 2004.
Brief description of amendment: The
amendment changes the frequency for
Technical Specification surveillance
requirement (SR) 3.1.4.2, which verifies
each tested control rod scram time is
within limits with reactor steam dome
pressure ≥ 800 psig. Specifically, the SR
frequency increases from 120 days to
200 days of cumulative operation in
MODE 1 (power operation).
Date of issuance: April 5, 2005.
Effective date: As of the date of
issuance to be implemented within 30
days.
Amendment No.: 283.
Facility Operating License No. DPR–
59: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: February 1, 2005 (70 FR
5241).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 5, 2005.
No significant hazards consideration
comments received: No.
Entergy Nuclear Operations, Inc.,
Docket No. 50–293, Pilgrim Nuclear
Power Station, Plymouth County,
Massachusetts
Date of application for amendment:
September 2, 2004.
Brief description of amendment: The
amendment revised Technical
Specification (TS) 4.5.B.2.2 to change
the surveillance requirement frequency
for air testing the drywell and
suppression pool spray headers and
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nozzles from ‘‘once per 5 years’’ to
‘‘following maintenance that could
result in nozzle blockage.’’
Date of issuance: April 12, 2005.
Effective date: As of the date of
issuance, and shall be implemented
within 60 days.
Amendment No.: 214.
Facility Operating License No. DPR–
35: The amendment revised the TSs.
Date of initial notice in Federal
Register: December 21, 2004 (69 FR
76490).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 12, 2005.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC,
Docket Nos. 50–352 and 50–353,
Limerick Generating Station, Units 1
and 2, Montgomery County,
Pennsylvania
Date of application for amendments:
April 13, 2004.
Brief description of amendments: The
amendments eliminate the requirements
in Technical Specifications (TSs)
associated with hydrogen recombiners,
and hydrogen and oxygen monitors.
Date of issuance: April 13, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment Nos.: 173 and 135.
Facility Operating License Nos. NPF–
39 and NPF–85. The amendments
revised the TSs.
Date of initial notice in Federal
Register: June 8, 2004 (69 FR 32073).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 13, 2005.
No significant hazards consideration
comments received: No.
Exelon Generation Company, LLC, and
PSEG Nuclear LLC, Docket Nos. 50–277
and 50–278, Peach Bottom Atomic
Power Station, Units 2 and 3, York and
Lancaster Counties, Pennsylvania
Date of application for amendments:
April 30, 2004.
Brief description of amendments: The
amendments modify technical
specification (TS) requirements to adopt
the provisions of Industry/TS Task
Force (TSTF) change TSTF–359,
‘‘Increased Flexibility in Mode
Restraints.’’
Date of issuance: April 11, 2005.
Effective date: As of the date of
issuance, to be implemented within 180
days.
Amendment Nos.: 252 and 255.
Renewed Facility Operating License
Nos. DPR–44 and DPR–56: The
amendments revised the Technical
Specifications.
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Date of initial notice in Federal
Register: October 12, 2004 (69 FR
60681).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 11, 2005.
No significant hazards consideration
comments received: No.
FirstEnergy Nuclear Operating
Company, Docket No. 50–440, Perry
Nuclear Power Plant, Unit 1, Lake
County, Ohio
Date of application for amendment:
August 31, 2004.
Brief description of amendment: The
amendment revised Technical
Specification 3.4.1, ‘‘Recirculation
Loops Operating,’’ associated with
single recirculation loop operation by
incorporating limits for the linear heat
generation rate fuel thermal limit into
the limiting condition for operation.
Date of issuance: March 31, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 90 days.
Amendment No.: 134.
Facility Operating License No. NPF–
58: This amendment revised the
Technical Specifications.
Date of initial notice in Federal
Register: January 4, 2005 (70 FR 401).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 31, 2005.
No significant hazards consideration
comments received: No.
Florida Power Corporation, et al.,
Docket No. 50–302, Crystal River Unit
No. 3 Nuclear Generating Plant, Citrus
County, Florida
Date of application for amendment:
September 21, 2004.
Brief description of amendment: The
amendment deletes the Technical
Specifications associated with hydrogen
monitors.
Date of issuance: April 5, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days of issuance.
Amendment No.: 216.
Facility Operating License No. DPR–
72: Amendment revises the Technical
Specifications.
Date of initial notice in Federal
Register: February 1, 2005 (70 FR
5245).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 5, 2005.
No significant hazards consideration
comments received: No.
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21469
Nuclear Management Company, LLC,
Docket No. 50–305, Kewaunee Nuclear
Power Plant, Kewaunee County,
Wisconsin
No significant hazards consideration
comments received: Comments received
were addressed in the Safety Evaluation
dated April 1, 2005.
Date of application for amendment:
July 6, 2004, as supplemented January
27, 2005.
Brief description of amendment: The
amendment relocates the calibration
requirement of Table TS 4.1–1, Item 22,
‘‘Accumulator Level and Pressure,’’ and
the surveillance requirements of Table
TS 4.1–1, Item 25, ‘‘Portable Radiation
Survey Instruments,’’ from the
Technical Specifications to licenseecontrolled documents.
Date of issuance: April 6, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days.
Amendment No.: 182.
Facility Operating License No. DPR–
43: Amendment revised the Technical
Specifications.
Date of initial notice in Federal
Register: August 31, 2004 (69 FR
53112).
The supplement dated January 27,
2005, provided additional information
that clarified the application, did not
expand the scope of the application as
originally noticed, and did not change
the Nuclear Regulatory Commission
staff’s original proposed no significant
hazards consideration. The
Commission’s related evaluation of the
amendment is contained in a Safety
Evaluation dated April 6, 2005.
No significant hazards consideration
comments received: No.
R.E. Ginna Nuclear Power Plant, LLC,
Docket No. 50–244, R.E. Ginna Nuclear
Power Plant, Wayne County, New York
Date of application for amendment:
July 26, 2004, as supplemented on
March 7, 2005.
Brief description of amendment: The
amendment revised the Technical
Specifications by eliminating the
requirements to provide the NRC
monthly operating reports and annual
occupational radiation exposure reports.
Date of issuance: April 13, 2005.
Effective date: As of the date of
issuance to be implemented within 60
days.
Amendment No.: 89.
Renewed Facility Operating License
No. DPR–18: Amendment revised the
Technical Specifications and/or
License.
Date of initial notice in Federal
Register: October 12, 2004 (69 FR
60685). The supplemental letter
provided additional information that
clarified the application, did not expand
the scope of the application as originally
noticed, and did not change the staff’s
original proposed no significant hazards
consideration determination.
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated April 13, 2005.
No significant hazards consideration
comments received: No.
PSEG Nuclear LLC, Docket Nos. 50–272
and 50–311, Salem Nuclear Generating
Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Southern California Edison Company, et
al., Docket Nos. 50–361 and 50–362,
San Onofre Nuclear Generating Station,
Units 2 and 3, San Diego County,
California
Date of application for amendments:
July 23, 2004, as supplemented January
6, 2005.
Brief description of amendments: The
amendments modified the Technical
Specification (TS) definition
OPERABLE with respect to
requirements for availability of normal
and emergency power. Additionally,
required actions for shutdown power
TSs were modified.
Date of issuance: April 1, 2005.
Effective date: As of date of issuance,
to be implemented within 60 days.
Amendment Nos.: 264 and 246.
Facility Operating License Nos. DPR–
70 and DPR–75: The amendments
revised the TSs.
Date of initial notice in Federal
Register: March 1, 2005 (70 FR 9983).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 1, 2005.
Date of application for amendments:
December 10, 2004.
Brief description of amendments:
These amendments delete the Technical
Specifications associated with hydrogen
monitors.
Date of issuance: March 29, 2005.
Effective date: March 29, 2005, to be
implemented within 60 days of
issuance.
Amendment Nos.: Unit 2—194; Unit
3—185.
Facility Operating License Nos. NPF–
10 and NPF–15: The amendments
revised the Technical Specifications.
Date of initial notice in Federal
Register: January 18, 2005 (70 FR
2896).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 29, 2005.
No significant hazards consideration
comments received: No.
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Southern Nuclear Operating Company,
Inc., et al., Docket Nos. 50–424 and 50–
425, Vogtle Electric Generating Plant,
Units 1 and 2, Burke County, Georgia
Dates of application for amendments:
February 26 and April 28, 2008, as
supplemented by letters dated July 8
and October 20, 2004.
Brief description of amendments: The
amendments revised Technical
Specification (TS) Section 5.6.6, Reactor
Coolant System (RCS) Pressure
Temperature Limits Report (PTLR), to
facilitate future licensee-controlled
changes to the PTLR. The changes
include a revised PTLR that provides
new heatup and cooldown limits and
Cold Overpressure Protection System
(COPS) set points, and to recalculate the
minimum size of the pressurizer power
operated relief valve orifice of the RCS
vent. In addition, the changes relocate
the COPS arming temperature to the
PTLR, and lower the COPS arming
temperature from 350 °F to 220 °F. The
licensee also included TS bases changes
to support the changes to the TSs.
Date of issuance: March 28, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 30 days from the date of
issuance.
Amendment Nos.: 136 (Unit 1) and
115 (Unit 2).
Facility Operating License Nos. NPF–
68 and NPF–81: Amendments revised
the Technical Specifications.
Date of initial notice in Federal
Register: April 13, 2004 (69 FR 19575)
and April 22, 2004 (69 FR 34707).
The supplements dated July 8 and
October 20, 2004, provided additional
information that clarified the
application, did not expand the scope of
the application as originally noticed,
and did not change the staff’s original
proposed no significant hazards
consideration determination as
published in the Federal Register.
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 28, 2005.
No significant hazards consideration
comments received: No.
Tennessee Valley Authority, Docket
Nos. 50–327 and 50–328, Sequoyah
Nuclear Plant, Units 1 and 2, Hamilton
County, Tennessee
Date of application for amendments:
October 14, 2004.
Brief description of amendments: The
amendments eliminate the technical
specification requirements to submit
monthly operating reports and annual
occupational radiation exposure reports.
Date of issuance: April 5, 2005.
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Effective date: As of the date of
issuance and shall be implemented
within 45 days.
Amendment Nos.: 300 and 289.
Facility Operating License Nos. DPR–
77 and DPR–79: Amendments revised
the technical specifications.
Date of initial notice in Federal
Register: February 1, 2005 (70 FR
5250).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 5, 2005.
No significant hazards consideration
comments received: No.
Tennessee Valley Authority, Docket No.
50–390, Watts Bar Nuclear Plant, Unit 1,
Rhea County, Tennessee
Date of application for amendment:
November 8, 2004.
Brief description of amendment: The
amendment eliminates the requirements
in Technical Specifications to submit
monthly operating reports and annual
occupational radiation exposure reports.
Date of issuance: March 21, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 45 days of issuance.
Amendment No.: 57.
Facility Operating License No. NPF–
90: Amendment revises the Technical
Specifications.
Date of initial notice in Federal
Register: January 18, 2005 (70 FR
2902).
The Commission’s related evaluation
of the amendment is contained in a
Safety Evaluation dated March 21, 2005.
No significant hazards consideration
comments received: No.
Virginia Electric and Power Company,
Docket Nos. 50–338 and 50–339, North
Anna Power Station, Units 1 and 2,
Louisa County, Virginia
Date of application for amendment:
September 8, 2004.
Brief description of amendment:
These amendments delete the Technical
Specifications associated with hydrogen
recombiners and hydrogen monitors.
Date of issuance: March 22, 2005.
Effective date: As of the date of
issuance and shall be implemented
within 60 days from the date of
issuance.
Amendment Nos.: 238 and 219.
Renewed Facility Operating License
Nos. NPF–4 and NPF–7: Amendments
change the Technical Specifications.
Date of initial notice in Federal
Register: January 18, 2005 (70 FR
2902).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 22, 2005.
No significant hazards consideration
comments received: No.
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Virginia Electric and Power Company, et
al., Docket Nos. 50–280 and 50–281,
Surry Power Station, Units 1 and 2,
Surry County, Virginia
Date of application for amendments:
June 23, 2004.
Brief Description of amendments:
These amendments revise the Technical
Specifications Section 3.16, ‘‘Emergency
Power System,’’ requirements for
verifying the operability of the
remaining emergency diesel generator
(EDG) when either unit’s dedicated EDG
or the shared backup EDG is inoperable.
Date of issuance: April 5, 2005.
Effective date: As of the date of
issuance, and shall be implemented
within 30 days.
Amendment Nos.: 241 and 240.
Renewed Facility Operating License
Nos. DPR–32 and DPR–37: Amendments
change the Technical Specifications.
Date of initial notice in Federal
Register: August 19, 2004 (69 FR
51490).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated April 5, 2005.
No significant hazards consideration
comments received: No.
Virginia Electric and Power Company, et
al., Docket Nos. 50–280 and 50–281,
Surry Power Station, Units 1 and 2,
Surry County, Virginia
Date of application for amendments:
December 21, 2004.
Brief Description of amendments:
These amendments revise the Technical
Specifications by eliminating the
requirements to submit monthly
operating reports and occupational
radiation exposure reports.
Date of issuance: March 22, 2005.
Effective date: March 22, 2005.
Amendment Nos.: 240 and 239.
Renewed Facility Operating License
Nos. DPR–32 and DPR–37: Amendments
change the Technical Specifications.
Date of initial notice in Federal
Register: January 18, 2005 (70 FR
2903).
The Commission’s related evaluation
of the amendments is contained in a
Safety Evaluation dated March 22, 2005.
No significant hazards consideration
comments received: No.
Dated at Rockville, Maryland, this 18th day
of April 2005.
For the Nuclear Regulatory Commission.
Ledyard B. Marsh,
Director, Division of Licensing Project
Management, Office of Nuclear Reactor
Regulation.
[FR Doc. 05–8166 Filed 4–25–05; 8:45 am]
BILLING CODE 7590–01–P
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[Federal Register Volume 70, Number 79 (Tuesday, April 26, 2005)]
[Notices]
[Pages 21449-21470]
From the Federal Register Online via the Government Printing Office [www.gpo.gov]
[FR Doc No: 05-8166]
-----------------------------------------------------------------------
NUCLEAR REGULATORY COMMISSION
Biweekly Notice; Applications and Amendments to Facility
Operating Licenses Involving No Significant Hazards Considerations
I. Background
Pursuant to section 189a. (2) of the Atomic Energy Act of 1954, as
amended (the Act), the U.S. Nuclear Regulatory Commission (the
Commission or NRC staff) is publishing this regular biweekly notice.
The Act requires the Commission publish notice of any amendments
issued, or proposed to be issued and grants the Commission the
authority to issue and make immediately effective any amendment to an
operating license upon a determination by the Commission that such
amendment involves no significant hazards consideration,
notwithstanding the pendency before the Commission of a request for a
hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from April 1, 2005, through April 14, 2005. The
last biweekly notice was published on April 12, 2005 (70 FR 19110).
Notice of Consideration of Issuance of Amendments to Facility Operating
Licenses, Proposed No Significant Hazards Consideration Determination,
and Opportunity for a Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination. Within 60 days after the date of publication of this
notice, the licensee may file a request for a hearing with respect to
issuance of the amendment to the subject facility operating license and
any person whose interest may be affected by this proceeding and who
wishes to participate as a party in the proceeding must file a written
request for a hearing and a petition for leave to intervene.
Normally, the Commission will not issue the amendment until the
expiration of 60 days after the date of publication of this notice. The
Commission may issue the license amendment before expiration of the 60-
day period provided that its final determination is that the amendment
involves no significant hazards consideration. In addition, the
Commission may issue the amendment prior to the expiration of the 30-
day comment period should circumstances change during the 30-day
comment period such that failure to act in a timely way would result,
for example in derating or shutdown of the facility. Should the
Commission take action prior to the expiration of either the comment
period or the notice period, it will publish in the Federal Register a
notice of issuance. Should the Commission make a final No Significant
Hazards Consideration Determination, any hearing will take place after
issuance. The Commission expects that the need to take this action will
occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules and
Directives Branch, Division of Administrative Services, Office of
Administration, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and should cite the publication date and page number of
this Federal Register notice. Written comments may also be delivered to
Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville,
Maryland, from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of
written comments received may be examined at the Commission's Public
Document Room (PDR), located at One White Flint North, Public File
[[Page 21450]]
Area O1F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
The filing of requests for a hearing and petitions for leave to
intervene is discussed below.
Within 60 days after the date of publication of this notice, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.309, which is available at the
Commission's PDR, located at One White Flint North, Public File Area
01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the Agencywide
Documents Access and Management System's (ADAMS) Public Electronic
Reading Room on the Internet at the NRC Web site, https://www.nrc.gov/
reading-rm/doc-collections/cfr/. If a request for a hearing or petition
for leave to intervene is filed within 60 days, the Commission or a
presiding officer designated by the Commission or by the Chief
Administrative Judge of the Atomic Safety and Licensing Board Panel,
will rule on the request and/or petition; and the Secretary or the
Chief Administrative Judge of the Atomic Safety and Licensing Board
will issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.309, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following general requirements: (1) The name, address, and telephone
number of the requestor or petitioner; (2) the nature of the
requestor's/petitioner's right under the Act to be made a party to the
proceeding; (3) the nature and extent of the requestor's/petitioner's
property, financial, or other interest in the proceeding; and (4) the
possible effect of any decision or order which may be entered in the
proceeding on the requestor's/petitioner's interest. The petition must
also set forth the specific contentions which the petitioner/requestor
seeks to have litigated at the proceeding.
Each contention must consist of a specific statement of the issue
of law or fact to be raised or controverted. In addition, the
petitioner/requestor shall provide a brief explanation of the bases for
the contention and a concise statement of the alleged facts or expert
opinion which support the contention and on which the petitioner/
requestor intends to rely in proving the contention at the hearing. The
petitioner/requestor must also provide references to those specific
sources and documents of which the petitioner is aware and on which the
petitioner/requestor intends to rely to establish those facts or expert
opinion. The petition must include sufficient information to show that
a genuine dispute exists with the applicant on a material issue of law
or fact. Contentions shall be limited to matters within the scope of
the amendment under consideration. The contention must be one which, if
proven, would entitle the petitioner/requestor to relief. A petitioner/
requestor who fails to satisfy these requirements with respect to at
least one contention will not be permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing.
If a hearing is requested, and the Commission has not made a final
determination on the issue of no significant hazards consideration, the
Commission will make a final determination on the issue of no
significant hazards consideration. The final determination will serve
to decide when the hearing is held. If the final determination is that
the amendment request involves no significant hazards consideration,
the Commission may issue the amendment and make it immediately
effective, notwithstanding the request for a hearing. Any hearing held
would take place after issuance of the amendment. If the final
determination is that the amendment request involves a significant
hazards consideration, any hearing held would take place before the
issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed by: (1) First class mail addressed to the Office of the
Secretary of the Commission, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001, Attention: Rulemaking and Adjudications
Staff; (2) courier, express mail, and expedited delivery services:
Office of the Secretary, Sixteenth Floor, One White Flint North, 11555
Rockville Pike, Rockville, Maryland, 20852, Attention: Rulemaking and
Adjudications Staff; (3) E-mail addressed to the Office of the
Secretary, U.S. Nuclear Regulatory Commission, HearingDocket@nrc.gov;
or (4) facsimile transmission addressed to the Office of the Secretary,
U.S. Nuclear Regulatory Commission, Washington, DC, Attention:
Rulemakings and Adjudications Staff at (301) 415-1101, verification
number is (301) 415-1966. A copy of the request for hearing and
petition for leave to intervene should also be sent to the Office of
the General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC
20555-0001, and it is requested that copies be transmitted either by
means of facsimile transmission to (301) 415-3725 or by e-mail to
OGCMailCenter@nrc.gov. A copy of the request for hearing and petition
for leave to intervene should also be sent to the attorney for the
licensee.
Nontimely requests and/or petitions and contentions will not be
entertained absent a determination by the Commission or the presiding
officer of the Atomic Safety and Licensing Board that the petition,
request and/or the contentions should be granted based on a balancing
of the factors specified in 10 CFR 2.309(a)(1)(i)-(viii).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's PDR, located at One White Flint North, Public File
Area 01F21, 11555 Rockville Pike (first floor), Rockville, Maryland.
Publicly available records will be accessible from the ADAMS Public
Electronic Reading Room on the Internet at the NRC Web site, https://
www.nrc.gov/reading-rm/adams.html. If you do not have access to ADAMS
or if there are problems in accessing the documents located in ADAMS,
contact the PDR Reference staff at 1 (800) 397-4209, (301) 415-4737 or
by e-mail to pdr@nrc.gov.
AmerGen Energy Company, LLC, Docket No. 50-461, Clinton Power Station,
Unit 1, DeWitt County, Illinois
Date of amendment request: February 25, 2005.
Description of amendment request: The proposed change would delete
Section 2.G of the Clinton's Facility Operating License (FOL), NPF-62,
which requires AmerGen Energy Company, LLC, to report violations of the
requirements contained in Section 2.C of this license. The proposed
change will reduce unnecessary regulatory burden and will allow AmerGen
to take full advantage of the revisions to Title 10, Code of Federal
Regulations (10
[[Page 21451]]
CFR), Section 50.72, ``Immediate notification requirements for
operating nuclear power reactors,'' and 10 CFR 50.73, ``Licensee event
report system.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
The proposed change involves an administrative change only. The
proposed change does not involve the modification of any plant
equipment or affect plant operation. The proposed change will have
no impact on any safety related structures, systems or components.
The reporting requirement section of the FOL is not required because
the requirements are either adequately addressed by 10 CFR 50.72 and
10 CFR 50.73, or other regulatory requirements, or are not required
based on the nature of the Condition.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
The proposed change has no impact on the design, function or
operation of any plant structure, system or component. The proposed
change is administrative in nature and does not affect plant
equipment or accident analyses. The reporting requirement section of
the FOL is not required because the requirements are either
adequately addressed by 10 CFR 50.72 and 10 CFR 50.73, or other
regulatory requirements, or are not required based on the nature of
the Condition.
Therefore, the proposed change will not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
The proposed change is administrative in nature, does not negate
any existing requirement, and does not adversely affect existing
plant safety margins or the reliability of the equipment assumed to
operate in the safety analysis. As such, there is no change being
made to safety analysis assumptions, safety limits or safety system
settings that would adversely affect plant safety as a result of the
proposed change. Margins of safety are unaffected by deletion of the
reporting requirement that is adequately addressed elsewhere.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendment involves no significant hazards consideration.
Attorney for licensee: Mr. Thomas S. O'Neill, Associate General
Counsel, Exelon Generation Company, LLC, 4300 Winfield Road,
Warrenville, IL 60555.
NRC Section Chief: Gene Y. Suh.
AmerGen Energy Company, LLC, Docket No. 50-461, Clinton Power Station,
Unit 1, DeWitt County, Illinois
Date of amendment request: March 25, 2005.
Description of amendment request: The proposed change would revise
Technical Specification Surveillance Requirement (SR) 3.6.1.3.8 to add
a note excluding leakage through primary containment penetrations 1MC-
101 and 1MC-102 from the secondary containment bypass leakage total
specified in the SR.
Implementation of this proposed change will provide operational
flexibility by allowing Clinton Power Station (CPS) to utilize the
additional margin in the regulatory dose limit analysis that supports
the implementation of the alternative source term.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed amendment adds a note excluding the leakage through
the primary containment purge lines from the secondary containment
bypass leakage based on separate analysis of these paths using the
assumptions in the alternative source term (AST) revision to the
loss of coolant accident (LOCA) analysis.
The proposed change does not require modification to the
facility. The proposed change in secondary containment bypass
leakage does not affect the operation of any facility equipment, the
interface between facility systems, or the reliability of any
equipment. In addition, secondary containment bypass leakage does
not constitute an initiator of any previously evaluated accidents.
Therefore, the proposed amendment does not involve a significant
increase in the probability of an accident previously evaluated.
The radiological consequences of the LOCA analysis using the
primary containment purge line leakage as separate from the
secondary containment bypass leakage, has been evaluated as part of
the application of AST assumptions. The results conclude that the
radiological consequences remain within applicable regulatory
limits.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed amendment create the possibility of a new
or different kind of accident from any accident previously
evaluated?
Response: No.
The proposed change does not affect the design, functional
performance or operation of the facility. No new equipment is being
introduced and installed equipment is not being operated in a new or
different manner. Similarly, the proposed change does not affect the
design or operation of any structures, systems or components
involved in the mitigation of any accidents, nor does it affect the
design or operation of any component in the facility such that new
equipment failure modes are created. There are no set points at
which protective or mitigative actions are initiated that are
affected by this proposed action. No change is being made to
procedures relied upon to respond to an off-normal event.
As such the proposed amendment will not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
Response: No.
Margins of safety are established in the design of components,
the configuration of components to meet certain performance
parameters, and in the establishment of set points to initiate
alarms or actions. The proposed change adds a note excluding the
leakage through the primary containment purge lines from the
secondary containment bypass leakage based on separate analysis of
these paths using the assumptions in the AST revision to the LOCA
analysis. There is no change in the design of the affected systems,
no alteration of the set points at which alarms or actions are
initiated, and no change in plant configuration from original
design.
The margin of safety is considered to be that provided by
meeting the applicable regulatory limits. The AST analysis indicates
that the doses following a LOCA remain within the regulatory limits,
and therefore, there is not a significant reduction in a margin of
safety. The AST analysis confirms the change continues to ensure
that the doses at the exclusion area and low population zone
boundaries, as well as the control room, are within the
corresponding regulatory limits.
Therefore, operation of CPS in accordance with the proposed
change will not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendment involves no significant hazards consideration.
Attorney for licensee: Mr. Thomas S. O'Neill, Associate General
Counsel,
[[Page 21452]]
Exelon Generation Company, LLC, 4300 Winfield Road, Warrenville, IL
60555.
NRC Section Chief: Gene Y. Suh.
AmerGen Energy Company, LLC, Docket No. 50-461, Clinton Power Station,
Unit 1, DeWitt County, Illinois
Date of amendment request: April 1, 2005.
Description of amendment request: The proposed changes would
incorporate into the Technical Specifications (TSs) the Oscillation
Power Range Monitor (OPRM) instrumentation that will be declared
operable within 30 days after completion of the February 2006 refueling
outage. The proposed changes would add TS Section 3.3.1.3,
``Oscillation Power Range Monitor (OPRM) Instrumentation,'' and would
revise TS Sections 3.4.1, ``Recirculation Loops Operating,'' and 5.6.5,
``Core Operating Limits Report (COLR).'' In addition, the changes would
insert a new TS section for the OPRM instrumentation, delete the
current thermal-hydraulic instability administrative requirements, and
add the appropriate references for the OPRM trip set points and
methodology. Clinton Power Station (CPS) will activate the automatic
reactor protection system (i.e., scram) outputs of the OPRM
instrumentation upon implementation of these proposed TS changes.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed changes specify limiting conditions for operation,
required actions and surveillance requirements for the OPRM system,
and allows operation in regions of the power to flow map currently
restricted by the requirements of the Interim Corrective Actions
(ICAs) and certain limiting conditions of operation of TS Section
3.4.1, ``Recirculation Loops Operating.'' The restrictions of the
ICAs and TS Section 3.4.1 were imposed to ensure adequate capability
to detect and suppress conditions consistent with the onset of
thermal-hydraulic oscillations that may develop into a thermal-
hydraulic instability event. A thermal-hydraulic instability event
has the potential to challenge the Minimum Critical Power Ratio
(MCPR) safety limit. The OPRM system can automatically detect and
suppress conditions necessary for thermal-hydraulic instability.
With the activation of the OPRM system, the restrictions of the ICAs
and TS Section 3.4.1 will no longer be required.
This proposed change has no impact on any of the existing
neutron monitoring functions. When the OPRM is operable with
operating limits as specified in the Core Operating Limits Report
(COLR), the OPRM can automatically detect the imminent onset of
local power oscillations and generate a trip signal. Actuation of a
Reactor Protection System (RPS) trip (i.e., scram) will suppress
conditions necessary for thermal-hydraulic instability and decrease
the probability of a thermal-hydraulic instability event. In the
event the trip capability of the OPRM is not maintained, the
proposed changes limit the period of time before an alternate method
to detect and suppress thermal-hydraulic oscillations is required.
CPS intends to utilize the ICAs as the alternative method for
ensuring thermal-hydraulic oscillations do not occur. Since the
duration of this period of time is limited, the increase in the
probability of a thermal-hydraulic instability event is not
significant.
Activation of the OPRM scram function will replace the current
methods that require operators to insert an immediate manual reactor
scram in certain reactor operating regions where thermal hydraulic
instabilities could potentially occur. While these regions will
continue to be avoided during normal operation, certain transients,
such as a reduction in reactor recirculation flow, could place the
reactor in these regions. During these transient conditions, with
the OPRM instrumentation scram function activated; an immediate
manual scram will no longer be required. This may potentially cause
a marginal increase in the probability of occurrence of an
instability event. This potential increase in probability is
acceptable because the OPRM function will automatically detect the
instability condition and initiate a reactor scram before the
Minimum Critical Power Ratio (MCPR) Safety Limit is reached.
Consequences of the potential instability event are reduced because
of the more reliable automatic detection and suppression of an
instability event, and the elimination of dependence on the manual
operator actions. Operators monitor for indications of thermal
hydraulic instability when the reactor is operating in regions of
potential instability as a backup to the OPRM instrumentation.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed changes replace procedural actions that were
established to avoid operating conditions where reactor
instabilities might occur with an NRC approved automatic detect and
suppress function (i.e., OPRM).
Potential failures in the OPRM trip function could result in
either failure to take the required mitigating action or an
unintended reactor scram. These are the same potential effects of
failure of the operator to take the correct appropriate action under
the current procedural actions. The effects of failure of the OPRM
equipment are limited to reduced or failed mitigation, but such
failure cannot cause an instability event or other type of accident.
The OPRM system uses input signals shared with the Average Power
Range Monitor (APRM) system and rod block functions to monitor core
conditions and generate a Reactor Protection System (RPS) trip when
required. Quality requirements for software design, testing,
implementation and module self-testing of the OPRM system provide
assurance that no new equipment malfunctions due to software errors
are created. The design of the OPRM system also ensures that neither
operation nor malfunction of the OPRM system will adversely impact
the operation of the other systems and no accident or equipment
malfunction of these other systems could cause the OPRM system to
malfunction or cause a different kind of accident. No new failure
modes of either the new OPRM equipment or of the existing APRM
equipment have been introduced.
Operation in regions currently restricted by the ICAs and TS
Section 3.4.1 is within the nominal operating domain and ranges of
plant systems and components for which postulated equipment and
accidents have been evaluated. Therefore, operation within these
regions does not create the possibility of a new or different kind
of accident from any previously evaluated.
These proposed changes which specify limiting conditions for
operations, required actions and surveillance requirements of the
OPRM system and allow operation in certain regions of the power-to-
flow map do not create the possibility of a new or different kind of
accident from any accident previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The OPRM system monitors small groups of Local Power Range
Monitor (LPRM) signals for indication of local variations of core
power consistent with thermal-hydraulic oscillations and generates
an RPS trip when conditions consistent with the onset of
oscillations are detected. An unmitigated thermal-hydraulic
instability event has the potential to result in a challenge to the
MCPR safety limit. The OPRM system provides the capability to
automatically detect and suppress conditions that might result in a
thermal-hydraulic instability event and thereby maintains the margin
of safety by providing automatic protection for the MCPR safety
limit while reducing the burden on the control room operators
significantly. The OPRM trip provides a trip output of the same type
as currently used for the APRM. Its failure modes and types are
similar to those for the present APRM output. Since the MCPR Safety
Limit will not be exceeded as a result of an instability event
following implementation of the OPRM trip function, it is concluded
that the proposed change does not reduce the margin of safety.
Operation in regions currently restricted by the requirements of
the ICAs and TS Section 3.4.1 is within the nominal operating domain
assumed for identifying the range of initial
[[Page 21453]]
conditions considered in the analysis of anticipated operational
occurrences and postulated accidents. Therefore, operation in these
regions does not involve a significant reduction in the margin of
safety.
The proposed changes, which specify limiting conditions for
operations, required actions and surveillance requirements of the
OPRIVI system and allow operation in certain regions of the power to
flow map, do not involve a significant reduction in a margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendment involves no significant hazards consideration.
Attorney for licensee: Mr. Thomas S. O'Neill, Associate General
Counsel, Exelon Generation Company, LLC, 4300 Winfield Road,
Warrenville, IL 60555.
NRC Section Chief: Gene Y. Suh.
AmerGen Energy Company, LLC, Docket No. 50-219, Oyster Creek Nuclear
Generating Station, Ocean County, New Jersey
Date of amendment request: February 25, 2005.
Description of amendment request: The proposed change would delete
Section 2.E of the Oyster Creek's Facility Operating License (FOL),
DPR-16, which requires AmerGen Energy Company, LLC, to report
violations of the requirements contained in Section 2.C of this
license. The proposed change will reduce unnecessary regulatory burden
and will allow AmerGen to take full advantage of the revisions to Title
10, Code of Federal Regulations (10 CFR), Section 50.72, ``Immediate
notification requirements for operating nuclear power reactors,'' and
10 CFR 50.73, ``Licensee event report system.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change involves an administrative change only. The
proposed change does not involve the modification of any plant
equipment or affect plant operation. The proposed change will have
no impact on any safety related structures, systems or components.
The reporting requirement section of the FOL is not required because
the requirements are either adequately addressed by 10 CFR 50.72 and
10 CFR 50.73, or other regulatory requirements, or are not required
based on the nature of the Condition.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of accident from any accident previously evaluated?
Response: No.
The proposed change has no impact on the design, function or
operation of any plant structure, system or component. The proposed
change is administrative in nature and does not affect plant
equipment or accident analyses. The reporting requirement section of
the FOL is not required because the requirements are either
adequately addressed by 10 CFR 50.72 and 10 CFR 50.73, or other
regulatory requirements, or are not required based on the nature of
the Condition.
Therefore, the proposed change will not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change is administrative in nature, does not negate
any existing requirement, and does not adversely affect existing
plant safety margins or the reliability of the equipment assumed to
operate in the safety analysis. As such, there is no change being
made to safety analysis assumptions, safety limits or safety system
settings that would adversely affect plant safety as a result of the
proposed change. Margins of safety are unaffected by deletion of the
reporting requirement that is adequately addressed elsewhere.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendment involves no significant hazards consideration.
Attorney for licensee: Mr. Thomas S. O'Neill, Associate General
Counsel, Exelon Generation Company, LLC, 4300 Winfield Road,
Warrenville, IL 60555.
NRC Section Chief: Richard J. Laufer.
Detroit Edison Company, Docket No. 50-341, Fermi 2, Monroe County,
Michigan
Date of amendment request: March 17, 2005.
Description of amendment request: The proposed amendment would
revise Technical Specification 3.4.10, ``Reactor Coolant System (RCS)
Pressure and Temperature (P/T) Limits,'' to replace the combination
figure with separate P/T limit figures for each one of the three
categories of operation: hydrostatic pressure test [Curve A], non-
nuclear heatup and cooldown [Curve B], and nuclear (core critical)
operation [Curve C]. The new curves also provide composite limits for
all reactor pressure vessel (RPV) regions including core beltline
region. RPV bottom head individual limit curves are superimposed on
Curves A and B. In addition, two sets of curves are calculated; one for
32 effective full power years (EFPY) which represents the end of the
current 40-year plant license and the other one is for 24 EFPY which
has been selected as an intermediate point between the current EFPY and
32 EFPY.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. The proposed change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
The revised P/T curves are based on the 1998 Edition of the
American Society of Mechanical Engineers (ASME) Boiler and Pressure
Vessel (B&PV) Code, Section XI, including the 2000 Addenda. This
edition of the Code has been approved for use in both 10 CFR 50.55a
and Regulatory Guide (RG) 1.147. The revised curves are also based
on updated fluence calculations performed utilizing NRC-approved
methodology consistent with RG 1.190 for calculating Reactor
Pressure Vessel (RPV) neutron fluence. Revised fluence calculations
are applicable for 24 and for 32 Effective Full Power Years (EFPY).
The 32 EFPY represents a conservative exposure level at the end of
the current 40-year plant operating license. The proposed change
incorporates adjustment of the reference temperature for all
beltline material to account for irradiation effects and provide a
comparable level of protection as previously evaluated and approved.
The adjusted reference temperature calculations were performed in
accordance with the requirements of 10 CFR 50 Appendix G using the
guidance contained in RG 1.99, Revision 2, to provide operating
limits for up to 32 EFPY.
There are no changes being made to the RCS pressure boundary or
to RCS material, design or construction standards. The proposed P/T
curves define limits that continue to ensure the prevention of
nonductile failure of the RCS pressure boundary. The revision of the
P/T curves does not alter any assumptions previously made in the
radiological consequence evaluations since the integrity of the RCS
pressure boundary is unaffected. Therefore, the proposed changes
will not significantly increase the probability or consequences of
an accident previously evaluated.
2. The proposed change does not create the possibility of a new
or different kind of accident from any accident previously
evaluated.
[[Page 21454]]
The revised P/T curves are based on a later edition and addenda
of the ASME Code that incorporates current industry standards for
the curves. The revised curves are also based on an RPV fluence that
has been recalculated in accordance with the methodology of RG
1.190. The proposed change does not involve a modification to plant
structures, systems or components. There is no effect on the
function of any plant system, and no newly introduced system
interactions. The proposed change does not create new failure modes
or cause any systems, structures or components to be operated beyond
their design bases. Therefore, the proposed change does not create
the possibility of a new or different kind of accident from any
previously evaluated.
3. The proposed change does not involve a significant reduction
in the margin of safety.
The proposed P/T curves define the limits of operation to
prevent nonductile failure of the RPV upper vessel, bottom head and
beltline region. The new curves conform to the guidance contained in
RG 1. 190, ``Calculational and Dosimetry Methods for Determining
Pressure Vessel Neutron Fluence,'' and RG 1.99, Revision 2,
``Radiation Embrittlement of Reactor Vessel Materials,'' and
maintain the safety margins specified in 10 CFR 50 Appendix G.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David G. Pettinari, Legal Department, 688
WCB, Detroit Edison Company, 2000 2nd Avenue, Detroit, Michigan 48226-
1279
NRC Section Chief: L. Raghavan.
Detroit Edison Company, Docket No. 50-341, Fermi 2, Monroe County,
Michigan
Date of amendment request: March 17, 2005. This amendment request
supercedes, in its entirety, a previous application dated March 19,
2004, published in the Federal Register on June 22, 2004 (69 FR 34698).
Description of amendment request: The proposed amendment would
revise Technical Specification (TS) 3.3.6.1, ``Primary Containment
Isolation Instrumentation,'' to correct a formatting error introduced
during conversion to Improved Technical Specifications (ITS) by
replacing ``1 per room'' with ``2'' for the required channels per trip
system for the reactor water cleanup (RWCU) area ventilation
differential temperature--high primary containment isolation
instrumentation.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change restores the number of Required Channels Per
Trip System of the RWCU Area Ventilation Differential Temperature--
High isolation, Function 5.c of Table 3.3.6.1-1 of TS 3.3.6.1,
Primary Containment Isolation Instrumentation, to its pre-ITS value
and adds a note to Table 3.3.6.1-1 of TS 3.3.6.1, Primary
Containment Isolation Instrumentation, that ensures, during
surveillance testing and normal operation, there will always be at
least one instrument monitoring for a small leak in all RWCU
locations. No changes in operating practices or physical plant
equipment are created as a result of this change. Therefore, the
proposed change does not involve a significant increase in the
probability or consequences of an accident previously evaluated.
2. Does the proposed change create the possibility of a new or
different type of accident from any accident previously evaluated?
Response: No.
The proposed change restores the number of Required Channels Per
Trip System of the RWCU Area Ventilation Differential Temperature--
High isolation, Function 5.c of Table 3.3.6.1-1 of TS 3.3.6.1,
Primary Containment Isolation Instrumentation, to its pre-ITS value
and adds a note to Table 3.3.6.1-1 of TS 3.3.6.1, Primary
Containment Isolation Instrumentation, that ensures, during
surveillance testing and normal operation, there will always be at
least one instrument monitoring for a small leak in all RWCU
locations. No physical change in plant equipment will result from
this proposed change. Therefore, the proposed change does not create
the possibility of a new or different type of accident from any
previously evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change restores the number of Required Channels Per
Trip System of the RWCU Area Ventilation Differential Temperature--
High isolation, Function 5.c of Table 3.3.6.1-1 of TS 3.3.6.1,
Primary Containment Isolation Instrumentation, to its pre-ITS value
and adds a note to Table 3.3.6.1-1 of TS 3.3.6.1, Primary
Containment Isolation Instrumentation, that ensures, during
surveillance testing and normal operation, there will always be at
least one instrument monitoring for a small leak in all RWCU
locations. Therefore, the proposed change does not involve a
significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: David G. Pettinari, Legal Department, 688
WCB, Detroit Edison Company, 2000 2nd Avenue, Detroit, Michigan 48226-
1279
NRC Section Chief: L. Raghavan.
Duke Energy Corporation, et al., Docket Nos. 50-413 and 50-414, Catawba
Nuclear Station, Units 1 and 2, York County, South Carolina
Date of amendment request: November 16, 2004.
Description of amendment request: The amendments would revise
Technical Specifications (TS) 3.5.2, ``Emergency Core Cooling System,''
TS 3.6.6, ``Containment Spray System,'' TS 3.6.17, ``Containment Valve
Injection Water System,'' TS 3.7.5, ``Auxiliary Feedwater System,'' TS
3.7.7, ``Component Cooling Water System,'' TS 3.7.8, ``Nuclear Service
Water System (NSWS),'' TS 3.7.10, ``Control Room Area Ventilation
System'' TS 3.7.12, ``Auxiliary Building Filtered Ventilation Exhaust
System,'' and TS 3.8.1, ``AC Sources-Operating'' for Catawba, Units 1
and 2. The revisions would allow for the ``A'' and ``B'' NSWS headers
to be take out of service for up to 14 days each for system upgrades.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does operation of the facility in accordance with the
proposed amendment involve a significant increase in the probability
or consequences of an accident previously evaluated?
Response: No.
The pipe repair project for the [nuclear service water system]
NSWS and proposed [technical specifications] TS changes have been
evaluated to assess their impact on normal operation of the systems
affected and to ensure that the design basis safety functions are
preserved. During the pipe repair the other NSWS train will be
operable and no major maintenance or testing will be done on the
operable train. The operable train will be protected to help ensure
it would be available if called upon.
This pipe repair project will enhance the long term structural
integrity in the NSWS system. This will ensure that the NSWS headers
maintain their integrity to ensure its ability to comply with design
basis requirements and increase the overall reliability for many
years.
The increased NSWS train unavailability as a result of the
implementation of this
[[Page 21455]]
amendment does involve a one time increase in the probability or
consequences of an accident previously evaluated during the time
frame the NSWS headers are out of service for pipe repair.
Considering this small time frame for the NSWS train outages with
the increased reliability and the decrease in unavailability of the
NSWS system in the future because of this project, the overall
probability or consequences of an accident previously evaluated will
decrease.
Therefore, because this is a temporary and not a permanent
change, the time averaged risk increase is acceptable. The increase
in the overall reliability of the NSWS along with the decreased
unavailability in the future because of the pipe repair project will
result in an overall increase in the safety of both Catawba units.
Therefore, the consequences of an accident previously evaluated
remains unaffected and there will be minimal impact on any accident
consequences.
2. Does operation of the facility in accordance with the
proposed amendment create the possibility of a new or different kind
of accident from any accident previously evaluated?
Response: No.
Implementation of this amendment would not create the
possibility of a new or different kind of accident from any accident
previously evaluated. The proposed temporary TS changes do not
affect the basic operation of the [emergency core cooling system]
ECCS, [containment spray system] CSS, [containment valve injection
water system] CVIWS, NSWS, [auxiliary feedwater] AFW, [component
cooling water] CCW, [control room area ventilation system] [sic]
CRAVS, [auxiliary building filtered ventilation exhaust system]
ABFVES, or [emergency diesel generator] EDG systems. The only change
is increasing the required action time frame from 72 hours (ECCS,
CSS, NSWS, AFW, CCW, and EDG) or 168 hours (CVIWS, CRAVS and ABFVES)
to 336 hours. The train not undergoing maintenance will be operable
and capable of meeting its design requirements. Therefore, only the
redundancy of the above systems is affected by the extension of the
required action to 336 hours. During the project, contingency
measures will be in place to provide additional assurance that the
affected systems will be able to complete their design functions.
No new accident causal mechanisms are created as a result of NRC
approval of this amendment request. No changes are being made to the
plant, which will introduce any new accident causal mechanisms.
3. Does operation of the facility in accordance with the
proposed amendment involve a significant reduction in the margin of
safety?
Response: No.
Implementation of this amendment would not involve a significant
reduction in a margin of safety. Margin of safety is related to the
confidence in the ability of the fission product barriers to perform
their design functions during and following an accident situation.
These barriers include the fuel cladding, the reactor coolant
system, and the containment system. The performance of these fission
product barriers will not be impacted by implementation of this
proposed temporary TS amendment. During the NSWS train outages, the
affected systems will still be capable of performing their required
functions and contingency measures will be in place to provide
additional assurance that the affected systems will be maintained in
a condition to be able to complete their design functions. No safety
margins will be impacted.
The probabilistic risk analysis conducted for this proposed
amendment demonstrated that the [core damage probability] CDP
associated with the outage extension is judged to be acceptable for
a one-time or rare evolution. Therefore, there is not a significant
reduction in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Ms. Lisa F. Vaughn, Legal Department
(PB05E), Duke Energy Corporation, 422 South Church Street, Charlotte,
North Carolina 28201-1006.
NRC Section Chief: John A. Nakoski.
Entergy Gulf States, Inc., and Entergy Operations, Inc., Docket No. 50-
458, River Bend Station, Unit 1, West Feliciana Parish, Louisiana
Date of amendment request: March 8, 2005.
Description of amendment request: The proposed amendment would
enable the licensee to make changes to the Updated Safety Analysis
Report (USAR) to reflect the use of the non-single-failure-proof Fuel
Building Cask Handling Crane (FBCHC) for dry spent fuel cask component
lifting and handling operations.
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Will operation of the facility in accordance with this
proposed amendment involve a significant increase in the probability
or consequences of an accident previously evaluated?
Response: No.
The proposed amendment introduces no new mode of plant
operations and does not affect Structures, Systems, and Components
(SSCs) associated with power production, accident mitigation, or
safe plant shutdown. The SSCs affected by this proposed amendment
are the Fuel Building Cask Handling Crane (FBCHC), the spent fuel
storage canister, the spent fuel transfer cask, and the spent fuel
inside the storage canister. A hypothetical 30 ft. drop of a loaded
spent fuel shipping cask from the FBCHC is part of the River Bend
Station (RBS) current licensing basis. With the proposed spent fuel
transfer cask design and procedural changes implemented, the FCHC
will be used to lift and handle a fuel-loaded spent fuel transfer
cask of the same maximum weight and approximately the same
dimensions as previously evaluated in the RBS USAR. The proposed
amendment involves the use of redundant crane rigging during most
lateral moves with a loaded spent fuel transfer cask, which provides
temporary single-failure proof design features to provide protection
against an uncontrolled lowering of the load or load drop. In those
cases where the spent fuel transfer cask is not supported with
redundant rigging, certain hypothetical, non-mechanistic load drops
have been postulated and evaluated, with due consideration of the
use of impact limiters in some locations.
With this amendment, the probability of a loaded spent fuel
transfer cask drop is actually less likely than previously evaluated
because the capacity of the spent fuel multi-purpose canister [MPC]
(68 fuel assemblies) is larger than the capacity of the shipping
cask described in the current licensing basis (18 fuel assemblies),
which means that fewer casks will be required to be loaded, lifted,
and handled for a given population of spent fuel assemblies. The
consequences of the hypothetical spent fuel transfer cask load drops
on plant SSCs are bounded by those previously evaluated for a
shipping cask. That is, there is no significant damage to the Fuel
Building structure or any SSCs used for safe plant shutdown. New
analyses of hypothetical drops of a loaded transfer cask or canister
confirm that there is no release of radioactive material from the
storage canister and no unacceptable damage to the fuel, MPC, or
transfer cask.
The hypothetical drop of a spent fuel canister lid into an open,
fuel-filled canister in the spent fuel pool during fuel loading has
also been evaluated. Again, this hypothetical accident is no more
likely to occur than previously considered due to the higher
capacity of the spent fuel transfer cask over the spent fuel
shipping cask (i.e., fewer casks will need to be loaded for a given
number of fuel assemblies). The radiological consequences of this
event due to the potential damage of spent fuel assemblies in the
canister onto which the lid could be dropped have been evaluated.
While more total fuel assemblies could potentially be damaged from a
spent fuel canister lid drop compared to that assumed for the fuel
handling accident described in the RBS current licensing basis, the
significantly longer decay time of the spent fuel assemblies in the
canister results in a much smaller source term, such that the
existing fuel handling accident described in USAR Section 15.7.4
provides a bounding evaluation for the radiological consequences MPC
lid drop. There is no rearrangement of the fuel or deformation of
the fuel basket in the canister such that a critical geometry is
created as a result of an MPC lid drop.
The likelihood of a spent fuel canister lid drop due to the
failure of a crane component due to overload is very unlikely
because the rated load of the crane (250,000 lbs) is
[[Page 21456]]
approximately 16 times the weight of components lifted to install
the canister lid.
2. Will operation of the facility in accordance with this
proposed amendment create the possibility of a new or different kind
of accident from any accident previously evaluated?
Response: No.
The proposed amendment introduces no new mode of plant
operations and does not affect SSCs associated with power
production, accident mitigation, or safe plant shutdown. The SSCs
affected by this proposed amendment are the non-single-failure-proof
FBCHC, the spent fuel canister, the spent fuel transfer cask, and
the spent fuel inside the canister. The design function of the FBCHC
is not changed. The proposed amendment does not create the
possibility of a new or different kind of accident due to credible
new failure mechanisms, malfunctions, or accident initiators. The
proposed amendment creates a new initiator of two accidents
previously evaluated and caused by the non-mechanistic single
failure of a component in the FBCHC load path.
The current licensing basis accidents for which new initiators
are created by this amendment are the spent fuel shipping cask drop
and the fuel handling accident. The RBS current licensing basis
includes evaluations of the consequences of a spent fuel shipping
cask drop and the consequences of the drop of a spent fuel assembly
into the reactor core shortly after shutdown and reactor head
removal. The new initiators include the drop of a spent fuel
transfer cask of the same maximum weight and approximately the same
dimensions as the shipping cask, and the drop of a spent fuel
canister lid into an open, fuel filled canister in the spent fuel
pool. Both of these new initiators create hypothetical accidents
that are comparable in consequences to those previously evaluated.
For the drop of a spent fuel transfer cask, the consequences are
bounded by the current licensing basis analysis of the spent fuel
shipping cask drop. That is, there is no significant damage to the
Fuel Building structure or any SSCs used for safe plant shutdown,
and there is no release of radioactive material. New analyses of the
drop of a loaded transfer cask confirm that there is no release of
radioactive material from the storage canister and no unacceptable
damage to the fuel, MPC, or transfer cask.
For the drop of the spent fuel canister lid, the significantly
longer decay time of the spent fuel assemblies in the canister
compared to a spent fuel assembly in a recently shutdown reactor
results in doses to the public that are less than the previously
analyzed fuel handling accident. There is no rearrangement of the
fuel in the canister such that a critical geometry is created as a
result of an MPC lid drop.
3. Will operation of the facility in accordance with this
proposed amendment involve a significant reduction in a margin of
safety?
Response: No.
The proposed amendment introduces no new mode of plant
operations and does not affect SSCs associated with power
production, accident mitigation, or safe plant shutdown. The SSCs
affected by this proposed amendment are the non-single-failure-proof
FBCHC, the spent fuel storage canister, the spent fuel transfer
cask, and the spent fuel inside the canister. Therefore, this
amendment does not affect the reactor or fuel during power
operations, the reactor coolant pressure boundary, or primary or
secondary containment. All activities associated with this amendment
occur in the Fuel Building or in the adjacent outdoor truck bay
area. The design function of the FBCHC is not changed. The proposed
changes to plant operating procedures needed to implement dry spent
fuel storage at RBS do not exceed or alter a design basis or safety
limit associated with plant operation, accident mitigation, or safe
shutdown. The FBCHC is used to lift and handle the spent fuel
canister lid over spent fuel in the canister while in the spent fuel
pool, and to lift and handle the spent fuel transfer cask, both when
it is empty and after it is loaded with spent fuel in the spent fuel
pool.
This proposed amendment results in a net safety benefit because
a larger capacity cask is being used to move spent fuel out of the
spent fuel pool that was previously evaluated (68 fuel assemblies
versus 18 fuel assemblies), while maintaining the same maximum
analyzed cask weight described in the USAR. This yields fewer casks
to be loaded, fewer heavy load lifts, and, as a result, fewer
opportunities for events such as load drops. Because the maximum
weight of the loaded spent fuel transfer cask is the same as that
assumed for the shipping cask and for which the FBCHC was designed,
all design safety margins for use of the FBCHC remain unchanged. The
rated capacity of the FBCHC is approximately 16 times that of
components lifted to place the spent fuel canister lid, yielding
significant safety margins for that particular lift.
Based on the above review, it is concluded that: (1) the
proposed amendment does not constitute a significant hazards
consideration as defined by 10 CFR 50.92; and (2) there is
reasonable assurance that the health and safety of the public will
not be endangered by the proposed amendment; and (3) this action
will not result in a condition which significantly alters the impact
of the station on the environment as described in the NRC Final
Environmental Impact Statement.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn,
1400 L Street, NW., Washington, DC 20005.
NRC Section Chief: Allen G. Howe.
Exelon Generation Company, LLC, Docket Nos. STN 50-456 and STN 50-457,
Braidwood Station, Unit Nos. 1 and 2, Will County, Illinois
Docket Nos. STN 50-454 and STN 50-455, Byron Station, Unit Nos. 1
and 2, Ogle County, Illinois
Docket No. 50-237, Dresden Nuclear Power Station, Unit 2, Grundy
County, Illinois
Docket Nos. 50-373 and 50-374, LaSalle County Station, Units 1 and
2, LaSalle County, Illinois
Date of amendment request: February 25, 2005.
Description of amendment request: The proposed change would delete
the applicable sections of the Facility Operating Licenses (FOLs); NPF-
72, NPF-77, NPF-37, NPF-66, DPR-19, NPF-11, and NPF-18, respectively;
which require Exelon Generation Company, LLC, to report violations of
the requirements contained in Section 2.C of the Braidwood Station,
Units 1 and 2, and Byron Station, Units 1 and 2 FOLs; Section 2.C of
the Dresden Nuclear Power Station, Unit 2, renewed FOL; and Sections
2.C and 2.E of the LaSalle County Station, Units 1 and 2, FOLs. The
proposed change will reduce unnecessary regulatory burden and will
allow Exelon to take full advantage of the revisions to Title 10, Code
of Federal Regulations (10 CFR), Section 50.72, ``Immediate
notification requirements for operating nuclear power reactors,'' and
10 CFR 50.73, ``Licensee event report system.''
Basis for proposed no significant hazards consideration
determination: As required by 10 CFR 50.91(a), the licensee has
provided its analysis of the issue of no significant hazards
consideration, which is presented below:
1. Does the proposed change involve a significant increase in
the probability or consequences of an accident previously evaluated?
Response: No.
The proposed change involves an administrative change only. The
proposed change does not involve the modification of any plant
equipment or affect plant operation. The proposed change will have
no impact on any safety related structures, systems or components.
The reporting requirement section of the FOL is not required because
the requirements are either adequately addressed by 10 CFR 50.72 and
10 CFR 50.73, or other regulatory requirements, or are not required
based on the nature of the Condition.
Therefore, the proposed change does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. Does the proposed change create the possibility of a new or
different kind of
[[Page 21457]]
accident from any accident previously evaluated?
Response: No.
The proposed change has no impact on the design, function or
operation of any plant structure, system or component. The proposed
change is administrative in nature and does not affect plant
equipment or accident analyses. The reporting requirement section of
the FOL is not required because the requirements are either
adequately addressed by 10 CFR 50.72 and 10 CFR 50.73, or other
regulatory requirements, or are not required based on the nature of
the Condition.
Therefore, the proposed change will not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. Does the proposed change involve a significant reduction in a
margin of safety?
Response: No.
The proposed change is administrative in nature, does not negate
any existing requirement, and does not adversely affect existing
plant safety margins or the reliability of the equipment assumed to
operate in the safety analysis. As such, there is no change being
made to safety analysis assumptions, safety limits or safety system
settings that would adversely affect plant safety as a result of the
proposed change. Margins of safety are unaffected by deletion of the
reporting requirement that is adequately addressed elsewhere.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Attorney for licensee: Mr. Thomas S. O'Neill, Associate General
Counsel, Exelon Generation Company, LLC, 4300 Winfield Road,
Warrenville, IL 60555.
NRC Section Chief: Gene Y. Suh.
Exelon Generation Company, LLC, Docket Nos. 50-352 and 50-353, Limerick
Generating Station, Unit Nos. 1 and 2, Montgomery County, Pennsylvania
Date of amendment request: February 25, 2005.
Description of amendment request: The proposed change would delete
the applicable sections of the Limerick Generating Station, Units 1 and
2, Facility Operating Licenses (FOLs), NPF-39 and NP